IR 05000255/2021002

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Integrated Inspection Report 05000255/2021002
ML21222A118
Person / Time
Site: Palisades Entergy icon.png
Issue date: 08/10/2021
From: Billy Dickson
NRC/RGN-III/DRP/B2
To: Corbin D
Entergy Nuclear Operations
References
IR 2021002
Download: ML21222A118 (18)


Text

SUBJECT:

PALISADES NUCLEAR PLANT - INTEGRATED INSPECTION REPORT 05000255/2021002

Dear Mr. Corbin:

On June 30, 2021, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Palisades Nuclear Plant. On July 20, 2021, the NRC inspectors discussed the results of this inspection with you and other members of your staff. The results of this inspection are documented in the enclosed report.

No findings or violations of more than minor significance were identified during this inspection.

This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely, Billy C. Dickson, Jr., Chief Branch 2 Division of Reactor Projects Docket No. 05000255 License No. DPR-20

Enclosure:

As stated

Inspection Report

Docket Number:

05000255

License Number:

DPR-20

Report Number:

05000255/2021002

Enterprise Identifier:

I-2021-002-0101

Licensee:

Entergy Nuclear Operations, Inc.

Facility:

Palisades Nuclear Plant

Location:

Covert, MI

Inspection Dates:

April 01, 2021 to June 30, 2021

Inspectors:

P. Laflamme, Senior Resident Inspector

V. Myers, Senior Health Physicist

C. St. Peters, Resident Inspector

Approved By:

Billy C. Dickson, Jr., Chief

Branch 2

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Palisades Nuclear Plant, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

No findings or violations of more than minor significance were identified.

Additional Tracking Items

None.

PLANT STATUS

The plant began the inspection period at rated thermal power and remained at or near rated thermal power for the entire inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

Starting on March 20, 2020, in response to the National Emergency declared by the President of the United States on the public health risks of the coronavirus (COVID-19), resident and regional inspectors were directed to begin telework and to remotely access licensee information using available technology. During this time, the resident inspectors performed periodic site visits each week, increasing the amount of time on site as local COVID-19 conditions permitted.

As part of their onsite activities, resident inspectors conducted plant status activities as described in IMC 2515, Appendix D; observed risk significant activities; and completed on site portions of IPs. In addition, resident and regional baseline inspections were evaluated to determine if all or a portion of the objectives and requirements stated in the IP could be performed remotely. If the inspections could be performed remotely, they were conducted per the applicable IP. In some cases, portions of an IP were completed remotely and on site. The inspections documented below met the objectives and requirements for completion of the IP.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

Seasonal Extreme Weather Sample (IP Section 03.01) (1 Sample)

(1) The inspectors evaluated readiness for seasonal extreme weather conditions prior to the onset of extreme heat for the following systems:

Switchyard, 1-2 startup transformer, and service water system on May 19, 2021

External Flooding Sample (IP Section 03.03) (1 Sample)

(1) The inspectors evaluated that flood protection barriers, mitigation plans, procedures, and equipment are consistent with the licensees design requirements and risk analysis assumptions for coping with external flooding on May 28, 2021.

71111.04 - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1)1-2 Startup transformer on April 19, 2021

(2) Right Train low pressure safety injection (SI) on April 16, 2021
(3) P-8C auxiliary feedwater (AFW) pump system on April 26, 2021
(4) Station 1 battery system on June 10, 2021

Complete Walkdown Sample (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated system configurations during a complete walkdown of the Left Train critical service water system on May 5, 2021.

71111.05 - Fire Protection

Fire Area Walkdown and Inspection Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated the implementation of the fire protection program by conducting a walkdown and performing a review to verify program compliance, equipment functionality, material condition, and operational readiness of the following fire areas:

(1) Fire Area 10: east engineered safeguards room, elevation 570' on April 9, 2021
(2) Fire Area 24: AFW pump room elevation, 571' on April 26, 2021
(3) Fire Area 28: west engineered safeguards room, elevation 570' on May 27, 2021
(4) Fire Areas 5 & 7: 1-1 diesel generator and fuel oil day tank rooms, elevation 590' on June 1, 2021

71111.07A - Heat Sink Performance

Annual Review (IP Section 03.01) (1 Sample)

The inspectors evaluated readiness and performance of:

(1) 1-2 emergency diesel generator (EDG) jacket water cooling heat exchanger on June 23, 2021

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)

(1) The inspectors observed and evaluated licensed operator performance in the Control Room during QO-1 SI actuation test (elevated risk evolution), Left Train, on May 26, 2021.

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

(1) The inspectors observed and evaluated PLSEG-LOR-21A-04; Abnormal Operating Procedure (AOP) Scenario on May 11, 2021.

71111.12 - Maintenance Effectiveness

Maintenance Effectiveness (IP Section 03.01) (2 Samples)

The inspectors evaluated the effectiveness of maintenance to ensure the following structures, systems, and components (SSCs) remain capable of performing their intended function:

(1) Radiation monitoring system on April 7, 2021 (2)4160V alternating current (HAC) system on June 8, 2021

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (6 Samples)

The inspectors evaluated the accuracy and completeness of risk assessments for the following planned and emergent work activities to ensure configuration changes and appropriate work controls were addressed:

(1) Yellow risk for planned high pressure SI system maintenance and testing on April 14, 2021
(2) Elevated risk due to letdown system isolation for planned maintenance and testing on April 22, 2021
(3) Elevated risk for planned component cooling water system testing on April 29, 2021
(4) Emergent work activities associated with main feed pump suction pressure oscillations due to CV-0608, T-5 level control valve, increased cycling, on May 6, 2021
(5) Yellow risk for planned AFW system testing coupled with predicted geomagnetic storm disturbance on May 12, 2021
(6) Elevated risk due to controller relay coil failure rendering all four atmospheric steam dump valves inoperable and subsequent repair on June 16, 2021

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 03.01) (6 Samples)

The inspectors evaluated the licensee's justifications and actions associated with the following operability determinations and functionality assessments:

(1)1-1 EDG turbocharger support crack evaluation on April 5, 2021

(2) D channel thermal margin monitor evaluation on April 15, 2021
(3) Direct current (DC) bus 2 ground detection Q-4 fuse circuitry evaluation on April 27, 2021
(4) Chemical and volume control system piping weld indication evaluation on May 11, 2021
(5) AFW P-8B outboard packing evaluation on May 17, 2021
(6) CV-3042 safety injection tank (SIT) T-82A pressure control evaluation on June 8, 2021

71111.19 - Post-Maintenance Testing

Post-Maintenance Test Sample (IP Section 03.01) (7 Samples)

The inspectors evaluated the following post-maintenance test activities to verify system operability and functionality:

(1) CV-2056, volume control tank (VCT) to vacuum degassifier tank (VDT) divert valve maintenance and testing on May 3, 2021
(2) CV-0608 T-5 level control valve and testing on May 11, 2021
(3) EDG 1-2 planned governor replacement and testing on May 19, 2021
(4) AFW P-8B packing replacement and testing on May 24, 2021
(5) MO-3012, low pressure SI to reactor coolant 2A maintenance and testing on May 25, 2021
(6) Steam generator A and B feed regulator bypass valve drain piping repairs and testing on May 28, 2021
(7) Thermal margin monitoring system Channel A repair and testing on June 3, 2021

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance tests:

Surveillance Tests (other) (IP Section 03.01)

(1) RO-128 EDG 1-2 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> run, on April 19-20, 2021 (2)1-1 EDG load reject surveillance test on April 12, 2021
(3) RO-127: AFW system 18-Month test on May 13, 2021
(4) QO-1: SI actuation system test - right train on May 26, 2021

Inservice Testing (IP Section 03.01) (1 Sample)

(1) QO-42: Shutdown cooling valves inservice test on June 15, 2021

FLEX Testing (IP Section 03.02) (1 Sample)

(1) FLEX standby PM: P-1003 Three Year Performance Test on April 14, 2021

71114.06 - Drill Evaluation

Select Emergency Preparedness Drills and/or Training for Observation (IP Section 03.01) (1 Sample)

(1) The inspectors observed an emergency preparedness (EP) drill on June 2,

RADIATION SAFETY

71124.02 - Occupational ALARA Planning and Controls

Radiological Work Planning (IP Section 03.01) (4 Samples)

The inspectors evaluated the licensees radiological work planning for the following work activities.

(1) Primary coolant pump seal replacement under Radiation Work Permit (RWP)2020-0417
(2) Fuel moves under RWP 2020-0430
(3) Reactor vessel reassembly under RWP 2020-0434
(4) Reactor head nozzle inspection and repair under RWP 2020-0450 Verification of Dose Estimates and Exposure Tracking Systems (IP Section 03.02) (4 Samples)

The inspectors evaluated dose estimates and exposure tracking for the following work activities.

(1) Primary coolant pump seal replacement under RWP 2020-0417
(2) Fuel moves under RWP 2020-0430
(3) Reactor vessel reassembly under RWP 2020-0434
(4) Reactor head nozzle inspection and repair under RWP 2020-0450

OTHER ACTIVITIES - BASELINE

===71151 - Performance Indicator Verification The inspectors verified licensee performance indicators submittals listed below:

IE03: Unplanned Power Changes per 7000 Critical Hours Sample (IP Section 02.02)===

(1) Unit 1 (April 1, 2020 - March 31, 2021)

MS05: Safety System Functional Failures (SSFFs) Sample (IP Section 02.04) (1 Sample)

(1) Unit 1 (April 1, 2020 - March 31, 2021)

71152 - Problem Identification and Resolution

Semiannual Trend Review (IP Section 02.02) (1 Sample)

(1) The inspectors reviewed the licensees Corrective Action Program (CAP) for potential adverse trends with a focus on low level human performance issues that might be indicative of a more significant safety issue during the period from January 1, 2021 to June 30, 2021.

Annual Follow-up of Selected Issues (IP Section 02.03) (1 Sample)

The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:

(1) Elevated unidentified primary coolant system (PCS) leakage condition evaluation as documented in CR-PLP-2021-1066 during the week of June 21,

INSPECTION RESULTS

Observation: Semiannual Trend Review 71152 The inspectors review focused on human performance issues and considered the results of daily inspector CAP item screening and licensee trending efforts. The inspectors review nominally considered the 6 months of January 2021 through June 2021, although some examples expanded beyond those dates when warranted by the scope of the trend.

The inspectors reviewed condition reports, trend reports, and human performance evaluations to address performance oversight at the site. During the inspection period, the inspectors noted a few challenges where low-level human performance errors occurred in multiple departments, including Operations, Training, and Maintenance. Examples include electricians losing control of jumpers multiple times, one of which resulted in the site entering an AOP due to an arc flash, unsecured training exams, workers not following procedure adherence while bypassing the reactor protection system during a surveillance test, and two near misses of dropped objects while working at heights. Although the above examples did not challenge safety function or equipment reliability, these issues illustrated a decline in using human performance tools, potentially impacting nuclear safety.

The licensee appropriately entered these issues into the CAP and completed timely evaluations addressing each challenge listed above. Corrective actions included training, site-wide communications reinforcing standards and expectations, and a re-emphasis on the following human performance tools: pre-job briefs; procedure use and adherence; and verification and validation activities. The inspectors determined that the corrective actions taken to date appeared to address the identified gaps effectively and plan to continue to evaluate these actions during routine observations and inspections.

Observation: Primary Coolant System Unidentified Leakage Evaluation 71152 The inspectors reviewed the events, circumstances, and causal evaluation associated with elevated primary coolant system (PCS) unidentified leakage rates that occurred in April of 2021. Their efforts included assessing the licensee's adverse condition monitoring plan, troubleshooting, failure mode analysis, trending, and aggregate review activities.

Additionally, the inspectors reviewed leakage trends, equipment condition assessments for the letdown system, primary coolant pump (PCP) seal leak off system, and control rod drive mechanism (CRDM) leakage collection manifold, along with monthly containment tour results and containment sump level monitoring. The inspectors also interviewed operators, maintenance workers, and engineering personnel to complete their assessment efforts.

In their review, the inspectors noted that most of the elevated unidentified leakage was accounted for by known leakage from the PCP seal leak off system, CRDM leakage collection manifold, and the letdown system to vacuum degassifier tank (VDT) via the VCT divergent valve bypass (3-way flow valve). Since the above sources cannot be quantitatively measured individually on a routine basis, the collective measurements must administratively be quantified as unidentified combined leakage as required by station procedures. As a corrective action, the licensee performed adjustments on the VCT divergent valve and periodically isolated the VDT while conducting daily unidentified leakage surveillance tests to better quantify and trend unidentified leakage rates. Therefore, since the licensee confirmed the sources of elevated leakage in both measure and location and associated corrective actions addressed the condition, the inspectors concluded the licensee actions taken were timely and effective commensurate with safety significance. In addition, the inspectors compared and contrasted their review of a similar leakage evaluation as documented in Palisades Inspection Report (IR) 2020001. In their current review, the inspectors noted that although the sources of leakage were the same, the leakage path, quantity, duration, and initiation of each source discussed above differed for the April 2021 occurrence.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

On July 20, 2021, the inspectors presented the integrated inspection results to Mr. D. Corbin, Vice President, Operations, and other members of the licensee staff.

On April 2, 2021, the inspectors presented the radiation protection inspection results to Mr. D. Corbin, Vice President, Operations, and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Corrective Action

Documents

CR-PLP-2021-

26

V-21H During Restoration and Test Run of Fan in Screen

House Discovered V-21A, Intake Structure Fresh Air Fan,

Had Excessive Noise and Vibration

04/15/2021

Miscellaneous

PLP-RPT-15-

00010

Palisades Nuclear Plant Flooding Hazard Re-Evaluation

Report

Procedures

AOP-38

Acts of Nature

71111.01

Work Orders

2926621-01

Warm Weather Checklist

05/18/2021

CR-PLP-2021-

01074

Penetration FZ-0547 has not been Included in the Procedure

DBD-7.10

04/20/2021

CR-PLP-2021-

01307

Bi-weekly Inspection of ED-02 (Station Battery #2) Under

Work Order 557033-01

05/17/2021

Corrective Action

Documents

CR-PLP-2021-

01575

Bi-weekly Inspection of ED-02 (Station Battery #2) Cell #43

06/15/2021

SOP-12

Feedwater

SOP-15

Service Water System

SOP-3

Engineered Safeguards

108

71111.04

Procedures

SOP-30

Station Power System

CR-PLP-2-21-

01081

EVI-1603 P-41 Battery Bank 2 Voltmeter Displaying Erratic

Readings

04/20/2021

CR-PLP-2021-

01038

South Wall of the 1-1 Diesel Generator Room was Found to

be Starting to Separate from the Barrier

04/16/2021

CR-PLP-2021-

01073

FZ-0547 has Cracking Along the Face of the Seal Where it

Meets the Penetrating Conduits

04/20/2021

CR-PLP-2021-

01342

Received Alarm EK-1148 Fire System Panel C-48, C-47A/B

or C C-49 Off Normal Unexpectedly

05/19/2021

Corrective Action

Documents

CR-PLP-2021-

01357

Door-187, DIG 1-2 K-68 Day Tank Room Entrance

05/20/2021

Corrective Action

Documents

Resulting from

Inspection

CR-PLP-2021-

01457

    • NRC Identified** During Plant Tour, NRC Resident

Identified a Small Amount of Fuel Oil (FO) on the Floor

Underneath MV-DE515, D/G 1-1 FO Day Tank T-25A Drain

06/01/2021

71111.05

Fire Plans

Fire Area 28

West Engineered Safeguards Room, Elevation 570'

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Pre-Fire Plan 10

East Engineered Safeguards Room, Elevation 570'

Pre-Fire Plan 24

Auxiliary Feedwater Pump Room, Elevation 571'

Corrective Action

Documents

CR-PLP-2021-

01330

During the Performance of WO 52878638-01 (Eddy Current

Testing of E-22B (EOG 1-2 Jacket Water Heat Exchanger))

it was Identified that Degradation in the Form of Pitting was

Occurring in E-22B

05/18/2021

Miscellaneous

Sample Heat Exchanger Visual Inspection Datasheet

05/18/2021

CEP-NDE-0902

ASME Section XI VT-2 Examination Record, E-22B, E-13B

05/19/2021

CH 1.11

MIC Control Program Inspection Report

05/17/2021

Procedures

SEP-HX-PLP-001

Supplemental HX Visual Inspection Checklist, EDG Jacket

Water Cooler

05/17/2021

2904475-01

K-6B 1-2 D/G, 24M (1 Cycle) PM

05/18/2021

2904475-02

K-6B; PMT: 24M (1 Cycle) PM of 1-2 D/G (OPS)

05/19/2021

71111.07A

Work Orders

2904475-03

E-22B, 1-2 D/G Jacket Water Cooler, Contingency Task for

Tube Plugging

05/18/2021

71111.11Q

Procedures

PLSEG-LOR-

21A-04

AOP Scenario

System Health Report

04/01/2016-

06/30/2016

System Health Report

10/01/2016-

2/31/2016

Functional Failure

Determination

Form

EX-10; Main Transformer Winding Temperature had Risen

to 81.5 Degrees

10/08/2019

PLP-RPT-12-

00026,

Maintenance Rule Scoping Document; 4160 Volt AC Power

System Health

Report Q2 - 2020

HAC - 4160 Volt AC System

05/10/2021

System Health

Report Q2 -2019

HAC - 4160 Volt AC System

05/10/2021

System Health

Report Q4 - 2019

HAC - 4160 Volt AC System

05/10/2021

71111.12

Miscellaneous

System Health

HAC - 4160 Volt AC System

05/10/2021

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Report Q4 - 2020

CR-PLP-2021-

01104

The Integrated Risk for the Operations PMT on the CV-

2056, Letdown to VCT or VDT, Following the Seat Load

Adjustment, was Inadvertently Made High Risk for the

Radiological Conditions

04/22/2021

CR-PLP-2021-

212

CV-0608, Moisture Separator Drain Tank T-5 Level Control,

Cycling

05/04/2021

CR-PLP-2021-

257

CRDM Cooling Fan Tripped Unexpectedly

05/11/2021

CR-PLP-2021-

260

MCC-10 Trip Troubleshooting Under Work Order 562603-01

05/12/2021

CR-PLP-2021-

265

The Control Room Entered AOP-38, Acts of Nature, Due to

Notification of a Geo Magnetic Storm with a K Index of 7

05/12/2021

CR-PLP-2021-

273

CRD-23 is About 185 Degrees and has Been Stable Since

Restoring the CRDM Cooling Fan

05/13/2021

Corrective Action

Documents

CR-PLP-2021-

282

During the 480 Volt MCC-10 There was a Subsequent Rise

in Pressure Seen in the P-50B Seal Upper and Middle State

Pressures

05/13/2021

Miscellaneous

White Paper

CV-2056, Letdown to Volume Control Tank (VCT) or

Vacuum Degassifier Tank (Diversion Valve) White Paper

04/14/2021

EN-OP-119

Protected Equipment Postings

71111.13

Procedures

SOP-10

Extraction and Heater Drain Systems

0098-0168-01

Cracked EDG Turbocharger Support - Past Operability

Evaluation

Calculations

0098-0169-02

Cracked EDG Turbocharger Support - Past Operability

Evaluation

CR-PLP-2019-

2323

During the Performance of QO-21A Smoke was Noted

Rising from the Inboard Pump Bearing Area

06/10/2019

CR-PLP-2019-

4060

Two Cracks were Found in a Turbocharger Support Weld on

Emergency Diesel Generator 1-1 (K-6A)

10/09/2019

CR-PLP-2021-

00458

During Inspection of K-6A, 1-1 Emergency Diesel Generator,

Identified Cracking on the West Side of the South Vertical

Turbocharger Support

2/18/2021

71111.15

Corrective Action

Documents

CR-PLP-2021-

Q-Level Fuses were Found to be Installed in a Safety

03/30/2021

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

00864

Related Application

CR-PLP-2021-

00999

During Real Time Clock Battery Replacement, Evidence of

Connector Melting was Identified on Plastic Battery

Connector (Molex)

04/13/2021

CR-PLP-2021-

01107

Possible Weld Leakage from Valve Body to Pipe Welded

Connection on CV-2056 (Letdown to CT-54 or DVT T-57

04/22/2021

CR-PLP-2021-

01107

Possible Weld Leakage from Valve Body to Pipe Welded

Connection on CV-2056

04/22/2021

CR-PLP-2021-

01114

Indications Were Found on the Discharge to the VCT Weld

for CV-2056

04/23/2021

CR-PLP-2021-

264

Steam Driven Auxiliary Feed Pump Outboard Pump Bearing

Seal Leakage was Observed at 48 DPM

05/12/2021

CR-PLP-2021-

272

Repack of P-8B (Steam Driven Auxiliary Feed Pump) per

Work Order 562621-01

05/13/2021

CR-PLP-2021-

274

During QO-21B Performed Under WO 52961213 a Speed

Adjustment was Required per Step 5.9.2

05/13/2021

CR-PLP-2021-

01340

During the First Post-Maintenance Test Start of K-6B, the

Fuel Oil Secondary Filter Diff Pressure Rose from 6 PSID

(EOG was Unloaded) to 13 PSID

05/19/2021

CR-PLP-2021-

01341

K-6B Fuel Oil Differential Pressure Indicator, was Out of

Spec High

05/19/2021

CR-PLP-2021-

01504

CV-3042 (Safety Injection Tank T-82A Pressure Control)

Showing Dual Indication

06/07/2021

CR-PLP-2021-

01537

VT-2 Inspection of Test RT-71 M

06/10/2021

CR-PLP-2021-

01538

VT-2 Inspection Portion of RT-71 M

06/20/2021

CR-PLP-2021-

01543

Right Train SIRWT Outlet Flange

06/10/2021

CR-PLP-2021-

01576

T-58 SIRW Tank Roof Walk Down with the NRC

06/15/2021

M-201, Sheet 1

Piping and Instrument Diagram, Primary Coolant System

Drawings

M-202, Sheet 1A

Piping and Instrument Diagram, Chemical and Volume

Control System

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Engineering

Evaluations

11-PAL-0051

Evaluation/Screening of Boric Acid Leakage, T-58, Safety

Injection Refueling Water Tank

Design Basis

Document 2.01

Low Pressure Safety Injection

Design Basis

Document 2.02

High Pressure Safety Injection

Miscellaneous

Design Basis

Document 2.05

Reactor Protective System Safety Injection Signal

Anticipated Transient Without Scram

EN-MA-125

Troubleshooting Control of Maintenance Activities

04/22/2021

Procedures

EPS-E-9

Use of Portable DC Ground Fault Detection System

00526705-02

P-8B: Restore/PMT After Outboard Packing Maintenance

11/13/2019

Work Orders

00559905-01

DC Bus #2 Ground Volt Indicator Repair

04/14/2021

CR-PLP-2021-

01108

Adjusted the Spring to Increase Seat Load by the Plug While

the Valve is in the "Extended" Position

04/22/2021

CR-PLP-2021-

267

During RO-97, Auxiliary Feedwater System Automatic

Initiation Test Procedure, Operations Could Not Perform

Step 5.6.12

05/12/2021

CR-PLP-2021-

271

Repack on P-8B, Steam Driven Auxiliary Feedwater Pump,

Under WO 00562621-01

05/12/2021

CR-PLP-2021-

01348

Field Voltage was Identified Out of Normal Range at 139

Volts for both the 1 Hour and 2 Hour Data Points

05/20/2021

Corrective Action

Documents

CR-PLP-2021-

01369

Received Alarm EK-0603D Nuclear-OT Power Deviation / T-

Inlet Off-Normal / Calculator Trouble Channel A

Unexpectedly

05/24/2021

EC-89735

"Line Kill" Leak Repair for MV-BW826, Steam Generator (E-

50B) Feed Regulator Bypass Valve (CV-0734) Outlet Drain

EC-89736

"Line Kill" Leak Repair for MV-FW827, Steam Generator (E-

50A) Feed Regulator Bypass Valve (DV-0735) Inlet Drain

Engineering

Changes

EC-89911

Temporary Leak Repair of Leaking Pipe-to-Tube Adapter

Joint Downstream of MV-CD623, P-1A Suction Flow Xmtr

FT-0711 Hi Side Root

Procedures

QO-21

Inservice Test Procedure Auxiliary Feedwater Pumps

05/13/2021

553840-01

LC-0608 Not Controlling Within Proper Band

05/11/2021

71111.19

Work Orders

553840-02

LC-0608 Not Controlling Within Proper Band (Prep Work)

2/21/2020

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Corrective Action

Documents

CR-PLP-2021-

267

Operations Could Not Perform Step 5.6.12 to Restore HS-

22B to Auto

05/12/2021

Miscellaneous

4Q2019 NRC Performance Indicators Unplanned Power

Changes per 7000 Critical Hours (IE03)

10/01/2019 -

2/31/2019

QO-1

Safety Injection System

QO-42

Inservice Testing of Shutdown Cooling Control Valves

RE-131

Diesel Generator 1-1 Load Reject

04/05/2021

Procedures

RO-128-2

Diesel Generator 1-2 24-Hour Load Run

2904702-01

FLEX Standby PM: K-1 Flex Three Year Load Test

04/06/2021

2904703-01

FLEX Standby PM: K-2 Flex Three Year Load Test

04/16/2021

2904787-01

Standby PM: P-990 Three Yr Performance Test (FSB B)

04/06/2021

71111.22

Work Orders

2904788-01

FLEX Standby PM: P-1003 Three Yr Performance Test

(FSB A)

04/06/2021

20-0417

RWP Review Package for Primary Coolant Pump

Replacement

03/02/2021

20-0430

RWP Review Package for Fuel Moves

10/01/2020

20-0434

RWP Review Package for reactor reassembly

2/05/2021

71124.02

Radiation Work

Permits (RWPs)

20-0450

RWP Review Package for Reactor Head Nozzle Inspection

and Repair

10/13/2020

4Q2019 NRC Performance Indicators Safety System

Functional Failures (MS05)

10/01/2019 -

2/31/2019

1Q2020 NRC Performance Indicators Safety System

Functional Failures (MS05)

01/01/2020 -

03/31/2020

2Q2020 NRC Performance Indicators Safety System

Functional Failures (MS05)

04/01/2020 -

06/31/2020

3Q2020 NRC Performance Indicators Safety System

Functional Failures (MS05)

07/01/2020 -

09/30/2020

4Q2020 NRC Performance Indicators Safety System

Functional Failures (MS05)

10/01/2020 -

2/31/2020

1Q2020 NRC Performance indicators Unplanned Power

Changes per 7000 Critical Hours (IE03)

01/01/2020 -

03/31/2020

2Q2020 NRC Performance Indicators Unplanned Power

Changes per 7000 Critical Hours (IE03)

04/01/2020 -

06/30/2020

71151

Miscellaneous

3Q2020 NRC Performance Indicators Unplanned Power

07/01/2020 -

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Changes per 7000 Critical Hours (IE03)

09/30/2020

4Q2020 NRC Performance Indicators Unplanned Power

Changes per 7000 Critical Hours (IE03)

10/01/2020 -

2/31/2020

CR-PLP-2021-

273

CRDM Cooling Fan was Lost

05/13/2021

CR-PLP-2021-

287

On May 14, 2021, the PCS Unidentified Leak Rate was

Measured to be 0.091 GPM

05/14/2021

CR-PLP-2021-

01308

The PCS Unidentified Leak Rate was Measured at 0.082

GPM

05/17/2021

CR-PLP-2021-

01322

CRDM Seal Leakage was Measured at 110m/min

05/17/2021

Corrective Action

Documents

CR-PLP-2021-

01460

During QI-9, Reactor Protective Trip Units, Additional Action

Taken During a Procedure Step

06/02/2021

February 2021 DPRM/APRM Report

2/2021

Miscellaneous

Adverse

Condition

Monitoring Plan

CRD-23, Control Rod Drive Mechanism, Elevated Leakoff

Temperature

05/17/2021

71152

Procedures

Procedure No.

4.19, Attachment

PCS Leakage Decision Flowchart

6