ML17285B080

From kanterella
Jump to navigation Jump to search
WPPS-2 Annual Operating Rept for 1989. W/900228 Ltr
ML17285B080
Person / Time
Site: Columbia Energy Northwest icon.png
Issue date: 12/31/1989
From: Powers C
WASHINGTON PUBLIC POWER SUPPLY SYSTEM
To: Martin J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
References
NUDOCS 9003140332
Download: ML17285B080 (192)


Text

ACCHZMTZD D)STR1SUTtON; DKMONSTRZT1ON SYSTEM REGULAT INFORMATION DISTRIBUTIOYSTEM (RIDS)

ACCESSION NBR: 90033:49332 DOC. DATE: 8+j .'Mj'3? NOTARIZED: NO y-FACIL:50-.397- WPP$ S Nuclear Project, Unit 2, Washington Public Powe DOCKET ¹ 05000397 AUTH.NAME AUTHOR AFFILIATION POWERFC.Mo Washington Public Power Supply System RECIP.NAME RECIPIENT AFFILIATION

SUBJECT:

"Annual Operating Rept for 1989." W/900228 lt DISTRIBUTION CODE: ZE47D COPIES RECEIVED:LT E CL ~ SIZE:

TITLE: 50.59 2Ginu~a

. Report of Changes, Tests or Experiments'ade W out Approv I NOTES: +~~A D RECIPIENT COPIES RECIPIENT COPIES S

ID CODE/NAME LTTR ENCL ID CODE/NAME - LTTR ENCL

~

PD5 LA 1 0 PD5 PD 5 5 SAMWORTHFR 1 0 I'NTERNAL::

6 6 AEOD/DOA 1 1

"" AEOD/DSP/TPAB ACRS'-

1 1 NRR/DLPQ/LHFB11 1 1 D NRR/DOEA/OEABll 1 1 @)RE+ PB1 1 2 2 NUDOCS-ABSTRACT 1 1 02 - 1 1 D RGN5 FXLE 01 1 1 8,

EXTERNAL: LPDR 1 1 NRC- PDR 1 1 NSXC 1 1 PdfS>>4~O~.

D S,

PZEASE HELP US IO RECCE %APZB! CXMHKT THE DOCUMEPZ CXNTBOL DESK, LISTS MR DOCUMEHIS KRJ DCKFT NEEDf TOTAL NUMBER OF COPIES REQUIRED: LTTR 25 ENCL 23

e t

~ 4

"ti WASHINGTON PUBLIC POWER SUPPLY SYSTEM F.O. Box 968 ~ 3000 George Washington Way ~ Richland, Washington 993$ 2 Docket No. 50-397 February 28, 1990 Mr. J. B. Martin Regional Administrator Region V U.S. Nuclear Regulatory Commission 1450 Maria Lane, Suite 210 Walnut Creek, California 94596

Dear Mr. Martin:

Subject:

NUCLEAR PLANT NO. 2 ANNUAL REPORT

Reference:

1) Title 10., Code of Federal Regulations, Part 50.59(b)
2) WNP-2 Technical Specifications, 6.9.1.4 and 6.9.1.5

~

Regulatory Guide 1.16, Reporting of Operating Information

')

Appendix A

- ==- In.-accordance with the above listed references, the Supply System hereby submits the Annual Report for calendar year 1989. Should you have any questions or commerits please contact G. L. Gelhaus, WNP-2 Assistant Plant Technical Manager.

Very truly yours, C M. Powers WNP-2 Plant Manager

/bc Attachments p/OP voosxeass2 s9123i

~

PDR R

ADOCK 05000S97.

PNU gP o

Pf

-2

.OPERA ~ ~

REPORT 1989 i>>

R i0 v ~

>> .'++/ $(>>>>$4'+P'>>>>>>>>>> w)>>~A+ ~~i)P'>>>> t~ty.{>>f'4 vf>> ~

,*, ~+/Hi>> 4, 4 ~, A>>

WhSHINGTON PUBLlC POWBR

"-.'=;
;".-4N %JPPLY SYSTEM.

~ 'I'

'f

~

~

I 9003140332

[(

f

TABLE OF CONTENTS

1.0 INTRODUCTION

...................... 1 1.1 1989 Power History Graph for MNP-2'........ 4 2.0 REPORTS ~ ~ ~

2.1 Annual Personnel Exposure and Monitoring, Report 2.2 Main Steam Line Safety/Relief Valve Challenges.............

2.3 Summary of Plant Operation ............ 11-2.4 Summary of Significant Maintenance Performed on Safety-Related Equipment 16 2.5 Indications of Failed Fuel 35 2.6 Plant Modifications.... 42 2.6.1 Plant Design Changes . . . . . . . . . ; 43 2..6.2 Lifted Leads and Jumpers . . . . . 54 2.6..3 FSAR Amendment Evaluations.... ~ ~ ~ ~ ~ 59 2.6.4" Other ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ 60 2.7 Plant Tests and Experiments . 74 2.8 Plant Procedure Changes . 75 2.9 Reactor Coolant Specific Activity Levels. ~ ~ ~ ~ ~ 79 2.9.1 MNP-2 Dose Equivalent Iodine Graph ~ ~, ~ 80 2.10 Diesel Generator Failures . . . . . . . . 81

~ ~ ~ ~ ~

2.11-Fire Protection Program Changes 90

0 (1

II l'

I Y c t

f

ANNUAL OPERATING REPORT OF WNP-2 FOR 1989 OOCKET NO. 50-397 FACILITY OPERATING LICENSE NO. NPF-21 Washington Public Power Supply System 3000 George Washington Way Richland, Washington 99352

1.0 INTRODUCTION

The 1989 Annual Operating Report of Mashington Publ i c Power Supply System Q Plant Number 2 (MNP-2) is provided as a supplement to the Honthly Operation Report. This report is submitted in accordance with the requirements of Federal Regulations and Facility Operating License NPF-21. It should be noted that, for ease. of reference and completeness, additional reports are also included. Plant MNP-2 is a 3323 HMt, BMR-5, which began commercial operation on, December 13, 1984.

8 On January 30, 1989 the reactor scrammed due to Turbine Control Valve Fast Closure actuation of the- Reactor Protection System (RPS) logic. The RPS logic actuated when the main generator 500Kv output breakers tripped as a result 'as of high currents created when a porcelain insulator, on the -output side of the 25/500Kv main transformer, shorted to ground. On February 2-, 1989, following a three-day outage to replace and clean several insulators, the Plant returned to normal operation. However, due to a problem with opening one of the four outboard. Hain Steam Isolation Valves, power output was limited to 78 percent.

The Plant continued to run in this configuration, with the valve closed and steam supplied through three of four main steam lines, until the Plant was shut down for the annual maintenance and refueling outage.

From April 28, 1989 until July 2, 1989 the Plant was, in a shutdown condition as .scheduled -for the annual maintenance and refueling outage. Following the outage; the Plant was restarted and operated until August 6, 1989 when a e-J reactor scram occurred due to the trip of a reactor feedwater pump caused by a problem in the= feedwater pump control oil system. On August 9, 1989 the Plant was restarted; The Plant was shut down and an Unusual -Event was declared on August 11, 1989 as a result of declaring six Class 1E, 480 volt A.C., Motor Control - Centers (HCCs) inoperable due to the discovery of a design defi-ciency.:All--of the affected HCC power supply circuit breakers were replaced with jumper cables of equal capacity with the exception of one, which was replaced, with-. a fused disconnect of equal capacity.. During restart, on August 17, 1989, another reactor scram occurred as a--result of=a surveillance being performed on a'eactor level instrument associated. with- the Automatic Oepressurization System (ADS).

On August 18, 1989 the reactor was restarted but power output was limited to 70 percent due to removing a reactor feedwater pump from service because of a bearing failure. One of two reactor pumps was repaired and the Plant returned to- full power on September 13, 1989. The Plant essentially remained at 100 percent power until September 21, 1989, when it was-shut down due to two leak-ing condenser .tubes and two ruptured bellows connections on a low-pressure steam extraction line. Repairs were made and the Plant was restarted on September 29, 1989 and ran at or near 1005 capacity for the remainder of the year (94 days).

5I Ouring 1989,:there were several examples of major accomplishments which required significant effort on the part of Supply System personnel to complete. The following is a summary of those efforts.

(a) The fourth refueling outage was successfully completed. Significant activities included:

o Preventive maintenance on the eight Main Steam Isolation Valves (MSIVs), and a major overhaul on the valve, that limited'lant power

.output to 78 p'ercent of capacity. Four of the valves were repaired to reduce the potential for valve binding caused by galling in the

-cylinders. Valve pistons of a new 'design by Rockwell, the MSIV supplier, were installed in those MSIVs.

o =

Overhaul of one of the two Reactor Feedwater Pump Turbines. The turbine was dismantled and the rotors were cleaned and inspected for-cracks or other defects.

o Inspection of two of the three Oiesel Generators.- This task included replacing power assemblies in the two engines.

o - Inspection of one of three Low-Pressure Turbine Rotors.

Non-: destructive examination of the rotor confirmed 17 crack indications and the blades. were replaced. Subsequent evaluations determined that the problems were limited to this single-rotor.

e- '0 activity included 0'aintenance on 40 Control Rod Orive Mechanisms (CROMs).

removing, replacing and rebuilding the CROMs.

Removal of a radioactive "hot spot" in the vessel dr ain to the This

-Reactor Mater Cleanup System. This activity required the installa-tion-of a temporary bottom head drain plug in the Reactor Pressure

.Vessel. The plug was installed from the top= of the vessel which required removal of four fuel assemblies, a control rod blade, guide tube and associated support pieces.

Removal of spent fuel assemblies and refueling the reactor. The refueling activity included replacing 136 fuel assemblies, using a fuel shuffle scheme.

(b) In terms of electrical output, MNP-2 delivered 6.1 billion kilowatt-hours to the. Bonneville Power Administration, surpassing the previous year'

record by more than 117 mi 1 lion kilowatt-hours.. In addition, the

- capacity factor for 1989 was a Plant record 63.78 percent (up from 62.38 percent in 1988).

-(c). A new monthly generation mark was established in Oecember, when 780 million kilowatt-hours were generated.

f (d) In December, MNP-2 celebrated five years of commercial operation. Since 1985, the 'lant has provided more than 28 million megawatt-hours of electricity to the Bonneville Power Administration.

In 1989, total radiation exposure at the Plant was 492 man-rem, as compared to the 1988 level of 352 man-rem. (The Institute for Nuclear Power Operation

.(INPO) has set;460 man-rem as the 1990 industry goal for BMRs.) Contributing to this increase were the following activities:

0 Removal and replacement of 40 Control Rod Drive Mechanisms (CRDMs).

During work on the first 20 CRDMs, the- man-rem exposure was 13.005.

As a:result of that exposure, temporary shielding was put into place and the man-rem exposure was reduced to 5.635 for the remaining 20-CRDMs.

o . Removal of the "hot spot" in a reactor bottom head drain line

.elbow. Before replacement, the "hot spot" area was reading between 2,000 and 3,000R., Total man-rem exposure for this activity was 18.836.

o . Modifications to the Control Rod Drive Rebuild Room and flushing of Low- Pressure Core Spray (LPCS) System lines. These actions were taken to reduce man-rem exposure in the future.

During the year NNP-2 received 23 'Notices of Violation (NOVs): One (1)

Level III, twenty-one (21) Level IY and one (1) .Level V. The Level III violation. was:-associated with commercial grade dedicati.on issues and included e a proposed $ 50,000 civil penalty.

Also during-1989, a total of 45 Licensee Event Reports (LERs) were written and submitted pursuant to the requirements of 10CFR50.73.-

-.. The-1989 capacity factors, based upon net electrical-'nergy output, are listed in the following table.

Month Ca acit Factor January 76.17 February 68.25 March 73.02 April 68.32

. Hay 0 June 0 July 88.47 August 52.94 September 58.39 October 88.80 November 95.84 December 95. 74 Overall 63.78

" Started Maintenance/Refueling Outage

~ Ended Maintenance/Refueling Outage

~ ~

~l Q I9 j

I i 4 ~ II 4," ~ i II >I ~

II III'

~ , ~ I I

0 WNP-2 Il,) I I> ' I I>I ~ "'> -' ~

1i> 1( 0 i I i ~ ~. I I"<<l>l'I('l<>>1k;= f ll* > i i ~ y~ gg ~ I q ~ > ) I<>> ~

' Is>)lit I-* l i. >> i>>III II>>l If llI>>

~ ill<<1 >c<] s I ~ > s ~ (II I~. >

~ i>> I ~ ii I 400 90 80 70 6$

E Q

50 I-40 65 30 0 Refuel tng

~4 20 Outag 8 10 0

January February March 'p'rll ' ',

M@ J f. Jurje= II ~ p)y'.: ','ugust'( 'September October November December 1989 Data based on average power generated per da . Therefor, recovery from a scram that ocurred within a 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> period, will not indicate a zero percent power level.

lu v,

I

2.0 REPORTS The r

-reports provided in this section meet the requirements of Federal Regula-tions (10CFR50.59)

~ and the MNP-2 Operating License. Complete, data for the year 1989 has been included.

f

'1 f

l

2.1 ANNUAL'ERSNINEL'EXPOSUfIE ANO NONI @RING REPORT I I SYSTEH I C POWER SUPPLYI

~

I WASHINOTOl RER-020

'ORK RADIA

/'.

EXPOSURE RECORDS AND JOB FUNCTION REPORT 16 APPENDIX A' Of/26/90 =.

I~~ I~ ~ ~

NUCLEAR PLANT NO. 2 REPORT FOR CALENDAR YEAR. 1989

~ I NUHBER OF PERSONS RECEIVIN4 OVER 100 ilREH TOTAL HAN-REtf 8TATION UTILITY CONTRACTORS STATION UTILITY CONTRACTORS EtPLOYEES EtMILOYEES AND OTHERS EtlPLOYEES EtlPLOYEES AND OTHERS OPERATIONS fl SURVEILLANCE t&INTENANCE PERSONNEl- 68. 105 0. 073 55. 753 40. 102 0. 027 31. 527

~ J'l OPERATINO PERSONNEL 42. 537 0. 000 0. 000 32. 471 0. 000 0. 000 HEALfH PHYSICS PERSONNE~&. 767 0:037 l5. 620 22. 13D 0."004 8. 943 II ~ I SUPERVISORY PERSONNEL 15. 073 1. 816 0. 283 h. 090 f. 472 0. 089 ENOINEERINO PERSONNEL 14. 164 9. 165 13. 565 4. 036 4. 399 h. 090 ROUTINE tlAINTENANCE HAINTENANCE PERSONNEL 23. 592 0. 139 23. 78$ 14. 824 0. 054 11. 054 L"I OP ERAT INO PERSONNEL i. 916 0. 000 0. 000 1. 571 0. OOO O. OOO PHYSICS PERSONNEE.=7. 561 0. 000 I. 266 i. 303 0. 000 1. 213 SUPERVISORY. PERSONNEL 2. 3&8 0. 000 0. 330 0. 980 0. 000 0. 103 ENOINEERINO PERSONNEL 3. 619 2. 498 4. 002 1. 052 0. 884 0. 669 40'II

=It 34I 54 I

I INSERVICE INSPECTION 'AINTENANCE PERSONNEL OPERATINO PERSONNEL HEACIH PHVSICE1'ERSONNEL~IE SUPERVISORY PERSONNEL END INEER I NO PERSONNEL

~

2. 790
2. 101
0. 715
3. 313
0. 000
0. 000 0; 000
0. 184
3. 116

. 7.

0.

0.

0.

9.

869 000 589 010 977 1'. 799

i. 512 1: 597
0. 487
1. 222 0.

0 0.

0.

f.

000 000 000 179 120

= 3. 919 0 000 0: 622

0. 004
2. 316

5:

SPEC IAL HAINTENANCE HAINTENANCE PERSONNEL OPERATINO PERSONNEL ALfH PHYSICS PERSONNEL 116. 436

1. 493

~07 I

1. 776 0.

0.

000 000 161. 313

0. 000
30. 639
89. 675
0. 555 6.723
0. 747 D. 000 D: 000

'. 9'P. 971

0. 000
30. 502 SUPERVISORY PERSONNEL 3. 313 0. 000 3. 386 2. 484 0. 000 857

)0. 462 6. 805 13. 340 3. 848 2. 766 5. 127 Il ~

ENOINEERINO PERSONNEL tlA'IHTCNANCd'PERSdf4NEL' I ' lf0 458'f I l f "1 f fO'.'OOd HI ' '

OOO 5. 319 0. 000 0. 000 34 4 WA8TE PROCESSINO OPERATIN4 PERSONNEL HEALTH PHYSICS PERSONNEL SUPERVISORY PERSONNEL '

0. 070.

0; 467

0. 000 '
0. 000'.
0. 000
0. 000
0. 000 700
0. 991
0. 022 0:523
0. 000
0. 000 000 000
0. 000 2: 797
i. 902 ENOINEERINQ PERSONNEL 'O. 000 ' '0. 000 ' 0. 000 0. 000 0. 000 0. 000 7

R EFUEL INQ HAINTENANCE PERSONNEL 15. 235 ' 0. 013 '

1. 220 13. 147
0. 714 0.

0.

004 000

0. 761
0. 000 OPERATINO PERSONNEL 1. 009 0. 000 0. 000 HEATH PHYSICS PERSONNEf. 0. 528 0, 000 2. 596 0. 723 0. 000 ~ 1: 257 SUPERVISORY PERSONNEL'. 542 0. 000 o. Ooo 0. 210 0. 000 .
0. 000

~ H ENOINEERINO PERSONNEL 1. 336 0. 604 0. 220 0. 358 0. 206 0. 067

0. 832 147. 232 TOTAL HAINTENANCE PERSONNEL OPERATINO PERSONNEL HEALTH PHYSICS"PERSONNEL SUPERVISORY PERSONNEL 234. 613

'9. 126

40. 672
22. 011
2. 001
0. 037'3.
0. 000
2. 000 249. 940
o. ooo 410
5. 000 1&4. 866
37. 245 35."499
10. 251

'"0.'. 0. 000 004 651

0. 000 "45."334
3. 955

~ I ENOINEER INO PERSONNEL 32. 894 22. 188 41. 104 10. 516 9. 375 14. 269

>>>>>>ORAND TOTAL>>>>>> 379. 316 26. 226 34'9. 454 258. 377 11. 862 210. 790

II I

2.2

~ MAIN STEAM LINE SAFETY/RELIEF VALVE CHALLENGES This section contains information concerning main steam line safety/relief

~

valve challenges for calendar year 1989 in accordance with the requirements of NUREG 0737, Item II.K.3.3, and as required by WNP-2 Technical Specifications,

~ ~ ~ ~

Administrative Controls section, paragraph 6.9.1.5(b).

FFiF 9TE -

01/30/89-" - HS-RV-18 1

E ~~~

TYPE OF ACTUATION A

PLANT CONDITION REASON FOR ACTUATION REACTOR POWER EEL 6X -

ASSOCIATED 89-002 01/30/89'. - HS-RV-lc A 65 - 89-002 The January'30; 19&9 actuations were in response to a turbine trip - reactor scram transient:

8

~d I 04/29/89 -- HS-RV-lA B D C - - 178$ :

04/29/89 - MS-RV-2A 8 D C ~, 17.8%

04/29/89 - HS-RV-3A 8 D C - . 17.8%

04/29/89 HS-RV-4A 8 D C- 17. 8$ .'-

. 04/29/89 HS-RV-18 8 D C - -',7.&X 04/29/89 -- MS-RV-28 8 D

~

C' 17.&X 04/29/89 -'. HS-RV-38 8 C--; 17. 85', "

04/29/89 HS-RV-48 8 D C .. 17.85 04/29/89 MS-RV-58 8 D C -'.17.85 04/29/89 -- HS-RV-1C 8 D C-- - 17.&X-04/29/89 HS-RV-2C D C'" 17.&X 04/29/89 -- HS-RV-3C 8 D C 17.8$

04/29/89 'S-RV-4C D= C - 17.85 04/29/89 - HS-RV-5C 8 D ~

C - - 17.&X-04/29/89 HS-RV-10 8 D 17.85 04/29/89 HS-RV-2D 8 D C- 17.85 04/29/89 - MS-RV-30 8 D C.- 17.85 04/29/89 -- HS-RV-4D 8 D C-- 17.85-04/29/89 HS-RV-1C C D C-- OX*-

2.2 MAIN STEAM LINE SAFETY/RELIEF VALVE CHALLENGES LContinued) e '

TYPE OF ACTUATION PLANT CONDITION REASON FOR

~E ACTUATION E<<E REACTOR POWER ASSOCIATED C'

04/29/89 MS-RV-48 C 05 04/29/89 HS-RV-28 0$

04/29/89 HS-RV>>38 E

C- 0$ =

04/29/89 MS-RV-58 C ~ Og-04/29/89 -- HS-RV-2C C 0$

04/29/89 HS-RV-18 05 The April 29, -1989 manual actuations were in response to valves being cycled

.to test acoustic monitors. The April'9, 1989 -spring actuations were in response to the valves being "simmered" four times for in-situ setpoint verification testing.

06/26/89 06/26/89

- HS-RV-3A

-- MS-RV-18 C

C The June -26;r- 1989 actuations were in response to the valves C.-

C',

.'. 1 5$

5X being "simmered" two times for in-situ setpoint verification testing.-.-

06/27/89

.06/27/89

-- MS-RV-4'A

- HS-RV-28 C

C C, C..

C C: 15f-1.55

-:The June ,A- 1989 actuations were in response to the valves. being "simmered" two times for in-situ setpoint verification testing.,-

HS-RV-18 8 C C== - 13.0X-

'3.5%

06/28/89

.06/28/89

- MS-RV-40

-- HS-RV-5C 8

8 C

C'6/28/89 C

C C

'3 5$

06/28/89 -= MS-RV-4A 8 C EC. 13. 5X

.06/28/89 -. HS-RV-30 ~ 8 C C 13.5%

06/28/89 - HS-RV-48 8 C 13.5f 06/28/89 MS-RV-4C , 8 C C 13.5%-

06/28/89 . HS-RV-58 '8 ,

C 13.55 06/28/89 - HS-RV-18 8 C C 1'3;5f

,06/28/89 - MS-RV-2C 8 C C- - 135X-06/28/89 -- HS-RV-2A 8 C. C- -- -13 5C-I

~

The June 28, ~ 1989 actuation of MS-RV-18 was in response to the valve being manually actuated,to clear seats and reseat to reduce leakage. The remainder of the June 28, 1989 actuations were in response to the valves being cycled to

~

verify operability and to test the acoustic monitors.

~ ~ ~

r

f h

I 1

K I

1 I

P

~

2.2 MAIN STEAM LINE SAFETY/RELIEF VALVE CHALLENGES (Continued)

TYPE OF PLANT REASON FOR REACTOR 3I

-:gA E"==C Il t ~E ACTUATION

~E CONDITION ACTUATION P ONER E E ASSOCIATED 08/16/89 - HS-RV-5C 8 C C 10K

- The August 16,.1989 actuation was in response to the valve being cycled to test the acoustic monitor.

8'

I

~

. 2.2 MAIN STEAM LINE SAFETY/RELIEF YALVE CHALLENGES (Continued)

T e of Actuation A. Automatic B. Remote Manual C. Spring Plant Condition A. Construction B. Startup or Power Ascension Tests in Progress C. Routine Startup

0. Routine Shutdown E. Steady State Operation F. Load Changes During Routine Operation G. Shutdown (Hot or Cold)

H. Ref uel ing Reason for Actuation A. Overpressure B. AOS or Other Safety System Test e

C.

0. Inadvertent (Accidental/Spurious)

E. Manual Relief NOTES:  : -1) = Remote-.manua1 actuations occurred in supjiort of acoustic monitor

.position indication calibration testTng required by Tecbnica1 Specifications LCO 3/4.4.2.

2) Spring set- testing was performed in accordance with ASME

-Section XI and Technical Specifications requirement in applica-bility paragraph 4.0.5.

-10'-

fl I ~ >t t >'ll'II> I> (s>tt,'. )>>s ~ . I ~ .>is I

~ ts)sl i )

>I I >slit l)s ( ~ )~ ~ tl Its )~ >(>i ( ~

tsar 2.3 SUHHARY OF PLANT OPERATION INCLUDING UNIT SHUTDOWNS/ OMER EDUCTIONS,,

t II >>>is(<It s ( ) t sist

~

I ~

t~~ ~ ( ( ~ ~ ~ ~

ls I ll I')))'

s DATE OUTAGE TYPE GENERATOR OFF-LINE HOURS CAUSE CODE SHUTDOWN>JN HETHOD LER NUHBER SYSTN COHPONENT l

lis

~ s OS

~

lt t I

~

s I t

s ~ s" i' (lt >, 't'>

.A D ACTIO I ( t tl ~

>t(t(

's'

~

s TO PREVENT REC RRENCE.

I i s . >

'(

(*

s (

I

!s

~ ~

. 1/7/89 S 82.9 HC HTEXCH-D The Plant was shut down to correct a condenser tube in-leakage problem.

Repairs were performed and unit returned to service.

1/30/89 F '3.2 . A 3 89-002 EB ELECON The generator tripped at lOOX power due to a fault on an insulator between the main step-up transformers and gen-erator disconnects. The insulator was replaced and inspection/cleaning was performed on remaining insulators prior to startup.

2/2/89 F 10.4 HF ZZZZ Generator was removed from service due to main condenser vacuum problems.

Low vacuum was caused by high conden-sate temperature as a result of cool-'ng tower problems.

>s( (I >ll( > ill I )s> I >ll I" ( I

>i ~ ) (tss 2/18/89 S 0 RB CONROD Reduced power to perform a scheduled control rod sequence exchange.

3/17/89 F I )0 5 89-006 AA ZZZZZ Reduced load due to an engineering

'is> " >t. )If analysis which indicated post loca

~ s>> I s ~ ~ t potential 'integr'dted 'ose rate " to control room personnel through venti-1'ation'ystem would exceed Tech Spec Limitations.'fter additional evalua-tion, errors were discovered in cali-brat ion methodology which alleviated the finding .,of the previous analysis.

i s" s

If If

4&

fl'f f' f i f I>II I' ;I I 0

I I I 11, I I ~ r ~ ~ I f'r ~ I rr I ~ I r I I I f

)f I ~ I. ~

l r ~ ~ << ~ r 2.3

SUMMARY

OF PLANT OPERATION INCLUDING UNIT SHUTDOWNS/POWER REDUCTIONS (Continued)

I fl 'I f f II) II:lf I r Ir

-'lr I r 1 I ~

lE: I" f j

~ I rf fl f.>> ~ f'"

if I i=- .Iflf ff I ~ r>> ~ r f GENERATOR I I fir I r r r OUTAGE OFF-LINE CAUSE SHUTDOWN LER DATE TYPE HOURS CORE HETHOO NUHRER SYSTEH CONPONENT CAUSE AND ACTION TO PREVENT RECURRENCE 4/28/89 S 1456.8 C 1 RC FUELXX The plant was shut down as scheduled thru for the annual refueling and mainte-6/28/89 nance outage.

6/29/89 S 33.5 3 89-028 HECFUN Generator was removed from grid to perform overspeed tests on turbine. A reactor scram occurred prior to com-pletion of tests.

6/30/89 S 31.7 HECFUN Generator was removed from grid to complete overspeed testing of turbine and perform scram time testing.

I 8/6/89 F 59.6 3 89-031 CH TURBIN Reactor scram from lOOX power on Low RPV Level. Initiated by trip of "8" reactor feedwater drive turbine on low lube oil pressure during testing of I ~

f rl I lr j (

r i f I )

~

lr l ll- ~

If~ rl! I ' ll I I l>>r H I backup oil pumps.

8/11/89 F 115 F -

1 89-034 EB ELECON Plant was shut down to resolve and correct electrical fuse coordination f",I r and separation issues on safety-related low voltage motor control

~

r~

~

  • ~

I 'rff'.f ' I f ~

1,

~ ~

I I ~

centers.

"rll I fl' r r<<r r, ~ r I 8/17/89 F 17.3 3 89-035 IA . INSTRU Reactor scram from 67% power due to inadvertent actuation of an RPV Low Level switch dur'ing execution of a Tech Spec Surveillance.

1 ir< ~ I, I r r j-0

~ ~

}>>lT }

T i iiu <)E I ' il' r; I i I II(II >> -' I < I' iii'I i l.:iii 2.3 SU MARY OF PLANT OPERATION INCLUDING UNIT SHUTDOWNS/POWER REDUCTIONS (Continued) n ij}

Ii j i ~

j , }, Ii i, GENERATOR II i)

OUTAGE i OFF-LINE CAUSE SjHUTDOWN LER i}P< i DATE TYPE I HOURS CODE .NETIIOD NUHDER SYSTEN D PONENT CAUSE AND ACTION TO PREVENT RECURRENCE i

9/21/89 F 29 A 1 HC

}(i 4 HTEXCH-D Plant was manually shut down because i>>lhi of rapidly increasing conductivity due to condenser tube in-leakage. Two damaged tubes were plugged and plant remained .down for repair of steam extraction lines.

9/22/89 S 167.2 H3 PIPEXX-E Plant remained down for repair/

replacement of two failed steam extraction line expansion bellows and condenser baffle repair. After com-pletion of repair to all damaged components, the plant was returned to service.

10/23/89 S '0 RB CONROD Reduced power to perform a scheduled control rod sequence exchange.

12/12/89 S 1 0

I ~

.Ii <., j ~

IHr I .I<I I t <5O<} iijil j<j'ili III( '"'CONROD """Red'uc'e'd 'PoQer'operform a control rod sequence exchange.

TOTAL GENERATOR OFF-LINE'OURS CAUSE 'CODE 'TOTAL FOR '1'989 j r I ~ j '- ~ j< I j II I ~ j ~ I I ~

A 5 411.9 8  ? 65.2'456.8 C 1 D 0 0 F 1 115.0 G 1 17.3 H 5 10.4

-TOTAL 2076.6

II f

(

0

2.3 SINHARY OF PLANT OPERATION INCLUDING UNIT SHUZDDMNS/PSKR REDUCTIONS (Continued)

SINSNY OF CODES SYSTEH OUTAGE TYPE CAUSE CODE SHUTDOMN HETHOD CODE SYSTEM DESCRIPTION F - Forced A Equipment Failure l Hanual AA Air Conditioning, Heating, Cooling 4 Ventilation Controls S Scheduled B Haintenance or Test 2 Hanual Scram CH Feedwater Systems 4 Controls C Refueling 3 Auto Scram EB AC Onsite Power Systems 4 Controls D Regulatory Restriction 4 Continued HA Turbine Generator 8, Controls E External Cause 5 Reduced Load HC Hain Condenser Systems !L Controls F - Administration 9 - Other, HF Circulating Mater Systems 4 Controls G - Personnel Error Other N Other Features of Steam 4 Power Conversion H Systems (not included elsewhere)

IA Reactor Trip Systems RB Reactivity Control Systems RC Reactor Core

~

J>>>>l ~ l>~>f i~ >' >>>> - > l>(l> ~ > >f >> t I

I~- > I

>l > *>> I>= I (~

i>> ( I l >I)

~

~ t> i>

2.3 SUHHARY OF PLANT OPERATION INCLUDING UNIT SHUTOQSS/POWER REDUCTIONS (Continued)

SUHHARY OF COHPONENI'ODES COHPONENT l'YPE COHPONENT TYPE COHPONENT TYPE/CODE INCLUDES: COHPONENT TYPE/CODE INCLUDES:

Control Rod Drive Control Rod Drive Hechanism Pipes, Fittings Pipes Hechanism (CONROD) (PIPEXX) Fittings Electrical Conductors Bus Turbines Steam Turbines (ELECON) Cable (TURBIN) Gas Turbines

.Hire Hydro Turbines Codes Not Applicable Fuel Elements (zczzz)

(FUELXX)

Neat Exchangers Condensers (NTEXCH) Coolers Evaporators Regenerative Heat Exchangers Steam Ge'nerators Fan Coil Units Instrumentation and Controllers Controls (INSTRU) Sensors/Detectors/Elements Indicators Differentials lntegrators (Totalizers)

Power Supplies Recorders Switches Transmitters .. g

~

/~ ~ > I ~ ~ > I ~

Computation Hoduies'echanical

- Hechanical Function Units Controllers (HECFUN) . Governors Gear Boxes

'aridrives Couplings

> ~ ~ ~

1>> <,~ ',~ ilia( 0 I -I

> ~ ~

~ ~ I $ I I I i I ml ~ ~ s

[

<I >,l i)l 4i,i 2.4 SIGNIFICAN MAINTENANCE PERFORMED ON SAFETY RELATED E UIPMEN EQUIPMENT REQUIRiNG PROBLEM MAINTENANCE S STE DESCRI ION CAUSE AC ION TAKE E-C1-1 DC Power System During performance of Silicon Control Replaced SCR Battery Charger weekly surveillance, Rectifier (SCR) firing board with Division I 125 Volt firing board was new like board.

battery charger would found defective. Performed not develop required operability test voltage. and verified charger operated proper ly.

E-C1-2 DC Power System While working in the Defective silicone Replaced damaged Battery Charger area, an electrician card. Rectifier firing board with noticed that the charger caused damage to same. Replaced was making an unusual firing board. defective silicone noise (with the Plant in card rectifier normal operation). with same.

DSA-C-1C HPCS Power- Nhile performing Previous installation Replaced unloader Diesel Starting preventive maintenance or repair had valve and Air (DSA)

" 'C'oV4"S+8$

on DSA diesel '"'

High Pressure

" apparently over't'ightened 'va I v'e " discharge valve with same.

during Plant and fitting resulting it

'enerator I

operation, was noted in cracking.

~

that 'the'unloader valve fitting and'ischarge ~ ~

valve were damaged.

I I

J V c 5 mr

ji << I, I III> ~

I 1),. "I ) ,, I,,I <

b0

< ~ )< )

) e ~ <)) ) II << <<I'<I< I j ) >) <

'J ) 1 'I/<

~ I << I 1>> ~

j'<)u1 I ~

) I<Is< I< )))

2 4 SIGNI ICAN AI ENA4CE PERFORMED -

SAFET RELATED E UIP ENT co tinued EQUIPHENT I )) 1< '.- f.<<>>).l 1.<<-)',I REQUIRING HAINTENANCE SYSTE PIIOBL'N' OCSCRIPTION '. CAUSE ACTION TAKEN DSA-C-'2C HPCS Power- While on tour, an Condensation in the Replaced the Diesel Starting operator noticed air line from the after suction and Air (DSA) leaking from the air cooler caused rust discharge valves intake on the backup and corrosion on the with same type.

starting ai.r. compr essor valve seats, which Verified for the'PCS diesel created a leak path. compressor generator DG-1C. operation.

CRD-CB-PlA Control Rod With the reactor. in Hode Racking mechanism Replaced broken Drive 1 at a 100 percent broke probably due to racking mechanism power, the racking wearout. with same type new mechanism was found- racking mechanism.

broke for the 4160 Volt Torqued hold-down circuit breaker. This bolts to 41 was discovered while ft/lbf. Observed attempting to return the racking in and Control Rod Drive "A" to verified pump service after repairing motor operated.

a minor seal leak.

RCIC-42-S21ASC 'eact'o'r"Core II)I'solation

'Wl'<le tkddbl 6 I shobti'rig 1

failure of the RCIC

'<'he Cab's'e 'u'n'kn'o'w'n" probably wearout.

,t Replaced undervoltage Cooling minimum flow return y'clay. Tested

)~

valve It8"the Suppression satisfactorily. *))

) ()<"

Poh't to"op'e'n"br to ~,< I <<

close, an undervoltage I-)

)i <<< I ~

'r'elegy in the valve motor

~ ... ~

I<,. ',

starter was'ound'burned I I ~ I I up." 'The'robl'em was identified 'during'OVATS test'ing.'

>0 f

~<< C7 I-

<<1 ~ ~ ~ ~ << ~ 1 ~ <<<<<< <<

2.4 -

SIGNI CAN H IN ENANCE PER ORHED ON SAFET E ATED E UIPHEN cont n ed EQUIPHENT REQUIRING PROBLEH AINTENANCE SYSTE DESCRI TION CAUSE C ION AKEN RPS-EPA-3D Reactor During performance of- Cause of failure Replaced the Protection surveillance channel traced to defective circuit board with System functional test, a circuit board. Cause the same type.

failure occurred in the of defective circuit Hodification undervoltage trip board is unknown. request issued to functional check for the request new design Reactor Protection of circuit boards System electrical to be implemented protection assembly. at next scheduled The undervoltage trip outage.

has a setpoint of 110.7 to 108.5 Volts and an allowable value of 108 Volts. The undervoltage trip occurred at 50.1 volts.

E-IN-2 Instrument AC An attempt to switch Synchronize input not Burnished contacts critical instrument being transmitted to functionally Power Supply Inverters i >e, < ii I power inyerter (Qggrter""woul'di nest synchronize or transfer showed

i I > 'i logic due to dirty cont'acts"dn"K7'relay'.

and tested unit.

i~i" Ii <<<<i (li forward.

=

I il silt. i,ii I ~ <<

<< 'g f < I If sir<<<< ~ <<i

/i

( i<<<< I<< ~l <<j ~ << i I

<< I <<<<> i I ) ) )I

i. ~ ~

t

~

~ <<<<

<<<< ~ << <<

i

f 11

S GNI ICA A ENANCE ERFORMED 0 SAFE RELA ED UI ENT co ti ued EQUIPMENT REQUIRING PROBLEM MAINTENANCE S S E DESCRI TION CAUSE ACTION AKE E-IN-3 Instrument AC Fuses to Division I Static switch logic Replaced static Power Supply critical instrument board (piece part of switch gate firing Inverters Power blew resulted in the inverter) was module with same tripping inverter unit found conducting one- and tested to alternate power half of load amps functional.

source and giving from the inverter and inverter trouble alarm. one-half from Fuses have blown alternate'power repeatedly. supply due to faulty static switch gate firing module. This failure was due to wearout and aging.

SGT-ESH-IA Standby Gas The electric strip The heater wire where Replaced shorted Treatment heater bank "A" Standby 2A on the it connects to the heaters with spare Gas heaters had frayed heaters. Taped Treatment train low insulation causing frayed insulation temperature alarm would the wire to short test pot clear. Pnnunciation against the,)eater

"' satisfactorily.

f'kemper'atur'e's'n'hain "b'okcover"."

I  !' l' Control Room.

II f ]

il

)

ll)g I }I

~

~ ~

~

1

)v l

~ I) 1))

1)) ) ~ - ~ l ~ ) ~ I 1

2 SIGNI CA HA E A CE E FOR EOON S FE ELA EO UI EN co t ued I ) ~ 1 ) ~

) l)( ) 1 1.1 IJ ~ )

EQUIPHENT REQUIRING PROBLEM HAI ENANC S STE OESCRIP ON CAUSE C ION AKEN RHR-P-2B ~ Residual Heat Information was received Cause of loose bolts Retorqued the Removal - Low that the Residual Heat on the RHR pump was bolts on RHR pump Pressure Removal (RHR) pumps at attributed to No. 2'o Injection LIHERIC experienced probable thermal specification.

loosening of pump hold .cycling causing the Initiated down bolts. WNP-2 found bolts .to relax. preventive one RHR pump which had maintenance hold down bolts that did measures to verify not meet specifications. adequate torquing on hold down bolts on all emergency core cooling systems.

CD RRC-P-lA Reactor An attempt to run The position switch Inserted spacers Recirculation Reactor Recirculation on the flow control between limit pump "A" at 60 Hertz was valve permissive. switch mounting unsuccessful. .The pump input to pump 60 bracket and limit was running at 15 Hertz Hertz logic was not switches.

at the 11),') -I/ I l(( ill l time..

I))'ll) I~ 1)lf ) ,, paking, up, y)th valve" Replaced mounting

'l ) '

11 1 g

~

1 1 l ) 1 1 1 in'losed'osition. 'bolts with longer

,1))), )'

bolts to provide sufficient thread eppagemept, to prevent bracket 11)l)l>> I) l' loosening...

/ ) ,PeI'formed, yol tage 1 1 check to verify

'ropep operability.'

  • ~P "! ,I l S G CANT HAI E ANCE PE ORHED 0 SA E ELA ED. E UI HE cont ued EQUI PHENT REQUIRING PROBLEH HAI TENA CE SSEH ESCRIP ION CAUS AC 0 TAKEN HS-RLY-K81D Hain Steam Hanual isolation relay Normal wear expected Replaced with exhibited excessive in GE "HFA" relays. rebuilt relay.

noise when running. Removed relay to be rebuilt and reused.

RCIC-DT-1 Reactor Core Check of suspected Carbon glands carbon Isolation Cooling leakage on inboard gland seal showed leakage in the interface area degraded.

'eplaced Sealant between gland seal housing and casing glands . Removed old sealant and applied tempfl ex between turbine casing halves showed wear joining compound .

and gland seal upper and deterioration. Performed in-housing. servi ce leak test .

RFM-DT-1B Reactor During unrelated Infra-red examination The check valve Feedwater maintenance on Reactor of hydraulic trip was replaced with Feedwater Pump '"B", oil assembly piping the same type.

was observed leaking in showed leak through Visual inspection the vicinity of the of the in-line check of the hydraulic

)ifdraul)c trip assembly.

valve probablg, due to trip assembly was wea'r'out.' 'p'erformed to

>II I - I I) I verify no leakage; I "

i>fs

I" f I t,

f h

l

2 SIG ICA HAI ANCE PERFORMED ON SAFE Y RE ATED E UI HEN co t fv ~

ued

~

~

(.

~jv I I,v v, ~

vvj~

EQUIPHENT REQUIRING PROBLEH HAIN ENANCE S S DESC P ION CAUSE ACTIO AKE CRD-FCV-2A Control Rod During routine The reason for flow Replaced faulty Drive observation, the oscillations was valve positioner indicated flow through attributed to a with spare.

the Control Rod Drive faulty valve Recalibrated valve flow controller valve 2A positioner. The and tested was observed,to be cause of faulty valve satisfactorily.

oscillating between 5 positioner was normal and 10 gpm when the wear..

controller was in automatic.

HS-V-28A Hain Steam Hain Steam Isolation Leak by main body The main body seat Valve 28A failed locaj seat due to surface was machined The leak rate test. imperfections. valve was retested and leakage was acceptable.

PSR-V-X77A/1 Post-Accident Containment isolation Cause unknown. Valve was PSR-V-X77A/2 Sampling valve for post-accident Probably due to valve disassembled and Radioactive

"" ' ' " sampling system

" 'l'6Lil 'le'ak" rath failed

'test'in(.'

disc

/~I f 4)I )1 wear.

v v ~ 'v/t(,I /l/

inspected. Hating

'surfaces were lapped to remove I

v ~ v minor rough spots I I )Iv( I ll and burrs. Valve I ll wa'scasse'mbl ed and leak tested

)< ~ ~

v ~

I I tv ) v) t v ~

satisfactorily.

~ 'v vv I I

~ ~

vl'

I>> j>>lrl>> 1 ~ r 1 Irl "- I 1 I ~ (,I I >>

~ II -1 I l>>p>> ~

r I ~ I ~

=(( I j 1 r ~

p(p .p pj>

~ ( I I ' .1 pjrplr ~ II >>

~ I" ( (>>I 1 ~ 'l(r>> Ir r Ipr ~ lp I {ir ~

I ll'>>

2 SIGN>>F1 CAN HAI E>>tANN ERFORHED 0 SAfE ELAEDEUIP ' s I E o t ued I P

~

EQUIPMENT REQUIRING PROBLEM p ~

(p

~ rr

~

~ ~

1

'- (

~

j. ~ .rp I I~ ~ P 1

1 j>>

I I r r I I" 1 I, .

~

MAINTENANCE SYSTE DESCRIP IO "'CAUSE 0 K RFW-V-10B Reactor During local leak rate The Stillman EP soft Replaced the Feedwater surveillance testing,'he seat seal had Stillman EP soft reactor feedwater excessive wear. seat seal.

swing check valve 108 Established four would not seal. year equipment qualification schedule for soft seal replacement.

RFW-V-65A Reactor During performance of Valve seat and disc Valve seat and Feedwater local leak rate testing, scratched due to disc lapped.

Reactor Feedwater supply unknown causes. Valve repacked and isolation valve showed torqued. Local excessive leakage. leak rate test performed satisfactorily.

SW-V-165B Standby Service Normal observation found Normal seat wear. Replaced seat and Water

'" ""' the 18-inch spray. pond "B" ring by-bass valve

'""'I'eikirig'6y'thj(,'e'at."' 1 l I jj ( ( (1 1 ~ ll 1 1 ( 1 j(

thrust collar.

Valve tested SW-V-'21'4"' 'tandby Service During surveillance testin'j'8f'"A" Standby Service Water Valve was Water emergency valve which supplies temporarily diesel g'ener'ator, engine co'o'I'in'g water to re'mov'ed tripped on high diesel engine heat and from'ervice

't'emp'erature'. .fatl'ed xchanger re'p)aced 4ith a 1

due to'disc to'pen spool'iece until

.separating from stem, a n'w valve can be most likely due to purchased and wearout. ins'tailed.

~, I

I'

)Ij)-r l l ~ 'l . ~, )

( )-:,)I. ~

I (l) l ( l I.'

)I rj I '()) ~ ) ( ') l (l

~')( f r (ll(. .'

2 4 S G C AI ENA C ER OR EOON SAF EL EO E UIPMEN co t n ed

~

(l r,l r)

~

l I

ir EQUIPHENT l ((l~

((r (l ~

l ) ( ~

- I ) ~

REQUIRING PROBLEM I ENANCE S STE OESCRI ON CAUSE "A'C '0 AKEN H

.SM-V-220A Standby Service Attempted to operate Broken stem nut and Replaced stem nut Mater Standby Service Mater lock nut resulted in and lock nut.

makeup valve to "A" stem assembly failure Valve retested diesel engine cooling and valve could not satisfactorily.

water . Valve would not be operated.

operate.

HPCS-MO-15 High Pressure During surveillance The worm shaft clutch Replaced entire Core Spray testing, Suppression gear assembly fell clutch assembly Pool suction valve would apart due to missing and worm shaft.

not operate via the split spacer which Revised procedures motor. Hotor ran, but acts as a seat for to inspect valve would not move. shaft set screws. assembly and re-The spacer was not stake set screws installed during if required.

manufacturing. Notified Limitorque of possible quality control

( ~,)(( ( ~ I j' (()ll )t((((( l j (l' f'll (} ((l ('( ( jl ( '(fl I( ' f ( I ( I / ))

d( ficiencies

" '4CFR

'(CFR Part P t 21 (ll,l )l) Report). Verified

~; I ll ( (

r)(jl operability of all

~ r, ~

l( "() ( I ) ((

'l l j safety related

( (

valves wi'th

~

I) 'I ) ) I(. )( rrj ~ ))ll Limitorque motor

'op'orator's of I - I(

I similar design

~

I, du< ing refueling outage.

I I ) () I l I i) ~ =

@ )

V 0

f II .i ~

, I') ) I< f ~

) ~

I ) .)f !t, i

~i) fl )) ~ I.) I I )~ -)ll" .

2 .SG CA INTE ANCE PERFORMED ON'SAFE ie[ll i I I "yl)

Y EL ED E UI E co t ue EQUIPHENT REQUIRING PROBLEH INTE ANCE S S E DESCR P ION CAUSE AC ION AKEN LPCS-HO-12 Low Pressure During performance of Limit switches on the Limit switches Core Spray the annual stroke. times valve operator, Rotor were adjusted to were found out of surveillance on the Low close at .5% open.

Pressure Core Spray adjustment. Cause of Valve functionally System, valve operator adjustment problem tested 012 indicated closed- was unknown. satisfactorily.

with 3500 gpm through the valve.

RC IC-HO-8 Reactor Core Reactor Core Isolation Limit switch 816 Adjusted limit Isolation Cooling turbine steam found closed and switch and Cooling supply valve trips rotor locked due to verified it opened overloads when operated. attempting to stroke during valve valve closed when it closing.

was 98% closed.

RFM-HO-112B Reactor During surveillance Rotors 1 and 2 on Adjusted rotors to Feedwater . test, motor operator for valve position limit actuate as Reactor Feedwater high switches were out. required to

" '4'gtlet'Aolationivalge pressure heater 6B

<<I I I' <

I)

' ' ) I " <<)

of'djustment.

properly open and

'close valve. The blew all three line valve was retested sy)ff I;)

s i]I -

fuses during open satisfactorily.

,I stroke;"'Valve remained 1

)/ ~ ~

(j );

in 'par ti'al'1'y'open ()>>,s position. The Plant was operating't. 71% power. l) I ) )(g p

'I ~ a

) ( i l <gi  ! p II

I:)

0 I! c'<tl<'I

< r<

SIGNI ICAN

~

H I)l< I NTE AflC I lr

'}~

PE I I

~ <i<i ~ I I

}<} i y ORH D 0 S

i'4

~C RELA llr<!

C

<}

}<<

I -.<

I.C O'E UIPHEN I

I I I l<< ~

~ <

'}Ir<

co t II. <<c ed I<! c ~

} (<Ii}<<c <<r I c

} }1*iI IIi<c }<<<I I EQUIPHENT r << II I }<I ) } I

                                                                 ~        ~                          <

REQUIRING HAIN ENANCE SYS E D SCRI ION CAUSE C IO AKE SW-HO-2A Standby Service After routine start of Valve operator had Valve operator Water Standby Service Water . broken worm gear and worm gear and "A" pump, it was noted associated gear associated gearing that outlet valve was damage due to was repaired. indicating intermediate essentially no grease Valve was returned open position. Valve in gear case. to service and was found 30 percent functionally open. Operator on tour tested. Five was directed to manually other valves were open valve to 100 inspected in the percent. Standby Service Water System to verify proper

                                                                                                                                                                                         'ubrication.

SW-HO-4B Standby Service During 'surveil1 ance Rotor Ol did not move number 1 Water testing, Standby'Service when valve closed. rotor to open with Mater inlet valve to handwheel 3.5 diesel generator 82 blew turns off of a fuse in one of the seated position.

                                       ')hike li663"dkt iiIII.'ttte '                                    I<) l h       i}     'I'I) ) ]ll l I I      }

cover.'djusted

                                                                                                                                            } }               "
                                                                                                                                                                "Tempted       for proper close cycle.                                                                                                             operability.
     <<I:i ll'II SW-HO-'44"'"     Standby Service         Whfle"attem)ting to                                                  Hotor leads Tl and T3                               The'ires           were Water'. "

C" opki ate St'a'n8by Service we9e" n'i eked by splic'ed an'd Tl was

                           'C Water supply valve to improper installation                  relugged.
                                                                                                                                                                  /! I L'6w'ressure Cote'pray                                               of     motor
                                                                                                                                                                       ~

r room'cooler; 'al've would not operate'lectrically ahd smoke was observed at'the valve operator. r ~

I I

2 SIG CANT N E ANCE ERFORHE ON SA E REL ED E UIPMEN cont ued EQUIPHENT REQUIRING PROBLEH AINTENANCE SSE DESC I TIO CAUSE C ION TAKEN SGT-ESH-1A Standby Gas The electric strip. The heater wire where Replaced shorted SGT-ESH-2A Treatment heater low temperature it connects to the heaters with spare alarms would not clear. heaters had frayed heaters. Taped Annunciation of insulation causing frayed insulation temperature is in the the wire to short test Hain Control Room. against the heater satisfactorily. box cover. DCM-TS-12Al Diesel Cooling During the Spring Unknown-Probably Replaced and Mater refueling outage, while wearout. tested temperature testing the 1A Emergency sensing switch. Diesel Generator, the Diesel Cooling Mater Temperature Sensing Element was found leaking. (((((I ( 't l !(((tl(t~(lt l i(( l>>l((i i( i ll >(I I; l>ilhlIi( (((t((l "<<(( ( (" 'l

                                                                                   ~ ((li~

(

g

                                                    'CQ
                                         ~
                                           ) <<))u ) ~, i       l i)<< e ~   l<) l < I~ I I)l <))l I)i< ) <<i<)) I I I'< .l) I <)< )'<    '    <"

I < ),< 2.4 SIGNIFICAN INTENANCE ERFORNED.O SAF RELATED E UIPHEN co tinued EQUIPHENT REQUIRING PROBLEN HAINTENANCE SYS EN DESCRIPTION CAUSE ACTION T KE LD-TS-619B Leak Detection Mith the plant operating Replaced the routine observation temperature trip unit found the output relay 619B on the leak chattering on detection system on temperature trip unit the main steam line 619B of the leak to the turbine detection system on the building. main steam line to the turbine building. Contacts on the temperature switch were worn due to normal wear. HS-LIS-24B . Hain Steam During performance of Contacts on the Changed wiring to HS-LIS-24D System the monthly 'surveillance switch were worn due use a spare test in the normal to normal wear. switch. Performed operating mode the level. surveillance indicating switches testing. (LIS) would not trip as )<i i bl j () l <i)llI ill l<l Vequir'eg" 'Thyme 'gwi tche's

    <)-'<'l) l'I                           provide input to the
  • Reactor Protection I

System'."" " I>> l )I <ll

                           ) ~ ~

ill) l), I<l ~ l .-" ) ))l'a) ) i I~ ~ Ilsuil st !i'I,) s,, I

2. -S G I CA INTENANCE E FDRilED'5N SAFE q ~

Y REL ED E UI NEN co t ue'd yr is sl Ia i(i as ~ Ill,i . I EQUIPHENT REQUIRING PROBLEH HA NTENANCE 'YS EH DESCRIP ION CAUSE AC IO AK HS-LIS-31C Hain Steam During the Spring These switches have a Replaced switch System Refueling Outage while history of failure with the same performing surveillance due to age. type. testing on Reactor Low Level 2 it was noted that the level

                                                           'ndicating switch (LIS) had considerable bounce.

HS-LIS-37A Hain Steam During the Spring The microswitch in Replaced and System Refueling Outage while the Level Indicating tested the micro filling the reactor Switch (LIS) was not switch. vessel level trip unit functioning properly exhibited considerable causing excessive bounce. movement. Probable cause is normal wear. HS-RIS-6IOD Radiat)on,

                                  'onito'ri'ng'     ' e,     Dur)ng,ge perforpanre,
                                                      '"'o'4"rotitiiie'serve'))lance The swltc re's'e't diie would not     Removed to'ormal 'drawer and defective
                   ' II I                                    testing with the plant                                  aging and         cyclic          replaced with the i I la s
              .r           1 I'-/I at power, the                  main steam               fatigue.                          same  type spare I        II Ig I    ~ s (HS)      'line ',r',ad,iation                                  hll                     dt aper, monitor (RIS)'hannel                                         <

Su'rveillance test

                                                             ,"D" downscale and                                                                       performed.

sl Re'p6'tpr Prot'ect'ion,, ~, I Sys'em tr'ips woul'd'no't clear. I I ~

                                                                 '    ~

0

                                           ]}}}iaa} } l,)}i        i    I-.. i"! ll                } i '>> x i'   ~
                                          }I        l
                                                       '.} I                                           I, >>!           i" i }. j}             !          l        I lii!'t i~
                                                       ~   l (!<'    !

l

                                                                                                                                                          !   ',    }

l }}ll!l } liig} } is) <I ~ i ~ ~ s ~ SIG IF CAN AI E A LE E ORI}ED'0 S I:E RELA E E UIPHEN cont nue ialiil e }i EQUI PHENT REQUIRING PROBLEN MAINTENANCE SSE ESCRI IO CAUSE C IO AKE RHR-PS-16A Residual Heat Mith the plant operating Cause unknown- Replaced pressure Removal normal observation probably wearout. switch with like revealed the Residual kind and performed Heat Removal (RHR) test. Pressure Switch (PS) which is an Automatic Depressurization System (ADS) permissive failed. SGT-TS-2A11 Standby Gas Mith the plant at power, Contacts for the Treatment the annunciator for a temperature switch temperature switch carbon adsorber strip (TS) showed open at and performed a heater low temperature ambient temperature.wearout.'eplaced satisfactory test. on the standby gas Cause most 'likely due treatment system came on to age or and stayed in. The strip heater would not heat. SLC-LS-600 'tandby'Li'qu'id ' ""'Ah'll'e 'pei'for'll}jhg'la ' tab'sQ 'i's'u'n'k'n'own'. 'Replaced level

    }~}'~ ~'}!    Control                                             test, with       'urveillance wearout of 'robably indicator and the plant operating at                                        Level Switch (LS).                     level switch.
      }.'i } }~-                         power",'the'Standby                                                                                  Completed Li)kaid Cont'r'o'I (SLC)                                                                             su'rveillance'test.

tank level indicating

                                        'met'er'-        was'tickihg
                                                 'seal'e.

at'id i I I i I

4 S G CA T NTE A CE OR ED 0 S E E A EO E UIPHEN continued EQUIPHENT REQUIRING PROBLEH AINTENA CE SSEH DESCRI T ON CAUSE AC ON AKEN SW-PS-1A Standby Service During Spring Refueling This was caused by a Replaced pressure Water Outage, while performing ruptured tube most switch and preventative maintenance likely caused by performed test. on the Service Water wearout. Pump the pump discharge pressure switch was found to be full of water. RFM-LIC-620 Reactor With the plant at power, The meter had an Replaced the Level Feedwater during routine "open" in the Indicating observation of the circuit. Cause was Controller (LIC) Reactor Feedwater (RFW) unknown. and performed startup valve Level satisfactory Indicating Controller retest. (LIC) meter went to zero when "tapped" by

                    ~ <:( '         fi'ngers. The performance of the system was igngffycted     (.'>l l
          ~

( 1'

A 4 1

(()> ~;t*l I.(1

                                                               ~r
                                                                                        =        I        I} !gal        }.> ~                     1>.ttl      '       '>1         Il trt(   I                      (g            I I

0 1 (%(> 1 ( ~

                                                                                                                                                                                                                      >I>t>                    ~ ~ (%

( ((,( }

                                             !( l .I (}                                                                                                        I I I'i>l(

1 ~

                                                                     >1>                                                                                            1
                                                                                                                                                                         ~  I 1

A ( i 1

                                                                            '(((((

1 fl(I( "( ~,(! 1 ( I ( 1 t>I ~ (>(1 ' ~ ~ 1 l((i (>>(l t>l ](!1(t(,I >> /I( }II 1 1%%. > ~ I ~ ~ SIGN C N AI A FE ( ~ % ~ Ek ORMED 0 SA E Il (lt i ( ( l(l l(I(

                                                                                   > ~

ED E U PHEN co t e I'ELA

                                             -!(II          (ii(   1 $>     I           1 EQUIPHENT                                                                             Ij>%}lit'ROBLEH REQUIRING A NTE ANCE           S S  E              1"(IDE'<CRI Ii '

0 '( '(I CAUSE 'AC IO AK HS-TR-614 Hain Steam While performing Found a loose Tightened loose surveillance testing of connection on the connection and the Hain Steam (HS) switch which actuates completed the Relief Valve Discharge the annunciation. surveillance test. Temperature Recorder (TR), with the plant at power, it was noted the I CAH operated alarm switch actuated but the control room alarm did not annunciate. HS-RIS-610B Radiation During a surveillance The radiation monitor Replaced drawer Honitoring test, with the plant at . drawer circuit was with a spare and FO I power, Hain Steam (HS) open. This was most performed ( Line Radiation likely due to age. satisfactory test. Indicating Switch (RIS) would not calibrate. DLO-H-P/2A2 Diesel((L1jbe.Oil}( }DOHng'r'Uutiiid( "'1 '(1 ( " 1Thh( 'so'ak'b'a'ck((pump " 'Replaced pump with. the 'bservation, a broken shear

                                                                                                                                                                                                              'ad motor coupling and
     <<(((((   '( }11                         plant operating at                                                                                  rpin on the motor                                                   shaft shear pin
      ~

(I( > I((( power',("it 'was found that shaft. Failure and returned to (' I( thd(}motor'o'p6rating the appe'ared to be normal r, I soak back pump

                                            'diehel( geherator engine 82'n'the-stahdbg for AC wear.

1 ~ '-I'%.' (.I

                                                                                                                                                                           -~     % ~ ~ ~

ser0ice."'% pbweY system was 'running but the'impeller has not ~ I~ turning."'I r I

h I

                                       ~ ',                  (I(!1   lii i
                                                                         ~      (i   ~

I >>i i } . IIl lI ! 'il !( (>> I I l

                                                               }   ~        I                                I~                    ~
                                                             } }lI    II   (    ll     (        (               l ill              Itl }I            '>> ~ ~

( I 11!}lli le! (

                                                                                         ~

l(s, ( Ie l>> (l il l ll l }>> GNI C N I E>>IA EE P RFOR EO'0 S A f3 E U E co 't ue I EQUIPHENT REQUIRING PROBLEH HAIN NA C S STE ESCR T ON CAUSE C 0 KE DLO-H-P/6 Diesel Lube Oil The motor driven oil The vibration was Replaced motor pump (P/6) on the High caused by a bearing with like kind. Pressure'ore Spray failure caused by the Diesel was observed to previous failure of have high vibration. the pump to motor coupling.. RCIC-H-P/3 Reactor Core The Reactor Core The pump motor shaft Realigned Pump and Isolation Isolation Cooling (RCIC) = was out of alignment. replaced motor Cooling water leg pump was bearings, observed running noisy and vibrating. RPS-H-HG) Reactor A loss of power was A motor bearing on Replaced motor Protection experienced on Reactor the motor-generator with spare and Protection System (RPS) set (RPS-HG-1) failed tested. bus IIAII~ probably due to normal wear.

                         ~

I ll l(! II I >>li ~ I" l!l I '}l>>}(( } j ( (l( (>>('(}} }l (i(} fl! I I l I! Ii(( (I l Il>>((>>,l(.'l(

                                                                                                                              }                                   t,            (i DLO-P-10                    Diesel Lube Oil                  During normal                                                     A    motor brush was                            Replaced motor I (i(! I >> I "l (I (
                  >>II observation                         it    was noted               excessively worn                                with spare and l

the }}}5'diesel generator causing reduced brush tested ( lu58 oil"soak'ack pump te'ns'ion which sal't)sfactorily. would trip on overload. resulted in brush to Ii, (I

                                                                                                  ~
                                                                                                    ~
                                                                                                      ',    'i   I, 2'ommutator'arcing.

I N

f l II I t P

                                                                                                                     'ill
                                                                                                                                                               ~ a ~

I ) i li ~ 'I

                                                                                                                       .,ol '
                                                                                                                                   )
                                                                                                                                   )
                                                                                                                                         " ~ \'I         l i,     I         I~ ~
                                                                                                                                     ~ I
                    .4  SIG     I     C N       AIN NA           CE         ERFORHEO            0      S FE        EL        EO E U           EN   cont e EQUIPHENT REQUIRING                                                             PROBLEM HAIN ENANCE             S S        H                            DESCRIPT ON                                              CAUSE                               C      IO       AKEN RCC-P-18              Reactor Building                      An      operator on tour                                 The cause was unknown               Bearing was Closed Cooling                        noted the outboard                                       but thought to be                   replaced.

on Reactor 'earing excessive lubrication Building Closed Cooling or expected end of (RCC) Pump "1B" was life for the bearing. running hot. RFW-P-1B Reactor During retest of the The inboard oil seal Replaced bearing Feedwater Reactor Feedwater Pump ring had been and associated oil 1B (RFW-P-1B) following improperly installed seal ring. maintenance the thrust and caused uneven bearing overheated. loading on the bearing. RFM-P-18

             .                                             'With the               plant at power                  .A small            orifice that. Bearing was a    high vibration alarm                                admits         oil to the           replaced and was received on Reactor                                  thrust bearing               was    lubrication
                                                 '         Feed.I Pump 4~ I           I 1B;(RFM-P-IB)

I Tfle drained. The

                                                                                                                caUs'e ff of the plugging" procedure was
                                        ~
                          ~ <
                              / ( ( J c   < >      I I 1 I            ~

f believed to be changed to require

  !>>~'< ~ ('il                                                                                                      was filter particles                   draining prior to
             / I I!                                                     (

I <>III t I

                                                                                      >>~ il caused by              filter       filter,changeout.

ch'a'ngeout. I I ~ I /I l <<,i('. lt ~

                                                                                                                      ~ ~     (

I

                                                             1
                                                                   'L I                     I  (      I

2.5 INOICATIONS OF FAILEO FUEL INTROOUCTION In accordance -with the commitment and requirements described in the MNP-2 = FSAR, Section 4.2.4.3, a visual inspection of discharged fuel from MNP-2, Cycle 4 was'erformed on October 5-10, 1989. The purpose of -the inspection was to= veri fy assembly and fuel rod structural.- integri ty. In addition, although . not. a commitment, a visual inspection of -selected discharged fuel channels was performed at the same time.

SUMMARY

OF INSPECTION RESULTS A. total of ten- assemblies and two channels discharged at the end of cycle 4 were inspected: No evidence of mechanical damage, geometric distortion or rod

             -;-.bow were observed.                All rods inspected appeared properly seated in the lower
                   ,   tie;plate. All: spacers appeared to be in proper position. The fuel exhibited nodular corrosion which covered portions of the clad: on fuel rods which were cleaned for =-.inspection.       The extent of coverage did sot .appear to be markedly changed from= previous inspections although some 'instances""of clad surface
    .-     .       :roughness .-were observed on profile. The assemblies.; uncleaned, generally
                     ~

conformed to-.General Electric (G.E.) visual standard,-2. However, in the

== .single instance where a fuel rod was cleaned of .surface crud, the observed
       .      ~

nodular= corrosion was substantially less than the 100$ coverage associated

                  . with visual         standard 2. Based on comparisons, with end of cycle 3 fuel,                    it appears that-.nodular corrosion is          still   taking place=.but the rate of growth appears to be low.

l' Fretting marks . appeared on several assemblies, particularly in the span 6 region. (See Results. of Fuel Examination. section-for span location defini-

                 -,tion). Investigation as to the cause of the
     --:- determined that they are caused by contact with scratches                               in. the 6th span has the- upp'et bracket of the WP-2 south -fuel preparation machine during de-channeling following discharge.                      The
 -,--=-,- other-scratches are assumed to be caused by foreign-'bjects or by rubbing
-.--"===- against-the spent fuel storage locations during fuel movement.:-None of the
          -'scratches . appeared to have sufficient depth to be of -concern. Two of the inspected assemblies appear to have contained foreign material.

Some scratches were noticed on the bottom of the lower tie plate on some assemblies which might be indicative of a slight bundle- rotation. On some assemblies, the tie rods are apparently growing faster than adjacent fuel rods. This is causing an apparent loss of tension on the tie rod hex nuts. One instance--of finger spring damage was recorded on a- photograph. The observed damage was most probably caused by fuel handling after--de-channeling although spring relocation would have the same affect. - The missions of the springs while in the core was not impacted. Fuel rod E-4 of Fuel Assembly LT3 511, which is the non-spacer/capture water rod, has what is either a clad imperfection or a foreign object wrapped around

                                                              ~         ~                           ~

it at least for 270'. ~ From the photographs, it is impossible to be differen-

                                                                                       ~   ~      ~              ~

tiate further; The phenomenon occurs low on the rod in what is the natural

                                                                                                         ~

enrichment zone of the core. t t

The inspected channels all exhibit a coating of flake-like oxide material. Some miscellaneous scratches were observed. There was no evidence of mechan-ical damage, holes in the channels or control rod shadowing effects. SELECTION OF ASSEMBLIES AND CHANNELS Our.ingT the spring 1989 refueling outage, 136 original core f.uel assemblies were, discharged-. Ten of these assemblies and two channels were selected for visual=- inspection. The ten assemblies represent greater than-5 percent of the = discharged fuel and are representative of the highest-burnup assemblies in the discharged batch. Visual examination of the peripheral fuel rods of these assemblies included observation for cladding defects, fretting, fuel rod bow, missing components, corrosion, deposition and geometric .distortion. The selected assemblies are all high enriched (2.19 =:weight . percent U-235; initial). -The two channels selected were representative of . the highest exposed channels discharged. Some- characteristics of the selected assemblies and -. channels are shown in Table l. TABLE 1.0 CYCLE 4 DISCHARGED FUEL ASSEMBLIES SELECTED FOR EXAMINATION MET ULTRA FUEL ASSEMBLY CHANNEL EXPOSURE - SIP . SONIC SUSPECT 'DENTIFICATION IDENTIFICATION ~HWD/NT  :- TEST TEST CELL LJT 522 25,817 LDT 770 25,217 X LJT 398. 26,026 -X LJT 525 26,006 -X LJT 414 25,961 LJT 713 26,209 LJT 604 25,991 LJT 511 25,971 X LJT 737 71895* 26,083 LJT 794 71473+ 22,33&

 "The channel has the same exposure as the assembly,       it was       on."
                                           - 36

l t 4

             - The     ten assemblies     inspected   have   exposures   ranging from,22,338  to 26,209 HMO/HT. The inspected assemblies include assemblies which were sipped and, in some cases,       ultrasonically tested for fuel leaks during the R-4 outage. In addition, some assemblies were located in fuel cells suspected of containing fuel leaks     as determined    from flux   tilt testing.

INSPECTION TECHNI UE

     -  -; The poolside -visual examination was performed with an underwater .periscope system. with results of the fuel inspection being recorded on the Nuclear Fuel
   =--'-'ransfer L'ist in addition to the inspectors working= notebook. Two sides of each -fuel 'assembly were viewed.           Photographs of selected points of interest
            -were taken.'           total of eight-eight photographs of the examined fuel and chan-were taken.      Fifty-four of these photographs- were successful. As the       '=nels.
             . Nuclear Fuel'ransfer         List log and accompanying notes constitute the permanent
record of the'nspection, successful photographs oF .all inspected locations

- . - -::.are 'ot required although certainly desired. =.The inspection procedure

        " =.involved moving the selected             selected fuel assembly- in a vertical direction
            'ut'f
            -past the: fixed periscope; This was accomplished by. raising the fuel assembl'y the spent fuel rack with the fuel. handling mast on the refuel bridge.
           ;'Channel 'inspection was performed in a similar manner;= A ptece of abrasive material was"used to remove the heavy layer of red-.'.colored surface crud from some of the edge-fuel;rods in order to assess the rate-of nodular growth.

INSPECTION CRITERIA

   ~ -..=Visual inspection of the selected fuel assemblies
             -o the following criteria:

Proper rod seating in the lower tie plate was performed according to o Rod bow and spacing o Spacer location and perpendicularity o Finger spring condition a Condition of ti.e rod hex nuts and other structural components o Nodular corrosion and crud scaling o Fuel rod fretting The channels -were inspected for spallation, wel'd failures, cracks and other structural failures, and buildup of oxidation. The results are discussed below. r

t RESULTS OF THE FUEL EXAMINATION With one possible exception, the inspected fuel assemblies

                                                     ~                                           exhibit good apparent integrity.~ The upper tie plates were level, fuel rod springs had
                                     ~                    ~

ample compression space, the rod nuts appeared snug except in one or two instances and all the fuel rods observed were properly seated in the lower tie

               ~
          =-

plate.- The -spacers appeared perpendicular to the fuel rods and were properly located. Host- finger spring sets observed displayed no damage.. Hinor finger

        -      spring damage -was observed in isolated cases.                The grid .spacers      in general exhibit    -a   heavy nodular buildup.       Exceptions   to   the  above    statements    along with  =specific      phenomena   observed  on specific  assemblies    are   discussed   below  on an assembTy basis.          The channels inspected displayed       no  'instances   of  spalla-tion, ':cracking     -'r  other loss of integrity. They did exhibit a heavy oxide corrosion covering on all non welded surfaces.
          'uring         the inspection, the Nuclear Fuel Transfer List was maintained, field
             .notes    were      obtained and photographs were taken.          Developed photographs were

'=; - not obtained for all inspection points. During the inspection activities,

       .- was discovered that the, photograph taken of the first .5 assemblies were not it correctly exposed. No attempt was made to re-examine and photograph these assemblies except for those cases where the inspection -notes indicated a potential-.anomaly. The following description of the specific assembly inspec-
             .tion- is. based-on the Nuclear Fuel Transfer List, the field notes and, where available, the photographs.
             ,In. discussing        specific fuel assembly observations, the following convention will   .be     used. With the threaded post of the assembly in the upper left
~-corner, -the top is side A, the right side 8, the bottom side C and the left
  ~.side= D, (See Figure 1). Fuel pin locations are identified as'ollows: With the threaded=- post in the upper left corner, the fuel rod columns are labeled
        =

from left to right A,B,C,D,E,F,G and H. The fuel rod; rows are 1,2,3,4,5,6,7,8 from-top to bottom. Fuel spacers are numbered 1 througlr 7 beginning at the lowest spacer and the regions between spacers, called spans, are numbered 1 through 8 beginning at the bottom of the fuel assembly; Nodular corrosion was observed to some degree on all of the- assemblies that were inspected.. The assemblies, uncleaned, generally conformed to G.E. visual standard =-2; However, in the single instance where a fuel rod was cleaned of surface crud; the observed nodular corrosion in no way approached the 100$ nodular or sheet coverage associated with visual standard 2. fuel Assembly .LJT 552 was inspected on sides A and B. No unusual mechanical features- were. observed. Scratch marks, later determined to be associated with de-channel.ing in the south preparation machine, 'were observed on both sides of the- bundle just below grid 6 as has been seen before. The outer appearance of the fuel generally conforms to G.E. visual standard 2. Fuel Assembly -L1T 770 was inspected on sides A and D. No mechanical anomalies were observed. The uncleaned fuel conforms in appearance to G.E. visual standard 2. . Preparation machine scratches were observed on both sides A & D just below grid 6. A small foreign object was observed at the span 4 height on fuel rod A-5 (side D).

Fuel Assembly LJT 398 was inspected on sides A and D. No mechanical anomal'ies were observed.. The uncleaned fuel appears to conform in appearance to G.E. visual standard 2. Scratches made by the south fuel preparation machine were observed below grid 6 on side.D. Fuel Assembly.=LJT 525 was inspected on sides A and .C. No unusua') mechanical

     .features were: observed.      The appearance of the uncleaned fuel assembly appears to be consistent with G.E. visual standard 2. Scratches were observed on side A, span 1 and span 5, which could have been caused by the spent fuel racks.

Side A .was the- second side inspected after assembly de-channeling. Scratches were observed on the nose cone of the lower tie plate; side A, which appear to have been caused by a slight rotating movement of the-. assembly. Fuel Assembly LJT 414 was inspected on sides C and D. No mechanical damage was, observed;. The appearance of the uncleaned fuel= appears to be consistent with G.E. visual standard 2. A foreign object was observed on the finger springs on side 0. Specific views were made of the lower tie plate, grid 5 and- upper tie plate of side C and the lower tie plate "span 1 and span 4 of =- side 0. The assembly was later re-inspected. On re-inspection, the foreign object was missing. Photographs were obtained of the lower tie plate span 5 and upper tie- plate of side C and the lower tie plate, span 1 and span 4 of

   -side -0. .Some finger spring damage was noted on side B as seen from side C.
  - The type. of damage      observed is caused either by contact with a fuel rack after de-channeling or by a loss of spring tension. In either case, the mission of the. finger springs while the fuel in the core was not impacted.        Some  evidence of minor bundle rotation can be seen on this photograph.

Fuel Assembly; LJT 713 was inspected on sides A and. 0. No mechanical damage was observed.. ~ The appearance of the uncleaned fuel';most closely matched G.E. visual standard 2. Preparation machine scratches were observed below grid 6

                           ~

on span 6 on'ides A and 0. A hex nut is shown backed off on Side A. The

--   backed off .appearance is most probably caused by greater differential fuel rod growth- of the.tie rod. There does not appear to be a concern for loss of the

=-= nut. Photographs were taken of span 1, span 4, span 6 and the upper tie plate of side A and span 2 and span 6 of side 0. Fuel Assembly- LJT 604 was inspected on sides A and 0. No- mechanical damage was observed.. A hex nut on a tie rod is shown backed off on the view of side

0. The appearance of the uncleaned fuel most closely matched G.E. visual standard 2.. Preparation machine scratches were observed on span 6 of side A.

Rotational type scratches can be observed on the lower tie plate view on side C. Photographs were taken of the lower tie plate and span 6 of side A and of the lower tie plate, span 3 and the upper tie plate of side D. Fuel 'Assembly LJT 511 was inspected on sides A and 0. The appearance of the uncleaned fuel most closely resembled G.E. visual standard 2. No mechanical damage. was observed other than the specific phenomena discussed below. Oe-channeling scratches were observed in span 6 on both sides A and 0. A roughness of the clad surface perhaps associated with enhanced corrosion may be observed, in span 6 of side A. A foreign object-or .clad bulge was observed between fuel rod columns E and F as viewed from side A on rod E-4. This is the water rod which is not the spacer capture rod in the G.E. fuel design for the -MNP-2 initial core. When viewed from side D, this same phenomenon can be

                                                -39" r

I

 ,I f>

seen between -fuel rod rows 3 and 4 and fuel rod rows 4 and 5. This object occurs in the span 1 region near the bottom of the lower end cap. This loca-tion appeared to be in the natural uranium blanked region of the core. Photo-

                . graphs    of the lower tie plate, span 3 and span 6 of side A (two photographs of the lower tie plate region) and six photographs of span 1, span 6 and the upper. tie plate (four photographs of'pan 1) were taken.               This;fuel assembly
     --was              located in a suspect cell during cycle 4 as .determined by flux                 tilt testing.
            --Fuel Assemb1y--LJT 737 was inspected on sides A and D. -No mechanical damage
           - was        observed.      The uncleaned fuel rods most closely conform to G.E. visual
              . standard 2. Some clad roughness can be observed in. profile on span 4 of side A. -.Preparation machine scratches can be observed on span- 6 of side A. One of'-

the: hex. nuts appears to have backed off a very small amount in the upper tie plate view: of side 0. Photographs were obtained for span 1, span 4 and span 6 of side A and span 1, span 5 and the upper tie plate of side D.--

              -Fuel Assemb1y-:LJT 794          was  inspected on sides A and 0. No. mechanical damage
 =.  -   -.       was    observed       The   fuel   (uncleaned) most closely resembled G.E. visual
           .- standard 2.. Some hex nuts loosening may be present;. Photographs were taken
              . of span:1,-. span       4 and the upper tie plate region of side A and. the lower tie
        - -- plate, span 4 and the upper tie plate of side 0. Th'en, a section of span 7 of side:- D was cleaned with an abrasive material (Scotch brite). After cleaning,
         --:"some ophite. oxide nodules could be observed on the clad surface.                   The nodular
           -. coverage - is=.estimated at less than 30$ which is less -than the -lOOC coverage usually associated with visual standard 2.
  ~

--=~ ----.- Channel startup. 71895,. which has been resident

                              .was inspected on sides A and 26,083- NNO/NT- and was measured for bow on 0.

fuel assembly

                                                                        ,This channel LJT 737 since  initial has an exposure just prior to inspection.

of The channel

        =-- passed the- measurement criteria. No mechanical anomal.ies                 were observed on the channel. =-,It--was covered with a heavy uniform oxide =layer, white in appear-
     = - -ance-, except--for the weld seam, visible on- side A, .-which exhibited occasional
    --.  .: whi,te oxide -nodules. Photographs top of side A and the 'bottom and middle of side 0 were obtained.

Channel 71473,. which has been resident on fuel assembly LJT 794 since initial startup, was inspected on sides A and D. This channel has an exposure of 22,338 HNO/NT- and was measured for bow just prior to inspection. The channel passed the measurement criteria. No mechanical anoma'l=ies were observed on the channel.= It was covered with a heavy white oxide layer except for the seam weld region ,The seam weld visible on side A, had occasional white modules

      ~
           -but was. mostly--clean of oxidation. Photographs of the top, middle and bottom regions of both side A and side 0 were obtained.

/l ~ ~ SPAN GRID 5 CHANNEL 5 FASTENER A 8 D . E 3 -0 FIGURE 1. FUEL ASSEMBLY MAP SHOHING LABELING CONVENTION

                                    - 41,

ll t h t f I

2. 6 PLANT MOOIFICATIONS Federal Regulations (10CFR50.59) and the Facility Operating License (NPF-21)
          .allow changes; to be made to the facility and procedures. as described in the
-:-;..- -Safety Analysis Report and tests or experiments to.be:conducted which are not described in the Safety Analysis Report without prior Nuclear Regulatory
      .=- Commission    (NRC) approval,    unless the proposed change,, test or experiment

--; . = .= involves a change in the Technical Specifications incorporated in. the license or an:wnreviewed safety question. In accordance with 10CFR50.59, -summaries of

         .-the" permanent-. design changes     and temporary plant-. modifications completed
in-1989 are provided. Included are summaries of the safety evaluations.

~h 2.6.1 PLANT OESIGN CHANGES The'following plant design changes were completed in 1989 and reported in accordance with 10CFR50.59. These modifications were -evaluated and it was determined that they did not (a) increase the probabi.lity of occurrence of an accident or malfunction of. the equipment important -to safety, as evaluated in the updated Final Safety Analysis Report (FSAR), previ-'usly WNP-2 (b) create the possibility of an accident or malfunction of a different type than previously evaluated in the FSAR, (c) reduce the:margin of safety as'efined in the basis for any MNP-2 Technical Specifications, or (d) require a change to the MNP-2 Technical Specifications and as such,

                                                                    =

prior NRC approval was not required. e 43-

t Plant Desi n Chan e 84-0190 Plant Design Change 84-0190 was initiated to modify breaker control logic to allow- operation of one Plant Service Mater (TSW) pump during a LOCA when off-site power is available. This modification will minimize loss oF TSW pumps and facilitate plant recovery from a LOCA. To prevent an undesirable bus transfer due to voltage transients caused by large motor starting during a LOCA with power supplied. from the startup trans-former (TR-S),- this design change provided ten second-time delays to the auto-

          -'atic         'starts of ECCS pumps on a LOCA initiation. However, the start interval between ECCS pumps on the same division remained the same (i.e., 5 seconds).

The safety analysis bounding times are unchanged. In addition, the automatic-trip of SH-75 and SH-85 on a LOCA signal was defeated and automatic shedding of SH-72 and SH-82 on a LOCA signal was provided. Automatic trip of SH-75 and SH-85 on loss of offsite power was retained. As a result, this allows for continued operation of the TSW pumps during a LOCA and with offsite power

       .. available.. Also, an electrical interlock was provided to prevent starting of the second TSW pump during a LOCA.
        =-=      This modification did not result in a change to the MNP-2 Technical Specifica-Nions or involve an unreviewed safety question because the margin of safety

@ - ---= was not reduced or the possibility of a different malfunction as defined in the -basis-- for -any Technical Specification was not increased. Redundant safe shutdown-equipment and systems will always 'remain operational- and the required

                .system response, times were not affected.        gualitatively, the probability of a successful shutdown following a LOCA with offsite power available and a TSW
               =pump available. was increased,      which qualitatively decreases the overall core damage    risk.

Plant Desi n Chan e 84-0623

   --= - Plant Design Change 84-0623 was initiated to modify-two Reactor Mater Clean-up (RMCU) valves. to decrease their stroke times for containment isolation.         Pre-vious.ly,- the--valves were 'blocked" from stroking full'.open to reduce the stem
          --travel--required to close. Blocking provided stroke times within the maximum allowable valve closure times.

This modification changed the design of the Limitorque operators to the RMCU-V-1 and RMCU-V-4 valves to increase the stroke speed of the valve. This

               -design satisfied the maximum al'Jowable stroke time without limiting the valve opening.

MNP-2 Technical Specifications 'r This modification did not result in a reduction in the margin of safety to the result in an unreviewed safety question because the valve closure times for the two RMCU containment isolation valves remained within the maximum allowable closure time. 44

'l Plant Desi n Chan e 84-1360 Plant Design Change 84-1360 was initiated to allow maintenance to be performed on one fire protection system in a given area without removing the fire 3 protecti on alarm capab i 1 i ty of a redundant system. This reduces the pos-

               ~

sibility of an undetected fire in areas where safety equipment is located

        ~

during periods of maintenance on fire protection equipment. This modification removed cross-connections between fire control panels FP-,CP-FCP1 and FP-CP-FCP2. When an alarm is activated on one fire suppression system for a given area due to actual conditions or maintenance activities, the alarm covering the same area will remain functional to alarm on actual conditions only. This- modification did not involve a change to the WNP-2 Technical Specifications or involve an unreviewed safety question because: (1) the margin of safety in Technical Specifications was not reduced, and (2) this change provides for increased fire protection during maintenance activities. Plant Desi n Chan e 85-0093

  ,Plant Design Change 85-0093 was initiated to reduce the maintenance frequency on the Diesel Starting- Air (OSA) system for the High Pressure Core Spray (HPCS) diesel engine and increase                the reliability of the OSA to the HPCS diesel engine. Two high maintenance valves were removed from the OSA system which reduced the overall DSA maintenance.                'lso,      OSA piping was rerouted to make redundant engine starting equipment=completely independent.                    As a result, the overall reliability of the HPCS system was increased.

This modification 'removed the crosstie between air receivers OSA-AR-1C and OSA-AR-2C, which included a globe valve (DSA-V-5) and a check valve '(OSA-V-6), respectively. A, new 2-inch line was added to the line coming from air receiver OSA-AR-lC, another 2-inch crosstie line was removed, and a block valve (DSA-V-84) was added to an existing crosstie line to make redundant OSA equipment completely independent. This modification did not result in a change to WNP-2 Technical Specifications or involve an unreviewed safety question because: (1) the modification increased the reliability of the OSA which increased to overall reliability of the HPCS system, and (2) the boundary conditions for the FSAR evaluations remained unchanged. 'e e Plant Desi n Chan e 85-0184 Plant Design .Change 85-0328 was'nitiated to increase the reliability of the portion of the leak detection system that monitors leakage from the reactor coolant pressure boundary. Monitoring is performed by sensing temperature

          -..increases and = initiating alarms and isolations. .The-. previous hardware had been- causing   'n  inordinate number of system isoIations:.caused by spurious trips.

The-. old system (Riley Model 86) was replaced with a General:..Electric NUMAC system (LD-MON-1A, LO-MON-18, LO-MON-2A, and LO-MON 28). In .addition, the system recorders (LD-TRS-608, LO-TRS-611, LD-TRS-622-,= and -LD-TRS-624) were replaced. with more reliable equipment; The new, monitors provide automatic

                                                                                          =

self-testing -.every 30 minutes that test all channels--and functions of the . '/C monitor.- In addition, there is constant- monitoring-for-power failure and open signal.. .The isolation logic and devices external -to the temperature

           -monitor units -were not changed.       A preoperational-.test     was- performed on the new equ'ipment prior to return to service.

The change of hardware involving the leak detection system'id not result in a

        ..-change-- to.= the NNP-2 Technical Specifications and:the - unreviewed safety

-..-=". ..-question: evaluation concluded: (1) the function and- performance- of the Leak Detection, did not change, (2) the margin of safety:provided in the technical

         .- specifications was not changed, and (3) the boundary-conditions for the FSAR evaluations were not changed.
                                                     - 46

Plant Desi n Chan e 85-0328 Plant Design Change 85-0328 was initiated to remove a highly radioactive scc-tion of- piping ("hot spot") in the drywell under the reactor pressure vessel. a Removal of the "hot spot" significantly reduced radiation exposure to person-nel performing..maintenance activities in the immediate area, particularly on

                                           ~

the control rod drives. This modification removed a two-inch drain line (2" RRC(51)-1) between Reactor Recirculation (RRC) line 4"RRC(51)-4-3 and the Equipment ;-Drains Radioactive (EDR) -system:header 4"EOR(47)-1 including valves RRC;V and RRC-V-30. Caps were installed -on the tees from the 4-inch RRC and ZDR 1-ines to maintain the reactor pressure boundary and seal off the opening to. the EDR header, respec- " tively.. =This line served no useFul function during operation or shutdown.

           .=.-The line would ease draining of the reactor vessel during decommissioning but it  is not required to achieve this draining.
                  .Implementation of this modification was done through =the- use of a reactor
     .,= ;: vessel bottom head drain plug for isolation between the reactor vessel and the 2-inch RRC drain line. The bottom head drain plug must also perform as a pressure bouhdary for hydrostatic testing of the:spool piece ,welds in the
         --. 4-inch RRC 1:ine to 1172 psig. The plug was back pressure tested to 1400 psig
=--.= -Co demonstrate-. acceptability. A 10CFR50.59 evaluation determined there was no unresolved safety question related to the implementi.ng =activities or the plant
               - configuration-. during           implementation oF this modification because:           (1) the boundary- conditions of the FSAR evaluations were not: changed because a 2-inch leak through- the bottom head drain at reactor shutdown conditions under atmos-
                -pheric pressure are well within the postulated design -basis conditions for the Smal.l Break <OCA, and (2) the implementing activiti~s did-'not rj.duce the mar-gin of safety in the MNP-2 Technical Specifications.-
--.- This modification did not result in a change to the MNP-2 Technical Specifica-tions or .involve an unreviewed safety question because: (1) removal of the
--. drain= line -and--valves reduces the possibility of an'inadvertent leak from the
                 -.reactor pressure vessel, and (2) the boundary conditions of the. FSAR evalua-tions were not changed.

Plant Desi n Chan e 85-0360 Plant Design Change 85-0360 was initiated to modify Class 1E and some non-lE

                 .4.16 KV and 6.9 KV Mestinghouse circuit breakers.                  A failed spot weld in the breaker linkage allowed the linkage to, decouple.               This; had the effect of ren-dering electrical control circuits as well as anti-pump circuits (to prevent multiple breaker closures during faulted conditions) inoperable in affected breakers.
             =

This design change fabricated and installed new linkage =in all Class 1E 4.16 KV and 6.9 KV Reactor Recirculation Pump Mestinghouse breakers. The new link-age piece used a pivot pin assembly that was plug. welded instead of spot welded. g- This modification did not result in a change to the MNP-2 Technical Specifica-

               . tions   or,  involve   an unreviewed      safety question because this design change cor-rects  a   potential problem with auxiliary switch linkages for 4.16 KV and 6.9 KV Mestinghouse           breakers,     and   thereby,. reduces the . probability of a malfunction of equipment important to safety.

Plant Desi n Chan e 85-447 & 86-0557 Plant Design Changes 85-0447 and 86-0557 were initiated to increase the time delay in the ground fault relay settings to prevent spurious alarms from power transients.

    -This .modifica'tion changed     the time delay on the GRC= type ground fault relays for  motor control centers, and 4.16 KV and 6.9 KV switchgears from 2 cycles to 30 cycl'es. The ground fault relays provide alarm only and do not perform any safety function.

This modification did not. result in a change to the MNP-2.Technical Specifica-tions or- result in an unreviewed safety question because: (1) the margin of was not reduced in the Technical Specifications, and (2) the boundary 'afety conditions of the FSAR evaluations remained unchanged:-- Plant Desi n Chan e 86-0218 Plant Design. Change 86-0218 was initiated to eliminate one of two fire sup-manual- pull stations in the Communications .Room (525-ft level) of the pression Radwaste Building because the station is inaccessible= =-=The one remaining pull station in the area is much more accessible than the-one removed. This- modification removed fire protection manual pull-station FPHPS-28/31. ---.-This modification did not result in a change to the MNP-2 Technical Specifica-tions or involve an unreviewed safety question because this is not a safety-

  . related    system, the modification has no affect on safety systems, and removal
  . of'-the jul.l,station did not reduce the margin of safety in the Technical Specifications.

Plant Desi n Chan e 86-0332 . =-Riant Design-.Change 86-0332 was initiated to provide .increased assurance

-=against..overpressurization of the diesel fuel day tank- for each of. the three d.ivisions- due..to failure of the transfer pump to stop on'igh level in the day tank.-.- This- -increases the reliability of the diesel fuel oil system, thereby increasing the reliability of the diesel-generators.
   ,This modification provided a passive overflow drain line. between the diesel fuel oil day tank and its associated underground storage tank for each division.

This modification did not result in a change to the MNP-2 Technical Specifica-tions or involve an unreviewed safety question because: (1)'he overall reliability of the diesel-generators was increased, and (2) the boundary conditions of the FSAR evaluations remained unchanged.

                                                - 48

u t I t

Plant Desi n Chan e 87-0031 Plant Design Change 87-0031 was initiated to modify motor-operated valve interlocks on the Residual Heat Removal (RHR) System to minimize the probabil-ity of inadvertent partial draining of~ the . reactor pressure vessel to the suppression pool. The existing design did not pose. a safety threat of com-pletely draining the reactor pressure vessel because the water level would not drop below the top of the jet pumps. This. design change provided additional electrical control interlocks of the auppression pool spray and,test, return valves, RHR-V-24A & -24B and RHR-V-27A

          & =278, respectively, with the RHR suction valves, RHR-V-6A & -6B.              The exist-ing interlock 'prevented opening of an RHR suction line valve           if  a suppression' pool. spray - or: test return valve in the same division is not fully closed.

This modification provided interlocks against the reverse process. That is, the -RHR suppression pool spray and test return valves in a given division are prevented from opening if the suction valve in the same division is open. There were"-no modifications to the WNP-2 Technical Specifications as a result of this design .change. This change did not involve an unreviewed safety ques-tion: because the probability of maintaining a safe shutdown condition is increased. and =the margin of safety in the Technical 5pecifications was not reduced.. Plant Desi n Chan e 87-0114 Plant Design Change 87-0114 was initiated as a human- factors improvement to - minimize the possibility of operator error by changing the physical location of. selected=power bus control switches. Changing -the- switch -locations made

          =lineup of the'witches relative to the sequence of manual operation consistent with all'ther- similar power bus control switches, 'improving the human-to-control board =interface.          This modification reduces the possibility of a reactor scram- due to operator error, which could occur              if the switches are operated out of sequence.

modification exchanged location of the following two pairs of switches on

=- -- .This Boa'rd- "C- -that control power between          the startup:- transformer. TR-S and bus SH-6; and the- normal transformer TR-N2 and SH-6: '(1) synchronizing selector switches CB-S6 and CB-N2/6 exchanged locations, and (2) startup feeder CB-S6 and normal feeder CB-N2/6 exchanged locations.
        . This design change did not result in           a change to the WNP-2 Technical Specifi-cations    or  involve   an   unreviewed   safety question because:       (1) all wiring
    ==-   remained the same; (2) only the location of switches changed, and (3) this modification- reduces the possibility of a reactor scram due to operator-error.

Plant Desi n Chan e 87-0316 Plant Design Change 87-0316 was initiated to provide annunciation to the main Control Room-operators when the transfer switch for the second of two Residual Heat Removal (RHR) boundary isolation suction valves .from the Reactor Pressure Vessel-(RPV) is not in its required position of "Emergency". The new annunci-ator will alert operators that the RHR System is=-incorrectly - lined-up and could lead to an overpressurization of the RHR System. This. modification changed existing wiring to energize an annunciator when the transfer switch for RHR-V-8 (switch number E-RHS-ARST24) is not in its position of "Emergency" during Modes 1, 2, or 3. The transfer switch

         - required for   RHR-V-8    must be in the "Emergency" position during normal. operation to prevent-
         'ain         it   from inadvertently opening simultaneously with RHR-V-9. during cer-accident conditions. Simultaneous opening of the two valves
      - -duringpostulated:

normal operation would lead to overpressurization-of-the RHR- System.

      -". This modification did not result in        a change    to the  WNP-2 =Technical Specifica-tions or involve       an. unreviewed safety question because:           (1)   the overall reliability of the      RHR System was improved, and (2) the boundary        conditions of the  FSAR  evaluations remained unchanged.

Plant Desi n Chan e 88-0038 Plant-Design Change 88-0038 was initiated to replace selected high maintenance

  -=.  .  -radiation     and turbidity recorders with low maintenance recorders.              Extensive manhours and spare parts were required to maintain the mechanical                      type recorders.
      -=. This=modification replaced five existing recorders with Yokogawa recorders and
          - installed- one-- additional       new Yokogawa      recorder.- The five replacement         .

,= =-.-;. recorders= consisted of one. turbidity recorder on the- Reactor Feedwater (RFM)

       -- system:-(RFM-TBR-622) and four radiation recorders on the Area Radiation Mon-
         - itor (ARH)- system (ARM-RR-600); Off-Gas (OG) system (OG-RR-601, OG-RR-604),

and Reactor: Building Exhaust Air (REA) system (REA-RR.-603).= The new recorder abilityy

          , was installed-for radiation recording on the Standby.=Service           Mater (SM) system (SM-RR-2)  .

These modifications did not result in a change to the WNP-2 Technical Speci-fications or involve an unreviewed safety question because: (1) the maintain-and rel iabi 1 i ty of the recorders were incr eased; (2) the boundary conditions of-.the FSAR were not changed, and (3) the margin of safety in the MNP-2 Technical Specifications was not reduced.. 0

Plant Oesi n Chan e 88-0056 Plant Oesign Change 88-0056 was initiated to add over pressure relief for the Reactor Building Outside Air (ROA) System. This prevents destructive over-pressurization of the reactor building as had occurred on February 14, 1988. This modification installed a relief damper for the ROA Heating and Ventila-tion Unit (HY) ROA-HV-1. In the event the Reactor Building Exhaust Air (REA) System fails -to start or initiation lags that of the ROA System could result

   =-in increased reactor building pressure, the back draft damper. provides a relief path back to the fan suction to prevent reactor- building.overpressuri-zation. The -relief damper is on the ROA fan intake and downstream of the ROA
     . supply valves. ROA-V-l and ROA-V-2 that close under LOCA or radioactive release
     . conditions."- Thus, this modification does not compromise Secondary Containment.
     -                                                                     Technical Specifica-This modification did not result in       a change  to the   WNP-2.

tions or involve an unreviewed safety question because it did not affect a safety=related system, the modification to the ROA system did not change the boundary conditions used in the FSAR, and the WNP-2 Technical Specifications were not affected. Plant Oesi n Chan e 88-0306 Plant . Oesign Change 88-0306 was initiated to provide increased assurance of

  =:appropriate .Control Room HVAC System operation following a design basis Loss of Coolant Accident (LOCA), thus ensuring Control: Room personnel post-event radiation doses remained within acceptable levels. 'uring a;LOCA, the normal fresh -air intake for the Control Room HVAC is isolated and two remote air intake lines are opened. Each remote air intake line has two isolation valves
wHh. one -valve powered from Oivision I and the other valve powered from Oivi-
    . sion II;- In. the unlikely event of a special        single.'failure (i.e., "hot short"
   - or "smart short") in a power division, a valve in each remote air intake line
could isolate.'ith the loss of all fresh air input, the Control Room HVAC would continue-to operate, but in the recirculation. mode. In .the recircula-ti.an-.-mode, the Control Room would not remain pressurized with respect to sur-rounding ==areas. Acceptable post-event radiation dases to Control Room per-
  --sonnel could not be assured because operating post-LOCA in this mode was not analyzed. (This condition was discussed in LER 88-031.)
      -This modification replaced the motor operators on the four remote air intake isolation valves (WOA-V-51A, -518, -52A, and -52B) with manual operators.

This .allowed one remote air intake line to be open continuously, thus assuring that- a single failure could not cause operation in the recirculation mode.

     ==Also, post-event manual transfer could be made to the other remote air intake
    ,-path     if  the currently open remote air intake path- reached 'unacceptably high radiation levels.

This modification did not involve a change to the WNP-2 Technical Specifica-tions=- or involve an unreviewed safety question because: (1) changing the -- ',remote air intake valves to require manual operation eliminates the possi-bi-lity of a single failure and ensures that the Control Room continues to meet the licensing design basis for analyzed radioactive dose rates; (2) no new event important to safety was creyted by this change, and (3) the margin of safety in th'e Technical Specifications was not reduced because one path will

 -.- always be operational and the time required for Operator action has minimal
      .dose impact.

I Plant Oesi n Chan e 88-0430 Plant Oesign Change 88-0430 was initiated to prevent premature failure of maintenance drain lines from two Main Steam (MS) trap stations. Orain valves were removed from each trap station and the lines capped to minimize flow

                -induced vibration forces that were causing maintenance line fatigue failures.

The drain lines were uncapped and the valves were- replaced during the R-4 maintenance outage. Additional supports were provided to reduce vibration forces to acceptable levels. This - modification removed two Main Steam valves (MS-V-239 5 MSV-2388) from Trap Station g2 drip leg piping and two Main Steam valves (MS-V-118C 8 MS-V-238C) from Trap Station g3 drip leg piping, and welded a cap to each of the respective drip legs. This resulted in temporarily disabling the drain capability of the trap stations until the maintenance outage. Oraining of the trap stations can only be performed during shutdown and is normally done during the maintenance outage to remove built-up debris. As a result, this modification did not impact safety-related equipment nor increase the potential to degrade related equipment (e.g., main turbine). Temporary removal of the valves did not require a modification to the WNP-2 Technical Specifications. This change did not involve an unreviewed safety question because the potential failure of the drip legs from vibration induced fatigue was reduced making the Main Steam system more reliable. Plant Oesi n Chan e 89-0141

              - Plant Oesign 'Change 89-0141 was initiated to ensure a Reactor Building pressure- of -0.6 inch water gage within the existing:.HVAC system capability.

The modification maintains adequate ventilation and. cooling within all areas of the Reactor Building.

               =This modification changed the pitch of the blades of the Reactor Building Outside. Air HVAC System fan ROA-FN-1A from a supply .flowrate of 90,000 cfm to
          . 70 000;:.elm. =.With a bui lding in-leakage of 5,000 cfm at -0.6 inch water gage
   =--"- -: and- a .nomina1- exhaust fan flowrate of 91,000 cfm for REA-FN=,

18, the new supply

       - -. fan configuration assures appropriate building pressure, even - with moderate winds, without creating excessive loads on the exhaust fans.              This 'xtends equipment life and increases overall Plant reliability. Also, a building
            ~   pressure of -.0;25 inch water gage can be maintained 'under design basis condi-tions. - Although the new air balance configuration reduces total ventilation flow-.-below design, adequate HVAC is still provided for all areas of the
          ==

Reactor Buildi;ng. This is because the capability of- HVAC system with the new ai.r balance configuration exceeds the actual building heat load which was determined to be less than the design building heat load. In addition, the requi-rement -to draw air from areas of minimum contamination through areas of higher contamination was satisfied.

              =

This modification did not result in a change to the WNP-2 Technical Specifica-t ~ ,

       -=
..tions or invo1ve an unreviewed safety question because: (1) supporting .calcu-lations -determined the HVAC system will meet the design basi's requirements as described in the FSAR; (2) the boundary conditions- of the FSAR evaluations were not changed, and (3) the margins of safety in the WNP-2 .Technical Specifications were not reduced.

1l Plant Desi n Chan e 89-0178 Plant -Design Change 89-0178 was initiated to reduce the time to energize the emergency buses (SM-7 & SM-8) from the backup emergency diesel-generators 8 (OG). - The relays that provide the contact permissive in the diesel-generator

   -    output   breaker    control circuit were electromechani.cal with marginal per-formance'. More   consistent OG start and load times-can=,be realized with solid state relays.

This modification replaced the existing electromechanical GE relay DG-RLY-59 OG1/OG2 -with = an ASEA (ITE-27N) relay of solid state design to improve per-formance of -the OG voltage permissive interlock for--output breaker closure.

   -'This change util improve pickup voltage repeatability and provide faster and .

more consistent diesel start-to-load acceptance times. This modification did not result in a change to the'NP-2 Technical Specifica-tions or involve an unreviewed safety question because the reliability and time to energize emergency buses from backup power was- improved. Plant Desi n Chan e 89-0200

   -    Plant Design--Change 89-0200 was initiated to minimize =the =-possibility of con-tainment -liquid bypass leakage through the Control: Rod- Drive (CRO) System.

Given --failure of the CRD pumps, the existing design= had the potential of

      'releasing radionuclides in excess of the 10CFR 100 guidelines. This was based upon the design basis post Loss-of-Coolant Accident (-LOCA) radiation dose ca1culations;::-This condition was identified as a result of a commitment       made
    ,   in; LER 88-012 to evaluate NNP-2 for possible unmonitored release paths.
   . The. design change installed two check valves (CRD-V=524.&.-525), a globe valve
       .(CRD-V-526), -and three vent lines and valves ups'tream -and between the two check valves and globe valve in the 2-inch CRO supply-. line upstream of two CRO filter  units-.(CRO-FU3A & -38). The check valves .perform the safety-related function of preventing bypass leakage from the reactor vessel to the area out-side of the reactor building during post-LOCA conditions..
 -    This modification did not result in a change to the NNP-2: Technical Specifica-tions or involve and unreviewed safety question because: (1) the probability of an unmonitored release from the CRD system was reduced; (2) the boundary conditions- used in the FSAR evaluations were not affected, and (3) the margin of safety in the Technical Specifications was not reduced.

2.6.2 LIFTED LEADS AND JUMPERS The following are summaries of. noteworthy changes made. in the facility by use of the Lifted Lead and Jumper (LLJ) Procedure (PPM 1.3.9) as required by 10CFR50.59.~ ~ Each change was evaluated and determined not to . represent an unreviewed 'afety question nor require a change - to the WNP-2 technical specifications. LLJ 289-207 (Change to.SM-7 and SM-8 Minimum Bus Voltage Annunciation) Problem Descri tion A. review being performed in response to an Operational=-Experience Report (OER) discovered.- a problem with equipment powered from some -distribution panels. This condition whould occur during plant conditions where bus voltage was slightly higher than the degraded voltage relay .pick-up. An urgent Plant Modification Request was immediately processed to provide. a permanent fix to this condition (See PMR 89-0159 under the Plant Modification Section of this report). Discussion and Corrective Action A -.Justification for Continued Operation was prepared which::-recommended that -=- .- plant operators be made aware of the changes in the--degraded- voltage relay protection'equirements. A Lifted Lead and Jumper-Temporary Modification was

  -.= approved which. changed the degraded voltage protection-to- provide annunciation

.: "=: in the 'control room upon the occurrence of the minimum acceptable voltage of 93%. -In - addition, plant annunciator procedures '(PPMs 4;800.C1-2.4 and 4.-.800;C5-. 2:4) were modified to require operator action-,if the alarm occurred.

  =-:-"A-. 50;59: evaluation was performed to support this temporary change= in         the plant electrical:         -configuration. The operation of the plant with this            temporary power-'upply in place did not result in a. change to=.the-WNP-2 Technical Speci-fications or involve an unreviewed safety question- because: =(1) the overall
  - -'.operation-.of;the undervoltage electrical protection..-.met-minimum -.requirements,
      .(2) the margin of safety provided in the technical specifications was not
      .changed, -.and (3) the boundary conditions for the:FSAR..evaluations were not changed.

J LLJ 289-0221= (Temporary Power Provided to Division II 24YOC Battery Chargers) Problem Oescri tion During the -Spring 1989 refueling outage transformers E-TR-8/81 and. E-TR-8/83 needed to be-.taken out of service for Division II= ma.intenance. Mith these transformers out of service the primary source of power to the Division II 24VOC system would be lost. Discussion and Corrective Action A Jumper and Lifted Lead request was processed and approved which allowed a temporary. power supply from a non-Division II source-to .be .connected to bat- --'". tery chargers E-CO-2A and 28. This allowed continued .operation. of control room instrumentation as desired by plant operations =and..prevented the bat-teries from dischar g in g durin g the Division II outa g e.

    =A. 50;59'. evaluation was performed to support this temporary change in the plant electrical conf igurati on. The operation of the plant wi th thi s temporary power supply ..in place di d not resul t in a change to the MNP-2 Techni ca 1

=- .=Specifications or involve an unreviewed safety question because: (1) main-taining the power to the Division II 24VDC system during -the Di.vision II out-age did-not-change the function of the system (2):the-. margin of safety pro-

       =vided in the. technical       specifications was not changed, and (3) the boundary conditions for the FSAR evaluations were not changed;-

LLJ 289-0222. ,(Temporary Power Provided to Division II: 125VOC Battery Chargers) Problem Oescri tion During 'the -Spring 1989 refueling outage transformers E-TR-8/Bl. and E-TR-8/83

    ;-.needed-.-to -be-. <aken. out-of-service for maintenance.-- Mith these transformers

. out 'of service the primary source of power to the Division- II-125VOC system would be lost. Discussion and Corrective Action A Jumper and Lifted Lead request was processed and approved which allowed a temporary power supply to be connected to distribution =panel OP-Sl-2 which al.lowed continued operation of control room instrumentation needed to monitor

   =. the- safe shutdown status of the plant and prevent the 81-2 batteries from dis-charging.-. This was done by providing a jumper between the 81-7 and Bl-2 bat-teries to allow the 81-7 charger to carry the load.
    -   A 50.59    evaluation   was performed  to support this temporary change in the plant electrical configuration.         The  operation of the plant with this temporary power supply in place did no't result in a change - to the MNP-2 Technical

--: Specifications or involve an unreviewed safety question because: (1) main-taining the power to the Division II 125VOC system during the Division II outage: did not change the, function of the system (2) -the margin of safety pro-vided in the technical specifications was not changed, and (3) the boundary conditions for the FSAR evaluations were not changed.' 55-

I 1 1

LLJ 289-9999 (Temporary Power Provided to MC-7A) Problem Descri tion During the Spring 1989 refueling outage transformer E-TR-7/73 needed to be taken out of service for Division I maintenance. Nith-this transformer out of ser vice the source of power to Motor Control Center MC-7A would be lost. This motor control center provides power to Division I plant monitoring instrumen-tation. -Plant operating personnel requested power to allow monitoring activi-ties to continue during the transformer outage.

    'iscussion      and  Corrective Action A   Jumper and Lifted Lead request was processed and approved which allowed a temporary power supply from a non-Division I source= to be connected to MC-7A via SL-73. This maintained power to battery chargers Cl-1 and C2-1 and allowed for continued operation of control room instrumentation as desired by plant operations.

A 50.59 evaluation was performed to support this temporary change in the plant electrical configuration. The = operation of the plant with this temporary power supply .in place did not result in a change to the MNP-2 Technical Specifications .or involve an unreviewed safety question because: (1) main-taining the power to the Division I MC-7A during the= Division I outage did not change the- function of the system (2) the margin of safety provided in the technical specifications was not changed, and (3) the boundary conditions for the FSAR evaluations were not changed. LLJ -289-0224 (Change to Make "Bridge-Over-Core" Interlock Functional) LLJ 289-0300 Problem Descri tion

-.. During the .Spring 1989 Refueling Outage conductors 1,84 and 186 in the refuel-ing. bridge takeup reel were found broken on two di-fferent occasions.    =

With

=     these conductors broken'he interlock for the "Bridge-Over-Core" was not functional.

Discussion and Corrective Action

    -Jumper and      Lifted Lead requests were approved which allowed the use of power from   a  spare: cable (SP-1) in place of the broken conductors.              This provided
--.power to the activity control unit logic to determine when the refuel bridge
     -is in "Over-The-Core" status for implementation of refuel mode interlocks.

A 50.59 evaluation was performed to support these temporary changes in the plant electrical configuration. The operation of the plant with this tem-porary power .supply in place did not result in a change to the MNP-2 Technical -- Specifications - or involve an unreviewed safety question because: (1) the

 - overall operation of the Refueling Bridge and its logic=and "interlocks did not
    .change, (2) the margin of safety provided in the technical specifications was not changed, and (3) the boundary conditions for the FSAR evaluations were not changed.

I 4 h I

LLJ -289-0225- :(Temporary Power Provided to Source and Intermediate Range Neutron Monitor Logic) Problem Descri tion the Spring 'uring 1989 Refueling Outage maintenance was required on the

     ,Division II safety-related Switchgear (SM-8). This, in turn, would cause a loss of power= to the Source and Intermediate Range Neutron Honitoring (SRM and IRH) logic circuits.                   This was unacceptable since refuel mode surveilla'nces were required which called for operation of the SRH/IRM logic.

Discussion and Corrective Action

                   " and=   Lifted Lead request was approved which allowed for temporary
    =-A   Jumper power to be supplied from a convenience outlet at -:the 522 foot. level of the Reactor Building to the SRM/IRM logic. This allowed the control rod block to be cleared and the refuel mode surveillances to proceed during the outage.

A 50;59 evaluation was performed to support these temporary changes in the plant'lectrrca1 configuration. oper~tion of the - - rary- power supply. in place did not result in a change plant The with this tempo-to= the MNP-2 Technical

   =Specifications'--or involve an unreviewed safety question -because:                            (1) the overall operation of the SRH/IRM and its. logic and -interlocks did not change, (2) 'the margin of safety provided in the technical specifications was not
   . changed;-     and -(3) the boundary conditions for the FSAR evaluations were not changed.
   ;  LLJ 289-316         -.(One         .Main    Steam   Relief Valve    Declared    Inoperable    Due   to Inadequate          Air Supply)

Problem Descri tion

   .-During.'he Spring 1989 refueling outage the flex-hose air supply (CIA-FLX-1C) to Main Steam- Relief Valve (MS-RV-2D) was found damaged beyond repair. The flex-hose could not be replaced prior to plant startup; Discussion and Corrective Action A   Lifted Lead and Jumper request was approved which removed the flex-hose from the.=relief valve and replaced it with a blind flange. Thus, the manual relief (air- actuated)- function of the valve was not operational. The safety (spring lift) function of the valve i s s t i 1 1 operational.,
   .A-50.59 evaluation           was-        performed to support    this temporary change in the plant      .

mechanical configuration. The operation. of the plant with this temporary flange in place did not result in a change to the MNP-2 Technical Specifica-tions or involve an unreviewed safety question because: (1) the overall oper-ation- and function of the relief and safety valves for the primary pressure boundary-did not change since only twelve of the eighteen valves are required to.;be operational ( In addition, this valve is not one of the Automatic Oepres-surization System Valves), (2) the margin of safety. provided in the technical specifications was not changed, and (3) the boundary conditions for the FSAR evaluations were not changed. t LLJ 289-469 - (Defeat of Alarm "Remote Shutdown or. Alternate- Remote Shutdown Transfer Switch Activated" ) r Problem Descri tion During the Spring 1989 refueling outage two fans in the Radwaste Building (WHA-FN-52B and MHA-FN-538) were being operated from Fire Remote Transfer Panel 1 (FRTP1) because of degraded voltage concerns,. When the fans'ontrol switch -is 'placed in EHERGENCY to operate the fans,. an alarm is generated to signal '-the cont'rol switch is not in NORHAL. This masks all other alarms that could be -generated if other NORHAL/EHERGENCY control switches were placed in EHERGENCY. Discussion and Corrective Action The a1arm- was- occurring because Fire Remote Transfer-Switch -(E-RHS-FRTS-5) was

                    -=to allow operation of the two fans from- FRTPl.

in emergency lifted A jumper and lead request was approved which deactivated the alarm-from E-RHS-FRTS-5. The defeat of'he alarm from E-RHS-FRTS-5 did not result in a change to the MNP-2 Technical Specifications or involve an unreviewed safety question because: "(1)- restoring the annunciator to a usable .state met all requirements and- allowed- monitoring of the remaining remote and .alternate remote shutdown panel switches;- (2) the margin of safety provided in =the technical specifica-

 -tions was-'ot changed, and (3) the boundary conditions for the FSAR evalua-tions were not changed.

LLJ 289-0493 -(Temporary Jumper to Allow Standby Service Mater Loop "A" to

            .: - -;--Remain     Operational    With  the,  Pump   Discharge   Valve   (SM-V-2A)

Non-operational in the Full Open Position) Problem Descri tion While =starting -the Standby Service Water- System "A" the pump discharge valve ~ (SM-V-2A)--failed to open. Further investigation found the valve operator motor still running but no longer engaged to the- operator. The valve was manually placed in the full open position and Standby. Service Mater Loop "A" continued. to operate. However, in this condition, if .the service water pump (SW-P-lA) were to trip (e.g., loss of off-site power)--the pump would not be able to start since it needs a "SW-V-2A CLOSED" permissive.to start. Discussion and Corrective Action I A Jumper/Lifted Lead request was approved which defeated the "SWV-2A CLOSED" permissive. The use of the Standby Service Mater Systems without the "SM-V-2A CLOSED" permissive did not result in a change to the MNP-2 Technical Specifi-cations -and the unreviewed safety question concluded'. (1) the performance of the Service Mater System met all requirements, (2)-;the margin of safety pro-vided -in the technical specifications was not changed, and (3) the boundary conditions for the FSAR evaluations were not changed.

2.6.3 FSAR AMENDMENT EVALUATIONS The following are summaries of changes made to the FSAR in Amendment 40 which were not initiated as a .result of a plant modification. As part of the process of submitting an FSAR change, an analysis is performed in accordance with 10CFR50.59 to ensure the proposed modification does .not involve an

       =-unreviewed - safety question.       The following summaries      represent -changes in
          'system operation, clarification and/or updates of system descriptions, clari-
  =- -.- fication of Supply System positions and, in some cases, changes to- commitments previously made in the FSAR.

Cha ter 9 Standb Service Mater

        =-MODIFICATION =-This    revision to the-FSAR changes      the requirement for minimum cooling water- flow to the Residual Heat Removal       (RHR) Loop   C  pump (RHR-P-2C) seal from 9 gpm to 0 gpm.

5 Basis For Chan e This change was based in part an the =similarity in design

 ==   -- and operating conditions during a design basis accident between the RHR Loop C
      = pump and'he      Low Pressure Core Spray (LPCS) pumps.       The design and size of the
        ; seals- are very"similar between the'PCS and RHR pumps. (i.e;--, 3=.5 inch OD shaft
  =-. versus 3.75 =inch OD shaft, respectively). The LPCS-.-pump and RHR Loop C pump
   -=-- seal flushing operating temperature conditions are-.:the. same (i.e., maximum
  .=... -.narmal operating water temperature is 120 F with a--peak temperature of 212'F
  -=. -for accident temperature).         During the Reactor Pressure Vessel (RPV) cooling
        -:mode, the; RHR -Loops A and B pump seal flushing line suction water temperature
         -reaches 335'.F.. Since the LPCS specification does not,-require cooling water for its- seal and the RHR Loop C pump seal does not experience the high temper-ature=-;fluid that Loops A and B do, - the Loop C RHR-.pump does. not require any cooling water flow.

2.6.4 OTHER The Plant Problems-Plant Problem Reports Procedure (PPH 1.3.15) provides instructions for the disposition and documentation of

                                 ~                         ~ ~
                                                                                         'lant  problems. An "imnediate disposition using the "Use-As-Is" or "Repair" options is considered
                       ~                    ~  ~

a.-"change.'ithin the definition of 10CFR50.59. . Each .item below has been

                                        ~                ~

evaluated to:.provide assurance that the disposition:. does. not .involve a change to the technical specifications or an unreviewed safety question.

                  -'CR 288-0356           (Maintenahce of Secondary Containment~me ative Pressure)

NCR 288-0357 Problem Oescri tion The FSAR (6.5.1- and (9.4.2) and the Technical Specifications (3/4.6.5) requi re

                  . the-.secondary containment (reactor building air space) to be less than .25
              "-..inches. of vacuum water gauge.               The pressure devices which measure this limit
 .- .- did not-;compensate for the environmental effects of. differential temperature
         =.
               .- and:could- have- resulted in a situation where the ='vacuum limit would not be maintained.-for- secondary containment.            In addition;- there is a documented
 = .  .-.          -concern--.regarding the re-establishment of secondary= containment: differential

'9 pressure following a design basis accident. Discussion and Corrective Action Justification- for Continued Operation (JCO) was prepared which concluded the 9', A existing setpoint for the pressure measuring devices of .60 inches of vacuum water--gauge -would accommodate the environmental .ef fects and maintain the

                .: required: vacuum           in the secondary containment during =-normal .operation. -A
              ':.- second -JCO. -was., prepared to justify operation of the: plant while calculations
  -": ..:are              .completed. on both offsite and onsite doses during postulated design basis accident. conditions with new secondary containment assumptions.
    -,.-    -,--     As= a consequence       of the evaluations performed in preparing the second JCO, the
Standby..'Gas.=Treatment System (SGTS) flow was increased=and.-.credi.-t "was taken for-,building,: inleakage less than the Technical Specification limits resulting
           ...:in- an = unreviewed safety question. The unreviewed s'afety -question- evaluation
               . concluded =the -function of the secondary, containment'ould               be maintained and
al.lt study, calculations show the offsite and onsite doses to be below 10CFR100 limits following design basis accidents. Ultimate'esolution of this problem
            - .- will involve:Technical Specification and FSAR- changes and require- significant cal'culational updates.

4'&'

              - PER     289-0009      (Emergency. Lighting Failure During Annual Discharge Test)

F. Problem Oescri tion Several eight- hour emergency battery lights failed their annual. discharge test

                               ~

being conducted by plant surveillance procedure (PPH J0.25.63).

                     ~
             ,    Discussion and Corrective Action
                                      /

Battery--units were replaced to the extent permitted--by available spares. A

 - -=='JCO was prepared which concluded that sufficient emergency lighting was         .
              =-available for operation', access and egress.                    This- included an evaluation of physical 1:ighting installed -arid functional, and a: drawing review to ensure' lighting was provided in all necessary areas. The-.disposition of this item was "Use-As-Is".

The use of-'he. Emergency Lighting System as-is did not. result in a change to the WNP Technical Specifications and the unreviewed safety question evalua-

          .='ion concluded: (1) the function                   and performance wf:       the Lighting System did
         '- not         change-,  (2) the margin of safety provided in the technical specifications wa's   not changed,    and   (3) the boundary conditions for.;        the;= FSAR:-evaluati'ons were not changed.

8 PER 289-019- : ( Ident1ffcat1on of Four New Fai1ure- Medea s.for the Containment Nitrogen System) Problem Oescri tion

            . Four; -.new    failure     modes   for the      Containment Nitrogen. (CN) System were
        =
                 .identified ='.that should        have   been    analyzed as part.- of the - plant design
    .  ;          including:.=-(1.), A postulated break in the Auxiliary"-Steam piping, (2) Swamping the -low flow vaporizer, (3) Design Basis Tornado; .and.- (4) Rupture of the Nitrogen Storage Tank or its associated piping.

Discussion and Corrective Action

          .      Each    .of .the -identified failure modes. were analyzed -and a -Justification for-Continued'peration was completed. The immediate disposition of this item was "Use-.As-, Is" .with a deviation to two plant procedures -and the placement of a
        .-..portable alarming oxygen monitor in the control room: under certain conditions.

A

.-- The. use. of the .Containment Nitrogen System as designed and constructed did not result.-in a: change to the WNP-2 'Technical Specifications and the unreviewed safety question evaluation concluded: (1) the potential for damage to plant equipment-.and--the containment was very low, (2) the margin of safety provided
            . in the technical specifications was not changed, and (3) the boundary conditions for the        FSAR  evaluations were not changed:

F l J t t, l I II f t

PER= 289=020: --(Secondary Fuse Covers Installed ==in Safety-Related Motor

                                , Control Centers Without Proper Design ControT)

Problem Oescri tion G

          - -Per'sonnel-   safety secondary fuse covers were instal.led in selected safety-relat'ed motor control centers without proper design'control-.             The covers were installed to alleviate a personnel         shock hazard   in  some  480 volt  motor control centers:.   'No   Plant Modification was processed     and   no;10CFR50.59  evaluation  was performed to evaluate the change.

Discussion and Corrective Action A Maintenance= Work Request (MWR) was initiated to inspect .and -record the type of'overs used in each location. A 10CFR50.59 evaluation was performed which

          - concluded:      -'1') that the probability of occurrence- or the. consequences of an
           - accident     or malfunction of equipment as evaluated= in--the FSAR would not be
 --- -'-'increased because the fuse covers were fabricated. of-insulation-material which
         '-.cannot" present any electrical failure mode and -,-,their ight construction prevented the possibility of seismic concerns, (2) there-was no possibility of
creating='an =accident or malfunction of a different=-type-.than evaluated pre-
         =
   --'   - viously:sn the-FSAR because the covers provided added insulation in the area of- the fuse blocks which add to the safety of the design by reducing .-the pos-
         'ibiTity         of- failure during accident conditions, and-(3)= the margin of safety.

~ ==- as defined in the Technical Specifications was not reduced.-- In'ddition, the process for performing plant modification was changed to clearly r'equire a formal modification before physical. changes.-.are initiated 'in the plant.

                                                          - 62'-

PER 289-026 (Gasket of Incorrect Thickness Installed in. Several Main Steam Safety/Relief Valves)

~

e Problem Oescri tion

            .The vendor for the Main Steam Safety/Relief Valves =specifies a 0.125 inch
     -'-="thick eductor (bonnet) gasket.                        The Supply System's               Materials Management System    incorrectly       specified     a   0.250     inch    thickness      for   the gasket and these were   procured    'and   installed     in   the   plant.      Mhen     this;problem.was        discovered in January     1989   eight     incorrect      gaskets      were     still    in--stock    -in   the   warehouse.
        =    Records     showed     that   at   least    10   of   the    incorrect      gaskets     had   been   withdrawn from spare stock previously,              of   which      four   were     wi-thdrawn-   From. the  warehouse and =installed on spare valves,               and    six    were     withdrawn    from-  the-  warehouse    and installed on     in-service       valves in      the   plant.

Oiscussion and Corrective Action The immediate -disposition for this item for the installed . in-service valves was =-to "Use-As-Is" based on the following actions: (1) the vendor (Crosby) was contacted to identify potential concerns associated with the incorrect gasket thickness, (.2)

    ==-" =be -in the conservative it  was concluded that the impact= on- the setpoint would direction, (3) blowout of.=- the. gasket - would not be 11kely because of a groove machined in the body, (4) any increased leakage would not *be a problem as            it    would be identified and dispositioned in accor-danc'e with existing procedures,                (5) misalignment of.=-the body-to-bonnet                 joint
         --would not-be        a    problem since the          alignment't          the joint is controlled by the diametral     fit   of the eductor in the body, and (6) valve function using the air
          =actuator would- not be affected by the thicker gasket; The incorrect installed
          -  gaskets will be replaced per the normal preventative:maintenance schedule.
       -'ther         corrective actions were taken                as    follows: ('1)- the --.incorrect "Material
            'Code:"- has- been    -deleted and replaced           by    the correct code, =-(2) new gaskets were
ordered and- the incorrect gaskets were scrapped, and- (-3) the correct gaskets were installed in. the spare valves.

The use- of. a -gasket of incorrect thickness did not result in a change to the MNP-2 Technical Specifications or involve an unreviewed- safety. question

                                                                                =

because: (1) the valve function and performance did. not -change, (2) the mar-gin of safety'rovided in the technical specifications was not changed, and (3)- the boundary conditions for the FSAR evaluations were not changed. 'e

t PER 289-029 Problem Descri (Limit Switches Vacuum and Connectors on Containment (Wetwell-Drywell) Breaker Valves Installed Without Proper Seismic and Environmental Qualification Review of the Design Change) tion

        <imit switches.'and connectors for nine containment=-(wetwell-drywell) vacuum breakers were installed without proper seismic and environmental qualification review of -the- design        change. The plant modification changed the type and mounting of -the position switches and added a CONAX connector for the wires
 .:     exiting the valve between the two discs. The connectors constitute part of the wetwell/drywell isolation as they penetrate between the dual disks of each wetwell/drywell       vacuum  breaker.

Discussion and Corrective Action

      -The .immediate .disposition for this item was "Use-As-Is"; The design change was -reissued;,and      reviewed to quality class I requirements     The -review showed the new switches were mounted with two more bolts than the original switch and the new switch had less mass than the old. Since the switch              itself  has no
       'safety.-.related= function (they are for indication -only)- the evaluation was
  --. limited to a seismic review of the mounting which met all -requirements.              -The connectors themselves were found to be specified to= quality class I require-
-:-;ments;. The- seal uses ceramic separators with Grayfoil packing to prevent leakage and leakage tests were performed on the seals;-

The use of- the -limit switches and connectors did not result in a change to the WNP-.2 Technical Specifications or involve an unreviewed safety question because". (1);-the wetwell-drywell vacuum breaker function and performance did

not change, (2), the margin of safety provided in the technical specifications was not changed, and (3) the boundary conditions for the FSAR evaluations were not changed.

e ti r, I

PER 89-033: (Residual Heat Removal Heat Exchanger Thermal Relief Valve Install ed Backwards) Problem Descri tion The Residual Heat Removal Heat Exchanger (RHR-HX-1A) service water (tube side) thermal relief valve (SW-RV-1A) was found to be installed backwards.

                                                                               =

The relief valve inlet was bolted to the discharge piping and the relief valve

             -discharge -was bolted to the heat exchanger tap. . SW-RV-1A provides thermal
           ;- overpressure      protection to RHR-HX-1A        if  the tube side =is isolated by its block valves (RHR.-.V.-14A and RHR-V-68A). This heat exchanger is used- for shutdown cooling and'lso functions as part of the Emergency Core Cooling System (ECCS) .

Discussion and Corrective Action The -immediate;disposition for this item was "Use-As-Is" until the system was available to reposition the valve during the next outage. Until that time thermal. relief .protection was provided by tagging open the service water iso-lation valve (RHR-V-14A). With this valve tagged open thermal overpressure of the heat exchanger could not occur.

         --.The use of..SW-RY-1A in the backwards configuration did not result in a change to- the WNP-2 Technical Specifications "or involve an unreviewed safety question because:     .'(1)--the RHR-HX-1A function. and performance did not change, (2) the margin=- of.-safety'rovided in the technical specifications was not changed, and (3) the boundary conditions for the FSAR evaluations were not changed.

PER 289-038 (Average Power Range Monitor Channel F. Placed in Bypass) Problem Descri tion

       -.. In January     21,  ~

1989 the Plant received a half scram caused by a loose K18 -=-:.-=

       .--    relay socket; The relay socket had               been loosened by .repeated removal of the
       .   - relay     in accordance with Average             Power Range Monitor (APRM) surveillance procedures.

Discussion and Corrective Action A =10CFR50.59 Safety Evaluation was performed to allow APRM Channel F to be

             -bypassed    until the next         outage when the defective -relay socket was replaced.

The APRM bypass selector switch for channels B, D, and F was caution tagged to select APRM F for bypass except while performing surveillance tests on APRM B or APRM -D. Operation with a single APRM bypassed was consistent with the FSAR and the :Technical Specifications. A plant shutdown occurred on January 30, 1989 and the K18 relay socket was replaced on January.31, 1989. The use of the .APRM System with Channel F placed in Bypass did not result in a change to the=- MNP-2 Techn.ical Specifications or involve an unreviewed safety question because: (1) the APRM function and performance did not change, (2) the margin of..safety provided in the technical specifications was not chang'ed, and (3)..the boundary conditions for the FSAR evaluations were not changed. /II L

PER 289-0041 (Check valves found installed backwards . in Diesel Starting System) Problem Oescri tion In January 1989 seven check valves were found installed backwards in the

         =.-     Diesel Starting. Air Systems for DGl and DG2. The. valves and attached lines were painted :in line and appeared to have been installed incorrectly in the factory. . The - valves are spring-ball check valves and are located in the
   .:.     : .bypass      line, that connects the air supply line to the=. starter pinions and to
               -the line leading between the pinions and the air, start relay valve. The
             . incorrect valve direction was noted by guality Assurance on a routine walkdown of the system.

Discussion and Corrective Action A Justification For Continued Operations (JCO) was prepared:and the immediate disposition- was "Use-As-Is". The JCO showed that the check valves in the air start logic provided no essential function and did -not- impact the operability of the diesel .generator units. This was due to the vent path of the external air port of the- upper air start motor pinion. In addition, there-was no indi-cation of any=.:malfunction in the air start system 'during several hundred starts- performed in the factory and during plant startup and"operation. The check; valves were installed in the correct orientation during the next refuel-ing outage in May 1989.

          . The use of..the.- Diesel Starting          Air check valves in the; backwards orientation not'result-. in a change to the MNP-2 Technical Specifications or involve an,      'id unreviewed-- safety question because:          (1) the Diesel =Generator.'function and

.; --.- -. performance did not change, (2) the margin of safety=provided in the technical

         ---specifications. was not changed, and (3) the boundary conditions for the FSAR evaluations were not changed.
=-- = .:PER 289-0094 =-(Failure of a Damper Motor in the Dieej .Generator Heating and Ventilating System)

Problem Descri tion A damper motor,, in the Diesel Mixed Air System (OMA-AO-51) failed in the

        -- recirculation position. This damper is an outdoor mixing damper for the air handling unit which cools Division II cable and equipment in the -corridor during diesel operation.

Discussion and Corrective Action This item was dispositioned "Use-As-Is". A JCO was prepared which included a calculation by Engineering which showed that adequate cooling was provided with the damper in the failed position.

    ---      -The,use -of-.the Diesel Mixed Air System with the failed- damper did not result i'n a change. to the. NNP-2 Technical Specifications or involve .an unreviewed Qt              safety question because:         (1) the performance of the system met all require-ments, (2) the margin of safety provided in the technical specifications was not changed, and (3) the boundary conditions for the FSAR evaluations were not changed.

lt PfR 289-0098- (Standby Service Mater Pumphouse Ash Filters Not Installed in Accordance Mith Design Requirements) Problem Oescri

                             ~

tion

                                 ~

9 ~

            -A review. of .the Standby Service Mater Pumphouse Heating and Ventilating System
        -   -revealed three deficiencies with regard to the ash fall- filters- needed to pro-tect against the design basis volcanic event. MNP-2 has two standby service water. pumphouses (an "A" and a "B" pumphouse) and each pumphouse has two sets
 ..  -     . of, fi.lters. - For one set of filters in each pumphouse-(PRA-FL-2A/2B)      the ash-fall. filter boxes were not accessible as they were. blanked off by installed sheet metal. = The second set of filters in each pumphouse (PRA-FL-lA/1B) were actual;ly installed in the filter boxes contrary to: design. requirements which call for filter installation only under abnormal conditions (ashfall). The third deficiency was the requirement in the plant -procedures for replacement of the filters every three hours or when the delta P indication across the filters - exceeds a predetermined value. The delta P -indicators were never installed.

Discussion and Corrective Action The immediate: disposition for this i tem was "Use-As-Is";-;.For PRAFL-2A/2B the sheet . metal -was removed and the filter boxes are-- now . accessible. For PRA-FL-1A/1B the filters were removed and placed in='tandby status. The requirement for delta P indication was removed from -.the -plant procedure.

        " plant operators are required to replace the filters every- three hours in The        the
           - event of an ashfall.      Calculations show that the three hour changeout time is very conservative.
       =. The use of.     %he Standby Service Mater Pumphouse ashfall filters in the "as-is"
          -  configuration:-did not result in a change to the MNP2 Technical Specifications
       -.= or involve arr-unreviewed safety question because: -(1) the performance of the
        --Service Mater -System was not degraded, (2) the margin of safety provided in the technical=.specifications was not changed, and (3) the boundary conditions for the FSAR evaluations were not changed.

I

       - PER   289-0179    (Calculated Non-Conservative Doses to Control      Room Operators NCR   288-0403    Post-LOCA)

Problem Oescri tion Under post-LOCA conditions engineering calculation NE-02-88-27 (performed in

        'support of     NCR 288-0403     took credit for 100% mixing of primary containment leakage   within   the  reactor   building volume before postulating a release to the environment- through the standby gas treatment system.         This assumption was in
conflict with -Regulatory Guide 1.3 and resulted in. a non-conservative dose estimate for the control room under accident conditions-. -.

Oiscussion and Corrective Action

 -       After   an evaluation by Plant Management the Shift Manager declared an Unusual Event and- a controlled shutdown of the plant commenced;         After three hours the shutdown was- halted at 52 percent power consistent with..the Engineering analy-sis indicating that the associated reduction in source term was adequate to
     - ensure     habitability while the calculation problem was being. resolved. Compen-satory measures were defined to assure control room habitability, including the: requirement that both control room remote air intakes remain open to
    ..assure- control room habitability, an operator be dedicated - to respond within
             'inutes to close one of the remote air intakes-.in the case of high                '0 radiation,    and= that system operating procedures be modified to reflect the new restrictions; - This problem was resolved by improving the calculational methodology and removing. unnecessary conservatism.
A-. 50.59 evaluation was performed to support the continued operation of the plant 'at full=gower. The operation of the plant with= the; revised-analysis and
the compensatory measures for control room ventilation--operation did not require a change to the NNP-2 Technical Specifications or involve an
 " unreviewed safety question. Resolution of the associated NCR (288-0403) on single failure =vulnerability of the control room remote intakes did necessi-

.'= tate a -Technical Specification change to exit the action statement requiring the control room pressurization mode of operation-.

                                                    - 68,-

L V

PER 289-0487 (Temporary Removal of Service Water Valves Associated with LLJ 289-0353 Diesel Cooling Mater) p LLJ 289-0376 Problem Oescri tion

       ,Surv'ei:llance'esting on the Division I Diesel Generator-showed increasing high temperature in the diesel cooling water. This event was traced, to the failure of serv'ice water inlet isolation valve SW-V-214 to properly .open-. This valve is -'in -.the line that sup'plies water to one of two Diesel Cooling Water (OCM) heat exchangers.

Discussion and Corrective Action A root cause analysis of the failure of SW-V-214 determined that the disc to shaft'ap'er. pins had corroded and subsequently worked loose. The recommended a'ction.*was:to:remove this valve and the other three .valves -.of the same design

 -: 'and application (SM-V-215, 216, and 217) to preclude the potential for similar

- - fai-lures. 'in the future. Jumper and lifted lead requests were -approved which replaced each -of the four valves with straight "spools".. Other service water

valves (SM-V-4A and SW-V-48) will be used for heat exchanger isolation.

The. use of -the Diesel Cooling Water and Standby Service Mater Systems without the--four-.isolation valves did not result in a change to the WNP-2 Technical

     - Specifications'r         involve an unreviewed safety question because:     (1) the per-formance. of the Division I and II Oiesels were unaffected, (2) .the margin of
 =.'safety provided in the technical specifications was not changed, and (3) the boundary conditions       for the  FSAR evaluations were not-changed.
  .   - PER   289-0573      (Temporary Change to Allow Repairs On=the. High Pressure   Core
    . LLJ 289-0429        Spray (HPCS) Air Compressor Diesel (DSA-ENG-C/2C))

PDF 289-0590 Problem Descri tion The- air start diesel (OSA-ENG-C/2C) on .the HPCS diesel Starting Air System (OSA)- was not functioning correctly as it would not shut down after an auto start. Discussion and Corrective 'Action A jumper. and. lifted lead request was approved which disabled the compressor and. plant procedures were deviated to allow for operation of the air start diesel in an emergency. The use, of .the Diesel Air Start System with the Diesel Compressor disabled did not result in. a change to the WNP-2 Technical Specifications or involve an unreviewed safety question because: (1) the performance of the HPCS met all requirements,. (-2) the margin of safety provided in==.the--technical specifica-tions was not changed, and (3) the boundary conditions for the FSAR evaluations were not changed'.

PER 289-0588 (Inadequate Service Water Flow Through Critical Switchgear Air Handling Unit) Problem Descri tion tQ

             -    Service water flow through critical switchgear air handling unit cooling coil WMA-CC-5381 could not be adjusted to a value greater than-58 GPM.             FSAR Table 9.2-5 requires': a minimum flow of 60 GPM. Partial .blockage . of the piping and/or cooling coils is indicated.

Discussion and Corrective Action

           =      A'.justification- for continued operation      was  prepared and a review of the Engi-neering calcul'ation showed       a minimum   flow of   54 GPM=- would provide adequate cooling.

The, operation of WMA-'C-5381 with slightly reduced flow. did not result in a

              . change -'to,the WNP-2 Technical Specifications or, involve an unreviewed safety
=-.'question because: (1) the cooling of the critical:.,switchgear rooms met min-
                '-imum requirements, (2) the margin of safety provided-in the technical specifi-
          -.- cations        was-'not changed, and (3) the boundary . conditions for the FSAR evaluations were not changed.
 .--.- -';       PER  289-0649     -(Recirculation Flow      Control    Valve  Penetration    Transmitted Vibration and Noise)

Problem Descri tion

At-'.the -83%-=.open position recirulation flow control--valve (RRC- FCV-60B)
            '::penetrations ;transmitted vibrations and noise. The- noise was noted in the northwest-" corner of the 501 foot elevation of the reactor building and the
    "-.:. " hydraulic lines. to Recirculation Cooling Pump "8" were-vibrating and noisy.

Q Discussion and Corrective Action

                 -The:valve was=opened to the full open position and- the vibration and noise stopped. Flow.'nd power traces obtained from the Transient Data Acquisition
      -. --'ystem were reviewed by Engineering. Copies of the .data'traces -were submitted
            . to -General Electric for review.            At the next outage. entry was, made into con-tainment and the valve and the area around the valve was inspected.                  All equipment appeared to be undamaged and operated normally; Plant; operation: with the noise    and  vibration did not result in    a change  to the WNP-2    Technical Specifications or involve an unreviewed safety question because:    -(1.).-the performance of the Recirculation. System met all.. require-ments;:.(2) the margin of safety provided in the technical specifications was not changed; and (3) the boundary conditions. For the FSAR .evaluations were not changed.

b PER 289-0650;, (Change to Reactor Recirculation Flow Control Val ves Runback Limit Setpoint) e POF 289-0653 ISCR-937 Problem Oescri tion A reactor scram occurred from 100K power when one- of the Reactor Feed Pumps

            (RFN-P-18) tripped. The scram occurred on low water. level since the remaining feed. pump was:not able to maintain vessel level. The problem was traced to an inappropriate Reactor Recirculation (RRC) runback setpoint;       =

Discussion and Corrective Action The procedure -.was devi'ated and the setpoint for the RRC. flow control valves (RRC-FCV-60A/8)- was changed from the incorrect 30$ -open position to the

             -correct 20$ -open position. This setpoint had been--veri. fied during plant
      ==    .startup as the correct value to allow for recovery from. a. feedpump        trip.

Plant operation with the revised flow control valve- setpoint did not result in a-.change'o -the NNP-2 Technical Specifications or involve an. u'nreviewed safety

          =    question .because:      (1) the performance of the Recirculation and .Level Control
         .- Systems- met."all- requirements, (2) the margin of safety provided in the techni-
".-cal "specifications was not changed, and (3) the boundary conditions for the FSAR evaluations were not changed.
           ; PER 289-0736        (Incorrect Duty Cycles for Safety-Related  -125VOC   Batteries)

Problem Oescri tion The Supply System's internal Safety System Functional Inspection .(SSFI) dis-covered an i:ncorrect assumption in the calculation of duty cycles for the Division -I and II Safety-Related 125VDC Batteries. 'hen calculations in

           ; breaker- actuation sequencing were made         it  was incorrectly .assumed

.-.:-"==.- spring -:charging motors associated with the 480VAC:-..switchgear. were energized that the

       --...=after -"closing". as is the case with 4160VAC switchgear.          However, the 480YAC switchgear motors are energized after breaker Trip". -. .

Discussion and Corrective Action A Justification for Continues Operation was prepared and approved. The 480VAC breaker. closing spring charging motors added a 10 second load during the first minute of. battery discharge of 50 Amps for Battery B1 1 and 60 Amps for Battery" 81-2.. The capacity requirement for these batteries -is determined by the steady state loads (two-hour) not by the first minute. loading. Therefore, adding the 480VAC breaker spring charging motors to -the first minute load did not change the battery capacity requirement. P lant :.operation with the existing Division I and -II 125VOC Batteries did result- -in a change to the NNP-2 Technicql Specifications and resul.ted in an unreviewed safety question evaluation w8ich showed: - (l) the existing bat- ' teries are capable of supplying the updated battery- duty cycles, (2) the margin of safety provided in the technica) specifications was not changed, and (3) the-boundary conditions for the FSAR evaluations were not changed.

                                                        - 71

1 I

PER 289-0747 ( Inadequate El ectri ca 1 Sepa i rat on and Non-Fail sa fe Oes i gn of the Reactor Building Exhaust Air Radiation Monitoring System) Problem Oescri tion Ouring the preparation oF a Plant Modification three discrepancies. were dis-

    -'overed     in the Reactor Building Exhaust Air (REA) radiation monitoring system. They = consisted of inadequate physical separation in Control Room cabinets, routi'ng of failsafe cable in non-Failsafe raceways outside of the control room, and a non-failsafe design response of:-the radiation monitors to inoperative/downscale conditions.

Discussion and Corrective Action A justification hourly.-fire for continued operation was prepared and approved by the Plant Manager. The failsafe circuits routed in non-failsafe raceways were placed on an -tour to minimize the probability of:a fire that could cause a

  . circuit 'fault    '-

and the REA radiation monitor downscale annunciato'r response procedure was revised to require operator action to place the affected trip monitor in -a. tripped condition upon receipt of a .valid downscale condition.

    -An- engineering -evaluation and a plant modificaion are being prepared to pro-vide a permanent change to correct the problem.

Plant operation with the REA radiation monitoring .system -"as-is" did not .* result in a -change to the WNP-2 Technical Specifications or involve an unreviewed safety question because: (1) the performance of the Radiation Monitoring System met all requirements, (2) the margin of safety provided in the- technical,.specifications was not changed, and (3) the boundary conditions for the FSAR evaluations were not changed. II PER 289-0860 (Plant Operation Mith RHR-V-40 Tagged in the Closed Position) PDF 289-0868 Problem Descri tion Generic letter 89-10, "Safety-Related Motor-Operated -Yalve Testing and Sur-veillance", caused .a review of motor operated valve operability. The results of this review showed that one of the Residual Heat Removal (RHR) Loop "B" Discharge Valves from the Supression Pool (RHR-V-40)-.to the main turbine condenser had a- motor operator that did not provide;-sufficient=starting. torque at degraded voltage to operate at the maximum design. differential pressures. Discussion and Corrective Action A Justification. for Continued Operation was prepared and -approved which placed RHR-V.-40 in a: closed danger tagged position. Manual- handwheel closure of the

        -.- valve is performed after each opening.                In addition, RHR-RLY-80/Y40, the relay
that acti vates: the Bypassed and Inoperable Status. Indication (BISI) for a series of motor operated valves was removed to clear=the BISI alarm associated with this valve.
            . Plant. operation          with RHR-V-40 in a closed danger tagged position did not result   -in-  a=- change to the NNP-2 Technical Specifications and the unreviewed
          . safety question              evaluation concluded:      (1) the .overall .operation of the
         .=

Residual Heat= Removal System did not change, (2) the-margin of safety provided

in the .technical specifications was not changed, and (3) the boundary con- .

ditions for the FSAR evaluations were not changed. a.

   ~                                              Generator  Room Postulated Accident Conditions)

Overtemperature

                                                                              'ER-.289-0869.-=(Diesel Conditions During Problem Descri        tion Calculation- of- diesel generator room ambient temperatures exceeded values

+:-.- ---..stated .in--the FSAR based on new diesel heat loads determined from a 24-hour test. =-Limiting temperatures were based on postulated accident conditions involving a Loss of Offsite Power during ashfall conditions: Discussion and Corrective Action A justification- for continued operation (JCO) was performed which showed that the plant could operate until the Spring 1990 refueling outage (through April) without changes- to the diesel room cooling system. The JCO was based on the

              -fact that the- hot weather that provides the limiting condition For the temperatures will not occur during that time period.--

Plant operation with the Diesel Room cooling 'as-is" did not result in a change =to the NNP-2 Technical Specifications or involve an unreviewed safety question because: (1) the performance of the diesel-room cooling systems will meet al-4 requirements during winter and spring conditions, (2) the margin of safety provided in the technical specifications was= not changed, and (3) the boundary conditions for the FSAR evaluations were not changed during the period of operation. l, 2.7 PLANT TESTS AND EXPERIMENTS This section of the report covers WNP-2 Plant tests and experiments not described in the Safety Analysis Report as required by 10CFR50.59. ARTIAL. DRAINING OF THE SPENT FUEL STORAGE POOL TEMPORARY PROCEDURE 2.8.14 A temporary procedure was written to lower the spent fuel pool level 19 inches to allow check valve maintenance to be performed; The. fuel pool diffuser check val ves- FPC-V-1 46A and FPC-V-1468 required -modi f i cat i ons to their internals to implement an Equipment Modification Specification. The controlled lowering of the spent fuel pool level by- 19 inches did n'ot result in =a:-change to the WNP-2 Technical Specifications or involve an unreviewed safety question because: (1) the performance of the fuel pool cooling systems met all requirements, (2) the margin -of- safety provided in the technical specifications was not changed, and (3) the -boundary conditions For the FSAR evaluations were not changed during the period of operation. WIDE RANGE NEUTRON MONITOR FINAL TESTS PPM 8.3.123 AND 8.3.74 Final testing w'as completed on the Wide Range Neutron- Monitor System installed per the requirements of Licensing Condition 16 and Regulatory Guide 1.97. The pressure integl ity of the in-containment cable assemby was verified using test procedur e PPH 8.3.123. During the subsequent startup= the system was cali. brated and an operabi1 i ty check was performed 3n - accordance with plant e

 ~    procedure PPH 8.3.74.

The performance of this final test did not result in .a change to the WNP-2 Technical. Specifications or involve an unreviewed. safety question because: (1) the -performance of the Wide Range Neutron Monitoring -System met all requirements,.'(2) the margin of safety provided in-.the -technical specifica-tions was not =-changed, and (3) the boundary conditions for the FSAR eval-uations were not changed. ROD WORTH MINIMIZER RWM PREOPERATIONAL TEST PPM 8.6.11 A preoperational test was performed on the Rod Worth Minimizer (RWM) following the modifications made by Computer Change Request (CCR) 001. The test ver-ified the operation of the replacement Rod Position Information System (RPIS) interface boards and the software change made to the existing Input/Output subroutines. The modifications resolved the problem: on the RWM with the

   . Select Error. Indication in the Transition Zone (greater than Low Power Set Point (LPSP) and less than Low Power Alarm Point (LPAP)).

The performance- of this preoperational test did not result in .a change to the WNP-2 Technical Specifications or involve an unreviewed'afety question

    = because'.  
                   .(1.)-.;the performance of the Rod Worth Minimizer..met all requirements,
      .(2)  -the   margie of safety provided in the technical specifications was not changed, and (3) the boundary conditions for the FSAR evaluations were not changed.

74-

! ',, ~ 2.8 PLAN

T. PROCEDURE

CHANGES The Plant Procedure control program requires a 10CFR50.59 evaluation whenever a procedure is'hanged which provides assurance that the disposition does not involve. a ..change to the technical specifications.- or an unreviewed safety questi'on. -;The:-following are summaries of significant--Plant Procedure changes. processed during 1989: POF 289-0152 . (Procedure Change to Allow the Reactor =.Mater Cleanup System

                      -'.(RWCU) to Operate During Modes 4 and 5 With Division          I  Power (SL-73) Out-of-Service)

Problem Oescri tion

   - A       Division I =Power Outage is normally required for maintenance activities
  .      during 'each refueling outage. When Safety-Related bus- SL is taken out of
=service. power - is, lost to the Reactor Water Cl.eanup System (RWCU) non-
        .regenerative heat exchanger outlet temperature switch-=.(RMCU-TIS-8). This, in turn, closes the outboard containment isolation valve (RWCU-V-4) which iso-lates the RWCU- System. During refueling there is a: need:to keep RWCU opera-tional to maintain ~ater quality.

Discussion and Corrective Action

    -    The; Plant Procedure on Removing SL-73 from Service (PPH 2;7.14) was changed to allow the: installation of a Lifted Lead and Jumper.:to deactivate the tempera-ture switch (RMCU-TIS-8) if preferred during an outage-;..     '.
A. 50-.59-.evaluation was performed to support this change in plant. procedures.

The operation of the plant with this jumper in pTace.would not result in a change =to.the.MNP-2 Technical Specifications or involve an unreviewed safety

-- question because: (1) the Reactor Water Cleanup .System can operate safely without the. temperature switch during Modes 4 and 5,.-(.2) the margin of safety p'rovided=.in-.the technical specifications was not changed;=.and (3) the boundary conditions for the FSAR evaluations were not changed. --'-

9

PDF 289-0289 -(Procedure Change to Allow Refuel Bridge. Operation With Node Switch In Shutdown) Problem Descri tion The. Reactor Manual Control System (Rf<CS)- logic was not designed correctly and can send incorrect signals to the mode switch for the Refueling Bridge. Discussion and Corrective Action A. procedure change (PPM 2.14.1) was processed to allow the installation of a jumper to defeat the bridge s logic input from RHCS on mode switch position. This will allow refuel bridge operation while the reactor mode switch is in shutdown. The jumper will simulate the reactor mode switch being in the refuel position thus allowing continued bridge .operation over the core.

   'mplementation of this change during the Spring 1989 refueling outage was not required. Implementation at any time in the future-will =require a Lifted Lead and Jumper.

A 50.59 evaluation was performed to support this change in plant procedures. The operation of the plant with this jumper in pTace .would not -result in a change -to the .WNP-2 Technical Specifications or involve an unreviewed safety question because: (1) the overall operation of the:refueling platform and its restrictions -.would not change, (2) the margin of=-safety= provided in the -'- technical- specifications was not changed, and (3) the boundary conditions for the FSAR evaluations were not changed.

    -PDF 289-0394    =  (Operation of the Residual Heat Removal       "B". Pump Without the Suction Valve Full Open Interlock)

Problem Descri tion During- the Spring 1989 refueling outage maintenance 'was being performed on the Limitorque Operator for the valve (RHR-V-9) that provides isolation'o the suction- of Residual Heat Removal Pump "8" (RHR-P-2B)..;.-RHR-V-9 -has a full.open interlock that=.-prevents the pump from starting if the.-valve is not fully open and-.trips the pump when the valve starts to close. It was desired "to have an additional shutdown cooling method available by using RHR loop "8" during this phase of the outage. Discussion and Corrective Action A 50.59.. Safety Significance review was performed to install an electrical jumper and a.:temporary procedure deviation was approved to change the operat-ing procedure -(PPH 2.4.2) to allow operation of RHR-P-28 without the RHR-V-9 full open interlock during the short period of time while maintenance was being performed on the Limitorque operator on RHR-V-9-.

- This- change did not result in a change to thh WNP-2 Tech'nical Specifications
 . or-.involve--an;unreviewed safety question because:        (1) the overall operation
   -of the Residual Heat Removal System was admipistratively controlled and did not change, (2) the margin of safety provided'n the'echnical specifications was not changed, and (3) the boundary conditions for the FSAR evaluations were not changed.

1, s I ISCR-920.;(Change to Reduce Temperature Range of'Accident Honitoring Recorder) .0 Problem Descri tion The Residual Heat Removal (RHR) Heat Exchanger Outlet Temperature had a range of 0 to 600 degrees F. This recorder is part of the accident monitoring

        .=instrumentation-and monitors the RHR and Fuel Pool Cooling -temperatures.             The readability of the chart recorder needed to be improved.

Discussion and Corrective Action

            -The -recorder- +ange was reduced to 0 to 500 degrees F. *The reduced        span  pro-.
  -:-" vided better resolution           in both the operating and accident-temperature    ranges.

This change'id not result in a change to the WNP-2 Technical Specifications or .invol've'.an unreviewed safety question because: (1) the overall operation of -the -accident monitoring instrumentation did not:change,. (2). the margin of

 ---; -.safety provided-'n the technical specifications was:not changed, and (3) the boundary conditions for the FSAR evaluations were not changed..

Pgp

                     -0 289-0949 (R

and t C t 1 4 li Inoperable Status Indication I ~tbl / Change) Problem Descri tion

         - Two    Reactor; Core 'solation Cooling Valves (RCIC-V-22 and .RCIC-V-59) were taken out-.of.-service to effect repair of RCIC-V-22. These two-valves are the test

'e, return: to Condensate Storage Tank flow control and stop valves, respectively. Deenergizing=-:and tagging out ihe valves caused the - Bypass. and Inoperable Status '.Indication (BISI) system to activate masking=.any signals that may be present on-eleven other RCIC valves associated with..annunciator 4.601.A4-6.8,

    '-.     '!RCIC DIVISION:-I OUT-OF-SERVICE" and the "MOTOR OPERATED VALVE NETWORK POWER LOSS/OVERLOAD" BISI.

Discussion and Corrective Action

           ;Relays    RCIC-RLY-80/22 and RCIC-RLY-80/59'ere pulled to allow the remaining motor;operated=valves to be monitored by the BISI system. Plant procedure PPH 4.601.A4-6.8 was deviated to show the change.

The -.oper.'ation of the plant with the BISI system modified as noted above did not. result, in- a change to the WNP-2 Technical Specifications and the unre-

  --= viewed safety .question concluded:             (1) the performance of the BISE System was.

improved,'.(2): the margin of safety provided in the technical specifications was not- changed', and (3) the boundary conditions for..the FSAR evaluations were not changed.

0 POF 289-964'. -(Modification of the Plant Procedure-. on Wire Marker Installation)

                                    ~

Problem Descri

                       ~

tion Q The plant procedure (PPM 10.25.61) used to mark cables .and wires in the plant

                                         ~   ~

required- clari:fication on the practice oF marking the wires which are broken out of a multi-conductor cable. 4 Discussion and Corrective Action

     =

The. plant procedure (PPM 10.25.61) was changed to -allow. the use of plastic sleeves or. Brady markers which have black lettering on -a white background as an approved installation method. The operation.=of the plant with the wire marking procedure. modified as noted above did;-not" result in a change to the WNP-2 Techni.cal Specifications and the unreviewed. safety 'uestion concluded: (1) the wire marking criteria and performance was not changed, (2) the margin of safety- provided in the tech-nical specifications was not changed, and (3) the boundary conditions for the FSAR evaluations were not changed. 0

2.9 REACTOR COOLANT SPECIFIC ACTIVITY LEVELS T his section contains information relative to reactor coolant cumulative iodine levels, iodine spikes and specific activity of all~isotopes other than iodine. The specific activity of the primary coolant was significantly. less than 0.2 microcuries per gram dose equivalent I-131 as set- forth in NNP-2 Technical Specification LCO 3/4.4.5 and paragraph 6.9.1.5 'c., (see 1989 cumulative iodine graph;= attached). The specific activity. of. the primary coolant was routinely 'sampled and analyzed as required by MNP-2-,Technical Specifications, . and was in all cases, less than or equal to 100/E microcuries per gram. A graph - showing cumulative iodine dose equivalent for .the calendar year 1989 fol 1 ows.

C9 Q (dl ) ll ll l I EACTOR DOSE .EQUIVAL'EN'T IODINE () c~ ~ e ucX/gm WNP-2 0.030 Z2DEQ PFlX S I

              ) I I
                    <)1     (3  1  ()                           (i/i   lO     4 () tl; il          lil I'I'I 0.025                     I:)r)i):)r yr   1    1
                                                     <1tl)f  I t) t>)-) )i)>>f<<       1 f,     ftftlfl 0.080 0.0%6 44*

Il O.oio lI

                                                                              )III         )II ll P(    I(>lI         i     I   I    I   (llli~'I )N)gi                 ll)lbllllll 0.005                                         +)  II ii      .,<<j                     ilies 0.000 W.ODB Of-Ol         03-02               05-01       '6-30               08-29             %0-28      42 27
                         -  Januar y I, %989 to December                            3i,      %989

1I (

2.10 REPORT OF OIESEL GENERATOR FAILURES This section contains information pertaining to the reporting of diesel

                  ~                                                     ~       ~

generator failures, valid and nonvalid, in accordance with the requirements

                                               ~      ~           ~           ~
                            ~

of MNP-2 Techqical Specification 4.8.1.1.3.

                        ~           ~ ~
                                                 ~      ~   This report provides the
   =:.-.information;-required by Regulatory Position C.3;b - of, Regulatory GUide
                          ~

1.108, Revision 1, August 1977.

                                               -   81

II l 1

Diesel Generator Failure Number One

1. Identity of diesel generator unit and date of failure:

Division Three Emergency Diesel Generator (OG-3) Hay 12, 1989

2. Number designation of failure in last 100 valid tests,.

Not applicable. This was a nonvalid failure. The unit was inoperable for maintenance overhaul activity.

3. .Cause of failure:

The- exact cause of the failure was not able to be determined. During

    --a   slow start test (nonvalid test) run of OG-3, the unit started at
     . full .speed (900 RPH) rather than slow speed (400= RPM) . as designed.

Subsequent tests were not able to duplicate the failure.-.

4. Corrective measures taken:

None.

5. Length of time diesel generator unit was unavailable: --

e'ot applicable for this nonvalid failure. Current surveillance test interval: Thirty-one days.

7. Verification of test interval:

The surveillance test interval of thirty-one days is in conformance with NRC Reg. Guide 1.108 position C.2.d.

Diesel Generator Failure Number Two Identity of diesel generator unit and date of failure: Division Three Emergency Diesel Generator (OG-3) Hay 13, 1989

2. Number designation of failure in last 100 valid, tests:

Not applicable. This was a nonvalid failure. The= test was. a nonvalid test- because it was testing a feature which was not-,a. part of the defined di.esel generator unit design.,

3. Cause of fai,lure:

The- failure was the result of 'a nonvalid test performed to discover if DG-3 would start with one of two starting air headers isolated. .. The ability to- start on one air header is not part of:-the OG-3 design. The cause of.'the failure to start was insufficient .capacity of only one

    'tarting     air header. The design of this system calls for two starting air headers.
4. Corrective measures taken:

None. Length of time diesel generator unit was unavailable:. Not applicable. This Has a nonvalid test.

6. Current surveillance test interval:

Thirty-one days.

7. Verification of test interval:
    -..The, surveillance test interval of thirty-one days        is in conformance with NRC Reg. Guide 1.108 position C.2.d.

0

Diesel Generator Failure Number Three

l. Identity of diesel generator unit
                          ~

and date of failure: 3 Division

                ~

One Emergency Diesel Generator (DG-1) May 18,~ 1989

2. Number designation of Failure in last 100 valid tests:

Not applicable. This was a nonvalid failure. The unit was inoperable for maintenance overhaul activity.

3. Cause of failure:
        -No  definite    cause   of failure was able to be identified.= The unit tripped during     an  end    of maintenance warranty run prior to declaration oF
      . operability. A thorough investigation was unable to identify a definite cause.- -The fault trip was not able to be repeated during follow-up testing.
4. Corrective measures taken: f
 =  =-==The 18=month       overhaul procedure was modified to include       a specific check of the    manual overspeed    trip mechanism.
5. Length of time diesel generator unit was unavailable:-.

Not applicable for this nonvalid failure. J

6. Current surveillance test interval:

Thirty-one days.

7. Verification of test interval:
 -.--. The'urveillance test interval of thirty-one days is -in. conformance with NRC Reg. Guide 1.108 position C.2.d.

/a Diesel Generator'Failure Number Four Identity of diesel generator unit and'date of failure. Division Two Emergency Diesel Generator (DG-2) May 20, 1989

2. Number designation of failure in last 100 valid tests.

Not- applicable. This was a nonvalid test failure. Per WNP- 2 Technical Speci fi cation Tab 1 e 4.8.1.1. 2-1, with the except i on of the semiannual fast start, no starting time requirements are required to meet the valid test requirements of NRC reg. Guide 1.108.

3. Cause of failure:

During performance of the 18 Month Logic System Functional Test DG-2 Loss of Power Test, the diesel generator did not attain rated speed within ten seconds of receiving a start signal. The cause of the failure was originally isolated to a broken pneumatic boost line which supplies the Woodward speed governor unit. This prevented the start boost signal from being received by the actuator and would have resulted in a decrease in fuel supply to the diesel during fast start.

4. Corrective measures taken:

The pneumatic line was repaired and the unit was retested.. The retest did not demonstrate acceptable starting time. (See Diesel Generator Failure 45.)

5. Length of time diesel generator unit was unavai.lable:

Not applicable for this nonvalid test.

6. Current surveillance test interval:

Thirty-one days

7. Verification of test interval.

The surveillance test interval of thirty-one days is in conformance with NRC Reg. Guide 1.108 position C.2.d.

I I t

Diesel Generator Failure Number Five .e'dentity of diesel generator unit and date of failure: Division Two Emergency Diesel Generator (DG-2) May 24, 1989

2. Number designation of failure in last 100 valid tests:

Not appli:cable. This was a nonvalid test failure. Per, WNP- 2 Technical Specification Table 4.8.1.1.2-1, with the exception of the semiannual fa'st start, no starting time requirements are required to meet the valid test requirements of NRC reg. Guide 1.108.

3. Cause of failure:

During performance of the 18 Month Logic System Functional Test DG-2 Loss of Power -Test, the diesel generator did not attain rated speed within ten seconds of receiving a start signal. The cause -of the failure was isolated to the voltage permissive relay DG-RLY-59/DG2 which provides a permiss.i-ve: signal to close the DG2 output breaker when generated voltage is - high - enough. The relay actuation setpoint calibration tolerance was found to'llow sufficient variation to affec't the 10 second start time under certain conditions.

4. Corrective measures taken:

e- The relay was recalibrated to obtain sufficient setpoint performance to

       -ensure--obtaining a maximum 10 second start time. :This mechanical relay was -.later replaced'ith a solid state relay which could be calibrated to perform consistently within the required tolerance.
5. Length of time diesel generator unit was unavailable:

Not applicable. This was a nonvalid failure.

6. Current surveillance test interval:

Thirty-one: days.

7. Verification of test interval:

The surveillance, test interval of thirty-one days is in conformance with NRC Reg. Guide 1.108 position C.2.d.

                                               - 86

Oiesel Generator Fai.lure Number Six 1.~ 'Identity of diesel generator unit

                           ~

and date of failure:

              ~

Oivision Three Emergency Oiesel Generator (OG-3) June 2, 1989

2. Number designation of failure in last 100 valid. tests:

Not applicable. This was a nonvalid failure as it was. due to personnel error.

3. Cause of failure:

Ouring performance of the Logic System Functional Loss of Power Test, the diesel'perator did not apply sufficient load soon enough after synchronization with the power grid to prevent a reverse power trip of the OG unit.

4. Corrective measures taken:

The operating procedure was'valuated for correctness and:-found to be acceptable. The operator was counselled. Length of time diesel generator unit was unavailable: OG3 was'navailable for approximately ten minutes while the protective e, relays were being reset. Current surveillance test interval: Thirty-one days

7. Verification of test interval:
   -.--. The   .surveillance test interval of thirty-one days fs =in conformance with NRC   Reg. Guide 1.108 position C.2.d.

0

                            . Diesel Generator Failure Number Seven Identity of diesel generator unit      and date   of failure:

Division One Emergency Diesel Generator (DG-1) June 9, 1989

2. Number designation of failure in last 100 valid tests:
       -'ot   app'licable. This was   a nonvalid  failure. This was not .a valid test failure.-    .Per MNP-2 Technical   Specification Table 4.8.1.1.2-1, with the exception of the semiannual fast start, no starting-.time- requirements are required to meet the valid test requirements of NRC Reg.- Guide 1.108.
3. Cause oF failure:
    ='uring       performance of the 18 Month Logic System functional Test        DG-1 Loss of  Power  Test, the diesel generator did not attain rated speed within ten seconds -of receiving a start signal.            The cause. of the Failure was incorrect connection of the start pneumatic boost signal to the Moodward
  -'- speed -governor unit.          This resulted in insufficient;:fuel.-supply to the diesel during fast start to ramp speed at the required-,- rate.,=.=-
4. Corrective measures taken:

Th'.'neumatic line was connected .to the correct port--on the governor

                                                                             =

actuator. The unit was then retested successfully: . The other diesel units were inspected for similar fault.

5. Length of. time diesel generator unit was unavailable:

h Not applicable to this nonvalid start.

6. Current surveillance test interval:

Thirty-one days

7. Verification of test interval:
       . The  surveillance test interval of thirty-one        days  is in conformance with
      - NRC   Reg. Guide 1.108 position C.2.d.

l~ t

Oiesel Generator Failure Number Ei ht Identity of diesel generator unit and date of failure:. Oivision One Emergency Oiesel Generator (OG-1) June 10, 1989

2. Number designation of failure in last 100 valid, tests:

Not applicable. This was a 'nonvalid failure. The failed valve is not a part of the defined diesel generator unit design.

3. Cause of fai.lure:

The. OG-1 -output circuit breaker was tripped by protective relay actuated by high engine cooling water temperature. This, in turn, shutdown the diesel= generator. The high engine cooling water temperature was caused by failure of the Standby Service Mater System cooling water inlet valve which:..supplies cooling water to the engine cooling water .heat exchanger. The valve-. disk separated f rom the operating stem and remained in the closed, position blocking cooling water flow..The-. pneumatic valve

             =

operator,;.however, stroked fully open showing a ful:1::open valve position indication. P 4~ Corrective measures taken: The faulty. valve was removed. The possible generic'mplications of this failure;; -were inves ti gated. These va 1 ves on ihe rema ining Oi ese 1 Generator units were removed. (See PER 289-0487.) Length'f time diesel generator unit was unavailable: Not applicable to this nonvalid failure.

6. Current surveillance test interval:
  ,Thirty-one days
7. Verification of test interval:

The surveillance test interval of thirty-one days is in conformance with NRC Reg. Guide 1.108 position C.2.d.

                                             - 89

1 2.11 FIRE PROTECTION PROGRAM CHANGES The following changes were made to the fire protection program during the calendar year. - These revisions were all made to plant procedure 1.3.10, Fire Protection Program, in which the procedure is included as part of the FSAR by reference. The procedure was revised to require all detectors in vital areas to

             .be    operational       at    all    times.      If   they are not operational compensatory       measures     must be taken.            The   revision    is  more restrictive     than the previous requirements.
2. Detector maintenance activities were removed from plant procedure 1.3.10 and moved to . volume 15 procedures. Haintenance activities
           ,  will.be performed in accordance with the applicable NFPA standards, as well as insurance              company and manufacturer          recommendations.

Maintenance activities will be scheduled via the Scheduled Maintenance System (SMS).

3. The minimum requirements for fire protection system pump and water
         =     supply operability were clarified. The requirement is: two 2000 gpm pumps and the 2500 gpm pump must be operable at all times.
4. Fire Suppression Hater System Maintenance activity descriptions were removed from plant procedure 1.3.10 and moved to volume 15 procedures. Fire Suppression Hater System Maintenance activities
          ;   will be performed in accordance with the applicable NFPA standards, as well as         insurance company and manufacturer recommendations.

Maintenance activities will be scheduled via . the Scheduled Maintenance System (SMS). 5.= Operability requirements for hydrants within the protected area were changed to require operability of only those hydrants that provide protection for equipment that, is required to be operable. This is more restrictive than the previous requirement.

    .6.       The compensatory actions associated              with an  impaired hydrant or hose
          -.house were changed in that a hose               is  now  required to be placed at an adjacent     hydrant/hose     house in 24 hours instead of one hour.              The basis-for the       change   is that a van is used by the fire brigade when responding      to fires     in the protected area.           The van has hose on board and can be used        to rapidly lay the hose for fire fighting.

7-. Maintenance activities associated with hydrants were removed from

              'plant procedure         1.3.10 and moved to volume 15 procedures.

Maintenance activities will be performed in accordance with the applicable NFPA standards, as well as insurance company and manufacturer recommendations. Maintenance activities will be scheduled via the Scheduled Maintenance System (SMS). 90-

IH

8. Operability requirements for hose stations were changed to require all hose stations in the Corridors, Turbine, Reactor, Radwaste and Diesel Buildings be operable anytime the equipment which the hydrant provides protection for is required to be operable. This is more restrictive than the previous requirement.
9. Hose station maintenance activity descriptions were removed from plant= procedure 1.3.10 and moved to volume 15 procedures. Hose station maintenance activities will be performed in accordance with
                -  the 'pplicable NFPA standards, as well as insur'ance .company and manufacturer        recommendations.          Maintenance     activities will be scheduled     via the Scheduled Maintenance System (SMS).

10; The requirements for a fire watch to be stationed for inoperable control room halon systems was removed since the control room is manned 24 hours per day and there are halon extinguishers available. A fire protection impairment must be issued. ll: Halon- fire protection maintenance activity descriptions were removed moved to volume 15 procedures. from plant procedure 1.3.10 and Halon fire protection maintenance activities will - be performed in

              '-accordance with the applicable NFPA standards, as well as insurance company 'and manufacturer           recommendations..       Maintenance activities will be scheduled via the Scheduled Maintenance System (SMS).
  '2.             .The'equirements
                  =suppression      systems for were compensatory changed     to measures    associated require a fire impairment with e              . permit. The requirement of a fire watch is needed only if a system is inoperable and the associated detection system is inoperable. If the detection system is operable an hourly fire tour must be established.
13. Various valve and fire protection equipment maintenance activity descriptions were removed from plant procedure 1.3;10 and moved to volume 15 procedures. Valve and fire protection maintenance activities will be performed in accordance with the applicable NFPA standards, as well as insurance company and manufacturer recommendations. Maintenance activities will be scheduled via the Scheduled Maintenance System (SMS).

14.. The- requirements for various inspection activities were changed to be ;in compliance with NFPA standards and insurance company and manufacturer recommendations. It additionally states that the maintenance will be scheduled via the Scheduled Maintenance System (SMS). The.. modifications to the Fire Protection Program as - described above did not r.esult 'in a change to the NNP-2'echnical Specifications since the Fire Protection, Te'chnical Specifications had been removed.-per Amendment 67. The unreviewed safety , question evaluation . concluded:- -:(1');- -the function and ~ performance of the Fire Protection Program did not" change; (2) the margin of safety provided in the technical, specifications was .not changed, and (3)'he boundary conditions for the FSAR evaluations were not'changed.

                                                      ; '91.- '
        .g r

>p l, I

     ~E}}