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{{#Wiki_filter:Initini Telhphon5                                                   Dtte cf Report Datt;<:                       1/14/74                       Occurrence   ,,      1/13/74             l
{{#Wiki_filter:Initini Telhphon5 Dtte cf Report Datt;<:
    .      .            -
1/14/74 Occurrence 1/13/74 lidtiniWritten Time of
                                                                                          '
' leport Date:
lidtiniWritten                                                     Time of
1/14/74 Occurrence:
  ' leport Date:                             1/14/74                       Occurrence:           1700
1700 OYSTER CREEK NUCLEAR GENEPATING STATION
                                                                '    '
~
                  .                                                                .
' FORKED RIVER, NEW JERSEY OS731 Abnormal Occurrence Report No. 50-219/74/ 3 IDE.DIFICATION Violation of the Technical Specifications, paragraph N/A Failure of Hydraulic Shock and Sway Arrestors on one Core
                                    '
. Spray System and two Isolation Condenser systems.
                          ~
.~
OYSTER CREEK NUCLEAR GENEPATING STATION
'Ihis event is considered to be an abnormal occurrence as de-fined in the Technical Specifications, paragraph 1.15D CONDITIONS PRIOR TO OCCURRENCE:
                                                ' FORKED RIVER, NEW JERSEY OS731
Steady State Power Routine Shutdown Hot Standby Operation A
                                                  -
Cold Shutdown Load Changes During Refueling Shutdown Routine Power Operation Routine Startup Other (Specify)
Abnormal Occurrence
        .                                              Report No. 50-219/74/ 3
                                                                                              .
                          .
                                                                                                      ,
IDE.DIFICATION                   Violation of the Technical Specifications, paragraph N/A             ,
* Failure of Hydraulic Shock and Sway Arrestors on one Core
                ,    ,
                                      . Spray System and two Isolation Condenser systems.
                                                                  -
                            -
      .
            ,
                                .~
                                        'Ihis event is considered to be an abnormal occurrence as de-
              ,
fined in the Technical Specifications , paragraph 1.15D               .
CONDITIONS PRIOR
* TO OCCURRENCE:                                 Steady State Power               Routine Shutdown Hot Standby                       Operation A       Cold Shutdown                     Load Changes During Refueling Shutdown               Routine Power Operation Routine Startup                   Other (Specify)
Operation
Operation
                                        -The plant was shutdown with reactor coolant at <212 F.
-The plant was shutdown with reactor coolant at <212 F.
                                                                            .
DESCRIPTION During the required inspection of.the Bergen P.aterson HSSA-10 0F OCCURRENCE:
                                                                                          .
units in the primary containment, five units were discovered to be devoid of fluid. They were located as follows:
                                                    .                                .
3 "A" Isolation Condenser 1.
                                              -
"B" Isolation Condenser 1 - Core Spray System #2 i
                                                                                      .
                                                                                            .
* DESCRIPTION                         During the required inspection of.the Bergen P.aterson HSSA-10 0F OCCURRENCE:                       units in the primary containment, five units were discovered to be devoid of fluid. They were located as follows:
  *
                    .
3   "A" Isolation Condenser
: 1. "B" Isolation Condenser 1 - Core Spray System #2
                                  .
i
{
{
!
f/Mo O 6 O THIS DOCUMENT CONTAINS l
l      f/Mo                       O6O                                          THIS DOCUMENT CONTAINS POOR QUAL.lTY PAGES
POOR QUAL.lTY PAGES
                              '
                                                                                                                  .


                                          .                  .
Abn;r:n1 Occurrence f._
                                            '
Reptrt No. 30-219/74/ 3
* Abn;r:n1 Occurrence                       f._                                         ,
(
* Reptrt No. 30-219/74/ 3
Page 2 r
                      ,
t APPAREST CAUSE Design Procedurc 0F OCCURRENCE:
(                                                      Page 2
F!anufacture Unusual Service Condition Installation /
      .                                                                          .
Inc. Environmental Construcrion Component Failure Ope rator Other (Specify)
        %*
The cause of snubb'cr inoperabil'ity was due to a loss of hydraulic fluid.
                                      '
'Ihc cause of fluid loss is presently
r               .                                                                    .
. under investigation.
* t                                       .
ANALYSIS OF The safety significance of t}}is occurrence was a partial O CCU.Y.E.NCE :
APPAREST CAUSE                           Design                               Procedurc 0F OCCURRENCE:                           F!anufacture                         Unusual Service Condition Installation /                       Inc. Environmental Construcrion                         Component Failure
Icss of the seismic rer,trnining ability for the ts o affected systccs.
            .                                      Ope rator                           Other (Specify)
1:ad the plant suffered a design bases carthouake, the probability that these two systems would hz.ve suffered structural damage was increased.
                  '
CORRECTIVE The failed units were replaced with units that were rebuilt ACTION:
              .
with ethylene propylene (Parker Grade E652-90) seal material.
                            '
e FAILURE DATA:
The cause of snubb'cr inoperabil'ity was due to a loss of
Flanufacturer:
                          .              hydraulic fluid.             'Ihc cause of fluid loss is presently
Bergen Paterson Type: ilSSA-10 Scrial Nos.:
    .                                . under investigation.
487S17 4874S7 477376 470924 469962 r
                    .
.O Prepared by:
                                                                                          -
..I f
                .
* _ c'
                  .                                                                      .
.Date:
                                                                  .
I/14/74 l.
                                                                                                  .
ANALYSIS OF                   The safety significance of t}}is occurrence was a partial O CCU.Y.E.NCE :                 Icss of the seismic rer,trnining ability for the ts o affected systccs.       1:ad the plant suffered a design bases carthouake, the probability that these two systems would hz.ve suffered structural damage was increased.
                                              .
                                                                    .
                                                    *
                                    .
                                                                              .
CORRECTIVE                     The failed units were replaced with units that were rebuilt ACTION:                         with ethylene propylene (Parker Grade E652-90) seal material.
                                                                                          .
* e
_
          .
                                                                                      .
                                            *
                                                                                  .
                                                                          '
FAILURE DATA:                 Flanufacturer: Bergen Paterson Type: ilSSA-10 Scrial Nos.:         487S17
                              -
4874S7
!                                                              477376 470924 469962
'
r                        .O Prepared by:             . .I         '.'        f
* _ c'               .Date:         I/14/74 l.
,}}
,}}

Latest revision as of 05:59, 24 December 2024

AO 50-219/74/3:on 740113,during Insp of Bergen-Paterson HSSA-10 Units Primary Containment Hydraulic Shock & Sway Arrestors Found Devoid of Fluid.Cause Under Study.Units to Be Replaced W/Units Rebuilt W/Ethylene Propylene Seal Matl
ML19347C804
Person / Time
Site: Oyster Creek
Issue date: 01/14/1974
From: Rone A
JERSEY CENTRAL POWER & LIGHT CO.
To:
References
AO-50-219-74-3, NUDOCS 8103040604
Download: ML19347C804 (2)


Text

Initini Telhphon5 Dtte cf Report Datt;<:

1/14/74 Occurrence 1/13/74 lidtiniWritten Time of

' leport Date:

1/14/74 Occurrence:

1700 OYSTER CREEK NUCLEAR GENEPATING STATION

~

' FORKED RIVER, NEW JERSEY OS731 Abnormal Occurrence Report No. 50-219/74/ 3 IDE.DIFICATION Violation of the Technical Specifications, paragraph N/A Failure of Hydraulic Shock and Sway Arrestors on one Core

. Spray System and two Isolation Condenser systems.

.~

'Ihis event is considered to be an abnormal occurrence as de-fined in the Technical Specifications, paragraph 1.15D CONDITIONS PRIOR TO OCCURRENCE:

Steady State Power Routine Shutdown Hot Standby Operation A

Cold Shutdown Load Changes During Refueling Shutdown Routine Power Operation Routine Startup Other (Specify)

Operation

-The plant was shutdown with reactor coolant at <212 F.

DESCRIPTION During the required inspection of.the Bergen P.aterson HSSA-10 0F OCCURRENCE:

units in the primary containment, five units were discovered to be devoid of fluid. They were located as follows:

3 "A" Isolation Condenser 1.

"B" Isolation Condenser 1 - Core Spray System #2 i

{

f/Mo O 6 O THIS DOCUMENT CONTAINS l

POOR QUAL.lTY PAGES

Abn;r:n1 Occurrence f._

Reptrt No. 30-219/74/ 3

(

Page 2 r

t APPAREST CAUSE Design Procedurc 0F OCCURRENCE:

F!anufacture Unusual Service Condition Installation /

Inc. Environmental Construcrion Component Failure Ope rator Other (Specify)

The cause of snubb'cr inoperabil'ity was due to a loss of hydraulic fluid.

'Ihc cause of fluid loss is presently

. under investigation.

ANALYSIS OF The safety significance of tis occurrence was a partial O CCU.Y.E.NCE : Icss of the seismic rer,trnining ability for the ts o affected systccs. 1:ad the plant suffered a design bases carthouake, the probability that these two systems would hz.ve suffered structural damage was increased. CORRECTIVE The failed units were replaced with units that were rebuilt ACTION: with ethylene propylene (Parker Grade E652-90) seal material. e FAILURE DATA: Flanufacturer: Bergen Paterson Type: ilSSA-10 Scrial Nos.: 487S17 4874S7 477376 470924 469962 r .O Prepared by: ..I f

  • _ c'

.Date: I/14/74 l. ,}}