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| number = ML17037C130
| number = ML17037C130
| issue date = 08/01/1972
| issue date = 08/01/1972
| title = Nine Mile Point Unit 1 - Letter Reporting an Orderly Shutdown on July 27, 1972 Due to Increasing Recirculation System Valve Packing Leakage within the Drywell
| title = Letter Reporting an Orderly Shutdown on July 27, 1972 Due to Increasing Recirculation System Valve Packing Leakage within the Drywell
| author name = Schneider F J
| author name = Schneider F
| author affiliation = Niagara Mohawk Power Corp
| author affiliation = Niagara Mohawk Power Corp
| addressee name = Skovholt D J
| addressee name = Skovholt D
| addressee affiliation = US Atomic Energy Commission (AEC)
| addressee affiliation = US Atomic Energy Commission (AEC)
| docket = 05000220
| docket = 05000220
Line 15: Line 15:


=Text=
=Text=
{{#Wiki_filter:AECDISTRIBUTION FORPART50DOCKETMATERIALTEMPORARY FORMFROM'iagara MohawkPowerCorpoSyracuse~
{{#Wiki_filter:AEC DISTRIBUTION FOR PART 50 DOCKET MATERIAL TEMPORARY FORM FI DATE OF DOC:      DATE REC'D    LTR    iRMO    RPT FROM'iagara             Mohawk Power Corpo      tion To:
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regarding an increasing recirculation syst va5W packing leakage within the drywell."
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FfteCy-..NIAGARA~&#x17d;MOHAWK300ERIE8OUIEVARDWESTSYRACUSE, H.Y.IS202NIAGARAMOHAWKPOWERCORPORATION August1,1972Mr.DonaldJ.SkovholtAssistant DirectorforReactorOperations DivisionofReactorLicensing UnitedStatesAtomicEnergyCommission Washington, D.C.205458
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==DearMr.Skovholt:==
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Re:Provisional Operating License:DPR-17DocketNo.:50-220AppendixA(Technical Specifications 3.3.1aand3.3.1b)ofProvisional Operating LicenseDPR-17forNineMilePointNuclearStation,UnitOlstates:3.3.1a"Aftercompletion ofthestartuptestprogramanddemonstration ofplantelectrical output,theprimarycontainment atmosphere shallbereducedtolessthanfivepercentoxygenwithnitrogengaswheneverthereactorcoolantpressureisgreaterthan110psigandthereactorisinthepoweroperating condition, exceptas.specified in"b"below."3.3.1b"Withinthe24hourperiodsubsequent toincreaseofthereactorcoolantpressureabove110psigwheneverthereactorisinthepower.operating conditj.on, thecontainment atmosphere oxygenconcentration shallbereducedtolessthanfivepercentbyweightandmaintained inthiscon-dition.Deinerting wascommenced 24hourspriortoamajorrefueling outageorotherscheduled shutdown."
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AnorderlyshutdownofUnit81,NineMilePointNuclearStationwasbegunonJuly27,1972duetoincreasing recirculation systemvalvepackingleakagewithinthedrywell.Following repacking oftheaffectedvalves,theunitwasrestarted onJuly30,1972andreached110psigat0700thatday.  
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Mx.DonaldJ.Skovho1tUnitedStatesAtomicEnergyCommission 0Page2Anagreement hadbeenmadepriortoshutdownwithNationalCylinderGas,anitrogengassupplierinConshohocken, Pa.fordeliveryoftwotrucksofnitrogenonJuly30,1972.Normalinertingrequires4-6hoursandcouldeasilybeaccomplished thatday,wellwithintherequired24hours.However,unknowntostationpersonnel, thegassupplierwashavingdifficulty inobtaining driversforthenecessary twotrucksofnitrogen.
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ThestartupoftheUnitbeyond110psigcontinued, basedupontheprioragreement thatnitrogenwouldbearrivingforinertingthatday.Atmidnight, July30,1972withnonitrogenforinertingonsite,itwasdeemednecessary bystationpersonnel toholdthermalpowerto1200MN(t)andnotcontinuewiththenormalscheduled startupuntilthedrywellwasinerted.ThefirsttruckofnitrogenarrivedatthestationthemorningofJuly31,1972andinertingbeganimmediately.
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Thedrywellatmosphere wasreducedtolessthanfivepercentoxygenat134Sthatday,reaching3.9percentat1400.Thestartupscheduled thencontinued.
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Thedrywellatmosphere remainedwithinspecification following inertingandwiththearrivalofthesecondtrucklateintheevening,July31,1972wasreducedtoitspresentlevelofonepercentbyweightofoxygen.Verytrulyyours,F.J.Schn'eider VicePresident eOperations 1tllJt}}
August 1, 1972 Mr. Donald J. Skovholt Assistant Director for Reactor Operations Division of Reactor Licensing                                                          8 United States Atomic Energy Commission Washington, D. C.      20545
 
==Dear Mr. Skovholt:==
 
Re:       Provisional Operating License:         DPR-17 Docket No.: 50-220 Appendix A (Technical Specifications 3.3.1 a and 3.3.1 b) of Provisional Operating License DPR-17 for Nine Mile Point Nuclear Station, Unit Ol states:
3.3.1      a "After completion of the startup test program and demonstration of plant electrical output, the primary containment atmosphere shall be reduced to less than five percent oxygen with nitrogen gas whenever the reactor coolant pressure is greater than 110 psig and the reactor is in the power operating condition, except as. specified in "b" below."
3.3.1      b "Within the 24 hour period subsequent to increase of the reactor coolant pressure above 110 psig whenever the reactor is in the power. operating conditj.on, the containment atmosphere oxygen concentration shall be reduced to less than five percent by weight and maintained in this con-dition. Deinerting was commenced 24 hours prior to a major refueling outage or other scheduled shutdown."
An      orderly shutdown of Unit 81, Nine Mile Point Nuclear          Station was begun on July 27, 1972 due to increasing recirculation system                valve packing leakage within the drywell. Following repacking of the                affected valves, the unit was restarted on July 30, 1972 and reached 110                psig at 0700 that day.
 
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0 Mx. Donald  J. Skovho1t                                                  Page 2 United States Atomic Energy Commission An agreement  had been made prior to shutdown with National Cylinder Gas, a nitrogen gas supplier in Conshohocken, Pa. for delivery of two trucks of nitrogen on July 30, 1972. Normal inerting requires 4 - 6 hours and could easily be accomplished that day, well within the required 24 hours. However, unknown to station personnel, the gas supplier was having difficulty in obtaining drivers for the necessary two trucks of nitrogen. The startup of the Unit beyond 110 psig continued, based upon the prior agreement that nitrogen would be arriving for inerting that day. At midnight, July 30, 1972 with no nitrogen for inerting on site,     it was deemed necessary by station personnel  to hold thermal  power  to 1200  MN(t) and not continue with the normal scheduled startup    until  the drywell  was inerted.
The  first  truck of nitrogen arrived at the station the morning of July 31,       1972 and  inerting began immediately. The drywell atmosphere was reduced to less than five percent oxygen at 134S that day, reaching 3.9 percent at 1400.
The  start up scheduled  then continued.
The drywell atmosphere remained within specification following inerting        and with the arrival of the second truck late in the evening, July 31, 1972        was reduced to its present level of one percent by weight of oxygen.
Very truly yours, F. J. Schn'eider Vice President  e Operations
 
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Latest revision as of 20:02, 4 February 2020

Letter Reporting an Orderly Shutdown on July 27, 1972 Due to Increasing Recirculation System Valve Packing Leakage within the Drywell
ML17037C130
Person / Time
Site: Nine Mile Point Constellation icon.png
Issue date: 08/01/1972
From: Schneider F
Niagara Mohawk Power Corp
To: Skovholt D
US Atomic Energy Commission (AEC)
References
Download: ML17037C130 (6)


Text

AEC DISTRIBUTION FOR PART 50 DOCKET MATERIAL TEMPORARY FORM FI DATE OF DOC: DATE REC'D LTR iRMO RPT FROM'iagara Mohawk Power Corpo tion To:

Syracuse~

F N. Y.

J. Schneider Mr. Skovholt 13202 8<<1-72 ORIG CC ('ENT 8.-4 2

~

AEC PDR SENT LOCAL PDR CLASS: U PROP INFO No CYS REC'D DOCKET No:

0 220 DE IPTION: ENCLOSURES:

Ltr reporting an incident on 7-27-72~

regarding an increasing recirculation syst va5W packing leakage within the drywell."

00 NOT REMOVE PLANT NAMES: Nine Mble II%NO'RFtIH Foa ACTION INFORMATION - 2 AB BUTLER L KNIEL L VASSALLO L ZIEMANN L KNIGHTON ENVIRO W/ Copies W/ Copies W/ Copies W/ 9 Copies W/ Copies CLARK(L) SCHWENCER(L) H. DENTON CHITtAtOOD(FM)

W/ Copies W/ Copies W/ Copies W/ Copies W/ Copies GOLLER(L) STOLZ(L) SCHEMEL (L ) DICKER(ENVIRO)

W/ Copies W/ Copies W/-=-Copies- -=-- =-- W/ -=Copies W/ Copies iNTERNAL DISTRXBUTION G TECH REVIEW lr VOLL14ER HARLESS WADE HAEC PDR +HENDRXE ~ENTON (4) SHAFER VOGCp ROOM P-506A g/SCHROEDER GRXMES PSM BROWN WNi&i'TZING/STAr(('ASE

~ MACCARY GAMMXLL SMILEX LANGE KASTNER NUSSBAUMER JAP IHD GIAl4BUSSO PAWLICKX BALIJQU) BRAITMAN

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~ SKOVHOLT-L v'TELLO EHVIRO MASON PIAHS P. COLLINS iMOORE MOLL?R WIISON MODOHALD REG OPR

~> THOMPSON TEDESCO DICKER KARI DUDE KNIGHTON SMITH

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August 1, 1972 Mr. Donald J. Skovholt Assistant Director for Reactor Operations Division of Reactor Licensing 8 United States Atomic Energy Commission Washington, D. C. 20545

Dear Mr. Skovholt:

Re: Provisional Operating License: DPR-17 Docket No.: 50-220 Appendix A (Technical Specifications 3.3.1 a and 3.3.1 b) of Provisional Operating License DPR-17 for Nine Mile Point Nuclear Station, Unit Ol states:

3.3.1 a "After completion of the startup test program and demonstration of plant electrical output, the primary containment atmosphere shall be reduced to less than five percent oxygen with nitrogen gas whenever the reactor coolant pressure is greater than 110 psig and the reactor is in the power operating condition, except as. specified in "b" below."

3.3.1 b "Within the 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> period subsequent to increase of the reactor coolant pressure above 110 psig whenever the reactor is in the power. operating conditj.on, the containment atmosphere oxygen concentration shall be reduced to less than five percent by weight and maintained in this con-dition. Deinerting was commenced 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> prior to a major refueling outage or other scheduled shutdown."

An orderly shutdown of Unit 81, Nine Mile Point Nuclear Station was begun on July 27, 1972 due to increasing recirculation system valve packing leakage within the drywell. Following repacking of the affected valves, the unit was restarted on July 30, 1972 and reached 110 psig at 0700 that day.

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0 Mx. Donald J. Skovho1t Page 2 United States Atomic Energy Commission An agreement had been made prior to shutdown with National Cylinder Gas, a nitrogen gas supplier in Conshohocken, Pa. for delivery of two trucks of nitrogen on July 30, 1972. Normal inerting requires 4 - 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and could easily be accomplished that day, well within the required 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. However, unknown to station personnel, the gas supplier was having difficulty in obtaining drivers for the necessary two trucks of nitrogen. The startup of the Unit beyond 110 psig continued, based upon the prior agreement that nitrogen would be arriving for inerting that day. At midnight, July 30, 1972 with no nitrogen for inerting on site, it was deemed necessary by station personnel to hold thermal power to 1200 MN(t) and not continue with the normal scheduled startup until the drywell was inerted.

The first truck of nitrogen arrived at the station the morning of July 31, 1972 and inerting began immediately. The drywell atmosphere was reduced to less than five percent oxygen at 134S that day, reaching 3.9 percent at 1400.

The start up scheduled then continued.

The drywell atmosphere remained within specification following inerting and with the arrival of the second truck late in the evening, July 31, 1972 was reduced to its present level of one percent by weight of oxygen.

Very truly yours, F. J. Schn'eider Vice President e Operations

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