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{{#Wiki_filter:e e VIRGINIA ELECTRIC AND POWER COMPANY RICHMOND, VIRGINIA 23261 July 13, 1995 U. S. Nuclear Regulatory Commission Attention:
{{#Wiki_filter:e                               e VIRGINIA ELECTRIC AND POWER COMPANY RICHMOND, VIRGINIA 23261 July 13, 1995 U. S. Nuclear Regulatory Commission                       Serial No.      95-353 Attention: Document Control Desk                         NO/RPC:vlh Washington, D. C. 20555                                   Docket Nos. 50-280 50-281 License Nos. DPR-32 DPR-37 Gentlemen:
Document Control Desk Washington, D. C. 20555 Gentlemen:
VIRGINIA ELECTRIC AND POWER COMPANY SURRY POWER STATION UNITS 1 AND 2 MONTHLY OPERATING REPORT Enclosed is the Monthly Operating Report for Surry Power Station Units 1 and 2 for the month of June 1995.
VIRGINIA ELECTRIC AND POWER COMPANY SURRY POWER STATION UNITS 1 AND 2 MONTHLY OPERATING REPORT Serial No. NO/RPC:vlh Docket Nos. License Nos. 95-353 50-280 50-281 DPR-32 DPR-37 Enclosed is the Monthly Operating Report for Surry Power Station Units 1 and 2 for the month of June 1995. Very truly yours, )!lil;J,4 M. L. Bowling, Manager Nuclear Licensing  
Very truly yours,
& Programs Enclosure cc: U. S. Nuclear Regulatory Commission Region II 101 Marietta Street, N. W. Suite 2900 Atlanta, Georgia 30323 Mr. M. W. Branch NRC Senior Resident Inspector Surry Power Station 9507190316 950630 PDR ADDCK 05000280 R PDR VIRGINIA ELECTRIC AND POWER COMPANY SURRY POWER STATION MONTHLY OPERATING REPORT REPORT No. 95-06 Approved:
    )!lil;J,4 M. L. Bowling, Manager Nuclear Licensing & Programs Enclosure cc:     U. S. Nuclear Regulatory Commission Region II 101 Marietta Street, N. W.
7 -/ 0 -'i!" Station Manager Date TABLE OF CONTENTS Section e Surry Monthly Operating Report No. 95-06 Page 2 of 19 Page Operating Data Report -Unit No. 1 .........................................................................................................
Suite 2900 Atlanta, Georgia 30323 Mr. M. W. Branch NRC Senior Resident Inspector Surry Power Station 9507190316 950630 PDR ADDCK 05000280 R                   PDR
3 Operating Data Report -Unit No. 2 .............................................................
 
: ...........................................
VIRGINIA ELECTRIC AND POWER COMPANY SURRY POWER STATION MONTHLY OPERATING REPORT REPORT   No. 95-06 Approved:
4 Unit Shutdowns and Power Reductions  
7 - /0 - 'i!"
-Unit No. 1 ....................................................................................
Station Manager     Date
5 Unit Shutdowns and Power Reductions  
 
-Unit No. 2 ....................................................................................
e   Surry Monthly Operating Report No. 95-06 Page 2 of 19 TABLE OF CONTENTS Section                                                                                                                                  Page Operating Data Report - Unit No. 1 ......................................................................................................... 3 Operating Data Report - Unit No. 2 ............................................................. : ........................................... 4 Unit Shutdowns and Power Reductions - Unit No. 1.................................................................................... 5 Unit Shutdowns and Power Reductions - Unit No. 2 .................................................................................... 6 Average Daily Unit Power Level - Unit No. 1.............................................................................................. 7 Average Daily Unit Power Level - Unit No. 2 .............................................................................................. 8 Summary of Operating Experience - Unit No. 1 ......................................................................................... 9 Summary of Operating Experience - Unit No. 2 ...................................................................... : .................. 9 Facility Changes That Did Not Require N RC Approval. .............................................................................. 1O Procedure or Method of Operation Changes That Did Not Require NRC Approval ........................................... 13 Tests and Experiments That Did Not Require NRC Approval ...................................................................... 14 Chemistry Report ............................................................................................................................. 15 Fuel Handling - Unit No. 1 ................................................................................................................... 16 Fuel Handling - Unit No. 2 ................................................................................................................... 16 Description of Periodic Test(s) Which Were Not Completed Within the Time Limits Specified in Technical Specifications ................................................................................................... 19
6 Average Daily Unit Power Level -Unit No. 1 ..............................................................................................
 
7 Average Daily Unit Power Level -Unit No. 2 ..............................................................................................
                            --                                                           e Surry Monthly Operating Report No. 95-06 Page 3 of 19 OPERATING DATA REPORT Docket No.:   50-280 Date:    07-05-95 Completed By:    D. Mason Telephone:   (804) 365-2459
8 Summary of Operating Experience  
: 1. Unit Name: .................................................. . Surry Unit 1
-Unit No. 1 .........................................................................................
: 2. Reporting Period: ......................................... . June, 1995
9 Summary of Operating Experience  
: 3. Licensed Thermal Power (MWt): ..................... ..               2441
-Unit No. 2 ......................................................................
: 4. Nameplate Rating (Gross MWe): ..................... ..               847.5
: ..................
: 5. Design Electrical Rating (Net MWe): ................ ..               788
9 Facility Changes That Did Not Require N RC Approval.  
: 6. Maximum Dependable Capacity (Gross MWe): .. ..                       820
..............................................................................
: 7. Maximum Dependable Capacity (Net MWe): ....... .                     781
1 O Procedure or Method of Operation Changes That Did Not Require NRC Approval ...........................................
: 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons:
13 Tests and Experiments That Did Not Require NRC Approval ......................................................................
: 9. Power Level To Which Restricted, If Any (Net MWe):
14 Chemistry Report .............................................................................................................................
: 10. Reasons For Restrictions, If Any:
15 Fuel Handling -Unit No. 1 ...................................................................................................................
This Month             YTD               Cumulative
16 Fuel Handling -Unit No. 2 ...................................................................................................................
: 11. Hours In Reporting Period ..........................                 720.0             4343.0             197423.0
16 Description of Periodic Test(s) Which Were Not Completed Within the Time Limits Specified in Technical Specifications  
: 12. Number of Hours Reactor Was Critical ..........                     720.0             4163.7             134633.4
...................................................................................................
: 13. Reactor Reserve Shutdown Hours ...............                         0                   0                 3774.5
19 
: 14. Hours Generator On-Line ...........................                 720.0             4129.2             132370.2
--e Surry Monthly Operating Report No. 95-06 Page 3 of 19 OPERATING DATA REPORT Docket No.: Date: Completed By: 50-280 07-05-95 D. Mason Telephone:
: 15. Unit Reserve Shutdown Hours .....................                     0                   0                 3736.2
(804) 365-2459 1 . Unit Name: .................................................. . 2. Reporting Period: ......................................... . 3. Licensed Thermal Power (MWt): .....................  
: 16. Gross Thermal Energy Generated (MWH) ......                     1747854.0           9986716.5           308440455.7
.. 4. Nameplate Rating (Gross MWe): .....................  
: 17. Gross Electrical Energy Generated (MWH) ....                     580410.0           3353980.0           100967813.0
.. 5. Design Electrical Rating (Net MWe): ................  
: 18. Net Electrical Energy Generated (MWH) ........                   557758.0           3232842.0           95941865.0
.. 6. Maximum Dependable Capacity (Gross MWe): .. .. 7. Maximum Dependable Capacity (Net MWe): ....... . Surry Unit 1 June, 1995 2441 847.5 788 820 781 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons: 9. Power Level To Which Restricted, If Any (Net MWe): 10. Reasons For Restrictions, If Any: This Month YTD Cumulative
: 19. Unit Service Factor ...................................             100.0%               95.1%                 67.0%
: 11. Hours In Reporting Period ..........................
: 20. Unit Availability Factor ...............................             100.0%               95.1%                 68.9%
720.0 4343.0 197423.0 12. Number of Hours Reactor Was Critical ..........
: 21. Unit Capacity Factor (Using MDC Net) ...........                     99.2%               95.3%                 62.6%
720.0 4163.7 134633.4 13. Reactor Reserve Shutdown Hours ...............
: 22. Unit Capacity Factor (Using DER Net) ...........                     98.3%               94.5%                 61.7%
0 0 3774.5 14. Hours Generator On-Line ...........................
: 23. Unit Forced Outage Rate ............................                   0.0%               4.9%                 16.4%
720.0 4129.2 132370.2 15. Unit Reserve Shutdown Hours .....................
: 24. Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Each):
0 0 3736.2 16. Gross Thermal Energy Generated (MWH) ...... 1747854.0 9986716.5 308440455.7
Refueling, September 7, 1995, 37 Days
: 17. Gross Electrical Energy Generated (MWH) .... 580410.0 3353980.0 100967813.0
: 25. If Shut Down at End of Report Period, Estimated Date of Start-up:
: 18. Net Electrical Energy Generated (MWH) ........ 557758.0 3232842.0 95941865.0
: 19. Unit Service Factor ...................................
100.0% 95.1% 67.0% 20. Unit Availability Factor ...............................
100.0% 95.1% 68.9% 21. Unit Capacity Factor (Using MDC Net) ...........
99.2% 95.3% 62.6% 22. Unit Capacity Factor (Using DER Net) ...........
98.3% 94.5% 61.7% 23. Unit Forced Outage Rate ............................
0.0% 4.9% 16.4% 24. Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Each): Refueling, September 7, 1995, 37 Days 25. If Shut Down at End of Report Period, Estimated Date of Start-up:
: 26. Unit In Test Status (Prior to Commercial Operation):
: 26. Unit In Test Status (Prior to Commercial Operation):
FORECAST ACHIEVED INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION OPERATING DATA REPORT -urry Monthly Operating Report No. 95-06 Page 4 of 19 Docket No.: Date: Completed By: 50-281 07-05-95 D. Mason 1 . Unit Name: .................................................. . 2. Reporting Period: ......................................... . 3. Licensed Thermal Power (MWt): ...................... . 4. Nameplate Rating (Gross MWe): ...................... . 5. Design Electrical Rating (Net MWe): ................. . 6. Maximum Dependable Capacity (Gross MWe): .. .. 7. Maximum Dependable Capacity (Net MWe): ....... . Surry Unit 2 June, 1995 2441 847.5 788 820 781 Telephone:
FORECAST             ACHIEVED INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION
(804) 365-2459 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons: 9. Power Level To Which Restricted, If Any (Net MWe): 10. Reasons For Restrictions, If Any: This Month YTD Cumulative
 
: 11. Hours In Reporting Period ..........................
                                                                                          -urry Monthly Operating Report No. 95-06 Page 4 of 19 OPERATING DATA REPORT Docket No.:   50-281 Date:  07-05-95 Completed By:  D. Mason Telephone:  (804) 365-2459
720.0 4343.0 194303.0 12. Number of Hours Reactor Was Critical ..........
: 1. Unit Name: .................................................. . Surry Unit 2
665.4 3098.6 131436.1 13. Reactor Reserve Shutdown Hours ...............
: 2. Reporting Period: ......................................... . June, 1995
0 0 328.1 14. Hours Generator On-Line ...........................
: 3. Licensed Thermal Power (MWt): ...................... .               2441
659.9 3028.7 129495.8 15. Unit Reserve Shutdown Hours .....................
: 4. Nameplate Rating (Gross MWe): ...................... .               847.5
0 0 0 16. Gross Thermal Energy Generated (MWH) ...... 1596999.9 7159394.4 302427858.
: 5. Design Electrical Rating (Net MWe): ................. .               788
7 17. Gross Electrical Energy Generated (MWH) .... 526630.0 2383865.0 98826159.0
: 6. Maximum Dependable Capacity (Gross MWe): .. ..                       820
: 18. Net Electrical Energy Generated (MWH) ........ 506995.0 2297384.0 93890420.0
: 7. Maximum Dependable Capacity (Net MWe): ....... .                     781
: 19. Unit Service Factor ...................................
: 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons:
91.7% 69.7% 66.6% 20. Unit Availability Factor ...............................
: 9. Power Level To Which Restricted, If Any (Net MWe):
91.7% 69.7% 66.6% 21. Unit Capacity Factor (Using MDC Net) ...........
: 10. Reasons For Restrictions, If Any:
90.2% 67.7% 62.0% 22. Unit Capacity Factor (Using DER Net) ...........
This Month             YTD               Cumulative
89.4% 67.1% 61.3% 23. Unit Forced Outage Rate ............................
: 11. Hours In Reporting Period ..........................                 720.0             4343.0             194303.0
8.3% 6.4% 13.2% 24. Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Each): 25. If Shut Down at End of Report Period, Estimated Date of Start-up:
: 12. Number of Hours Reactor Was Critical ..........                     665.4             3098.6             131436.1
: 13. Reactor Reserve Shutdown Hours ...............                         0                   0                 328.1
: 14. Hours Generator On-Line ...........................                 659.9             3028.7             129495.8
: 15. Unit Reserve Shutdown Hours .....................                     0                   0                   0
: 16. Gross Thermal Energy Generated (MWH) ......                     1596999.9           7159394.4         302427858. 7
: 17. Gross Electrical Energy Generated (MWH) ....                     526630.0           2383865.0           98826159.0
: 18. Net Electrical Energy Generated (MWH) ........                   506995.0           2297384.0           93890420.0
: 19. Unit Service Factor ...................................               91.7%               69.7%               66.6%
: 20. Unit Availability Factor ...............................             91.7%               69.7%               66.6%
: 21. Unit Capacity Factor (Using MDC Net) ...........                     90.2%               67.7%               62.0%
: 22. Unit Capacity Factor (Using DER Net) ...........                     89.4%               67.1%               61.3%
: 23. Unit Forced Outage Rate ............................                   8.3%               6.4%               13.2%
: 24. Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Each):
: 25. If Shut Down at End of Report Period, Estimated Date of Start-up:
: 26. Unit In Test Status (Prior to Commercial Operation):
: 26. Unit In Test Status (Prior to Commercial Operation):
INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION FORECAST ACHIEVED e Surry Monthly Operating Report No. 95-06 Page 5 of 19 UNIT SHUTDOWN AND POWER REDUCTION
FORECAST            ACHIEVED INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION
{EQUAL TO OR GREATER THAN 20%) REPORT MONTH: June, 1995 (1) (2) (3) (4) (5) Method Docket No.: 50-280 Unit Name: Surry Unit 1 Date: 07-05-95 Completed by: Craig Olsen Telephone:
 
{804) 365-2155 Duration of LER System Component Cause & Corrective Action to Date Type Hours Reason Shutting No. Code Code Prevent Recurrence 950612 N/A N/A (1) F: Forced S: Scheduled B (2) REASON: Down Rx N/A N/A A -Equipment Failure (Explain)
e Surry Monthly Operating Report No. 95-06 Page 5 of 19 UNIT SHUTDOWN AND POWER REDUCTION
B Maintenance or Test C Refueling D Regulatory Restriction SG E Operator Training & Licensing Examination F Administrative G Operational Error (Explain)
{EQUAL TO OR GREATER THAN 20%)
(4) Exhibit G -Instructions for Preparation of Data Entry Sheets for Licensee Event Report (LER) File (NU REG 0161) RV Reduced power to facilitate replacement of condensate system relief valve, 1-CN-RV-113B. (3) METHOD: 1 -Manual 2 -Manual Scram. 3 -Automatic Scram. 4 -Other (Explain)
REPORT MONTH:   June, 1995 Docket No.:   50-280 Unit Name:   Surry Unit 1 Date: 07-05-95 Completed by:   Craig Olsen Telephone:   {804) 365-2155 (1)                  (2)        (3)                  (4)        (5)
(5) Exhibit 1 -Same Source.
Method Duration                   of       LER     System   Component   Cause & Corrective Action to Date     Type       Hours     Reason     Shutting     No.       Code       Code       Prevent Recurrence Down Rx 950612     N/A        N/A         B          N/A       N/A        SG        RV        Reduced power to facilitate replacement of condensate system relief valve, 1-CN-RV-113B.
(1) e Surry Monthly Operating Report No. 95-06 Page 6 of 19 UNIT SHUTDOWN AND POWER REDUCTION (EQUAL To OR GREATER THAN 20%) REPORT MONTH: June, 1995 Method (5) Docket No.: 50-281 Unit Name: Surry Unit 2 Date: 07-05-95 Completed by: Craig Olsen Telephone:
(1)                           (2)                                                    (3)
(804) 365-2155 Duration of LER System Component Cause & Corrective Action to Date Type Hours 950614 F 60.1 (1) F: Forced S: Scheduled Reason Shutting No. Code Down Rx A 3 2-95-EL 006-00 (2) REASON: A -Equipment Failure (Explain)
F:   Forced                 REASON:                                              METHOD:
B Maintenance or Test C Refueling D Regulatory Restriction Code Prevent Recurrence PMG Automatic reactor trip due to main transformer generator differential lockout. (3) METHOD: 1 -Manual 2 -Manual Scram. 3 -Automatic Scram. 4 -Other (Explain)
S:   Scheduled               A - Equipment Failure (Explain)                       1 - Manual B     Maintenance or Test                           2 - Manual Scram.
E Operator Training & Licensing Examination F Administrative G Operational Error (Explain)
C     Refueling                                     3 - Automatic Scram.
(4) Exhibit G -Instructions for Preparation of Data Entry Sheets for Licensee Event Report (LER) File (NUREG 0161) (5) Exhibit 1 -Same Source.
D     Regulatory Restriction                         4 - Other (Explain)
MONTH: June, 1995 Day 1 2 3 4 5 6 7 8 9 10 11 12 13 14 15 16 INSTRUCTIONS -urry Monthly Operating Report No. 95-06 Page 7 of 19 AVERAGE DAILY UNIT POWER LEVEL Average Daily Power Level (MWe-Net) Day 786 17 786 18 785 19 784 20 785 21 787 22 786 23 784 24 783 25 783 26 782 27 747 28 736 29 776 30 763
E     Operator Training & Licensing Examination F     Administrative G     Operational Error (Explain)
* 762 Docket No.: 50-280 Unit Name: Surry Unit 1 Date: 07-06-95 Completed by: Barry C. Bryant Telephone:
(4)                                                                                 (5)
(804) 365-2786 Average Daily Power Level (MWe-Net) 782 780 780 778 776 779 778 776 773 771 771 775 768 741 On this format, list the average daily unit power level in MWe -Net for each day in the reporting month. Compute to the nearest whole megawatt.
Exhibit G - Instructions for Preparation of Data Entry Sheets                     Exhibit 1 - Same Source.
MONTH: June, 1995 Day 2 3 4 5 6 7 8 9 10 11 12 13 14 15 16 INSTRUCTIONS e e Surry Monthly Operating Report No. 95-06 Page 8 of 19 AVERAGE DAILY UNIT POW.ER LEVEL Average Daily Power Level (MWe -Net) Day 774 17 759 18 778 19 776 20 776 21 777 22 775 23 773 24 772 25 771 26 761 27 776 28 780 29 462 30 0 0 Docket No.: 50-281 Unit Name: Surry Unit 2 Date: 07-06-95 Completed by: Barry C. Bryant Telephone:
for Licensee Event Report (LER) File (NU REG 0161)
(804) 365-2786 Average Daily Power Level (MWe -Net) 521 778 778 778 776 778 777 774 777 773 776 777 777 775 On this format, list the average daily unit power level in MWe -Net for each day in the reporting month. Compute to the nearest whole megawatt.
 
.urry Monthly Operating Report No. 95-06 Page 9 of 19  
e Surry Monthly Operating Report No. 95-06 Page 6 of 19 UNIT SHUTDOWN AND POWER REDUCTION (EQUAL To OR GREATER THAN 20%)
REPORT MONTH: June, 1995 Docket No.:   50-281 Unit Name:   Surry Unit 2 Date:   07-05-95 Completed by:   Craig Olsen Telephone:     (804) 365-2155 (1)                  ~          ~                  ~          (5)
Method Duration                 of       LER     System Component     Cause & Corrective Action to Date     Type       Hours     Reason   Shutting     No.     Code     Code      Prevent Recurrence Down Rx 950614      F      60.1        A         3       2     EL       PMG       Automatic reactor trip due to 006-00                          main transformer generator differential lockout.
(1)                          (2)                                                  (3)
F:  Forced                  REASON:                                            METHOD:
S:  Scheduled              A - Equipment Failure (Explain)                    1 - Manual B    Maintenance or Test                          2 - Manual Scram.
C    Refueling                                    3 - Automatic Scram.
D    Regulatory Restriction                        4 - Other (Explain)
E     Operator Training & Licensing Examination F     Administrative G     Operational Error (Explain)
(4)                                                                               (5)
Exhibit G - Instructions for Preparation of Data Entry Sheets                   Exhibit 1 - Same Source.
for Licensee Event Report (LER) File (NUREG 0161)
 
                                                                                    -urry Monthly Operating Report No. 95-06 Page 7 of 19 AVERAGE DAILY UNIT POWER LEVEL Docket No.:   50-280 Unit Name:   Surry Unit 1 Date: 07-06-95 Completed by:   Barry C. Bryant Telephone:   (804) 365-2786 MONTH:    June, 1995 Average Daily Power Level                          Average Daily Power Level Day                    (MWe- Net)                  Day                  (MWe- Net) 1                        786                      17                        782 2                        786                      18                        780 3                        785                      19                      780 4                        784                      20                        778 5                        785                      21                        776 6                        787                      22                        779 7                        786                      23                        778 8                        784                      24                        776 9                        783                      25                        773 10                        783                      26                        771 11                        782                      27                        771 12                        747                      28                        775 13                        736                      29                        768 14                        776                      30                      741 15                        763
* 16                        762 INSTRUCTIONS On this format, list the average daily unit power level in MWe - Net for each day in the reporting month. Compute to the nearest whole megawatt.
 
e                                                   e Surry Monthly Operating Report No. 95-06 Page 8 of 19 AVERAGE DAILY UNIT POW.ER LEVEL Docket No.:   50-281 Unit Name:   Surry Unit 2 Date: 07-06-95 Completed by:   Barry C. Bryant Telephone:   (804) 365-2786 MONTH:    June, 1995 Average Daily Power Level                         Average Daily Power Level Day                    (MWe - Net)                 Day                  (MWe - Net) 774                      17                        521 2                        759                      18                        778 3                        778                       19                      778 4                        776                      20                        778 5                        776                      21                        776 6                        777                      22                        778 7                        775                      23                        777 8                        773                      24                        774 9                        772                      25                        777 10                        771                      26                        773 11                        761                      27                        776 12                        776                      28                        777 13                        780                      29                        777 14                        462                      30                      775 15                          0 16                          0 INSTRUCTIONS On this format, list the average daily unit power level in MWe - Net for each day in the reporting month. Compute to the nearest whole megawatt.
 
                                                                                  .urry Monthly Operating Report No. 95-06 Page 9 of 19


==SUMMARY==
==SUMMARY==
OF OPERATING EXPERIENCE MONTHNEAR:
OF OPERATING EXPERIENCE MONTHNEAR: June, 1995 The following chronological sequence by unit is a summary of operating experiences for this month which required load reductions or resulted in significant non-load related incidents.
June, 1995 The following chronological sequence by unit is a summary of operating experiences for this month which required load reductions or resulted in significant non-load related incidents.
UNIT ONE:
UNIT ONE: 06/01/95 06/12/95 06/13/95 06/30/95 UNIT Two: 06/01/95 06/14/95 06/16/95 06/17/95 06/30/95 0000 1830 The reporting period began with the unit operating at 100% power, 825 MWe. Started power reduction to facilitate replacement of Condensate system relief valve RV-113B. 2004 Stopped power reduction at 78%, 630 MWe. 0520 Started power increase.
06/01/95         0000     The reporting period began with the unit operating at 100% power, 825 MWe.
0745 Stopped power increase at 100%, 820 MWe. 2400 The reporting period ended with the unit operating at 100% power, 820 MWe. 0000 The reporting period began with the unit operating at 100% power, 810 MWe. 1415 Automatic reactor trip due to main transformer generator differential lockout. 2050 Reactor critical.
06/12/95          1830    Started power reduction to facilitate replacement of Condensate system relief valve 1-CN-RV-113B.
0224 Generator on line. Started power increase.
2004     Stopped power reduction at 78%, 630 MWe.
0322 Stopped power increase at 26%, 180 MWe to perform main transformer testing. 0530 Started power increase.
06/13/95          0520     Started power increase.
1510 Stopped power increase at 100%, 820 MWe 2400 The reporting period ended with the unit operating at 100% power, 820 MWe.
0745     Stopped power increase at 100%, 820 MWe.
FS 94-37 DCP 87-009-2 DCP 87-023-2 DCP 87-021-3 e FACILITY CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTHNEAR:
06/30/95          2400     The reporting period ended with the unit operating at 100% power, 820 MWe.
June, 1995 Updated Final Safety Analysis Report Change (Safety Evaluation No. 95-061) Surry Monthly Operating Report No. 95-06 Page 10 of 19 6-01-95 UFSAR Change 94-37 revised Section 9.10, "Fire Protection," to indicate that other materials, as well as foam, are used to seal penetrations to achieve a three hour fire rating. The subject change was administrative in nature and did not involve physical changes to the plant. Therefore, an unreviewed safety question does not exist. Design Change Package (Safety Evaluation No. 91-037) 6-07-95 Design Change Package (DCP) 87-009-2 installed recirculation test piping, valves, and instrumentation to permit periodic full flow testing of the Unit 2 Auxiliary Feedwater (AFW) system pumps. The modification also allows (with operator action) AFW flow back to the emergency condensate storage tank when steam generator flow requirements decrease to less than the minimum recommended continuous flow for the AFW pumps. This modification does not affect the normal operation of the AFW pumps or the capability of the AFW system to perform its safety functions.
UNIT Two:
The recirculation piping will normally be isolated from the AFW system by administratively controlled valves. Therefore, an unreviewed safety question does not exist. Design Change Package 6-07-95 Design Change Package (DCP) 87-023-2 replaced the Unit 2 Recirculating Spray Heat Exchangers (RSHX), the outside RSHX discharge piping, and service water inlet piping elbows. The new heat exchangers and the originals are of like design with the same duty and pressure drop characteristics.
06/01/95          0000     The reporting period began with the unit operating at 100% power, 810 MWe.
The material composition of the new heat exchangers and associated piping is superior to that of the originals.
06/14/95          1415     Automatic reactor trip due to main transformer generator differential lockout.
The performance characteristics of the Recirculating Spray system was not altered by this DCP. Therefore, an unreviewed safety question does not exist. Design Change Package 6-08-95 Design Change Package (DCP) 87-021-3 replaced the Unit 1 and Unit 2 Bearing Cooling Heat Exchangers with larger capacity heat exchangers to increase the heat transfer rate. The new heat exchangers are similar to the design of the originals and meet the original temperature and pressure specifications.
06/16/95          2050     Reactor critical.
The function of the nonsafety-related Bearing Cooling system was not altered by this DCP. Therefore, an unreviewed safety question does not exist.
06/17/95          0224     Generator on line. Started power increase.
SE 95-064 DCP 87-008-1 DCP 87-028-1 FACILITY CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTHNEAR:
0322     Stopped power increase at 26%, 180 MWe to perform main transformer testing.
June, 1995 Safety Evaluation e Surry Monthly Operating Report No. 95-06 Page 11 of 19 6-16-95 Safety Evaluation 95-064 assessed the performance of Preventive Electrical Maintenance Procedure EMP-P-RT-209, "Protective Relay In Service Reading Procedure," to obtaining in-service readings from the Unit 2 main transformer differential relays, phase A, B, and C during power ascension following a unit start-up in June 1995. The evaluation concluded that this activity was acceptable.
0530     Started power increase.
The protective functions of the subject relays were disabled as the in-service readings were taken on each (one at a time) and back-up relaying was maintained to provide fault protection.
1510     Stopped power increase at 100%, 820 MWe 06/30/95          2400     The reporting period ended with the unit operating at 100% power, 820 MWe.
The activity did not affect the Electrical Distribution system or reduce the Technical Specifications margin of safety. Therefore, an unreviewed safety question does not exist. Design Change Package (Safety Evaluation No. 90-191) 6-20-95 Design Change Package (DCP) 87-008-1 installed recirculation test piping, valves, and instrumentation to permit periodic full flow testing of the Unit 1 Auxiliary Feedwater (AFW) system pumps. The modification also allows (with operator action) AFW flow back to the emergency condensate storage tank when steam generator flow requirements decrease to less than the minimum recommended continuous flow for the AFW pumps. This modification does not affect the normal operation of the AFW pumps or the capability of the AFW system to perform its safety functions.
 
The recirculation piping will normally be isolated from the AFW system by administratively controlled valves. Therefore, an unreviewed safety question does not exist. Design Change Package (Safety Evaluation No. 90-205) 6-20-95 Design Change Package (DCP) 87-028-1 replaced the Unit 1 Component Cooling Heat Exchangers 1-CC-E-1 A and 1-CC-E-1 B. The new heat exchangers and the originals are of like design with the same duty and pressure drop characteristics.
e  Surry Monthly Operating Report No. 95-06 Page 10 of 19 FACILITY CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTHNEAR: June, 1995 FS 94-37    Updated Final Safety Analysis Report Change                                         6-01-95 (Safety Evaluation No. 95-061)
The material composition of the new heat exchangers is superior to that of the originals.
UFSAR Change 94-37 revised Section 9.10, "Fire Protection," to indicate that other materials, as well as foam, are used to seal penetrations to achieve a three hour fire rating.
The performance characteristics of the Component Cooling system were not altered by this DCP. Therefore, an unreviewed safety question does not exist.
The subject change was administrative in nature and did not involve physical changes to the plant. Therefore, an unreviewed safety question does not exist.
TM S1-95-06 FS 95-24 FACILITY CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR:
DCP 87-009-2 Design Change Package                                                               6-07-95 (Safety Evaluation No. 91-037)
June, 1995 Temporary Modification (Safety Evaluation No. 95-066) -urry Monthly Operating Report No. 95-06 Page 12 of 19 6-27-95 Temporary Modification (TM) S1-95-06 installed a mechanical jumper to temporarily route the discharge of Fish Spray system pumps to a strainer inlet to facilitate the replacement of FS system piping. An operational check was performed to ensure the mechanical jumper could adequately support the operation of the nonsafety-related FS system. The TM did not affect related systems or components Therefore, an unreviewed safety question does not exist. Updated Final Safety Analysis Report Change (Safety Evaluation No. 95-073) 6-30-95 UFSAR Change 95-24 revised the Safety Analysis Limit (SAL) for the minimum Chemical Addition Tank inventory from 4200 gallons to 3800 gallons to be consistent with Engineering Standard STD-GN-0030.
Design Change Package (DCP) 87-009-2 installed recirculation test piping, valves, and instrumentation to permit periodic full flow testing of the Unit 2 Auxiliary Feedwater (AFW) system pumps. The modification also allows (with operator action) AFW flow back to the emergency condensate storage tank when steam generator flow requirements decrease to less than the minimum recommended continuous flow for the AFW pumps.
This modification does not affect the normal operation of the AFW pumps or the capability of the AFW system to perform its safety functions. The recirculation piping will normally be isolated from the AFW system by administratively controlled valves. Therefore, an unreviewed safety question does not exist.
DCP 87-023-2 Design Change Package                                                               6-07-95 Design Change Package (DCP) 87-023-2 replaced the Unit 2 Recirculating Spray Heat Exchangers (RSHX), the outside RSHX discharge piping, and service water inlet piping elbows.
The new heat exchangers and the originals are of like design with the same duty and pressure drop characteristics. The material composition of the new heat exchangers and associated piping is superior to that of the originals. The performance characteristics of the Recirculating Spray system was not altered by this DCP. Therefore, an unreviewed safety question does not exist.
DCP 87-021-3 Design Change Package                                                               6-08-95 Design Change Package (DCP) 87-021-3 replaced the Unit 1 and Unit 2 Bearing Cooling Heat Exchangers with larger capacity heat exchangers to increase the heat transfer rate.
The new heat exchangers are similar to the design of the originals and meet the original temperature and pressure specifications. The function of the nonsafety-related Bearing Cooling system was not altered by this DCP. Therefore, an unreviewed safety question does not exist.
 
e  Surry Monthly Operating Report No. 95-06 Page 11 of 19 FACILITY CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTHNEAR: June, 1995 SE 95-064    Safety     Evaluation                                                               6-16-95 Safety Evaluation 95-064 assessed the performance of Preventive Electrical Maintenance Procedure EMP-P-RT-209, "Protective Relay In Service Reading Procedure," to obtaining in-service readings from the Unit 2 main transformer differential relays, phase A, B, and C during power ascension following a unit start-up in June 1995.
The evaluation concluded that this activity was acceptable. The protective functions of the subject relays were disabled as the in-service readings were taken on each (one at a time) and back-up relaying was maintained to provide fault protection. The activity did not affect the Electrical Distribution system or reduce the Technical Specifications margin of safety. Therefore, an unreviewed safety question does not exist.
DCP 87-008-1 Design Change Package                                                               6-20-95 (Safety Evaluation No. 90-191)
Design Change Package (DCP) 87-008-1 installed recirculation test piping, valves, and instrumentation to permit periodic full flow testing of the Unit 1 Auxiliary Feedwater (AFW) system pumps. The modification also allows (with operator action) AFW flow back to the emergency condensate storage tank when steam generator flow requirements decrease to less than the minimum recommended continuous flow for the AFW pumps.
This modification does not affect the normal operation of the AFW pumps or the capability of the AFW system to perform its safety functions. The recirculation piping will normally be isolated from the AFW system by administratively controlled valves. Therefore, an unreviewed safety question does not exist.
DCP 87-028-1 Design Change Package                                                               6-20-95 (Safety Evaluation No. 90-205)
Design Change Package (DCP) 87-028-1 replaced the Unit 1 Component Cooling Heat Exchangers 1-CC-E-1 A and 1-CC-E-1 B.
The new heat exchangers and the originals are of like design with the same duty and pressure drop characteristics. The material composition of the new heat exchangers is superior to that of the originals. The performance characteristics of the Component Cooling system were not altered by this DCP. Therefore, an unreviewed safety question does not exist.
 
                                                                -urry Monthly Operating Report No. 95-06 Page 12 of 19 FACILITY CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR:   June, 1995 TM S1-95-06 Temporary Modification                                                             6-27-95 (Safety Evaluation No. 95-066)
Temporary Modification (TM) S1-95-06 installed a mechanical jumper to temporarily route the discharge of Fish Spray system pumps to a strainer inlet to facilitate the replacement of FS system piping.
An operational check was performed to ensure the mechanical jumper could adequately support the operation of the nonsafety-related FS system. The TM did not affect safety-related systems or components Therefore, an unreviewed safety question does not exist.
FS 95-24    Updated Final Safety Analysis Report Change                                         6-30-95 (Safety Evaluation No. 95-073)
UFSAR Change 95-24 revised the Safety Analysis Limit (SAL) for the minimum Chemical Addition Tank inventory from 4200 gallons to 3800 gallons to be consistent with Engineering Standard STD-GN-0030.
The SAL: change affected accident analysis assumptions and did not involve any physical changes to the plant. An engineering evaluation of the subject change concluded that affected accident analyses remain acceptable with no reduction in the Technical Specifications margin of safety. Therefore, an unreviewed safety question does not exist.
The SAL: change affected accident analysis assumptions and did not involve any physical changes to the plant. An engineering evaluation of the subject change concluded that affected accident analyses remain acceptable with no reduction in the Technical Specifications margin of safety. Therefore, an unreviewed safety question does not exist.
1 [2]-ES-3.2 1 [2]-E-3 1 [2]-ECA-3.1 1 [2]-ECA-3.2 1 [2]-ECA-3.3 O-TOP-4060 ROP-1.57 ROP-1.58 FS 95-23 1 [2]-DRP-003 1 [2]-PT-36 OC-3[4] e Surry Monthly Operating Report No. 95-06 Page 13 of 19 PROCEDURE OR METHOD OF OPERATION CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTHNEAR:
 
June, 1995 Emergency Operating Procedures (Safety Evaluation No. 95-060) 6-01-95 Emergency Procedures 1 [2]-ES-3.2, "Post-SGTR Cooldown Using Slowdown," 1 [2]-E-3, "Steam Generator Tube Rupture," 1 [2]-ECA-3.1, "SGTR with Loss of Reactor Coolant -Subcooled Recovery," 1 [2]-ECA-3.2, "SGTR with Loss of Reactor Coolant -Saturated Recovery," and 1 [2]-ECA-3.3, "SGTR Without Pressurizer Pressure Control," were revised to provide operational guidance for minimizing contamination of secondary systems in the event of a steam generator tube rupture (SGTR) and to provide a method to blow down a steam generator following such an event. These changes, which were made in response to SOER 93-1, improve the recovery capability following a SGTR event. The changes did not affect the accident analyses or reduce the Technical Specifications margin of safety. Therefore, an unreviewed safety question does not exist. Temporary Operating Procedure Radwaste Operating Procedures (Safety Evaluation No. 95-059) 6-01-95 Temporary Operating Procedure O-TOP-4060, "Chemical Waste Transfer from the Storage Area to the Radwaste Facility," was developed and Radwaste Operating Procedures ROP-1.57, "Installing Temporary Hose for Transferring S/G Cleaning Liquids to the SRF," and ROP-1.58, "Removing Temporary Hose Used to Transfer S/G Cleaning Liquids to the SRF," were revised to provide instructions for the installation and operation of a temporary piping and hose system to transfer liquid waste from temporary storage tanks at the Radiological Controlled Area yard to the Surry Radwaste Facility Liquid Waste system. The liquid waste was generated during the 1994 Unit 1 Steam Generator Chemical Cleaning outage. A spill control plan and procedures, in conjunction with dikes and berms to contain isolable leaks from the temporary storage tanks and piping, are in place to ensure compliance with effluent Technical Specifications.
e    Surry Monthly Operating Report No. 95-06 Page 13 of 19 PROCEDURE OR METHOD OF OPERATION CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTHNEAR: June, 1995 1[2]-ES-3.2   Emergency Operating Procedures                                                      6-01-95 1[2]-E-3     (Safety Evaluation No. 95-060) 1[2]-ECA-3.1 1[2]-ECA-3.2  Emergency Procedures 1[2]-ES-3.2, "Post-SGTR Cooldown Using Slowdown," 1[2]-E-3, 1[2]-ECA-3.3  "Steam Generator Tube Rupture," 1[2]-ECA-3.1, "SGTR with Loss of Reactor Coolant -
Therefore, an unreviewed safety question does not exist. Updated Final Safety Analysis Report Change Design Reference Procedures Operations Periodic Tests Operations Checklists (Safety Evaluation No. 95-070) 6-29-95 UFSAR Section 6.2.3.11.1, "Low-Head Safety Injection Pumps [NPSH Requirements]," Design Reference Procedures 1 [2]-DRP-003, "Curve Book," Operations Periodic Test 1 [2]-PT-36, "Instrument Surveillance," and Operations Checklists OC-3[4], "Containment Envelope Limits Check," were revised to reflect a change in the Refueling Water Storage Tank temperature lower limit from 40 °F to 33 °F. An engineering analysis of the subject change concluded that the minimum containment design pressure will not be exceeded with the appropriate adjustment in the containment air partial pressure.
Subcooled Recovery," 1[2]-ECA-3.2, "SGTR with Loss of Reactor Coolant - Saturated Recovery," and 1 [2]-ECA-3.3, "SGTR Without Pressurizer Pressure Control," were revised to provide operational guidance for minimizing contamination of secondary systems in the event of a steam generator tube rupture (SGTR) and to provide a method to blow down a steam generator following such an event.
Therefore, an unreviewed safety question does not exist. 
These changes, which were made in response to SOER 93-1, improve the recovery capability following a SGTR event. The changes did not affect the accident analyses or reduce the Technical Specifications margin of safety. Therefore, an unreviewed safety question does not exist.
-urry Monthly Operating Report No. 95-06 Page 14 of 19 TESTS AND EXPERIMENTS THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR:
O-TOP-4060    Temporary Operating Procedure                                                       6-01-95 ROP-1.57      Radwaste Operating Procedures ROP-1.58      (Safety Evaluation No. 95-059)
June, 1995 None During the Reporting Period CHEMISTRY REPORT MONTH/YEAR:
Temporary Operating Procedure O-TOP-4060, "Chemical Waste Transfer from the Storage Area to the Radwaste Facility," was developed and Radwaste Operating Procedures ROP-1.57, "Installing Temporary Hose for Transferring S/G Cleaning Liquids to the SRF," and ROP-1.58, "Removing Temporary Hose Used to Transfer S/G Cleaning Liquids to the SRF," were revised to provide instructions for the installation and operation of a temporary piping and hose system to transfer liquid waste from temporary storage tanks at the Radiological Controlled Area yard to the Surry Radwaste Facility Liquid Waste system.
June, 1995 Unit No. 1 Primary Coolant Analysis Max. Min. Avg. Gross Radioactivity, 11Ci/ml 3.54E-1 2.37E-1 2.91E-1 Suspended Solids, ppm 50.01 50.01 50.01 Gross Tritium, µCi/ml 1.29E-1 1.07E-1 1.16E-1 1131, µCi/ml 7.1 OE-4 4.34E-4 6.12E-4 113111133 0.08 0.06 0.07 Hydrogen, cc/kg 43.8 34.0 38.9 Lithium, ppm 1.71 1.16 1.47 Boron -10, ppm* 37.8 19.6 29.4 Oxygen, (DO), ppm 50.005 50.005 50.005 Chloride, ppm 0.004 50.001 0.001 pH at 25 degree Celsius 7.56 7.32 7.43 Boron -1 O = Total Boron x 0.196 Comments:
The liquid waste was generated during the 1994 Unit 1 Steam Generator Chemical Cleaning outage.
None e Surry Monthly Operating Report No. 95-06 Page 15 of 19 Unit No. 2 Max. Min. Avg. 2.18E-1 3.59E-3 1.52E-1 50.01 50.01 50.01 3.32E-1 2.19E-1 2.85E-1 1.82E-4 2.43E-5 1.07E-4 0.09 0.06 0.07 45.8 30.5 37.7 2.33 2.08 2.21 286 187 214 50.005 50.005 50.005 0.006 0.002 0.004 6.74 6.37 6.63 New or Spent Fuel Shipment Date Stored or Number Received New Fuel Unit 1 Batch 16 Shipment 1 6/27/95 6/29/95 FUEL HANDLING UNITS 1 & 2 MONTHNEAR:
A spill control plan and procedures, in conjunction with dikes and berms to contain non-isolable leaks from the temporary storage tanks and piping, are in place to ensure compliance with effluent Technical Specifications. Therefore, an unreviewed safety question does not exist.
June, 1995 Number of Assemblies Assembly ANSI eer Shiement Number Number 8 40A LM11J2 43A LM11J5 41A LM11J3 46A LM11J8 54A LM11JG 50A LM11JC 45A LM11J7 49A LM11JB 12 63A LM11JR 56A LM11JJ 53A LM11JF 60A LM11JN 03A LM11GZ 02A LM11GY 39A LM11J1 09A LM11H5 47A LM11J9 57A LM11JK 58A LM11JL 55A LM11JH e Surry Monthly Operating Report No. 95-06 Page 16 of 19 New or Spent Initial Fuel Shipping Enrichment Cask Activitl'.
FS 95-23      Updated Final Safety Analysis Report Change                                           6-29-95 1[2]-DRP-003  Design Reference Procedures 1[2]-PT-36    Operations Periodic Tests OC-3[4]       Operations Checklists (Safety Evaluation No. 95-070)
4.0079 10.14 Ci 4.0034 4.0159 4.0115 4.0022 4.0119 4.0009 4.0058 4.0110 14.94 Ci 4.0043 3.9960 4.0048 3.8039 3.8051 4.0118 3.8052 4.0109 3.9961 4.0067 4.0024
UFSAR Section 6.2.3.11.1, "Low-Head Safety Injection Pumps [NPSH Requirements],"
.. ... -' New or Spent Fuel Shipment Date Stored or Number Received Spent Fuel Cask CASTOR V/21 500.11-020 6/16/95 FUEL HANDLING UNITS 1 & 2 MONTH/YEAR:
Design Reference Procedures 1[2]-DRP-003, "Curve Book," Operations Periodic Test 1[2]-PT-36, "Instrument Surveillance," and Operations Checklists OC-3[4], "Containment Envelope Limits Check," were revised to reflect a change in the Refueling Water Storage Tank temperature lower limit from 40 °F to 33 °F.
June, 1995 Number of Assemblies Assembly ANSI eer Shiement Number Number 21 2A5 LM04TF OA1 LM04UT OA5 LM04TL 1A9 LM04TJ 1P5 LM05XC 2P3 LM05X7 3P6 LM05XV 3P7 LM05XR 3P8 LM05XT 4P1 LM09PC 4P9 LM05YU 2A8 LM04U3 5P1 LM05YF 5P9 LM05Y7 2A9 LM04UW 3A5 LM04V1 3A8 LM04UB OP6 LM05Y4 OP? LM05JX OP9 LM05XD 1PO LM05X8 e Surry Monthly Operating Report No. 95-06 Page 17 of 19 New or Spent Initial Fuel Shipping Enrichment Cask Activitl 3.393 N/A 2.901 2.901 2.901 3.607 3.607 3.607 3.607 3.607 3.607 3.607 3.393 3.607 3.607 3.393 3.393 3.393 3.607 3.607 3.607 3.607 
An engineering analysis of the subject change concluded that the minimum containment design pressure will not be exceeded with the appropriate adjustment in the containment air partial pressure. Therefore, an unreviewed safety question does not exist.
.. ' '
 
* New or Spent Fuel Shipment Date Stored or Number Received Spent Fuel Cask CASTOR V/21 500.11-024 6/28/95 FUEL HANDLING UNITS 1 & 2
                                                  -urry Monthly Operating Report No. 95-06 Page 14 of 19 TESTS AND EXPERIMENTS THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR: June, 1995 None During the Reporting Period
* MONTHNEAR:
 
June, 1995 Number of Assemblies Assembly ANSI eer Shiement Number Number 21 G09 LM01QC J37 LM035G J38 LM035S J39 LM035Q S24 LMOOVE 825 LMOOVQ J45 LM035H 5A7 LM04UM 826 LMOOVD 6A3 LM04UZ S27 LMOOVF S11 LMOOTV S31 LMOOVP C36 NOANSI 817 LMOOV7 J05 LM034F 818 LMOOV9 J19 LM035A J33 LM035F 821 LMOOVB 823 LMOOU8 e Surry Monthly Operating Report No. 95-06 Page 18 of 19 New or Spent Initial Fuel Shipping Enrichment Cask Activitz'.
e  Surry Monthly Operating Report No. 95-06 Page 15 of 19 CHEMISTRY REPORT MONTH/YEAR: June, 1995 Unit No. 1                      Unit No. 2 Primary Coolant Analysis          Max.        Min.        Avg. Max.        Min.        Avg.
2.111 N/A 2.902 2.902 2.902 2.606 2.606 2.902 3.393 2.606 3.393 2.606 2.606 2.606 3.117 2.606 2.902 2.606 2.902 2.902 2.606 2.606 
Gross Radioactivity, 11Ci/ml         3.54E-1     2.37E-1     2.91E-1 2.18E-1     3.59E-3      1.52E-1 Suspended Solids, ppm                  50.01      50.01      50.01  50.01        50.01        50.01 Gross Tritium, µCi/ml                1.29E-1    1.07E-1    1.16E-1 3.32E-1     2.19E-1     2.85E-1 1131, µCi/ml                          7.1 OE-4    4.34E-4    6.12E-4 1.82E-4      2.43E-5      1.07E-4 113111133                              0.08        0.06        0.07    0.09        0.06        0.07 Hydrogen, cc/kg                        43.8        34.0       38.9    45.8        30.5        37.7 Lithium, ppm                            1.71        1.16        1.47    2.33        2.08        2.21 Boron - 10, ppm*                        37.8        19.6        29.4    286          187          214 Oxygen, (DO), ppm                    50.005      50.005      50.005 50.005      50.005      50.005 Chloride, ppm                          0.004      50.001      0.001  0.006        0.002        0.004 pH at 25 degree Celsius                7.56        7.32        7.43    6.74        6.37         6.63 Boron - 1O = Total Boron x 0.196 Comments:
. Number e Surry Monthly Operating Report No. 95-06 Page 19 of 19 DESCRIPTION OF PERIODIC TEST(S) WHICH WERE NOT COMPLETED WITHIN THE TIME LIMITS SPECIFIED IN TECHNICAL SPECIFICATIONS MONTH/YEAR:
None
June, 1995 Title LER Number O-EPT-0102-01 Monthly Station Battery Cell Voltage Check 50-280/ 95-004-00}}
 
eSurry Monthly Operating Report No. 95-06 Page 16 of 19 FUEL HANDLING UNITS 1 & 2 MONTHNEAR: June, 1995 New or Spent                  Number of                                         New or Spent Fuel Shipment Date Stored or  Assemblies    Assembly       ANSI     Initial    Fuel Shipping Number      Received    eer Shiement     Number       Number Enrichment    Cask Activitl'.
New Fuel Unit 1 Batch 16 Shipment 1      6/27/95          8          40A        LM11J2    4.0079        10.14 Ci 43A        LM11J5    4.0034 41A        LM11J3    4.0159 46A        LM11J8    4.0115 54A        LM11JG    4.0022 50A        LM11JC    4.0119 45A        LM11J7    4.0009 49A        LM11JB    4.0058 6/29/95          12          63A        LM11JR    4.0110         14.94 Ci 56A        LM11JJ    4.0043 53A        LM11JF    3.9960 60A        LM11JN    4.0048 03A        LM11GZ    3.8039 02A        LM11GY    3.8051 39A        LM11J1    4.0118 09A        LM11H5    3.8052 47A        LM11J9    4.0109 57A        LM11JK    3.9961 58A        LM11JL    4.0067 55A        LM11JH    4.0024
 
..                                                                           eSurry Monthly Operating Report No. 95-06
        -
  ... '                                                                                       Page 17 of 19 FUEL HANDLING UNITS 1 & 2 MONTH/YEAR: June, 1995 New or Spent                  Number of                                          New or Spent Fuel Shipment Date Stored or Assemblies    Assembly        ANSI    Initial      Fuel Shipping Number      Received    eer Shiement    Number        Number  Enrichment    Cask Activitl Spent Fuel Cask CASTOR V/21 500.11-020 6/16/95         21          2A5          LM04TF    3.393            N/A OA1         LM04UT   2.901 OA5         LM04TL   2.901 1A9         LM04TJ   2.901 1P5        LM05XC     3.607 2P3         LM05X7   3.607 3P6         LM05XV   3.607 3P7         LM05XR   3.607 3P8         LM05XT   3.607 4P1         LM09PC   3.607 4P9         LM05YU   3.607 2A8         LM04U3   3.393 5P1         LM05YF   3.607 5P9         LM05Y7   3.607 2A9         LM04UW     3.393 3A5         LM04V1   3.393 3A8         LM04UB   3.393 OP6         LM05Y4   3.607 OP?         LM05JX   3.607 OP9         LM05XD   3.607 1PO         LM05X8   3.607
* eSurry Monthly Operating Report No. 95-06
..'
  '
FUEL HANDLING Page 18 of 19 UNITS 1 & 2
* MONTHNEAR: June, 1995 New or Spent                   Number of                                          New or Spent Fuel Shipment Date Stored or  Assemblies    Assembly        ANSI    Initial      Fuel Shipping Number      Received    eer Shiement    Number        Number  Enrichment     Cask Activitz'.
Spent Fuel Cask CASTOR V/21 500.11-024 6/28/95          21          G09        LM01QC    2.111            N/A J37        LM035G    2.902 J38          LM035S    2.902 J39        LM035Q    2.902 S24        LMOOVE    2.606 825        LMOOVQ    2.606 J45        LM035H    2.902 5A7        LM04UM    3.393 826        LMOOVD    2.606 6A3          LM04UZ    3.393 S27          LMOOVF    2.606 S11          LMOOTV    2.606 S31          LMOOVP    2.606 C36          NOANSI    3.117 817          LMOOV7    2.606 J05        LM034F    2.902 818          LMOOV9    2.606 J19        LM035A    2.902 J33        LM035F    2.902 821          LMOOVB    2.606 823          LMOOU8    2.606
 
.~
eSurry Monthly Operating Report No. 95-06 Page 19 of 19 DESCRIPTION OF PERIODIC TEST(S) WHICH WERE NOT COMPLETED WITHIN THE TIME LIMITS SPECIFIED IN TECHNICAL SPECIFICATIONS MONTH/YEAR: June, 1995 Number                                     Title                                  LER Number O-EPT-0102-01              Monthly Station Battery Cell Voltage Check                  50-280/
95-004-00}}

Revision as of 00:43, 21 October 2019

Monthly Operating Repts for June 1995 for Surry Power Station Units 1 & 2.W/950713 Ltr
ML18153A703
Person / Time
Site: Surry  Dominion icon.png
Issue date: 06/30/1995
From: Bryant B, Mason D, Olsen C
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
NUDOCS 9507190316
Download: ML18153A703 (20)


Text

e e VIRGINIA ELECTRIC AND POWER COMPANY RICHMOND, VIRGINIA 23261 July 13, 1995 U. S. Nuclear Regulatory Commission Serial No.95-353 Attention: Document Control Desk NO/RPC:vlh Washington, D. C. 20555 Docket Nos. 50-280 50-281 License Nos. DPR-32 DPR-37 Gentlemen:

VIRGINIA ELECTRIC AND POWER COMPANY SURRY POWER STATION UNITS 1 AND 2 MONTHLY OPERATING REPORT Enclosed is the Monthly Operating Report for Surry Power Station Units 1 and 2 for the month of June 1995.

Very truly yours,

)!lil;J,4 M. L. Bowling, Manager Nuclear Licensing & Programs Enclosure cc: U. S. Nuclear Regulatory Commission Region II 101 Marietta Street, N. W.

Suite 2900 Atlanta, Georgia 30323 Mr. M. W. Branch NRC Senior Resident Inspector Surry Power Station 9507190316 950630 PDR ADDCK 05000280 R PDR

VIRGINIA ELECTRIC AND POWER COMPANY SURRY POWER STATION MONTHLY OPERATING REPORT REPORT No. 95-06 Approved:

7 - /0 - 'i!"

Station Manager Date

e Surry Monthly Operating Report No. 95-06 Page 2 of 19 TABLE OF CONTENTS Section Page Operating Data Report - Unit No. 1 ......................................................................................................... 3 Operating Data Report - Unit No. 2 ............................................................. : ........................................... 4 Unit Shutdowns and Power Reductions - Unit No. 1.................................................................................... 5 Unit Shutdowns and Power Reductions - Unit No. 2 .................................................................................... 6 Average Daily Unit Power Level - Unit No. 1.............................................................................................. 7 Average Daily Unit Power Level - Unit No. 2 .............................................................................................. 8 Summary of Operating Experience - Unit No. 1 ......................................................................................... 9 Summary of Operating Experience - Unit No. 2 ...................................................................... : .................. 9 Facility Changes That Did Not Require N RC Approval. .............................................................................. 1O Procedure or Method of Operation Changes That Did Not Require NRC Approval ........................................... 13 Tests and Experiments That Did Not Require NRC Approval ...................................................................... 14 Chemistry Report ............................................................................................................................. 15 Fuel Handling - Unit No. 1 ................................................................................................................... 16 Fuel Handling - Unit No. 2 ................................................................................................................... 16 Description of Periodic Test(s) Which Were Not Completed Within the Time Limits Specified in Technical Specifications ................................................................................................... 19

-- e Surry Monthly Operating Report No. 95-06 Page 3 of 19 OPERATING DATA REPORT Docket No.: 50-280 Date: 07-05-95 Completed By: D. Mason Telephone: (804) 365-2459

1. Unit Name: .................................................. . Surry Unit 1
2. Reporting Period: ......................................... . June, 1995
3. Licensed Thermal Power (MWt): ..................... .. 2441
4. Nameplate Rating (Gross MWe): ..................... .. 847.5
5. Design Electrical Rating (Net MWe): ................ .. 788
6. Maximum Dependable Capacity (Gross MWe): .. .. 820
7. Maximum Dependable Capacity (Net MWe): ....... . 781
8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons:
9. Power Level To Which Restricted, If Any (Net MWe):
10. Reasons For Restrictions, If Any:

This Month YTD Cumulative

11. Hours In Reporting Period .......................... 720.0 4343.0 197423.0
12. Number of Hours Reactor Was Critical .......... 720.0 4163.7 134633.4
13. Reactor Reserve Shutdown Hours ............... 0 0 3774.5
14. Hours Generator On-Line ........................... 720.0 4129.2 132370.2
15. Unit Reserve Shutdown Hours ..................... 0 0 3736.2
16. Gross Thermal Energy Generated (MWH) ...... 1747854.0 9986716.5 308440455.7
17. Gross Electrical Energy Generated (MWH) .... 580410.0 3353980.0 100967813.0
18. Net Electrical Energy Generated (MWH) ........ 557758.0 3232842.0 95941865.0
19. Unit Service Factor ................................... 100.0% 95.1% 67.0%
20. Unit Availability Factor ............................... 100.0% 95.1% 68.9%
21. Unit Capacity Factor (Using MDC Net) ........... 99.2% 95.3% 62.6%
22. Unit Capacity Factor (Using DER Net) ........... 98.3% 94.5% 61.7%
23. Unit Forced Outage Rate ............................ 0.0% 4.9% 16.4%
24. Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Each):

Refueling, September 7, 1995, 37 Days

25. If Shut Down at End of Report Period, Estimated Date of Start-up:
26. Unit In Test Status (Prior to Commercial Operation):

FORECAST ACHIEVED INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION

-urry Monthly Operating Report No. 95-06 Page 4 of 19 OPERATING DATA REPORT Docket No.: 50-281 Date: 07-05-95 Completed By: D. Mason Telephone: (804) 365-2459

1. Unit Name: .................................................. . Surry Unit 2
2. Reporting Period: ......................................... . June, 1995
3. Licensed Thermal Power (MWt): ...................... . 2441
4. Nameplate Rating (Gross MWe): ...................... . 847.5
5. Design Electrical Rating (Net MWe): ................. . 788
6. Maximum Dependable Capacity (Gross MWe): .. .. 820
7. Maximum Dependable Capacity (Net MWe): ....... . 781
8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons:
9. Power Level To Which Restricted, If Any (Net MWe):
10. Reasons For Restrictions, If Any:

This Month YTD Cumulative

11. Hours In Reporting Period .......................... 720.0 4343.0 194303.0
12. Number of Hours Reactor Was Critical .......... 665.4 3098.6 131436.1
13. Reactor Reserve Shutdown Hours ............... 0 0 328.1
14. Hours Generator On-Line ........................... 659.9 3028.7 129495.8
15. Unit Reserve Shutdown Hours ..................... 0 0 0
16. Gross Thermal Energy Generated (MWH) ...... 1596999.9 7159394.4 302427858. 7
17. Gross Electrical Energy Generated (MWH) .... 526630.0 2383865.0 98826159.0
18. Net Electrical Energy Generated (MWH) ........ 506995.0 2297384.0 93890420.0
19. Unit Service Factor ................................... 91.7% 69.7% 66.6%
20. Unit Availability Factor ............................... 91.7% 69.7% 66.6%
21. Unit Capacity Factor (Using MDC Net) ........... 90.2% 67.7% 62.0%
22. Unit Capacity Factor (Using DER Net) ........... 89.4% 67.1% 61.3%
23. Unit Forced Outage Rate ............................ 8.3% 6.4% 13.2%
24. Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Each):
25. If Shut Down at End of Report Period, Estimated Date of Start-up:
26. Unit In Test Status (Prior to Commercial Operation):

FORECAST ACHIEVED INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION

e Surry Monthly Operating Report No. 95-06 Page 5 of 19 UNIT SHUTDOWN AND POWER REDUCTION

{EQUAL TO OR GREATER THAN 20%)

REPORT MONTH: June, 1995 Docket No.: 50-280 Unit Name: Surry Unit 1 Date: 07-05-95 Completed by: Craig Olsen Telephone: {804) 365-2155 (1) (2) (3) (4) (5)

Method Duration of LER System Component Cause & Corrective Action to Date Type Hours Reason Shutting No. Code Code Prevent Recurrence Down Rx 950612 N/A N/A B N/A N/A SG RV Reduced power to facilitate replacement of condensate system relief valve, 1-CN-RV-113B.

(1) (2) (3)

F: Forced REASON: METHOD:

S: Scheduled A - Equipment Failure (Explain) 1 - Manual B Maintenance or Test 2 - Manual Scram.

C Refueling 3 - Automatic Scram.

D Regulatory Restriction 4 - Other (Explain)

E Operator Training & Licensing Examination F Administrative G Operational Error (Explain)

(4) (5)

Exhibit G - Instructions for Preparation of Data Entry Sheets Exhibit 1 - Same Source.

for Licensee Event Report (LER) File (NU REG 0161)

e Surry Monthly Operating Report No. 95-06 Page 6 of 19 UNIT SHUTDOWN AND POWER REDUCTION (EQUAL To OR GREATER THAN 20%)

REPORT MONTH: June, 1995 Docket No.: 50-281 Unit Name: Surry Unit 2 Date: 07-05-95 Completed by: Craig Olsen Telephone: (804) 365-2155 (1) ~ ~ ~ (5)

Method Duration of LER System Component Cause & Corrective Action to Date Type Hours Reason Shutting No. Code Code Prevent Recurrence Down Rx 950614 F 60.1 A 3 2 EL PMG Automatic reactor trip due to 006-00 main transformer generator differential lockout.

(1) (2) (3)

F: Forced REASON: METHOD:

S: Scheduled A - Equipment Failure (Explain) 1 - Manual B Maintenance or Test 2 - Manual Scram.

C Refueling 3 - Automatic Scram.

D Regulatory Restriction 4 - Other (Explain)

E Operator Training & Licensing Examination F Administrative G Operational Error (Explain)

(4) (5)

Exhibit G - Instructions for Preparation of Data Entry Sheets Exhibit 1 - Same Source.

for Licensee Event Report (LER) File (NUREG 0161)

-urry Monthly Operating Report No. 95-06 Page 7 of 19 AVERAGE DAILY UNIT POWER LEVEL Docket No.: 50-280 Unit Name: Surry Unit 1 Date: 07-06-95 Completed by: Barry C. Bryant Telephone: (804) 365-2786 MONTH: June, 1995 Average Daily Power Level Average Daily Power Level Day (MWe- Net) Day (MWe- Net) 1 786 17 782 2 786 18 780 3 785 19 780 4 784 20 778 5 785 21 776 6 787 22 779 7 786 23 778 8 784 24 776 9 783 25 773 10 783 26 771 11 782 27 771 12 747 28 775 13 736 29 768 14 776 30 741 15 763

  • 16 762 INSTRUCTIONS On this format, list the average daily unit power level in MWe - Net for each day in the reporting month. Compute to the nearest whole megawatt.

e e Surry Monthly Operating Report No. 95-06 Page 8 of 19 AVERAGE DAILY UNIT POW.ER LEVEL Docket No.: 50-281 Unit Name: Surry Unit 2 Date: 07-06-95 Completed by: Barry C. Bryant Telephone: (804) 365-2786 MONTH: June, 1995 Average Daily Power Level Average Daily Power Level Day (MWe - Net) Day (MWe - Net) 774 17 521 2 759 18 778 3 778 19 778 4 776 20 778 5 776 21 776 6 777 22 778 7 775 23 777 8 773 24 774 9 772 25 777 10 771 26 773 11 761 27 776 12 776 28 777 13 780 29 777 14 462 30 775 15 0 16 0 INSTRUCTIONS On this format, list the average daily unit power level in MWe - Net for each day in the reporting month. Compute to the nearest whole megawatt.

.urry Monthly Operating Report No. 95-06 Page 9 of 19

SUMMARY

OF OPERATING EXPERIENCE MONTHNEAR: June, 1995 The following chronological sequence by unit is a summary of operating experiences for this month which required load reductions or resulted in significant non-load related incidents.

UNIT ONE:

06/01/95 0000 The reporting period began with the unit operating at 100% power, 825 MWe.

06/12/95 1830 Started power reduction to facilitate replacement of Condensate system relief valve 1-CN-RV-113B.

2004 Stopped power reduction at 78%, 630 MWe.

06/13/95 0520 Started power increase.

0745 Stopped power increase at 100%, 820 MWe.

06/30/95 2400 The reporting period ended with the unit operating at 100% power, 820 MWe.

UNIT Two:

06/01/95 0000 The reporting period began with the unit operating at 100% power, 810 MWe.

06/14/95 1415 Automatic reactor trip due to main transformer generator differential lockout.

06/16/95 2050 Reactor critical.

06/17/95 0224 Generator on line. Started power increase.

0322 Stopped power increase at 26%, 180 MWe to perform main transformer testing.

0530 Started power increase.

1510 Stopped power increase at 100%, 820 MWe 06/30/95 2400 The reporting period ended with the unit operating at 100% power, 820 MWe.

e Surry Monthly Operating Report No. 95-06 Page 10 of 19 FACILITY CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTHNEAR: June, 1995 FS 94-37 Updated Final Safety Analysis Report Change 6-01-95 (Safety Evaluation No.95-061)

UFSAR Change 94-37 revised Section 9.10, "Fire Protection," to indicate that other materials, as well as foam, are used to seal penetrations to achieve a three hour fire rating.

The subject change was administrative in nature and did not involve physical changes to the plant. Therefore, an unreviewed safety question does not exist.

DCP 87-009-2 Design Change Package 6-07-95 (Safety Evaluation No.91-037)

Design Change Package (DCP) 87-009-2 installed recirculation test piping, valves, and instrumentation to permit periodic full flow testing of the Unit 2 Auxiliary Feedwater (AFW) system pumps. The modification also allows (with operator action) AFW flow back to the emergency condensate storage tank when steam generator flow requirements decrease to less than the minimum recommended continuous flow for the AFW pumps.

This modification does not affect the normal operation of the AFW pumps or the capability of the AFW system to perform its safety functions. The recirculation piping will normally be isolated from the AFW system by administratively controlled valves. Therefore, an unreviewed safety question does not exist.

DCP 87-023-2 Design Change Package 6-07-95 Design Change Package (DCP) 87-023-2 replaced the Unit 2 Recirculating Spray Heat Exchangers (RSHX), the outside RSHX discharge piping, and service water inlet piping elbows.

The new heat exchangers and the originals are of like design with the same duty and pressure drop characteristics. The material composition of the new heat exchangers and associated piping is superior to that of the originals. The performance characteristics of the Recirculating Spray system was not altered by this DCP. Therefore, an unreviewed safety question does not exist.

DCP 87-021-3 Design Change Package 6-08-95 Design Change Package (DCP) 87-021-3 replaced the Unit 1 and Unit 2 Bearing Cooling Heat Exchangers with larger capacity heat exchangers to increase the heat transfer rate.

The new heat exchangers are similar to the design of the originals and meet the original temperature and pressure specifications. The function of the nonsafety-related Bearing Cooling system was not altered by this DCP. Therefore, an unreviewed safety question does not exist.

e Surry Monthly Operating Report No. 95-06 Page 11 of 19 FACILITY CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTHNEAR: June, 1995 SE 95-064 Safety Evaluation 6-16-95 Safety Evaluation 95-064 assessed the performance of Preventive Electrical Maintenance Procedure EMP-P-RT-209, "Protective Relay In Service Reading Procedure," to obtaining in-service readings from the Unit 2 main transformer differential relays, phase A, B, and C during power ascension following a unit start-up in June 1995.

The evaluation concluded that this activity was acceptable. The protective functions of the subject relays were disabled as the in-service readings were taken on each (one at a time) and back-up relaying was maintained to provide fault protection. The activity did not affect the Electrical Distribution system or reduce the Technical Specifications margin of safety. Therefore, an unreviewed safety question does not exist.

DCP 87-008-1 Design Change Package 6-20-95 (Safety Evaluation No.90-191)

Design Change Package (DCP) 87-008-1 installed recirculation test piping, valves, and instrumentation to permit periodic full flow testing of the Unit 1 Auxiliary Feedwater (AFW) system pumps. The modification also allows (with operator action) AFW flow back to the emergency condensate storage tank when steam generator flow requirements decrease to less than the minimum recommended continuous flow for the AFW pumps.

This modification does not affect the normal operation of the AFW pumps or the capability of the AFW system to perform its safety functions. The recirculation piping will normally be isolated from the AFW system by administratively controlled valves. Therefore, an unreviewed safety question does not exist.

DCP 87-028-1 Design Change Package 6-20-95 (Safety Evaluation No.90-205)

Design Change Package (DCP) 87-028-1 replaced the Unit 1 Component Cooling Heat Exchangers 1-CC-E-1 A and 1-CC-E-1 B.

The new heat exchangers and the originals are of like design with the same duty and pressure drop characteristics. The material composition of the new heat exchangers is superior to that of the originals. The performance characteristics of the Component Cooling system were not altered by this DCP. Therefore, an unreviewed safety question does not exist.

-urry Monthly Operating Report No. 95-06 Page 12 of 19 FACILITY CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR: June, 1995 TM S1-95-06 Temporary Modification 6-27-95 (Safety Evaluation No.95-066)

Temporary Modification (TM) S1-95-06 installed a mechanical jumper to temporarily route the discharge of Fish Spray system pumps to a strainer inlet to facilitate the replacement of FS system piping.

An operational check was performed to ensure the mechanical jumper could adequately support the operation of the nonsafety-related FS system. The TM did not affect safety-related systems or components Therefore, an unreviewed safety question does not exist.

FS 95-24 Updated Final Safety Analysis Report Change 6-30-95 (Safety Evaluation No.95-073)

UFSAR Change 95-24 revised the Safety Analysis Limit (SAL) for the minimum Chemical Addition Tank inventory from 4200 gallons to 3800 gallons to be consistent with Engineering Standard STD-GN-0030.

The SAL: change affected accident analysis assumptions and did not involve any physical changes to the plant. An engineering evaluation of the subject change concluded that affected accident analyses remain acceptable with no reduction in the Technical Specifications margin of safety. Therefore, an unreviewed safety question does not exist.

e Surry Monthly Operating Report No. 95-06 Page 13 of 19 PROCEDURE OR METHOD OF OPERATION CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTHNEAR: June, 1995 1[2]-ES-3.2 Emergency Operating Procedures 6-01-95 1[2]-E-3 (Safety Evaluation No.95-060) 1[2]-ECA-3.1 1[2]-ECA-3.2 Emergency Procedures 1[2]-ES-3.2, "Post-SGTR Cooldown Using Slowdown," 1[2]-E-3, 1[2]-ECA-3.3 "Steam Generator Tube Rupture," 1[2]-ECA-3.1, "SGTR with Loss of Reactor Coolant -

Subcooled Recovery," 1[2]-ECA-3.2, "SGTR with Loss of Reactor Coolant - Saturated Recovery," and 1 [2]-ECA-3.3, "SGTR Without Pressurizer Pressure Control," were revised to provide operational guidance for minimizing contamination of secondary systems in the event of a steam generator tube rupture (SGTR) and to provide a method to blow down a steam generator following such an event.

These changes, which were made in response to SOER 93-1, improve the recovery capability following a SGTR event. The changes did not affect the accident analyses or reduce the Technical Specifications margin of safety. Therefore, an unreviewed safety question does not exist.

O-TOP-4060 Temporary Operating Procedure 6-01-95 ROP-1.57 Radwaste Operating Procedures ROP-1.58 (Safety Evaluation No.95-059)

Temporary Operating Procedure O-TOP-4060, "Chemical Waste Transfer from the Storage Area to the Radwaste Facility," was developed and Radwaste Operating Procedures ROP-1.57, "Installing Temporary Hose for Transferring S/G Cleaning Liquids to the SRF," and ROP-1.58, "Removing Temporary Hose Used to Transfer S/G Cleaning Liquids to the SRF," were revised to provide instructions for the installation and operation of a temporary piping and hose system to transfer liquid waste from temporary storage tanks at the Radiological Controlled Area yard to the Surry Radwaste Facility Liquid Waste system.

The liquid waste was generated during the 1994 Unit 1 Steam Generator Chemical Cleaning outage.

A spill control plan and procedures, in conjunction with dikes and berms to contain non-isolable leaks from the temporary storage tanks and piping, are in place to ensure compliance with effluent Technical Specifications. Therefore, an unreviewed safety question does not exist.

FS 95-23 Updated Final Safety Analysis Report Change 6-29-95 1[2]-DRP-003 Design Reference Procedures 1[2]-PT-36 Operations Periodic Tests OC-3[4] Operations Checklists (Safety Evaluation No.95-070)

UFSAR Section 6.2.3.11.1, "Low-Head Safety Injection Pumps [NPSH Requirements],"

Design Reference Procedures 1[2]-DRP-003, "Curve Book," Operations Periodic Test 1[2]-PT-36, "Instrument Surveillance," and Operations Checklists OC-3[4], "Containment Envelope Limits Check," were revised to reflect a change in the Refueling Water Storage Tank temperature lower limit from 40 °F to 33 °F.

An engineering analysis of the subject change concluded that the minimum containment design pressure will not be exceeded with the appropriate adjustment in the containment air partial pressure. Therefore, an unreviewed safety question does not exist.

-urry Monthly Operating Report No. 95-06 Page 14 of 19 TESTS AND EXPERIMENTS THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR: June, 1995 None During the Reporting Period

e Surry Monthly Operating Report No. 95-06 Page 15 of 19 CHEMISTRY REPORT MONTH/YEAR: June, 1995 Unit No. 1 Unit No. 2 Primary Coolant Analysis Max. Min. Avg. Max. Min. Avg.

Gross Radioactivity, 11Ci/ml 3.54E-1 2.37E-1 2.91E-1 2.18E-1 3.59E-3 1.52E-1 Suspended Solids, ppm 50.01 50.01 50.01 50.01 50.01 50.01 Gross Tritium, µCi/ml 1.29E-1 1.07E-1 1.16E-1 3.32E-1 2.19E-1 2.85E-1 1131, µCi/ml 7.1 OE-4 4.34E-4 6.12E-4 1.82E-4 2.43E-5 1.07E-4 113111133 0.08 0.06 0.07 0.09 0.06 0.07 Hydrogen, cc/kg 43.8 34.0 38.9 45.8 30.5 37.7 Lithium, ppm 1.71 1.16 1.47 2.33 2.08 2.21 Boron - 10, ppm* 37.8 19.6 29.4 286 187 214 Oxygen, (DO), ppm 50.005 50.005 50.005 50.005 50.005 50.005 Chloride, ppm 0.004 50.001 0.001 0.006 0.002 0.004 pH at 25 degree Celsius 7.56 7.32 7.43 6.74 6.37 6.63 Boron - 1O = Total Boron x 0.196 Comments:

None

eSurry Monthly Operating Report No. 95-06 Page 16 of 19 FUEL HANDLING UNITS 1 & 2 MONTHNEAR: June, 1995 New or Spent Number of New or Spent Fuel Shipment Date Stored or Assemblies Assembly ANSI Initial Fuel Shipping Number Received eer Shiement Number Number Enrichment Cask Activitl'.

New Fuel Unit 1 Batch 16 Shipment 1 6/27/95 8 40A LM11J2 4.0079 10.14 Ci 43A LM11J5 4.0034 41A LM11J3 4.0159 46A LM11J8 4.0115 54A LM11JG 4.0022 50A LM11JC 4.0119 45A LM11J7 4.0009 49A LM11JB 4.0058 6/29/95 12 63A LM11JR 4.0110 14.94 Ci 56A LM11JJ 4.0043 53A LM11JF 3.9960 60A LM11JN 4.0048 03A LM11GZ 3.8039 02A LM11GY 3.8051 39A LM11J1 4.0118 09A LM11H5 3.8052 47A LM11J9 4.0109 57A LM11JK 3.9961 58A LM11JL 4.0067 55A LM11JH 4.0024

.. eSurry Monthly Operating Report No. 95-06

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... ' Page 17 of 19 FUEL HANDLING UNITS 1 & 2 MONTH/YEAR: June, 1995 New or Spent Number of New or Spent Fuel Shipment Date Stored or Assemblies Assembly ANSI Initial Fuel Shipping Number Received eer Shiement Number Number Enrichment Cask Activitl Spent Fuel Cask CASTOR V/21 500.11-020 6/16/95 21 2A5 LM04TF 3.393 N/A OA1 LM04UT 2.901 OA5 LM04TL 2.901 1A9 LM04TJ 2.901 1P5 LM05XC 3.607 2P3 LM05X7 3.607 3P6 LM05XV 3.607 3P7 LM05XR 3.607 3P8 LM05XT 3.607 4P1 LM09PC 3.607 4P9 LM05YU 3.607 2A8 LM04U3 3.393 5P1 LM05YF 3.607 5P9 LM05Y7 3.607 2A9 LM04UW 3.393 3A5 LM04V1 3.393 3A8 LM04UB 3.393 OP6 LM05Y4 3.607 OP? LM05JX 3.607 OP9 LM05XD 3.607 1PO LM05X8 3.607

  • eSurry Monthly Operating Report No. 95-06

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FUEL HANDLING Page 18 of 19 UNITS 1 & 2

  • MONTHNEAR: June, 1995 New or Spent Number of New or Spent Fuel Shipment Date Stored or Assemblies Assembly ANSI Initial Fuel Shipping Number Received eer Shiement Number Number Enrichment Cask Activitz'.

Spent Fuel Cask CASTOR V/21 500.11-024 6/28/95 21 G09 LM01QC 2.111 N/A J37 LM035G 2.902 J38 LM035S 2.902 J39 LM035Q 2.902 S24 LMOOVE 2.606 825 LMOOVQ 2.606 J45 LM035H 2.902 5A7 LM04UM 3.393 826 LMOOVD 2.606 6A3 LM04UZ 3.393 S27 LMOOVF 2.606 S11 LMOOTV 2.606 S31 LMOOVP 2.606 C36 NOANSI 3.117 817 LMOOV7 2.606 J05 LM034F 2.902 818 LMOOV9 2.606 J19 LM035A 2.902 J33 LM035F 2.902 821 LMOOVB 2.606 823 LMOOU8 2.606

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eSurry Monthly Operating Report No. 95-06 Page 19 of 19 DESCRIPTION OF PERIODIC TEST(S) WHICH WERE NOT COMPLETED WITHIN THE TIME LIMITS SPECIFIED IN TECHNICAL SPECIFICATIONS MONTH/YEAR: June, 1995 Number Title LER Number O-EPT-0102-01 Monthly Station Battery Cell Voltage Check 50-280/

95-004-00