ML070780439: Difference between revisions

From kanterella
Jump to navigation Jump to search
(Created page by program invented by StriderTol)
 
(Created page by program invented by StriderTol)
 
(2 intermediate revisions by the same user not shown)
Line 16: Line 16:


=Text=
=Text=
{{#Wiki_filter:I Enfwgy I CONDITION REPORT I CR-PNP-~OO~-O~O~~
{{#Wiki_filter:I           Enfwgy               I   CONDITION REPORT                         I C R - P N P - ~ O O ~ - O ~ OI ~ ~
I Originator: CONVERTED DATA Originator Group:
Originator: CONVERTED DATA                                   Originator Phone: 0 Originator Group: CONVERTED DATA                               Operability Required: N Reportability Required: N Supervisor Name: CONVERTED DATA Discovered Date: 09/10/2001 0O:OO                                   Initiated Date: 09/10/2001 0O:OO Condition
CONVERTED DATA Supervisor Name: CONVERTED DATA Discovered Date: 09/10/2001 0O:OO Originator Phone:
0 Operability Required:
N Reportability Required:
N Initiated Date:
09/10/2001 0O:OO Condition


== Description:==
== Description:==
Line 29: Line 24:


== Description:==
== Description:==
Suggested Action
Suggested Action


Line 34: Line 30:


EQUIPMENT:
EQUIPMENT:
Tap Name REFERENCE ITEMS:
Tap Name                         Tag Suffix Name Component Code Process System Code 61 REFERENCE ITEMS:
Type Code CONVERTED PR Tag Suffix Name Component Code Process System Code 61 Description PR.01.4048 i Entergy ADMIN CR-PNP-2001-04048 Initiated Date:
Type Code                    Description CONVERTED PR                PR.01.4048
9/10/2001 0:OO Owner Group  
 
:Environmental Staff Current Contact:
i Entergy                             ADMIN                         CR-PNP-2001-04048 Initiated Date: 9/10/2001 0:OO Owner Group :Environmental Staff Current
MILLER, R. Current Significance:
 
C - CORRECTION Closed by: MILLER, R. 9/17/2001 0:OO Summary
==Contact:==
MILLER, R.
Current Significance: C - CORRECTION Closed by: MILLER, R.                                     9/17/2001 0:OO Summary


== Description:==
== Description:==
RECEVIED SBO DG FUEL TANK LEAKAGE ALARM ALERT WET PROBES 1 Remarks
RECEVIED SBO DG FUEL TANK LEAKAGE ALARM ALERT WET PROBES 1 Remarks


Line 49: Line 48:


== Description:==
== Description:==
SEE CORRECTIVE ACTION RESPONSE.
SEE CORRECTIVE ACTION RESPONSE.
I I A S S I G N M E N T S I CR-PNP-2001-04048 Version: 1 Significance Code: C - CORRECTION Classification Code: NON-SIGNIFICANT Owner Group: Environmental Staff Performed By: Scheffer,Jacob J 09/10/2001 0O:OO Assignment
 
I A SSIGNMENTS                I CR-PNP-2001-04048 I
Version: 1 Significance Code: C - CORRECTION Classification Code: NON-SIGNIFICANT Owner Group: Environmental Staff Performed By: Scheffer,Jacob J               09/10/20010O:OO Assignment


== Description:==
== Description:==


REVIEW THE ISSUES IDENTIFIED IN THIS PROBLEM REPORT REGARDING REGULATORY ISSUES. DOES ALARM REQUIRE AN ACTION ON OUR PART. DETERMINE AND IMPLEMENT REQUIRED CORRECTIVE ACTIONS.
REVIEW THE ISSUES IDENTIFIED IN THIS PROBLEM REPORT REGARDING REGULATORY ISSUES. DOES ALARM REQUIRE AN ACTION ON OUR PART.
CORRECTIVE ACTION 1 CR-PNP-2001-04048 CA Number: 1 Assigned By:
DETERMINE AND IMPLEMENT REQUIRED CORRECTIVE ACTIONS.
Regulatory  
 
& Industry Affairs Staff Assigned To: Environmental Staff RIGGS, W.
CORRECTIVE ACTION                                         1 CR-PNP-2001-04048 CA Number:               1 Assigned By: Regulatory & Industry Affairs Staff                           RIGGS, W.
SchefferJacob J Subassigned To : Originated By: RIGGS, W. Performed By: SCHEFFER, J. Subperformed By: Approved By:
Assigned To: Environmental Staff                                           SchefferJacob J Subassigned To :
Closed By: RIGGS, W. 9/10/2001 0O:OO:OO 9/13/2001 0O:OO:OO 9/13/2001 0O:OO:OO Current Due Date: 09/13/2001 Initial Due Date: 09/13/2001 CA Type: GENERAL Plant Constraint:
Originated By: RIGGS, W.                                                     9/10/2001 0O:OO:OO Performed By: SCHEFFER, J.                                                   9/13/2001 0O:OO:OO Subperformed By:
NONE CA
Approved By:
Closed By: RIGGS, W.                                                   9/13/2001 0O:OO:OO Current Due Date: 09/13/2001                               Initial Due Date: 09/13/2001 CA Type: GENERAL Plant Constraint: NONE CA


== Description:==
== Description:==


REVIEW THE ISSUES IDENTIFIED IN THIS PROBLEM REPORT REGARDING REGULATORY ISSUES.
REVIEW THE ISSUES IDENTIFIED IN THIS PROBLEM REPORT REGARDING REGULATORY ISSUES. DOES ALARM REQUIRE AN ACTION ON OUR PART.
DOES ALARM REQUIRE AN ACTION ON OUR PART. DETERMINE AND IMPLEMENT REQUIRED CORRECTIVE ACTIONS. Response:
DETERMINE AND IMPLEMENT REQUIRED CORRECTIVE ACTIONS.
Subresponse  
 
: CONVERTED DATA Closure Comments: MEMO DETAILING THE RESULTS OF THE REVIEW AND THE CORRECTIVE ACTIONS TAKEN. [Note; Joe Egan for J. Scheffer, 9/13/01]
===Response===
Problem report 01.4048.00  
CONVERTED DATA Subresponse :
[Received SBO DG "leak" alarm] has been reviewed and the conclusion reached that there is no need for any external notifications and there is no regulatory issue, based on the following information:  
Closure Comments:
: 1) The alarm is an indication of water in the tank's annulus (it is a double walled fiberglass tank). MR 01 118604 was submitted to check for the presence of water in the fuel oil. 2) There is no evidence of a release of diesel fuel oil fiom either underground storage tank (T-160 A or B) for the SBO (Station Blackout)
MEMO DETAILING THE RESULTS OF THE REVIEW AND THE CORRECTIVE ACTIONS TAKEN.
Diesel. Tank fuel levels have remained constant before and after this alarm. Therefore, there is no leak to the environment and no need for any notifications.  
[Note; Joe Egan for J. Scheffer, 9/13/01]
: 3) This is a repeat occurrence (alarm with no indication of tank integrity problem).
Problem report 01.4048.00 [Received SBO DG "leak" alarm] has been reviewed and the conclusion reached that there is no need for any external notifications and there is no regulatory issue, based on the following information:
The system engineer is aware of this and is expecting that the upgrade to the leak detection instrumentation (PDC 00-16) will address this problem.  
: 1) The alarm is an indication of water in the tank's annulus (it is a double walled fiberglass tank). MR 01 118604 was submitted to check for the presence of water in the fuel oil.
: 2) There is no evidence of a release of diesel fuel oil fiom either underground storage tank (T-160 A or B) for the SBO (Station Blackout) Diesel. Tank fuel levels have remained constant before and after this alarm. Therefore, there is no leak to the environment and no need for any notifications.
: 3) This is a repeat occurrence (alarm with no indication of tank integrity problem). The system engineer is aware of this and is expecting that the upgrade to the leak detection instrumentation (PDC 00-16) will address this problem.
: 4) Any future alarms do require actions, similar to what was done in this instance (validate alarm, increase monitoring, investigate equipment condition, etc.).
: 4) Any future alarms do require actions, similar to what was done in this instance (validate alarm, increase monitoring, investigate equipment condition, etc.).
Based on this, I conclude all immediate corrective actions are in place or have been completed. This action item for Environmental (regarding regulatory issues) should be closed.}}
Based on this, I conclude all immediate corrective actions are in place or have been completed. This action item for Environmental (regarding regulatory issues) should be closed.}}

Latest revision as of 13:25, 7 December 2019

CR-PNP-2001-04048, Received SBO DG Fuel Tank Leakage Alarm Alert Wet Probes
ML070780439
Person / Time
Site: Pilgrim
Issue date: 09/10/2001
From:
Entergy Corp
To:
Office of Nuclear Reactor Regulation
References
CR-PNP-201-04048
Download: ML070780439 (4)


Text

I Enfwgy I CONDITION REPORT I C R - P N P - ~ O O ~ - O ~ OI ~ ~

Originator: CONVERTED DATA Originator Phone: 0 Originator Group: CONVERTED DATA Operability Required: N Reportability Required: N Supervisor Name: CONVERTED DATA Discovered Date: 09/10/2001 0O:OO Initiated Date: 09/10/2001 0O:OO Condition

Description:

RECEVED SBO DG FUEL TANK LEAKAGE ALARM ALERT WET PROBES Immediate Action

Description:

Suggested Action

Description:

EQUIPMENT:

Tap Name Tag Suffix Name Component Code Process System Code 61 REFERENCE ITEMS:

Type Code Description CONVERTED PR PR.01.4048

i Entergy ADMIN CR-PNP-2001-04048 Initiated Date: 9/10/2001 0:OO Owner Group :Environmental Staff Current

Contact:

MILLER, R.

Current Significance: C - CORRECTION Closed by: MILLER, R. 9/17/2001 0:OO Summary

Description:

RECEVIED SBO DG FUEL TANK LEAKAGE ALARM ALERT WET PROBES 1 Remarks

Description:

PR=EF SBO DG FUEL TANK LEAKAGE C191 B. CHENARD Closure

Description:

SEE CORRECTIVE ACTION RESPONSE.

I A SSIGNMENTS I CR-PNP-2001-04048 I

Version: 1 Significance Code: C - CORRECTION Classification Code: NON-SIGNIFICANT Owner Group: Environmental Staff Performed By: Scheffer,Jacob J 09/10/20010O:OO Assignment

Description:

REVIEW THE ISSUES IDENTIFIED IN THIS PROBLEM REPORT REGARDING REGULATORY ISSUES. DOES ALARM REQUIRE AN ACTION ON OUR PART.

DETERMINE AND IMPLEMENT REQUIRED CORRECTIVE ACTIONS.

CORRECTIVE ACTION 1 CR-PNP-2001-04048 CA Number: 1 Assigned By: Regulatory & Industry Affairs Staff RIGGS, W.

Assigned To: Environmental Staff SchefferJacob J Subassigned To :

Originated By: RIGGS, W. 9/10/2001 0O:OO:OO Performed By: SCHEFFER, J. 9/13/2001 0O:OO:OO Subperformed By:

Approved By:

Closed By: RIGGS, W. 9/13/2001 0O:OO:OO Current Due Date: 09/13/2001 Initial Due Date: 09/13/2001 CA Type: GENERAL Plant Constraint: NONE CA

Description:

REVIEW THE ISSUES IDENTIFIED IN THIS PROBLEM REPORT REGARDING REGULATORY ISSUES. DOES ALARM REQUIRE AN ACTION ON OUR PART.

DETERMINE AND IMPLEMENT REQUIRED CORRECTIVE ACTIONS.

Response

CONVERTED DATA Subresponse :

Closure Comments:

MEMO DETAILING THE RESULTS OF THE REVIEW AND THE CORRECTIVE ACTIONS TAKEN.

[Note; Joe Egan for J. Scheffer, 9/13/01]

Problem report 01.4048.00 [Received SBO DG "leak" alarm] has been reviewed and the conclusion reached that there is no need for any external notifications and there is no regulatory issue, based on the following information:

1) The alarm is an indication of water in the tank's annulus (it is a double walled fiberglass tank). MR 01 118604 was submitted to check for the presence of water in the fuel oil.
2) There is no evidence of a release of diesel fuel oil fiom either underground storage tank (T-160 A or B) for the SBO (Station Blackout) Diesel. Tank fuel levels have remained constant before and after this alarm. Therefore, there is no leak to the environment and no need for any notifications.
3) This is a repeat occurrence (alarm with no indication of tank integrity problem). The system engineer is aware of this and is expecting that the upgrade to the leak detection instrumentation (PDC 00-16) will address this problem.
4) Any future alarms do require actions, similar to what was done in this instance (validate alarm, increase monitoring, investigate equipment condition, etc.).

Based on this, I conclude all immediate corrective actions are in place or have been completed. This action item for Environmental (regarding regulatory issues) should be closed.