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{{#Wiki_filter:This report provides the results the Accident Sequence Precursor (ASP) Program for 2021. In addition, trends and key insights are provided for the past 10 years (2012 through 2021 ).
{{#Wiki_filter:0 This report provides the results the Accident Sequence Precursor (ASP) Program for 2021. In addition, trends and key insights are provided for the past 10 years (2012 through 2021).
U.S. Nuclear Regulatory Commission Accident Sequence Precursor (ASP) Program 2021 Annual Report June 2022 Christopher Hunter (301) 415-1394 christopher.hunter@nrc.gov Performance and Reliability Branch Division of Risk Analysis Office of Nuclear Regulatory Research U.S. Nuclear Regulatory Commission Washington, DC 20555-0001


U.S. Nuclear Regulatory Commission Accident Sequence Precursor (ASP) Program 2021 Annual Report
1
 
June 2022
 
Christopher Hunter (301) 415-1394 christopher.hunter@nrc.gov
 
Performance and Reliability Branch Division of Risk Analysis Office of Nuclear Regulatory Research U.S. Nuclear Regulatory Commission Washington, DC 20555- 0001
 
0
: 1. 2021 ASP RESULTS There were 135 licensee event reports (LERs) issued in calendar year 2021. From these LERs, 104 (approximately 77 percent) were screened out in the initial screening process and 31 events were selected and analyzed as potential precursors. The overall number of LERs and potential precursors continues to decrease to historical lows. Figure 1 provides a breakdown of the number of LERs reviewed by the ASP Program since the switch was made to review LERs issued on a calendar-year basis in 2016.
: 1. 2021 ASP RESULTS There were 135 licensee event reports (LERs) issued in calendar year 2021. From these LERs, 104 (approximately 77 percent) were screened out in the initial screening process and 31 events were selected and analyzed as potential precursors. The overall number of LERs and potential precursors continues to decrease to historical lows. Figure 1 provides a breakdown of the number of LERs reviewed by the ASP Program since the switch was made to review LERs issued on a calendar-year basis in 2016.
The ASP Program is looking at the potential of other data sources for potential precursors due the decreasing LERs for failures that have been Figure 1. ASP Program LER Review Breakdown reported historically.
The ASP Program is looking at the potential of other data sources for potential precursors due the decreasing LERs for failures that have been reported historically.
 
Figure 1. ASP Program LER Review Breakdown Of the 31 potential precursors, 4 events were determined to exceed the ASP Program threshold and, therefore, are precursors. An independent ASP analysis was performed to determine the risk significance for three of these precursors. One precursor was the result of greater-than-Green inspection finding identified in 2021.1 Table 1 provides a brief description of all precursors identified in 2021. The three precursors identified in 2021 using an independent ASP analysis were compared with results from Management Directive (MD) 8.3, NRC Incident Investigation Program, (ML18073A200) and Significance Determination Process (SDP). This comparison is provided in Appendix A.
Of the 31 potential precursors, 4 events were determined to exceed the ASP Program threshold and, therefore, are precursors. An independent ASP analysis was performed to determine the risk significance for three of these precursors. One precursor was the result of greater -than-Green inspection finding identified in 2021. 1 Table 1 provides a brief description of all precursors identified in 2021. The three precursors identified in 2021 using an independent ASP analysis were compared with results from Management Directive (MD) 8.3, NRC Incident Investigation Program,
Table 1. 2021 Precursors Plant/Description LER/IR Event Date Exposure Time CCDP/
(ML18073A200) and Significance Determination Process (SDP). This comparison is provided in Appendix A.
CDP Davis-Besse, Emergency Diesel Generator (EDG) Speed Switch Failure due to Direct Current System Ground (ML21356A058) 346-21-001 2/12/21 9 days White Finding Davis-Besse, Field Flash Selector Switch Failure Results in EDG Unavailability (ML22164A812) 05000346/2021050 (No LER was issued) 5/27/21 99 days 9x10-6 Davis-Besse, Reactor Trip due to Failed Uninterruptible Power Supply (UPS) and Steam Feedwater Rupture Control System Actuations (ML22125A048) 346-21-003 7/8/21 Initiating Event 3x10-6 Waterford, Loss of Offsite Power (LOOP) during Hurricane Ida (ML22122A190) 382-21-001 8/29/21 Initiating Event 5x10-4 After further analysis, the remaining 27 LERs identified by the initial LER screening were determined not to be precursors. Additional information on the LERs determined not to be precursors via an ASP analysis or by acceptance of SDP results is provided in Appendix B. The evaluation of other hazards beyond internal events (e.g., internal fires, seismic events) did not result in any additional precursors in 2021.
 
1 Two additional potentially greater-than-Green inspection findings, a finalized greater-than-Green cybersecurity finding at Davis-Besse Nuclear Station (ML20091L428) and a preliminary White radiation protection finding at Columbia Generating Station (ML21347A988), were identified in 2021. However, these findings were not associated with increased risk to core damage and, therefore, are out of the scope of the ASP Program.  
Table 1. 2021 Precursors Plant/Description LER/IR Event Exposure CCDP/
Date Time CDP Davis-Besse, Emergency Diesel Generator (EDG) Speed Switch 346 -21 -001 2/12/21 9 days White Failure due to Direct Current System Ground ( ML21356A058 ) Finding Davis-Besse, Field Flash Selector Switch Failure Results in EDG 05000346/2021050 5/27/21 99 days 9 x10 -6 Unavailability (ML22164A812 ) (No LER was issued)
Davis-Besse, Reactor Trip due to Failed Uninterruptible Power 346 -21 -003 7/8/21 Initiating 3x10 -6 Supply (UPS) and Steam Feedwater Rupture Control System Event Actuations (ML22125A048 )
Waterford, Loss of Offsite Power (LOOP) during Hurricane Ida 382 -21 -001 8/29/21 Initiating 5x10 -4 (ML22122A190 ) Event
 
After further analysis, the remaining 27 LERs identified by the initial LER screening were determined not to be precursors. Additional information on the LERs determined not to be precursors via an ASP analysis or by acceptance of SDP results is provided i n Appendix B. The evaluation of other hazards beyond internal events (e.g., internal fires, seismic events) did not result in any additional precursors in 2021.
 
1 Two a dditional potentially greater -than-Green inspection findings, a finalized greater -than-Green cybersecurity finding at Davis-Besse Nuclear Station ( ML20091L428) and a preliminary White radiation protection finding at Columbia Generating Station (ML21347A988), were identified in 2021. However, these findings were not associated with increased risk to core damage and, therefore, are out of the scope of the ASP Program.
 
1
: 2. ASP TRENDS
 
Table 2. Precursor Trend Results Precursor Group Trend p-value All Precursors Decreasing 0.00001 Important Precursors [i.e., conditional core No=Trend = 4 =
damage probability (CCDP) or increase in core damage probability (CDP 10- 4]=
Precursors with CCDP/CDP 10-5 = aecreang = =
ftiing=bvents = aecreang = 002 =
aegraded=Contio = aecreang = 001 =
illms = aecreang = =
badl = No=Trend = 9 =
Bli -tateoeaor=EBto)rso = aecreang = =
mressuzed -tater=oeaoto)=mrersors = aecreang = 0002 =
=
Thes Apm=tnds,=g=with=the= r=of=the =Apm=index indic =NoC= sight=and=licei= tivi effecvd=that=licsiskent=iativ=areot= =
r n=reasing=risk=profilendusy. = Figure 2. Occurrence Rate of All Precursors
 
ADDITIONAL PRECURSOR TRENDS
 
0.18 0.45 0.09 0.16 Initiating Events 0.40 BWR Precursors 0.08 LOOPs with CCDP in the 1E-6 Range Degraded Conditions PWR Precursors LOOPs with CCDP in the 1E-5 Range 0.14 0.35 PWR Trend 0.07 IE Trend LOOP Important Precursors 0.12 DC Trend 0.30 BWR Trend 0.06 Trend
 
0.10 0.25 0.05
 
0.08 0.20 0.04
 
0.06 0.15 0.03
 
0.04 0.10 0.02
 
0.02 0.05 0.01
 
0.00 0.00 0.00 2012 2013 2014 2015 2016 2017 2018 2019 2020 2021 2012 2013 2014 2015 2016 2017 2018 2019 2020 2021 2012 2013 2014 2015 2016 2017 2018 2019 2020 2021 Year YearYear Figure 3. Occurrence Rate of Initiating E vent Figure 4. Occurrence Rate of BWR and PWR Figure 5. Occurrence Rate of LOOP and Degraded Condition Precursors Precursors Precursors


2
2
: 3. KEY INSIGHTS
: 2. ASP TRENDS Table 2. Precursor Trend Results Precursor Group Trend p-value All Precursors Decreasing 0.00001 Important Precursors [i.e., conditional core damage probability (CCDP) or increase in core damage probability (CDP) 10-4]
 
No Trend 0.4 Precursors with CCDP/CDP 10-5 Decreasing 0.01 Initiating Events Decreasing 0.002 Degraded Conditions Decreasing 0.001 LOOPs Decreasing 0.01 EDG Failures No Trend 0.9 Boiling-Water Reactor (BWR) Precursors Decreasing 0.02 Pressurized-Water Reactor (PWR) Precursors Decreasing 0.0002 These ASP trends, along with the results of the ASP index, indicate that NRC oversight and licensing activities remain effective and that licensee risk management initiatives are not resulting in an increasing risk profile for the industry.
Key insights based on the review of the 99 precursors that were identified in the past decade (2012-2021) are provided in this section. Note that additional insights can be Figure 6. Precursor Breakdown by Risk Bin gathered by using the publicly available ASP Program Dashboard. 25 20 20 There were 5 important precursors identified 15 during this period, all of were due to initiating events (4 LOOPs and a loss of service water). 10 7
Figure 2. Occurrence Rate of All Precursors ADDITIONAL PRECURSOR TRENDS Figure 3. Occurrence Rate of Initiating Event Figure 4. Occurrence Rate of BWR and PWR Figure 5. Occurrence Rate of LOOP and Degraded Condition Precursors Precursors Precursors 0.00 0.02 0.04 0.06 0.08 0.10 0.12 0.14 0.16 0.18 2012 2013 2014 2015 2016 2017 2018 2019 2020 2021 Precursor Occurrence Rate Year Initiating Events Degraded Conditions IE Trend DC Trend 0.00 0.05 0.10 0.15 0.20 0.25 0.30 0.35 0.40 0.45 2012 2013 2014 2015 2016 2017 2018 2019 2020 2021 Precursor Occurrence Rate Year BWR Precursors PWR Precursors PWR Trend BWR Trend 0.00 0.01 0.02 0.03 0.04 0.05 0.06 0.07 0.08 0.09 2012 2013 2014 2015 2016 2017 2018 2019 2020 2021 Precursor Occurrence Rate Year LOOPs with CCDP in the 1E-6 Range LOOPs with CCDP in the 1E-5 Range LOOP Important Precursors Trend
 
5 3 2 2 1 1 1 The ratio of precursors identified via greater -0 LOOP Loss of Transient Loss of Loss of Inadvertent Loss of Loss of than-Green vs. independent ASP evaluations CondenserElectricalFeedwaterSafetyShutdownService Heat Sink Bus Injection Cooling Water continues to decrease. In 2016, the 10-year percentage was 69 percent, but is currently Figure 7. Most Frequent Initiating Event Precursor Types 54 percent.


3
: 3. KEY INSIGHTS Key insights based on the review of the 99 precursors that were identified in the past decade (2012-2021) are provided in this section. Note that additional insights can be gathered by using the publicly available ASP Program Dashboard.
There were 5 important precursors identified during this period, all of were due to initiating events (4 LOOPs and a loss of service water).
The ratio of precursors identified via greater-than-Green vs. independent ASP evaluations continues to decrease. In 2016, the 10-year percentage was 69 percent, but is currently 54 percent.
The most frequent initiating events that resulted in precursors were LOOPs and losses of a condenser heat sink.
The most frequent initiating events that resulted in precursors were LOOPs and losses of a condenser heat sink.
Natural phenomena caused 11 precursors, with snow/ice and lightning the most frequent causes.
The most frequent structure, system, and component (SSC) failures observed in precursors were associated with EDGs, flood protection, and switchyard.
A review of the precursors associated with inspection findings that had a significant impact on the risk of the event were most likely due to inadequate procedures or design issues.
There are no indications of increasing risk due to the potential cumulative impact of risk-informed initiatives.
No new component failure modes or mechanisms were identified. In addition, the likelihood and impacts of accident sequences have not changed.
Long duration LOOPs occurring at single-unit site have a high likelihood of resulting in a higher-risk precursors.
Figure 6. Precursor Breakdown by Risk Bin Figure 7. Most Frequent Initiating Event Precursor Types Figure 8. Natural Phenomena Precursors Causes Figure 9. Most Frequent Precursor SSC Failures Figure 10. Dominant Precursor SSC Failures 20 7
3 2
2 1
1 1
0 5
10 15 20 25 LOOP Loss of Condenser Heat Sink Transient Loss of Electrical Bus Loss of Feedwater Inadvertent Safety Injection Loss of Shutdown Cooling Loss of Service Water
# of Precursors 22 13 11 7
7 6
5 4
2 0
5 10 15 20 25 EDGs Flood Protection Switchyard HPCI Other SSCs Electical Buses SRVs RCIC Recirculation
# of Precursors 29%
38%
20%
12%
1%
Design Issues Inadequate Procedures Ineffective Corrective Action Program Human Errors Deficient Training


Natural phenomena caused 11 precursors, with snow/ice and lightning the most frequent Figure 8. Natural Phenomena Precursors Causes causes.
4
EDGs 22 The most frequent structure, system, and Flood Protection13 component (SSC) failures observed in Switchyard 11 precursors were associated with EDGs, flood HPCI 7 protection, and switchyard. Other SSCs 7 Electical Buses 6 A review of the precursors associated with SRVs5 inspection findings that had a significant RCIC 4 impact on the risk of the event were most likely Recirculation2 due to inadequate procedures or design 05101520 25
: 4. ASP INDEX The ASP index shows the cumulative plant average risk from precursors on an annual basis.
# of Precursors issues. Figure 9. Most Frequent Precursor SSC Failures
Unlike the trend analyses performed on various precursor groups that are focused on the occurrence rate of precursors, the ASP index is focused on the total risk due to all precursors.
 
There are no indications of increasing risk due to the potential cumulative impact of risk - Design Issues informed initiatives. 12% 1%
29% Inadequate No new component failure modes or Procedures mechanisms were identified. In addition, the 20% Ineffective Corrective likelihood and impacts of accident sequences Action Program have not changed. Human Errors
 
Long duration LOOPs occurring at single-unit 38% Deficient Training site have a high likelihood of resulting in a higher-risk precursors.
Figure 10. Dominant Precursor SSC Failures
 
3
: 4. ASP INDEX
 
The ASP index shows the cumulative plant average risk from precursors on an annual basis.
Unlike the trend analyses performed on various precursor groups that are focused on the occurrence rate of precursors, the ASP index is focused on the total risk due to all precur sors.
Therefore, the ASP index provides a unique way to evaluate the risk of longer-term degraded conditions over the entire duration of the condition.
Therefore, the ASP index provides a unique way to evaluate the risk of longer-term degraded conditions over the entire duration of the condition.
The ASP index does not exhibit a statistically significant trend (p-value = 0.7) for the past decade (2012-2021). The total risk associated with precursors (99 total precursors) is dominated by the 5 important precursors, which account for approximately 60 percent of the total risk due to all precursors. The other 94 precursors account for approximately 47 percent to the total risk due to all precursors.
Figure 3. ASP Index A description of how the ASP index is calculated is provided in past annual reports, which can be accessed from the ASP Program Public Webpage.


The ASP index does not exhibit a statistically significant trend (p-value = 0.7) for the past Figure 3. ASP Index decade (2012 - 2021). The total risk associated with precursors (99 total precursors) is dominated A description of how the ASP index is calculated by the 5 important precursors, which account for is provided in past annual reports, which can be approximately 60 percent of the total risk due to accessed from the ASP Program Public all precursors. The other 94 precursors account Webpage.
A-1 Appendix A: Comparison of 2021 ASP Analyses The three precursors identified in 2021 using an independent ASP analysis were compared with results from MD 8.3 and SDP analyses, as shown in the following table. Given the three programs have different functions, it is expected that the results are likely to be different.
for approximately 47 percent to the total risk due to all precursors.
Event Description Program Results SPAR Model/Methodology Improvements and Insights Davis-Besse, IR 05000346/
 
2021050 Field Flash Selector Switch Failure Results in EDG Unavailability MD 8.3. CDP estimated to be in the range of 7x10-7 to 5x106, which led to a special inspection. See IR 05000346/2021050 (ML21321A365) for additional information.
4 Appendix A: Comparison of 2021 ASP Analyses
Credit for FLEX mitigation strategies was provided using with updated reliability data provided by the Pressurized Water Reactor Owners Group (PWROG). Modified FLEX modeling according to review of licensees final integrated plan.
 
SDP. No performance deficiency was identified for this event; therefore, no SDP evaluation was performed.
The three precursors identified in 2021 using an independent ASP analysis were compared with results from MD 8.3 and SDP analyses, as shown in the following table. Given the three programs have different functions, it is expected that the results are likely to be different.
ASP. CDP = 9x10-6; EDG unavailable for 99 days. See final ASP analysis (ML22164A812) for additional information.
 
Davis-Besse, LER 346 003 Reactor Trip due to Failed UPS and Steam Feedwater Rupture Control System Actuations MD 8.3. CCDP = 1x106, which led to a special inspection. See IR 05000346/2021050 (ML21321A365) for additional information.
Event Description Program Results SPAR Model/Methodology Improvements and Insights Davis-Besse, IR 05000346/ MD 8.3. CDP estimated to be in the range of Credit for FLEX mitigation strategies 2021050 Field Flash Selector - T=t 6, which led to a special was provided using with updated Switch Failure Results in EDG inspection. See IR 05000346/2021050 reliability data provided by the Unavailability (ML21321A365) for additional information. Pressurized Water Reactor Owners SDP. No performance deficiency was Group (PWROG ). Modified FLEX identified for this event; therefore, no SDP modeling according to review of evaluation was performed. licensees final integrated plan.
Modified loss of condenser heat sink event tree to account for potential overcooling. Used IDHEAS-ECA for human reliability analysis of critical human failure event.
ASP. CDP = 9 -6;=bad=unavailae=f=
SDP. Three Green findings were identified.
= days.=peeinalnali EMi222 )=additialmion. =
The first finding was associated with the licensee failure to appropriately classify the digital electro-hydraulic control UPS battery bank as non-critical as required by component classification procedures. The second finding was associated with the licensee failing to establish procedural guidance for transferring the gland sealing steam supply from the main steam system to the auxiliary steam system following a reactor trip. The third finding was associated with the licensee failure to have an appropriate procedure for the replacement of main steam isolation valve limit switch. All three findings were screened out (i.e., no detailed risk evaluation was performed). See IR 05000346/2021050 (ML21321A365) for additional information.
Davis-Besse, LER 346 MD 8.3. CCDP = 1x10 6, which led to a special Modified loss of condenser heat sink 003 Reactor Trip due to Failed inspection. See IR 05000346/2021050 event tree to account for potential UPS and Steam Feedwater (ML21321A365) for additional information. overcooling. Used IDHEAS-ECA for Rupture Control System SDP. Three Green findings were identified. human reliability analysis of critical Actuations The first finding was associated with the human failure event.
ASP. CCDP = 3x10-6; loss of condenser heat sink and overcooling. See final ASP analysis (ML22125A048) for additional information.
licensee failure to appropriately classify the digital electro-hydraulic control UPS battery bank as non-critical as required by component classification procedures. The second finding was associated with the licensee failing to establish procedural guidance for transferring the gland sealing steam supply from the main steam system to the auxiliary steam system following a reactor trip. The third finding was associated with the licensee failure to have an appropriate procedure for the replacement of main steam isolation valve limit switch. All three findings were screened out (i.e., no detailed risk evaluation was performed). See IR 05000346/2021050 ( ML21321A365) for additional information.
Waterford, LER 382 21 001 LOOP during Hurricane Ida MD 8.3. No evaluation performed.
ASP. CCDP = 3x10 -6; loss of condenser heat sink and overcooling. See final ASP analysis (ML22125A048) for additional information.
Credit for FLEX mitigation strategies was provided using with updated reliability data provided by the PWROG.
Waterford, LER 382 21 001 MD 8.3. No evaluation performed. Credit for FLEX mitigation strategies LOOP during Hurricane Ida SDP. No performance deficiency was was provided using with updated identified for this event; therefore, no SDP reliability data provided by the PWROG.
Modified FLEX modeling according to review of licensees final integrated plan. Performed MELCOR calculations to support credit for long-term turbine-driven emergency feedwater pump operation. Performed event analyses for other plants that have experienced a LOOP during a hurricane in the past 20 years to develop generic risk insights.
evaluation was performed. Modified FLEX modeling according to ASP. CCDP = 5x10 -4; weather-related LOOP review of licensees final integrated occurred during Hurricane Ida. See final ASP plan. Performed MELCOR calculations analysis (ML22122A190) for additional to support credit for long-term turb ine-information. driven emergency feedwater pump operation. Performed event analyses for other plants that have experienced a LOOP during a hurricane in the past 20 years to develop generic risk insights.
SDP. No performance deficiency was identified for this event; therefore, no SDP evaluation was performed.
 
ASP. CCDP = 5x10-4; weather-related LOOP occurred during Hurricane Ida. See final ASP analysis (ML22122A190) for additional information.  
A-1 Appendix B: 202 1 ASP Program Screened Analyses
 
The table in this appendix provides the justification for each LER that was screened out of the ASP Program based on a simplified or bounding analysis or by acceptance of SDP results. Note that the justification reflects the status of the LER (open or closed) at the time of the ASP completion date.
While ASP analysts monitor the final SDP evaluation of all findings for including g reater-t han-Green findings as precursors, the screen-out justification is not updated retroactively for events that were initially screened out by an ASP analysis and are later assessed as Green (i.e., very low safety significance) in the final SDP evaluation.


Plant LER Event Description LER Screen Criterion Date Date Classification Date Date Date Assigned Completed Comanche Peak 1 445-20-001 12/16/20 MFW Pump Failure to Trip 2/11/21 2/23/21 3b 3/18/21 4/7/21 Analyst Screen-Out Analyst Justification. This condition is not discussed in an inspection report (IR) to date; the LER remains open. On October 10, 2020, during a planned shutdown for refueling outage, operators could not manually trip main feedwater (MFW) pump 1A from the main control room (MCR). Subsequent attempts to trip the pump locally also failed. Operators declared 1 of 2 input signals to engineered safety feature actuation system (ESFAS) instrumentation inoperable for function 6.g of Technical Specification (TS) 3.3.2, which uses a twoof two logic to automatically start both motor-driven auxiliary feedwater (MDAFW) pumps when both MFW pumps trip. The manual trip failed because MFW pump 1A trip oil pressure did not lower when operators attempted to trip the pump from the MCR and locally. Non-licensed operators closed the steam supply valves to the MFW pump 1A turbine and manually lowered trip oil pressure to activate the ESFAS trip signal. A search of LERs did not yield any windowed events. Although the anticipatory start function ofthe MDAFW pumps upon a loss of both MFW pumps was lost due to this failure, the other automatic start signals (e.g., low steam generator level) were not affected and remained available. In addition, the operators had the ability to manually start the MDAFW pumps. Given these considerations, the risk of this condition is qualitatively determined to be below the ASP Program threshold and, therefore, is not a precursor.
B-1 Appendix B: 2021 ASP Program Screened Analyses The table in this appendix provides the justification for each LER that was screened out of the ASP Program based on a simplified or bounding analysis or by acceptance of SDP results. Note that the justification reflects the status of the LER (open or closed) at the time of the ASP completion date.
Shearon Harris 400-21-002 12/17/20 All ECCS Accumulator 2/15/21 3/2/21 3d 3/18/21 4/7/21 Analyst Isolation Valves Closed in Screen-Out Mode 3 With RCS Pressure Greater than 1000 psig Analyst Justification. This condition is not discussed in an IR to date; the LER remains open. On December 17, 2020, with the plant in Mode 3, reactor coolant system (RCS) pressure was being controlled between 900-1000 psig with all three cold leg accumulator discharge valves closed. Operators were manually controlling RCS pressure manual using a pressurizer spray valve with only one reactor coolantpump (RCP) running, which reduced the pressurizer spray effectiveness resulting in an RCS pressure increase. MCR operators took immediate actions to stop the pressure increase by fully opening the pressurizer spray vale, reducing charging flow, and turning off all pressurizer heaters.
While ASP analysts monitor the final SDP evaluation of all findings for including greater-than-Green findings as precursors, the screen-out justification is not updated retroactively for events that were initially screened out by an ASP analysis and are later assessed as Green (i.e., very low safety significance) in the final SDP evaluation.
Plant LER Event Date Description LER Date Screen Date Criterion Date Assigned Date Completed Classification Comanche Peak 1 445-20-001 12/16/20 MFW Pump Failure to Trip 2/11/21 2/23/21 3b 3/18/21 4/7/21 Analyst Screen-Out Analyst Justification. This condition is not discussed in an inspection report (IR) to date; the LER remains open. On October 10, 2020, during a planned shutdown for refueling outage, operators could not manually trip main feedwater (MFW) pump 1A from the main control room (MCR). Subsequent attempts to trip the pump locally also failed. Operators declared 1 of 2 input signals to engineered safety feature actuation system (ESFAS) instrumentation inoperable for function 6.g of Technical Specification (TS) 3.3.2, which uses a two of two logic to automatically start both motor-driven auxiliary feedwater (MDAFW) pumps when both MFW pumps trip. The manual trip failed because MFW pump 1A trip oil pressure did not lower when operators attempted to trip the pump from the MCR and locally. Non-licensed operators closed the steam supply valves to the MFW pump 1A turbine and manually lowered trip oil pressure to activate the ESFAS trip signal. A search of LERs did not yield any windowed events. Although the anticipatory start function of the MDAFW pumps upon a loss of both MFW pumps was lost due to this failure, the other automatic start signals (e.g., low steam generator level) were not affected and remained available. In addition, the operators had the ability to manually start the MDAFW pumps. Given these considerations, the risk of this condition is qualitatively determined to be below the ASP Program threshold and, therefore, is not a precursor.
Shearon Harris 400-21-002 12/17/20 All ECCS Accumulator Isolation Valves Closed in Mode 3 With RCS Pressure Greater than 1000 psig 2/15/21 3/2/21 3d 3/18/21 4/7/21 Analyst Screen-Out Analyst Justification. This condition is not discussed in an IR to date; the LER remains open. On December 17, 2020, with the plant in Mode 3, reactor coolant system (RCS) pressure was being controlled between 900-1000 psig with all three cold leg accumulator discharge valves closed. Operators were manually controlling RCS pressure manual using a pressurizer spray valve with only one reactor coolant pump (RCP) running, which reduced the pressurizer spray effectiveness resulting in an RCS pressure increase. MCR operators took immediate actions to stop the pressure increase by fully opening the pressurizer spray vale, reducing charging flow, and turning off all pressurizer heaters.
However, these actions were not performed in time to prevent RCS pressure from exceeding 1000 psig. TS require that the cold leg accumulators be operable in Mode 3 when RCS pressure is greater than 1000 psig. Since all three cold leg accumulator discharge valves were closed, this TS requirement was not met for approximately 15 minutes until operators were able to reduce RCS pressure below 1000 psig. A search of LERs did not yield any windowed events. Because the licensee restored RCS pressure below 1000 psig within 15 minutes, the exposure time was not longer than the TS allowed outage time. Therefore, an evaluation of this condition under the ASP Program to determine whether it is a precursor is not warranted.
However, these actions were not performed in time to prevent RCS pressure from exceeding 1000 psig. TS require that the cold leg accumulators be operable in Mode 3 when RCS pressure is greater than 1000 psig. Since all three cold leg accumulator discharge valves were closed, this TS requirement was not met for approximately 15 minutes until operators were able to reduce RCS pressure below 1000 psig. A search of LERs did not yield any windowed events. Because the licensee restored RCS pressure below 1000 psig within 15 minutes, the exposure time was not longer than the TS allowed outage time. Therefore, an evaluation of this condition under the ASP Program to determine whether it is a precursor is not warranted.
Limerick 1 352-20-002 11/16/20 HPCI and RCIC Were Not 1/26/21 2/3/21 3d 3/29/21 4/7/21 Analyst Aligned for Service During Screen-Out Startup Resulting in TS Violations Analyst Justification. This condition is not discussed in any IR to date; the LER remains open. On November 16, 2020, Unit 1 was starting up when the reactor steam dome pressure exceeded 150 psig without the reactor core isolation cooling (RCIC) system being aligned for service,which is contrary to TS 3.7.3. Reactor steam dome pressure continued to increase above 200 psig without the highpressure coolant -
Limerick 1 352-20-002 11/16/20 HPCI and RCIC Were Not Aligned for Service During Startup Resulting in TS Violations 1/26/21 2/3/21 3d 3/29/21 4/7/21 Analyst Screen-Out Analyst Justification. This condition is not discussed in any IR to date; the LER remains open. On November 16, 2020, Unit 1 was starting up when the reactor steam dome pressure exceeded 150 psig without the reactor core isolation cooling (RCIC) system being aligned for service, which is contrary to TS 3.7.3. Reactor steam dome pressure continued to increase above 200 psig without the high-pressure coolant injection (HPCI) system being aligned for service and, therefore, the plant entered TS 3.5.1. During a shift change the oncoming MCR operating crew recognized HPCI was still isolated and immediately began to warm-up the HPCI system and align HPCI for operation. RCIC and HPCI were aligned for service and declared operable approximately 90 minutes and 2 hours after reactor steam dome pressure exceeded 150 psig and 200 psig, respectively. This condition was caused by the failure of operators to correctly perform the startup procedure. A search of LERs did not yield any windowed events. Because the licensee restored HPCI and RCIC within their TS required action times and the exposure times were not longer than the TS allowed outage times for those systems, an evaluation of this condition under the ASP Program to determine whether it is a precursor is not warranted.
injection (HPCI) system being aligned for service and, therefore, the plant entered TS 3.5.1. During a shift change the oncoming MCR operating crew recognized HPCI was still isolated and immediately began to warm-up the HPCI system and align HPCI for operation. RCIC and HPCI were aligned for service and declared operable approximately 90 minutes and 2 hours after reactor steam dome pressure exceeded 150 psig and 200 psig, respectively.This condition was caused by the failure of operators to correctly perform the startup procedure. A search of LERs did not yield any windowed events. Because the licensee restored HPCI and RCIC within their TS required action times and the exposure times were not longer than the TS allowed outage times for those systems, an evaluation of thiscondition under the ASP Program to determine whether it is a precursor is not warranted.
LaSalle 2 374-21-001 12/23/20 HPCS Inoperable due to Water Leg Pump Breaker Cubicle Motor Contactor 2/18/21 3/2/21 3d 4/16/21 4/27/21 Analyst Screen-Out Analyst Justification: This condition is not discussed in any IR to date; the LER remains open. On December 23, 2020, the Unit 2 high-pressure core spray (HPCS) water leg pump tripped due to a breaker fault. Operators subsequently declared the HPCS system inoperable according to TS. The RCIC system was verified to be operable. The affected breaker cubicle control power transformer and motor starter contactor were replaced and the HPCS system was declared operable approximately 13 hours after the initial failure. A search of LERs did not yield any windowed events. Since the HPCS system was unavailable for less than the limits of TS Limiting Condition of Operation (LCO) 3.5.1, Condition B (14 days), this condition is screened out and is not considered a precursor.  
LaSalle 2 374-21-001 12/23/20 HPCS Inoperable due to 2/18/21 3/2/21 3d 4/16/21 4/27/21 Analyst Water Leg Pump Breaker Screen-Out Cubicle Motor Contactor Analyst Justification: This condition is not discussed in any IR to date; the LER remains open. On December 23, 2020, the Unit 2 high-pressure core spray (HPCS) water leg pumptripped due to a breaker fault.Operators subsequently declared the HPCS system inoperable according to TS. The RCIC system was verified to be operable. The affected breaker cubicle control power transformer and motor starter contactor were replaced and the HPCS system was declared operable approximately 13 hours after the initial failure. A search of LERsdid not yield any windowed events. Since the HPCS system was unavailable for less than the limits of TS Limiting Condition of Operation (LCO) 3.5.1, Condition B (14 days), this condition is screened out and is not considered a precursor.


B-1 Plant LER Event Description LER Screen Criterion Date Date Classification Date Date Date Assigned Completed Susquehanna 1 387-21-001 3/9/21 Unplanned lnoperability of 5/6/21 5/13/21 3d 5/27/21 6/9/21 Analyst the HPCI System due to a Screen-Out PCIV Failure to Stroke Full Closed On-Demand due to an Intermittent Break in the Close Control Circuitry Analyst Justification. This condition is not discussed in any IR to date, the LER remains open. On March 9, 2021, during performance of quarterly HPCI system valve exercising, the HPCI turbine exhaust vacuum breaker inboard isolation valve (HV155F079) failed to stroke fully closed. The closure function of this valve supports primary containment isolation; however, this function was maintained given the outboard containment isolation valve (HV155F075) successfully stroked closed. The direct cause of the condition was an intermittent break in the valves close control circuitry likely due to dirty contacts on the HPCI turbine exhaust vacuum breaker inboard isolation valve hand switch. Key corrective actions includeplanned replacement of the hand switch. After the initial failure, operators successfully stroked HV155F079 open and closed within acceptance times. Although the HPCI system was TS inoperable for approximately 39 hours, operators could manually open HV155F079 to restore HPCI availability. A search of LERs did not yield any windowed events. Because the licensee restored HPCI within their TS required action time and the exposure time was not longer than the TS allowed outage time, an evaluation of this condition under the ASP Program to determine whether it is a precursor is not warranted.
B-2 Plant LER Event Date Description LER Date Screen Date Criterion Date Assigned Date Completed Classification Susquehanna 1 387-21-001 3/9/21 Unplanned lnoperability of the HPCI System due to a PCIV Failure to Stroke Full Closed On-Demand due to an Intermittent Break in the Close Control Circuitry 5/6/21 5/13/21 3d 5/27/21 6/9/21 Analyst Screen-Out Analyst Justification. This condition is not discussed in any IR to date, the LER remains open. On March 9, 2021, during performance of quarterly HPCI system valve exercising, the HPCI turbine exhaust vacuum breaker inboard isolation valve (HV155F079) failed to stroke fully closed. The closure function of this valve supports primary containment isolation; however, this function was maintained given the outboard containment isolation valve (HV155F075) successfully stroked closed. The direct cause of the condition was an intermittent break in the valves close control circuitry likely due to dirty contacts on the HPCI turbine exhaust vacuum breaker inboard isolation valve hand switch. Key corrective actions include planned replacement of the hand switch. After the initial failure, operators successfully stroked HV155F079 open and closed within acceptance times. Although the HPCI system was TS inoperable for approximately 39 hours, operators could manually open HV155F079 to restore HPCI availability. A search of LERs did not yield any windowed events. Because the licensee restored HPCI within their TS required action time and the exposure time was not longer than the TS allowed outage time, an evaluation of this condition under the ASP Program to determine whether it is a precursor is not warranted.
Palo Verde 2 529-21-002 5/19/21 Reactor Trip during Plant 7/16/21 8/5/21 1d/2h 8/6/21 8/12/21 Analyst Protection System Screen-Out Surveillance Testing Analyst Justification. This event is not discussed in any IR to date; the LER remains open. On May 19, 2021, an invalid actuation of the safety injection (SI), containment isolation, and main steam isolation signals occurred resulting in an automatic reactor trip due to high pressurizer pressure caused by the closure of the main steam isolation valves (MSIVs). The essential AFW pumps automatically started due to low steam generator (SG) level. Both trains of the high-pressure safety injection (HPSI) and low-pressure safety injection (LPSI),
Palo Verde 2 529-21-002 5/19/21 Reactor Trip during Plant Protection System Surveillance Testing 7/16/21 8/5/21 1d/2h 8/6/21 8/12/21 Analyst Screen-Out Analyst Justification. This event is not discussed in any IR to date; the LER remains open. On May 19, 2021, an invalid actuation of the safety injection (SI), containment isolation, and main steam isolation signals occurred resulting in an automatic reactor trip due to high pressurizer pressure caused by the closure of the main steam isolation valves (MSIVs). The essential AFW pumps automatically started due to low steam generator (SG) level. Both trains of the high-pressure safety injection (HPSI) and low-pressure safety injection (LPSI),
containment spray, and essential spray pond pumps automatically started due to the SI actuation signal. RCS pressure remainedabove the HPSI pump head and, therefore, no injection into the RCS occurred during this event. In addition, the emergency diesel generators (EDGs) automatically started; however, the EDGs did not load onto their respective buses because they remained supplied by offsite power.
containment spray, and essential spray pond pumps automatically started due to the SI actuation signal. RCS pressure remained above the HPSI pump head and, therefore, no injection into the RCS occurred during this event. In addition, the emergency diesel generators (EDGs) automatically started; however, the EDGs did not load onto their respective buses because they remained supplied by offsite power.
Operators reset SI actuation signal, closed the HPSI and LPSI injection valves, and stopped all HPSI, LPSI, and containment spray pumps as directed by the emergency operating procedures (EOPs). Although the steam supply to the MFW pumps was interrupted by the closure of the MSIVs, the condensate system continued to operate, and condenser vacuum remained intact. MFW was potentially recoverable using existing plant procedures in approximately 30 minutes. This event was caused by invalid trip signal that occurred during plant protection system functional testing. A search of LERs did not yield any windowed events. The risk of this event is bounded by a non-recoverable loss of main feedwater and/or condenser heat sink. Therefore, the risk of this event is below the ASP Program threshold and is not a precursor.
Operators reset SI actuation signal, closed the HPSI and LPSI injection valves, and stopped all HPSI, LPSI, and containment spray pumps as directed by the emergency operating procedures (EOPs). Although the steam supply to the MFW pumps was interrupted by the closure of the MSIVs, the condensate system continued to operate, and condenser vacuum remained intact. MFW was potentially recoverable using existing plant procedures in approximately 30 minutes. This event was caused by invalid trip signal that occurred during plant protection system functional testing. A search of LERs did not yield any windowed events. The risk of this event is bounded by a non-recoverable loss of main feedwater and/or condenser heat sink. Therefore, the risk of this event is below the ASP Program threshold and is not a precursor.
Peach Bottom 2 277-21-001 4/29/21 HPCI System Declared 6/24/21 7/22/21 3d 8/6/21 8/12/12 Analyst Inoperable Due to Instrument Screen-Out Power Inverter Failure Analyst Justification. This condition is not discussed in any IR to date; the LER remains open. On April 29, 2021, the HPCI system inverter circuit failure alarm was received the MCR. Operators immediately noticed erratic performance of HPCI system pressure instruments and a loss of the expected status display on the HPCI flow controller. Examination of the HPCI rack-mounted inverter revealed that the power indicator light was cycling on and off. Further inspection of the HPCI back panel revealed that the logic bus power monitoring relay was chattering. In the event of a valid HPCI initiation signal, the erratic power supply to the HPCI flow controller would have resulted in a loss of HPCI safety function. On April 30th, the inverter replacement was completed, andHPCI function was restored after satisfactorily testing was completed. The exposure time for the failed HPCI inverter was approximately 15 hours. A search of LERs identified LER 277-21-002 as a potential windowed event. The windowed aspect of these two events will be evaluated as part of the ASP evaluation of LER 277-21- 002.
Peach Bottom 2 277-21-001 4/29/21 HPCI System Declared Inoperable Due to Instrument Power Inverter Failure 6/24/21 7/22/21 3d 8/6/21 8/12/12 Analyst Screen-Out Analyst Justification. This condition is not discussed in any IR to date; the LER remains open. On April 29, 2021, the HPCI system inverter circuit failure alarm was received the MCR. Operators immediately noticed erratic performance of HPCI system pressure instruments and a loss of the expected status display on the HPCI flow controller. Examination of the HPCI rack-mounted inverter revealed that the power indicator light was cycling on and off. Further inspection of the HPCI back panel revealed that the logic bus power monitoring relay was chattering. In the event of a valid HPCI initiation signal, the erratic power supply to the HPCI flow controller would have resulted in a loss of HPCI safety function. On April 30th, the inverter replacement was completed, and HPCI function was restored after satisfactorily testing was completed. The exposure time for the failed HPCI inverter was approximately 15 hours. A search of LERs identified LER 277-21-002 as a potential windowed event. The windowed aspect of these two events will be evaluated as part of the ASP evaluation of LER 277-21-002.
Because the licensee restored HPCI within their TS required action time (14 days) and the exposure time was not longer than the TS allowed outage time, an evaluation of this condition under the ASP Program to determine whether it is a precursor is not warranted.
Because the licensee restored HPCI within their TS required action time (14 days) and the exposure time was not longer than the TS allowed outage time, an evaluation of this condition under the ASP Program to determine whether it is a precursor is not warranted.
Braidwood 1 456-21-001 4/23/21 Train A and B Source Range 6/21/21 7/8/21 3a 7/19/21 8/25/21 Analyst Neutron Flux Trip Functions Screen-Out Bypassed During Plant Startup Analyst Justification. This condition is not discussed in any IR to date; the LER remains open. On April 23, 2021, during reactor startup activities with the plant in Mode 2, operators identified that both trains A and B source range neutron flux reactor tripfunctions were bypassed. Operators immediately took the bypass switches to normal in accordance with TS. The incorrect position of the source range neutron flux reactor trip functions existed since April 21st while the plant was in Mode 5 operation. A licensee review determined that on April 21st, with the plant in Mode 5, both source range neutron flux trips were placed in bypass per procedure in support of switchyardactivities.
Braidwood 1 456-21-001 4/23/21 Train A and B Source Range Neutron Flux Trip Functions Bypassed During Plant Startup 6/21/21 7/8/21 3a 7/19/21 8/25/21 Analyst Screen-Out Analyst Justification. This condition is not discussed in any IR to date; the LER remains open. On April 23, 2021, during reactor startup activities with the plant in Mode 2, operators identified that both trains A and B source range neutron flux reactor trip functions were bypassed. Operators immediately took the bypass switches to normal in accordance with TS. The incorrect position of the source range neutron flux reactor trip functions existed since April 21st while the plant was in Mode 5 operation. A licensee review determined that on April 21st, with the plant in Mode 5, both source range neutron flux trips were placed in bypass per procedure in support of switchyard activities.
After the switchyard activities were completed, operators failed to restore the source range neutron flux trips per procedure. A search of LERs did not yield any windowed events. The source range neutron flux trips provide protection during postulated uncontrolled rod withdrawal events. The source range detectors provide indication of an RCS boron dilution event. However, there are diverse trip and indications for both of these events (e.g., power range high neutron flux trip, volume control tank level alarm, etc.). Given the availability of the redundant, but diverse systems and the short exposure time of less than 3 days, the risk of this condition is qualitatively determined to be below the ASP Program threshold and, therefore, is not a precursor.
After the switchyard activities were completed, operators failed to restore the source range neutron flux trips per procedure. A search of LERs did not yield any windowed events. The source range neutron flux trips provide protection during postulated uncontrolled rod withdrawal events. The source range detectors provide indication of an RCS boron dilution event. However, there are diverse trip and indications for both of these events (e.g., power range high neutron flux trip, volume control tank level alarm, etc.). Given the availability of the redundant, but diverse systems and the short exposure time of less than 3 days, the risk of this condition is qualitatively determined to be below the ASP Program threshold and, therefore, is not a precursor.  


B-2 Plant LER Event Description LER Screen Criterion Date Date Classification Date Date Date Assigned Completed Peach Bottom 2 277-21-002 5/18/21 SRV lnoperability Due to 7/16/21 8/5/21 3d 7/29/21 8/25/21 Analyst Nitrogen Leakage from Screen-Out Braided Hose Wear Analyst Justification. This condition is not discussed in any IR to date; the LER remains open. On March 21, 2021, operators noted that the instrument nitrogen compressors were increasing in run hours, with all other related parameters steady. The condition was monitored and trended, and investigation determined the most likely cause to be nitrogen leakage within primary containment. A second step increase in nitrogen leakage occurred in May, which led to the decision to decrease reactor power to allow for entry into primary containment and investigate the source of leakage. On May 18th, the licensee identified that the nitrogen supply to safety relief valve (SRV) RV-2 071K was the source of the leak. Specifically, the stainless-steel braided hoses that supply and return nitrogen from the actuating solenoid valve had failed. This valve is one of five automatic depressurization system (ADS) valves and, therefore, the ADS function was declared inoperable according to TS 3.5.1. The failure of the braided hoses did not affect the overpressure function of SRV RV 02-071K. Note that the other four ADS valves use hard pipe for the instrument nitrogen supplies and returns. The hoses were replaced on May 18th and the unit was returned to full power. A search of LERs identified LER 277-21 -001 as a potential windowed event. A risk assessment was performed assuming the unavailability of ADS valve 71K to open for its depressurization function. A potentially conservative exposure time of 75 days (March 5th to May 18th) was used. This analysisresulted in a CDP of 4E -9 from internal events, internal fires, internal floods, seismic hazards, high winds, and tornados. A sensitivity analysis assuming the concurrent unavailability of the HPCI system for an exposure time of 15 hours (from LER 277-21-001) results in a CDP of 4E -7, which is dominated by the risk of the HPCI failure during postulated internal fires scenarios.The risk of this condition, including the windowed aspects of LER 277-21-001, is below the ASP Program threshold and is not a precursor.
B-3 Plant LER Event Date Description LER Date Screen Date Criterion Date Assigned Date Completed Classification Peach Bottom 2 277-21-002 5/18/21 SRV lnoperability Due to Nitrogen Leakage from Braided Hose Wear 7/16/21 8/5/21 3d 7/29/21 8/25/21 Analyst Screen-Out Analyst Justification. This condition is not discussed in any IR to date; the LER remains open. On March 21, 2021, operators noted that the instrument nitrogen compressors were increasing in run hours, with all other related parameters steady. The condition was monitored and trended, and investigation determined the most likely cause to be nitrogen leakage within primary containment. A second step increase in nitrogen leakage occurred in May, which led to the decision to decrease reactor power to allow for entry into primary containment and investigate the source of leakage. On May 18th, the licensee identified that the nitrogen supply to safety relief valve (SRV) RV-2-02-071K was the source of the leak. Specifically, the stainless-steel braided hoses that supply and return nitrogen from the actuating solenoid valve had failed. This valve is one of five automatic depressurization system (ADS) valves and, therefore, the ADS function was declared inoperable according to TS 3.5.1. The failure of the braided hoses did not affect the overpressure function of SRV RV-2-02-071K. Note that the other four ADS valves use hard pipe for the instrument nitrogen supplies and returns. The hoses were replaced on May 18th and the unit was returned to full power. A search of LERs identified LER 277-21-001 as a potential windowed event. A risk assessment was performed assuming the unavailability of ADS valve 71K to open for its depressurization function. A potentially conservative exposure time of 75 days (March 5th to May 18th) was used. This analysis resulted in a CDP of 4E-9 from internal events, internal fires, internal floods, seismic hazards, high winds, and tornados. A sensitivity analysis assuming the concurrent unavailability of the HPCI system for an exposure time of 15 hours (from LER 277-21-001) results in a CDP of 4E-7, which is dominated by the risk of the HPCI failure during postulated internal fires scenarios. The risk of this condition, including the windowed aspects of LER 277-21-001, is below the ASP Program threshold and is not a precursor.
Palisades 255-21-001 6/16/21 Atmospheric Steam Dump 8/13/21 8/30/21 3i 8/30/21 9/8/21 Analyst Valves Inoperable Due to Screen-Out Relay Failure Analyst Justification. This condition is briefly mentioned in IR 05000255/2021002 (ML21222A118); the LER remains open. On June 16, 2021, operators smelled an acrid odor in the MCR. A subsequent investigation revealed that the steam dump control relay failed as result of a short circuit in the coil, which rendered all four atmospheric dump valves (ADVs) inoperable.The total relief capacity of the ADVs is a steam flow of 30% with the reactor at full power and their operation prevents lifting the main steam safety valves following a turbinetrip. The failed relay coil resulted in an overcurrent condition causing the supply fuse to open disabling both the ADVs automatic fast-open function and manual operation.The relay failure was due to age being beyond the vendor recommended life for a normally energized relay because the licensee had improperly classified it as a low-duty cycle instead of a high-duty cycle.The fuse and relay were replaced and the ADVs were returned to service approximately 12 hours later.A search of LERs did not yield any windowed events.Because the licensee restored the ADVs within their TS required action time (24 hours) and the exposure time was not longer than the TS allowed outage time for the system, an evaluation of this condition under the ASP Program to determine whether it is a precursor is not warranted.
Palisades 255-21-001 6/16/21 Atmospheric Steam Dump Valves Inoperable Due to Relay Failure 8/13/21 8/30/21 3i 8/30/21 9/8/21 Analyst Screen-Out Analyst Justification. This condition is briefly mentioned in IR 05000255/2021002 (ML21222A118); the LER remains open. On June 16, 2021, operators smelled an acrid odor in the MCR. A subsequent investigation revealed that the steam dump control relay failed as result of a short circuit in the coil, which rendered all four atmospheric dump valves (ADVs) inoperable. The total relief capacity of the ADVs is a steam flow of 30% with the reactor at full power and their operation prevents lifting the main steam safety valves following a turbine trip. The failed relay coil resulted in an overcurrent condition causing the supply fuse to open disabling both the ADVs automatic fast-open function and manual operation. The relay failure was due to age being beyond the vendor recommended life for a normally energized relay because the licensee had improperly classified it as a low-duty cycle instead of a high-duty cycle. The fuse and relay were replaced and the ADVs were returned to service approximately 12 hours later. A search of LERs did not yield any windowed events. Because the licensee restored the ADVs within their TS required action time (24 hours) and the exposure time was not longer than the TS allowed outage time for the system, an evaluation of this condition under the ASP Program to determine whether it is a precursor is not warranted.
Hope Creek 354-21-001 6/14/21 SRV As-Found Setpoint 8/13/21 8/27/21 3i 8/30/21 9/15/21 Analyst Failures Screen-Out Analyst Justification. This condition is not discussed in any IR to date; the LER remains open. On June 14, 2021, tests of the pilot stage assemblies of SRVs A and Jexceeded the lift setting tolerance of the nominal setpoint values prescribed in TS. In addition, SRV R failed to lift when tested. Hope Creek has 14 safety-related main steam SRVs that provide reactor pressure vessel overpressure protection and an automatic/manual depressurization function. The setpoint exceedance for SRVs A and J was attributed to corrosion bonding between the pilot discs and seating surfaces.The cause of SRV R not lifting was main disc and piston thread wear.SRV R was replaced, and the seven two-stage SRVs (including SRVs A and J) werereplaced with threestage models.- A searchof LERs did not yield any windowed events.
Hope Creek 354-21-001 6/14/21 SRV As-Found Setpoint Failures 8/13/21 8/27/21 3i 8/30/21 9/15/21 Analyst Screen-Out Analyst Justification. This condition is not discussed in any IR to date; the LER remains open. On June 14, 2021, tests of the pilot stage assemblies of SRVs A and J exceeded the lift setting tolerance of the nominal setpoint values prescribed in TS. In addition, SRV R failed to lift when tested. Hope Creek has 14 safety-related main steam SRVs that provide reactor pressure vessel overpressure protection and an automatic/manual depressurization function. The setpoint exceedance for SRVs A and J was attributed to corrosion bonding between the pilot discs and seating surfaces. The cause of SRV R not lifting was main disc and piston thread wear. SRV R was replaced, and the seven two-stage SRVs (including SRVs A and J) were replaced with three-stage models. A search of LERs did not yield any windowed events.
Although SRVs A and J exceeded their lift setpoints by slightly greater than 3%, the licensee determined that both SRVs would have remained available to prevent overpressure of the reactor pressure vessel according to the margins of the plants design analysis. In addition, TS only requires 13 of 14 SRVs to be operable and, therefore, the failure of SRV R did not affect the availability of overpressure protection of the reactor pressure vessel. Given these considerations, an evaluation of this condition under the ASP Program to determine whether it is a precursor is not warranted.
Although SRVs A and J exceeded their lift setpoints by slightly greater than 3%, the licensee determined that both SRVs would have remained available to prevent overpressure of the reactor pressure vessel according to the margins of the plants design analysis. In addition, TS only requires 13 of 14 SRVs to be operable and, therefore, the failure of SRV R did not affect the availability of overpressure protection of the reactor pressure vessel. Given these considerations, an evaluation of this condition under the ASP Program to determine whether it is a precursor is not warranted.
Fermi 341-21-001 5/3/21 Unrecognized Impact of 7/1/21 7/22/21 3d 7/23/21 9/15/21 Analyst Opening of Barrier Doors on Screen-Out HELB Analysis Analyst Justification. This condition is not discussed in any IR to date; the LER remains open. On May 3, 2021, the licensee determined that the reactor building steam tunnel door had been open on several occasions for longer than was required for personnel ingress/egress.If a postulated high-energy line break (HELB) had occurred while the door was open, equipment outside the reactor building steam tunnel could have been adversely impacted by the post-HELB conditions. The maximum time the door was open over any 1year period was -
Fermi 341-21-001 5/3/21 Unrecognized Impact of Opening of Barrier Doors on HELB Analysis 7/1/21 7/22/21 3d 7/23/21 9/15/21 Analyst Screen-Out Analyst Justification. This condition is not discussed in any IR to date; the LER remains open. On May 3, 2021, the licensee determined that the reactor building steam tunnel door had been open on several occasions for longer than was required for personnel ingress/egress. If a postulated high-energy line break (HELB) had occurred while the door was open, equipment outside the reactor building steam tunnel could have been adversely impacted by the post-HELB conditions. The maximum time the door was open over any 1-year period was approximately 12 hours. A search of LERs did not yield any windowed events. A risk assessment was performed assuming that the reactor building steam tunnel door was open for an exposure time of 12 hours using the Fermi SPAR model that was modified by Idaho National Laboratory (INL) to include a main steam line break (MSLB) event tree. This risk assessment conservatively assumed that HPCI, RCIC, residual heat removal (RHR), and low-pressure core spray (LPCS) would fail as the result of post-HELB conditions during a postulated MSLB in the reactor building steam tunnel with the door open. The MLSB initiating event frequency is considered bounding because not all steam line breaks would occur in the reactor building steam tunnel. This analysis resulted in a CDP of 2E-10. The risk of this degraded condition is below the ASP Program threshold and, therefore, is not a precursor.  
approximately 12 hours. A search of LERs did not yield any windowed events. A risk assessment was performed assuming that the reactor building steam tunnel door was open for an exposure time of 12 hours using the Fermi SPAR model thatwas modified by Idaho National Laboratory (INL) to include a main steam line break (MSLB) event tree. This risk assessment conservatively assumed that HPCI,RCIC, residual heat removal (RHR), and low-pressure core spray (LPCS) would fail as the result of post-HELB conditions during a postulated MSLB in the reactor building steam tunnel with the door open. The MLSB initiating event frequency is considered bounding because not all steam line breaks would occur in the reactor building steam tunnel.This analysis resulted in a CDP of 2E-10.The risk of this degraded condition is below the ASP Program threshold and, therefore, is not a precursor.


B-3 Plant LER Event Description LER Screen Criterion Date Date Classification Date Date Date Assigned Completed Susquehanna 2 388-21-001 7/6/21 Condition Prohibited by TS 9/1/21 9/3/21 3d 9/7/21 10/14/21 Analyst Due to Drift of Reactor Screen-Out Pressure Switch Analyst Justification. This condition is not discussed in any IR to date; the LER remains open. On July 6, 2021, the channel D of reactor steam dome pressure low permissive pressure switch dropped below TS allowable value, which is intended to ensure that the emergency core cooling system (ECCS) injection prevents the fuel peak cladding temperature from exceeding regulatory limits. In addition, channel C was under surveillance test when operator found the instrument drift on channel D and, therefore, two channels were inoperable at the same time. Although the drift of channel D was below the TS allowable value, the as-found set point remained above the limit assumed in the accident analysis and, therefore, the licensee determined that ECCS remained available. Since ECCS remained available, this condition is not a precursor, and a review of potential windowed events was not needed.
B-4 Plant LER Event Date Description LER Date Screen Date Criterion Date Assigned Date Completed Classification Susquehanna 2 388-21-001 7/6/21 Condition Prohibited by TS Due to Drift of Reactor Pressure Switch 9/1/21 9/3/21 3d 9/7/21 10/14/21 Analyst Screen-Out Analyst Justification. This condition is not discussed in any IR to date; the LER remains open. On July 6, 2021, the channel D of reactor steam dome pressure low permissive pressure switch dropped below TS allowable value, which is intended to ensure that the emergency core cooling system (ECCS) injection prevents the fuel peak cladding temperature from exceeding regulatory limits. In addition, channel C was under surveillance test when operator found the instrument drift on channel D and, therefore, two channels were inoperable at the same time. Although the drift of channel D was below the TS allowable value, the as-found set point remained above the limit assumed in the accident analysis and, therefore, the licensee determined that ECCS remained available. Since ECCS remained available, this condition is not a precursor, and a review of potential windowed events was not needed.
Hatch 1 321-21-003 9/8/21 HPCI System Discharge 11/1/21 11/18/21 3d 11/19/21 11/30/21 Analyst Valve Failure to Open Screen-Out Analyst Justification. This condition is not discussed in any IR to date; the LER remains open. On September 8, 2021, the HPCI pump discharge isolation valve was stroked closed as a part of surveillance testing. Subsequent attempts by operators to reopen the valve failed.
Hatch 1 321-21-003 9/8/21 HPCI System Discharge Valve Failure to Open 11/1/21 11/18/21 3d 11/19/21 11/30/21 Analyst Screen-Out Analyst Justification. This condition is not discussed in any IR to date; the LER remains open. On September 8, 2021, the HPCI pump discharge isolation valve was stroked closed as a part of surveillance testing. Subsequent attempts by operators to reopen the valve failed.
HPCI was declared inoperable in accordance with TS. Licensee troubleshooting determined that the pinion gear key in the valve actuator had not been properly staked during maintenance activities completed in 2006, which resulted in the key moving and the pinion gear disengaging from the actuator motor shaft. This issue was corrected on September 9th and HPCI was returned to operable status. The HPCI pump discharge isolation valve is normally open valve and does not change position during HPCI operations. Therefore, the exposuretime of the loss of HPCI system function was limited to the 2 days when the valve was closed on September 8th and 9 th. A search of LERs did not yield any windowed events. Since the HPCI system was unavailable for less than the limits of TS, this condition is screened out and is not considered a precursor.
HPCI was declared inoperable in accordance with TS. Licensee troubleshooting determined that the pinion gear key in the valve actuator had not been properly staked during maintenance activities completed in 2006, which resulted in the key moving and the pinion gear disengaging from the actuator motor shaft. This issue was corrected on September 9th and HPCI was returned to operable status. The HPCI pump discharge isolation valve is normally open valve and does not change position during HPCI operations. Therefore, the exposure time of the loss of HPCI system function was limited to the 2 days when the valve was closed on September 8th and 9th. A search of LERs did not yield any windowed events. Since the HPCI system was unavailable for less than the limits of TS, this condition is screened out and is not considered a precursor.
Point Beach 1 266-21-001 7/31/21 MFW Pump Trip Results in 9/28/21 10/19/21 2h 10/20/21 12/6/21 Analyst Manual Reactor Trip Screen-Out Analyst Justification. This event is not discussed in any IR to date; the LER remains open. On July 31, 2021, operators manually tripped the reactor due to the failure of the MFW pump B motor. After the reactor trip, the AFW pumps started and restored SG inventorylevels. During the trip response, a condenser steam dump valve cycled but did not fully close, requiring operators to locally close the valve to prevent additional reactor cooldown. In addition, thecrossover steam dump valves did not close resulting in deterioratingvacuum in the main condenser. Operators subsequently closed the valves resulting in the unavailability of the main condenser. The SG ADVs were used for decay heat removal. During the feedwater transition, the MFWregulating bypass valve B did not maintain proper control of SG levels in automatic requiring operators to takemanual control of the valve.MFW pump A remained available throughout the event; however, reactor power was too high to support the loss of one of the two MFW pumps without requiringa reactor trip. A search of LERs did not yield any windowed events. The risk of this event is bounded by a non-recoverable loss of main feedwater and/or condenser heat sink. Therefore, the risk of this event is below the ASP Program threshold and is not a precursor.
Point Beach 1 266-21-001 7/31/21 MFW Pump Trip Results in Manual Reactor Trip 9/28/21 10/19/21 2h 10/20/21 12/6/21 Analyst Screen-Out Analyst Justification. This event is not discussed in any IR to date; the LER remains open. On July 31, 2021, operators manually tripped the reactor due to the failure of the MFW pump B motor. After the reactor trip, the AFW pumps started and restored SG inventory levels. During the trip response, a condenser steam dump valve cycled but did not fully close, requiring operators to locally close the valve to prevent additional reactor cooldown. In addition, the crossover steam dump valves did not close resulting in deteriorating vacuum in the main condenser. Operators subsequently closed the valves resulting in the unavailability of the main condenser. The SG ADVs were used for decay heat removal. During the feedwater transition, the MFW regulating bypass valve B did not maintain proper control of SG levels in automatic requiring operators to take manual control of the valve. MFW pump A remained available throughout the event; however, reactor power was too high to support the loss of one of the two MFW pumps without requiring a reactor trip. A search of LERs did not yield any windowed events. The risk of this event is bounded by a non-recoverable loss of main feedwater and/or condenser heat sink. Therefore, the risk of this event is below the ASP Program threshold and is not a precursor.
Perry 440-21-001 6/1/21 Division 3 EDG lnoperability 7/28/21 8/19/21 3d 8/20/21 12/6/21 Analyst Resulting in an Operation or Screen-Out Condition Prohibited by TS Analyst Justification. This condition is not discussed in any IR to date; the LER remains open. On June 1, 2021, erratic output voltage was observed on the division 3 EDG approximately 45seconds after starting during monthly surveillance testing. The operators initially believed that the EDG was still operable; however, a subsequent evaluation did not support continued operability and the division 3 EDG was later declared inoperable on June 3rd according to TS. On June 4th, voltage regulator was replaced and was tested satisfactory, thus restoring the division 3 EDG to operable status. Discussions with NRC inspectors indicate that although the voltage fluctuation exceeded the TS limit, the voltages and frequencies experienced during the surveillance test weresufficient to support successful operation of the division 3 EDG.
Perry 440-21-001 6/1/21 Division 3 EDG lnoperability Resulting in an Operation or Condition Prohibited by TS 7/28/21 8/19/21 3d 8/20/21 12/6/21 Analyst Screen-Out Analyst Justification. This condition is not discussed in any IR to date; the LER remains open. On June 1, 2021, erratic output voltage was observed on the division 3 EDG approximately 45 seconds after starting during monthly surveillance testing. The operators initially believed that the EDG was still operable; however, a subsequent evaluation did not support continued operability and the division 3 EDG was later declared inoperable on June 3rd according to TS. On June 4th, voltage regulator was replaced and was tested satisfactory, thus restoring the division 3 EDG to operable status. Discussions with NRC inspectors indicate that although the voltage fluctuation exceeded the TS limit, the voltages and frequencies experienced during the surveillance test were sufficient to support successful operation of the division 3 EDG.
Since the division 3 EDG remained available, this condition is not a precursor, and a review of potential windowed events was not needed.
Since the division 3 EDG remained available, this condition is not a precursor, and a review of potential windowed events was not needed.
Nine Mile Point 1 220-21-002 9/25/21 Isolation of both Emergency 11/19/21 12/3/21 3d 12/6/21 12/7/21 Analyst Condensers due to loss of Screen-Out UPS 162A Analyst Justification. This condition is not discussed in any IR to date; the LER remains open. On September 25, 2021, the MCR operators received multiple annunciators due to the loss of power to reactor protection system (RPS) bus 11 caused by the failure of the uninterruptible power supply (UPS) 162A. The loss of power to RPS bus 11 resulted in a half scram, isolation of the reactor water cleanupsystem, and isolation of both emergency condensers. Operators subsequently declared the emergency condenser system inoperable according to TS, which requires operators to manually shutdown that plant within 1 hour. Operators reenergized RPS bus 11 from instrumentation bus 130A in approximately 24 minutes. Both emergency condensers were restored to standby in approximately 39 minutes and 48 minutes respectively and, therefore, the reactor shutdown was no longer required. A search of LERs did not yield any windowed events. A risk assessment was performed assuming the unavailability of both emergency condensers for 1 hour, which is the minimum exposure time allowed by SAPHIRE.
Nine Mile Point 1 220-21-002 9/25/21 Isolation of both Emergency Condensers due to loss of UPS 162A 11/19/21 12/3/21 3d 12/6/21 12/7/21 Analyst Screen-Out Analyst Justification. This condition is not discussed in any IR to date; the LER remains open. On September 25, 2021, the MCR operators received multiple annunciators due to the loss of power to reactor protection system (RPS) bus 11 caused by the failure of the uninterruptible power supply (UPS) 162A. The loss of power to RPS bus 11 resulted in a half scram, isolation of the reactor water cleanup system, and isolation of both emergency condensers. Operators subsequently declared the emergency condenser system inoperable according to TS, which requires operators to manually shutdown that plant within 1 hour. Operators reenergized RPS bus 11 from instrumentation bus 130A in approximately 24 minutes. Both emergency condensers were restored to standby in approximately 39 minutes and 48 minutes respectively and, therefore, the reactor shutdown was no longer required. A search of LERs did not yield any windowed events. A risk assessment was performed assuming the unavailability of both emergency condensers for 1 hour, which is the minimum exposure time allowed by SAPHIRE.
This analysis resulted in a CDP of 1E-nternal=ev,=ssmicgh=windsiludinados)fnal=flnd=fir sci=are=notlile=mmAo=m; =wevriskmpacsiateth=these=hazs=expec mim=due=to=the=vyhorsmson.=Tisk=of=this=degraded=cspmrr hold,=
This analysis resulted in a CDP of 1E-8 from internal events, seismic hazards, and high winds (including tornados). Internal flooding and fire scenarios are not included in the Nine Mile Point 1 SPAR model; however, the risk impact associated with these hazards is expected to be minimal due to the very short exposure time of this condition. The risk of this degraded condition is below the ASP Program threshold and, therefore, is not a precursor.  
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B-4 Plant LER Event Description LER Screen Criterion Date Date Classification Date Date Date Assigned Completed Limerick 1 352-21-001 9/23/21 HPCI Inoperable Due to 11/22/21 12/3/21 3d 12/6/21 12/15/21 Analyst Remote Shutdown Panel Screen-Out Switch Failure Analyst Justification. This condition is not discussed in any IR to date; the LER remains open. On September 23, 2021, the licensee was scheduled to perform the HPCI logic system functional isolation logic test and the HPCI pump valve and flow test. The HPCI logic system function isolation test was completed successfully. However, during the initial start of the turbine during the HPCI pump valve andflow test the indicated turbine speed on the plant computer point and MCR tachometer was downscale. The test was subsequently aborted when the HPCI pump was not able to meet the TS requirements for rated flow and discharge pressure. Licensee troubleshooting determined a high contact resistance existed in the HPCI emergency shutdown switch located on the remote shutdown panel. The purpose of this switch is to terminate or prevent HPCI injection from the remote shutdown panel under various fire safe shutdown events. The HPCI emergency shutdownswitch high resistance was attributed to mechanical switch degradation that was introduced by cycling the switch during the HPCI logic system functional isolation logic test, which was performed 1 hour and 32 minutes prior to the HPCI pump valve and flow surveillancetest. A search of LERs did not yield any windowed events. The HPCI system was unavailable for less than TS allowed outage time of 14 days. In addition, the failure of the HPCI emergency shutdown switch was in the safe direction (i.e., the high contact resistance would have terminated HPCI injection if manipulated during a MCR abandonment scenario). Given these considerations, the risk of this condition is qualitatively determined to be below the ASP Program threshold and, therefore, is not a precursor.
Vogtle 1 424-21-001 9/16/21 Train A SI Pump 11/15/21 11/18/21 3d 11/19/21 12/15/21 Analyst Inoperability Causes the Unit Screen-Out to operate in a Condition Prohibited by TS Analyst Justification. This condition is not discussed in any IR to date, the LER remains open. During the refueling outage on September 16, 2021, plant operators conducted a surveillance test of SI pump 1A. During the test, pump bearing temperatures rose rapidly requiring operators to secure the pump. A subsequent licensee investigation found a piece of plastic tubing between the gears of the lube oil pump, which resulted in lack of oil to the two bearings causing their failure. The pump was returned to operable status on September 29 th after the bearing were replaced and the system was flushed.Improper oil sampling of SI pump 1A performed on September 6, 2021, introduced the foreign material into the pump's oil system.The plant entered into Mode 4 on September 12 th as part a refueling outage. A search of LERs did not yield any windowed events. A risk assessment was performed assuming the SI pump 1A was failed for an exposure time of 138 hours (September 6th through September 12th). This analysis resulted in a mean CDP 2E -8 from internal events, internal fires, internal floods, seismic hazards, and high winds (including tornados). The risk of this degraded condition is below the ASP Program threshold and, therefore, is not a precursor.
Browns Ferry 1 and 259-21-001 3/3/21 480V Load Shed Logic 11/22/21 12/3/21 3e 12/6/21 1/10/22 Analyst 2 Inoperable Longer than Screen-Out Allowed by TS due to Failed Relay Analyst Justification. This condition is not discussed in any IR to date; the LER remains open. On September 23, 2021, the division I 480V load shed logic for Units 1 and 2 was declared inoperable during the performance of surveillance testing. During the test, relay 0- RLY-231-00A7 failed to energize due to an open circuit in the coil. The division I 480V was declared inoperable according to TS. The relay was replaced and the division I 480V load shed logic was declared operable on September 25th. A subsequent engineering evaluation determined that relay 0-RLY-231- 00A7 was likely failed since the last time it was energized during testing on March 3, 2021. During this period, the division II 480V load shed logic was out of service twice to support testing on March 4th and May 19 th for a total of 78 hours. A search of LERs did not yield any windowed events. The loss of both divisions of the load shed logic would result in the failure of all four shared EDGs between Units 1 and 2 given a concurrent lossoffsite power (LOOP) and loss-of-coolant accident (LOCA) event. The SPAR models include the load shed logic as part of the EDG sequencer component boundary, which does not allow the modeling of this degraded condition. Model changes were made to include the failure of both divisions of load shed logic given a concurrent LOOP and LOCA would result in the failure of all four Unit 1 and 2 EDGs. A risk assessment was performed assuming (a.) the unavailability of the division I load shed logic from March 3, 2021,until September 25, 2021 (i.e., an exposure time of 207 days) and (b.) the unavailability of both EDG sequencers for an exposure time of 78 hours. These assessments result in a mean CDP of 8E-10 and 5E-9 from internal events, seismic hazards, and high winds (including tornados), respectively. These results are conservative because the FLEX mitigation strategies were not credited. The risk impact is dominated by seismic scenarios that result in concurrent LOOP and LOCA. Internal flooding and fire scenarios are not included in the Browns Ferry SPAR model; however, the risk impact associated with these hazards is expected to be small for this condition because these hazards are unlikely to lead to concurrent LOOP and LOCA. The risk of this degraded condition is below the ASP Program threshold and, therefore, is not a precursor.


B-5 Plant LER Event Description LER Screen Criterion Date Date Classification Date Date Date Assigned Completed Diablo Canyon 2 323-21-001 7/22/21 EDG Declared Inoperable 9/20/21 9/29/21 3e 9/30/21 1/10/22 Analyst due to Low Frequency Screen-Out Condition Discovery during Routine Surveillance Analyst Justification. This condition is not discussed in any IR to date; the LER remains open. On July 21, 2021, EDG 2-3 was started on a simulated under-voltage signal for routine surveillance testing. With the mode select switch in the AUTO position, the frequency indicated 58.9 Hz, which is below the TS required minimum of 59.5 Hz. Operators placed the EDG 2-3 mode select switch in MANUAL and the frequency and speed were adjusted into their proper band and the test was completed meeting the acceptance criteria. The cause of the EDG 2-3 low frequency condition was due to an inadequately performed postmaintenance testing on June 30, 2021. Specifically, the testing -
B-5 Plant LER Event Date Description LER Date Screen Date Criterion Date Assigned Date Completed Classification Limerick 1 352-21-001 9/23/21 HPCI Inoperable Due to Remote Shutdown Panel Switch Failure 11/22/21 12/3/21 3d 12/6/21 12/15/21 Analyst Screen-Out Analyst Justification. This condition is not discussed in any IR to date; the LER remains open. On September 23, 2021, the licensee was scheduled to perform the HPCI logic system functional isolation logic test and the HPCI pump valve and flow test. The HPCI logic system function isolation test was completed successfully. However, during the initial start of the turbine during the HPCI pump valve and flow test the indicated turbine speed on the plant computer point and MCR tachometer was downscale. The test was subsequently aborted when the HPCI pump was not able to meet the TS requirements for rated flow and discharge pressure. Licensee troubleshooting determined a high contact resistance existed in the HPCI emergency shutdown switch located on the remote shutdown panel. The purpose of this switch is to terminate or prevent HPCI injection from the remote shutdown panel under various fire safe shutdown events. The HPCI emergency shutdown switch high resistance was attributed to mechanical switch degradation that was introduced by cycling the switch during the HPCI logic system functional isolation logic test, which was performed 1 hour and 32 minutes prior to the HPCI pump valve and flow surveillance test. A search of LERs did not yield any windowed events. The HPCI system was unavailable for less than TS allowed outage time of 14 days. In addition, the failure of the HPCI emergency shutdown switch was in the safe direction (i.e., the high contact resistance would have terminated HPCI injection if manipulated during a MCR abandonment scenario). Given these considerations, the risk of this condition is qualitatively determined to be below the ASP Program threshold and, therefore, is not a precursor.
sequence did not fully consider the need for revalidation of frequency following setting of the EDG governor following maintenance activities.
Vogtle 1 424-21-001 9/16/21 Train A SI Pump Inoperability Causes the Unit to operate in a Condition Prohibited by TS 11/15/21 11/18/21 3d 11/19/21 12/15/21 Analyst Screen-Out Analyst Justification. This condition is not discussed in any IR to date, the LER remains open. During the refueling outage on September 16, 2021, plant operators conducted a surveillance test of SI pump 1A. During the test, pump bearing temperatures rose rapidly requiring operators to secure the pump. A subsequent licensee investigation found a piece of plastic tubing between the gears of the lube oil pump, which resulted in lack of oil to the two bearings causing their failure. The pump was returned to operable status on September 29th after the bearing were replaced and the system was flushed. Improper oil sampling of SI pump 1A performed on September 6, 2021, introduced the foreign material into the pump's oil system. The plant entered into Mode 4 on September 12th as part a refueling outage. A search of LERs did not yield any windowed events. A risk assessment was performed assuming the SI pump 1A was failed for an exposure time of 138 hours (September 6th through September 12th). This analysis resulted in a mean CDP 2E-8 from internal events, internal fires, internal floods, seismic hazards, and high winds (including tornados). The risk of this degraded condition is below the ASP Program threshold and, therefore, is not a precursor.
The Diablo Canyon USAR Section 8.3.1.1.6.1.13, Selection of Diesel Generator Set Capacity for Standby Power Supplies, refers to Safety Guide 9, March 1971, Selection of DG Capacity for Standby Power Supplies, (ML12305A251). The safety guide allows frequency to decrease by 2% during recovery from transients (i.e., approximately 1.2 Hz). Since the frequency only decreased by 1.1 Hz, the EDG remained functional within the limits of the safety guide capacity. Since EDG 23 remained available, this condition is not a -precursor, and a review of potential windowed events was not needed.
Browns Ferry 1 and 2
Grand Gulf 416-21-003 9/9/21 HPCS Declared Inoperable 11/4/21 11/18/21 3d 11/19/21 1/11/22 Analyst Screen-Out Analyst Justification. This condition is not discussed in any IR to date; the LER remains open. On September 9, 2021, the MCR received an alarm for HPCS out of service along with HPCS motor operated valve/overload power loss status light. In addition, the HPCS minimum flow to suppression pool light indication was lost. Licensee troubleshooting revealed that this condition was caused by the failure of the alarm relay associated with HPCS minimum flow to suppression pool breaker due to the shorting of its coil. This failed relay subsequentlycaused the control circuit fuse to blow resulting in the inability to open the HPCS minimum flow valve to the suppression pool. The licensee took immediate action and replaced the damaged relay and associated control fuse. A search of LERs did not yield any windowed events.
259-21-001 3/3/21 480V Load Shed Logic Inoperable Longer than Allowed by TS due to Failed Relay 11/22/21 12/3/21 3e 12/6/21 1/10/22 Analyst Screen-Out Analyst Justification. This condition is not discussed in any IR to date; the LER remains open. On September 23, 2021, the division I 480V load shed logic for Units 1 and 2 was declared inoperable during the performance of surveillance testing. During the test, relay 0-RLY-231-00A7 failed to energize due to an open circuit in the coil. The division I 480V was declared inoperable according to TS. The relay was replaced and the division I 480V load shed logic was declared operable on September 25th. A subsequent engineering evaluation determined that relay 0-RLY-231-00A7 was likely failed since the last time it was energized during testing on March 3, 2021. During this period, the division II 480V load shed logic was out of service twice to support testing on March 4th and May 19th for a total of 78 hours. A search of LERs did not yield any windowed events. The loss of both divisions of the load shed logic would result in the failure of all four shared EDGs between Units 1 and 2 given a concurrent loss offsite power (LOOP) and loss-of-coolant accident (LOCA) event. The SPAR models include the load shed logic as part of the EDG sequencer component boundary, which does not allow the modeling of this degraded condition. Model changes were made to include the failure of both divisions of load shed logic given a concurrent LOOP and LOCA would result in the failure of all four Unit 1 and 2 EDGs. A risk assessment was performed assuming (a.) the unavailability of the division I load shed logic from March 3, 2021, until September 25, 2021 (i.e., an exposure time of 207 days) and (b.) the unavailability of both EDG sequencers for an exposure time of 78 hours. These assessments result in a mean CDP of 8E-10 and 5E-9 from internal events, seismic hazards, and high winds (including tornados), respectively. These results are conservative because the FLEX mitigation strategies were not credited. The risk impact is dominated by seismic scenarios that result in concurrent LOOP and LOCA. Internal flooding and fire scenarios are not included in the Browns Ferry SPAR model; however, the risk impact associated with these hazards is expected to be small for this condition because these hazards are unlikely to lead to concurrent LOOP and LOCA. The risk of this degraded condition is below the ASP Program threshold and, therefore, is not a precursor.  
Because the licensee restoredthe HPCS within their TS required action time (14 days) and the exposure time was not longer than the TS allowed outage time for the system, an evaluation of this condition under the ASP Program to determine whether it is a precursor is not warranted.
Susquehanna 1 387-21-004 10/7/21 Loss of 1B RHRSW Pump 12/1/21 1/3/22 3d 1/4/21 1/20/22 Analyst due to Cable Damage During Screen-Out Excavation Activities Analyst Justification. This condition is not discussed in any IR to date; the LER remains open. On October 7, 2021, operators observed current oscillations during a run of residual heat removal service water (RHRSW) pump 1B. Operators secured the pump and entered TS 3.7.1, Condition B for an inoperable RHRSW subsystem. Licensee troubleshooting identified the cause of the current oscillations to be a ground on the B-phase power cable for the pump that was likely damaged during excavation activities on September 23, 2021. The power cable was replaced and the RHRSW system was declared operable on October 11th. On September 19, 2021, the RHRSW train A subsystem was declared inoperable due to ultimate heat sink spray array and bypass valve alignments to support spray array inspection and nozzle cleaning. However, the licensee determined that the RHRSW train A subsystem remained available. A search of LERs did not yield any windowed events. A risk assessment was performed assuming the RHRSW pump 1B was failed from September 23rd until October 11th (i.e., an exposure time of 19 days). This analysis resulted in a CDP of 2E-omnal=ev,=ssmicgh=windsiluding=
tornados).=A=rie=rndic=that=tst=is=likyyonsvative=E i.e.,=by=at=least=an=orr=of=mtude)auscrs -
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ication.=fn=addion,=the=hum=error=prabili=forontai t=vng=appearsyonsvative=forsir=an icabllmci.=fntern=flng=and=fire=sci=are=nln=the=pt=1=pmAo=modelcens isk=
imati=the=hazs=avlable r,=speciccio=imatiss=labls=timiskmpac nal=flcis=expecmimson.=Tisk=frnal=firesscio =coulis=
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i = P41- -00P= =rabldue=to= =1/10/22= = 1/10/22= 1/21/22 Analyst t=lxion = Screen-Out Analyst Justification. This condition is not discussed in any IR to date; the LER remains open. On June 3,2021, the licensee was performing the HPCI condensate storage tank (CST) level channel functional test and the HPCI pump suction isolation valve from the suppression pool took approximately 5 minutes to open on the simulated low CST level signal. This condition resulted in the plant entering TS 3.3.5.1, Actions D.2.1 and D.2.2, which allows 24 hours to place the channel in trip or to align HPCI pump suction to the suppression pool. The licensee HPCI suction was transferred to the suppression pool later on June 3rd. Licensee troubleshooting of the condition identified an oxidated relay contact was the cause of the slow opening of the suction isolation valve. The licensee laterdetermined that this condition affected both channels and, therefore, the licensee should have declared the HPCI system inoperable according to TS 3.3.5.1, Action D.1. After repair of the relay was completed and reperforming the HPCI CST level channel functional test, the licensee declared the HPCI system operable on June 4th. A licensee evaluation determined that HPCI would operate as designed for most of the 5 minutes it would take to automatically transfer suction from the CST to the suppression pool. However, CST level would have lowered to a level where air entrainment would have occurred and, therefore, HPCI would have tripped on a low suction pressure signal without operator action. Upon completion of the late suction transfer, suction pressure wouldbe restored, and HPCI would automatically restart if demanded and continue to inject. In addition, procedures direct operators to complete any incomplete automatic actions manually, which means there was a high likelihood that operators would complete the HPCI suction transfer prior to HPCI tripping on low suction pressure given this condition. Because the HPCI would have restarted automatically if the slow transfer resulted in a low suction trip, HPCI remained available and, therefore, this condition is not a precursor, and a review of potential windowed events was not needed.


B-6 Plant LER Event Description LER Screen Criterion Date Date Classification Date Date Date Assigned Completed Calvert Cliffs 2 318-21-003 8/10/21 AFW Pump Inoperable Due 9/23/21 9/29/21 3b 9/30/21 2/2/21 Analyst to Improper Reset of Trip Screen-Out Throttle Valve Analyst Justification. A Green finding was identified in IR 05000318/2021002 ( ML21222A039 ); the LER remains open. On August 10, 2021, the licensee received an inspection report documenting the NRCs position that the turbine -driven auxiliary feedwater (TDAFW) pump 22 was considered inoperable from March 20, 2021, until March 26, 2021, because its trip throttle valvewas not reset properly. Specifically, the trip throttle valve, which is part of the pump overspeed trip mechanism, did not appear to be aligned properly such that the trip hook and latch-up lever were not fully engaged. The licensee later determined that the post-maintenance procedure had inadequate instructions regarding the verification that trip hook and latch -up lever were fully engaged. NRC inspectors determined that the licensee failure to properly reset the TDAFW pump 22 trip throttle in accordanc e with the surveillance test procedure was a performance deficiency. The inspectors determined that the performance deficiency was more than minor; however, the degraded condition did not represent a loss of safety function of one train of a multi-train sy stem for greater than its TS allowed outage time. Therefore, the performance deficiency was determined to be Green (i.e.,
B-6 Plant LER Event Date Description LER Date Screen Date Criterion Date Assigned Date Completed Classification Diablo Canyon 2 323-21-001 7/22/21 EDG Declared Inoperable due to Low Frequency Condition Discovery during Routine Surveillance 9/20/21 9/29/21 3e 9/30/21 1/10/22 Analyst Screen-Out Analyst Justification. This condition is not discussed in any IR to date; the LER remains open. On July 21, 2021, EDG 2-3 was started on a simulated under-voltage signal for routine surveillance testing. With the mode select switch in the AUTO position, the frequency indicated 58.9 Hz, which is below the TS required minimum of 59.5 Hz. Operators placed the EDG 2-3 mode select switch in MANUAL and the frequency and speed were adjusted into their proper band and the test was completed meeting the acceptance criteria. The cause of the EDG 2-3 low frequency condition was due to an inadequately performed post-maintenance testing on June 30, 2021. Specifically, the testing sequence did not fully consider the need for revalidation of frequency following setting of the EDG governor following maintenance activities.
very low safety significance). A search for windowed events identifiedLER 318-2021- 002 associated with a failed main feedwater regulating valve on March 21st, which resulted in a subsequent manual reactor trip.A risk assessment was performed assuming a reactor trip with the failure of the TDAFW pump 22 to evaluate this windowed event. Recovery of TDAWF pump 22 was not considered, which is potentially conservative. This analysis resulted in a CCDP of 1.5E-6,which is below the plant-specific CCDP for a nonrecoverable loss of feedwater and condenser heat sink of 2.8E-6 for Calvert Cliffs Unit 2. The risk of this condition, along with the windowed March 21 st reactor trip, is below the ASP Program threshold and, therefore, is not a precursor.
The Diablo Canyon USAR Section 8.3.1.1.6.1.13, Selection of Diesel Generator Set Capacity for Standby Power Supplies, refers to Safety Guide 9, March 1971, Selection of DG Capacity for Standby Power Supplies, (ML12305A251). The safety guide allows frequency to decrease by 2% during recovery from transients (i.e., approximately 1.2 Hz). Since the frequency only decreased by 1.1 Hz, the EDG remained functional within the limits of the safety guide capacity. Since EDG 2-3 remained available, this condition is not a precursor, and a review of potential windowed events was not needed.
Susquehanna 2 346-21-003 10/11/21 Automatic Reactor Scram 12/9/21 2/28/22 2h 2/28/22 3/8/22 Analyst due to Main Turbine Trip Screen-Out Analyst Justification. This event is not discussed in any IR to date; the LER remains open. On October 11, 2021, the Unit 2 reactor automatically scrammed due to a main turbine trip. The MCR received indication of a main turbine trip with both divisions of the RPS actuated and all control rods inserted. The turbine bypass valves (TBVs) opened automatically to control reactor pressure but failed to reclose causing the reactor to depressurize. Operators closed the MSIVs to stop reactor depressurization and manually initiated HPCI and RCIC to control reactor water level. Subsequently, operators maintained reactor water level in the normal operating band using RCIC and controlled reactor pressure using HPCI and the main steam line drains. The reactor recirculation pumps tripped on end-of-cycle trip. The licensee is still investigating the cause of the main turbine trip. A preliminary licensee investigation identified that a failed pressure transmitter resulted in the TBVs to close. A search of LERs did not yield any windowed events. The risk of this event is bounded by a non-recoverable loss of main feedwater and/or condenser heat sink. Therefore, the risk of this event is below the ASP Program threshold and is not a precursor.
Grand Gulf 416-21-003 9/9/21 HPCS Declared Inoperable 11/4/21 11/18/21 3d 11/19/21 1/11/22 Analyst Screen-Out Analyst Justification. This condition is not discussed in any IR to date; the LER remains open. On September 9, 2021, the MCR received an alarm for HPCS out of service along with HPCS motor operated valve/overload power loss status light. In addition, the HPCS minimum flow to suppression pool light indication was lost. Licensee troubleshooting revealed that this condition was caused by the failure of the alarm relay associated with HPCS minimum flow to suppression pool breaker due to the shorting of its coil. This failed relay subsequently caused the control circuit fuse to blow resulting in the inability to open the HPCS minimum flow valve to the suppression pool. The licensee took immediate action and replaced the damaged relay and associated control fuse. A search of LERs did not yield any windowed events.
Nine Mile Point 1 220-21-001 9/25/21 Isolation of Both Emergency 11/19/21 3/7/22 3a 3/8/22 3/17/22 SDP Condensers due to Loss of Screen-Out UPS 162A A Green finding was identified in IR 05000220/2021004 (ML22026A350); the LER is closed. On September 25, 2021, the MCR received multiple annunciators concurrent with a loss and subsequent restoration of RPS bus 11 on UPS 162A. This resulted in ahalf scram, reactor water cleanup isolation, and isolation of both emergency condensers. The emergency condenser system was declared inoperable and TS 3.1.3, LCO E was entered. Operators restored power to RPS bus 11 in 24 minutes using an alternative source. Both emergency condensers were restored to standby within 48 minutes. NRC inspectors determined that the licensee failure to ensure that an identified deviation from the normal operating frequency of UPS 162A was promptly identified and corrected was a performance deficiency. This performance deficiency was determined to be Green (i.e., very low safety significance) using the screening questions provided in Appendix A of Inspection Manual Chapter 0609. A search of LERs did not yield any windowed events. The SDP risk assessment is accepted as the ASP Program result, in accordance with RIS 2006-024, because there was no reactor trip nor windowed event. The risk of this condition is below the ASP Program threshold and, therefore, is not a precursor.
Because the licensee restored the HPCS within their TS required action time (14 days) and the exposure time was not longer than the TS allowed outage time for the system, an evaluation of this condition under the ASP Program to determine whether it is a precursor is not warranted.
Fermi 341-21-002 8/22/21 Unplanned Inoperability of 10/21/21 11/5/21 3d 11/8/21 6/7/22 Reject HPCI System Due to an Inverter Circuit Failure A detailed ASP analysis determined that the m =oncrent=degrons =identio=wasess=than=the=Apm=
Susquehanna 1 387-21-004 10/7/21 Loss of 1B RHRSW Pump due to Cable Damage During Excavation Activities 12/1/21 1/3/22 3d 1/4/21 1/20/22 Analyst Screen-Out Analyst Justification. This condition is not discussed in any IR to date; the LER remains open. On October 7, 2021, operators observed current oscillations during a run of residual heat removal service water (RHRSW) pump 1B. Operators secured the pump and entered TS 3.7.1, Condition B for an inoperable RHRSW subsystem. Licensee troubleshooting identified the cause of the current oscillations to be a ground on the B-phase power cable for the pump that was likely damaged during excavation activities on September 23, 2021. The power cable was replaced and the RHRSW system was declared operable on October 11th. On September 19, 2021, the RHRSW train A subsystem was declared inoperable due to ultimate heat sink spray array and bypass valve alignments to support spray array inspection and nozzle cleaning. However, the licensee determined that the RHRSW train A subsystem remained available. A search of LERs did not yield any windowed events. A risk assessment was performed assuming the RHRSW pump 1B was failed from September 23rd until October 11th (i.e., an exposure time of 19 days). This analysis resulted in a CDP of 2E-7 from internal events, seismic hazards, and high winds (including tornados). A review of these results indicates that this result is likely very conservative (i.e., by at least an order of magnitude) because cross-unit common-cause failure (CCF) of the RHRSW pumps is the dominant failure and the existing CCF data does not currently support this application. In addition, the human error probability for containment venting appears to be very conservative for loss of instrument air and applicable LOOP scenarios. Internal flooding and fire scenarios are not included in the Susquehanna Unit 1 SPAR model. Licensee risk information for these hazards is available; however, specific scenario information for this condition is not available at this time. The risk impact from internal flooding scenarios is expected to be minimal for this condition. The risk from internal fires for this scenario could be dominant this condition; however, it is unlikely to result in exceeding the precursor threshold by itself. Given these considerations, the risk of this degraded condition is judged to be below the ASP Program threshold and, therefore, is not a precursor.
mrogr=thrhold=of=10 - 6 =re,=isrs.=The=detlpm=analysiss=publicly=avlable=E Mi22158A092 =
Fermi 341-21-003 6/3/21 HPCI Inoperable due to Contact Oxidation 12/29/21 1/10/22 3d 1/10/22 1/21/22 Analyst Screen-Out Analyst Justification. This condition is not discussed in any IR to date; the LER remains open. On June 3,2021, the licensee was performing the HPCI condensate storage tank (CST) level channel functional test and the HPCI pump suction isolation valve from the suppression pool took approximately 5 minutes to open on the simulated low CST level signal. This condition resulted in the plant entering TS 3.3.5.1, Actions D.2.1 and D.2.2, which allows 24 hours to place the channel in trip or to align HPCI pump suction to the suppression pool. The licensee HPCI suction was transferred to the suppression pool later on June 3rd. Licensee troubleshooting of the condition identified an oxidated relay contact was the cause of the slow opening of the suction isolation valve. The licensee later determined that this condition affected both channels and, therefore, the licensee should have declared the HPCI system inoperable according to TS 3.3.5.1, Action D.1. After repair of the relay was completed and reperforming the HPCI CST level channel functional test, the licensee declared the HPCI system operable on June 4th. A licensee evaluation determined that HPCI would operate as designed for most of the 5 minutes it would take to automatically transfer suction from the CST to the suppression pool. However, CST level would have lowered to a level where air entrainment would have occurred and, therefore, HPCI would have tripped on a low suction pressure signal without operator action. Upon completion of the late suction transfer, suction pressure would be restored, and HPCI would automatically restart if demanded and continue to inject. In addition, procedures direct operators to complete any incomplete automatic actions manually, which means there was a high likelihood that operators would complete the HPCI suction transfer prior to HPCI tripping on low suction pressure given this condition. Because the HPCI would have restarted automatically if the slow transfer resulted in a low suction trip, HPCI remained available and, therefore, this condition is not a precursor, and a review of potential windowed events was not needed.  
=


B-7}}
B-7 Plant LER Event Date Description LER Date Screen Date Criterion Date Assigned Date Completed Classification Calvert Cliffs 2 318-21-003 8/10/21 AFW Pump Inoperable Due to Improper Reset of Trip Throttle Valve 9/23/21 9/29/21 3b 9/30/21 2/2/21 Analyst Screen-Out Analyst Justification. A Green finding was identified in IR 05000318/2021002 (ML21222A039); the LER remains open. On August 10, 2021, the licensee received an inspection report documenting the NRCs position that the turbine-driven auxiliary feedwater (TDAFW) pump 22 was considered inoperable from March 20, 2021, until March 26, 2021, because its trip throttle valve was not reset properly. Specifically, the trip throttle valve, which is part of the pump overspeed trip mechanism, did not appear to be aligned properly such that the trip hook and latch-up lever were not fully engaged. The licensee later determined that the post-maintenance procedure had inadequate instructions regarding the verification that trip hook and latch-up lever were fully engaged. NRC inspectors determined that the licensee failure to properly reset the TDAFW pump 22 trip throttle in accordance with the surveillance test procedure was a performance deficiency. The inspectors determined that the performance deficiency was more than minor; however, the degraded condition did not represent a loss of safety function of one train of a multi-train system for greater than its TS allowed outage time. Therefore, the performance deficiency was determined to be Green (i.e.,
very low safety significance). A search for windowed events identified LER 318-2021-002 associated with a failed main feedwater regulating valve on March 21st, which resulted in a subsequent manual reactor trip. A risk assessment was performed assuming a reactor trip with the failure of the TDAFW pump 22 to evaluate this windowed event. Recovery of TDAWF pump 22 was not considered, which is potentially conservative. This analysis resulted in a CCDP of 1.5E-6, which is below the plant-specific CCDP for a nonrecoverable loss of feedwater and condenser heat sink of 2.8E-6 for Calvert Cliffs Unit 2. The risk of this condition, along with the windowed March 21st reactor trip, is below the ASP Program threshold and, therefore, is not a precursor.
Susquehanna 2 346-21-003 10/11/21 Automatic Reactor Scram due to Main Turbine Trip 12/9/21 2/28/22 2h 2/28/22 3/8/22 Analyst Screen-Out Analyst Justification. This event is not discussed in any IR to date; the LER remains open. On October 11, 2021, the Unit 2 reactor automatically scrammed due to a main turbine trip. The MCR received indication of a main turbine trip with both divisions of the RPS actuated and all control rods inserted. The turbine bypass valves (TBVs) opened automatically to control reactor pressure but failed to reclose causing the reactor to depressurize. Operators closed the MSIVs to stop reactor depressurization and manually initiated HPCI and RCIC to control reactor water level. Subsequently, operators maintained reactor water level in the normal operating band using RCIC and controlled reactor pressure using HPCI and the main steam line drains. The reactor recirculation pumps tripped on end-of-cycle trip. The licensee is still investigating the cause of the main turbine trip. A preliminary licensee investigation identified that a failed pressure transmitter resulted in the TBVs to close. A search of LERs did not yield any windowed events. The risk of this event is bounded by a non-recoverable loss of main feedwater and/or condenser heat sink. Therefore, the risk of this event is below the ASP Program threshold and is not a precursor.
Nine Mile Point 1 220-21-001 9/25/21 Isolation of Both Emergency Condensers due to Loss of UPS 162A 11/19/21 3/7/22 3a 3/8/22 3/17/22 SDP Screen-Out A Green finding was identified in IR 05000220/2021004 (ML22026A350); the LER is closed. On September 25, 2021, the MCR received multiple annunciators concurrent with a loss and subsequent restoration of RPS bus 11 on UPS 162A. This resulted in a half scram, reactor water cleanup isolation, and isolation of both emergency condensers. The emergency condenser system was declared inoperable and TS 3.1.3, LCO E was entered. Operators restored power to RPS bus 11 in 24 minutes using an alternative source. Both emergency condensers were restored to standby within 48 minutes. NRC inspectors determined that the licensee failure to ensure that an identified deviation from the normal operating frequency of UPS 162A was promptly identified and corrected was a performance deficiency. This performance deficiency was determined to be Green (i.e., very low safety significance) using the screening questions provided in Appendix A of Inspection Manual Chapter 0609. A search of LERs did not yield any windowed events. The SDP risk assessment is accepted as the ASP Program result, in accordance with RIS 2006-024, because there was no reactor trip nor windowed event. The risk of this condition is below the ASP Program threshold and, therefore, is not a precursor.
Fermi 341-21-002 8/22/21 Unplanned Inoperability of HPCI System Due to an Inverter Circuit Failure 10/21/21 11/5/21 3d 11/8/21 6/7/22 Reject A detailed ASP analysis determined that the CDP of the concurrent degraded conditions identified in the LER was less than the ASP Program threshold of 10-6 and, therefore, is not a precursor. The detailed ASP analysis is publicly available (ML22158A092).}}

Latest revision as of 16:54, 27 November 2024

U.S. NRC Accident Sequence Precursor Program 2021 Annual Report
ML22151A163
Person / Time
Issue date: 06/30/2022
From: Christopher Hunter
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Hunter, Christopher - 301 415 1394
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ML22167A097 List:
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Download: ML22151A163 (13)


Text

0 This report provides the results the Accident Sequence Precursor (ASP) Program for 2021. In addition, trends and key insights are provided for the past 10 years (2012 through 2021).

U.S. Nuclear Regulatory Commission Accident Sequence Precursor (ASP) Program 2021 Annual Report June 2022 Christopher Hunter (301) 415-1394 christopher.hunter@nrc.gov Performance and Reliability Branch Division of Risk Analysis Office of Nuclear Regulatory Research U.S. Nuclear Regulatory Commission Washington, DC 20555-0001

1

1. 2021 ASP RESULTS There were 135 licensee event reports (LERs) issued in calendar year 2021. From these LERs, 104 (approximately 77 percent) were screened out in the initial screening process and 31 events were selected and analyzed as potential precursors. The overall number of LERs and potential precursors continues to decrease to historical lows. Figure 1 provides a breakdown of the number of LERs reviewed by the ASP Program since the switch was made to review LERs issued on a calendar-year basis in 2016.

The ASP Program is looking at the potential of other data sources for potential precursors due the decreasing LERs for failures that have been reported historically.

Figure 1. ASP Program LER Review Breakdown Of the 31 potential precursors, 4 events were determined to exceed the ASP Program threshold and, therefore, are precursors. An independent ASP analysis was performed to determine the risk significance for three of these precursors. One precursor was the result of greater-than-Green inspection finding identified in 2021.1 Table 1 provides a brief description of all precursors identified in 2021. The three precursors identified in 2021 using an independent ASP analysis were compared with results from Management Directive (MD) 8.3, NRC Incident Investigation Program, (ML18073A200) and Significance Determination Process (SDP). This comparison is provided in Appendix A.

Table 1. 2021 Precursors Plant/Description LER/IR Event Date Exposure Time CCDP/

CDP Davis-Besse, Emergency Diesel Generator (EDG) Speed Switch Failure due to Direct Current System Ground (ML21356A058) 346-21-001 2/12/21 9 days White Finding Davis-Besse, Field Flash Selector Switch Failure Results in EDG Unavailability (ML22164A812) 05000346/2021050 (No LER was issued) 5/27/21 99 days 9x10-6 Davis-Besse, Reactor Trip due to Failed Uninterruptible Power Supply (UPS) and Steam Feedwater Rupture Control System Actuations (ML22125A048) 346-21-003 7/8/21 Initiating Event 3x10-6 Waterford, Loss of Offsite Power (LOOP) during Hurricane Ida (ML22122A190) 382-21-001 8/29/21 Initiating Event 5x10-4 After further analysis, the remaining 27 LERs identified by the initial LER screening were determined not to be precursors. Additional information on the LERs determined not to be precursors via an ASP analysis or by acceptance of SDP results is provided in Appendix B. The evaluation of other hazards beyond internal events (e.g., internal fires, seismic events) did not result in any additional precursors in 2021.

1 Two additional potentially greater-than-Green inspection findings, a finalized greater-than-Green cybersecurity finding at Davis-Besse Nuclear Station (ML20091L428) and a preliminary White radiation protection finding at Columbia Generating Station (ML21347A988), were identified in 2021. However, these findings were not associated with increased risk to core damage and, therefore, are out of the scope of the ASP Program.

2

2. ASP TRENDS Table 2. Precursor Trend Results Precursor Group Trend p-value All Precursors Decreasing 0.00001 Important Precursors [i.e., conditional core damage probability (CCDP) or increase in core damage probability (CDP) 10-4]

No Trend 0.4 Precursors with CCDP/CDP 10-5 Decreasing 0.01 Initiating Events Decreasing 0.002 Degraded Conditions Decreasing 0.001 LOOPs Decreasing 0.01 EDG Failures No Trend 0.9 Boiling-Water Reactor (BWR) Precursors Decreasing 0.02 Pressurized-Water Reactor (PWR) Precursors Decreasing 0.0002 These ASP trends, along with the results of the ASP index, indicate that NRC oversight and licensing activities remain effective and that licensee risk management initiatives are not resulting in an increasing risk profile for the industry.

Figure 2. Occurrence Rate of All Precursors ADDITIONAL PRECURSOR TRENDS Figure 3. Occurrence Rate of Initiating Event Figure 4. Occurrence Rate of BWR and PWR Figure 5. Occurrence Rate of LOOP and Degraded Condition Precursors Precursors Precursors 0.00 0.02 0.04 0.06 0.08 0.10 0.12 0.14 0.16 0.18 2012 2013 2014 2015 2016 2017 2018 2019 2020 2021 Precursor Occurrence Rate Year Initiating Events Degraded Conditions IE Trend DC Trend 0.00 0.05 0.10 0.15 0.20 0.25 0.30 0.35 0.40 0.45 2012 2013 2014 2015 2016 2017 2018 2019 2020 2021 Precursor Occurrence Rate Year BWR Precursors PWR Precursors PWR Trend BWR Trend 0.00 0.01 0.02 0.03 0.04 0.05 0.06 0.07 0.08 0.09 2012 2013 2014 2015 2016 2017 2018 2019 2020 2021 Precursor Occurrence Rate Year LOOPs with CCDP in the 1E-6 Range LOOPs with CCDP in the 1E-5 Range LOOP Important Precursors Trend

3

3. KEY INSIGHTS Key insights based on the review of the 99 precursors that were identified in the past decade (2012-2021) are provided in this section. Note that additional insights can be gathered by using the publicly available ASP Program Dashboard.

There were 5 important precursors identified during this period, all of were due to initiating events (4 LOOPs and a loss of service water).

The ratio of precursors identified via greater-than-Green vs. independent ASP evaluations continues to decrease. In 2016, the 10-year percentage was 69 percent, but is currently 54 percent.

The most frequent initiating events that resulted in precursors were LOOPs and losses of a condenser heat sink.

Natural phenomena caused 11 precursors, with snow/ice and lightning the most frequent causes.

The most frequent structure, system, and component (SSC) failures observed in precursors were associated with EDGs, flood protection, and switchyard.

A review of the precursors associated with inspection findings that had a significant impact on the risk of the event were most likely due to inadequate procedures or design issues.

There are no indications of increasing risk due to the potential cumulative impact of risk-informed initiatives.

No new component failure modes or mechanisms were identified. In addition, the likelihood and impacts of accident sequences have not changed.

Long duration LOOPs occurring at single-unit site have a high likelihood of resulting in a higher-risk precursors.

Figure 6. Precursor Breakdown by Risk Bin Figure 7. Most Frequent Initiating Event Precursor Types Figure 8. Natural Phenomena Precursors Causes Figure 9. Most Frequent Precursor SSC Failures Figure 10. Dominant Precursor SSC Failures 20 7

3 2

2 1

1 1

0 5

10 15 20 25 LOOP Loss of Condenser Heat Sink Transient Loss of Electrical Bus Loss of Feedwater Inadvertent Safety Injection Loss of Shutdown Cooling Loss of Service Water

  1. of Precursors 22 13 11 7

7 6

5 4

2 0

5 10 15 20 25 EDGs Flood Protection Switchyard HPCI Other SSCs Electical Buses SRVs RCIC Recirculation

  1. of Precursors 29%

38%

20%

12%

1%

Design Issues Inadequate Procedures Ineffective Corrective Action Program Human Errors Deficient Training

4

4. ASP INDEX The ASP index shows the cumulative plant average risk from precursors on an annual basis.

Unlike the trend analyses performed on various precursor groups that are focused on the occurrence rate of precursors, the ASP index is focused on the total risk due to all precursors.

Therefore, the ASP index provides a unique way to evaluate the risk of longer-term degraded conditions over the entire duration of the condition.

The ASP index does not exhibit a statistically significant trend (p-value = 0.7) for the past decade (2012-2021). The total risk associated with precursors (99 total precursors) is dominated by the 5 important precursors, which account for approximately 60 percent of the total risk due to all precursors. The other 94 precursors account for approximately 47 percent to the total risk due to all precursors.

Figure 3. ASP Index A description of how the ASP index is calculated is provided in past annual reports, which can be accessed from the ASP Program Public Webpage.

A-1 Appendix A: Comparison of 2021 ASP Analyses The three precursors identified in 2021 using an independent ASP analysis were compared with results from MD 8.3 and SDP analyses, as shown in the following table. Given the three programs have different functions, it is expected that the results are likely to be different.

Event Description Program Results SPAR Model/Methodology Improvements and Insights Davis-Besse, IR 05000346/

2021050 Field Flash Selector Switch Failure Results in EDG Unavailability MD 8.3. CDP estimated to be in the range of 7x10-7 to 5x106, which led to a special inspection. See IR 05000346/2021050 (ML21321A365) for additional information.

Credit for FLEX mitigation strategies was provided using with updated reliability data provided by the Pressurized Water Reactor Owners Group (PWROG). Modified FLEX modeling according to review of licensees final integrated plan.

SDP. No performance deficiency was identified for this event; therefore, no SDP evaluation was performed.

ASP. CDP = 9x10-6; EDG unavailable for 99 days. See final ASP analysis (ML22164A812) for additional information.

Davis-Besse, LER 346 003 Reactor Trip due to Failed UPS and Steam Feedwater Rupture Control System Actuations MD 8.3. CCDP = 1x106, which led to a special inspection. See IR 05000346/2021050 (ML21321A365) for additional information.

Modified loss of condenser heat sink event tree to account for potential overcooling. Used IDHEAS-ECA for human reliability analysis of critical human failure event.

SDP. Three Green findings were identified.

The first finding was associated with the licensee failure to appropriately classify the digital electro-hydraulic control UPS battery bank as non-critical as required by component classification procedures. The second finding was associated with the licensee failing to establish procedural guidance for transferring the gland sealing steam supply from the main steam system to the auxiliary steam system following a reactor trip. The third finding was associated with the licensee failure to have an appropriate procedure for the replacement of main steam isolation valve limit switch. All three findings were screened out (i.e., no detailed risk evaluation was performed). See IR 05000346/2021050 (ML21321A365) for additional information.

ASP. CCDP = 3x10-6; loss of condenser heat sink and overcooling. See final ASP analysis (ML22125A048) for additional information.

Waterford, LER 382 21 001 LOOP during Hurricane Ida MD 8.3. No evaluation performed.

Credit for FLEX mitigation strategies was provided using with updated reliability data provided by the PWROG.

Modified FLEX modeling according to review of licensees final integrated plan. Performed MELCOR calculations to support credit for long-term turbine-driven emergency feedwater pump operation. Performed event analyses for other plants that have experienced a LOOP during a hurricane in the past 20 years to develop generic risk insights.

SDP. No performance deficiency was identified for this event; therefore, no SDP evaluation was performed.

ASP. CCDP = 5x10-4; weather-related LOOP occurred during Hurricane Ida. See final ASP analysis (ML22122A190) for additional information.

B-1 Appendix B: 2021 ASP Program Screened Analyses The table in this appendix provides the justification for each LER that was screened out of the ASP Program based on a simplified or bounding analysis or by acceptance of SDP results. Note that the justification reflects the status of the LER (open or closed) at the time of the ASP completion date.

While ASP analysts monitor the final SDP evaluation of all findings for including greater-than-Green findings as precursors, the screen-out justification is not updated retroactively for events that were initially screened out by an ASP analysis and are later assessed as Green (i.e., very low safety significance) in the final SDP evaluation.

Plant LER Event Date Description LER Date Screen Date Criterion Date Assigned Date Completed Classification Comanche Peak 1 445-20-001 12/16/20 MFW Pump Failure to Trip 2/11/21 2/23/21 3b 3/18/21 4/7/21 Analyst Screen-Out Analyst Justification. This condition is not discussed in an inspection report (IR) to date; the LER remains open. On October 10, 2020, during a planned shutdown for refueling outage, operators could not manually trip main feedwater (MFW) pump 1A from the main control room (MCR). Subsequent attempts to trip the pump locally also failed. Operators declared 1 of 2 input signals to engineered safety feature actuation system (ESFAS) instrumentation inoperable for function 6.g of Technical Specification (TS) 3.3.2, which uses a two of two logic to automatically start both motor-driven auxiliary feedwater (MDAFW) pumps when both MFW pumps trip. The manual trip failed because MFW pump 1A trip oil pressure did not lower when operators attempted to trip the pump from the MCR and locally. Non-licensed operators closed the steam supply valves to the MFW pump 1A turbine and manually lowered trip oil pressure to activate the ESFAS trip signal. A search of LERs did not yield any windowed events. Although the anticipatory start function of the MDAFW pumps upon a loss of both MFW pumps was lost due to this failure, the other automatic start signals (e.g., low steam generator level) were not affected and remained available. In addition, the operators had the ability to manually start the MDAFW pumps. Given these considerations, the risk of this condition is qualitatively determined to be below the ASP Program threshold and, therefore, is not a precursor.

Shearon Harris 400-21-002 12/17/20 All ECCS Accumulator Isolation Valves Closed in Mode 3 With RCS Pressure Greater than 1000 psig 2/15/21 3/2/21 3d 3/18/21 4/7/21 Analyst Screen-Out Analyst Justification. This condition is not discussed in an IR to date; the LER remains open. On December 17, 2020, with the plant in Mode 3, reactor coolant system (RCS) pressure was being controlled between 900-1000 psig with all three cold leg accumulator discharge valves closed. Operators were manually controlling RCS pressure manual using a pressurizer spray valve with only one reactor coolant pump (RCP) running, which reduced the pressurizer spray effectiveness resulting in an RCS pressure increase. MCR operators took immediate actions to stop the pressure increase by fully opening the pressurizer spray vale, reducing charging flow, and turning off all pressurizer heaters.

However, these actions were not performed in time to prevent RCS pressure from exceeding 1000 psig. TS require that the cold leg accumulators be operable in Mode 3 when RCS pressure is greater than 1000 psig. Since all three cold leg accumulator discharge valves were closed, this TS requirement was not met for approximately 15 minutes until operators were able to reduce RCS pressure below 1000 psig. A search of LERs did not yield any windowed events. Because the licensee restored RCS pressure below 1000 psig within 15 minutes, the exposure time was not longer than the TS allowed outage time. Therefore, an evaluation of this condition under the ASP Program to determine whether it is a precursor is not warranted.

Limerick 1 352-20-002 11/16/20 HPCI and RCIC Were Not Aligned for Service During Startup Resulting in TS Violations 1/26/21 2/3/21 3d 3/29/21 4/7/21 Analyst Screen-Out Analyst Justification. This condition is not discussed in any IR to date; the LER remains open. On November 16, 2020, Unit 1 was starting up when the reactor steam dome pressure exceeded 150 psig without the reactor core isolation cooling (RCIC) system being aligned for service, which is contrary to TS 3.7.3. Reactor steam dome pressure continued to increase above 200 psig without the high-pressure coolant injection (HPCI) system being aligned for service and, therefore, the plant entered TS 3.5.1. During a shift change the oncoming MCR operating crew recognized HPCI was still isolated and immediately began to warm-up the HPCI system and align HPCI for operation. RCIC and HPCI were aligned for service and declared operable approximately 90 minutes and 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> after reactor steam dome pressure exceeded 150 psig and 200 psig, respectively. This condition was caused by the failure of operators to correctly perform the startup procedure. A search of LERs did not yield any windowed events. Because the licensee restored HPCI and RCIC within their TS required action times and the exposure times were not longer than the TS allowed outage times for those systems, an evaluation of this condition under the ASP Program to determine whether it is a precursor is not warranted.

LaSalle 2 374-21-001 12/23/20 HPCS Inoperable due to Water Leg Pump Breaker Cubicle Motor Contactor 2/18/21 3/2/21 3d 4/16/21 4/27/21 Analyst Screen-Out Analyst Justification: This condition is not discussed in any IR to date; the LER remains open. On December 23, 2020, the Unit 2 high-pressure core spray (HPCS) water leg pump tripped due to a breaker fault. Operators subsequently declared the HPCS system inoperable according to TS. The RCIC system was verified to be operable. The affected breaker cubicle control power transformer and motor starter contactor were replaced and the HPCS system was declared operable approximately 13 hours1.50463e-4 days <br />0.00361 hours <br />2.149471e-5 weeks <br />4.9465e-6 months <br /> after the initial failure. A search of LERs did not yield any windowed events. Since the HPCS system was unavailable for less than the limits of TS Limiting Condition of Operation (LCO) 3.5.1, Condition B (14 days), this condition is screened out and is not considered a precursor.

B-2 Plant LER Event Date Description LER Date Screen Date Criterion Date Assigned Date Completed Classification Susquehanna 1 387-21-001 3/9/21 Unplanned lnoperability of the HPCI System due to a PCIV Failure to Stroke Full Closed On-Demand due to an Intermittent Break in the Close Control Circuitry 5/6/21 5/13/21 3d 5/27/21 6/9/21 Analyst Screen-Out Analyst Justification. This condition is not discussed in any IR to date, the LER remains open. On March 9, 2021, during performance of quarterly HPCI system valve exercising, the HPCI turbine exhaust vacuum breaker inboard isolation valve (HV155F079) failed to stroke fully closed. The closure function of this valve supports primary containment isolation; however, this function was maintained given the outboard containment isolation valve (HV155F075) successfully stroked closed. The direct cause of the condition was an intermittent break in the valves close control circuitry likely due to dirty contacts on the HPCI turbine exhaust vacuum breaker inboard isolation valve hand switch. Key corrective actions include planned replacement of the hand switch. After the initial failure, operators successfully stroked HV155F079 open and closed within acceptance times. Although the HPCI system was TS inoperable for approximately 39 hours4.513889e-4 days <br />0.0108 hours <br />6.448413e-5 weeks <br />1.48395e-5 months <br />, operators could manually open HV155F079 to restore HPCI availability. A search of LERs did not yield any windowed events. Because the licensee restored HPCI within their TS required action time and the exposure time was not longer than the TS allowed outage time, an evaluation of this condition under the ASP Program to determine whether it is a precursor is not warranted.

Palo Verde 2 529-21-002 5/19/21 Reactor Trip during Plant Protection System Surveillance Testing 7/16/21 8/5/21 1d/2h 8/6/21 8/12/21 Analyst Screen-Out Analyst Justification. This event is not discussed in any IR to date; the LER remains open. On May 19, 2021, an invalid actuation of the safety injection (SI), containment isolation, and main steam isolation signals occurred resulting in an automatic reactor trip due to high pressurizer pressure caused by the closure of the main steam isolation valves (MSIVs). The essential AFW pumps automatically started due to low steam generator (SG) level. Both trains of the high-pressure safety injection (HPSI) and low-pressure safety injection (LPSI),

containment spray, and essential spray pond pumps automatically started due to the SI actuation signal. RCS pressure remained above the HPSI pump head and, therefore, no injection into the RCS occurred during this event. In addition, the emergency diesel generators (EDGs) automatically started; however, the EDGs did not load onto their respective buses because they remained supplied by offsite power.

Operators reset SI actuation signal, closed the HPSI and LPSI injection valves, and stopped all HPSI, LPSI, and containment spray pumps as directed by the emergency operating procedures (EOPs). Although the steam supply to the MFW pumps was interrupted by the closure of the MSIVs, the condensate system continued to operate, and condenser vacuum remained intact. MFW was potentially recoverable using existing plant procedures in approximately 30 minutes. This event was caused by invalid trip signal that occurred during plant protection system functional testing. A search of LERs did not yield any windowed events. The risk of this event is bounded by a non-recoverable loss of main feedwater and/or condenser heat sink. Therefore, the risk of this event is below the ASP Program threshold and is not a precursor.

Peach Bottom 2 277-21-001 4/29/21 HPCI System Declared Inoperable Due to Instrument Power Inverter Failure 6/24/21 7/22/21 3d 8/6/21 8/12/12 Analyst Screen-Out Analyst Justification. This condition is not discussed in any IR to date; the LER remains open. On April 29, 2021, the HPCI system inverter circuit failure alarm was received the MCR. Operators immediately noticed erratic performance of HPCI system pressure instruments and a loss of the expected status display on the HPCI flow controller. Examination of the HPCI rack-mounted inverter revealed that the power indicator light was cycling on and off. Further inspection of the HPCI back panel revealed that the logic bus power monitoring relay was chattering. In the event of a valid HPCI initiation signal, the erratic power supply to the HPCI flow controller would have resulted in a loss of HPCI safety function. On April 30th, the inverter replacement was completed, and HPCI function was restored after satisfactorily testing was completed. The exposure time for the failed HPCI inverter was approximately 15 hours1.736111e-4 days <br />0.00417 hours <br />2.480159e-5 weeks <br />5.7075e-6 months <br />. A search of LERs identified LER 277-21-002 as a potential windowed event. The windowed aspect of these two events will be evaluated as part of the ASP evaluation of LER 277-21-002.

Because the licensee restored HPCI within their TS required action time (14 days) and the exposure time was not longer than the TS allowed outage time, an evaluation of this condition under the ASP Program to determine whether it is a precursor is not warranted.

Braidwood 1 456-21-001 4/23/21 Train A and B Source Range Neutron Flux Trip Functions Bypassed During Plant Startup 6/21/21 7/8/21 3a 7/19/21 8/25/21 Analyst Screen-Out Analyst Justification. This condition is not discussed in any IR to date; the LER remains open. On April 23, 2021, during reactor startup activities with the plant in Mode 2, operators identified that both trains A and B source range neutron flux reactor trip functions were bypassed. Operators immediately took the bypass switches to normal in accordance with TS. The incorrect position of the source range neutron flux reactor trip functions existed since April 21st while the plant was in Mode 5 operation. A licensee review determined that on April 21st, with the plant in Mode 5, both source range neutron flux trips were placed in bypass per procedure in support of switchyard activities.

After the switchyard activities were completed, operators failed to restore the source range neutron flux trips per procedure. A search of LERs did not yield any windowed events. The source range neutron flux trips provide protection during postulated uncontrolled rod withdrawal events. The source range detectors provide indication of an RCS boron dilution event. However, there are diverse trip and indications for both of these events (e.g., power range high neutron flux trip, volume control tank level alarm, etc.). Given the availability of the redundant, but diverse systems and the short exposure time of less than 3 days, the risk of this condition is qualitatively determined to be below the ASP Program threshold and, therefore, is not a precursor.

B-3 Plant LER Event Date Description LER Date Screen Date Criterion Date Assigned Date Completed Classification Peach Bottom 2 277-21-002 5/18/21 SRV lnoperability Due to Nitrogen Leakage from Braided Hose Wear 7/16/21 8/5/21 3d 7/29/21 8/25/21 Analyst Screen-Out Analyst Justification. This condition is not discussed in any IR to date; the LER remains open. On March 21, 2021, operators noted that the instrument nitrogen compressors were increasing in run hours, with all other related parameters steady. The condition was monitored and trended, and investigation determined the most likely cause to be nitrogen leakage within primary containment. A second step increase in nitrogen leakage occurred in May, which led to the decision to decrease reactor power to allow for entry into primary containment and investigate the source of leakage. On May 18th, the licensee identified that the nitrogen supply to safety relief valve (SRV) RV-2-02-071K was the source of the leak. Specifically, the stainless-steel braided hoses that supply and return nitrogen from the actuating solenoid valve had failed. This valve is one of five automatic depressurization system (ADS) valves and, therefore, the ADS function was declared inoperable according to TS 3.5.1. The failure of the braided hoses did not affect the overpressure function of SRV RV-2-02-071K. Note that the other four ADS valves use hard pipe for the instrument nitrogen supplies and returns. The hoses were replaced on May 18th and the unit was returned to full power. A search of LERs identified LER 277-21-001 as a potential windowed event. A risk assessment was performed assuming the unavailability of ADS valve 71K to open for its depressurization function. A potentially conservative exposure time of 75 days (March 5th to May 18th) was used. This analysis resulted in a CDP of 4E-9 from internal events, internal fires, internal floods, seismic hazards, high winds, and tornados. A sensitivity analysis assuming the concurrent unavailability of the HPCI system for an exposure time of 15 hours1.736111e-4 days <br />0.00417 hours <br />2.480159e-5 weeks <br />5.7075e-6 months <br /> (from LER 277-21-001) results in a CDP of 4E-7, which is dominated by the risk of the HPCI failure during postulated internal fires scenarios. The risk of this condition, including the windowed aspects of LER 277-21-001, is below the ASP Program threshold and is not a precursor.

Palisades 255-21-001 6/16/21 Atmospheric Steam Dump Valves Inoperable Due to Relay Failure 8/13/21 8/30/21 3i 8/30/21 9/8/21 Analyst Screen-Out Analyst Justification. This condition is briefly mentioned in IR 05000255/2021002 (ML21222A118); the LER remains open. On June 16, 2021, operators smelled an acrid odor in the MCR. A subsequent investigation revealed that the steam dump control relay failed as result of a short circuit in the coil, which rendered all four atmospheric dump valves (ADVs) inoperable. The total relief capacity of the ADVs is a steam flow of 30% with the reactor at full power and their operation prevents lifting the main steam safety valves following a turbine trip. The failed relay coil resulted in an overcurrent condition causing the supply fuse to open disabling both the ADVs automatic fast-open function and manual operation. The relay failure was due to age being beyond the vendor recommended life for a normally energized relay because the licensee had improperly classified it as a low-duty cycle instead of a high-duty cycle. The fuse and relay were replaced and the ADVs were returned to service approximately 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> later. A search of LERs did not yield any windowed events. Because the licensee restored the ADVs within their TS required action time (24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />) and the exposure time was not longer than the TS allowed outage time for the system, an evaluation of this condition under the ASP Program to determine whether it is a precursor is not warranted.

Hope Creek 354-21-001 6/14/21 SRV As-Found Setpoint Failures 8/13/21 8/27/21 3i 8/30/21 9/15/21 Analyst Screen-Out Analyst Justification. This condition is not discussed in any IR to date; the LER remains open. On June 14, 2021, tests of the pilot stage assemblies of SRVs A and J exceeded the lift setting tolerance of the nominal setpoint values prescribed in TS. In addition, SRV R failed to lift when tested. Hope Creek has 14 safety-related main steam SRVs that provide reactor pressure vessel overpressure protection and an automatic/manual depressurization function. The setpoint exceedance for SRVs A and J was attributed to corrosion bonding between the pilot discs and seating surfaces. The cause of SRV R not lifting was main disc and piston thread wear. SRV R was replaced, and the seven two-stage SRVs (including SRVs A and J) were replaced with three-stage models. A search of LERs did not yield any windowed events.

Although SRVs A and J exceeded their lift setpoints by slightly greater than 3%, the licensee determined that both SRVs would have remained available to prevent overpressure of the reactor pressure vessel according to the margins of the plants design analysis. In addition, TS only requires 13 of 14 SRVs to be operable and, therefore, the failure of SRV R did not affect the availability of overpressure protection of the reactor pressure vessel. Given these considerations, an evaluation of this condition under the ASP Program to determine whether it is a precursor is not warranted.

Fermi 341-21-001 5/3/21 Unrecognized Impact of Opening of Barrier Doors on HELB Analysis 7/1/21 7/22/21 3d 7/23/21 9/15/21 Analyst Screen-Out Analyst Justification. This condition is not discussed in any IR to date; the LER remains open. On May 3, 2021, the licensee determined that the reactor building steam tunnel door had been open on several occasions for longer than was required for personnel ingress/egress. If a postulated high-energy line break (HELB) had occurred while the door was open, equipment outside the reactor building steam tunnel could have been adversely impacted by the post-HELB conditions. The maximum time the door was open over any 1-year period was approximately 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />. A search of LERs did not yield any windowed events. A risk assessment was performed assuming that the reactor building steam tunnel door was open for an exposure time of 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> using the Fermi SPAR model that was modified by Idaho National Laboratory (INL) to include a main steam line break (MSLB) event tree. This risk assessment conservatively assumed that HPCI, RCIC, residual heat removal (RHR), and low-pressure core spray (LPCS) would fail as the result of post-HELB conditions during a postulated MSLB in the reactor building steam tunnel with the door open. The MLSB initiating event frequency is considered bounding because not all steam line breaks would occur in the reactor building steam tunnel. This analysis resulted in a CDP of 2E-10. The risk of this degraded condition is below the ASP Program threshold and, therefore, is not a precursor.

B-4 Plant LER Event Date Description LER Date Screen Date Criterion Date Assigned Date Completed Classification Susquehanna 2 388-21-001 7/6/21 Condition Prohibited by TS Due to Drift of Reactor Pressure Switch 9/1/21 9/3/21 3d 9/7/21 10/14/21 Analyst Screen-Out Analyst Justification. This condition is not discussed in any IR to date; the LER remains open. On July 6, 2021, the channel D of reactor steam dome pressure low permissive pressure switch dropped below TS allowable value, which is intended to ensure that the emergency core cooling system (ECCS) injection prevents the fuel peak cladding temperature from exceeding regulatory limits. In addition, channel C was under surveillance test when operator found the instrument drift on channel D and, therefore, two channels were inoperable at the same time. Although the drift of channel D was below the TS allowable value, the as-found set point remained above the limit assumed in the accident analysis and, therefore, the licensee determined that ECCS remained available. Since ECCS remained available, this condition is not a precursor, and a review of potential windowed events was not needed.

Hatch 1 321-21-003 9/8/21 HPCI System Discharge Valve Failure to Open 11/1/21 11/18/21 3d 11/19/21 11/30/21 Analyst Screen-Out Analyst Justification. This condition is not discussed in any IR to date; the LER remains open. On September 8, 2021, the HPCI pump discharge isolation valve was stroked closed as a part of surveillance testing. Subsequent attempts by operators to reopen the valve failed.

HPCI was declared inoperable in accordance with TS. Licensee troubleshooting determined that the pinion gear key in the valve actuator had not been properly staked during maintenance activities completed in 2006, which resulted in the key moving and the pinion gear disengaging from the actuator motor shaft. This issue was corrected on September 9th and HPCI was returned to operable status. The HPCI pump discharge isolation valve is normally open valve and does not change position during HPCI operations. Therefore, the exposure time of the loss of HPCI system function was limited to the 2 days when the valve was closed on September 8th and 9th. A search of LERs did not yield any windowed events. Since the HPCI system was unavailable for less than the limits of TS, this condition is screened out and is not considered a precursor.

Point Beach 1 266-21-001 7/31/21 MFW Pump Trip Results in Manual Reactor Trip 9/28/21 10/19/21 2h 10/20/21 12/6/21 Analyst Screen-Out Analyst Justification. This event is not discussed in any IR to date; the LER remains open. On July 31, 2021, operators manually tripped the reactor due to the failure of the MFW pump B motor. After the reactor trip, the AFW pumps started and restored SG inventory levels. During the trip response, a condenser steam dump valve cycled but did not fully close, requiring operators to locally close the valve to prevent additional reactor cooldown. In addition, the crossover steam dump valves did not close resulting in deteriorating vacuum in the main condenser. Operators subsequently closed the valves resulting in the unavailability of the main condenser. The SG ADVs were used for decay heat removal. During the feedwater transition, the MFW regulating bypass valve B did not maintain proper control of SG levels in automatic requiring operators to take manual control of the valve. MFW pump A remained available throughout the event; however, reactor power was too high to support the loss of one of the two MFW pumps without requiring a reactor trip. A search of LERs did not yield any windowed events. The risk of this event is bounded by a non-recoverable loss of main feedwater and/or condenser heat sink. Therefore, the risk of this event is below the ASP Program threshold and is not a precursor.

Perry 440-21-001 6/1/21 Division 3 EDG lnoperability Resulting in an Operation or Condition Prohibited by TS 7/28/21 8/19/21 3d 8/20/21 12/6/21 Analyst Screen-Out Analyst Justification. This condition is not discussed in any IR to date; the LER remains open. On June 1, 2021, erratic output voltage was observed on the division 3 EDG approximately 45 seconds after starting during monthly surveillance testing. The operators initially believed that the EDG was still operable; however, a subsequent evaluation did not support continued operability and the division 3 EDG was later declared inoperable on June 3rd according to TS. On June 4th, voltage regulator was replaced and was tested satisfactory, thus restoring the division 3 EDG to operable status. Discussions with NRC inspectors indicate that although the voltage fluctuation exceeded the TS limit, the voltages and frequencies experienced during the surveillance test were sufficient to support successful operation of the division 3 EDG.

Since the division 3 EDG remained available, this condition is not a precursor, and a review of potential windowed events was not needed.

Nine Mile Point 1 220-21-002 9/25/21 Isolation of both Emergency Condensers due to loss of UPS 162A 11/19/21 12/3/21 3d 12/6/21 12/7/21 Analyst Screen-Out Analyst Justification. This condition is not discussed in any IR to date; the LER remains open. On September 25, 2021, the MCR operators received multiple annunciators due to the loss of power to reactor protection system (RPS) bus 11 caused by the failure of the uninterruptible power supply (UPS) 162A. The loss of power to RPS bus 11 resulted in a half scram, isolation of the reactor water cleanup system, and isolation of both emergency condensers. Operators subsequently declared the emergency condenser system inoperable according to TS, which requires operators to manually shutdown that plant within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />. Operators reenergized RPS bus 11 from instrumentation bus 130A in approximately 24 minutes. Both emergency condensers were restored to standby in approximately 39 minutes and 48 minutes respectively and, therefore, the reactor shutdown was no longer required. A search of LERs did not yield any windowed events. A risk assessment was performed assuming the unavailability of both emergency condensers for 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />, which is the minimum exposure time allowed by SAPHIRE.

This analysis resulted in a CDP of 1E-8 from internal events, seismic hazards, and high winds (including tornados). Internal flooding and fire scenarios are not included in the Nine Mile Point 1 SPAR model; however, the risk impact associated with these hazards is expected to be minimal due to the very short exposure time of this condition. The risk of this degraded condition is below the ASP Program threshold and, therefore, is not a precursor.

B-5 Plant LER Event Date Description LER Date Screen Date Criterion Date Assigned Date Completed Classification Limerick 1 352-21-001 9/23/21 HPCI Inoperable Due to Remote Shutdown Panel Switch Failure 11/22/21 12/3/21 3d 12/6/21 12/15/21 Analyst Screen-Out Analyst Justification. This condition is not discussed in any IR to date; the LER remains open. On September 23, 2021, the licensee was scheduled to perform the HPCI logic system functional isolation logic test and the HPCI pump valve and flow test. The HPCI logic system function isolation test was completed successfully. However, during the initial start of the turbine during the HPCI pump valve and flow test the indicated turbine speed on the plant computer point and MCR tachometer was downscale. The test was subsequently aborted when the HPCI pump was not able to meet the TS requirements for rated flow and discharge pressure. Licensee troubleshooting determined a high contact resistance existed in the HPCI emergency shutdown switch located on the remote shutdown panel. The purpose of this switch is to terminate or prevent HPCI injection from the remote shutdown panel under various fire safe shutdown events. The HPCI emergency shutdown switch high resistance was attributed to mechanical switch degradation that was introduced by cycling the switch during the HPCI logic system functional isolation logic test, which was performed 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> and 32 minutes prior to the HPCI pump valve and flow surveillance test. A search of LERs did not yield any windowed events. The HPCI system was unavailable for less than TS allowed outage time of 14 days. In addition, the failure of the HPCI emergency shutdown switch was in the safe direction (i.e., the high contact resistance would have terminated HPCI injection if manipulated during a MCR abandonment scenario). Given these considerations, the risk of this condition is qualitatively determined to be below the ASP Program threshold and, therefore, is not a precursor.

Vogtle 1 424-21-001 9/16/21 Train A SI Pump Inoperability Causes the Unit to operate in a Condition Prohibited by TS 11/15/21 11/18/21 3d 11/19/21 12/15/21 Analyst Screen-Out Analyst Justification. This condition is not discussed in any IR to date, the LER remains open. During the refueling outage on September 16, 2021, plant operators conducted a surveillance test of SI pump 1A. During the test, pump bearing temperatures rose rapidly requiring operators to secure the pump. A subsequent licensee investigation found a piece of plastic tubing between the gears of the lube oil pump, which resulted in lack of oil to the two bearings causing their failure. The pump was returned to operable status on September 29th after the bearing were replaced and the system was flushed. Improper oil sampling of SI pump 1A performed on September 6, 2021, introduced the foreign material into the pump's oil system. The plant entered into Mode 4 on September 12th as part a refueling outage. A search of LERs did not yield any windowed events. A risk assessment was performed assuming the SI pump 1A was failed for an exposure time of 138 hours0.0016 days <br />0.0383 hours <br />2.281746e-4 weeks <br />5.2509e-5 months <br /> (September 6th through September 12th). This analysis resulted in a mean CDP 2E-8 from internal events, internal fires, internal floods, seismic hazards, and high winds (including tornados). The risk of this degraded condition is below the ASP Program threshold and, therefore, is not a precursor.

Browns Ferry 1 and 2

259-21-001 3/3/21 480V Load Shed Logic Inoperable Longer than Allowed by TS due to Failed Relay 11/22/21 12/3/21 3e 12/6/21 1/10/22 Analyst Screen-Out Analyst Justification. This condition is not discussed in any IR to date; the LER remains open. On September 23, 2021, the division I 480V load shed logic for Units 1 and 2 was declared inoperable during the performance of surveillance testing. During the test, relay 0-RLY-231-00A7 failed to energize due to an open circuit in the coil. The division I 480V was declared inoperable according to TS. The relay was replaced and the division I 480V load shed logic was declared operable on September 25th. A subsequent engineering evaluation determined that relay 0-RLY-231-00A7 was likely failed since the last time it was energized during testing on March 3, 2021. During this period, the division II 480V load shed logic was out of service twice to support testing on March 4th and May 19th for a total of 78 hours9.027778e-4 days <br />0.0217 hours <br />1.289683e-4 weeks <br />2.9679e-5 months <br />. A search of LERs did not yield any windowed events. The loss of both divisions of the load shed logic would result in the failure of all four shared EDGs between Units 1 and 2 given a concurrent loss offsite power (LOOP) and loss-of-coolant accident (LOCA) event. The SPAR models include the load shed logic as part of the EDG sequencer component boundary, which does not allow the modeling of this degraded condition. Model changes were made to include the failure of both divisions of load shed logic given a concurrent LOOP and LOCA would result in the failure of all four Unit 1 and 2 EDGs. A risk assessment was performed assuming (a.) the unavailability of the division I load shed logic from March 3, 2021, until September 25, 2021 (i.e., an exposure time of 207 days) and (b.) the unavailability of both EDG sequencers for an exposure time of 78 hours9.027778e-4 days <br />0.0217 hours <br />1.289683e-4 weeks <br />2.9679e-5 months <br />. These assessments result in a mean CDP of 8E-10 and 5E-9 from internal events, seismic hazards, and high winds (including tornados), respectively. These results are conservative because the FLEX mitigation strategies were not credited. The risk impact is dominated by seismic scenarios that result in concurrent LOOP and LOCA. Internal flooding and fire scenarios are not included in the Browns Ferry SPAR model; however, the risk impact associated with these hazards is expected to be small for this condition because these hazards are unlikely to lead to concurrent LOOP and LOCA. The risk of this degraded condition is below the ASP Program threshold and, therefore, is not a precursor.

B-6 Plant LER Event Date Description LER Date Screen Date Criterion Date Assigned Date Completed Classification Diablo Canyon 2 323-21-001 7/22/21 EDG Declared Inoperable due to Low Frequency Condition Discovery during Routine Surveillance 9/20/21 9/29/21 3e 9/30/21 1/10/22 Analyst Screen-Out Analyst Justification. This condition is not discussed in any IR to date; the LER remains open. On July 21, 2021, EDG 2-3 was started on a simulated under-voltage signal for routine surveillance testing. With the mode select switch in the AUTO position, the frequency indicated 58.9 Hz, which is below the TS required minimum of 59.5 Hz. Operators placed the EDG 2-3 mode select switch in MANUAL and the frequency and speed were adjusted into their proper band and the test was completed meeting the acceptance criteria. The cause of the EDG 2-3 low frequency condition was due to an inadequately performed post-maintenance testing on June 30, 2021. Specifically, the testing sequence did not fully consider the need for revalidation of frequency following setting of the EDG governor following maintenance activities.

The Diablo Canyon USAR Section 8.3.1.1.6.1.13, Selection of Diesel Generator Set Capacity for Standby Power Supplies, refers to Safety Guide 9, March 1971, Selection of DG Capacity for Standby Power Supplies, (ML12305A251). The safety guide allows frequency to decrease by 2% during recovery from transients (i.e., approximately 1.2 Hz). Since the frequency only decreased by 1.1 Hz, the EDG remained functional within the limits of the safety guide capacity. Since EDG 2-3 remained available, this condition is not a precursor, and a review of potential windowed events was not needed.

Grand Gulf 416-21-003 9/9/21 HPCS Declared Inoperable 11/4/21 11/18/21 3d 11/19/21 1/11/22 Analyst Screen-Out Analyst Justification. This condition is not discussed in any IR to date; the LER remains open. On September 9, 2021, the MCR received an alarm for HPCS out of service along with HPCS motor operated valve/overload power loss status light. In addition, the HPCS minimum flow to suppression pool light indication was lost. Licensee troubleshooting revealed that this condition was caused by the failure of the alarm relay associated with HPCS minimum flow to suppression pool breaker due to the shorting of its coil. This failed relay subsequently caused the control circuit fuse to blow resulting in the inability to open the HPCS minimum flow valve to the suppression pool. The licensee took immediate action and replaced the damaged relay and associated control fuse. A search of LERs did not yield any windowed events.

Because the licensee restored the HPCS within their TS required action time (14 days) and the exposure time was not longer than the TS allowed outage time for the system, an evaluation of this condition under the ASP Program to determine whether it is a precursor is not warranted.

Susquehanna 1 387-21-004 10/7/21 Loss of 1B RHRSW Pump due to Cable Damage During Excavation Activities 12/1/21 1/3/22 3d 1/4/21 1/20/22 Analyst Screen-Out Analyst Justification. This condition is not discussed in any IR to date; the LER remains open. On October 7, 2021, operators observed current oscillations during a run of residual heat removal service water (RHRSW) pump 1B. Operators secured the pump and entered TS 3.7.1, Condition B for an inoperable RHRSW subsystem. Licensee troubleshooting identified the cause of the current oscillations to be a ground on the B-phase power cable for the pump that was likely damaged during excavation activities on September 23, 2021. The power cable was replaced and the RHRSW system was declared operable on October 11th. On September 19, 2021, the RHRSW train A subsystem was declared inoperable due to ultimate heat sink spray array and bypass valve alignments to support spray array inspection and nozzle cleaning. However, the licensee determined that the RHRSW train A subsystem remained available. A search of LERs did not yield any windowed events. A risk assessment was performed assuming the RHRSW pump 1B was failed from September 23rd until October 11th (i.e., an exposure time of 19 days). This analysis resulted in a CDP of 2E-7 from internal events, seismic hazards, and high winds (including tornados). A review of these results indicates that this result is likely very conservative (i.e., by at least an order of magnitude) because cross-unit common-cause failure (CCF) of the RHRSW pumps is the dominant failure and the existing CCF data does not currently support this application. In addition, the human error probability for containment venting appears to be very conservative for loss of instrument air and applicable LOOP scenarios. Internal flooding and fire scenarios are not included in the Susquehanna Unit 1 SPAR model. Licensee risk information for these hazards is available; however, specific scenario information for this condition is not available at this time. The risk impact from internal flooding scenarios is expected to be minimal for this condition. The risk from internal fires for this scenario could be dominant this condition; however, it is unlikely to result in exceeding the precursor threshold by itself. Given these considerations, the risk of this degraded condition is judged to be below the ASP Program threshold and, therefore, is not a precursor.

Fermi 341-21-003 6/3/21 HPCI Inoperable due to Contact Oxidation 12/29/21 1/10/22 3d 1/10/22 1/21/22 Analyst Screen-Out Analyst Justification. This condition is not discussed in any IR to date; the LER remains open. On June 3,2021, the licensee was performing the HPCI condensate storage tank (CST) level channel functional test and the HPCI pump suction isolation valve from the suppression pool took approximately 5 minutes to open on the simulated low CST level signal. This condition resulted in the plant entering TS 3.3.5.1, Actions D.2.1 and D.2.2, which allows 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> to place the channel in trip or to align HPCI pump suction to the suppression pool. The licensee HPCI suction was transferred to the suppression pool later on June 3rd. Licensee troubleshooting of the condition identified an oxidated relay contact was the cause of the slow opening of the suction isolation valve. The licensee later determined that this condition affected both channels and, therefore, the licensee should have declared the HPCI system inoperable according to TS 3.3.5.1, Action D.1. After repair of the relay was completed and reperforming the HPCI CST level channel functional test, the licensee declared the HPCI system operable on June 4th. A licensee evaluation determined that HPCI would operate as designed for most of the 5 minutes it would take to automatically transfer suction from the CST to the suppression pool. However, CST level would have lowered to a level where air entrainment would have occurred and, therefore, HPCI would have tripped on a low suction pressure signal without operator action. Upon completion of the late suction transfer, suction pressure would be restored, and HPCI would automatically restart if demanded and continue to inject. In addition, procedures direct operators to complete any incomplete automatic actions manually, which means there was a high likelihood that operators would complete the HPCI suction transfer prior to HPCI tripping on low suction pressure given this condition. Because the HPCI would have restarted automatically if the slow transfer resulted in a low suction trip, HPCI remained available and, therefore, this condition is not a precursor, and a review of potential windowed events was not needed.

B-7 Plant LER Event Date Description LER Date Screen Date Criterion Date Assigned Date Completed Classification Calvert Cliffs 2 318-21-003 8/10/21 AFW Pump Inoperable Due to Improper Reset of Trip Throttle Valve 9/23/21 9/29/21 3b 9/30/21 2/2/21 Analyst Screen-Out Analyst Justification. A Green finding was identified in IR 05000318/2021002 (ML21222A039); the LER remains open. On August 10, 2021, the licensee received an inspection report documenting the NRCs position that the turbine-driven auxiliary feedwater (TDAFW) pump 22 was considered inoperable from March 20, 2021, until March 26, 2021, because its trip throttle valve was not reset properly. Specifically, the trip throttle valve, which is part of the pump overspeed trip mechanism, did not appear to be aligned properly such that the trip hook and latch-up lever were not fully engaged. The licensee later determined that the post-maintenance procedure had inadequate instructions regarding the verification that trip hook and latch-up lever were fully engaged. NRC inspectors determined that the licensee failure to properly reset the TDAFW pump 22 trip throttle in accordance with the surveillance test procedure was a performance deficiency. The inspectors determined that the performance deficiency was more than minor; however, the degraded condition did not represent a loss of safety function of one train of a multi-train system for greater than its TS allowed outage time. Therefore, the performance deficiency was determined to be Green (i.e.,

very low safety significance). A search for windowed events identified LER 318-2021-002 associated with a failed main feedwater regulating valve on March 21st, which resulted in a subsequent manual reactor trip. A risk assessment was performed assuming a reactor trip with the failure of the TDAFW pump 22 to evaluate this windowed event. Recovery of TDAWF pump 22 was not considered, which is potentially conservative. This analysis resulted in a CCDP of 1.5E-6, which is below the plant-specific CCDP for a nonrecoverable loss of feedwater and condenser heat sink of 2.8E-6 for Calvert Cliffs Unit 2. The risk of this condition, along with the windowed March 21st reactor trip, is below the ASP Program threshold and, therefore, is not a precursor.

Susquehanna 2 346-21-003 10/11/21 Automatic Reactor Scram due to Main Turbine Trip 12/9/21 2/28/22 2h 2/28/22 3/8/22 Analyst Screen-Out Analyst Justification. This event is not discussed in any IR to date; the LER remains open. On October 11, 2021, the Unit 2 reactor automatically scrammed due to a main turbine trip. The MCR received indication of a main turbine trip with both divisions of the RPS actuated and all control rods inserted. The turbine bypass valves (TBVs) opened automatically to control reactor pressure but failed to reclose causing the reactor to depressurize. Operators closed the MSIVs to stop reactor depressurization and manually initiated HPCI and RCIC to control reactor water level. Subsequently, operators maintained reactor water level in the normal operating band using RCIC and controlled reactor pressure using HPCI and the main steam line drains. The reactor recirculation pumps tripped on end-of-cycle trip. The licensee is still investigating the cause of the main turbine trip. A preliminary licensee investigation identified that a failed pressure transmitter resulted in the TBVs to close. A search of LERs did not yield any windowed events. The risk of this event is bounded by a non-recoverable loss of main feedwater and/or condenser heat sink. Therefore, the risk of this event is below the ASP Program threshold and is not a precursor.

Nine Mile Point 1 220-21-001 9/25/21 Isolation of Both Emergency Condensers due to Loss of UPS 162A 11/19/21 3/7/22 3a 3/8/22 3/17/22 SDP Screen-Out A Green finding was identified in IR 05000220/2021004 (ML22026A350); the LER is closed. On September 25, 2021, the MCR received multiple annunciators concurrent with a loss and subsequent restoration of RPS bus 11 on UPS 162A. This resulted in a half scram, reactor water cleanup isolation, and isolation of both emergency condensers. The emergency condenser system was declared inoperable and TS 3.1.3, LCO E was entered. Operators restored power to RPS bus 11 in 24 minutes using an alternative source. Both emergency condensers were restored to standby within 48 minutes. NRC inspectors determined that the licensee failure to ensure that an identified deviation from the normal operating frequency of UPS 162A was promptly identified and corrected was a performance deficiency. This performance deficiency was determined to be Green (i.e., very low safety significance) using the screening questions provided in Appendix A of Inspection Manual Chapter 0609. A search of LERs did not yield any windowed events. The SDP risk assessment is accepted as the ASP Program result, in accordance with RIS 2006-024, because there was no reactor trip nor windowed event. The risk of this condition is below the ASP Program threshold and, therefore, is not a precursor.

Fermi 341-21-002 8/22/21 Unplanned Inoperability of HPCI System Due to an Inverter Circuit Failure 10/21/21 11/5/21 3d 11/8/21 6/7/22 Reject A detailed ASP analysis determined that the CDP of the concurrent degraded conditions identified in the LER was less than the ASP Program threshold of 10-6 and, therefore, is not a precursor. The detailed ASP analysis is publicly available (ML22158A092).