ML17286A630

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Annual Operating Rept of WNP-2 for 1990. W/910307 Ltr
ML17286A630
Person / Time
Site: Columbia Energy Northwest icon.png
Issue date: 12/31/1990
From: John Baker
WASHINGTON PUBLIC POWER SUPPLY SYSTEM
To: Martin
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
NUDOCS 9103070055
Download: ML17286A630 (149)


Text

ACCELERATED DISTRIBUTION DEMONSTRATION SYSTEM '

REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)

ACCESSION NBR:9103070055 DOC.DATE: 90/12/31 NOTARIZED: NO=- DOCKET'g FACIL:50-397 WPPSS Nuclear Project, Unit 2, Washington Public Powe 05000397 AUTH. NAME AUTHOR AFFILIATION BAKER,J.W. Washington Public Power Supply System RECIP.NAME RECIPIENT AFFILIATION

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SUBJECT:

"WPPS-2 Annual Operating Rept for 1990." W/undated ltr. I DISTRIBUTION CODE: IE47D COPIES RECEIVED:LTR .ENCL SIZE: ~ D TITLE: 50.59 Annual Report of Changes, Tests or Experiments Made W/out Approv 1

NOTES: S RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD5 LA 1 0 PD5 PD 5 5 ENG, P. L. 1 0 INTERNAL: ACRS 6 6 AEOD/DOA 1 1 AEOD/DS P/TPAB 1 1 NRR -DHPQy'B11 1 1 NRR/DOEA/OEAB11 1 1 G F 02 1 1 RGN5 FILE 01 1 1 S EXTERNAL: NRC PDR 1 1 NSIC 1 1 D

A D

D NOTE TO ALL "RIDS" RECIPIENTS:

PLEASE HELP US TO REDUCE WASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOM P l-37 (EXT. 20079) TO ELIMINATEYOUR NAME FROM DISTRIBUTION LISIS FOR DOCUMENTS YOU DON'T NEED!

TOTAL NUMBER OF COPIES REQUIRED: LTTR 21 ENCL 19

WASHINGTON PUBLIC POWER SUPPLY SYSTEM P.O. Box 968 ~ 3000 George Washington Way ~ Richland, Washington 99352 Docket No. 50-397 W.J 7, ~T l I Document Control Desk U.S. Nuclear Regulatory Commission Washington, D.C. 20555

Dear Mr,

Martin:

Subject:

NUCLEAR PLANT NO. 2 ANNUALOPERATING REPORT 1990

'eference: 1) Title 10, Code of Federal Regulations, Part 50.59(b)

2) WNP-2 Technical Specifications, 6.9,1.4 and 6.9.1.5
3) Regulatory Guide 1.16, Reporting of Operation Information Appendix A In accordance with the above listed references, the Supply System hereby submits the Annual Operating Report for calendar year 1990. Should you have any questions or comments, please contact G. L. Gelhaus, WNP-2 Assistant Plant Technical Manager.

Very truly yours, gati cl//~

. W. Baker WNP-2 Plant Manager JWB:CLF:dm Attachments CC: Mr. John B. Martin, NRC Region V Mr. C. Sorenson, NRC Resident Inspector'(M/D 901A)

Mr. D. L. Williams, BPA (M/D 399) e$

Mr. R. F. Mazurkiew'icz, BPA (M/D 399)

~055 PP 3.2 P $ 0307'CK ADOC 0'5000397 pDp PDP R

t ML14350A144 Forwards Addi Info re Station Blackout, Per 910425 Telcon w/ NRC 8 Science Applications Intl Corp.. Dated May 7, 1991.

431-97-0141 box ¹8

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//9l p3p7pp55 ANNUALOPERATING REPORT OF WNP-2 FOR 1990 DOCKET NO. 50-397 FACILI'IYOPERATING LICENSE NO. NPF-21 Washington Public Power Supply System 3000 George Washington Way Richland, Washington 99352

'I J TABLE F NTENT

1.0 INTRODUCTION

1.1 1990 WNP-2 Load. Profile 1.2 Reactor Coolant Specific Activity Levels 2.0 REPORTS 2.1 Annual Personnel Exposure and Monitoring Report 2.2 Main Steam Line Safety/Relief Valve Challenges 2.3 Summary of Plant Operation 10 2.4 Significant Corrective Maintenance Performed on Safety-Related Equipment 16 2.5 Indications of Failed Fuel 46 2.6 10CFR50.59 Changes, Tests, and Experiments 47 2.6.1 Plant Modifications 48 2.6.2 Lifted Leads and Jumpers (Temporary Changes) 56 2.6.3 FSAR Evaluations 70 2.6.4 Problem Evaluations 73 2.6.5 Plant Tests and Experiments 79 2.6.6 Plant Procedure Changes 81 2.6.7 Fire Protection Program Changes 83 2.7 Diesel Generator Failures 87

D N The 1990 Annual Operating Report of Washington Public Power Supply'ystem Plant Number 2 (WNP-2) is

'ubmitted in accordance with the requirements of Federal Regulations and Facility Operating License NPF-21.

Plant WNP-.2 is a 3323 MWt, BWR-5, which began commercial operation on December 13, 1984.

Following a record 203 consecutive days of operation, the Plant was shutdown on April21, 1990 for the annual maintenance and refueling outage. The outage had originally been scheduled for 45 days; however, on May 27, 1990 the Division 1 Emergency Diesel Generator failed approximately six hours into a 24-hour, full-load run due to the failure of the diesel generator slip ring end bearing. During an investigation into this event it was also discovered that both the Division 1 and Division 2 Emergency Diesel Generators had shorted fi'eld pole windings which were evaluated as being the result of manufacturing defects. The Divisiori 1 Diesel Generator had to be completely rewound, resultirig in a seven-week extension of the outage. Following successful Diesel Generator repair and testing efforts, the Plant was restarted on August 4, 1990 and operated until September 25, 1990 when the reactor was manually scrammed after experiencing main turbine hydraulic control oil pressure problems in the Digital Electro-Hydraulic (DEH) System. The oil pressure problems were caused by a broken pipe nipple in the auto-stop oil header portion of the Turbine Lube Oil System. Repairs were made and the Plant was restarted on September 30, 1990 following a five-day outage.

On November 2, 1990 the Plant was manually shutdown after confirmation by Nondestructive Examination (NDE) testing of a small crack in a 3/4-inch drain line off of the High Pressure Core Spray (HPCS) System injection header. The crack was repaired and NDE testing was performed on 104 welds on similar drains in the Emergency Core Cooling -System (ECCS) prior to returningg the Plant to service on November 11, 1990.

On December 7, 1990 the Main Generator tripped at 100 percent power following Qashover-to-ground on a "B" phase high voltage insulator between the main step-up transformers and generator disconnects. The electrical fault (flashover) was due to Circulating Water (CW) System cooling tower chemical deposits having built up on the insulator, with wet and icing conditions contributing to provide a conductive path over the surface of the insulator. The damaged insulator stack was replaced and all other 500 KV, 230 KV and 115 KV insulators in the main transformer yard were inspected and cleaned. The Plant was restarted on December 9, 1990 and ran at or near 100 percent capacity for the remainder of the year.

During 1990, there were several examples of major accomplishments which required significant effort on the part of Supply System personnel to complete. The following is a summary of those efforts.

(a) The fifth refueling outage was successfully completed. Significant activities included:

o Preventive maintenance on the remaining four Main Steam Isolation Valves (MSIVs).

Bearing repair and complete rewind of the Division I Emergency Diesel Generator.

Inspection of two of the three Emergency Diesel Generators and. overhauling the High Pressure Core Spray (HPCS) diesel engine.

Inspection of one of three Low-Pressure Turbine Rotors. Non-destructive examination of the rotor confirmed crack indications and four blades were replaced.

Preventative Maintenance on 30 Control Rod Drive Mechanisms (CRDMs). This activity included removing, replacing and rebuilding the CRDMs.

Replacement of the rubber seals between the low-pressure turbines and the condenser boxes to minimize air leakage into the condenser.

o Removal of spent fuel assemblies and refueling the reactor. The refueling activity included replacing 152 fuel assemblies, using a fuel shuffle scheme.

(b) The best operating cycle of 203 days of continuous operation ended when the Plant was shutdown for the annual maintenance and refueling outage. During this cycle 6.5 billion net kilowatt-hours were generated, enough electricity to supply the annual needs of more than 400,000 all-electric homes.

Furthermore, the capacity factor for the operating cycle was more than 84 percent.

(c) During October, 1990 a new monthly generation record was set when the Plant provided 787,321 megawatt-hours of electricity to the Bonneville Power Administration's regional transmission system.

This compares to the old plant record of 780,000 megawatt-hours generated during December, 1989.

In 1990 total radiation exposure at the Plant was 535 man-rem, as compared to the 1989 level of 492 man-rem.

(The Institute for Nuclear Power Operation (INPO) had set 460 man-rem as the 1990 industry goal for BWRs.)

During the year WNP-2 received 15 NRC Notices of Violation (NOVs): One (1) Level II, one (1) Level III, twelve (12) Level IV and one (1) Level V. The Level II violation was associated with previous (1986) fire protection issues for which no response was required, nor was a civil penalty proposed. The Level IIIviolation was associated with previous (1986) equipment qualification issues pertaining to splices in containment and included a proposed $ 50,000 civil penalty, Also during 1990, a total of 32 Licensee Event Reports (LERs) were written and submitted pursuant to the requirements of 10CFR50.73, as compared to a total of 45 LERs submitted during 1989.

The 1990 capacity factors, based upon net electrical energy output, are listed in the following table.

January 93.59 February 93.77 March 91.87 April 55.80 hfay 0 June 0 July 0 August 67. 12 September 78.24 October 96.51 November 62.15

~Dce mar $ 4, l4 Overall 59.86

  • Started Maintenance/Refueling Outage Ended Maintenance/Refueling Outage

0

. I 1990 WNP-2 L AD PR FILE The 1990 Power History graph for WNP-2 is shown below.

WNP 2 LOAI) I'I~OI'ILK CALENDAR q'Epyp yBBO Percent of lisle'I Los!I MCCalratts (Cross) Fercent of Raled Load Mcc ~ Trail ~ (flross)

LOOTS ! 1<0 100. ~

I LAO 1000 1000 SHVTWVH fOR R j

00. 80 i TVRDLCC COHIROL TLV fVCL COASTOOaH 800 k CO.'17ROL ROO SrllfT fVCL CO~re 80- pi R S OVTACC R S OVTACC 600 800 fLLV1'CO crrcsfico Aorl Io.r AOO Aoo "0 DO I RCARIÃO k Zo>>

Zpo STI!OoiC fRODLCJIS OX O.i F

(sL QUARTER 1990 21td QUARTER 1990 Mccalfalts (Cross) I'crccnl of Rated Load McC ~ Iratts (CI'oss) Percent of Raled Load I IAO 100- lliO 100.

1000 1000 sHvrco lrr Dvc To Rr SCRAN OCC io SHVTDOa'H DVC TO HPCS Dll!I V IDJC CJLIC1 IXXO'Ll TOR flASHOIYR RfV fVNR fROOICHS DCII PROOLCIIS 60-RCCO !tel'ROH 800 600 DCH RROOLCHS 60- 60 ~

60 1' OVTACC 600 47CHDCO eo>> Ao AOO coo

>>0 ~

ZO. ~

ZOO Zoo STARTVP ITIOJI R S 0'

1 DI'<l QUARTER (990 4th QUARTER (990

1 2 REA R LANT PE IFI This section contains information relative to reactor coolant cumulative iodine levels, iodine spikes and specific activity of all isotopes other than iodine, and is reported in accordance with Technical Specifications paragraph g 6.9.1.5.c.

The specific activity of the primary coolant was significantly less than 0.2 microcuries per gram dose equivalent I-131 as set forth in WNP-2 Technical Specification LCO 3/4.4.5. The specific activity of the primary coolant was routinely sampled and analyzed as required by WNP-2 Technical Specifications, and was in all cases, less than or equal to 100/2 microcuries per gram.

uCi/gm 10'EACTOR SPECIFIC ACTIVITY HNP-2 SPACT 10' I

10 10 01-01 02-19 04-09 05-28 07-16 09-03 10-22 12-10 1990 1990 e

4 The reports provided in this section meet the requirements of Federal Regulations and the WNP-2 Operating License. They cover the requirements of the WNP-2 Technical Specifications, Sections 6.9.1.4 and 6.9.1.5, and provide the information specified by 'Regulatory Guide =1.16, Reporting of Operating Information. In addition, Section 2.6 provides the information required by 10CFR50.59 Changes, Tests, and Experiments.

1A LP R NNEL EXP URE ND M NIT RIN REP RT The information provided in this section of the report is required by the WNP-2 Technical Specifications, Section 6.9.1.5.a, and Regulatory Guide 1.16, Revision 4.

RKR-020 RADIATION EXPOSURE RECORDS 02/08/91 10t47 WORK AND etOS FUNCTIOtt REPORT / 1 ~ 16 APPENDIX A NUCLEAR PL4NT NO ~ 2 REPORT FOR CALENDAR YEAR 1990 NVHSER OF PERSONS RECEIVINC OVER 100 tLREtt TOTAL ttAN-REtt STATION UTILITY CONTRACTORS STATION UTILITY CONTRACTOR EttPLOYEES EttPLOYEES AttD OTHERS EttPLOYEES EttPLOYEES AND OTHERS

'85 '" 0 ~ 808

~JPERATIONSW SURVEILLANCE HAINTKNANCE PERSONNEL" 42 12 ~ 135 28 '36 '

~ 274 9.008 OPER4TINC PERSONNEL 47e684 1 e086 Oe000 42 '04 0 ~ 163 0 ~ 000 HEALTH PHYSICS PERSONNEL SUPERVISORY'PERSONNEL 29 ~ 777

'69 Oe000 15e458 2'80 0 000 '9 ~ 798 12 Oe964 Oe000 4e570 0 ~ 231 Oe000 ENCINEERINC PERSONNEL 4 '39 9e411 2,053 1 ~ 104 3 ~ 142 0 525 ROUTINE tl4INTKNANCE - ' 'ttAINTENANCK PERSONNEL 174e403 Oe178 186. 685 141 ~ 120 0 060 L06 ~ L10 OPERATING PERSONNEL 2 '13 0 'S6 0 F 000 2e 795 0 014 0.000 HE4LTH PHYSICS PERSONNEL 8 '65 0 ~ 000 41 ~ 595 10 ~ 130 Oe000 30.589

'UPERVISORY. PERSONNEL '

13 ~ 174 ~ 594 2 297 be 147 0 586 0.498 ENGINEERING PERSONNEL 20e576 17e948 2be804 7e 671 beb07 8.894

'NSERVICE INSPECTION" "'4INTENANCE"PERSONNEL 0 ~ 573 0 F 000 2 ~ 921 Oeb3S 0 ~ 000"" 2 ~ 164 OPERATINC PERSONNEL 0 F 008 0 F 000 0.000 0 009 0 000 0 000 HEALTH PHYSICS PERSONNEL 0 '53 0 F 000 Oe419 0 '09 0 ~ 000 0 '63 SUPERVISORY PERSONNEL 0 '77 0 ~ 511 0 ~ 180 Oe023 0 ~ 163 0 ~ 051 ENGINEERING PERSONNEL I ~ 623 1 ~ 053 9 F 100 Oe479 0 '53 2 ~ 133 f PECIAL tthINTENANCE 'AINTENANCE'ERSONNEL OPERATINC PERSONNEL 15 ~ 158 0 '68 0e Oe000 014 65 '47 0 ~ 000 16el21 0 '58

'0 0 000 005 24 446 0.000 HEALTH PHYSICS PERSONNEL 0 '77 Oe000 3 '59 1 ~ 106 0.000 2 ~ 252 SUPERVISORY PERSONNEL 0 949 0 '31 0 '23 OeS14 Oe 191 0 149 KNCINEKRINC PERSONNEL 1 ~ 031 3ebb6 5e688 0 ~ 367 I ~ 147 le322 WASTE PROCESS INC "' ttAINTENANCE'PERSONNEL 8.580 0 F 000 3e676 5.905 0.000 I ~ 562 OPERATING PERSONNEL 0 ~ 112 0 F 000 Oe000 0 ~ 164 0.000 0 F 000 HEALTH PHYSICS PERSONNEL. 3 ~ 0'96 0 F 000 Le902 2.799 0 000 3e181 SUPERVISORY PERSONNEL 0 ~ 041 0.000 0 000 0 '37 0.000 0.000

'92 F

ENGINEERING PERSONNEL 0 0 ~ 316 0 '07 0 '37 0 '46 Oe033 REFUELINC 'tl4INTKNANCK PERSONNEL OPERATING PERSONNEL 2.424 2 '16 0.000 0 F 000 0 018 0 F 000 1 ~

3.817 654 0 F 000 0 000 0 '09 0 ~ OCO HEALTH PHYSICS PERSONNEL

'UPERVISORY PERSONNEL Oeb78 0 F 000 0 ~ 016 1 ~ 431 De000 0 '19 1 e 031 0 ~ 000 Oe000 0.270 0.000 0.000 ENCINEERINC PERSONNEL 0 ~ 000 0 076 0 '96 0 F 000 0 019 De074 TOTAL "" tLAINTENANCE PERSONNEL 243 '23 1 ~ 000 270eb82 193.774 0 '39 143 '99 OPERATING PERSONNEL 53 ~ 101 1 ~ 172 Oe000 49 '47 0. 177 Oe000 HEALTH PHYSICS PERSONNEL 43 '46 0 F 000 62 '49 36 155 0 F 000 46.202 SUPERVISORY PERSONNEL 27.341 4,000 3e000 11 861 1 ~ 171 Oe698 ENGINEERING PERSONNEL 28 161 32e470 44 248 9.653 11.514 12 ~ 981

~ +iGRAND TOTALtt4 395 '72 38 '42 380 379 300 '95 13 F 201 203 e 180

2 A TE M L AFETY RE IEF VALVE HALLEN This section contains information concerning main steam line safety/relief valve (SRV) challenges for calendar

~ ~ ~ ~ ~ ~ ~

ear 1990 in accordance with the requirements of NUREG 0737, Item II.K.3.3, and as required by WNP-2

~

~ ~ ~

~ ~

echnical Specifications, Administrative Controls section, paragraph 6.9.1.5{b).

~ ~

There were no SRV actuations in the first quarter of 1990.

TYPE OF REASON FOR PRIOR PLANT POWER

~OX' COMPONENT ACTUATION ACTUATION CONDITIONS M~DR" ~DE ~E' LEVEL

~o ASSOCIATED

~ER 04/21/90 MS-RV-1A B D 15 04/21/90 MS-RV-2A B C D 14 04/21/90 MS-RV-3A B C D 15 04/21/90 MS-RV-4A B C D 15 04/21/90 MS-RV-1B B C D 14 04/21/90 MS-RV-2B B C D 15 04/21/90 MS-RV-3B B C D 15 04/21/90 MS-RV-4B B C '

D 15 04/21/90 MS-RV-5B B C 14 04/21/90 MS-RV-1C B C D 15 04/21/90 MS-RV-2C B C D 14 04/21/90 MS-RV-3C B C D 15 04/21/90 MS-RV-4C B C D 14 04/21/90 =

MS-RV-5C B C D 15 04/21/90 MS-RV-1D C D 14 Il /21/90 MS-RV-2D 04/21/90 MS-RV-3D B C D 15 04/21/90 MS-RV-4D B C D 15 These actuations were performed to test acoustic monitors.

04/21/90 MS-RV-1A C C D 04/21/90 MS-RV-2A C C D 04/21/90 MS-RV-4A C C D 04/21/90 MS-RV-1C C C D 04/21/90 MS-RV-3C C C D 04/21/90 MS-RV<C C C D 04/21/90 MS-RV-5C C C D 04/21/90 MS-RV-1D C C D 04/21/90 MS-RV-3D C C D 04/21/90 MS-RV-4D C C D These actuations involved "simmering" the valves for in-situ setpoint verification testing. SRV-2A was "simmered" six times; SRV-1D, four times; all other SRVs, two times.

~ Codes are explained on page 9.

~~ 2D manual operator not functional. Acoustic monitor verified on 8/6/90 prior to resuming operations.

2 2 MAIN TEAM LINE AFETY RELIEF VALVE HALLEN ES I,'Continued)

DATE 08/05/90 08/05/90 08/05/90

~

MS-RV-1A MS-RV-2A MS-RV-3A TYPE OF REASON FOR PRIOR PLANT COMPONENT ACTUATION ACTUATION CONDITIONS QQ(~DE~

C C

C CQDDE'DE C

C C

C C

C

'OWER LEVEL

~o 1.5 1.5 1.5 ASSOCIATED

~ER 08/05/90 MS-RV-3B C C C 1.5 08/05/90 MS-RV-4B C C C 1.5 08/05/90 MS-RV-SB C C C 1.5 These actuations involved "simmering" the valves for in-situ setpoint verification testing. Each valve "simmered" two times.

08/06/90 MS-RV-1A B C C 15 08/06/90 MS-RV-2A B C C 15 08/06/90 MS-RV-3A B C C 15 08/06/90 MS-RV-4A B C C 15 08/06/90 MS-RV-1B B C C 15 08/06/90 MS-RV-2B B C C 15 08/06/90 MS-RV-3B B C C 15 08/06/90 MS-RV-4B B C C 15 8/06/90 MS-RV-SB B C C 15 8/06/90 MS-RV-1C B C C 15 08/06/90 MS-RV-2C B C C 15 08/06/90 MS-RV-3C B C C 15 .

08/06/90 MS-RV-4C B C C 15 08/06/90 MS-RV-SC B C C 15 08/06/90 MS-RV-1D B C C 15 08/06/90 MS-RV-2D B C C 15 08/06/90 MS-RV-3D B C C 15 08/06/90 MS-RV-4D B C C 15 08/07/90 MS-RV-SB B C C 15 09/29/90 MS-RV-1B B C C 15 These actuations were performed to test acoustic monitors.

F urth uarter 12/07/90 MS-RV-1B 90-031 This actuation was in response to a unit trip.

~ Codes are explained on page 9.

0 I

22 AIN TEAM INE AFETY RELIEF VA V HA LEN (Continued)

'CD~:

e fAc 'n A. Automatic B. Remote Manual C. Spring Plant nditio A. Construction B. Startup or Power Ascension Tests in Progress C. Routine Startup D. Routine Shutdown E. Steady State Operation F. Load Changes During Routine Operation G. Shutdown (Hot or Cold)

H. Refueling Regs n for A t ati n A. Overpressure B. ADS or Other Safety System C. Test D. Inadvertent (Accidental/Spurious)

E. Manual Relief

+NOTE/: 1) Remote manual actuations occurred in support of acoustic monitor position indication calibration testing required by Technical Specification LCO 3/4.4.2.

2) Spring set testing was performed in accordance with ASME Section XI and Technical Specification 4.0.5 requirements.

MARY F PLANT PERATI N This section of the report responds to the requirements of Regulatory Guide 1.16, Revision 4, Section C.l.b.

Major safety-related corrective maintenance which is covered in Section 2.4.

10

J hlhl~ ' ':h hh GENERATOR l)OVEN SIIU'I'(J'l'AGE.Ol'I'-LINL'AIJSE I.ER i') hhTI'. 'L'i'~lh: 10l I I. C'.0 ')I. ('.0 'IB Nl llvlllf. 8 .'f'M C'.0 '0 Iig'~(.'L': Ec C.' ' PRf BNT C I.I.II I '.~C'.

I/30/90 S RB CON ROD Reduced power to perform a control rod sequence exchange.

-l/2 I /90 S 259 l. l RC PUEI..XX Plant shutdown as scheduled for refueling outage I45.

Outage extended due to the -failure of a Diesel Generator, 8/7/g0 S 4.55 0 l IIA MECPI JN Generator was removed from grid to perform overspeed testing of main turbine. It was then returned to service after successful cotnpletion of overspeed tests.

9/22/9t) S l being initiated at 40% power. Repairs were n>ade and the Itydfaullc system tested prior to returning unit to service.

l 0 . 0 . "~A (Continued)

GENERATOR SIIUT OU'I'AGE OPP-I.INE CAIJSE BONN LER J

~l) g'r: T+~~AU tS l'.OD: E.O: U CO PO+BBfg C IJ 0 0 R ~

F t IJRRB C>>

11/2/90 F 208.1 90-028 SF PIPEXX The plant was shut down after confirmation by NDE testing of a crack in a 3/4" drain line off HPCS injection header. The crack was repaired and NDF testing was performed on 104 welds on similar drains in the ECCS system prior to returning plant to service.

l I/28/90 F CII INSTR Ij I'ower was reduced due to feedwater level control difficulties caused by valve linkage problems.

I 2/7/90 I" 79.7 3 90-031 BB ELECON Generator tripped at 100% power following flashover to ground on a "8" phase high voltage insulator between the main stepup transformers and.generator disconnects. The damaged insulator was replaced and the remaining insulators were cleaned and inspected prior to restart.

0 TOTAL CII."NI.'RATOI( OFF-LINE

~C.' IS~C'.A~il 9R9 A 4 405.1 13 I 4.55 C I 2591.1 D 0 0 I'l 0 0 0 0 ll 2 0

'I'()'I'Al. 3000.75

2~3,'IIMMARJJ ALt~PI. gJ'l'1'.l<A'f'l{}g(ColllulUal)

SI JMh4ARY AF CAlil:.S SYSTEM c'ilgwu,c'o~g,'SLltl'g'p~o'~pl!T~lN) c'Al)li Sg TF > SCRI T AN I' I'ofcetl A - Equipment Failure I - Manual AA Air Conditioning, Ileating, Cooling &

Ventilation Controls S - Scheduled lk - Maintenance or Test 2 - Manual Scram Cl I Feedwater Systems & Controls C - Refueling 3 - Auto Scratn AC Onsite Power Systems & Controls D - Regulatory Restriction 4 - Conttnued I IA Turbine Generator & Controls I: - I".xternal Cause 5 - Reduced I oad I IC Main Condenser Systems & Controls F - Adn)inistration 9 - Other IIF Circulating V/ater Systems & Controls Cj - Personnel Error Otl>er Features of Steatn & Power Conversion II - Other Systems (not included elsewhere) .

IA Reactor Trip Systems RI) Reactivity Control Systems IeC Reactor Core Sl'.niergency Core Cooling System & Controls

COMPONEN'.I'I'YPL COMPONENT TYPE f

CAht~AQI.tf 'LQPPJCAI)Q ('.OMPA B F./CAD I CI.IJDFS'ontrol Roll Drive, Control Rod Dl'lve Mechanlsnl Mechanical Function Units Mechanical Controllers, l41eehanisnl (CONRAD) (M EC I'LJN) Governors Gear 13oxes Varid rives Iilectrieal Conductors 13)ls Couplings (Ill.t:('.AN) Cable Wire I'ipes, Fittings I'ipes (I'lI'Il>iX) Fittings I'uel 1)lenlents

~

(I'IJl I.XX) 'I'ul hines Steanl Turbines

('I'l.J R I3I N) Gas Turbines 1.

I lent I'xchangers Col)lie))sers Hydro Turbines (I I'I'I':X('.l l) Coolers 'olles Evllpl)fatl)fs Not Applicable Regenerative I eat Exchangers1 ('I.'IX')

Steanl Generlltol's I an Coll (Jnlts lnstrulnentation and Controllers Controls (I NS'I'Rl J) Sensors/Detectors/Elelnents Indicators Differentials

('I'otalizers)

'ntegrators Power S upi) I ies Recorders Switches Translnitters-Colnputation Mo<lules

2 4 ST NTFT ANT RRE VE MA NAN E R RMED N AF Y-RELATED E UIPMENT This section of the report is provided in accordance with the requirements of Regulatory Guide 1.16, Revision 4, Section C.l.b(2)(e).

16

2,~SLCigfLJC'.AgJ C.Q~RIiC"QVI'.J4fA~T ' C'B PBR ORML'I> ASSAI'E -RBI..D B IJIP B T ll()I I I PM EN'I' liCJI II III NCI PROBLEM klAIN- SYSTEM DLSCRIPTION CAUS)'. ACTION TAKEN

'I'I.'NANCI.

DSA-C-2C IIPCS I'ower- Witli tlie plant in a scheduled Tlie hydraulic unloader Hydraulic unloader assembly I)iesel Starting Air refueling outage, operators assenibly was found was replaced with new same perforniing tlie nionthly installed witli the ports 180 type assenibly and operability operability surveillance on the degrees out of alignment. was functionally verified.

higli pressure core spray diesel noted tlie air conipressor for the diesel starting air would not lo id to sufticlellt I)fessure.

h5-d2- Main Stean> Willi tlie plant in its annual I iises in llie nuitor operator Replaced tlie blown fuses and 8l3A6I) . ret'iieli>>g outage, inain control sliil'lel cubicle had blowll. took data with inconclusive rooin ol)erators attempting to open Iilectriciaiis ineggered, took results. No further work tile illillllstcani line inboard drain stroke tiine and ainperage performed at tliis time.

valve to inain coiidenser using tlie reailings after installing new handswitch observed the valve lusus, biit were unable to would iiiit open. Valve would not ileterniine tlie cause of tlie have opened reinotely, but manual blown tuses.

opt fiition was still available. This caused the main steam line to be degrailed. The plant was not affected.

n C CO C o .~n I B L'QUIP M L'NT I(EQlllRIN(i PROBI.EM MAIN- SYSTEM DES CI(IPTION CAUSE ACTION TAKEN TENANCE RCIC Reactor Core Isolatioa With the plant in a scheduled Coil on the close contactor Replaced bad coil with same S I I D3C . Cooling refueling outage, operators were did not piss resistance and type neW coil. Verified proper perforlning valve lineups as continuity checks. Cause of valve operation.

required to perfornl monthly bad coil unknown. This surveillance on the reactor core resulted in loss of the train isolation cooling system. While supplying the alternate water attempting to stroke the valve for source for the suppression alternative pool supply from open pool, but there was no effect to close position, the control fuses on the plant.

blew. 'I'he fuses w<<re replaced once, but again blew while trying to close the valve from the control rooII1.

I(CIC-A2- RL'actor Core Isolation With the plant in a scheduled Plant electricians found the Coil was replaced with same S I I I)3C Cooling refueling outage, the Inain control l25V I)C coil on the right type new coil and valve was rooIn rL.ceived a call reporting hand contactor had burned. stroked to verify operability.

smoke conling fronl a motor Cause of burned coil was control center. Operators un k n01vn.

responLled and noted the cubicle was for reactor core isolation cooling valve IO, which had just b<<en stroked under the 28-day operability surv<<illance.

2 4 II[CIiLRCC.'A~TCAUIlf C."~I~BAI TR C'.8 I'BRPO MI'.I'I 0 NA E T rqIJII MENT I( I!()I I I I( I NG PROI3I.I!M hjAIN- SYSTI!M DES CR I I'1'ION CA I JSI'. ACI'ION TAKEN

-'I'I!NANCE 1< PS-4'2- l4'.actof I fotectloll Plant was in Mode 5 (Refueliog) Tlie overload lieater block -

Replaced the overload heater h I G'2/h IS I duriog scheduled outage, when ihe was fL)i)oil burned. The block and the overload relay.

fcactof pfott.'ctloil systelo olotof cause of tlie burned overload Placed the asseolbly into generator set "I3" tripped oo heiitL'l block was unknown. service and verified proper startiog as iiidicateLI by a loain operability.

control rooio alario. Plant was in a Division II sclieduled oiitage, aod wlieo retiiroiog Division II to sefvlcL'hL'. reactor pfotect!L)ll systeol "l3" served by Division II tripped causing a loss of Train I3.

I<I'S-Ill'A-3I'eactor I'rotectioo Plant in Mode 5 for refueling Pailiire was traced tn the The circuit board and circuit

.outage, control roool received an circiiit bi)afit (piece part of breaker were replaced with alai'ol oil sllutilown cooling the circuit breaker) which new, like components. Tlie isolatioo due to an overvoltage trip was Ieiooved aod returned assembly was calibrated and on the reactor protective systeio to General Electric (GE) declared operable. Circuit electi ical protective asseolbly Niiclear I!oergy Division for boards will be modified to the channel "I"". Operators failure aoalysis. GE revised GE design.

reestablishcd shutdown cooling, siibsequeotly reported the but received two subsequeot caiise, of failure was an isolatioos after which the breaker engllleerlllg defect in the wool(i oot fL'.close. circuit board low frequency tiole delay function.

Cl 0

L'QlJIPM 1.N'1' 8 N\B~Llu'..'I'Ill'. hlkltl1~ '. s L)01 J I RING PI(0131.LM MAIN- ~ SYSTL)M DLSCRIP'fION CA 1JSI'. . ACTION fAKBN TI!NANCI!

RWCL J Nuclear Steam Supply During valve lineups prior to Previous repair of thermal Relanded wires correctly at the S21A413 Shutoff (NSSS) functional testing of the reactor blocks in the motor control motor control center thermal water cl<<anup system perfornled center done earlier in the block. Verified valve during the annual refueling outage had replaced the operation from the control outage, operators were attempting wiring for the control switch room handswitch.

to open the outboard containment operation incorrectly.

isolation valve using its hlul(lswllch In th('lilul con'tfol foDul. I he valve would not open using lh<<handswitch.

CITED-IICII- Control Rod Drive l)uring scheduled refueling Connector had worn out due Replaced worn out connector 1033 outage, the nlain control roon) t() overuse/overtightening. with same type new connector.

rcc<<iv<<d "Accunlulalor Trouble" Pressurized the instrument

'larm on Acculnulator 10-43 block and "Snoop" tested for which would not reset. Operators leakage.

investigat<<d and found nitrogen leal age at the acculnulator cap connector. Attempts to tighten the conne<<tor were unsuccessful in stopplug leakage.

EQI I I VMEN'I' EQI I I RI NCi PRO131.EM h<AIN- SYSTEM DESC.'Itl PTION CAIJSB ACTION TAKEN

'I'I)NANCE CRD->>Cu- Control Rod Drive Plant was in scheduled refueling Connector had worn out due Replaced the worn out 1839 outage when the nlain control to overuse a))LI/or over- connector with salne type ))L:w room received an "Accumulator tlghtcnlng. connector. Assembly was then Troubl>>" alarm on Accunlulator pressurized and "Snoop" tested 18-39. Operators investigated and for leakage with no leakage found leakage on the accumulator evident.

connector. Attelnpts to tighten the connL:ctof w>>re unsuccessful in stopping the leak.

. DCi-I!NCi-1131 Eluerge>>cy I'ower Plant in full power operation. The setscrew which holds Readjusted the trip lever arm During performance of lnonthly the trip lever arnl in proper and tightened the setscrew operability surveillance of the "8" position had not been properly. Checked all other cnlL'rgency power diesel engines, tight<<nell sufficiently engines for proper setscrew the engines tripped on.appar<<nt c;ulsing lhe arnl to slip on installation.

ovefsl)L:ed sigl)al with no the shaft to the, point where indication of actual overspeed it initiated the trip signal.

conditiL)n. Cal)se of loose setscrew tllought to be due to initial installation done prior to pl'ult slaf top.

C CA C..n.n EQU1PML'NT REQ(JIRlNG PROBLEM MAIN- DESCRlPTION CAUSE ACTION TAKEN TL<<HANCL'YSTEM DG-ENG- Eioergency Power During the 24 hoiir, foll-load run I:ailore analysis results The generator was repaired at DGl on the Division l emergency concliuled that the thrust an offsite repair shop. Repair diesel generator (performed during bearing failed due to loss of work consisted of bearing the outage to fulfillTechnical lubrication caused by replacement and rewindiog.

Specification requirements), tlie leakage of oil from the The generator was reinstalled generalor was tripped by conlrol bearing oil reservoir. and operationally tested. Since rooio operators diie to excessive l.cakage was caused by an the plant was already in an beariog leoiperature afoul inadequate o-ring seal as a outage, the plant effect was subsequent fire. 'l'he fire was resiilt of an extra o-ring that'tlie outage had to be extinguished and an unusual event groove machined into the extended due to Technical was declared at 1810 hours0.0209 days <br />0.503 hours <br />0.00299 weeks <br />6.88705e-4 months <br />. bearing.which prevented a Specification requirements for System redundancy was lost. tiglit seal. This extra two diesel generators operable groove did not appear on during power operations.

any design drawings and is considered a manufacturing det'cct.

I) l.O-llew-2132 l)icscl l.obe Oil During scheduled maintenance 0-riog seal liad failed, most Disassembled the flexible performed on llie Division I likely diie to wear. connection and removed the o-emergency diesel during scheduled ring. Replaced the o-ring with refoeliog outage, a diesel lube oil same type new o-ring.

leak at llie piping exiting llie Reassembled connection arid diesel lobe oil lieat. exchanger was verified ho visible leakage.

olisel'ved.

I'.()I I I Vtvl I.'O'I'(E()

I I I R IN(I PROI3I.EM MAIN- S YS'I'I"'M DIRAC RIPTION CALJSI ACTION TAKEN

'I'I)NANCI:

I') CW-I IX-I C III'CS Power - Diesel V/ith the plant in a scheduled Inspection of the tube sheet Tube sheet was reassembled Cooliog Water refueling outage and the high showed that the joint with new flange gasket aod pressure core spray diesel in al)p'Ireotly had been packing. A satisfactory ioaioteoaoce mode, operators asselobled without packing system leakage test was then noted that the diesel cooling water between the tube sheet and performed.

expansion tank required filling at shell joint. No visible least twice for the previous three daloage of the tube sheet (lays. I hey also note(l lhe oil wlls evltleot.

level io the engine so)op had increased io the saoie tiiue fraine.

A leak in lhe diesel cooling water to oil systeol was suspected l>SA-I'-3I3 I)iesel Slartiog Air Plant was in a scheduled refueling Contacts for decreasing A spare set of contacts on the outage. Duriog the perforo)ance presslire signal were saole switch were utilized to of biaooual calibration, the diesel degraded aod unable to restore the pressure switch to starting air pressure switcll for the allow circuit completion. tlie original configuration.

2 coolpressor failed calibration. Cause ot bad contacts was Calibration was then Tlie switch woo)ld not close on attributed to wear-out. performed successfully.

decreasing pl'essufe.

LQIJll'MI:NT It EAU I R IN' PROBI.EM hi AIN- SYSTEM DES CI( I P'I'ION CAIJSE ACTION TAKEN Tl:NANCE DO-I.S-21 IIPCS Power - Diesel Plant was in Mode 5, with the Instrument and control Technicians removed the I'uel Oil )node switch locked in refuel. technicians were unable to broken pieces of terminal During perfonnance of biweekly repeat the failure; however, block and verit)ed the switch diesel tlay tanl'perability they did Il))d and remove cycled properly through three surveillance, operators noted that two pieces of broken transfer functions, the level switch (to start the ten))inal block within the tra))st'er pu)up on low oil level) instru)uent housing. No was not t))ruing on the pun)p with other evidence of failure or

)J low level condition in the tank. (lan)age was found.

I III'hV-I'./P-l 5 I'cod water Nitl) the plant in a scheduled ,'I'he root cause was The instrument was replaced ref))cling ()otage, technicians were )n)hn~)wn. with a same type new per for)nhlg the 24 n)onth instrument. The calibration

'surveillance on the, current to was then performed pneu)untie converter to feedwater successfully.

flow ci)))trol valve "15". The converter wo)lid )lot operate repeatedly.

2 J Nfc'QIElc,'A)ifo'.0Rl<l.PQY~~A1 +Jl: ld~c'f. P~BPARMLI) APJ ~g+ < 1 I p I!()0 I VML'O'I' I"'()I I I I'( I N() PROBI.EM KIAIN- S YSTI'.M D)ACTII)'I'ION CALISI: ACI'ION TAKEN

'I'L'NANCE III W-I./I'-2A I'e<<dwater With the plant in its annual Cause of drifting problenl Removed defective unit from ref))eli>>g outage, Instrulnent and wits unknown. service and replaced with a Control (INC) technicians were new same type unit. The peffofnllng the 24 nlonth calibration was then calibration on the reactor feed successfully completed.

punlp I A discharge electlo/t)neunlatic converter Ill)w signal to lh>> te)npefalufe contfol v:live. 'I'h<< technicians were unabb. to calibrate the unit due to co>>tinu<<d drifting.

hIS-I(IS-f)(lllt I<<<acti)f I'rotectil)n I'lant op<<rating at full power. I'!x;lct c;<<lse unknown. lteplaced the drawer unit with I)uflug I)effolnlance of lnonthly 'I'hqse units have a history a spare sanle type drawer and surveillance test, main steanl line of problems, suspect end-of- finished perfonnance of radiation indicating switch "8" lile aging or wear-out. surveillance test satisfactorily.

channel was found with the setpoint out of acceptance range and, during attempts to recalibrate, it was drifting excessively.

I!QI I I I'kt I:O'I' L()till<I N(i PROBI.EM .

MAIN- SYSTI'.M DESCRI VTION CALISI. ACTION TAKEN

'I'I:NANCI.

h;IS-RIS-6IOD Reactor Protection Plant OI)crating at 100% Iiower. Voltage readings indicated Replaced "Jl" connector with Main control fooln of)eratofs signal input cable had loose same type new connector.

noted spurious downscale trips on sliield connection at "JI" Placed unit into service and tlie "D" cliannel niain steain line plug connector. Cause of observed iiornial operation radiation inonitor. loose connection was unknown.

I<I I I<-I'1'-15B I(esidual I Ieat I(enioval/Low Press Injection 'I'Iie During normal operation, an annual sllfveillance procedure was perfornied on tlie loop "B" residiial Iieat reinoval flow transinitter. It showed a very sluggisli response from iransniitter exliibited the saiiie syinpton>s of possible till oil loss documented by Nuclear Regulatory Coniniission Bulletin 90-01.

'I'he bulletin considers a fill Replaced with the saine niodel Rosemount transmitter from a different manufacturing lot.

The original flow transmitter was sent back to Roseinount to be tested for possible design or approxiinalely 15 mA/DC to 20 oil loss failure to be a manufacturing flaws.

mA/DC. It took tlie unit Rosellloilllt design appfoxllllalely 16 lnlnutes to inailequacy.

cliange by 5 mA/DC. System function was not affected because the transmitter only provides indicatioii for accident monitoring response.

Z~~Cg ~

C Cn KEMBWJIM:

IiQIJ I PM L'NT REQI JIBING

'I'L'NANCL'ROBLEM MAIN- SYSTEM DESCRIPTION CAI.JSE ACTION TAKEN R) W-DPT- .

Peedwater With the plant in normal full A flow transmitter The transmitter was replaced 4A power operation, operators downstreain of the level with a new same type observed the reactor feedwater indicator was found to be Rosemount transmitter from a level indicator "606A" would exhibiting signs of a manufacturing- lot subsequent occasionally drift as low as 23" possible fill oil loss failure to the fill oil loss problem.

reactor level (nornial is 35"). as docuniented in the The original transmitter has

'I'his resulted in a power spike due Nuclear Regulatory been sent to Rosemount for to level fluctuations since the level Commission Bulletin 90-01. testing and evaluation.

indication lias inputs to the feedwatir punip control and is, tlierefore, susceptible to sill)se(lilellt reactor level changes.

Ol)<<r itors tagged the "A" cllalillel olll of service.

~ g SLCQIP[C.~'JAIIRQC."I')VL~A~'~Q~C'+~l'.Ltml(MI.ll(i~Sf . - .I. D . IJ ~B EQI l I PM LJSI'CTION EN'I'(EQI J IR IN(j P ROB LI"'

h'I AlN- SYSTEM DESCRIP'I'ION CA TAKEN

'I'I!NANCI'.

Itl'1V-Dl'I'- I <<edwater Twenty four monlh calibration Atuplifter circuit board and Removed defective circuit 803C performed on the "C" tnain steam calibration circuit board, boards and replaced with new line flow transmitter showed the which are piece parts of the same type boards. Performed instruntent would not calibrate traustuitter, were found recalibration and returned within acceptance tolerances. The d<<fective. Most likely due instrument to service.

systenl was in a maintenance lo wear-out from age.

tnode during the annual refu<<ling outage. As found values were out of sp<<ciflcation below the manut'acturer's recommendations.

No 'I'eciutical Speciftcation requireiuents are associated with ibis instrun>e>>i.

2 IG C ORR E I ORME 0 F - I.

EQUIPMENT.

REQUIRING PROBLEM MAIN- ~ S YSTEM DESCRIPTION CAUSE ACTION TAKEN TENANCE RRC-PT-148 Reactor Protection This transmitter, which serves as This is a suspected fill oil Transmitter was replaced with the flow biased average power loss failure as addressed in a new same type transmitter.

range monitor trip signal to the Nuclear Regulatory -The original transmitter was reactor protection system, was Commission Bulletin 90-01. removed and sent to identified by Rosemount as Rosemount for testing to coming from a manufacturing lot confirm a'fill oil loss identified with a high failure rate condition.

diie to loss of fill oil as addressed in Nuclear Regulatory Commission Bulletin 90-01. This transmitter was replaced as a preventive measure.-

2 4 SIGNIFIC'.A T C'0 REC fIVE MAINTFNANCF.PER ORMI.D 0 SAF Y-REI.. E Ul E EQUIPMENT REQUIRING PROBLEM MAIN- SYSTEM DESCRIPTION CAUSE ACTION TAKEN TENANCE C

RRC-P f- l4D Reactor Protection This transmitter, which provides This is a suspected fill oil Transmitter was replaced with flow biased average power range loss failure as addressed in new same type transmitter.

nionitor trip signal to the reactor Nuclear Regulatory The removed transmitter will protection systein, is one Coniniission Bulletin 90-01. be sent to Rosemount for identified by Rosemount as testing to confirm a fill oil loss coming from a ruanufacturing lot condition.

with a high failure rate due to loss of fill oil as addressed in Nuclear Regulatory Cominission Bulletin 90-Ol. This did not fail, but was reniovcd from service in accordance with Rosemount's recominendation.

2 4 SJCINIFJC.'ANT C.'ORRFC'.TIVE MAINTFNA C.'F. PBRFORMBO O SAFET -REL TFD E IJIPMF.

EQII I P MENT REQUIRING PROBLEM MAIN- SYSTEM DESCRII'TION CAUSE ACTION TAKEN Tl NANCE RRC-P f-24B Reactor Protection This transmitter, which serves as Tliis is a suspected filloil Transmitter was replaced with the tlow biased average power loss failure as addressed in new same type Rosemount range nionitor trip signal to the Nuclear Regulatory transmitter. The removed reactor protection system, was Commission Bulletin 90-01. transmitter will be sent to identified by Rosemount as Rosemount for testing to coming from a inanufacturing lot confirm a fill oil loss identified with a Iiigh failure rate condition.

due to loss of fill oil as addressed in Nuclear Regulatory Coiiiiinssioii Biilletiii90-01. fhis did not fail, but was removed troni service in accordance with Rosemount's recomniendation.

C C C0 04 . 0 EQUIPMENT REQUIRING PROBLEM MAIN- SYSTEM DESCRIPTION CAUSE ACTION TAKEN TENANCE MS-I.T-26C Nuclear Steam Supply While conducting the yearly Pill oil loss in Rosemount Installed new transmitter and Sliutoff (NSSS) channel calibration performed transmitters are caused by a tested per surveillance during the refueling outage on the inanufacturing defect as procedure. This is a suspected reactor pressure vessel level tnitlincd in NRC Bulletin fill oil loss failure. The transniit ter loop "C", technicians 90-0l. original transniitter was sent to noted the transmitter was Rosemount for testing.

exhibiting a sustained drift. This is one of the symptoms of fill oil loss a Rosenlount trallsllllttef lnay exhibit inunediately prior tu failure.

RCIC-P-3 Reactor Core Isolation Plant in Mode l, 87, 5% power Bearing failed due to Installed new pump shaft, Cool lilg "Coasidown" to scheduled iinl)roper adjustn)ent on the inboard and outboard bearing refueling outage. Control roon> bearing oiler such that and seal covers. Returned received a "Reactor Core Isolation essentially no oil was pump to service and performed Cooling Water Leg Puinp Motor available for lubrication. a visual leakage test with no Overload" alum) and pun)p trip. 'l'liis caused subsequent leakage observed. All Operators closed the trip tlirottle pillllp slialt damage. replacement parts were the valve aiid declared systen) . same type as the original.

illopefilble.

2~~hi "/~C! )i~CQ~R>PIj+'~BMA

" . C'.. FRFARhLR~I) (1 SA . -R ..A F Il F F E(pl J IP M LN'I't EQl J ITIN(I PROIILEM MAIN- SYSTEM DLSCI<IPTION CAlJSB ACTION TAKEN TENANCL DO-P-1A Diesel Fuel Oil Willi tlie plant in Mode 5, The inipeller was found The pump was reassembled refueling outage, operators placed rubbing oil the pump bowl with new gasket material and tlic diesel oil fuel transfer pump because tlie thrust retaining the adjusting nut lock tab and into service for sampling of the bolt i)ad become loose when coupling spider were diesel day tank fuel. While tlic tile locking tab had come off reinstalled correctly. System puilip was running it exhibited as a result of incorrect effect was degraded clianncl excessive noise and vibration. positioiiing of the coupling since the pump would have Tile pilnlp was subscfllleliily taken sl)ilier. Most likely due to been able to operate, but nuit at out of service for repair. previous inaintenance. its designed performance capacity.

S I.C-P-18 Slanilby I.iquid During normal full power Crankcase cover bolts were Disassembled crankcase cover Coiitrol ol)cfiltion, pcl'solllicl on 'slril)pe(l illillallowed leak and cleaned gasket seating liiiulagellicllt ovcfvlcw touf noted tliri)iigli. Cause of stripped surfaces. Renloved worn an oil leak froih tile standby liquid bolts most likely due to gasket and replaced witli same coiltfol Ik punip hciul ai'ca. wear-oiit froin use. type new gasket. Replaced stripped crankcase bolts witll new longer bolts and torqued to 90 inch-. pounds. Vcrilied no visible leakage.

I'.QI) II'MENT Rl'.Q0 I R INCi PROBI.EM MAIN-TI'NANCE SYSTEM DESCRIPTION CAIJSI.'CTION TAKEN MS-RV-I B Main Steam During annual channel calibration I'lant electricians found a The connector was surveillance perfornied during the pin in tlie electrical disassembled and the pin refueling outage, the main steam "Cannon" plug connector pushed back in place. 'I'he relief valve "IB" would not open puslied back sucli that no connector was reinstalled and by n>cans of its handswitch located continuity lo the solenoid the surveillance was completed in the, niain control roon>. This was present. Cause of satisfactorily.

resulleil in a loss of llie "IB" niisplaced pin was unknown.

relief valve, liiit tliere was no signiticant effect on tlie plant due lo systeni design redundancy.

I(CIC-V-I l I Reactor Core Isolation Witli the reactor at 8 percent Valve internals were stuck Valve was disassembled and

(.Ooli lig power and Iiolding, awaiting the iliie to lack of adequate internals were cleaned and reactor core isolation system liibrication and dirt buildup, lubricated. Valve was operability test performance caiise uiil'nown. reassembled and flow verified.

following repair on an isolation valve, tlie 2" check valves on the turbine exhaust vacuuin relief line were loilllilslilck closed. Valves are iequireil open for increased power operation, so plant slartup was delayed for valve repair.

L(jiI I PM EN'I't I:QtII I( I NCi Pl(OI)I.EM MAIN- SYS'I'EM DESCliIP I'ION CAUSI'. ACTION TAKEN

~

TENANCE ILCIC-V-II2 I(eactnr Core Isolation Witli the reactor at 8 percent Valve internals were stuck Valve was disassembled and Cooling power and holding, awaiting the due to lack of adequate internals were cleaned and reactor core isolation system lubrication and dirt buildup, lubricated. Valve was operability test performance cause unknown. reassembled and flow verified.

following repair on an isolation valve, the 2" check valves on the turbine exliaust vacuum relief line were found stuck closed. Valves are required open for increased power operation, so plant slartup was delayed for valve repair.

2 4 /ICE@'ICA~C'.Ag~l.C".DVQJvfAltt'I'~I'. M~rt'.~r<<I'O<<M<:.n O~g B IJ /@FAT EQUI PM EN'I'EQl J I I( I NCi PROI)I.EM MAIN- SYSTEM DESCIIIPTION CAIJSE ACTION TAKEN

'I'EN ANCE IICIC-V-8 I(caclor Core Isolation Post oiodification testing on the A roiitiiie review of the Troubleshooting efforts Cooliilg reactor core isolation cooliog procedure performed on identified a lack of sufficient steam siipply to tile turbioe August 18, 1990 discovered lubrication on the valve stem isolation valve required the tlie excessive closing time from ioadequate maintenance.

pcrforoiance of the Technical data. After evaluation and Valve stem was lubricated and Speci llcatioo surveillance test on retesting tlie valve was the operability surveillance test thc valve resiilting io a 10.8 (lccl life(l inoperable. Had was performed satisfactorily.

secooll closiog tiole. The tile valve been required to procedural actioo range, based on perform its safety fuoction, ASMI: puolp aod valve in-service tliis condition alone woold test prLigralo criteria, is less tlian oot li>>ve resulted in a failure or at 10 secoods. During review ot lhL: vlllve to isolate.

aod apl)roval of the surveillance procedure, ilo oile noticed the excessive closiog time which shool(l hilve fl:suited in declariog tile valve aod the system inoperable witll a 14 day limitiog cooilitioo for operation, and a 4-liour valve liloitiog condition for OPL'.fillinn.

L'(lII I PM) N'I' I:QI)I RI NCi PROBI.EM MAIN- SYSTEM DESCI(IP'I'ION CAIJSE ACTION TAKEN TENANCE IIII R-V- I I I A Residual Heat During scheduled refueling Packing material had worn Removed a couple of layers of I(eniuval/Low Press outage, with tlie "A" loop residual out. the old packing and repacked Injection heat reinoval systeni in with new material in a iuaintenance/test mode, operators sufficient amount to return the on toiir noted an excessive packing flange to its correct packing leak from the l4" gate position. Reinstalled packing valve on tlie retiirn to tlie reactor flange and torqued gland nuts.

pressure vessel. Operators noted Performed a visual leak test tlie valve probably needed packing with no evident leakage.

since tlie fullower had bottoined out.

DSA-RV-9ll Diesel Starting Air During perfonnance of annual lift Valve seating surfaces were Valve was disassembled, test, tlie relief valve servicing the fouled with rust/corrosion cleaned, and inspected in diesel starting air tank "5D" an(l would llot seat properly. accordance withplant exhibit<<d leakage past the seat. procedures. Valve seat was lapped and valve was reassembled and retested satisfactorily.

DSA-V-32A Diesel Starting Air With tlie plant in normal full Exact cause of valve Faulty valve was reinoved and power operation, operator on tour sticking open was unknown. replaced with new same type noted tlie drain valve for the diesel valve. System was pressurized starting air receiver would not and visually checked for close wllell lliallilallyoperated. leakage.

S 0

I <QI 1 I PM 1.'NT R O'QI I I Rl NCj MAIN-

'I'liNANCL'YSTI'.M PROBI.EM DESCR I O'I'ION CAlISL'CTION TAKEN SI.C-RV-2&13 Standby I.iquid During annual safety relief valve Seat leakage was due to Seating surfaces were Control testing perforn>cd during tl>e nozzle dunnage resulting machined, valve was bench-scheduled refueling outage, the froni forcig>> material tested satisfactorily, and relief valve for standby liquid between tl>e nozzle and disc, reinstalled in the system.

control pump "10" showed leakage past the seat.

SI.C-RV-29B Standby I.iquid During annual safety relief valve Seat leakage was due to Seating surfaces were Control testing perforn>ed during the nozzle damage resulting machined, valve was bench-sclteduled refueling outage, the from foreign material tested satisfactorily, and relief valve for standby liquid between the nozzle and disc. reinstalled in the system.

control pump "IB" showed leakage past the seat.

list I I P M IDENT R I.'Q t J I I< I NCi PROI)l.l'.M MA IN- SYSTI'M DISCI( I PTION CAt JSI'; ACTION 'I'AKEN

'I'IiNANCI."

C'AC-l:CV-lA Coinbustible Gas During local leak rate testing Valve seating surfaces were Valve was disasseinbled and Control perforo>ed during tt>e annual found not niating properly, the seating surfaces were refueling outage, the containment tnosl likely due to wear-out. lapped. A blue check was atmosplteric control drywell performed to verify a good suction outboard isolation valve seal. Valve was returned to did not >neet local leak rate- service and a satisfactory local acceplance criteria. Leakage -

leak rate test was performed.

crit<<riu I'or tlute entire containiu<<nt isolation systen> was within specittcation, so there was no syste<n or plant effect.

CAC-I'C.'V- I lt Coinhustible Gas During annual local leak rate test Valve seating surfaces were Valve was disassembled and Control of tl>e containment atmospl>eric not mating properly to seating surfaces were lapped.

control containinent isolation provide a good seal, tnost A blue check was performed valve, tlute valve exhibited high* likely due lo wear-out, to assure a good seal. Valve leakage. Although this valve was returned to service and a leakage was out of specification satisfactory local leak rate test for leakage, ttte total containtnent was performed.

leakage was within specification so tl>ere was no system or plant effect.

'!-!I'!~BC'~*!!IlRIM".l

-8 '"- !'"'"-'.~!I-I!QI.JIPML'NT R IiQIJ IR I NG PROBI.EM MAIN- SYS'I'EM nI>cail I ION CAUSE ACTION TAKEN

'I'L'NA NCL'AC-PCV-48 Combostitile Gas With Iilant in scheduled refueling Valve seating surfaces were Valve was disassembled and Cootrol outage, the containment not oiatiog properly due to seating surfaces were lapped.

atoiospheric control discharge to wear-oui caused by Valve was reassembled and llie wclwell outboard cootainineot corrosiioi. leak test was performed isolation valve showed leakage satisfactorily.

thro<<gli tlie seat during perforoiaiice of ihe 24 ioo>>th leak test surv<<illaoce.

CAC-V- l3 Coiobiistible Gas Wilh tlie plant in an annual Illsl)eclloll of the valve The brass imbeddment was Coolrol rel'ueliog outage, tlie oiotor r<<ve;iled a sioall piece of, reinoved and valve stem operator for tlie contaiooient lirass i>>iliedded in the root threads were cleaned. The aloioslilieric control 4" gale valve llir<<ail of tlie valve stem valve was electronically to coolaioioeot tripped ils causiiig Ihe sleoi nut to gall stroked and stroke time overloads with tlie valve 10 tlie stein. Cause of brass verified within 'I'eclinical perceot frooi closed seat ii>>b<<ildloelit was illiknown. Speci ficatioo acceptance range.

iodicalion. 'Iliis resulted io a loss of one of the four trains serving coolaioioent, but oo significaot plaot effect. 'I'lie systcoi was io lllaililcliallceat tile tililt: of discovery.

al-Mt~I"BzM!~M'": .".L~~ "ti, I': ' '. BL L'QlJI PM LNT Ikf QljIliINCI PROBI.EM MAIN- YS'I'L'M DESCI(IPTION rAtISI: ACTION TAKEN

'I'L'NA NCI.'

I I PCS-V-23 IIigh Prcssure Core During performaoce of the high 'I'lie root cause of tliis event Faulty valve was temporarily Sl) fity l)fcssilfe cofc spray systelll was ao ioadequate torque isolated to prevent systeni flow opcrabilily surveillance test, llie swilcli suiting on the valve. diversion. The torque switcli test rcturii valve to tlie siipprcssion setting was increased and tlie pool failed to go fullshut. The valve was satisfactorily tested.

valve indicated full closed, but tlie oiioiioiiio flow valve did oot cooic open aod flow iodicatioo ilid not go to zero. Tliis caiised the itiversio>> of systcio flow frooi spray.

tli'n-vessel MS-h;IO-160C Maill Stealll During normal full power 0-rings liad evidence of Disassembled fittings at operation, operator on turbine wear iloc lo cyclic aging. accumulator and replaced o-buildiiig tour observed oil leakage ring with same type.

at tlic oiaio sleaoi bypass valve l(eassembled and verified no hydraulic operator. Oil was leakage visible.

.leaking frooi lhe fitting going into the top of tlie accumulator.

a~snq~ir r~ rnRRrr". vi'. H CBPER ARMI.11AhfSAF. - E.. UP B T I'.quil MEN r R I'.FIJI RING PROBI.EM MAIN- SYSTEM DESCRIPTION CAlJSI'. ACTION TAKEN

'I'ENANCE MS-MO-68 Main Steanl During the annual refueling I'.Iectricians found the local The indicator was positioned outage, operators attempted to position indicator at the to show correct position open the main steatn line outboard valve operator was showing indication and the nuts were drain valve to drain to the reverse indication. The tigt>tened. Tive valve was condenser from a handswitch in indicator consists of 2 nuts stroked electrically to verify the main cdntrol room. flic valve with a waslier in between, proper operation.

blew all tliree niain line fuses as the nuts were loose; most sltown by loss of indication in tive lil;ely balue to earlier work

, tnain control rooin. Tltis resulted perl'onned on tl>e operator ih a loss of tive retnote operation tl>is saiue outage.

of tlute outboard drain function, but no sit,nificant plant effect.

0 2~SQ+IQCQQT COIQBC~IV I . CB BRI ORM .D ON 8 -BLTBD. 711 B EQIJIPMLNT RI.'Ql I I RING PROBI.EM MAIN- SYSTEM DESCRIPTION CAIJSE ACTION TAKEN

'I'ENANCII MSI.C-MO- Main Steam During performance of annual Unscltcduied splice was Damaged section of cable and lA motor inspection, testing, and tound witlt pinched wires splice were removed and a

<naintenance procedure, a sl>ort to due to incorrect installation. new splice was performed.

groun(l was found wl>ile The procedure was then meggering tive motor for tl>e tnain completed satisfactorily.

stean> leakage control valve "lA"

{inboard exhaust to the reactor huil(ling). Systetn design is such that system retnains functional witli loss of a single con>ponent, so this failure, resulted in degraded pertorn>ance for the "A" train.

0 I."Q(JIPMENT I( I:QIJ I RING PROBI.EM MAIN- SYSTI'M D)SCRIPTION CA) JSI'. ACTION TAKEN Tl'.NANCE RCIC-MO-8 Reaclor Core Isolation During perfonnance of a quarterly 'I'he cause was unknown, Limit switch number 8 of rotor Coohog surveillance perfonoed at full but susp<<cl IIIoit switch was 2 was adjusted to 94 percent power, it was discovered that oot of adjostmeot. of full stroke to pass the

.reactor core isolation cooling inlet surveillance requirements. An turbine valve closing tiIoe was less engineering analysis was than the value listed in the performed to change ihe valve Technical Speci fications. stroke length to provide both Allhoogh the reaction closing liole satisfactory stroke liroes aod was slower lhIul fe(luired, it did adequate steam supply, not atlect systeIo or plaot operation. The valve deIooostrated foll opening and closiog capability.

RII R-MO- CootaioIoeot Spray Plant operating at l00% power. I'lant electriciaos Removed and inspected torque 16A During perfonnance of quarterly IlisasscoIblul the valve switch for any other damage.

surveillance oo loop "A" residual opeI'Ilol'od found torque Replaced the sante torque heat r<<Iooval system operability, switch contact llogers out of switch in the operator, the motor operator for the upper aligoIoeot, preventing installiog it with proper drywell spray outboard isolation contact closure. Cause of alignment. Verified operator valve would not close completely aligooIeot problem opened and closed the valve.

electrically. Operators manually unknown.

closetl lhe valve anti de-energized the valve operator.

IlQUIPMEN'I'

-I(I:@II lltlNCl PROBI.BM hIAI¹ SYSTEM DESCRI 1'TION CAUSE ACTION TAKEN

'1'I:.NANCE IIPCS MO-I I I ligh Pressure Core With the plant in a scheduled Valve was found stopping Limit switch was adjusted to Spray refueling outage, operators were approximately six hand stop open movement at 90.S performi<<g the suction transfer wheel turns from backseat. percent. Valve was o'perability surveillance when the Cause of the valve being out satisfactorily tested.

high pressure core spray return to of adjustment is unknown.

ihe co<<de<<sate storage tanks valve I'his <ious not reduce the oper ltor I'ept tripping the breaker flow to lhe core spray in whe<< tile valve went ln the open thill ll<<lre Is lulothef directio<<. islllalio<<valve upstream of this valve that was lunctlonlll

2 INDI ATI N F FAILED F L is section is provided in accordance with the requirements of the WtTP-2 FSAR, Section 4.2.4.3 and Regulatory Guide 1.16, Revision 4, Section C.l.b.(4).

A visual inspection of discharged fuel from WNP-2, Cycle 5, was performed from July 31 to August 3, 1990.

The purpose of the inspection was to verify assembly and fuel rod structural integrity of discharged fuel. In addition, a visual inspection of selected discharged fuel channels was performed at the same time. An inspection of the suspected Advanced Nuclear Fuels (ANF) leaker was performed by ANF on May 22-24, 1990. Inspection of the three suspected General Electric (GE) leakers was performed by GE on July 26-30, 1990. The results of these inspections are summarized herein.

MMARYOF IN, PE TI NR LT Inspection of suspected leaker XN-1114 by ANF identified fuel rod A07 as failed and A08 as damaged. The appearance and position of the damaged areas indicate fretting from a non-fuel-related object.

Inspection of suspected leaker LJT799 by GE identified rod F02 as failed. The failure mechanism appeared to be accelerated corrosion or Crud Induced Localized Corrosion (CILC). The remainder of the assembly appeared normal.

nspection of suspected leaker LJT653 by GE identified rod Cl as failed. The Cl rod was broken between seven and ten inches above the lower end plug. The specific failure mechanism has not been identified.

Inspection of suspected leaker LJT749 by GE identified rod D6 as failed. The cladding was heavily corroded and spalled. The failure mechanism appears to be (CILC).

A total of eight assemblies and three channels discharged at the end of Cycle 5 were inspected. No evidence of mechanical damage, geometric distortion or rod bow was observed. All rods inspected appeared properly seated in the lower tie plate. All spacers appeared to be in proper position. The fuel cladding was covered with heavy crud and, in some instances, showed signs of slight spalling.

Inspection of the three channels revealed heavy crud deposition and some evidence of corrosive interaction with the upper guide. No evidence of unusual behavior was observed.

46

HAN T AND XPERIME Federal Regulations (10CFR50.59) and the Facility Operating License (NPF-21) allow changes to be made to the facility and procedures as described in the Safety Analysis Report and tests or experiments to be conducted which are not described in the Safety Analysis Report without prior Nuclear Regulatory Commission (NRC) approval, unless the proposed change, test or experiment involves a change in the Technical Specifications incorporated in the license or an unreviewed safety question. In accordance with 10CFR50.59, summaries of the permanent design changes and temporary plant modifications completed in 1990 are provided. Included are summaries of the safety evaluations.

0 2 PLANT M DI I ATI N

{. ermanent Plant Modifications at WNP-2 are implemented with a Plant Modification Request (PMR). The ollowing PMRs implemented in 1990 required a Safety Evaluation in acc'ordance with 10CFR50.59. Each permanent change was evaluated and determined not to represent an Unreviewed Safety Question nor require a change to the WNP-2 Technical Specifications.

2.6.1.1

//~9~2 PPM ~2 This PMR modified the Control Room HVAC System. Control Room Humidifiers were disabled and the Control Room HVAC Procedure (PPM 2.7.1) was revised due to operational problems with the units.

Excessive condensation in the supply ducting and subsequent "rain-out" of the supply register would occur during Humidifier operation.

The FSAR states that the Control Room humidity would be controlled by Humidifier WMA-HU-55A/Bbetween 30 and 50% during normal operation. A Hygrothermograph was used to collect humidity data in the Control Room. The ventilation system is always in the cooling mode; therefore, the humidity is naturally stable. The data collected indicated 17 to 30% relative humidity. The FSAR limits are for personnel comfort. The American Society of Heating, Refrigerating, and Air-Conditioning Engineers (ASHRAE), which sets the HVAC tandards, recommends 20 to 60% Relative Humidity for human comfort.

v Disabling the humidifiers is a modification that did not result in a change to the WNP-2 Technical Specifications and the Unreviewed Safety Question evaluation concluded that (1) the performance of the Control Room ventilation system met all requirements, (2) the margin of safety provided in the Technical Specifications was not changed, and (3) the boundary conditions for the FSAR evaluation were not changed.

2.6.1.2 Plant Modification 85-0744 was initiated as a product improvement modification to the HPCS Diesel Air Start system's pressure switches for the air compressors.

The set points for Diesel Start Air Pressure Switches 15 and 16 (DSA-PS-15 and 16) were changed in a more conservative direction as a result of the deadbands of the new switches. This prevented excessive wear on the diesel driven air compressor by allowing the motor driven air compressor to maintain more air in the tanks.

It also coordinated the alarm switches better to the compressor switches.

48

(.

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e Safety Evaluation showed that the proposed change would not increase the probability or consequence of an accident or malfunction of equipment important to safety since the change increased the overall reliability

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of the HPCS Diesel Air Start System.

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'I 2.6.1.3 4-Main Steam Valve 22A (MS-V-22A) stuck in the close position in 1988. This PMR was the modification to the internals of the remaining four Main Steam Isolation Valves (MSIV) MS-V-22B & C and 28 B & C. The first four valves were modified during the 1989 refueling outage. The modification made the valve operation smoother and more reliable.

The change decreased the amount of friction that must be overcome to close the valve and reduced the chances of galling of the valve body bore. The new disk-piston assembly and stem/stem-disk assembly are lighter than the original valve internals. The new disk piston also has a grey cast iron rider ring.

v r

The replaced valve internals improved the overall reliability of the valves and did not affect the valve function.

No change to the WNP-2 Technical Specifications was necessary since the Technical Specifications do not describe the internal details of the assembly. There was no Unreviewed Safety Question since the function of e valve did not change and probability of failure decreased.

2.6.1.4 Plant Modification 89-'0198 was initiated to modify the cooling water supply to the Division I and II Emergency Diesel Generators. Normally closed air operated butterfly valves SW-V-214, 215 (Div I) and SW-V-216, 217 (Div Il) were completely removed from the cooling water supply lines to their respective diesel jacket water heat exchangers to enhance diesel reliability. ASME qualified spacers (i.e. "spool pieces") were installed in place of the wafer style butterfly valves.

One of these four identical valves previously had suffered a disc-to-stem separation because of corrosion of the pins that held the disc to the stem. In evaluating alternative design changes to correct the problem, it was determined that the valves actually served no purpose relative to either the diesel generator or the cooling water system (the diesel keep-warm system is unaffected by the presence of cooling water through the service water side of the jacket water heat exchanger). The valves had been supplied as a part of the diesel skid because the diesel vendor anticipated that, depending upon the design and limitations of the customer's cooling water system, it might be desirable to isolate the cooling water from the diesel when the diesel was not running.

af Ev1 mm

~

Because the WNP-2 emergency service water system is dedicated to safety-related loads and is properly balanced when all loads are in service, isolating the water when the diesel was not running served no real purpose. ~ Additionally, from a diesel reliability standpoint, having the valves closed actually posed an 49

~

challenge to diesel's ability to meet its safety function since the valves had to open from their

~

unnecessary ~ ~ ~

ormally-closed positions for the diesel to receive adequate cooling. Deleting the valves solved the corrosion

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roblem with the added benefit of enhanced diesel reliability. This modification did not result in a change to

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the WNP-2 Technical Specifications or involve an Unreviewed Safety Question because the margin to safety

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as defined in the basis of any Technical Specification was not reduced,-nor was the possibility of a different accident or malfunction as previously evaluated in the FSAR created. The probability of occurrence or the consequences of an accident or malfunction of equipment important to safety previously evaluated in the FSAR was also not increased.

2.6.1.5 This Plant Modification removed all controls, displays, and alarms associated with the Steam Condensing mode of Residual Heat Removal (RHR) operation. The Steam Condensing mode of RHR operation will not be used at WNP-2 and these deactivated controls, indications and alarms in the control room and remote shutdown panels were no longer required.

fet v I i n umm This change did not result in a change to the WNP-2 Technical Specifications or involve an Unreviewed Safety Question because: (1) the margin of safety in the Technical Specifications was not reduced by the removal of these deactivated components, and (2) the analysis in the FSAR did not take credit for the Steam Condensing mode of RHR operation. ~

2.6.1.6

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The Emergency Control Room Chillers would auto start when all permissives were met. This resulted in unwanted Emergency Control Room Chiller starts. The change provided a manual switch in the Control Room to remotely start the chillers. This change only affects how and when the Emergency Control Room Chillers are to be started and does not affect the actual operation of the chillers.

Safet Ev lua i n ummarv This modification did not result in a reduction in the margin of safety to the WNP-2 Technical Specifications or involve an Unreviewed Safety Question. The analysis concluded that a manual start of the fans could be performed by Plant Operations with no decrease in overall plant safety.

2.6.1.7 This PMR changed the power source to the "Z" Signal Trip Units. The "Z" signal trip units are radiation monitors that have GM detectors mounted in the Reactor Building Ventilation exhaust plenum. They provide a trip signal to relay logic in Relay Cabinets RC-I and RC-2. These Relay Cabinets initiate an NSSSS Group 3 (Reactor Building and Balance of Plant Containment) Isolation.

50

This change was made to eliminate ESF actuations that occurred when power was lost to the "Z" signal trip nits. Before, the change power was supplied from the Reactor Protection System (RPS) Motor Generator Sets A and B. When an "MG set trip" occurred, a "Z" signal trip would be initiated. This provided unnecessary actuation of equipment such as Standby Gas Treatment, shutdown of normal Reactor Building Heating 'and Ventilating Systems, and startup of ECCS Motor Control Center Room Fans. This change provided divisional uninterruptable power from Inverters IN-2 and IN-3; thereby preventing unnecessary actuation. The change also corrected some problems with the implementation of fail-safe design requirements.

f Ev 'n m This change did not result in a change to the WNP-2 Technical Specifications or involve an Unreviewed Safety Question. This change did not change any of the system functions. It improved the reliability of the power supplied to the trip units and corrected the discrepancies between the present configuration and the WNP-2 design requirements for fail safe circuits.

2.6.1.8 PMR 8-Plant Modification 88-0038-04 replaces existing high maintenance recorders with current technology-based low maintenance units. The following process recorders were replaced:

1. PI-COMP-TR618A, spared in place trend recorder
2. RRC-FR-614, Recirculation Flow.
3. RRC-TR-650, Recirculation Pump Suction Temperature.
4. RCWU-CR-601, Reactor Water Cleanup Inlet Conductivity. Conductivity High/Low alarms functions are now generated internal to the recorder.
5. RWCU-CR-603, Reactor Water Cleanup Outlet Conductivity.

The modification changes are Class II and Seismic 1M that follow the original design intent. The new equipment is mounted with approved seismic mounting and hardware.

afet Ev 1 ati n umm This modification has followed current design criteria for seismic mounting, separation, and isolation.

Therefore, the addition of the new recorders did not result in a change to the WNP-2 Technical Specifications or result in an Unreviewed Safety Question because the margin of safety was not reduced or the possibility of an different malfunction as defined in the basis for any Technical Specification was not increased.

2.6.1.9 PMR8-Plant Modification 88-0038-06 was initiated to remove AR-RR-21, Mechanical Vacuum Pump recorder, and install a new recorder, SW-RR-1 in the same panel. The new recorder monitors the Mechanical Vacuum Pump outlet (moved from AR-RR-21) and also the liquid radwaste discharge and service water effiuent (RHR Loop A).

This modification makes the information required for 10CFR20 monitoring more readily available with the addition of the new recorder.

51

fe Ev 1 ai is modification has followed current design criteria for seismic mounting,'eparation, and isolation.

Therefore, the addition of the new recorder did not result in a change to the WNP-2 Technical Specifications or result in an Unreviewed Safety Question because the margin of safety was not reduced, nor was the possibility of an different malfunction as defined in the basis for any Technical Specification increased.

2.6.1.10

~R Plant Design Change 88-0041 was initiated to modify two of eight Primary Containment annulus drain lines, removing the existing blind flanges and replacing them with a flange and 3/4" drain valve on each drain line.

The other six drain lines were previously modified in 1984 to include drain valves such that, in the closed position, the ECCS pump rooms would remain isolated from each other in case of room flooding, but would

,allow periodic monitoring of the drain lines (by opening the drain valves) to check for evidence of water in the annulus sand pocket region. The two lines modified under Design Change 88-0041 were not modified in 1984 due to their location. These lines terminate in the Reactor Building crane bay and, as such, would provide a direct path from Secondary Containment to the outside environment if the drain valves (ifpresent) were open and the Reactor Building crane bay doors were open. However, in light of recent concerns over the possibility of Primary Containment wall corrosion in the sand pocket region (NRC Generic Letter 87-05), WNP-2 determined that a means to periodically monitor the drain lines in the crane bay was necessary, and that administrative means would be employed to assure that Secondary Containment would not be breached by the opening of the new drain valves when the crane bay doors are open.

This modification provided a means to monitor the sand pocket region of the south quadrant of the Primary Containment annulus on a frequent basis without removal of a blind flange. Equipment Operator rounds include a weekly verification that no water is present in these two (and the other six) drain lines. The modification consisted of replacing the altering the existing blind flange design, adding a welded pipe nipple and 3/4" globe valve to each location.

fet Evaluation umma This modification did not result in a change to the WNP-2 Technical Specifications or involve an Unreviewed Safety Question because the consequences of an accident (affecting offsite dose limits) are not changed. The added drain valves are locked-closed valves and have caution labels mounted above them stating "Do Not Open This Valve When The Crane Bay Doors Are Open". Additionally, the applicable plant procedure governing the opening of the crane bay doors when Secondary Containment is required (Operating Conditions 1, 2, &

3) was revised to include verification of the locked closed status of these drain valves prior to opening the crane bay doors.

52

2.6.1.11

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- 2 C

PMR 88-0264-1 was initiated to provide power and control for the motor operator for non-safety related valve RFW-V-14. Position limit switch contacts on Class 1E valves RFW-V-65A and 65B were used to restrict

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operation of RFW-V-14. The interlocks with valves RFW-V-65A and 65B will eliminate a potential reactor vessel drain down path which could occur during Long Cycle RWCU System operation ifvalves RFW-V-65A or 65B were opened while RFW-V-14 was opened.

fe Evl i n mm This modification did not result in a change to the WNP-2 Technical Specifications or involve an Unreviewed Safety Question because the margin of safety was not reduced nor was the possibility of a different accident or malfunction as defined in the basis for any Technical Specification increased.

2.6.1 12=

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This Plant Modification changed the Anticipated Transient Without Scram /Recirculation Pump Trip (ATWS/RPT) logic from a one-out-of-two to a one-out-of-two twice actuating device logic. In addition, a contact was added to the test switch circuit to allow testing of the 147 tripping relay without actually tripping the respective recirculation pump.

afet v 1 i n mm his change did not result in a change to the WNP-2 Technical Specifications or involve an Unreviewed Safety Question because the Technical Specifications did not describe the logic to be used and the change decreased the probability of system failure.

2.6.1.13 PMR -02 9-1 Plant Modification 88-0299-16 was initiated to relocate Main Steam Pressure Transmitters (MS-PT-8A, B, and C), and add piping supports inside the condenser. These pressure transmitters are non-safety related and measure main condenser absolute pressure. The change did not degrade or affect any Class I system. The Unreviewed Safety Question Analysis was required by procedure because FSAR figure 3.2-23A, Turbine Main Exhaust and Steam System, was changed to show the new pressure tap locations for the transmitters. The original design intent was maintained.

afet Eval ai n umm This modification will not result in a change to the WNP-2 Technical Specifications or result in an unreviewed safety question. This modification maintains the original intent to monitor condenser pressure. The addition of supports inside the condenser will lessen the probability of an already analyzed condition.

53

2.6.1.14 MR - 2 e existing deactivated CIA compressors on 501'levation of the reactor building were occupying valuable space. It was determined that the area was required for better access to the drywell during outages and this Plant Modification Record (PMR) was implemented to remove the compressors.

4 Ev 1 i The CIA compressors were designed to be the backup system for the cryogenic nitrogen source. During the, 1988 refueling outage the CIA compressors were eliminated as a supply source by capping the common discharge line. The compressors are not safety-related and are not addressed in the Technical Specifiicatiions.

The physical removal of the compressors does not increase the probability of an accident or create a different type of accident.

2.6.1.15 PER '~1(

During reanalysis of the RFW System piping for snubber optimization inside primary containment, it was iscovered that the Architect/Engineer's (A/E's) analysis for determination of operational clearances between he RFW pipe whip restraints and RFW piping had neglecte'd to consider certain thermal transient events which occur periodically during normal plant operation. When the piping thermal movements under these transient conditions are factored into the clearance calculations, it is revealed that there is a possibility that RFW piping could contact the pipe whip restraints during some plant shutdowns, startups and scram events. A Justification for Continued Operation (JCO) was completed as part of Problem Evaluation Request (PER)90-109. This JCO concluded that Plant Operations could continue until the refueling outage in April 1990.

The detailed RFW System analysis indicated that the calculated interferences, between the piping and whip restraints, did not violate any ASME Code allowable piping stress or WNP-2 loading crite'ria, Increased RPV nozzle loads were also evaluated and accepted by GE.

During the R-5 outage, all RFW pipe whip restraints were examined for interferences. No observable damage or linear indications were found from extensive NDE ( i.e. visual,.MT, and UT examinations) of the piping at critical welds and PWS structures as well as at the piping attachment to the'PV at two critical nozzles.

The thermally interfering PWS structures were removed from the system by eliminating pipe break locations by means of implementation of the newly refined RFW thermal transient load definition. Based on the NDE results and calculations completed by the Supply System and General Electric, it is concluded that no damage has resulted to either the RPV or the RFW piping. During the Spring 1990 Refueling Outage Plant Modification Record (PMR)90-061 was implemented to remove or disable selected pipe whip restraints to eliminate the pipe clearance problem.

54

e v mm is modification did not result in a change to the WNP-2 Technical Specifications or involve an Unreviewed

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Safety Question because the margin of safety was not reduced. The Technical Specifications do not address margins of safety relative to pipe break postulation. This modification reduces the possibility of a pipe break

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by signi6cantly increasing the RFW system's structural integrity and; therefore, the overall plant safety margin relative to LOCA postulation is increased.

2.6.1 16

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MRR 7 This Plant Modification Record (PMR) was implemented to assure the overload protection would not interfere with the safety function of the Containment Recirculation Fans (CRA-FN-3A, SA, SB, and SC) under accident loading with maximum or minimum voltage at the motor. This change provided a heater one size larger than described in the FSAR, for the thermal overload protection relays.

f Evalu ti n m a This modification did not result in a change to the WNP-2 Technical Specifications or involve an Unreviewed Safety Question because the margin of safety was not reduced or the possibility of a different accident or malfunction as defined in the basis for any Technical Specification was not increased.

.6.1.17

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~M N gag This change provides the utility interface (electrical, plumbing, fire protection, etc.) for the Plant Engineering Center at WNP-2 which will provide permanent housing for a large fraction of the Technical Personnel supporting Plant Operation. It also changes some of the descriptive material provided in Section 2.1.1.1 of the FSAR.

afet Evalua ion umma The safety evaluation reviewed the utility interface connections between the new Plant Engineering Center and WNP-2. All changes to Plant Design were found to be Quality Class II and the interfaces had no effect on any safety-related plant systems.

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2L D LEAD A PER m hne e following are summaries of temporary changes made in the facility by use of the Lifted Lead and Jumper (LLJ) Procedure (PPM 1.3.9). As required by 10CFR50.59, each change was evaluated and determined not to represent an Unreviewed Safety Question nor require a change to the WNP-2 Technical Specifications.

2.6.2.1 The purpose of this temporary change was to allow de-energization of Main Steam Line Radiation Monitor (MS-RIS-601B) without tripping the B Gland'eal Exhaust Fan. The change was accomplished by jumpering out the contacts of relays K70 and K73 for the gland exhaust fan trips on the Main Steam Rad Monitor Channel B.

This change did not require either a Technical Specification change or result in an Unreviewed Safety Question because the Technical Specifications do not discuss this particular trip, credit is not taken for this trip in the Accident Analysis and, if a Main Steam Line High Radiation Monitor trip signal were to be received while these jumpers were installed, the main steam isolation valves would close, isolating the reactor from the condenser. If, because of a single failure, the Main Steam Isolation Valves were to fail to close on the High Radiation signal, the Air Ejector Suction Valve from the Condenser (AR-V-1) would close, also isolating the l ndenser from the gland exhausters.

2.6.2.2 These temporary changes are associated with the Air Removal (AR) System. Division I gland seal steam exhauster AR-EX-1A was out of service for corrective maintenance with Division II exhauster in service.

Technical Specification required surveillance testing of Division II main steam line radiation monitors MS-RIS-610B and MS-RIS-610D normally requires transfer to the Division I exhauster ifthe Division II unit is on line to preclude tripping. To allow completion of surveillance testing, the trip function from the monitor under test was defeated; To allow completion of required surveillance testing, the high-high and inop trip functions from the respective monitor to the exhauster was defeated by jumper installation. The jumper was removed upon completion of the surveillance.

P The jumper installation was a temporary change to facilitate testing and the redundant Division II monitor trip functions were still operable. No credit is taken in the Technical Specifications for this trip function and failure of this system to isolate is bounded by failure of the Off-Gas system (FSAR 15.7.1), which is less limiting.

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2.6.2.3 1 n v I h n ti nd rv illan Pr c u e is temporary change allowed the High Pressure Core Spray (HPCS) Diesel Generator to be maintained in the droop mode of operation until a new isochronous/droop switch could be procured and installed. Two electrical jumpers were installed within the HPCS Diesel Generator isochronous/droop selection circuitry to place the speed governor permanently in the droop mode of operation. The failure of the switch within the HPCS DG selection circuitry required the installation of the jumpers to assure the unit had the capability to be parallelled to the offsite source for testing purposes. The switch was discovered to have intermittent contacts which, when in the droop mode of operation, could result in the diesel generator to revert to the isochronous mode of operation. This caused the unit to become unstable when paralleled to the offsite source (See LER 90-004 for additional details).

fet Evalu ti n u m Various test data for the HPCS Diesel Generator were reviewed. This test data showed that the unit design had the capability to meet all regulatory requirements when in the droop mode of operation. Acceptable diesel generator starting times and HPCS pump acceleration capabilities were demonstrated in this mode of operation.

The only result of operating in the droop mode of operation is that the steady state speed would be slightly less due to the droop characteristics when the engine was loaded, The droop was set during startup testing at 3.15% for load changes from 0 to 100%. This represented a minimum steady state frequency of 58.2 hertz.

This was well within the Technical Specification steady state frequency requirement of 57 hertz.

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.6.2.4 LU 9~

~ ~

This Temporary Change involved the Air Removal (AR) System. The Division I gland seal steam exhauster AR-EX-1A was out of service for corrective maintenance with Division II exhauster in service. Tech Spec required surveillance testing of the Division II main steam line radiation monitors MS-RIS-610B and MS-RIS-610D normally requires transfer to the Division I exhauster if the Division II unit is on line to preclude tripping. To allow completion of surveillance testing, the trip function from the monitor under test was defeated.

To allow completion of required surveillance testing, the high-high and inop trip functions from the respective monitor to the exhauster was defeated by jumper installation in accordance with approved plant procedures.

The jumper was removed upon completion of the surveillance.

afet Eval ia i n umma The jumper installation was a temporary change to facilitate testing and the redundant Division II monitor trip functions were still operable. No credit is taken in the Technical Specifications for this trip function and failure of this system to isolate is bounded by failure of Off-Gas (FSAR 15.7.1) and is less limiting.

57

'I 2.6.2.5 L - 2 is temporary change was made to assure one of the Bypass and Inoperable Status Indication (BISI) alarms associated with the Residual Heat Removal (RHR) "B" System remain operational. The RHR Heat Exchanger "B" Inboard and Outboard Vent Valves (RHR-V-73B and RHR-V-74B) had been de-energized and danger tagged for corrective maintenance. This caused the two BISI relays associated with these valves (RHR-RLY-80/V73B and RHR-RLY-80/V74B) to actuate the BISI alarm "RHR B/C MOV NETWORK PWR LOSS/OL".

This, in turn, actuated the alarm on Panel 601 "RHR B OUT OF SERVICE". With this alarm in, all other alarms associated with "RHR B OUT OF SERVICE" would be masked. This temporary change removed relays RHR-RLY-80-V73B and RHR-RLY-80-V74B which cleared the alarms described above.

af Evlu in umm The removal of these relays will enhance safety by allowing other alarm conditions associated with the annunciators to be communicated to the Plant Operators. The BISI indication is the only function of the two removed relays. The power was removed and clearance tags hung, and further warning is not required on the inoperability of these valves. The valves are shut and de-energized as they are not required to open except for venting or filling operations.

2.6.2.6 LLJ -1 2 and 1 DF 0-1 and 1 This temporary change was written to allow the Bypassed and Inoperable Status Indication (BISI) to function in a normal manner while maintenance was being performed on the Control Room Chiller units (CCH-CR-1A and CCH-CR-1B). The BISI inputs (CCH-CR-.1A PWR LOSS and CCH-CR-1B PWR LOSS) were removed to allow other alarm conditions to be communicated to Plant Operators.

fet Ev lu i n umm This change did not result in a change to the WNP-2 Technical Specifications or involve an Unreviewed Safety Question. The Chiller Units had the power removed and they were tagged out of service. This change allowed other alarms associated with Control Room Heating and Ventilating conditions to function to alert Plant Operators to system problems.

2.6.2.7 LLJ -142 14 1 187 1 18 197 20 2 2 I 2 2 7 27 During the annual refueling outage a number of temporary changes are required to support electrical power requirements. This need occurs when a piece of electrical equipment is taken out of service for maintenance during the outage and power needs to be supplied to the loads normally fed by this equipment from another source. The electrical Lifted Leads and Jumpers listed above were written to implement this type of temporary change during the 1990 Refueling Outage.

58

0 fe Ev o u ch of the above temporary changes were evaluated to assure they did not result in a change to the WNP-2 Technical Specifications or involve an Unreviewed Safety Question. The evaluation made sure (1) the margin of safety in the Technical Specifications was not reduced, and (2) the boundary conditions of the FSAR evaluations were not changed. Specific factors considered included fusing in the involved circuits, cable size, divisional separation between circuits, and the status of the plant during the time the temporary change would be in effect.

2.6.2.8

~L~14 This temporary change involved the deactivation of the Residual Heat Removal (RHR) Suppression Pool Cooling Test Return Valve (RHR-V-21) which was de-energized due to a positioning problem. With RHR-V-21 de-energized, the RHR "B" Bypass and Inoperable Status Indication (BISI) alarm was continuously energized which prevented other inputs to the BISI from warning the Plant Operators of an abnormal condition. This temporary change removed the BISI relay RHR-RLY-80/V21 from its socket and cleared the BISI alarm while maintenance was performed on RHR-V-21.

afet Eval ai n mm The relay removed provides indication only, The RHR-V-21 valve which feeds this relay is de-energized in the closed position. Thus, the RHR system was otherwise fully operational and no Technical Specification requirements were affected.

2.6.2.9

~LLJ -1 1 This temporary change was made to supply temporary seal cooling water to Air Removal Pump Number 1 (AR-P-1). Water from the Demineralized Water (DW) system was supplied by means of hose connections to maintain seal cooling to AR-P-1. The normal cooling source is from the Turbine Service Water (TSW) System.

fet Evaluati n S mrna This change did not result in a change to WNP-2 Technical Specifications or an involve Unresolved Safety Question since those portions of the Demineralized Water and TSW systems do not affect equipment important to safety and neither system is Technical Specification related.

59

0 2.6.2.10 LJ -1 2 24 24 247 24 These temporary changes were made during a maintenance activity to change out selected safety related HFA relays during the"'annual R5 refueling outage. The activity is a result of an- on going maintenance 'program aimed at periodic inspection and maintenance of all Plant-installed, GE-type HFA relays. To implement this change a jumper is used to maintain the continuity of the relay system AC neutral while changing selected relays.

Due to the design of the relay logic AC power distribution system, several relays have AC neutrals that are in parallel with each other. The maintenance activity targeted several relays on the same neutral run. Several other relays that use the same neutral were not involved with the activity. This "Daisy Chain" of neutrals would affect non-targeted relays when targeted relays were determed and removed from the plant. Installation of the jumper allowed the non-targeted relays to remain energized by jumpering the neutral around the targeted relays.

fe Ev l ati n umma This jumper installation did not result in a change to Plant Technical Specifications or present an Unreviewed Safety Question because the jumper was a temporary installation to keep plant systems in their normal lineup during the on-going maintenance activity. The jumper maintained the system logic in a lineup consistent with the description of the system in the FSAR and allowed the down-stream logic to perform in a manner consistent with Plant Technical Specifications. Those relays that were changed out as a result of the maintenance activity were declared inoperable during the maintenance activity and were not returned to service until after the jumper as removed and operability testing was completed.

2.6.2.11 L~LT -214 This temporary change was performed during the refueling outage to allow the Source Range Monitor (SRM) and Intermediate Range Monitor ARM) Surveillance to be performed to verify operation of the "RODOUT BLOCK" Annunciator. An electrical jumper was used to bypass the "B" Channel of the Refuel-Bridge-Over-Core Interlock to clear the "RODOUT BLOCK" caused by a malfunctioning limit switch in the Refuel Platform.

af Eva i n umm This change did not result in a change to the WNP-2 Technical Specifications or involve an Unreviewed Safety Question. The "A" Channel remained operable during this operation. The Refuel Bridge was not over the core and it was tagged out of service to prohibit movement over the core.

60

2.6,2.12 2 1 During routine maintenance activity associated with 4160 volt breaker 8-85/1, two of the three installed degraded voltage relays were damaged. They were installed on the door of a cubicle and were impacted by the circuit breaker during removal. One relay was available in spares, and was installed to replace one of the two relays. Additional spare relays were placed on order. A temporary change was made to place the channels for the inoperable relay in the trip condition.

afe vluti n mm This evaluation found that this configuration did not constitute an Unreviewed Safety Question because the degraded grid condition continued to be monitored by the remaining relays. The net effect was a logic change from two-out-of-three to one-out-of-two. This jumper was installed in accordance with the direction provided in an action statement within the Plant Technical Specifications.

2.6.2.13 LL~g-2'g During a power outage on 480 Volt Switchgear Unit 11 (SL-11) temporary power was needed for the Clearwell Transfer Pump (FW-P-3A). This pump receives its power from Motor Control Center 1C (E-MC-1C) which is fed by SL-11. An electrical jumper was provided to supply power to cubicle 4D of MC-1C from Motor ontrol Center 5A (E-MC-SA).

afet Ev lu i n umma This change did not result in a change to the WNP-2 Technical Specifications or involve an Unreviewed Safety Question. Installing this temporary power source allowed this source of water to remain operable. All circuits involved in this temporary change are non-safety related and the wire installed was sized for the load.

2,6.2.14 LLJ -2 and -2 1 This temporary change was made using electrical jumpers to the Plant during the refueling outage. A.Local Leak Rate Test (LLRT) required the opening of the High Pressure Core Spray (HPCS) Injection Valve (HPCS-V-4) with a High Reactor Water Level (Level 8) condition. The high water level condition would normally require HPCS-V-4 closure.

afe Ev I ti n mrna At this point during the outage the HPCS Pump (HPCS-P-1) fuses were pulled to prevent the pump from

~ In addition, the manual isolation valve between HPCS-V-4 and the vessel (HPCS-V-51) was closed. 'unning.

Thus, the movement of HPCS-V-4 to perform the LLRT could not accidentally inject water in the vessel or drain water from the vessel. Therefore, this activity did not result in a change to the WNP-2 Technical

~

Specifications or involve an Unreviewed Safety Question.

61

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ih ~~<<" ~<'A<<g,~~ ' ' ' i '

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<<"'.6.2.15 2

The purpose of this temporary change was to allow running the Reactor Recirculation pump on 15 Hz while the Reactor Protective System (RPS) was de-energized for work during the refueling outage. The change was accomplished by installing jumpers in the RRC pump trip circuit.

This change did not require either a Technical Specification change or result in an Unreviewed Safety Question because the pump trip due to valve isolation signal is only required, by the Technical Specifications, to be operational in Modes 1, 2 or 3. These jumpers were only installed during Mode 5.

2.6.2.16 LLL9~2 This temporary change removed selected fuses to prevent the Reactor Recirculation pump from tripping on an ATWS signal when the Reactor Protective System (RPS) was de-energized for work during the refueling outage. The change was accomplished by removing fuses F-8 in the ATWS trip circuit of RRC pump B.

's change did not require either a Technical Specification change or result in an Unreviewed Safety Question

~ ~ ~ ~ ~

because the ATWS-RPT is only required to be operable in Mode l. The Reactor was in Mode 5 for the entire

~

~

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time the fuses were removed.

2.6.2.17 LLL99&2 <<

This change was a temporary jumper to provide level indication at the remote shutdown panel while a qualified splice was installed.

f v i n The reactor was in a analyzed condition, shutdown, depressurized and flooded. The temporary jumper did not increase the probability of previously-evaluated accidents nor increase their consequences. The temporary jumper did not remove the reactor from its analyzed condition and; therefore, did not create the possibility of an accident of a different type than had been previously evaluated, nor does the jumper reduce any Technical Specification margin of safety.

62

2.6.2.18 LJ 274 Temporary changes90-274 and 90-368 were installed in the plant to provide power to the "Hydrobroom" u'sed on the 606 foot level of the Reactor Building. The "Hydrobroom" is used to decontaminate the reactor cavity during the refueling outage.

'I ~'

v Temporary power was provided from Motor Control Center 7C-B (MC-7C-B) Cubicle 5E. This Motor Control Center is not safety-related and the change did not increase the probability of occurrence of an accident or malfunction of equipment important to safety. The cable, fusing and MC-7C-B were all sufficient to power the "Hydrobroom" at the required 87 amperes of 480 volt AC power.

2.6.2.19 L -2 The changes were temporary jumpers in local racks at WNP-2. The jumpers were inserted to preclude RPS Channel A trips from RPV level (MS-LIS-24A Ec MS-LIS-24C) and Drywell pressure (C72-N002C) while installing qualified splices in the rack. An isolation of MSL drain valves from a trip of C72-N002C or B22-N061C was also prevented.

I afet Evaluati n mm The reactor was shutdown, depressurized and flooded. Temporarily removing one channel of RPV level input from RPS did not alter the capability of scramming. Removing one channel of drywell pressure from RPS did not increase the probability of an accident since the drywell was open, nor were the consequences of any previously evaluated accident increased. Installing the jumpers did not create the possibility of an accident of a different type than has been previously evaluated.

2.6.2.20 LLJ ~)~2+

The purpose of this change was to add a source of demineralized water to the Control Rod Drive (CRD) system during the CRD system outage such that the Hydraulic Control Units (HCUs) would not become air bound.

During the outage of the CRD pumps and a portion of the system, a mechanical jumper was added to the system such that Demineralized Water (DW) at normal DW water pressures could be supplied to the CRD HCUs by means of the CRD system charging water line. This kept them full and prevented air binding of the accumulators.

Safet Evaluati n umma No change to the Technical Specifications was required because the system was removed from service. The ddition of the jumper did not cause operability problems to a system already declared inoperable. The action statement of Technical Specification 3.1.3.5.B had been completed.

63

6.2.21 Allof the temporary changes listed above were as a result of the Instrumentation Wire Splice Inspection Work.

The wire splices were repaired during R5 outage and involved Instrument'Racks on the 522 foot level of the Reactor Building. The instruments involved with the splices are connected to the Reactor Protection System (RPS). The method chosen to accomplish the repair was to install a temporary jumper while the instrument was out of service. The jumper was installed to replace the switch or relay contacts in the instrument associated with the SCRAM logic while the splice work was being accomplished. The jumper was removed when the splice work was completed. This was done to avoid an unplanned challenge to the SCRAM logic.

/

These changes did not result in a change to the WNP-2 Technical Specifications or involve an Unreviewed Safety Question. All of the instruments jumpered were monitoring plant parameters that were invalid while the plant is in an outage condition. The signals included signals such as high vessel pressure, which cannot occur while the vessel head is off. Therefore, none of these affected any of the USQ evaluation criteria.

2.6.2.22 LLL9&398 7

7 During the Spring 1989 refueling outage (R-4) the fiex hose (CIA-FLX-1C) which supplies air to the actuator for Main Steam Relief Valve (MS-RV-2D) was found damaged and was removed from service until a new one could be installed. It was intended to replace the flex hose in the Spring 1990 outage (R-5); however, due to procurement problems, the new flex hose was not available for installation prior to the originally scheduled startup from R-5. Since MS-RV-2D was still capable of opening in the safety mode (relief mode was declared out of service), it was necessary to be able to open MS-RV-2D manually at approximately 10% reactor power to perform the RSV Acoustic Monitor test and calibration as required by Technical Specifications. With CIA-FLX-1C removed, the required surveillance of the Acoustic monitor was not possible; and, therefore, LLJ 90-308 was installed to provide a temporary air supply from RHR-AO-41A to MS-RV-2D to be used to open the SRV manually while the reactor was at 10% power. Air Operator RHR-AO-41A had been previously deactivated and, therefore, its air supply was available for use to temporarily operate MS-RV-2D.

The change disconnected the air supply to RHR-AO-41A. This air supply was then connected to a temporary pipe routed from the vicinity of RHR-AO-41A to MS-RV-2D where it was temporarily connected to MS-AO-2D. The CAS Supply to RHR-AO-41A is isolatable by two locked-closed valves outside containment, so that at all times other than the Acoustic Monitor surveillance testing, the air supply to RHR-AO-41A and temporarily MS-RV-2D is isolated to maintain containment integrity.

The delay in startup from R-5, caused by the rebuilding of an emergency generator, allowed additional time .

for procurement of the new fiex hose, which was subsequently installed. The temporary air line from RHR-0-41A to MS-RV-2D was removed and LLJ 90-308 and its associated procedure changes, PDF 90-576 and DF 90-647, were canceled in July, 1990.

fe Evlu 'n u ma

~

e change did not require a Technical Specification change and did not resuJ.t in an Unreviewed Safety

~

Question because the jumper was for temporary actuation of MS-RV-2D only to meet Technical Specification

~ ~

~

requirements for the associated Acoustic Monitor; the jumper was isolatable from outside containment by two

~ ~

locked-closed valves to maintain containment integrity and prevent introduction of air into the containment during normal operation, 'the jumper was supported at suitable intervals to ensure it remains in place during if a seismic event; a missile'analysis was performed to ensure that the temporary air line did fall it could not damage any component in its zone of influence; there were no affects that the jumper could produce that would increase the probability or consequences of an accident; there are no new events that the jumper could cause; and use of the jumper would maintain the margin of safety by enabling the calibration of the MS-RV-2D Acoustic Monitor.

2.6.2.23 LLLK2>>

Required relief valve testing on the "B" RHR loop requires the loop to be drained. The draining of the loop causes the loss of the "B" loop for potential use as an alternate shutdown cooling path. This. temporary change provided blank flanges to replace relief valves while the relief valves were being tested.

afet Evaluation mrna I

To allow the "B" loop to be available while the relief valves were being tested, ASME blank flanges were staged and ready to be installed under the guidance of an ASME Section XI plan and a Maintenance Work Request (MWR). In the event that the loop was required, the flanges would have been installed and the loop filled and put into service. These valves provide thermal over pressure protection. At full RHR pump shutoff head, these valves are not required for pressure protection. In the event the loop was filled, manual venting and monitoring of system pressure and temperature would provide adequate protection. This was applicable only in Modes 4 and 5. Therefore, this activity did not result in a change to WNP-2 Technical Specifications or involve an Unreviewed Safety Question.

2.6.2.24 LLJI~~44 This temporary change provided for opening Reactor Outside Air Damper 3B (ROA-AD-3B) for purging the dry well. The change was made to install a nitrogen bottle to ROA-AD-3B to provide opening air pressure.

Safet Ev I a i n mrna This change did not result in a change to the WNP-2 Technical Specifications or involve an Unresolved Safety Question because (1) containment isolation capability was provided by Containment Supply Purge Valves 1,2,3, and 4 ( CSP-V-1,2,3,and 4), (2) failure of the nitrogen supply would have resulted in the damper failing in the closed position, and (3) ROA-AD-3B is not listed in the Technical Specifications as a containment isolation valve.

65

2.6.2.25 LJ -4 4

~RR2 - 7 This temporary change corrected a problem with the HPCS 125 volt battery, Weekly battery surveillance discovered that all electrolyte had leaked from cell ¹9.

A JCO was prepared which concluded that the HPCS battery would be capable of meeting the design requirements with one cell removed, i. e., a 57-cell battery. The evaluation included a review of the most recent battery performance test and the design requirements. The immediate disposition of this item was to jumper cell '¹9 until a replacement cell could be prepared for installation.

af Evl m The use of the HPCS battery with 57 cells did not result in a change to the WNP-2 Technical Specifications and the Unreviewed Safety Question evaluation concluded (1) the HPCS battery was capable of performing its design function, (2) the margin of safety provided in the Technical Specifications was not changed, and (3) the boundary conditions for the FSAR evaluations were not changed.

2.6.2.26 LU -4 -4 - 2 - 27 - 6 and hese temporary changes were associated with a low voltage condition detected by surveillance testing on cells 39 and 40 of battery E-B1-1. The safety function of Battery E-Bl-1 is to provide 125 Volt DC power to the Division 1 safety-related loads including critical switchgear control power and various other control functions.

Battery E-Bl-1 is comprised of 58, type GN-13, cells and is manufactured by Exide Corporation. Each cell is required to produce 2.13 volts of DC power. The temporary changes involved electrical connections to remove the two cells from service, charge the cells, and place the cells back into service.

afe Ev I ati n umma Cells.39 and 40 could only be removed from service if E-Bl-1 remained capable of providing the voltage and current required by its connected loads during malfunctions and accident conditions. The latest surveillance test data was evaluated and analysis was performed which showed the battery would be capable of producing the required 105 Volts at ".End-of-Discharge Voltage" conditions with the two cells removed. During cell charging, the safety evaluation provided assurahce that the battery would remain functional under all conditions, including seismic events. Finally, during re-connection of the cells an evaluation was performed to ensure that the charger was capable of supplying the load for a short period of time when the battery was taken out of service.

66

0 2.6.2.27 LJ 0-24 n 4 The valve position signal was temporarily removed from the RCIC-V-8 NOT FULLY OPEN SIGNAL so the DIV 1 OUT OF SERVICE annunciator could be activated by another Bypass and Inoperable Status (BISI) alarm until the valve limit switch could be adjusted. The wire was lifted in the control room that removed the valve position signal. The BISI was still available for a remote manual closure of RCIC-V-8, and the position indication lights in the control room were still available.

afet Evalu ti n umma This did not result in a change to the WNP-2 Technical Specifications and the Unreviewed Safety Question concluded (1) the operation of RCIC-V-8 was not affected, (2) the valve position can be monitored by the position indication lights, (3) the RCIC DIV 1 OUT OF SERVICE ANNUNCIATOR would be available to monitor the other 13 parameters instead of being in an alarming condition, (4) the margin of safety provided in the Technical Specifications was not changed, and (5) the boundary conditions for the FSAR evaluation were not changed.

2.6.2.28 L~~0- S HPCS-V-23 was declared inoperable due to its failure to fully close during surveillance testing. HPCS-V-23 as subsequently manually closed using the handwheel and de-energized at the MCC by opening its control

~

power breaker. The BISI (Bypass and Inoperable Status Indication) annunciator circuit logic associated with

~

HPCS MOV power network is configured such that, ifany HPCS MOV power is lost (as is the case when the MOV power circuit breaker is opened), an alarm occurs. With any HPCS system BISI annunciator illuminated, the "HPCS System Out-Of-Service" annunciator will also illuminate. These two illuminated annunciators, understood by Control Room Operators as being associated with the HPCS-V-23 being de-energized, would mask any other MOV power loss elsewhere in the HPCS system; a condition which could place the HPCS system in a inoperable condition.

afet Ev lua i n umma A Jumper/Lifted Lead request was approved which removed HPCS-RLY-80/V23 from the BISI circuit, extinguishing the "MOV Network Power Loss" and "HPCS System Inoperable" ahnunciators even though the HPCS-V-23 power circuit breaker was open. This allowed the BISI circuit to continue to monitor all other MOVs and inoperable status inputs and respond accordingly by annunciation. Removal of this relay from the BISI circuit did not result in a change to the WNP-2 Technical Specifications or involve an Unreviewed Safety Question because (1) HPCS-V-23 is an HPCS pump test return line isolation valve required to be closed in order for the HPCS system to perform its safety function, (2) HPCS-V-23 was manually closed and de-energized and as such did not require BISI monitoring for loss of power, and (3) removal of HPCS-RLY-80/V23 allowed the BISI circuit to function as designed with the HPCS-V-23 control power circuit breaker open, Therefore, the margin of safety provided in the Technical Specifications was not changed, and the boundary conditions for the FSAR evaluations were not changed.

67

2.6.2.29 One of two New Fuel Vault criticality monitors failed and was spuriously alarming. The instrument was deactivated by disconnecting the appropriate amphenol connectors.

f v u n m The Technical Specifications require operable criticality monitors only when fuel exists in the New Fuel Vault.

There is no fuel in the vault, with no plan to utilize the vault in the near future. Therefore, this activity did not result in a change to WNP-2 Technical Specifications or involve an Unreviewed Safety Question.

2.6.2.30 LLJ ~gg The purpose of this temporary change was to allow operation of the refueling bridge while the over-the-core position switches were malfunctioning. The change was accomplished by installing jumpers on the refueling bridge bypassing the bridge over-the-core position switches.

afe Evalu ti n mrna

~

This change did not require either a Technical Specification change or result in an Unreviewed Safety Question l

ecause the over-the-core interlock is designed to prevent withdrawing or installing fuel into the core when a control rod was withdrawn by preventing bridge movement over the core. Moving fuel in the core can only

~

be physically accomplished in Mode 5. The jumpers were only installed in Mode 1.

2.6.2.31 LLLIi~2 A temporary jumper was installed to allow the installation of a temporary control air dryer to take the place of the nonfunctional permanent dryer. The CAS dryer outlet filters had failed due to overheating. The dryer was taken out of service until the dryer was repaired, Since the cause of the high temperature could not be immediately determined, a new heatless-drying tower was purchased. This temporary tower was connected with hoses to the pre-filters and after-filters.

fe Ev l ti n mm The use of the temporary dryer did not result in a change to the WNP-2 Technical Specifications and the Unreviewed Safety Question concluded (1) the performance of the Control Air System met all requirements, (2) the margin of safety provided in the Technical SpecificatIons was not changed, and (3) the boundary conditions for the FSAR evaluations were not changed.

2.6.2.32 4

The purpose of this temporary change was to defeat a rod block caused by a defective refueling bridge over-the-core interlock switches. The change was accomplished by installing jumpers in the refueling bridge rod block circuit bypassing the bridge over-the-core position switches.

f Ev mm This change did not require either a Technical Specification change or result in an Unreviewed Safety Question because the over-the-core interlock is designed to prevent withdrawing or inserting a control rod when the bridge is over the core (potentially installing fuel into or removing fuel from the core). Fuel can only moved in the core in Mode 5. The jumpers were only installed in Modes 1 and 2.

2.6.2.33 LL~g PER 2 - 72 P ER 290-0972 was written when a cross-connect was found between the Sanitary Drain (SD) and Reactor Exhaust Systems (REA). This resulted in an unanalyzed bypass of Secondary Containment as reported in LER 90-032.

A Jumper and Lifted Lead (LLJ 90-651) was issued to install a plug in the sanitary drain system at the 439" elevation in the reactor building to prevent a possible unmonitored release of liquid radioactive material after an accident. A PMR was written to permanently eliminate the REA and SD system cross-connect.

fet Evalu i n mm This modification to add the temporary plug in the Sanitary Drain System did not result in a change to the WNP-2 Technical Specifications or involve an Unresolved Safety Question because the margin of safety was not reduced and the possibility of a different malfunction as defined in the basis for any Technical Specification was not increased. Secondary Containment integrity has always been maintained and test results have been acceptable. During a Post-Accident Condition the Reactor Building is maintained at a negative pressure.

69

2. F AR EVAL ATI N eneral changes to the'SAR evaluated within the definition of 10CFR50.59 are reported in this section.

2.6.3.1 MIN R Y E REL AD H N The purpose of this change was to accurately describe the reactor core as loaded for Cycle 6. Certain minor changes were required since the Cycle Submittal in the spring.

The changes required and reasons for each are as follows:

A. Two lead fuel assemblies, XN-1163 and XN-1164, contained two segmented rods in each assembly which were not growing as rapidly as the other rods in the assembly. If left in the assembly, these rods had a potential to become loose in the upper tieplate due to improper seating of the endcap in the tieplate. We had planned to replace these rods with inert rods, but the NRC would not accept the vendor's approach to the replacement analysis. However, the NRC would accept the replacement of the segmented rods with natural uranium rods. This replacement was performed during the refueling outage.

B. During the disassembly and reassembly of fuel bundle XN-1163 during the refueling outage, a single finger spring tab became bent over during the underwater channeling process. The only possible repair was to break the tab free of the assembly. Accounting for the bundle's core loading position, Advanced Nuclear Fuels (ANF) performed an analysis which demonstrated that the small increase in bypass leakage through the modified finger spring would not have significant impact on the bundle's thermal hydraulic performance.

During the fuel sipping effort performed in the outage, it was determined that bundle XN-1114 had a fuel pin leak. A data search revealed that XN-1029, a bundle planned for discharge, possessed very nearly the same nuclear characteristics as XN-1114. ANF preformed an analysis which showed that the substitution of XN-1029 for XN-1114 in the core loading scheme would have no significant steady state or transient impact on the core.

afet Eval ati n umma No change to the Technical Specifications was required and no Unreviewed Safety Question resulted from these changes because the analyses, in all cases, demonstrated that core transient and steady state limits would not be significantly affected.

70

2.6.3.2 This Safety Analysis Report (SAR) Change Notice (SCN) revised the Emergency Preparedness Plan for WNP-

2. Numerous updates were made to the Plan to accurately describe the current methods of handling emergencies at WNP-2. This included an update of the titles of State Agencies, removal of the requirement for an Interplant Operations Communications Channel between WNP-1 and WNP-2 since WNP-1 is not operational, movement of the First Aid Facility.to a different location, a clarification of methods used for Dose Projection, and numerous other minor changes.

afe Ev I ma The Safety Evaluation concluded that the changes made enhanced the ability of WNP-2 to respond to emergencies. This change did not result in a change to the WNP-2 Technical Specifications or involve an Unreviewed Safety Question.

2.6.3.3 KHKQ This SCN revised the FSAR by removing the requirement to perform Local Leak Rate Testing (LLRT) on test, vent and drain connection valves which are located within the Primary Containment boundary.

is change to the FSAR eliminated local leak rate testing on approximately 173 test, vent, or drain valves, all being 3/4" diameter globe valves which are normally closed and capped during power operations. This change was made to reduce outage LLRT efforts and decrease personnel exposure, fet Ev luati n umma This change did not result in a change to the WNP-2 Technical Specifications in that these valves were not included in the applicable Technical Specification section which lists the main line containment isolation valves requiring LLRT. This change did not involve an Unreviewed Safety Question because the consequences of an accident was not increased, nor was the margin of safety defined in the basis for any Technical Specification reduced. These test, vent, and drain connection valves are normally closed and capped during power operations and are verified closed every 31 days as required by plant Technical Specifications. The consequences of a accident are not increased by this change in that these valves are tested for leakage as part of the overall Type A Integrated Leak Rate Test and; therefore, do not represent an untested containment isolation boundary.

2.6.3.4 KNUB'his item changed the WNP-2 Physical Security Plan by deleting the requirement that all Supply System employees have a physical examination in order to obtain unescorted access to the Plant.

71

fe Ev lu ti n umm is change did not result in a change to the WNP-2 Technical Specifications or involve an Unreviewed Safety Question. No reasonable relationship existed between .the need for a physical examination and unescorted access for non-security personnel.

2.6.3.5 KKSh993 This change to the WNP-2 Physical Security Plan deletes the requirement for a separate vital area for the Remote Shutdown Room and allows the securing of Alternate Access (AAP) Point badges and keycards in the Access Control Station when the AAP is not manned.

af Evl mm The Remote Shutdown Room does not need to be controlled as a separate vital area since it is located in a larger vital island. Securing badges and key cards in the AAP Access Control Station when the AAP is unattended enhances the security of badges and keycards located there.

2.6.3.6

~ ~ ~

SG> %824 is SCN revised the content of SAR Chapter 13, Conduct of Operations, It modified this chapter to reflect the current organization and made several other updates to reflect the current Supply System conduct of operations.

afet Evaluation umma Changes were reviewed to assure there was no change to the Technical Specifications and that they did not involve an Unreviewed Safety Question. The independence of the Quality Assurance-related organizations to, perform their duties was maintained in the reorganization.

2.6.3.7

~N~) - 8 The Off-Site Dose Calculation Manual (ODCM) was modified to update details of the Radiological Environmental Monitoring Program described in Section 5.0. Tables were updated to reflect the current sampling locations used to support WNP-2 Operations.

afet Evalua ion umma The change provided updated maps and tabular data on sample locations. The consequences of an accident are not changed as a result of this update. In addition, the margin of safety as defined in the bases of the Technical

~

pecifications is not reduced. ~

72

2 4 PR LEM EVAL ATI N e Plant Problems-Plant Problem Reports Procedure (PPM 1.3.15) provides instructions for the disposition and documentation of plant problems. An immediate disposition using the "Use-As-Is" or "Repair" options is considered a "change" within the definition of 10CFR50.59. Each item below has been evaluated to provide assurance that the disposition did not involve a change to the Technical Specifications or involve an Unreviewed Safety Question.

2.6.4.1

~PR '9J)~7 This Problem Evaluation Report documented an error found in the meteorology calculations in Amendment 36 of the FSAR. The data was found to be non-conservative by approximately a factor of 10. Specifically, the values for the source term dispersion pattern relative concentration factor, X/Q, were specified incorrectly.

afet v lu io mm A previous Justification for Continued Operation (JCO), Nonconformance Report 288-0357, was revised to address this issue and the offsite consequences were found to be acceptable. The previous JCO reviewed the issue of Secondary Containment draw-down time following a postulated Design Basis Accident (DBA) condition. During this review the incorrect X/Q values were discovered. Further review showed these erroneous X/Q values were not used in support of the Chapter 15 accident analysis. Corrected meteorological data was ubmitted in an August 1990 FSAR amendment. The Chapter 15 analysis will be revised by October 1991 to address the changed X/Q values.

9

~2-2.6.4.2 92 Diving inspections of two Service Water (SW) System pipe supports revealed accelerated corrosion degradation on approximately one-third of the hex-nuts applied to the baseplate concrete anchor studs. The baseplates are submerged within the 1B service water spray pond and are associated with hanger mark numbers SW-936N and SW-937N, The concrete anchor studs as well as the coated support steel did not show any appreciable corrosion degradation.

Under water repair actions were successfully completed with hex-nut materials selected for optimum corrosion performance when combined with newly installed (enhanced) cathodic protection elements. Torquing requirements at all concrete anchor bolt locations were satisfied and it was concluded that both SW-936N and SW-937N were restored to their original design integrity.

fet Eval a ion umma In the interim, prior to the repair effort, a full deadweight and seismic analysis of the service water piping was completed assuming that the corrosion affected baseplates were out of service (i.e., they retained zero load

~ ~

carrying capability). These analyses demonstrated that, in spite of the conservatively assumed degraded piping

~

upport condition, ASME Code piping stress limits were still satisfied. In addition, the system was stable under

~

the slightly-increased seismic deflections. These results constituted the basis of a Justification for Continued

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73

0

~

Operation (JCO) and the conclusion that an Unreviewed Safety Question did not exist since 1) no service water

~

~ ~ ~

perational function was impaired, 2) design basis pressure boundary stress limits were not exceeded under

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~ ~ ~

orst case assumptions of baseplate integrity, and 3) no Technical Specification margin of safety was reduced.

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Finally, it should be noted that, following discovery of the situation, repairs to the supports were completed

~

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in a timely manner (approximately a three week period) by a contract diving team. The probability of a major seismic event occurring in this brief window is remote. The plant was also in a shutdown condition during the course of the repair efforts.

2.6.4.3

~R2 A Justification for Continued Operation (JCO) was written to support the condition of the emergency Control Room Chillers. One division was operable and one division was inoperable for maintenance and replacement of parts. The redundant unit was unavailable to provide Emergency Control Room Cooling in the emergency condition. The emergency Control Room Chiller design basis is to provide additional cooling capacity for personnel comfort such that the temperature is less than 85'F in the Control Room. The Standby Service Water system alone can provide sufficient cooling for equipment operability with Control Room temperatures below 104'F.

Plant Procedures were deviated to incorporate instructions to reduce Control Room lighting to limit heat generation at the operators'iscretion when the temperature is between 85'nd 104'F Post-accident.

There is no Technical Specification which addresses the availability'of the Emergency Control Room Chillers.

The evaluation demonstrated that the unavailability of'one Emergency Control Room Chiller does not present a hazard to public safety, or to the safety of the Plant personnel.

The unavailability of one Emergency Control Room Chiller did not result in a change to the WNP-2 Technical Specifications, and the Unreviewed Safety Question evaluation concluded: The probability or consequences of

'a new accident is not increased, no new accident or malfunction could be introduced, and the margin of safety for control room personnel performance is not affected.

2.6.4.4 PEl~ ~77 During the annual refueling outage, the breaker (E-CB-73/7A) between the Low Voltage Critical Switchgear (E-SL-73) and Motor Control Center 7A (E-MC-7A) tripped causing a loss of power to several loads including Reactor Protection System (RPS) Bus A. Loss of power to RPS Bus A caused a half-scram in RPS Division A and multiple primary containment isolations, which are Engineered Safety Feature (ESF) actuations (See LER 90-013 for further details).

The root cause evaluation required a test of the breaker and no Quality Class I spare breakers were available as a replacement. The decision was made to install a Quality Class II breaker in the circuit while the problem reaker (E-CB-73/7A)'as tested.

74

f Evl i n mm e Safety Evaluation directed that all loads fed by breaker 7-73 be considered inoperable during the presence of the Quality Class II breaker. A complete divisional outage is allowed with the plant in Modes 4 or 5, which

~ ~

~

was the case during the installation of the temporary breaker. Therefore; this activity did not result in a change:

to the WNP-2 Technical Specifications or involve an Unreviewed Safety Question.

2.6.4.5

~2 An AC voltage drop test on the field windings for division II Diesel Generator (DG-GEN-DG2) was performed in June 1990. This test revealed that the windings for pole no. 6 had shorted turns.

DG-GEN-DG2 has eight field poles on the rotor which provide field flux required to generate voltage in'he stator of the generator. An AC voltage drop test was performed by applying 120vac across two opposite poles in series. Then the voltage across each pole was measured. For good windings, the voltage drop across each pole should be equal (60v each). When 120v ac was applied across pole no. 2 and pole no. 6 in series, the voltage drop across these poles was measured to be 84v and 36v respectively. This indicated that some of the winding turns on pole no. 6 were shorted.

S fe Ev 1 i n umma Safety Evaluation was performed to justify continued operation with the above condition on DG-GEN-DG2.

The evaluation showed that shorted turns could h'ave the following effects on the generator performance:

Reduce the magnetic flux produced by the pole and; hence, reduce the generator output voltage for a given field current.

Increase heating within the pole winding and degrade it with time.

iii) Unbalance the magnetic field across the air gap, causing vibration.

Following the discovery of the shorted turns, the unit was run at 100% for 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />. During this test the field current at full load was 142 amps which is less than the rated current of 168 amps for the voltage regulator.

The AC voltage drop test was repeated after the run and there was no change in the test results. Also, the surveillances were reviewed and no excessive vibration was noted.

A new procedure was implemented to periodically perform the AC voltage drop test. The latest test was performed on January 28, 1991. Results of these tests did not show any noticeable degradation of pole windings.

From the tests performed to-date, it is clear that the unit is capable to perform its safety function (i.e., to supply the Division II loads on loss of offsite power).

The review of tests performed on the unit concluded that (1) the performance of the unit met all requirements, (2) the margin of safety provided in the Technical Specifications was not changed, and (3) the boundary conditions for the FSAR evaluations were not changed.

75

2.6.4.6

~ ~

PER~ii~2 This Problem Evaluation Report address the problem of high failure rate on Rosemont 1153 Series B and D

~

pressure Transmitters due to loss of fill-oil. NRC Notice 90-01 required a documented basis for continued operation for transmitters of this type. Ten of these devices are installed in the plant.

fe Ev n u m The earliest symptom a model 1153 Series B or D transmitter will exhibit prior to failure is that, ifit is leaking fill-oil,a sustained drift will be observed. The calibration data for the installed transmitters were reviewed and found to show no drift trends indicative of a fill-oil loss failure. Drift data was found to be within the Rosemount limits for response time degradation. The. existing surveillance monitoring will be continued, with transmitter calibration data analyzed for sustained drift. This resolution is considered a short term solution until the transmitters are replaced.

2.6.4.7

~2II-PPM4 2 E PFlw h This Problem Evaluation Report described a problem with the circuit breaker (CB-RPT-3A and 3B) and switch design associated with the Reactor Recirculation (RRC) Pumps. Breakers CB-RPT-3A and 3B were found to

~

not have a seal-in function that seals in the trip circuit after a trip signal is received. If the ATWS signal t ~

clears, reclosing the tripping circuit before RRC.pump speed decays below the low speed pickup point, the pump would re-energize and continue to run at low speed.

Changes were implemented in appropriate procedures to prevent the possibility of the inadvertent restart, at 15 Hz operation, of the RRC pumps after a pump trip from 60 Hz operation is initiated by the ATWS RPT signal. This was done by using the "pull to lock" function in the CB-RPT-3A and 3B switches, which prevents-the energization of the 15 Hz power circuit even if all permissives are in the enable condition.

Safet Ev luati n umma The Safety Evaluation showed that neither a Technical Specification change was required nor did an Unreviewed Safety Question exist in the application of the Emergency Operating Procedure (EOP) to the WNP-2 ATWS analyses. The study showed that the re-energization event resulted in only a comparatively small quantity of energy being generated; that is, even if the RRC pumps experience a restart after the ATWS signal clears, the effects of the energy produced are bounded by the results of the full power analysis conducted as a part of the same program. The "pull to lock" function is, therefore, a redundant action that enhances the mitigating responses to the ATWS transient. Moreover, the "pull to lock" function does not adversely impact other transients or functions of the RRC Low Frequency Motor Generator (LFMG) mode.

76

2.6.4.8 The Problem Evaluation Report was written because the'atigue analysis for the Reactor Core Isolation Cooling

.(RCIC) head spray piping and associated RPV nozzle did not reflect actual plant practice. Actual use of RCIC is more frequent than was accounted for in the original analyses. Also, RCIC use occurs during "shutdowns" and "other scram" situations during which RCIC use was not originally anticipated.

There was no change to the physical plant. A Justification For Continued Operation (JCO) was prepared and approved. The WNP-2 specifications and related calculations were revised to reflect actual plant use.

Reanalysis by GE of the RCIC Head Spray nozzle is required and engineering services for this effort are being procured.

The additional use of RCIC was reviewed and it was determined that sufficient margin exists in the RCIC head spray piping and the reactor vessel nozzle designs to accommodate current WNP-2 operating practices.

The number of system operational cycles are considered in the ASME code-required fatigue analysis of pressure boundary analysis for the RCIC head spray. The first analysis is the Architect/Engineer's two'ifferent analysis of the Head Spray piping. The other analysis is the GE evaluation of the RPV RCIC Head Spray nozzle.

This Problem Evaluation Request described a potentially-nonconservative Primary Containment Instrumentation Piping Thermal Analysis. The instrumentation piping attached to process lines within primary containment were analyzed (over their full length) by the Architect Engineer at the associated process line operating temperature.

These instrument lines are uninsulated, dead-ended services and, as such, they carry no process flow. As a result, the instrument lines only maintain the process line temperature within ten to fifteen pipe diameters of their attachment point to the process line. The balance of the line is, thus, in equilibrium with the containment ambient temperature. All of the subject instrument lines are 3/4 or one (1) inch stainless steel pipe runs.

vl The described elevated instrumentation piping thermal analysis fault is conservative (i.e. it over predicts stresses) in many cases. However, cases do exist where the excess instrument line thermal expansion works to reduce piping thermal stress states by achieving a false net zero thermal anchor movement between the large bore process piping and the attached instrument piping. Fortunately, the small diameter instrument piping has a high degree of flexibility and can accommodate significant displacements without developing thermal expansion stress responses which exceed ASME Code limits. As an example, a worst case configured instrument system (designated X42a) was reanalyzed and it was shown that the increased thermal stresses were still in compliance with ASME limits. As a followup, a survey of ~11 inside containment instrument piping anchor groups was completed and the susceptible cases were identified'or thermal reanalysis and full requalification in compliance with ASME Code requirements. Where needed, support adjustments will be

~ ~

~

mpleted at the next maintenance outage to assure that good design practices for thermal expansion are adhered to in all WNP-2 piping installations. ~

77

A JCO was prepared based on the cited analysis results of instrument system X42a, a worst case configuration.

on these analyses it was concluded that an Unreviewed Safety Question did not exist since 1) no strumentation function was impaired, 2) design basis pressure boundary stresses met the requirements of the

=

governing ASME Code, and 3) no Technical Specification margin of safety was reduced.

2.6.4.10 PER 'g~

This Problem Evaluation Request described a problem with the LOCA accident analysis supporting the 9 X 9 fuel. It had been determined that the current fuel vendor had not accounted for the time required to accelerate the HPCS pump from de-energized to rated conditions.

f v ai n mm C

A Justification For Continued Operation (JCO) was written which showed that, by changing the initiation signal for the HPCS start, the timing used in the analysis was acceptable. The fuel vendor, Advanced Nuclear Fuels (ANF), assumed flow to commence within 18.5 seconds after the start of the LOCA, and for the HPCS system to receive a start signal on low water level at 7.5 seconds into the LOCA. By taking credit for high drywell pressure as the initiation signal, the HPCS system receives the initiation in less than one second. This allows greater than.5 seconds for the HPCS pump to achieve rated speed, making the 18.5 second assumption bounding. Further, the LOCA analysis had approximately 450'F margin to the 10CFR50.46 peak cladding temperature (PCT) requirements. This change did not constitute a change to Technical Specifications in that PCS was always operable, and there would be no change required to the APLHGR curves. These are the only

,items germane to this subject in the plant Technical Specifications.

2 PLANT T AND EXPERIMENT f

This section of the report covers WNP-2 Plant tests and experiments not described in the Safety Analysis Report as required by 10CFR50.59.

2.6.5.1 em Pr re 4 Governor valves used to control'steam flow to the main turbine are controlled by DEH (a Digital Electro-Hydraulic control system). In order to assess the impact of governor valve position on plant thermal efficiency while at near 100% reactor power, one of the two partially-open governor valves was placed in valve test, In a controlled manner, the two governor valves were repositioned with one -10% open and the other -90%

open. To preclude any uncertainty about DEH response in the event that a bypass valve opened causing a DEH mode change [changing from mode 4 (Turbine Follow Reactor Manual Mode) to mode 3 (Turbine Load Control Mode)] while the governor valves were in test, a temporary jumper was installed.

f Evl i n mm The functionality of the DEH control system with the jumper installed and with the governor valves in an optimized configuration did not result in a change to WNP-2 Technical Specifications or involve an Unreviewed Safety Question because (1) the function of the DEH control system in mode 4.did not change, (2) the margin f safety provided in the Technical Specifications was not changed, and (3) the boundary conditions for the SAR were not changed.

2.6.5.2 Tem ora Procedure 2 8.14 This temporary procedure provided direction for partial draining of the Spent Fuel Storage Pool. The Spent Fuel Pool B diffuser check valve, FPC-V-146B, appeared to be stuck shut. The valve is located in one of the two diffuser lines that supplies the Spent Fuel Pool. The valve is approximately 19 inches below the water line of the Pool. The valve could not be isolated from the Spent Fuel Pool, so the level was lowered below that of the valve to perform the maintenance.

afe Ev luati n umma The temporary procedure provided the cautions and directions to lower the pool level in a controlled manner.

The procedure required entrance into the action statement for Technical Specification 3.9.9, which prohibits fuel handling or the transfer of any load over the pool while the pool level was lowered. Therefore, the basis for the specification, prevention of spent fuel damage, was maintained.

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2.6.5.3

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P re 2 This temporary procedure was performed to determine the operability of valve MS-V-146. The valve was not stroke tested following maintenance on the valve stem packing. Without post-maintenance testing, the valve could not be considered operable. When the lack of testing was discovered the valve was declared inoperable and the Technical Specification action statement (L.C.O. 3.6.1.4) for the loss of one MSLC subsystem was entered. With the plant at power the valve could not be fully closed without causing a plant shutdown. This procedure was written to partially close the valve and take a current signature during the stroke to determine if the valve motor current remained within acceptable limits.

Safe val n mm IfMS-V-146 were to close it would result in isolation of the Main Steam Bypass Valves located downstream.

generator load rejection with bypass valve failure is an analyzed accident and has a failure probability in the moderate frequency range. To increase the probability of this accident during this test would require either the valve MS-V-146 going full closed, thus isolating bypass valve capability, or having reduced bypass capacity while the v'alve is stroked partially closed.

There was no discernable increase in probability for failing the valve MS-V-146 closed. The procedure had a precaution/limitation that required opening the electrical disconnect switch if the valve moved more than 15 seconds. During performance of the procedure, personnel were stationed at the MCC cubicle and were in

~

contact with the control room. During installation of the switch, all work was "second verified" and the

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peration of the switch was tested during the installation. To close the valve inadvertently would require the

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simultaneous failure of the switch and the electrical disconnect which is not credible. There, is no increase in the failure frequency from "moderate" to "normal." ~

The testing of valve MS-V-146 did not increase the consequences of any analyzed accidents. Generator load reject with bypass failure already bounds the worst-case failure during this test of fully closing MS-V-146.

There were no off-site dose consequences from the generator load reject with bypass failure.

2.6.5.4 TelTI Pr e ure .111 This temporary procedure was written and performed to investigate operation of the Reactor Water Cleanup (RWCU) System at increased flow rates. The flow rate was increased to 183 percent of normal to allow evaluation of system performance under controlled conditions. The results of this test were used to establish a routine higher flowrate in the RWCU system to improve reactor water chemistry.

afet Ev lug i n mrna This change did not result in a change to the WNP-2 Technical Specifications or involve an Unreviewed Safety Question because (1) the margin of safety in the Technical Specifications was not reduced by the temporary increase in RWCU flow rate, and (2) the boundary conditions of the FSAR evaluations were not impacted by the flow increases.

80

PL NTPR D E HAN e Plant Procedure control program requires a 10CFR50.59 evaluation whenever a procedure is changed, which provides assurance that the disposition does not involve a change to the Technical Specifications or involve an Unreviewed Safety Question. Plant procedure changes associated with other change documents such as Plant Modifications or Lifted Leads and Jumpers are described in other subsections of. this report. The following are summaries of significant Plant Procedure changes not covered elsewhere in this report that were processed during 1990:

2.6.6.1

~PM 7 2 2

22 Plant Procedures were modified to ensure Diesel Generator operability under accident conditions that could result in elevated temperatures in the Diesel Electrical Equipment Rooms. A recalculation had found that the Emergency Diesel Generator Static Exciter Voltage Regulator (SEVR) would not function in the high temperatures found in the equipment rooms (see LER 90-020 for additional details). The revised plant procedures call for Plant Operators to remove SEVR subcompartment doors to limit the temperature rise when room temperatures exceed predetermined limits.

afe Evaluati n umma The safety evaluation concluded the DG operating margins were maintained and the basis for the Technical Specifications had not changed. An Unreviewed Safety Question did not exist since the procedure changes allow the SEVR (and therefore, the Diesel Generators) to operate satisfactorily within the design basis.

2.6.6.2 PDF -1 2 nd 1 2

~IR~121

~PER 1~7 This procedure and instrument setpoint change was made to match Reactor Water Cleanup (RWCU) Flow Transmitter 41 (RWCU-FT-41) to its flow element orientation. The change used an empirically-based calibration curve to match RWCU-FT-41 with the flow element.

afet Evalua ion umma This change did not result in a change to the WNP-2 Technical Specifications or involve a Unreviewed Safety Question because, (1) the change did not result in a loss of isolation capability for the RWCU system, and (2) this instrument is not used to support the high energy line break safety analysis.

81

2.6.2.3 PPM2 7 2 d 1 ese changes to plant procedures were initiated as a result of GE SIL 502 (OER 89075), which identified potential violations to the critical po'wer ratio during a single turbine valve slow closure transient. The changes raised the normal DEH flow limiter setting from 110% to 130% in order to be above the GE-re'commended minimum of 115.5% and provide increased operational reliability.

S fe Ev a' mm This did not require a change to the WNP-2 Technical Specifications or result in an Unreviewed Safety because the new setting resulted in only a minor change to a non-limiting transient (Pressure Regulator 'uestion Failure-Open, FSAR 15.1.3). The sequence of events and; hence, the consequences of this type of malfunction are changed. The G.E. Transient Safety Analysis Design Report for WNP-2 (GEZ-6413) indicates that a DEH flow limiter setting of 130% will result in a turbine trip due to level swell as a result of a pressure regulator failure. A DEH flow limiter setting of 110% yields an MSIV isolation as a result of a pressure regulator failure. This change in the sequence of events is bounded by the turbine trip/generator load reject transient which is considered separately. Therefore, the consequences of this change in DEH flow limiter setting are not considered to be increased.

2.6.6.4 PPM4 2 S R nd 6 This procedure change and Instrument Setpoint Change Requests 985 and 986 revised the high radiation alarm setpoints for two Area Radiation Monitors (ARM-RIS-24 and ARM-RIS-5), to compensate for increased background radiation levels. Background 'radiation levels increased due to fuel handling operations during Refueling Outage RS. Alarm setpoints are selected to provide indication of any abnormal increase in radiation levels, while minimizing false alarms. The setpoints were subsequently lowered post-outage reflecting decreased background levels.

fet Ev luati n mrna These instruments are not specifically addressed in the WNP-2 Technical Specifications. ARM alarm setpoints are dependant on background radiation levels. Periodic adjustments for changes in background due to changes in operating conditions or special evolutions does not constitute a modification or change that has the potential for reducing any safety margins, nor increase or create the possibility or probability of occurrence of an accident or malfunction.

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2 7 FIRE R PR RAM HAN e following changes involving the Fire Protection Program are reported in accordance with the NRC Letter ated May 25, 1989 which approved Amendment No. 67 to the Facility Operating License.

2.6.7.1 SCN 89429 was developed to incorporate into the FSAR those fire protection requirements which were removed from the Technical Specifications in Amendment 67. The SCN incorporates minor changes to the fire protection program as follows:

1. This change (paragraph F.5.2.3.d) revises the Technical Specification 4.7.6.1.1.d requirement that the fire protection water system be demonstrate operable "at least once every six months by performance of a system flush". The SCN requires that the main fire header be flushed annually.

The Technical Specifications defined the fire protection water system as water supply, pumps, and distribution piping to the yard hydrant curb valves, the last valve ahead of the water flow alarm device on each sprinkler or hose standpipe, and the last valve ahead of the deluge valve on each deluge or spray system required to be operable in accordance with Specifications 3.7.6.2, 3.7.6.4 and 3.7.6.5.

The implementation of the Technical Specification requirements to perform a system flush every six months would; therefore, ensure that the water flow path to each required sprinkler system, water spray system, hydrant valve, or hose standpipe was free of obstruction every six months.

The SCN, through requirements for ring header flush, hydrant flow tests, sprinkler system testing and hose station flow tests ensures that the testable sections of the fire water system are clear. The lead-ins to the sprinkler systems are not flushed (main drain. tests) to reduce the potential for radioactive contamination during testing (due to the large quantity of water discharge with no connection to plant drain system). The SCN reduces the frequency of flushing to an annual basis, based on recent testing which showed minimal debris.

2. Technical Specification 4.7.6.1.2.c required a diesel inspection at least once per 18 months. SCN paragraph F.5.2.3.2.c specifies that the diesel be inspected in accordance with the diesel manufacturer's recommendations. This change avoids unnecessary tear-downs of the diesel, as the manufacturer does not recommend inspection every 18 months.
3. Technical Specification 3.7.6.2 required a continuous fire watch in the event that a spray/sprinkler system which protects redundant systems or components is inoperable. The SCN paragraph F.5.3.2.a specifies the systems which protect redundant systems or components (systems ¹65, ¹66). Because these two systems are pre-action systems, the SCN allows the pre-action system to be operated as a wet-pipe system to.provide suppression coverage in lieu of posting a continuous fire watch, until the system is restored to full operability as a pre-action system.'.

SCN paragraph F.5.2.3 does not include Technical Specification 4.7.6.1.2.a.2 statement that fire pumps be tested "on recirculation flow". This change in wording is not significant.

83

Le 0

SCN paragraph F.5.7.3.2 states that fire doors willbe verified closed daily during routine operator plant tours and inspected weekly to verify that the doors are not damaged or obstructed. Removed Technical Specification 4.7.7.2 required unlocked fire doors without electrical supervision to be verified closed daily. Reference to testing of electrical supervision of the doors is removed as this testing is not applicable to fire doors at WNP-2.

SCN paragraph F.5.7.3.1,d has been added to allow to clarify the inspection requirements for certain access doors not normally used for personnel traffic. The access "doors" are often classed as penetrations and inspected under the requirements of removed Technical Specification 4.7.7.1.

Therefore, for consistency with the removed Technical Specifications, the SCN requires these doors to be inspected at least once per 18 months.

7. SCN paragraph F.5.6.2 differs from removed Technical Specification 3.7.6.5 in that the Technical Specification required that backup fire hose be provided within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> if the hydrant provides the primary means of fire suppression. The SCN allows 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> to provide the backup hose. This change was based on the inventory of fire hose in the Fire Brigade Van.
8. Removed Technical Specification 4.7.6.5.b specified the spring/fall months for a six-month hydrant inspections. SCN paragraph F.5.6.3.b specifies hydrant barrel should be verified "drained", and the removed Technical Specification required that the hydrant barrel be verified "dry" This change is not

~

significant.

9. SCN paragraph F.5.5.2 differs from removed Technical Specification 3.7.6.4 in that the removed

~ Technical Specification allows 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> to install compensatory hose in any area protected by fixed fire suppression system. The SCN specifies 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> for installation of compensatory hose for all essential hose stations. This change is more conservative than removed Technical Specification requirements.

10. SCN paragraph F.5.4.3.c. 1 differs from removed Technical Specification 4.7.6.3.c.l in that the SCN does not specify verification of actuation of associated closure devices. As the PGCC halon systems do not include any associated closure devices, this change does not appear significant.

SCN paragraph F.5.8.2 differs from removed Technical Specification 3.3.7.9 in that the removed Technical Specification action statement allowed different compensatory actions based on the function of the inoperable detector (early warning or used to actuate a fire suppression system). Under certain conditions, the removed Technical Specification allowed the inoperable detectors to be restored to service within 14 days or a fire tour be established within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />. For simplicity, the SCN does not distinguish between the function of the different detectors, but requires a fire tour to be established within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> if any of the required detectors is out of service. The removed Technical Specification option to not post a fire tour if the detector is restored to service within a certain time period is not included in the SCN as an option. The removed Technical Specification basis has been modified to reflect this program change and is incorporated in the SCN in paragraph F.5.1.1.

12. SCN table F.5-3 differs from removed Technical Specification.7.7.9 in that the SCN does not specify the type or number of detectors installed in each plant area and does not distinguish between early warning and detectors which actuate fire suppression systems. The type, number, and function of each detector was included in the removed Technical Specifications as the Technical Specification allowed different compensatory measures based on the detector function. The SCN requires the compensatory measures to be initiated when ~an detector within an essential fire detection zone is inoperable.

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13. SCN paragraph F.5.8.3 differs from removed Technical Specification 4.3.7.9. The removed Technical

' Specification required all detectors be verified operable by performance of a channel functional test at least once per six months. The SCN modifies the frequency of testing for smoke detectors to require visual inspection every six months and a channel functional test every 12 months. Similarly, normally inaccessible detectors are tested during cold shutdown exceeding 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> unless tested in the previous 12 months. The NFPA 72D detector supervision circuits are verified operable during the channel functional test of the detector zone.. The change in the frequency of the channel functional tests for smoke detectors was previously resolved.

14. Technical Specification 4.7.6.3 required the performance of a flow test through accessible headers and nozzles of the PGCC halon systems every 18 months to assure no blockage. SCN paragraph.5.4.3.e requires the performance of this test every five years based on the following:
a. The PGCC area is not readily accessible; therefore, the halon nozzles are not subject to inadvertent damage or plugging.,
b. The reduction of the test frequency reduces the challenges to the system caused by the complexity of the test and reset procedure.

2.6.7.2 N -24 This SCN revised the fire door inspections from daily to weekly and makes provisions for not performing the

'nspections if plant conditions (Such as ALARA) cause a conflict.

This change does not increase the probability of occurrence of an accident or- malfunction of equipment important to safety, as the change does not modify plant equipment. The change affects only the procedural means to ensure that unlocked fire doors are checked shut daily.

2.6.7.3 The frequency for testing of the high temperature alarms associated with the manually actuated suppression-systems on the Standby Gas Treatment (SGT) System charcoal filter beds (Fire Protection Procedures 15.2.34 and 15.2.35) was changed from semi-annual to refueling outage.

2.6.7.4 The fire door routine test procedure, PPM 15.1.2, was modified to add an annual inspection of fire door clearances and latching mechanisms. Although not specifically required by the fire protection program, this change was initiated to provide assurance that the fire doors continue to conform to the installation requirements of NFPA 80, "Standard for Fire Doors and Windows".

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V I

2.6.7.5 4

A temporary change was made to pressurize the Fire Protection System with the Potable water system while the Circulating Water Basin was drained during the annual refueling outage. The cross-tie provided added

'assurance that the fire protection needs of the plant would be met.

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0 7 P. RT F I L E AT R IL This section contains information pertaining to the reporting of diesel generator failures, valid and nonvalid, in accordance with the requirements of WNP-2 Technical Specification 4.8.1.1.3, This report provides the information required by Regulatory Position C.3.b of Regulatory Guide 1.108, Revision 1, August 1977.

rF il m r n

1. -

Identity of diesel generator unit and date of failure:

Division Two Emergency Diesel Generator (DG-2)

January 7, 1990

2. Number designation of failure in last 100 valid tests:

This was the Second Failure of the last 100 valid tests.

3. Cause of failure:

During performance of the Monthly Surveillance Test, the Division Two Diesel Generator tripped on Engine Overspeed. An Investigation revealed that the Limit Switch Linkage Arm Set Screw was found to be loose. This limit switch monitors the position of the Overspeed Reset Lever, and initiates a trip of both engines when upward movement of either reset lever is detected.

4. Corrective measures taken:

The limit Switch Linkage Arm was readjusted to the proper position, consistent with the other Engine Devices. The Allen Set Screw was then tightened to maintain this linkage position.

5. Length of time diesel generator unit was unavailable:

The Diesel Generator was out of service for 15 1/2 hours, and returned to service at 1810 Hrs on Sunday January 7, 1991.

6. Current surveillance test interv'al:

Thirty-one days,

7. Verification of test interval:

The surveillance test interval of thirty-one days is in conformance with NRC Reg.

Guide 1.108 position C.2.d.

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Die el en Failur N m er F ur Identity of diesel generator unit and date of failure:

Division Three Emergency Diesel Generator (DG-3)

May 23, 1990

2. Number designation of failure in last 100 valid tests:

This was the Second Failure of the last 100 valid tests.

3. Cause of failure:

While performing the HPCS DG LOCA Test per PPM 7.4.8.1.1.2.8, at step C.5) the HPCS Diesel Generator exhibited erratic frequency and voltage control. When the operator tried to raise the load, the frequency and the voltage both started oscillating.

The High Pressure Core Spray Pump, HPCS-P-1 was tripped off line, and then the HPCS Diesel Generator was tripped. Troubleshooting of the Engine controls revealed cold solder joints on the Woodward governor control board.

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4. Corrective measures taken:

All Woodward Governor controls on the other units were inspected as well as the new unit installed on the HPCS Diesel. Cold solder connections were also found on the new control board that was to be installed on the HPCS Diesel, and were repaired prior to installation. No other. suspect solder connections were found on any control board inspected.

5. Length of time diesel generator unit was unavailable:

The HPCS Diesel Generator was out of service for 9 days and returned to operable status on June 1, 1991 at 0640.

6. Current surveillance test interval:

The testing frequency was accelerated to once every 7 days. This accelerated testing continued for 20 consecutive tests, ending on October 26, 1990.

7. Verification of test interval:

The surveillance test interval of seven days is in conformance with WNP-2 Technical Specifications Table Number 4.8.1.1.2-1.

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