ML070780439

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CR-PNP-2001-04048, Received SBO DG Fuel Tank Leakage Alarm Alert Wet Probes
ML070780439
Person / Time
Site: Pilgrim
Issue date: 09/10/2001
From:
Entergy Corp
To:
Office of Nuclear Reactor Regulation
References
CR-PNP-201-04048
Download: ML070780439 (4)


Text

I Enfwgy I CONDITION REPORT I C R - P N P - ~ O O ~ - O ~ OI ~ ~

Originator: CONVERTED DATA Originator Phone: 0 Originator Group: CONVERTED DATA Operability Required: N Reportability Required: N Supervisor Name: CONVERTED DATA Discovered Date: 09/10/2001 0O:OO Initiated Date: 09/10/2001 0O:OO Condition

Description:

RECEVED SBO DG FUEL TANK LEAKAGE ALARM ALERT WET PROBES Immediate Action

Description:

Suggested Action

Description:

EQUIPMENT:

Tap Name Tag Suffix Name Component Code Process System Code 61 REFERENCE ITEMS:

Type Code Description CONVERTED PR PR.01.4048

i Entergy ADMIN CR-PNP-2001-04048 Initiated Date: 9/10/2001 0:OO Owner Group :Environmental Staff Current

Contact:

MILLER, R.

Current Significance: C - CORRECTION Closed by: MILLER, R. 9/17/2001 0:OO Summary

Description:

RECEVIED SBO DG FUEL TANK LEAKAGE ALARM ALERT WET PROBES 1 Remarks

Description:

PR=EF SBO DG FUEL TANK LEAKAGE C191 B. CHENARD Closure

Description:

SEE CORRECTIVE ACTION RESPONSE.

I A SSIGNMENTS I CR-PNP-2001-04048 I

Version: 1 Significance Code: C - CORRECTION Classification Code: NON-SIGNIFICANT Owner Group: Environmental Staff Performed By: Scheffer,Jacob J 09/10/20010O:OO Assignment

Description:

REVIEW THE ISSUES IDENTIFIED IN THIS PROBLEM REPORT REGARDING REGULATORY ISSUES. DOES ALARM REQUIRE AN ACTION ON OUR PART.

DETERMINE AND IMPLEMENT REQUIRED CORRECTIVE ACTIONS.

CORRECTIVE ACTION 1 CR-PNP-2001-04048 CA Number: 1 Assigned By: Regulatory & Industry Affairs Staff RIGGS, W.

Assigned To: Environmental Staff SchefferJacob J Subassigned To :

Originated By: RIGGS, W. 9/10/2001 0O:OO:OO Performed By: SCHEFFER, J. 9/13/2001 0O:OO:OO Subperformed By:

Approved By:

Closed By: RIGGS, W. 9/13/2001 0O:OO:OO Current Due Date: 09/13/2001 Initial Due Date: 09/13/2001 CA Type: GENERAL Plant Constraint: NONE CA

Description:

REVIEW THE ISSUES IDENTIFIED IN THIS PROBLEM REPORT REGARDING REGULATORY ISSUES. DOES ALARM REQUIRE AN ACTION ON OUR PART.

DETERMINE AND IMPLEMENT REQUIRED CORRECTIVE ACTIONS.

Response

CONVERTED DATA Subresponse :

Closure Comments:

MEMO DETAILING THE RESULTS OF THE REVIEW AND THE CORRECTIVE ACTIONS TAKEN.

[Note; Joe Egan for J. Scheffer, 9/13/01]

Problem report 01.4048.00 [Received SBO DG "leak" alarm] has been reviewed and the conclusion reached that there is no need for any external notifications and there is no regulatory issue, based on the following information:

1) The alarm is an indication of water in the tank's annulus (it is a double walled fiberglass tank). MR 01 118604 was submitted to check for the presence of water in the fuel oil.
2) There is no evidence of a release of diesel fuel oil fiom either underground storage tank (T-160 A or B) for the SBO (Station Blackout) Diesel. Tank fuel levels have remained constant before and after this alarm. Therefore, there is no leak to the environment and no need for any notifications.
3) This is a repeat occurrence (alarm with no indication of tank integrity problem). The system engineer is aware of this and is expecting that the upgrade to the leak detection instrumentation (PDC 00-16) will address this problem.
4) Any future alarms do require actions, similar to what was done in this instance (validate alarm, increase monitoring, investigate equipment condition, etc.).

Based on this, I conclude all immediate corrective actions are in place or have been completed. This action item for Environmental (regarding regulatory issues) should be closed.