ML18139A866: Difference between revisions

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| issue date = 11/01/1980
| issue date = 11/01/1980
| title = LER 80-036/03L-0:on 801101,discovered That MOV-FW-251B Could Not Be Closed from Control Room.Caused by Misplacement of Limitorque Cover & Three Broken Control Wires.Cover & Wires Replaced
| title = LER 80-036/03L-0:on 801101,discovered That MOV-FW-251B Could Not Be Closed from Control Room.Caused by Misplacement of Limitorque Cover & Three Broken Control Wires.Cover & Wires Replaced
| author name = WILSON J L
| author name = Wilson J
| author affiliation = VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
| author affiliation = VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
| addressee name =  
| addressee name =  

Revision as of 06:58, 17 June 2019

LER 80-036/03L-0:on 801101,discovered That MOV-FW-251B Could Not Be Closed from Control Room.Caused by Misplacement of Limitorque Cover & Three Broken Control Wires.Cover & Wires Replaced
ML18139A866
Person / Time
Site: Surry Dominion icon.png
Issue date: 11/01/1980
From: Joshua Wilson
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML18139A865 List:
References
LER-80-036-03L-02, LER-80-36-3L-2, NUDOCS 8012030723
Download: ML18139A866 (2)


Text

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_COMMISSION

  • LICENSEE EVENT REPORT A COl\'7RD:..

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C TI I V I A I s I p Is 1 2 101 ° I O I -I O I O I O I O I O I-1° I O 101 4 1 1 1 1 1 1 1 1 101 I I © 8 9 LICENSEE CODE 1.t. 1S LICENSE NUMBER 2S 26 LICENSE TYPE 30 57 CAT SB ON'T 8 :;:~~~ ~I o I s I o I o I o I 2 I s 11 101 11 11 o 111 s I o l©J 1 11 Io 11 1 s i o I G) 60 61 DOCKET NUMBER 68 69 EVENT DATE 74 7S REPORT DATE 80 EVENT DESCRIPTIDN AND PROBABLE CONSEQUENCES

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  • I With the unit at hot shutdown, it was'-di.scovered that MOV-FW-251B could not be closed fran the Control Room. Th-i.s event is reportable per T.S. 6.6.2.b. (2). Nonnal feed control was Js~lishetl and the auxiliary feedwater system was secured. Hence, MOV-FW-LE] I . . . 251B was not requiretl to.be closetl to control steam generator level. Therefore, the health and safety of the public were not affectetl.

SYSTEM CODE ,c jH I@ 9 10 c:;.... LE R/RO LVENT YEAR v.:.J REPORT 1 8 i O i NUMBER 21 . 22 CAUSE CAUSE COMP. CODE . SUBCODE COMPONENT CODE SUBCODE ~@ l.£...1@ IVIAjLIVIE IX I@ LI 11 12 13 18 19 SEQUENTIAL OCCURRENCE REPORT REPORT NO. CODE TYPE VALVE SUBCOOE ~@ 20 I I 10 I 3 l 6 I I ......-1 10 13 I Ll.l I I 23 24 26 27 28 29 30 31 -REVISION NO. LQ_J 32 80 ACTION FUTURE EFFECT SHUTDOWN r:;;:;.. ATTACHMENT NPR04 PRIME COMP. TAKEN ACTION ON PLANT METHO_D HOURS SUBMITTED FORM SUB. SUPPLIER _COMPONENT MANUFACTURER

@J@l!.J@ W@ ~ *1 o Io Io Io I I.LJ@-. LliJ@) ~@ 33 34 . 3S 36 37 40 41 . 42 43 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS @ lw I o! 3 lo I 44 47 !The limitorque cover was found not to be placetl and three control wires brolcen. The IDJ I r~on for the cover not being placeo and wires broken can not be dete:rmineo.

These I wires* were replaced and the valve testetl satisfactorily.

The cover was also replacetl.

Im -ill] :ill] 8 9 FACILITY . 'Jo' STATUS % POWER OTHER STATUS 1-:::::J QI] ~J@ I O I O I O l@'"-1 _N_/A ___ _ METHOD OF . A DISCOVERY

-DISCOVERY DESCRIPTION

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80 8 9 ,, 12 . LOSS OF 0~ DAMAGE TO FACILITY '4J' *.,

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  • ATI'ACHMENT 1 (PAGE 1 OF 1. SURRY POWER STATION, UNIT 2 DOCKET NO; 50-281 REPORI' NO; 80-036/031r-0 EVENT ,DATE: 11-01-80 SUBJECT':

MOV-FW-251B INOPERABLE

1. EVENT DESCRIPI'ION:

' With the unit at hot shutdown following a reactor trip, MOV-FW-251B was in a position to fulfill its required safety function, subsequently it*was discovered that MOV-FW-251B would not respond to control switch operation.

'Ibis event is reportable per T.S. 6.6.2.b.(2).

2. PROBABLE *cON~S: This valve is one of six valves that are used to control steam generator level when the auxiliary feedwater systan is in operation.

With MOV-Th,._251B failed in the open position, existing procedures provide for on-off control of aux. feed pumps to control S/G level. Hc:wever, long before this was necessary, nonnal feed was re-established and the auxiliary feed systanwas removed from service. Therefore, the health and safety of the public were not affected.

3. CAUSE: The limitorque cover was found not to be placed and three control wires broken. The reason for the cover not being placed and wire broken can not be detennined.
4. IMMEDIATE (X)RREx::'I'IVE ACI'ION: The imnediate corrective action:was to transfer steam generator level control to. the main feed system. 5. -SUBSEOOENT
  • coRREx::TIVE ACI'ION: The subsequent corrective action was to repair the broken wires and replace the cover. The MOV was subsequently tested satisfactorily.
6. ACI'ION TAKEN 'TO PREVEm' 'RECURRENCE:

None. 7. GENERIC IMPLICATIONS:

None.