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| number = ML11138A321
| number = ML11138A321
| issue date = 06/08/2011
| issue date = 06/08/2011
| title = May 9, 2011, Summary of Telephone Conference Call Held Between NRC and Pseg Nuclear, LLC, Concerning Status of Hope Creek Drywell Air Gap Drains
| title = May 9, 2011, Summary of Telephone Conference Call Held Between NRC and PSEG Nuclear, LLC, Concerning Status of Hope Creek Drywell Air Gap Drains
| author name = Cunanan A D
| author name = Cunanan A
| author affiliation = NRC/NRR/DLR/RPB1
| author affiliation = NRC/NRR/DLR/RPB1
| addressee name =  
| addressee name =  
Line 15: Line 15:


=Text=
=Text=
{{#Wiki_filter:UNITED NUCLEAR REGULATORY WASHINGTON, D.C. 20555*0001 June 8,2011 LICENSEE:
{{#Wiki_filter:UNITED STATES NUCLEAR REGULATORY COMMISSION WASHINGTON, D.C. 20555*0001 June 8,2011 LICENSEE:       PSEG Nuclear, LLC FACILITY:       Hope Creek Generating Station
PSEG Nuclear, LLC FACILITY:
Hope Creek Generating Station  


==SUBJECT:==
==SUBJECT:==


==SUMMARY==
==SUMMARY==
OF TELEPHONE CONFERENCE CALL HELD ON MAY 9, 2011, BETWEEN THE U.S. NUCLEAR REGULATORY COMMISSION AND PSEG NUCLEAR, LLC, CONCERNING THE STATUS OF THE HOPE CREEK DRYWELL AIR GAP DRAINS The U.S. Nuclear Regulatory Commission (NRC or the staff) and representatives of PSEG Nuclear, LLC, and Exelon held a telephone conference call on May 9, 2011, on the status of the Hope Creek Generating Station drywell air gap drains. Enclosure 1 provides a listing of the participants and Enclosure 2 contains a brief summary of the discussion and status of the item. The applicant had an opportunity to comment on this summary. Arthur Cunanan, Project Manager Projects Branch '( Division of License Renewal Office of Nuclear Reactor Regulation Docket No. 50-354  
OF TELEPHONE CONFERENCE CALL HELD ON MAY 9, 2011, BETWEEN THE U.S. NUCLEAR REGULATORY COMMISSION AND PSEG NUCLEAR, LLC, CONCERNING THE STATUS OF THE HOPE CREEK DRYWELL AIR GAP DRAINS The U.S. Nuclear Regulatory Commission (NRC or the staff) and representatives of PSEG Nuclear, LLC, and Exelon held a telephone conference call on May 9, 2011, on the status of the Hope Creek Generating Station drywell air gap drains. provides a listing of the participants and Enclosure 2 contains a brief summary of the discussion and status of the item.
The applicant had an opportunity to comment on this summary.
Arthur Cunanan, Project Manager Projects Branch '(
Division of License Renewal Office of Nuclear Reactor Regulation Docket No. 50-354


==Enclosures:==
==Enclosures:==
: 1. List of Participants  
: 1. List of Participants
: 2. Summary of meeting discussion cc w/encls: Distribution via Listserv PARTICIPANTS Arthur Cunanan Bennett Brady Rajender Auluck Abdul Sheikh Brian Harris Bo Ph am Harold Gray John Hufnagel Josh Moss George Seibold Don Warfle Ali Fakhar Jim Stavely TELEPHONE CONFERENCE HOPE CREEK GENERATING LICENSE RENEWAL LIST OF MAY AFFILIATIONS U.S. Nuclear Regulatory Commission (NRC) NRC NRC NRC NRC NRC NRC Exelon Exelon Exelon Exelon PSEG Nuclear (PSEG) PSEG ENCLOSURE
: 2. Summary of meeting discussion cc w/encls: Distribution via Listserv
 
TELEPHONE CONFERENCE CALL HOPE CREEK GENERATING STATION LICENSE RENEWAL APPLICATION LIST OF PARTICIPANTS MAY 9,2011 PARTICIPANTS                    AFFILIATIONS Arthur Cunanan                  U.S. Nuclear Regulatory Commission (NRC)
Bennett Brady                  NRC Rajender Auluck                NRC Abdul Sheikh                    NRC Brian Harris                    NRC Bo Pham                        NRC Harold Gray                    NRC John Hufnagel                  Exelon Josh Moss                      Exelon George Seibold                  Exelon Don Warfle                      Exelon Ali Fakhar                      PSEG Nuclear (PSEG)
Jim Stavely                    PSEG ENCLOSURE 1


==SUMMARY==
==SUMMARY==
OF MEETING DISCUSSION ON WHETHER THE GAS TURBINE HOPE CREEK GENERATING STATION IS IN THE SCOPE OF LICENSE MAY The U.S. Nuclear Regulatory Commission (NRC or the staff) and representatives of PSEG Nuclear, LLC (PSEG or the applicant) held a telephone conference call on May 9, 2011, on the status of the Hope Creek Generating Station drywell air gap drains. The applicant provided an update of the drywell air gap drains. In preparation to clearing the air gap drains, the applicant examined one of the air gap drains and found the drain was blocked six (6) feet prior to reaching the drywell shell. The applicant was not able to detect an exit port to the air gap drains when it sent a boroscope through the instrument lines. The other three air gap drains were not inspected.
OF MEETING DISCUSSION ON WHETHER THE GAS TURBINE AT HOPE CREEK GENERATING STATION IS IN THE SCOPE OF LICENSE RENEWAL MAY 9,2011 The U.S. Nuclear Regulatory Commission (NRC or the staff) and representatives of PSEG Nuclear, LLC (PSEG or the applicant) held a telephone conference call on May 9, 2011, on the status of the Hope Creek Generating Station drywell air gap drains.
The current configuration of the air gap drains are unknown. The staff stated that the applicant's statement, during the conference call, needs to be submitted on the docket. The staff also stated some of the existing enhancement of the ASME Section XI, subsection IWE, are not applicable, since the configuration of the air gap drains are unknown. The SER section needs updating to include amendments or modifications to the programs existing enhancements in order for the staff to conclude an acceptance of the program. The staff will also establish a license condition for the applicant to: Perform boroscope and ultrasonic thickness (UT) measurements every outage until drainage is established Submit a report to the staff summarizing the results from the boroscope examinations and the UT measurements Perform UT measurements of the drywell shell, after the drainage is established from all four quadrants, during the next three refueling outages to establish a corrosion rate to demonstrate that the drywell structural integrity will be maintained through the period of extended operation The applicant understands that they will be submitting a statement on the docket and the staff will be establishing a license condition.
The applicant provided an update of the drywell air gap drains. In preparation to clearing the air gap drains, the applicant examined one of the air gap drains and found the drain was blocked six (6) feet prior to reaching the drywell shell.
No RAls will be issued based on this conference call. ENCLO'SURE June 8,2011 LICENSEE:
The applicant was not able to detect an exit port to the air gap drains when it sent a boroscope through the instrument lines. The other three air gap drains were not inspected. The current configuration of the air gap drains are unknown.
PSEG Nuclear, LLC FACILITY:
The staff stated that the applicant's statement, during the conference call, needs to be submitted on the docket. The staff also stated some of the existing enhancement of the ASME Section XI, subsection IWE, are not applicable, since the configuration of the air gap drains are unknown. The SER section needs updating to include amendments or modifications to the programs existing enhancements in order for the staff to conclude an acceptance of the program.
Hope Creek Generating Station
The staff will also establish a license condition for the applicant to:
* Perform boroscope and ultrasonic thickness (UT) measurements every outage until drainage is established
* Submit a report to the staff summarizing the results from the boroscope examinations and the UT measurements
* Perform UT measurements of the drywell shell, after the drainage is established from all four quadrants, during the next three refueling outages to establish a corrosion rate to demonstrate that the drywell structural integrity will be maintained through the period of extended operation The applicant understands that they will be submitting a statement on the docket and the staff will be establishing a license condition.
No RAls will be issued based on this conference call.
ENCLO'SURE 2
 
ML11138A321 OFFICE      LADLR                PM:RPB1:DLR            BC:RPB1 :DLR      PM:RPB1:DLR
~ME          YEdmonds              ACunanan                BPham              ACunanan 06/7/11              06/7/11                06/8/11            06/8/11
~ATE Memorandum to PSEG Nuclear. LLC from A. Cunanan. dated June 8. 2011


==SUBJECT:==
==SUBJECT:==
==SUMMARY==
OF TELEPHONE CONFERENCE CALL HELD ON MAY 9,2011, BETWEEN THE U.S. NUCLEAR REGULATORY COMMISSION AND PSEG NUCLEAR, LLC, CONCERNING THE STATUS OF THE HOPE CREEK DRYWELL AIR GAP DRAINS The U.S. Nuclear Regulatory Commission (NRC or the staff) and representatives of PSEG Nuclear, LLC, and Exelon held a telephone conference call on May 9, 2011, on the status of the Hope Creek Generating Station drywell air gap drains. Enclosure 1 provides a listing of the participants and Enclosure 2 contains a brief summary of the discussion and status of the item. The applicant had an opportunity to comment on this summary. IRA! Arthur Cunanan, Project Manager Projects Branch 1 Division of License Renewal Office of Nuclear Reactor Regulation Docket No. 50-354
==Enclosures:==
: 1. List of participants
: 2. Summary of meeting discussion cc w/encls: Distribution via Listserv DISTRIBUTION:
See next page ADAMS Accession No ML 11138A321 OFFICE LADLR PM:RPB1:DLR BC:RPB1 :DLR PM:RPB1:DLR YEdmonds ACunanan BPham ACunanan 06/7/11 06/7/11 ! 06/8/11 06/8/11 OFFICIAL RECORD Memorandum to PSEG Nuclear. LLC from A. Cunanan. dated June 8. 2011


==SUMMARY==
==SUMMARY==
OF TELEPHONE CONFERENCE CALL HELD ON MAY 9, 2011, BETWEEN THE U.S. NUCLEAR REGULATORY COMMISSION AND PSEG NUCLEAR, LLC, CONCERNING STATUS OF HOPE CREEK DRYWELL AIR GAP DRAINS DISTRIBUTION:
OF TELEPHONE CONFERENCE CALL HELD ON MAY 9, 2011, BETWEEN THE U.S. NUCLEAR REGULATORY COMMISSION AND PSEG NUCLEAR, LLC, CONCERNING STATUS OF HOPE CREEK DRYWELL AIR GAP DRAINS DISTRIBUTION:
HARDCOPY:
HARDCOPY:
DLRRF E-MAIL: PUBLIC RidsNrrDlr Resource RidsNrrDlrRpb1 Resource RidsNrrDlrRpb2 Resource RdsNrrDlrRarb Resource RidsNrrDlrRasb Resource RidsNrrDlrRapb Resource RidsOgcMailCenter Resource BPham ACunanan BBrady LPerkins REnnis CSanders BHarris,OGC ABurritt, RI RConte. RI MModes, RI DTifft, RI NMcNamara, RI}}
DLRRF E-MAIL:
PUBLIC RidsNrrDlr Resource RidsNrrDlrRpb1 Resource RidsNrrDlrRpb2 Resource RdsNrrDlrRarb Resource RidsNrrDlrRasb Resource RidsNrrDlrRapb Resource RidsOgcMailCenter Resource BPham ACunanan BBrady LPerkins REnnis CSanders BHarris,OGC ABurritt, RI RConte. RI MModes, RI DTifft, RI NMcNamara, RI}}

Latest revision as of 22:43, 10 March 2020

May 9, 2011, Summary of Telephone Conference Call Held Between NRC and PSEG Nuclear, LLC, Concerning Status of Hope Creek Drywell Air Gap Drains
ML11138A321
Person / Time
Site: Hope Creek PSEG icon.png
Issue date: 06/08/2011
From: Cunanan A
License Renewal Projects Branch 1
To:
Cunanan, A. 415-3897
References
Download: ML11138A321 (5)


Text

UNITED STATES NUCLEAR REGULATORY COMMISSION WASHINGTON, D.C. 20555*0001 June 8,2011 LICENSEE: PSEG Nuclear, LLC FACILITY: Hope Creek Generating Station

SUBJECT:

SUMMARY

OF TELEPHONE CONFERENCE CALL HELD ON MAY 9, 2011, BETWEEN THE U.S. NUCLEAR REGULATORY COMMISSION AND PSEG NUCLEAR, LLC, CONCERNING THE STATUS OF THE HOPE CREEK DRYWELL AIR GAP DRAINS The U.S. Nuclear Regulatory Commission (NRC or the staff) and representatives of PSEG Nuclear, LLC, and Exelon held a telephone conference call on May 9, 2011, on the status of the Hope Creek Generating Station drywell air gap drains. provides a listing of the participants and Enclosure 2 contains a brief summary of the discussion and status of the item.

The applicant had an opportunity to comment on this summary.

Arthur Cunanan, Project Manager Projects Branch '(

Division of License Renewal Office of Nuclear Reactor Regulation Docket No. 50-354

Enclosures:

1. List of Participants
2. Summary of meeting discussion cc w/encls: Distribution via Listserv

TELEPHONE CONFERENCE CALL HOPE CREEK GENERATING STATION LICENSE RENEWAL APPLICATION LIST OF PARTICIPANTS MAY 9,2011 PARTICIPANTS AFFILIATIONS Arthur Cunanan U.S. Nuclear Regulatory Commission (NRC)

Bennett Brady NRC Rajender Auluck NRC Abdul Sheikh NRC Brian Harris NRC Bo Pham NRC Harold Gray NRC John Hufnagel Exelon Josh Moss Exelon George Seibold Exelon Don Warfle Exelon Ali Fakhar PSEG Nuclear (PSEG)

Jim Stavely PSEG ENCLOSURE 1

SUMMARY

OF MEETING DISCUSSION ON WHETHER THE GAS TURBINE AT HOPE CREEK GENERATING STATION IS IN THE SCOPE OF LICENSE RENEWAL MAY 9,2011 The U.S. Nuclear Regulatory Commission (NRC or the staff) and representatives of PSEG Nuclear, LLC (PSEG or the applicant) held a telephone conference call on May 9, 2011, on the status of the Hope Creek Generating Station drywell air gap drains.

The applicant provided an update of the drywell air gap drains. In preparation to clearing the air gap drains, the applicant examined one of the air gap drains and found the drain was blocked six (6) feet prior to reaching the drywell shell.

The applicant was not able to detect an exit port to the air gap drains when it sent a boroscope through the instrument lines. The other three air gap drains were not inspected. The current configuration of the air gap drains are unknown.

The staff stated that the applicant's statement, during the conference call, needs to be submitted on the docket. The staff also stated some of the existing enhancement of the ASME Section XI, subsection IWE, are not applicable, since the configuration of the air gap drains are unknown. The SER section needs updating to include amendments or modifications to the programs existing enhancements in order for the staff to conclude an acceptance of the program.

The staff will also establish a license condition for the applicant to:

  • Perform boroscope and ultrasonic thickness (UT) measurements every outage until drainage is established
  • Submit a report to the staff summarizing the results from the boroscope examinations and the UT measurements
  • Perform UT measurements of the drywell shell, after the drainage is established from all four quadrants, during the next three refueling outages to establish a corrosion rate to demonstrate that the drywell structural integrity will be maintained through the period of extended operation The applicant understands that they will be submitting a statement on the docket and the staff will be establishing a license condition.

No RAls will be issued based on this conference call.

ENCLO'SURE 2

ML11138A321 OFFICE LADLR PM:RPB1:DLR BC:RPB1 :DLR PM:RPB1:DLR

~ME YEdmonds ACunanan BPham ACunanan 06/7/11 06/7/11 06/8/11 06/8/11

~ATE Memorandum to PSEG Nuclear. LLC from A. Cunanan. dated June 8. 2011

SUBJECT:

SUMMARY

OF TELEPHONE CONFERENCE CALL HELD ON MAY 9, 2011, BETWEEN THE U.S. NUCLEAR REGULATORY COMMISSION AND PSEG NUCLEAR, LLC, CONCERNING STATUS OF HOPE CREEK DRYWELL AIR GAP DRAINS DISTRIBUTION:

HARDCOPY:

DLRRF E-MAIL:

PUBLIC RidsNrrDlr Resource RidsNrrDlrRpb1 Resource RidsNrrDlrRpb2 Resource RdsNrrDlrRarb Resource RidsNrrDlrRasb Resource RidsNrrDlrRapb Resource RidsOgcMailCenter Resource BPham ACunanan BBrady LPerkins REnnis CSanders BHarris,OGC ABurritt, RI RConte. RI MModes, RI DTifft, RI NMcNamara, RI