05000270/LER-1977-012-01, /01X-0:on 770927,primary to Secondary Leak Found Coming from 2B once-through Steam Generator.Cause Undetermined.Leak Plugged
| ML19317F329 | |
| Person / Time | |
|---|---|
| Site: | Oconee |
| Issue date: | 10/07/1977 |
| From: | Ken Wilson DUKE POWER CO. |
| To: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| Shared Package | |
| ML19317F325 | List: |
| References | |
| LER-77-012-01X, LER-77-12-1X, NUDOCS 8001100704 | |
| Download: ML19317F329 (7) | |
| Event date: | |
|---|---|
| Report date: | |
| 2701977012R01 - NRC Website | |
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DUKE POWER Ont!'A!W OCONCE Ut;IT 2 Report Number:
R0-270/77-12 Occurrence'Date:
October 7,1977
. Report Date: February 15, 1978 Facility:
Unit 2, Seneca, South Carolina Identifica' tion of Occurrence:
Primary-to-Secondary Leak through B
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Once Through SteamcGenerator (OTSG)
Conditions Prior to Occurrence:
80 percent Full-Power Description of Occurrence:
' On September 27, 1977 air injector radiation monitor RIA-40 indicated a primary-to-secondary Icak of approximately 0.2 gpm.
Power was reduced to 67 pc.rcent to ' reduce powdex contamination. Subsequently, because of an apparently incrcasing Icak rate the unit was shut down on
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October 7, 1977.. Af ter a 21 day outage and several unsuccessful attempts to find the leak the unit was -returned to power operation on October 28, 1977. A second unsuccessful attempt to-locate the leak was made from November,3 to 12, 1977.
On December 29, 1977 the unit was shut down to repair a-_ control rod stator, remove install.ed steam generator instrumentation 'and make -another attempt at 17 ocating the indicated leak.
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.Tu e-77-25 was discovered to be leaking. Fiber optic and eddy-current examinations indicated a 90 circumferential' crack near.
the upper tube sheet. The tube;was stabilized and plugged.
The instrumented ' tubes (6), which showed considerable wall thinning, were also plugged A11 -(7) previously plugged tubes were re-plugged as a precautionary measure., Hydrostatic tests showed no further Icaks and the unit was-returned to power operation on January 16, 1978.
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Apparent Cause of.0ccurrence:
The exact cause of_tlue incident cannot be determined. The primary-to-secondary 11cak could have been _ caused.by either' tube 77-25 or any of the:seven replugged. tubes. The Nucicar Steam Supply System supplier, Babcock 'and Wilcox, and Duke Power Company are continuing to investigate the ' tube. leak problem. '
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DI KE l'O',il:R Co*tt'ANY OCONCE UNIT 2 (Cont'd)
Analysis of Occurrence:
All liquid and gaseous waste releasts were controlled and accounted for within applicabic criteria.
Plant personnel exposure totalled 11.48 man-rem.
The reactor coolant boundary was re-established by the tube repair. Therefore, the health and safety of the public were not endan-gered.
Corrective Action
Tube 77-25 was stabilized and plugged.
Previously instrumented tubes which showed appreciable wall thinning were also plugged. All pre-viously plugged tubes were re-plugged.
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.1 SUMMARY OF HAJOR OTSG TUBE EXPER1ENCE AT OCONEE~
.# TUBESLEXAMINED
- GENERATOR ROR. TUBE
. ELEVATION 1DATE TUBE. LEAKER CONDITION ACTION RO#
(excludes.. leakers)
LANE.
1-AL
'7 7 '
.17j Tubesheet
~10/31/76 Yes
'ths
. Crack Plugged
' R0-269/76-17 153 1-A 77 18 Tubesheet.
10/31/76 Yes-No
. Distorted Eddy Plugged Current Signal 1-B 114. 109-14th. Plate 12/8/76 No Yes No Visual
' Nailed-R0-269/76-19 139 Inspection 1-B 113 115 14th Plate 12/8/76 No No Distorted Eddy-Plugged Currant Signal 1-B 113 110 14th Plate 12/8/76 No No Similar to Nailed 114/109 1-B '
75 18 Tubesheet 12/8/76 Yes No 300 Crack Nailed
- 1-B
'75 12
.Tubesheet 1/15/77 Yes Yes 350. Crack Nailed R0-269/77-2
'140 1-B 81 128 Tubesheet 1/15/77 RNo No Eddy Current Nailed Indication 1-B 32 13 14th Plate 2/28/77 No Yes Eddy Current Nailed RO-269/77-8 3%
I.ndication 1-B 33 14 14th Plate 2/28/77 No No Eddy Current Nailed Indication 1-B 77 25 14th Plate 2/28/77 Yes No Eddy Current P.emoved Indication 1-B 2
7 13th Plate 2/28/77 No No Eddy Current Plugged Indication 1-3 2
8 13th Plate 2/28/77 No No Eddy Current Plugged
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Indication 1-B 101 40 4th Plate 2/28/77 No No Eddy Current Plugged Indication
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SUMMARY OF MMOR OTSG TUBE EXPERIENCE AT OCONEE (CONT'D).
- TUB'ES EXAMINED LANE l GENERATOR ' ROW, TUBE.
ELEVATION
- DATE TUBE LEAKER CONDITION ACTION
. ROP (excludes leakers) 1-B -
77-25 Tubesheet 3/22/77
.Yes Yes Weld Crack Replugged R0-269/77-11 100 1-BL
.77 3,5,8' ---
.3/22/77 Yes 1No Distorted Plugged Eddy Current
- - Signal 1-B.
77 15.
Tubesheet 5/7/77 Yes Yes Crack Plugged R0-269/77-16 507 Removed 5/7/77 Yes No 1-B
!77 ~
18 5/7/77
- - No
~No Distorted Plugged 1-B
' 17 5
Eddy Current Signal 2-B 77 23 Tubesheet 12/4/76 Yes Yes 270 Crack, Removed R0-270/76-15 133 Hole 2-B 77-27 15th Plate 12/4/76 Yes No Wear Appearance Removed 2-B 124 42 12th Plate 12/4/76 No No Eddy Current Flugged Indication, 40-60%
2-B 118 52 12th Plate 12/4/76 No No Similar to Left 124/42, 15%
3-8 77 11 15th Plate 7/21/76 Yes Yes No Visual Plugged R0-287/76-10 9
Inspection 3-B 77 19 15th Plate 2/14/77 Yes
.Yes Eddy Current Nailed R0-287 /77-2 142 45 Crack L3-8 77 12,13,14,15 2/14/77 Yes No Eddy Current Nailed 16,17,18,20, 21 3-B 75 2
2/14/77 Yes No Eddy Current Nailed
m CONEE'(CONT'D) k--
SUMMARY OF MAJOR OTSG TUBE EXPERIENCE AT O
'# TUBES EXAMINED '
(excludes leakers)
LANE ACTION
- - RO #
_. '..j
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TUBE JLEAKER CONDITION ELEVATION DATE
- - GENERATOR'. ROW, TUBE q.
133 JRO-287/77-8' 3-B T78' 1
f15th Plate-' 6/10/77' No Yes. ~90 Crack 6-1/8" Nailed.
longitudinal B..
77 2
Tubesheet 7/14/77-Yes Yes 60 -90 ' Crack Nailed R0-287 /77-10
'120 Nailed' 7/14/77 Yes
.No 2-B
,77 25' Tubesheet 1/14/78 Yes Yes 90 Crack Nailed
' R0-270 /7 7 :3-B.
. 77 1-1/14/78-Yes No Eddy Current Plugged Indication, SOAK 2-B 75 - 21 Plugged 1/14/78 Yes No Eddy Current Indication, SOAK B 77 4
1/14/78 Yes No Eddy Current Plugged Indication, SOAK 2-B-77 18 1/14/78 Yes No Eddy' Current Plugged Indication, SOAK 2-B 77 19 1/14/78 Yes No Eddy Current Plugged Indication, SOAK 2-B 77 21 1/14/78 Yes No Eddy Current Plugged Indication, SOAK 2-B 78 4
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EVENT DESCmFTION AND PRCS A8L$ CONSECUE**CESa primary-to-secondary leak wa e
e l_On September 27. 1977 down on October 7 for 21 days but the j
o 2 QJ 2] I f rom the 2B OTSG. ' The unit was shut was begun on j
Another unsuccessful shutdown l_ leak could not he located.
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During an unscheduled outage to repair a control ro o 4 lo1511 November 3.
13 other tubes were y
1eak was located an (the Icaking tube was plugged.
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