ML19317F329: Difference between revisions
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DUKE POWER Ont!'A!W OCONCE Ut;IT 2 Report Number: R0-270/77-12 Occurrence'Date: October 7,1977 | DUKE POWER Ont!'A!W OCONCE Ut;IT 2 Report Number: R0-270/77-12 Occurrence'Date: October 7,1977 | ||
. Report Date: February 15, 1978 Facility: Unit 2, Seneca, South Carolina | . Report Date: February 15, 1978 Facility: Unit 2, Seneca, South Carolina | ||
~ | ~ | ||
Identifica' tion of Occurrence: Primary-to-Secondary Leak through B | Identifica' tion of Occurrence: Primary-to-Secondary Leak through B Once Through SteamcGenerator (OTSG) | ||
Once Through SteamcGenerator (OTSG) | |||
Conditions Prior to Occurrence: 80 percent Full-Power Description of Occurrence: | Conditions Prior to Occurrence: 80 percent Full-Power Description of Occurrence: | ||
' On September 27, 1977 air injector radiation monitor RIA-40 indicated a primary-to-secondary Icak of approximately 0.2 gpm. Power was reduced . | ' On September 27, 1977 air injector radiation monitor RIA-40 indicated a primary-to-secondary Icak of approximately 0.2 gpm. Power was reduced . | ||
Line 32: | Line 29: | ||
~ | ~ | ||
of an apparently incrcasing Icak rate the unit was shut down on October 7, 1977. . Af ter a 21 day outage and several unsuccessful attempts to find the leak the unit was -returned to power operation on October 28, 1977. A second unsuccessful attempt to-locate the leak was made from November,3 to 12, 1977. On December 29, 1977 the unit was shut down to repair a-_ control rod stator, remove install.ed steam generator instrumentation 'and make -another attempt at 71 ocating the indicated leak. .Tub e-77-25 was discovered to be leaking. Fiber optic and eddy-current examinations indicated a 90 circumferential' crack near. | of an apparently incrcasing Icak rate the unit was shut down on October 7, 1977. . Af ter a 21 day outage and several unsuccessful attempts to find the leak the unit was -returned to power operation on October 28, 1977. A second unsuccessful attempt to-locate the leak was made from November,3 to 12, 1977. On December 29, 1977 the unit was shut down to repair a-_ control rod stator, remove install.ed steam generator instrumentation 'and make -another attempt at 71 ocating the indicated leak. .Tub e-77-25 was discovered to be leaking. Fiber optic and eddy-current examinations indicated a 90 circumferential' crack near. | ||
the upper tube sheet. The tube;was stabilized and plugged. The instrumented ' tubes (6), which showed considerable wall thinning, were also plugged A11 -(7) previously plugged tubes were re-plugged as a precautionary measure., Hydrostatic tests showed no further Icaks and the unit was- returned to power operation on January 16, 1978. | the upper tube sheet. The tube;was stabilized and plugged. The instrumented ' tubes (6), which showed considerable wall thinning, were also plugged A11 -(7) previously plugged tubes were re-plugged as a precautionary measure., Hydrostatic tests showed no further Icaks and the unit was- returned to power operation on January 16, 1978. | ||
. ~. | . ~. | ||
Line 38: | Line 34: | ||
The exact cause of_tlue incident cannot be determined. The primary-to-secondary 11cak could have been _ caused.by either' tube 77-25 or any of ' | The exact cause of_tlue incident cannot be determined. The primary-to-secondary 11cak could have been _ caused.by either' tube 77-25 or any of ' | ||
the:seven replugged. tubes. The Nucicar Steam Supply System supplier, Babcock 'and Wilcox, and Duke Power Company are continuing to investigate the ' tube. leak problem. ' ' | the:seven replugged. tubes. The Nucicar Steam Supply System supplier, Babcock 'and Wilcox, and Duke Power Company are continuing to investigate the ' tube. leak problem. ' ' | ||
1 | 1 O | ||
-m 6 Gi J f; | -m 6 Gi J f; | ||
s | s | ||
'80.01100 ] o | '80.01100 ] o | ||
DI KE l'O',il:R Co*tt'ANY OCONCE UNIT 2 (Cont'd) | DI KE l'O',il:R Co*tt'ANY OCONCE UNIT 2 (Cont'd) | ||
Analysis of Occurrence: | Analysis of Occurrence: | ||
Line 52: | Line 44: | ||
Corrective Action: | Corrective Action: | ||
Tube 77-25 was stabilized and plugged. Previously instrumented tubes which showed appreciable wall thinning were also plugged. All pre-viously plugged tubes were re-plugged. | Tube 77-25 was stabilized and plugged. Previously instrumented tubes which showed appreciable wall thinning were also plugged. All pre-viously plugged tubes were re-plugged. | ||
5 4 | |||
9 e | 9 e | ||
t | t | ||
: 4. __. | : 4. __. | ||
.1 | .1 | ||
==SUMMARY== | ==SUMMARY== | ||
Line 74: | Line 58: | ||
: GENERATOR ROR . TUBE . ELEVATION | : GENERATOR ROR . TUBE . ELEVATION | ||
' R0-269/76-17 153 | ' R0-269/76-17 153 | ||
'ths . Crack Plugged | 'ths . Crack Plugged | ||
.17j Tubesheet ~10/31/76 Yes 1-AL '7 7 ' | .17j Tubesheet ~10/31/76 Yes 1-AL '7 7 ' | ||
No . Distorted Eddy Plugged Tubesheet. 10/31/76 Yes-1-A 77 18 Current Signal | No . Distorted Eddy Plugged Tubesheet. 10/31/76 Yes-1-A 77 18 Current Signal R0-269/76-19 139 No Yes No Visual ' Nailed-1-B 114. 109- 14th. Plate 12/8/76 Inspection No Distorted Eddy- Plugged No 1-B 113 115 | ||
R0-269/76-19 139 No Yes No Visual ' Nailed-1-B 114. 109- 14th. Plate 12/8/76 Inspection No Distorted Eddy- Plugged No 1-B 113 115 | |||
* 14th Plate 12/8/76 Currant Signal No No Similar to Nailed 1-B 113 110 14th Plate 12/8/76 114/109 . | * 14th Plate 12/8/76 Currant Signal No No Similar to Nailed 1-B 113 110 14th Plate 12/8/76 114/109 . | ||
Yes No 300 Crack Nailed 1-B ' 75 18 Tubesheet 12/8/76 Nailed R0-269/77-2 '140 1/15/77 Yes Yes 350 . Crack | Yes No 300 Crack Nailed 1-B ' 75 18 Tubesheet 12/8/76 Nailed R0-269/77-2 '140 1/15/77 Yes Yes 350 . Crack | ||
Line 85: | Line 66: | ||
1-B 81 128 Tubesheet 1/15/77 RNo Indication RO-269/77-8 3% | 1-B 81 128 Tubesheet 1/15/77 RNo Indication RO-269/77-8 3% | ||
No Yes Eddy Current Nailed 1-B 32 13 14th Plate 2/28/77 I.ndication No No Eddy Current Nailed , | No Yes Eddy Current Nailed 1-B 32 13 14th Plate 2/28/77 I.ndication No No Eddy Current Nailed , | ||
1-B 33 14 14th Plate 2/28/77 Indication Eddy Current P.emoved 25 14th Plate 2/28/77 Yes No 1-B 77 Indication | 1-B 33 14 14th Plate 2/28/77 Indication Eddy Current P.emoved 25 14th Plate 2/28/77 Yes No 1-B 77 Indication No Eddy Current Plugged 13th Plate 2/28/77 No 1-B 2 7 Indication , | ||
No Eddy Current Plugged 13th Plate 2/28/77 No 1-B 2 7 Indication , | |||
~ | ~ | ||
No No Eddy Current Plugged 1- 3 2 8 13th Plate 2/28/77 Indication No No Eddy Current Plugged 1- B 101 40 4th Plate 2/28/77 Indication | No No Eddy Current Plugged 1- 3 2 8 13th Plate 2/28/77 Indication No No Eddy Current Plugged 1- B 101 40 4th Plate 2/28/77 Indication | ||
_ _1._ | _ _1._ | ||
~ | ~ | ||
Line 102: | Line 76: | ||
OF MMOR OTSG TUBE EXPERIENCE AT OCONEE (CONT'D) . | OF MMOR OTSG TUBE EXPERIENCE AT OCONEE (CONT'D) . | ||
# TUB'ES EXAMINED .. | # TUB'ES EXAMINED .. | ||
LANE | LANE ACTION . ROP (excludes leakers) | ||
ACTION . ROP (excludes leakers) | |||
TUBE. ELEVATION :DATE TUBE LEAKER CONDITION , , | TUBE. ELEVATION :DATE TUBE LEAKER CONDITION , , | ||
l GENERATOR ' ROW, 100 Yes Weld Crack Replugged R0-269/77-11 1-B - 77- 25 Tubesheet 3/22/77 .Yes Yes Distorted Plugged 1-BL .77 3,5,8' --- .3/22/77 1No Eddy Current | |||
l GENERATOR ' ROW, | -Signal | ||
* Plugged R0-269/77-16 507 5/7/77 Yes Yes Crack 1-B. 77 15. Tubesheet , | |||
100 | |||
Yes Distorted Plugged 1-BL .77 | |||
3,5,8' --- .3/22/77 1No Eddy Current | |||
-Signal | |||
Plugged R0-269/77-16 507 5/7/77 Yes Yes Crack 1-B. 77 15. Tubesheet , | |||
No --- Removed 18 --- 5/7/77 Yes 1-B !77 ~ | No --- Removed 18 --- 5/7/77 Yes 1-B !77 ~ | ||
~No Distorted Plugged , | ~No Distorted Plugged , | ||
5/7/77 -No , | 5/7/77 -No , | ||
1-B ' 17 5 --- | 1-B ' 17 5 --- | ||
* Eddy Current | * Eddy Current Signal Removed R0-270/76-15 133 Yes Yes 270 Crack, 2-B 77 23 Tubesheet 12/4/76 Hole Yes No Wear Appearance Removed 2-B , | ||
Signal Removed R0-270/76-15 133 | |||
Yes Yes 270 Crack, 2-B 77 23 Tubesheet 12/4/76 Hole Yes No Wear Appearance Removed 2-B , | |||
77- 27 15th Plate 12/4/76 No Eddy Current Flugged 2-B 124 42 12th Plate 12/4/76 No Indication, 40-60% | 77- 27 15th Plate 12/4/76 No Eddy Current Flugged 2-B 124 42 12th Plate 12/4/76 No Indication, 40-60% | ||
No Similar to Left 2-B 118 52 12th Plate 12/4/76 No 124/42, 15% | No Similar to Left 2-B 118 52 12th Plate 12/4/76 No 124/42, 15% | ||
Line 134: | Line 91: | ||
21 , | 21 , | ||
2 2/14/77 Yes No Eddy Current Nailed 3-B 75 | 2 2/14/77 Yes No Eddy Current Nailed 3-B 75 | ||
m . | m . | ||
k-- CONEE'(CONT'D) ' ' | k-- CONEE'(CONT'D) ' ' | ||
Line 153: | Line 99: | ||
LANE - RO # (excludes leakers) ~ | LANE - RO # (excludes leakers) ~ | ||
_ . ' ..j ACTION - | _ . ' ..j ACTION - | ||
DATE TUBE JLEAKER CONDITION | DATE TUBE JLEAKER CONDITION | ||
- GENERATOR'. ROW , TUBE ELEVATION q. | - GENERATOR'. ROW , TUBE ELEVATION q. | ||
133 JRO-287/77-8' No Yes. ~90 Crack 6-1/8" Nailed. | 133 JRO-287/77-8' No Yes. ~90 Crack 6-1/8" Nailed. | ||
3-B T78' 1 f15th Plate-' 6/10/77' longitudinal | 3-B T78' 1 f15th Plate-' 6/10/77' longitudinal | ||
'120 Nailed R0-287 /77-10 Yes Yes 60 -90 ' Crack 2 Tubesheet 7/14/77-B . . 77 Nailed' | '120 Nailed R0-287 /77-10 Yes Yes 60 -90 ' Crack 2 Tubesheet 7/14/77-B . . 77 Nailed' 7/14/77 Yes .No ' | ||
:3-B. . 77 1- ' R0-270 /7 7 90 Crack Nailed Yes Yes 2-B ,77 25' Tubesheet'' 1/14/78 Eddy Current Plugged Yes No 1/14/78- Indication, SOAK 2-B 75 - 21 --- | |||
7/14/77 Yes .No ' | |||
:3-B. . 77 1- ' R0-270 /7 7 90 Crack Nailed Yes Yes 2-B ,77 25' Tubesheet'' 1/14/78 Eddy Current Plugged Yes No | |||
1/14/78- Indication, SOAK 2-B 75 - 21 --- | |||
Eddy Current Plugged Yes No 4 --- 1/14/78 Indication, SOAK B 77 Eddy Current Plugged Yes No 77 18 --- 1/14/78 Indication, SOAK . | Eddy Current Plugged Yes No 4 --- 1/14/78 Indication, SOAK B 77 Eddy Current Plugged Yes No 77 18 --- 1/14/78 Indication, SOAK . | ||
2-B- | 2-B-Eddy' Current Plugged Yes No 19 --- 1/14/78 Indication, SOAK 2-B 77 Eddy Current Plugged Yes No 21 --- 1/14/78 | ||
* Indication, SOAK 2-B 77 Eddy Current Plugged Yes No 4 -- 1/14/78 Indication, SOAK 2-B 78 Y | |||
Eddy' Current Plugged Yes No 19 --- 1/14/78 Indication, SOAK 2-B 77 | e O | ||
A . . . +.N .nes w .- | |||
Eddy Current Plugged Yes No 21 --- 1/14/78 | |||
* Indication, SOAK 2-B 77 Eddy Current Plugged Yes No 4 -- 1/14/78 Indication, SOAK 2-B 78 | |||
=>w = w .ese p e - | =>w = w .ese p e - | ||
.eembaspee 4e | .eembaspee 4e | ||
-m. | -m. | ||
e . e a U. S. Nuct EAR n g cutAT OMY Ceuuse,e, icy EXHIBIT A N aC FOR*d y,4 111H LICENSEE EVENT REPORT l j@ tettA s raWT OR TYPE ALL RECUIRED 14 FCAV AfiCW I l l l CcNTmot stocit: 1 i 101 0] | |||
e . e a | |||
101 0] | |||
4lll11111]@l j. lg $7 0.A 7 se JS @ 3 yCgt.sg tyrt JO lo lil in i e I n i elv 12j@16 01 01 -1010101 14 010 l UCt%gg nuassEM 7 8 9 UCteette COQ ( | 4lll11111]@l j. lg $7 0.A 7 se JS @ 3 yCgt.sg tyrt JO lo lil in i e I n i elv 12j@16 01 01 -1010101 14 010 l UCt%gg nuassEM 7 8 9 UCteette COQ ( | ||
y o.n | y o.n | ||
Line 192: | Line 121: | ||
l O I occ. s ir ,,uOl0 n. 1012 l 710.Ol_1 10 l O l7 17 I 7 ]@[0 | l O I occ. s ir ,,uOl0 n. 1012 l 710.Ol_1 10 l O l7 17 I 7 ]@[0 | ||
..,r cose*T 73 Md 3 | ..,r cose*T 73 Md 3 | ||
.. Evt r e rt lolil e e | .. Evt r e rt lolil e e h ified as coning 3 f EVENT DESCmFTION AND PRCS A8L$ CONSECUE**CESa primary-to-secondary leak wa o 2 l_On September 27. 1977 j down on October 7 for 21 days but the was begun on j QJ 2] I f rom the 2B OTSG.Another ' The unsuccessful unit was shut shutdown o 4 l_ leak could not he located. d stator the y During an unscheduled outage to repair a control ro y lo1511 November 3. 13 other tubes were 1eak was located an (the Icaking tube was plugged. (see ; | ||
h ified as coning 3 f EVENT DESCmFTION AND PRCS A8L$ CONSECUE**CESa primary-to-secondary leak wa o 2 l_On September 27. 1977 j down on October 7 for 21 days but the was begun on j QJ 2] I f rom the 2B OTSG.Another ' The unsuccessful unit was shut shutdown o 4 l_ leak could not he located. d stator the y During an unscheduled outage to repair a control ro y lo1511 November 3. 13 other tubes were 1eak was located an (the Icaking tube was plugged. (see ; | |||
@l This is the 13th OTSG tube Icak at Oconee | @l This is the 13th OTSG tube Icak at Oconee | ||
@ l_niunood or renlunned. i h d by the repairs. | @ l_niunood or renlunned. i h d by the repairs. | ||
* J QJ a j 1 attached). _The RC boundary was re-establ s e c v.tv e causs c c:ureusvt: ce succes a.. stecces | * J QJ a j 1 attached). _The RC boundary was re-establ s e c v.tv e causs c c:ureusvt: ce succes a.. stecces | ||
' '' ' sistiu coes scaess Cece cces os I,c 1 c l@ l,Ej@ | ' '' ' sistiu coes scaess Cece cces os I,c 1 c l@ l,Ej@ | ||
: i. i 3 u[u _J@ l 11l Tl E I X l Cl | : i. i 3 u[u _J@ l 11l Tl E I X l Cl OCCUAst%CE i. | ||
OCCUAst%CE i. | |||
mtPCMT n | mtPCMT n | ||
:o | :o | ||
Line 207: | Line 132: | ||
, . $20Vi=T1 AL aircat =o. | , . $20Vi=T1 AL aircat =o. | ||
y coes 10l 1l:s W [---j yu h ,"uarao 10 I 1 l 2l sa n j,y, ,, l!_avtur ve>a l- .-] : | y coes 10l 1l:s W [---j yu h ,"uarao 10 I 1 l 2l sa n j,y, ,, l!_avtur ve>a l- .-] : | ||
:s 2r r.:mr . x : m ::,, | :s 2r r.:mr . x : m ::,, | ||
L :.7 lu7l a 2 | L :.7 lu7l a 2 c r a . l 018l9. le3 )z.=w .t:x.. | ||
c r a . l 018l9. le3 )z.=w .t:x.. | |||
[lj@ [Lj@ (N_j@ In101115]@ ., | [lj@ [Lj@ (N_j@ In101115]@ ., | ||
L. Aj@ | L. Aj@ | ||
Line 219: | Line 141: | ||
LAdh | LAdh | ||
= = m u@ | = = m u@ | ||
The corrective action, CAcss cesemencN ANocometenvt AcncNs g i The cause of OTSG tube leaks at Oconec tisd tubes. undetermined. Future g the olunninn of leaking or previously instrumen e i | The corrective action, CAcss cesemencN ANocometenvt AcncNs g i The cause of OTSG tube leaks at Oconec tisd tubes. undetermined. Future g the olunninn of leaking or previously instrumen e i | ||
i l_taken was 3 gj l_ action will be determined by research now in progress. 1 1 | i l_taken was 3 gj l_ action will be determined by research now in progress. 1 1 | ||
Line 228: | Line 149: | ||
'NA l A [_jhI_ Onor, tor Observat ion so l 01 81 d @ l___ '' ** ** | 'NA l A [_jhI_ Onor, tor Observat ion so l 01 81 d @ l___ '' ** ** | ||
3 lEj@ | 3 lEj@ | ||
' 8,jnvnySrsvr c | ' 8,jnvnySrsvr c assovat oc acnvnv h tectrica ce .ett,se @ | ||
assovat oc acnvnv h tectrica ce .ett,se @ | |||
i | i | ||
=etresso o* = stress J l | =etresso o* = stress J l s^ 80 | ||
s^ 80 | |||
= | = | ||
* 8 L2J@ L2!el ** | * 8 L2J@ L2!el ** | ||
j | j | ||
' ' eenscu 'e*6 xposO nas ts eticanevo= @ | ' ' eenscu 'e*6 xposO nas ts eticanevo= @ | ||
=vuna = | =vuna = | ||
Line 245: | Line 161: | ||
' ' ' ,1..c,. d'..uv'.'.,u [ | ' ' ' ,1..c,. d'..uv'.'.,u [ | ||
esunsea m 0tScmitt1CM to fiTal l_ ni ol0j@ln nA , | esunsea m 0tScmitt1CM to fiTal l_ ni ol0j@ln nA , | ||
, ,. naCE To eaciuty 4033 Cs om ca I het Ct50p6p T10te " | |||
, ,. naCE To eaciuty | ur- NAC USE cNLY llJ.2Je t,_2J@l- io I' j liiiiiiiiiiii ,, | ||
i fit 51 L.xl@7"3c ,,ne;h33y,'"*"l Erel,,n,t i nn of unscheduled (704) 373-8197 outanes | |||
4033 Cs om ca I het Ct50p6p T10te " | |||
ur- NAC USE cNLY | |||
llJ.2Je t,_2J@l- io I' j liiiiiiiiiiii ,, | |||
i fit 51 L.xl@7"3c ,,ne;h33y,'"*"l Erel,,n,t i nn of unscheduled | |||
(704) 373-8197 outanes | |||
* e ee is __ | * e ee is __ | ||
, s cu ,, | , s cu ,, | ||
sauscrencrrasn_K. R. Wilson ! | sauscrencrrasn_K. R. Wilson ! | ||
#}} | #}} |
Revision as of 08:00, 1 February 2020
ML19317F329 | |
Person / Time | |
---|---|
Site: | Oconee ![]() |
Issue date: | 10/07/1977 |
From: | Ken Wilson DUKE POWER CO. |
To: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
Shared Package | |
ML19317F325 | List: |
References | |
LER-77-012-01X, LER-77-12-1X, NUDOCS 8001100704 | |
Download: ML19317F329 (7) | |
Text
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. f-Q v
DUKE POWER Ont!'A!W OCONCE Ut;IT 2 Report Number: R0-270/77-12 Occurrence'Date: October 7,1977
. Report Date: February 15, 1978 Facility: Unit 2, Seneca, South Carolina
~
Identifica' tion of Occurrence: Primary-to-Secondary Leak through B Once Through SteamcGenerator (OTSG)
Conditions Prior to Occurrence: 80 percent Full-Power Description of Occurrence:
' On September 27, 1977 air injector radiation monitor RIA-40 indicated a primary-to-secondary Icak of approximately 0.2 gpm. Power was reduced .
to 67 pc.rcent to ' reduce powdex contamination. Subsequently, because
~
of an apparently incrcasing Icak rate the unit was shut down on October 7, 1977. . Af ter a 21 day outage and several unsuccessful attempts to find the leak the unit was -returned to power operation on October 28, 1977. A second unsuccessful attempt to-locate the leak was made from November,3 to 12, 1977. On December 29, 1977 the unit was shut down to repair a-_ control rod stator, remove install.ed steam generator instrumentation 'and make -another attempt at 71 ocating the indicated leak. .Tub e-77-25 was discovered to be leaking. Fiber optic and eddy-current examinations indicated a 90 circumferential' crack near.
the upper tube sheet. The tube;was stabilized and plugged. The instrumented ' tubes (6), which showed considerable wall thinning, were also plugged A11 -(7) previously plugged tubes were re-plugged as a precautionary measure., Hydrostatic tests showed no further Icaks and the unit was- returned to power operation on January 16, 1978.
. ~.
Apparent Cause of.0ccurrence:
The exact cause of_tlue incident cannot be determined. The primary-to-secondary 11cak could have been _ caused.by either' tube 77-25 or any of '
the:seven replugged. tubes. The Nucicar Steam Supply System supplier, Babcock 'and Wilcox, and Duke Power Company are continuing to investigate the ' tube. leak problem. ' '
1 O
-m 6 Gi J f;
s
'80.01100 ] o
DI KE l'O',il:R Co*tt'ANY OCONCE UNIT 2 (Cont'd)
Analysis of Occurrence:
All liquid and gaseous waste releasts were controlled and accounted for within applicabic criteria. Plant personnel exposure totalled 11.48 man-rem. The reactor coolant boundary was re-established by the tube repair. Therefore, the health and safety of the public were not endan-gered.
Corrective Action:
Tube 77-25 was stabilized and plugged. Previously instrumented tubes which showed appreciable wall thinning were also plugged. All pre-viously plugged tubes were re-plugged.
5 4
9 e
t
- 4. __.
.1
SUMMARY
OF HAJOR OTSG TUBE EXPER1ENCE AT OCONEE~
.# TUBESLEXAMINED LANE. (excludes.. leakers) .
- ACTION RO# ,
1DATE TUBE . LEAKER CONDITION
- GENERATOR ROR . TUBE . ELEVATION
' R0-269/76-17 153
'ths . Crack Plugged
.17j Tubesheet ~10/31/76 Yes 1-AL '7 7 '
No . Distorted Eddy Plugged Tubesheet. 10/31/76 Yes-1-A 77 18 Current Signal R0-269/76-19 139 No Yes No Visual ' Nailed-1-B 114. 109- 14th. Plate 12/8/76 Inspection No Distorted Eddy- Plugged No 1-B 113 115
- 14th Plate 12/8/76 Currant Signal No No Similar to Nailed 1-B 113 110 14th Plate 12/8/76 114/109 .
Yes No 300 Crack Nailed 1-B ' 75 18 Tubesheet 12/8/76 Nailed R0-269/77-2 '140 1/15/77 Yes Yes 350 . Crack
- 1-B '75 12 .Tubesheet No Eddy Current Nailed .
1-B 81 128 Tubesheet 1/15/77 RNo Indication RO-269/77-8 3%
No Yes Eddy Current Nailed 1-B 32 13 14th Plate 2/28/77 I.ndication No No Eddy Current Nailed ,
1-B 33 14 14th Plate 2/28/77 Indication Eddy Current P.emoved 25 14th Plate 2/28/77 Yes No 1-B 77 Indication No Eddy Current Plugged 13th Plate 2/28/77 No 1-B 2 7 Indication ,
~
No No Eddy Current Plugged 1- 3 2 8 13th Plate 2/28/77 Indication No No Eddy Current Plugged 1- B 101 40 4th Plate 2/28/77 Indication
_ _1._
~
SUMMARY
OF MMOR OTSG TUBE EXPERIENCE AT OCONEE (CONT'D) .
- TUB'ES EXAMINED ..
LANE ACTION . ROP (excludes leakers)
TUBE. ELEVATION :DATE TUBE LEAKER CONDITION , ,
l GENERATOR ' ROW, 100 Yes Weld Crack Replugged R0-269/77-11 1-B - 77- 25 Tubesheet 3/22/77 .Yes Yes Distorted Plugged 1-BL .77 3,5,8' --- .3/22/77 1No Eddy Current
-Signal
- Plugged R0-269/77-16 507 5/7/77 Yes Yes Crack 1-B. 77 15. Tubesheet ,
No --- Removed 18 --- 5/7/77 Yes 1-B !77 ~
~No Distorted Plugged ,
5/7/77 -No ,
1-B ' 17 5 ---
- Eddy Current Signal Removed R0-270/76-15 133 Yes Yes 270 Crack, 2-B 77 23 Tubesheet 12/4/76 Hole Yes No Wear Appearance Removed 2-B ,
77- 27 15th Plate 12/4/76 No Eddy Current Flugged 2-B 124 42 12th Plate 12/4/76 No Indication, 40-60%
No Similar to Left 2-B 118 52 12th Plate 12/4/76 No 124/42, 15%
Plugged R0-287/76-10 9 11 15th Plate 7/21/76 Yes Yes No Visual 3-8 77 Inspection Nailed R0-287 /77-2 142 19 15th Plate 2/14/77 Yes .Yes Eddy Current 3-B 77 45 Crack 12,13,14,15 2/14/77 Yes No Eddy Current Nailed L3-8 77 16,17,18,20, .
21 ,
2 2/14/77 Yes No Eddy Current Nailed 3-B 75
m .
k-- CONEE'(CONT'D) ' '
SUMMARY
OF MAJOR OTSG TUBE EXPERIENCE AT O '# TUBES EXAMINED '
LANE - RO # (excludes leakers) ~
_ . ' ..j ACTION -
DATE TUBE JLEAKER CONDITION
- GENERATOR'. ROW , TUBE ELEVATION q.
133 JRO-287/77-8' No Yes. ~90 Crack 6-1/8" Nailed.
3-B T78' 1 f15th Plate-' 6/10/77' longitudinal
'120 Nailed R0-287 /77-10 Yes Yes 60 -90 ' Crack 2 Tubesheet 7/14/77-B . . 77 Nailed' 7/14/77 Yes .No '
- 3-B. . 77 1- ' R0-270 /7 7 90 Crack Nailed Yes Yes 2-B ,77 25' Tubesheet 1/14/78 Eddy Current Plugged Yes No 1/14/78- Indication, SOAK 2-B 75 - 21 ---
Eddy Current Plugged Yes No 4 --- 1/14/78 Indication, SOAK B 77 Eddy Current Plugged Yes No 77 18 --- 1/14/78 Indication, SOAK .
2-B-Eddy' Current Plugged Yes No 19 --- 1/14/78 Indication, SOAK 2-B 77 Eddy Current Plugged Yes No 21 --- 1/14/78
- Indication, SOAK 2-B 77 Eddy Current Plugged Yes No 4 -- 1/14/78 Indication, SOAK 2-B 78 Y
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e . e a U. S. Nuct EAR n g cutAT OMY Ceuuse,e, icy EXHIBIT A N aC FOR*d y,4 111H LICENSEE EVENT REPORT l j@ tettA s raWT OR TYPE ALL RECUIRED 14 FCAV AfiCW I l l l CcNTmot stocit: 1 i 101 0]
4lll11111]@l j. lg $7 0.A 7 se JS @ 3 yCgt.sg tyrt JO lo lil in i e I n i elv 12j@16 01 01 -1010101 14 010 l UCt%gg nuassEM 7 8 9 UCteette COQ (
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.. Evt r e rt lolil e e h ified as coning 3 f EVENT DESCmFTION AND PRCS A8L$ CONSECUE**CESa primary-to-secondary leak wa o 2 l_On September 27. 1977 j down on October 7 for 21 days but the was begun on j QJ 2] I f rom the 2B OTSG.Another ' The unsuccessful unit was shut shutdown o 4 l_ leak could not he located. d stator the y During an unscheduled outage to repair a control ro y lo1511 November 3. 13 other tubes were 1eak was located an (the Icaking tube was plugged. (see ;
@l This is the 13th OTSG tube Icak at Oconee
@ l_niunood or renlunned. i h d by the repairs.
- J QJ a j 1 attached). _The RC boundary was re-establ s e c v.tv e causs c c:ureusvt: ce succes a.. stecces
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The corrective action, CAcss cesemencN ANocometenvt AcncNs g i The cause of OTSG tube leaks at Oconec tisd tubes. undetermined. Future g the olunninn of leaking or previously instrumen e i
i l_taken was 3 gj l_ action will be determined by research now in progress. 1 1
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ur- NAC USE cNLY llJ.2Je t,_2J@l- io I' j liiiiiiiiiiii ,,
i fit 51 L.xl@7"3c ,,ne;h33y,'"*"l Erel,,n,t i nn of unscheduled (704) 373-8197 outanes
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sauscrencrrasn_K. R. Wilson !