ML19339C618: Difference between revisions

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UCENSEE EVENT REPORT CONTROL BLOCK: l 1
l    l      l    l    l lh 6
(PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)
  ,R lM !N lP lI lN l 2 l@l 0 l0 l- l 0 l0 LICENSE    14 l 0 l NUMSER 0 l Ol -l0 l 0 l@l4  25      26 l1 LICENSE l1 l1 TYPEl 1 JOl@]67 CAT l 68 l@
8 9            LICENSEE CODE                      15 WON'T 1o111            E'RU 60l t l@l61o l 5101010                            ' 31 o l 61@l          i l oEVENT l i IDATE a l s i o74l@l i l 11            i l 21 a l n80l@
7      8                                                    OOCKET NUMBER                68  89                                  7S      REPORT DATE EVENT DESCRIPTION AND PROBABLE CONSEQUENCES 01o g;                  At Unit I refueling the Unit 1 circulating water intake bay was drained. In                                                                        j
    ,g,3      ,        preparation for additional work in the area, several other drains dumping into the ;
lo 64 l l          bay were isolated. The water supply to No. 121 Pump Priming Exhauster was also                                                                      l 1o isI l            isolated causing loss of prime to No. 21 Cooling Water Pump and loss of cooling                                                                    l lo is l I          water header pressure. Both diesel cooling water pumps started on low pressure.                                                                    l lo l7 l l            No effect on public health and safety since redundant equipment was operable.                                                                    1 inggi l            Not repetitive. Tech Spec 3.3.D.1,a applies.                                                                                                      J E            CODE        SU8C E                  COMPONENT CODE                SUB DE        S      E lo19]                            lW l Al@ y@ l Zl@ l Xl Xl Xl Xl Xl Xlh l Z l@ y @                                                          20 7    8                          9          10          11            12            13                          18        19 SEQUENTIAL                      OCCURRENCE          REPORT                  REVISION
                                    ,,,, EVENT YEAR                            R EPORT NO.                        CODE              TYPE                      NO.
gug h "LER/RO l218l0l g23 l 0l 3l 2l 24            26 y
27 l0l3l W        M lL l 30 b31 W
32
                                    .            22 K N ACT ON                ON PL NT            ME                      HOURS 22        S8 I          POR      8. SUPPLI R          MAN F CTURER l3JG gl34Xlg                    {4g 3                  l36Z l@
l 0l 0l 0l 37 l
40 gg 41 gg 42 l Z lg l Zl 9 l 9 l 9lg 43            44            4; CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h yl                The priming exhauster was returned to service and No. 21 Cooling Water Pump was                                                                      l l
again made operable. The pump was inoperable about 2 hours. Piping modifications I
      ,,,,,;          are being considered te allow maintenance in these areas without affecting operation;
    ,, ,,,g            of the opposite unit.                                                                                                                              l uLjl                                                                                                                                                                  I 7    8 9                                                                                                                                                            80 S                    % POWER                        OTHER STATUS              DIS O RY                          DISCOVERY DESCRIPTION 11 151 l E l@ l 1l0 l0 l@] NA                                                          l    lA l@l        ODerator Observation                                        I A TIVITY Co TENT RELEASED OF RELEASE                            AMOUNT oF ACTIVITY                                                  LCT.ATION OF RELE ASE y y' *@ l Zl@]                                    NA                                    l        l NA                                                                  l PERSONNE$ EXPOSURES NUMBER                TYPE        DESCRIPTION NA                                                                                                            l 11 l 71 l 0 l 0 l 0 l@l Z l@l PE RSONNE L INJU      IES NUMBER                oESCniPriON@
[TTIl8 l90 l 0 l 0 l@l12                    NA                                                                                                                        l 11                                                                                                                                      80
[\ -          LOSS OF OR DAMAGE TO FACILITY Q TYPE          DESCRIPTION                    %.,/
NA                                                                                                                                      l 1G]D8 LzJ@l 7        9              10                                                                                                                                            80 g        ISSUE'        l  @NADESCRIPTION                            _
j llllllllllllli 1      a9 8011180A.W NAME OF PREPARER
                                                                          .      nstad                                      PHONE:
                                                                                                                                              '3                                *}}

Latest revision as of 12:05, 31 January 2020

LER 80-032/03L-0:on 801013,during Refueling,Circulating Water Intake Bay Was Drained.Caused by Inoperable Priming Exhauster & Cooling Water Pump 21.Piping Mods Are Being Considered to Allow Maint W/O Effecting Operation
ML19339C618
Person / Time
Site: Prairie Island Xcel Energy icon.png
Issue date: 11/12/1980
From: Hunstad A
NORTHERN STATES POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML19339C611 List:
References
LER-80-032-03L, LER-80-32-3L, NUDOCS 8011180689
Download: ML19339C618 (1)


Text

_.

UCENSEE EVENT REPORT CONTROL BLOCK: l 1

l l l l l lh 6

(PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)

,R lM !N lP lI lN l 2 l@l 0 l0 l- l 0 l0 LICENSE 14 l 0 l NUMSER 0 l Ol -l0 l 0 l@l4 25 26 l1 LICENSE l1 l1 TYPEl 1 JOl@]67 CAT l 68 l@

8 9 LICENSEE CODE 15 WON'T 1o111 E'RU 60l t l@l61o l 5101010 ' 31 o l 61@l i l oEVENT l i IDATE a l s i o74l@l i l 11 i l 21 a l n80l@

7 8 OOCKET NUMBER 68 89 7S REPORT DATE EVENT DESCRIPTION AND PROBABLE CONSEQUENCES 01o g; At Unit I refueling the Unit 1 circulating water intake bay was drained. In j

,g,3 , preparation for additional work in the area, several other drains dumping into the ;

lo 64 l l bay were isolated. The water supply to No. 121 Pump Priming Exhauster was also l 1o isI l isolated causing loss of prime to No. 21 Cooling Water Pump and loss of cooling l lo is l I water header pressure. Both diesel cooling water pumps started on low pressure. l lo l7 l l No effect on public health and safety since redundant equipment was operable. 1 inggi l Not repetitive. Tech Spec 3.3.D.1,a applies. J E CODE SU8C E COMPONENT CODE SUB DE S E lo19] lW l Al@ y@ l Zl@ l Xl Xl Xl Xl Xl Xlh l Z l@ y @ 20 7 8 9 10 11 12 13 18 19 SEQUENTIAL OCCURRENCE REPORT REVISION

,,,, EVENT YEAR R EPORT NO. CODE TYPE NO.

gug h "LER/RO l218l0l g23 l 0l 3l 2l 24 26 y

27 l0l3l W M lL l 30 b31 W

32

. 22 K N ACT ON ON PL NT ME HOURS 22 S8 I POR 8. SUPPLI R MAN F CTURER l3JG gl34Xlg {4g 3 l36Z l@

l 0l 0l 0l 37 l

40 gg 41 gg 42 l Z lg l Zl 9 l 9 l 9lg 43 44 4; CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h yl The priming exhauster was returned to service and No. 21 Cooling Water Pump was l l

again made operable. The pump was inoperable about 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />. Piping modifications I

,,,,,; are being considered te allow maintenance in these areas without affecting operation;

,, ,,,g of the opposite unit. l uLjl I 7 8 9 80 S  % POWER OTHER STATUS DIS O RY DISCOVERY DESCRIPTION 11 151 l E l@ l 1l0 l0 l@] NA l lA l@l ODerator Observation I A TIVITY Co TENT RELEASED OF RELEASE AMOUNT oF ACTIVITY LCT.ATION OF RELE ASE y y' *@ l Zl@] NA l l NA l PERSONNE$ EXPOSURES NUMBER TYPE DESCRIPTION NA l 11 l 71 l 0 l 0 l 0 l@l Z l@l PE RSONNE L INJU IES NUMBER oESCniPriON@

[TTIl8 l90 l 0 l 0 l@l12 NA l 11 80

[\ - LOSS OF OR DAMAGE TO FACILITY Q TYPE DESCRIPTION  %.,/

NA l 1G]D8 LzJ@l 7 9 10 80 g ISSUE' l @NADESCRIPTION _

j llllllllllllli 1 a9 8011180A.W NAME OF PREPARER

. nstad PHONE:

'3 *