ML18024B179: Difference between revisions

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| issue date = 12/05/1979
| issue date = 12/05/1979
| title = RO 50-296/79-19:on 791204,during Augmented Ultrasonic Insp of Core Spray Piping,Indication Located Adjacent to safe-end to Core Spray Pipe Weld.Caused by Stress Corrosion Cracking.Piping Replaced W/Carbon Steel
| title = RO 50-296/79-19:on 791204,during Augmented Ultrasonic Insp of Core Spray Piping,Indication Located Adjacent to safe-end to Core Spray Pipe Weld.Caused by Stress Corrosion Cracking.Piping Replaced W/Carbon Steel
| author name = ABERCROMBIE H
| author name = Abercrombie H
| author affiliation = TENNESSEE VALLEY AUTHORITY
| author affiliation = TENNESSEE VALLEY AUTHORITY
| addressee name =  
| addressee name =  
Line 14: Line 14:
| page count = 4
| page count = 4
}}
}}
See also: [[followed by::IR 05000296/1979019]]


=Text=
=Text=
{{#Wiki_filter:REGULAT INFORMATION
{{#Wiki_filter:REGULAT       INFORMATION DISTRIBUTION             STER (ADIOS) .
DISTRIBUTION
ACCESSION NBR:7912190554                 DOC.DATE: 79/ 12/05            NOTARIZEDa. NO        DOCKET FACIL:50 259 drowns Ferry i~luclear Power Stations Unit 1r Tennessee                        05000259 50=2o0~owns Pet ry Nuclear Power Station< Unit 2i Tennessee                        05000260 50   299r'owns Ferry Nuclear Power Stations Unit 3i Tennessee                    0500029o A   ~
STER (ADIOS).ACCESSION NBR:7912190554
          ~ cs r4             AU HUH AFF IL I A T ION T
DOC.DATE: 79/FACIL:50 259 drowns Ferry i~luclear Power 50=2o0~owns
AbE <CHONUIE~H,           Tennessee Valley 4uthor ity RECIP,NA~E                 RECIPIENT AFFILIATION I
Pet ry Nuclear Power 50 299r'owns Ferry Nuclear Power A~~cs r4 AU T HUH AFF IL I A T ION AbE<CHONUIE~H, Tennessee Valley 4uthor RECIP,NA~E
 
RECIPIENT AFFILIATION
==SUBJECT:==
12/05 NOTARIZEDa.
RO   50 296/79-19:on 791204iduring auqmented ul trasonic insp of units 3 core spray piping<indication located adjacent to safe end to core spray pipe weld.Caused oy stress corrosion cracxing.Piping replaced w/carbon steel.
NO Stations Unit 1r Tennessee Station<Unit 2i Tennessee Stations Unit 3i Tennessee ity DOCKET 05000259 05000260 0500029o I SUBJECT: RO 50 296/79-19:on
orsr~rsvrros coos:           .aaars   covrzs I'I1Lk.: Ltfc. (Uackf i t) r scsrvso:era      /  soccer    srzs:~
791204iduring
NOTES:
auqmented ul trasonic insp of units 3 core spray piping<indication
REC IP IEN l         COPIES                HEC IP IEN T          COPIES ID CODE/NAKE           LTl'R ENCL         Iu CODt/NAi~E         LTTh ENCL INTEHNALa      0    R  G  FrlE            1  ~
located adjacent to safe end to core spray pipe weld.Caused
02 hHC PDR                 1 04 I                        2              HPA                       1 NSIC                        1              H   IRELAND               1 S  HANAUEH                  1 txTERNAL: 03 LPDR TOTAL NUh]HER OF COPIES           RE4UIRtD:   L TTR     9   E!')CL gag
oy stress corrosion cracxing.Piping
 
replaced w/carbon steel.orsr~rsvrros
3XLECOPY 'K) RRC 12/5/79
coos:.aaars covrzs r scsrvso:era
                                                              '.',=,:;jRC RFCI'
/soccer srzs:~I'I1Lk.: Ltfc.(Uackf i t)NOTES: REC IP IEN l ID CODE/NAKE INTEHNALa 0 R G FrlE 04 I NSIC S HANAUEH COPIES LTl'R ENCL 1~2 1 1 HEC IP IEN T Iu CODt/NAi~E
                                                                -!   ANTP.. ".-'.-
02 hHC PDR HPA H IRELAND COPIES LTTh ENCL 1 1 1 txTERNAL: 03 LPDR TOTAL NUh]HER OF COPIES RE4UIRtD: L TTR 9 E!')CL gag  
l.'-..8, Huc1ear Regulatory Coamission Reg,ion 4X 101 Nazietta      Street                                    ~g gpss     5   AIf;   00 i P. O'RBLLY.
Suk.te 3100 Atlanta, Georgia        30303                                                                        'C. M. UPRIGHl' 0 CHENDLMj lV. S. RENTAL, F. J. LONG E, Q. E. MURPHY AFRO-50-296/>919                                                                                      ,9. T. SUTHERLAND P
3XLECOPY'K)RRC 12/5/79 l.'-..8, Huc1ear Regulatory
K M.C   RK Reported under Technical Specification 6.7.2.a(9)
Coamission
Date of Occurrence;         12/4/79 Speci.frication              Time of Occurrence:       9:30 a,m.       Unit         3
Reg,ion 4X 101 Nazietta Street Suk.te 3100 Atlanta, Georgia 30303 AFRO-50-296/>919
'reehnical                       involved:       Hone Conditions Prior to Occurrence: Unit. 3 in refueling mutate.                         Vases         1 and 2 in normal operation at 995 MVe and 735 Yde, respectkvelr.
P'.',=,:;jRC
58entffication       and Deacr'i tioa 6f. Occurrence:       QiHe perfomfr;g an 'augmented uLtrasonic       inspection   of unit   3 coze spray piping, sn bd%cat5on was locet~
RFCI'-!ANTP..".-'.-~g gpss 5 AIf;00 i P.O'RBLLY.'C.M.UPRIGHl'0 CHENDLMj lV.S.RENTAL, F.J.LONG E, Q.E.MURPHY ,9.T.SUTHERLAND
ad3scent to the       safe-end   to   core   sprsy pipe ~~M (weld Ho. DC&-3-l8)                   ~
K M.C RK Reported under Technical Specification
fnspection       was performed   et>en   though   chks piping var being rap~sc:ed during the exfsting. scheduled outage.             There veze no resulting significant occur" fences, no previous similar events, and no danger to the health or                         safeL)'f
6.7.2.a(9)
    'the pub1ic.
Date of Occurrence;
A     grant   Cause of Occurrence.         Subseouent metallurgica1 analysis of the removed     ultrasonic indication       area revealed stress-corrosion cracking. in the weld heat-affected'cone         ek gabe   %0-inc> diameter, scb Gute 80, P-~>
12/4/79 Time of Occurrence:
less-stee1       pipei   A detai1ed metaLLurgical report,         is forthcoTair~
9:30 a,m.Unit 3'reehnical
Qtbez Related Events: %e potent%ax foz stress-cozz.Agon cracking, in certai>
Speci.frication
stain ess-steeK P.ping, his been previousl) ibex'iie5 Cenectt.ve Action T'eken nr Planned; Piping oa unit 3 was chansed out and replaced with carbon steel, L>nit 2 core spray piping vas chST'.ged to c-rhnn itee1 on a previous outage. LTnit X zefueliag. outage begins DanuaTy iK2, indi-                          LSM, at >+feb time we will perform an insenCce inspection to deterTnine cations ex%st.         If indications are observed,. eweKuatMa and sobseqeent repafra aa   necessa~ &El       be performed.
involved: Hone Conditions
r   <
Prior to Occurrence:
8 i.. AberczoTUbie Tosser 'Plant Superintendent
Unit.3 in refueling mutate.Vases 1 and 2 in normal operation at 995 MVe and 735 Yde, respectkvelr.
%res     Vert'y Huclear PLaat                                                                               P 001
58entffication
                                                                            '18190     QS$                     g/g
and Deacr'i tioa 6f.Occurrence:
 
QiHe perfomfr;g
T}}
an'augmented
uLtrasonic
inspection
of unit 3 coze spray piping, sn bd%cat5on was locet~ad3scent to the safe-end to core sprsy pipe~~M (weld Ho.DC&-3-l8)~fnspection
was performed et>en though chks piping var being rap~sc:ed during the exfsting.scheduled outage.There veze no resulting significant
occur" fences, no previous similar events, and no danger to the health or safeL)'f'the pub1ic.A grant Cause of Occurrence.
Subseouent
metallurgica1
analysis of the removed ultrasonic
indication
area revealed stress-corrosion
cracking.in the weld heat-affected'cone
ek gabe%0-inc>diameter, scb Gute 80, P-~>less-stee1
pipei A detai1ed metaLLurgical
report, is forthcoTair~
Qtbez Related Events:%e potent%ax foz stress-cozz.Agon
cracking, in certai>stain ess-steeK P.ping, his been previousl)
ibex'iie5 Cenectt.ve
Action T'eken nr Planned;Piping oa unit 3 was chansed out and replaced with carbon steel, L>nit 2 core spray piping vas chST'.ged to c-rhnn itee1 on a previous outage.LTnit X zefueliag.
outage begins DanuaTy 2, LSM, at>+feb time we will perform an insenCce inspection
to deterTnine
iK indi-cations ex%st.If indications
are observed,.
eweKuatMa and sobseqeent
repafra aa necessa~&El be performed.
r<8 i..AberczoTUbie
Tosser'Plant Superintendent
%res Vert'y Huclear PLaat P 001'18190 QS$g/g  
T
}}

Latest revision as of 02:56, 22 October 2019

RO 50-296/79-19:on 791204,during Augmented Ultrasonic Insp of Core Spray Piping,Indication Located Adjacent to safe-end to Core Spray Pipe Weld.Caused by Stress Corrosion Cracking.Piping Replaced W/Carbon Steel
ML18024B179
Person / Time
Site: Browns Ferry Tennessee Valley Authority icon.png
Issue date: 12/05/1979
From: Abercrombie H
TENNESSEE VALLEY AUTHORITY
To:
References
NUDOCS 7912190554
Download: ML18024B179 (4)


Text

REGULAT INFORMATION DISTRIBUTION STER (ADIOS) .

ACCESSION NBR:7912190554 DOC.DATE: 79/ 12/05 NOTARIZEDa. NO DOCKET FACIL:50 259 drowns Ferry i~luclear Power Stations Unit 1r Tennessee 05000259 50=2o0~owns Pet ry Nuclear Power Station< Unit 2i Tennessee 05000260 50 299r'owns Ferry Nuclear Power Stations Unit 3i Tennessee 0500029o A ~

~ cs r4 AU HUH AFF IL I A T ION T

AbE <CHONUIE~H, Tennessee Valley 4uthor ity RECIP,NA~E RECIPIENT AFFILIATION I

SUBJECT:

RO 50 296/79-19:on 791204iduring auqmented ul trasonic insp of units 3 core spray piping<indication located adjacent to safe end to core spray pipe weld.Caused oy stress corrosion cracxing.Piping replaced w/carbon steel.

orsr~rsvrros coos: .aaars covrzs I'I1Lk.: Ltfc. (Uackf i t) r scsrvso:era / soccer srzs:~

NOTES:

REC IP IEN l COPIES HEC IP IEN T COPIES ID CODE/NAKE LTl'R ENCL Iu CODt/NAi~E LTTh ENCL INTEHNALa 0 R G FrlE 1 ~

02 hHC PDR 1 04 I 2 HPA 1 NSIC 1 H IRELAND 1 S HANAUEH 1 txTERNAL: 03 LPDR TOTAL NUh]HER OF COPIES RE4UIRtD: L TTR 9 E!')CL gag

3XLECOPY 'K) RRC 12/5/79

'.',=,:;jRC RFCI'

-! ANTP.. ".-'.-

l.'-..8, Huc1ear Regulatory Coamission Reg,ion 4X 101 Nazietta Street ~g gpss 5 AIf; 00 i P. O'RBLLY.

Suk.te 3100 Atlanta, Georgia 30303 'C. M. UPRIGHl' 0 CHENDLMj lV. S. RENTAL, F. J. LONG E, Q. E. MURPHY AFRO-50-296/>919 ,9. T. SUTHERLAND P

K M.C RK Reported under Technical Specification 6.7.2.a(9)

Date of Occurrence; 12/4/79 Speci.frication Time of Occurrence: 9:30 a,m. Unit 3

'reehnical involved: Hone Conditions Prior to Occurrence: Unit. 3 in refueling mutate. Vases 1 and 2 in normal operation at 995 MVe and 735 Yde, respectkvelr.

58entffication and Deacr'i tioa 6f. Occurrence: QiHe perfomfr;g an 'augmented uLtrasonic inspection of unit 3 coze spray piping, sn bd%cat5on was locet~

ad3scent to the safe-end to core sprsy pipe ~~M (weld Ho. DC&-3-l8) ~

fnspection was performed et>en though chks piping var being rap~sc:ed during the exfsting. scheduled outage. There veze no resulting significant occur" fences, no previous similar events, and no danger to the health or safeL)'f

'the pub1ic.

A grant Cause of Occurrence. Subseouent metallurgica1 analysis of the removed ultrasonic indication area revealed stress-corrosion cracking. in the weld heat-affected'cone ek gabe %0-inc> diameter, scb Gute 80, P-~>

less-stee1 pipei A detai1ed metaLLurgical report, is forthcoTair~

Qtbez Related Events: %e potent%ax foz stress-cozz.Agon cracking, in certai>

stain ess-steeK P.ping, his been previousl) ibex'iie5 Cenectt.ve Action T'eken nr Planned; Piping oa unit 3 was chansed out and replaced with carbon steel, L>nit 2 core spray piping vas chST'.ged to c-rhnn itee1 on a previous outage. LTnit X zefueliag. outage begins DanuaTy iK2, indi- LSM, at >+feb time we will perform an insenCce inspection to deterTnine cations ex%st. If indications are observed,. eweKuatMa and sobseqeent repafra aa necessa~ &El be performed.

r <

8 i.. AberczoTUbie Tosser 'Plant Superintendent

%res Vert'y Huclear PLaat P 001

'18190 QS$ g/g

T