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LICENSEE EVENT RF. PORT | |||
-y .'.7cL aLOcx. I 1 | |||
I I I I 1 6 | |||
l@ nLEAss PauNT OR TYPE ALL I!ECUIRED INFOi!MATloN) l o I - l l " I r I T' l c ! s l I l@l o I o 10 l o I o I o I o l 0 l o l o i o l@l k 1111l111]@l l lg 7 s 9 uCEssEE = =E ia :S uCENsENuueEs :3 . act:,3E v , 3a 37 Ca; 3, CON'T lclii | |||
"'.',"y | |||
; l L @l O f S l 01010121815 l@lllll2lhl?18l@l112lolel~I: l@ | |||
3 60 61 DCOKET NLMBER 68 69 EV ENT O ATE 74 75 AE809T OATE dJ EVENr DESCRIPTION AND PRC8 ABLE CONSECUENCES h l o' 6 2 l lDuring the parfor w ce of shutdown cooling interlock test (ST-SDC-1) it was discoveredt i o e a i I that PC-1053 was not operating. Further investigation showed relay 9h-3h7/3h8 (the l I o i A I l valve closing relay) was not vired to PC-1053 and was inoperable since the 1977 l lo46; } Refueling Outage. The redundant shutdown cooling interloch PC-105 was operable duringl l0t6l l this period. l l 017 l l l t o ia l ! - I | |||
; es 3 SYSTEM CAUSE CAUSE COMP. vatyE CODE COCE SUSCOCE COMPCNENT CODE SueCODE SUBCOCE | |||
:7 i:19l 8 9 l El El@ 10 11 | |||
@ 1; | |||
@ lR lE ll IA lY IX l@ @@ W @ | |||
13 18 13 20 | |||
,,,, SEcufNTIAL cCOUR RENCE REPCRT REV'SICN gg e EVENT YE AR mE*CRT NC. COCE vpE NC. | |||
@, age,go g IT 18 I l--J l o l h 12 I lA I ol ?l ILI l' I Of | |||
_i 22 :2 24 a :: := a ao si :2 ACTtON . FUTURE EpsECT SMUT 0cWN ATTACMMENT N*m O 4 PatME COMP. COM*CNEN* | |||
TAKEN ACTICN ON PLANT METHCO hours -- SUSMITTED FORM aus. SUP*LIEm MANUS AC 1,;RER IFl@izl@ Izl@ 12 l@ I o 10 l o l o l I44 Yl@ Ll1@ l43Al@ l ci of 81 (47 3-33 34 25 . 36 de_ 40 42 ais CAUSE CESORIPTION AND CORRECTIVE AC*lCNS h ji i o , l During installation of Pcver Operated Felief Valve Modification du-ine the icT" ! | |||
;i,., Irefueling cutare, relay 9h-3h7/?h6 was inadve- entiv disee ne ai f-rn 00-102 . *4e 1 l | |||
t., il error vas not .Stected prier te subsecuent unit operatien since it was no- kncv- a- I | |||
[- j jthe '' a -kat the shutdevn cocline pressu~e interlock sve-a- kd keen effected. U:c- f i .! Idiscovery redundant interlock vas provided and both inter 10cks tested satisfactorilv. I 7 3 3 40 pactLITV a ME* WOO C8 STATUS %PCWER QTHER STATUS - CISCOV ERY OISCOVERY OES0miPTICN 4-i li i t al 5W@ l 01010 7 to l@l HA 12 is 44 l3l@l as as Surveillance '"est so l | |||
ACTIVITY CONTENT | |||
=ELEASEs CraELEASE Av0uNTCs Ac tvi Y -- | |||
LO:ATION Os aE .EASE --8 iiisiIZlhl2!@l d 3 10 | |||
'EASCNNEL EXPOSupfS 11 HA 44 l ! | |||
45 UA 3c I | |||
w M.E. -, :ES:=i- ,eN m is: | |||
7 t101O!o!@lcl@l 6 i tt 1 13 na gg i | |||
8EaSONNE. .mbniES w veer ::.uminmeN -- 1 i ,,i 5!0106o!@l 7 i t1 t: | |||
na i | |||
^ | |||
t , n i. li s. | |||
'JP. ' "iSs'#0T'"" @ | |||
A 7812296Fa4 ; | |||
a i *; ,; | |||
SL E L:Ot *v g ,.- .---c .~. . , | |||
R,,,N e . | |||
I: ;i l.S$ ah | |||
'T i-v l:ES: ' | |||
I!s .If i ' l t ' I f 1 - | |||
4 9 j . ,e 3 -i fi | |||
; ., O.*n-g-- ., .- +-. | |||
-'' #* ,,n ./a~~~~~~'#* | |||
' ~~~'' ~~ '''~~'Y~~'-- | |||
NAME ** *ac8 A AEm 8-CN E- | |||
~ _. .__ .. | |||
1 lIR 78-Oh2 0-^a Public Power District Fort Calhoun Station Unit ilo. 1-Docket No. 05000285 | |||
: i. Attachment No. 1 Safet1 Analysis The Fort Calhoun Station Unit No.1 safety syste= is so designed that no l | |||
single inoperable channel can prevent the perfomance of a safety function if j required. During the ti=e in which PC-105B was inoperable, Plos, the redund-ant channel was operable. | |||
I The function of the shutdown cooling interlock is to provide automatic isolation of the shutdevn cooling isolation valves HCV-3kT and ECV-3h8 to protect the safety injection piping in the event the reactor coolant loop | |||
( pressure' exceeds 250 psia while on the shutdown ecoling decay heat renoval syste=. Operator action and the auto =atic operation of P105 intericek pro-vided adequate protection'of the piping during the ti=e PC-1053 was inoperable. | |||
It should be noted that .HCV-3kT'and ECV-3h8 are locked closed during power operation. Opening these valves when reactor coolant system pressure is greater than 250 psia is prevented bf: | |||
: 1. Ad=inistrative control of key operated control switch, | |||
: 2. P-105 pressure interlock, and , | |||
3 PC-1053 pressure switch interlock. | |||
PC-1053 was incapable cf perfor-4ng its interlock function as a result of this incident. Pressure channel 113/115 nov perfor=s this interlock function 4 | |||
in conforance with the design package. | |||
s | |||
". // / r l bl i | |||
I | |||
.-,nn, +-, . , - - - , - . ~ . - - ~ = - - , ,, - | |||
.,.v,,, - - - , - , - . . , .-, , , , , , | |||
~IF. 78-Ch2 C=aha Public Pcver District Fort Calhoun Station Uni,:Ic. 1 tocket UO. 050002B5 | |||
. Attach =ent No. 2 Corrective Action to P-event Rececu-rence Adherence to the recently revised Station Modi'.ication Control Procedure should prevent reoccurrence of this type incident. | |||
,,e' W | |||
( | |||
d I | |||
i | |||
7.2?. 7S-ch2 C=aha Public Power Distric: | |||
Fort Calhoun Station Unit No. 1 Docket No. 03000233 | |||
* Attachnent No. 3 Failure Dsts This is the first installation e - -epor.able at the Fort Calhoun Statics Unit no. 1. | |||
i h0 k | |||
1}} |
Revision as of 17:40, 25 July 2020
ML20071G327 | |
Person / Time | |
---|---|
Site: | Fort Calhoun |
Issue date: | 12/22/1978 |
From: | Mehaffey R, Gordon Peterson OMAHA PUBLIC POWER DISTRICT |
To: | |
Shared Package | |
ML20071G324 | List: |
References | |
LER-78-042-03L, LER-78-42-3L, NUDOCS 7812290228 | |
Download: ML20071G327 (4) | |
Text
- _ _ .
LICENSEE EVENT RF. PORT
-y .'.7cL aLOcx. I 1
I I I I 1 6
l@ nLEAss PauNT OR TYPE ALL I!ECUIRED INFOi!MATloN) l o I - l l " I r I T' l c ! s l I l@l o I o 10 l o I o I o I o l 0 l o l o i o l@l k 1111l111]@l l lg 7 s 9 uCEssEE = =E ia :S uCENsENuueEs :3 . act:,3E v , 3a 37 Ca; 3, CON'T lclii
"'.',"y
- l L @l O f S l 01010121815 l@lllll2lhl?18l@l112lolel~I
- l@
3 60 61 DCOKET NLMBER 68 69 EV ENT O ATE 74 75 AE809T OATE dJ EVENr DESCRIPTION AND PRC8 ABLE CONSECUENCES h l o' 6 2 l lDuring the parfor w ce of shutdown cooling interlock test (ST-SDC-1) it was discoveredt i o e a i I that PC-1053 was not operating. Further investigation showed relay 9h-3h7/3h8 (the l I o i A I l valve closing relay) was not vired to PC-1053 and was inoperable since the 1977 l lo46; } Refueling Outage. The redundant shutdown cooling interloch PC-105 was operable duringl l0t6l l this period. l l 017 l l l t o ia l ! - I
- es 3 SYSTEM CAUSE CAUSE COMP. vatyE CODE COCE SUSCOCE COMPCNENT CODE SueCODE SUBCOCE
- 7 i:19l 8 9 l El El@ 10 11
@ 1;
@ lR lE ll IA lY IX l@ @@ W @
13 18 13 20
,,,, SEcufNTIAL cCOUR RENCE REPCRT REV'SICN gg e EVENT YE AR mE*CRT NC. COCE vpE NC.
@, age,go g IT 18 I l--J l o l h 12 I lA I ol ?l ILI l' I Of
_i 22 :2 24 a :: := a ao si :2 ACTtON . FUTURE EpsECT SMUT 0cWN ATTACMMENT N*m O 4 PatME COMP. COM*CNEN*
TAKEN ACTICN ON PLANT METHCO hours -- SUSMITTED FORM aus. SUP*LIEm MANUS AC 1,;RER IFl@izl@ Izl@ 12 l@ I o 10 l o l o l I44 Yl@ Ll1@ l43Al@ l ci of 81 (47 3-33 34 25 . 36 de_ 40 42 ais CAUSE CESORIPTION AND CORRECTIVE AC*lCNS h ji i o , l During installation of Pcver Operated Felief Valve Modification du-ine the icT" !
- i,., Irefueling cutare, relay 9h-3h7/?h6 was inadve- entiv disee ne ai f-rn 00-102 . *4e 1 l
t., il error vas not .Stected prier te subsecuent unit operatien since it was no- kncv- a- I
[- j jthe a -kat the shutdevn cocline pressu~e interlock sve-a- kd keen effected. U:c- f i .! Idiscovery redundant interlock vas provided and both inter 10cks tested satisfactorilv. I 7 3 3 40 pactLITV a ME* WOO C8 STATUS %PCWER QTHER STATUS - CISCOV ERY OISCOVERY OES0miPTICN 4-i li i t al 5W@ l 01010 7 to l@l HA 12 is 44 l3l@l as as Surveillance '"est so l
ACTIVITY CONTENT
=ELEASEs CraELEASE Av0uNTCs Ac tvi Y --
LO:ATION Os aE .EASE --8 iiisiIZlhl2!@l d 3 10
'EASCNNEL EXPOSupfS 11 HA 44 l !
45 UA 3c I
w M.E. -, :ES:=i- ,eN m is:
7 t101O!o!@lcl@l 6 i tt 1 13 na gg i
8EaSONNE. .mbniES w veer ::.uminmeN -- 1 i ,,i 5!0106o!@l 7 i t1 t:
na i
^
t , n i. li s.
'JP. ' "iSs'#0T'"" @
A 7812296Fa4 ;
a i *; ,;
SL E L:Ot *v g ,.- .---c .~. . ,
R,,,N e .
I: ;i l.S$ ah
'T i-v l:ES: '
I!s .If i ' l t ' I f 1 -
4 9 j . ,e 3 -i fi
- ., O.*n-g-- ., .- +-.
- #* ,,n ./a~~~~~~'#*
' ~~~ ~~ '~~'Y~~'--
NAME ** *ac8 A AEm 8-CN E-
~ _. .__ ..
1 lIR 78-Oh2 0-^a Public Power District Fort Calhoun Station Unit ilo. 1-Docket No. 05000285
- i. Attachment No. 1 Safet1 Analysis The Fort Calhoun Station Unit No.1 safety syste= is so designed that no l
single inoperable channel can prevent the perfomance of a safety function if j required. During the ti=e in which PC-105B was inoperable, Plos, the redund-ant channel was operable.
I The function of the shutdown cooling interlock is to provide automatic isolation of the shutdevn cooling isolation valves HCV-3kT and ECV-3h8 to protect the safety injection piping in the event the reactor coolant loop
( pressure' exceeds 250 psia while on the shutdown ecoling decay heat renoval syste=. Operator action and the auto =atic operation of P105 intericek pro-vided adequate protection'of the piping during the ti=e PC-1053 was inoperable.
It should be noted that .HCV-3kT'and ECV-3h8 are locked closed during power operation. Opening these valves when reactor coolant system pressure is greater than 250 psia is prevented bf:
- 1. Ad=inistrative control of key operated control switch,
- 2. P-105 pressure interlock, and ,
3 PC-1053 pressure switch interlock.
PC-1053 was incapable cf perfor-4ng its interlock function as a result of this incident. Pressure channel 113/115 nov perfor=s this interlock function 4
in conforance with the design package.
s
". // / r l bl i
I
.-,nn, +-, . , - - - , - . ~ . - - ~ = - - , ,, -
.,.v,,, - - - , - , - . . , .-, , , , , ,
~IF. 78-Ch2 C=aha Public Pcver District Fort Calhoun Station Uni,:Ic. 1 tocket UO. 050002B5
. Attach =ent No. 2 Corrective Action to P-event Rececu-rence Adherence to the recently revised Station Modi'.ication Control Procedure should prevent reoccurrence of this type incident.
,,e' W
(
d I
i
7.2?. 7S-ch2 C=aha Public Power Distric:
Fort Calhoun Station Unit No. 1 Docket No. 03000233
- Attachnent No. 3 Failure Dsts This is the first installation e - -epor.able at the Fort Calhoun Statics Unit no. 1.
i h0 k
1