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| issue date = 11/26/1980
| issue date = 11/26/1980
| title = Interim Deficiency Rept Re Inadequacy of Sway Brace Brackets Mfg by Power Piping Co,Initially Reported on 800820.Caused by Undersized Welds & Poor Weld quality.In-plant Insp of Brackets Performed.Next Rept Is Scheduled for 810202
| title = Interim Deficiency Rept Re Inadequacy of Sway Brace Brackets Mfg by Power Piping Co,Initially Reported on 800820.Caused by Undersized Welds & Poor Weld quality.In-plant Insp of Brackets Performed.Next Rept Is Scheduled for 810202
| author name = MATLOCK R G
| author name = Matlock R
| author affiliation = WASHINGTON PUBLIC POWER SUPPLY SYSTEM
| author affiliation = WASHINGTON PUBLIC POWER SUPPLY SYSTEM
| addressee name = ENGELKEN R H
| addressee name = Engelken R
| addressee affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
| addressee affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
| docket = 05000397
| docket = 05000397
Line 16: Line 16:


=Text=
=Text=
{{#Wiki_filter:REGULATOR'NFORHATION DISTRIBUTIONi TEH (RIDS)ACCESSION NBR: 8012030728 DOC~DATE: 80/11/26 NOT'ARIZEOo NO DOCKKtl'ACIL:50-397 tirPPSS Nuclear Pr oject~Unit,.2i Nashington Public Powe 05000397 AUTH'AHE, AUTHOR AFFiILrIATION HATLOCKER.G..
{{#Wiki_filter:REGULATOR'NFORHATION DISTRIBUTIONi                         TEH     (RIDS)
AashingtonI Pub.lic Power Supply System REC'IP~NAHE.RKCTIP1IE(4'T~
ACCESSION NBR: 8012030728                 DOC   ~ DATE: 80/11/26       NOT'ARIZEOo NO tirPPSS   Nuclear     Pr oject~ Unit,. 2i Nashington Public               Powe 05000397 DOCKKtl'ACIL:50-397 AUTH'AHE,     HE        AUTHOR AFFiILrIATION HATLOCKER.G..             AashingtonI Pub.lic Power Supply System REC'IP ~ NAHE.           RKCTIP1IE(4'T~   AFFILIATION ENGELKENER ~       ,       Region     5E- San     Franc:iscor Office of the Directo.r                                 g rl
AFFILIATION ENGELKENER
~HE~, Region 5E-San Franc:iscor Office of the Directo.r g rl  


==SUBJECT:==
==SUBJECT:==
Interlim def i c1i ency rept re inadequacy of0 sway br ace brackets mfg b',y Power Piping Co,iinitially reported on 800820.Caused by undersized welds&poor weld quality,In~plant insp of brackets performed;Next rept is:-scheduled for 810202..DISTRIBUTION CODE': BO ISO COPIES RECEIVED:LITR L<ENCLI J SIZE'I TLE: Const r uc t i on De f i c i ency Repo r t (10CFR50,55KI)
Interlim def i c1i ency rept re inadequacy of0 sway br ace brackets mfg b',y Power Piping Co,iinitially reported on 800820.Caused by undersized welds & poor weld quality,In~plant insp of brackets performed;Next rept is:- scheduled for 810202..
NOTES:PH: 2 copies oif al,l mater:i el.05000397 REC'IP IENTi I D CODE'/N AHE i" ACTION: A/D LrICENSNGT 04 RUSHBROOKgH
DISTRIBUTION CODE': BO ISO COPIES RECEIVED:LITR L< ENCLI                         J   SIZE'I TLE: Const r uc t i on De f i c i ency Repo r t (10CFR50,55KI)
~, 06 INTERNALi:
NOTES:PH:     2 copies     oif   al,l mater:i   el.                                               05000397 REC'IP IENTi               COPIES                RECIPIENT              COPIES ID  CODE'/N AHE     i"     LlTTR ENCl            ID, CODE/NAHEl        LiTTR ENCl)
AD/RCI/IEi 1,7 ASLBP/Ju HARD KDO&STAFFr 19 HYD/GKOI BR.22 LiIC QUALI BR 12 NRC PDR 02.KV 13 EG FiII.E" 01, DKV 21 COPIES LlTTR ENCl 1.1 1 1 1 1 1 1 1 1 1.1 1"-1 1 1 l.1 1 1 1.RECIPIENT ID, CODE/NAHEl YOUNGBLOODrB'5 LiYNCHeD~07 AEOD 18 D/DIR HUii F'ACii 5 EQUIP QUALl BR1.1 I&EI 09 HP A.20 OELD'1 QA BR 14 RUTHERFORDErJ.
ACTION:     A/D LrICENSNGT 04               1.      1      YOUNGBLOODrB'5                        1 RUSHBROOKgH     ~ ,   06       1        1      LiYNCHeD ~      07                  1 INTERNALi: AD/RCI/IEi               1,7       1        1      AEOD            18              1  1 ASLBP/Ju HARD                   1        1      D/DIR HUii  F'ACii 5            1  1 KDO & STAFFr           19       1        1      EQUIP QUALl BR1.1                1  1 HYD/GKOI BR.           22       1.      1      I &EI          09                  1 LiIC QUALI BR NRC PDR KV 12 02.
IK COPIES LiTTR ENCl)1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 EXTERNALt:
13 1"-
ACRS NSIC'6 08 16 16 1: 1 LPDR.03 1 1 TOTALS NUHBER OFI COPiiKS RKQUIRED: LiTTR ENCLl 0 r ,1 I W wl Washington Public Power.Supply, System A JOINT OPERATING AG)PCY-P.O.BOX 966-'000 GEO.WASHINGTON WAY RICHLANO, WASHINGTON 99352 PHONE'I509I 372.5000 Docket.No.50.-39T November 26,.1980 G02-80-271'I Hr;.R'.H"Ehgelken:..
1 l.
Director" Nucl'ear, Regulatory Commission Regi'on V'uite, 202, Walnut Creek.Plaza 1900 N.Cal'ifornia.
1 1
Blvd.Wal nut Creek,.CA'.94596  
1 OELD'1 HP A.
QA BR 20 14 1
1 1
1 1
1 EG FiII.E"            01,      1       1     RUTHERFORDErJ. IK              1   1 DKV 21            1.
NSIC'6 EXTERNALt: ACRS 08 16 1:
16 1
LPDR.           03               1   1 TOTALS NUHBER OFI COPiiKS RKQUIRED: LiTTR                           ENCLl
 
r 0
,1 I W
 
wl Washington Public Power. Supply, System A JOINT OPERATING AG)PCY-P.O. BOX 966-'000 GEO. WASHINGTON WAY   RICHLANO, WASHINGTON 99352   PHONE'I509I 372.5000 Docket. No. 50.-39T                                       November 26,. 1980 G02-80-271'I Hr;. R'. H "Ehgelken:.. Director" Nucl'ear, Regulatory Commission Regi'on 202, Walnut Creek. Plaza V'uite, 1900 N.           Cal'ifornia. Blvd.
Wal nut Creek,. CA'.             94596


==Subject:==
==Subject:==
.WPPSS NUCLEAR'ROJECT'O..
.           WPPSS   NUCLEAR'ROJECT'O.. 2 DOCKET'O.. 50-39T, CPPR-93 REPORTABLE DEFICIENCY - 10CFR50.55 e
2 DOCKET'O..
50-39T, CPPR-93 REPORTABLE DEFICIENCY
-10CFR50.55 e  


==Reference:==
==Reference:==
(a).Telecon.(A2-80-309 dated 8/20/80,  
(a). Telecon   .(A2-80-309 dated 8/20/80,


==Subject:==
==Subject:==
Notification:
Notification: of Reportable- 10CFR50.55(e)
of Reportable-10CFR50.55(e)(b): G02-80-'08.'ated-9/19/80,  
(b): G02-80-'08.'ated- 9/19/80,


==Subject:==
==Subject:==
.Reportabl'e Deficiency
. Reportabl'e Deficiency                   'I
'I
 
==Dear Hr. Engelken:==
 
In accordance. with the, provisions of 10CFR50.55(e), your staff was informed. by references (a) and. (b) of a, reportable deficiency relative to.- sway brace brackets.
Attached is our follow-up report which provides the status                        of the program initiated to resolve this deficiency.
A final report will be- submitted, when- the                program      is completed'nd evaluated.
II
  ~H                      UJ Vv)      P),
                      <oe gI
    &4J


==Dear Hr.Engelken:==
t 0
In accordance.
    ~
with the, provisions of lOCFR50.55(e), your staff was informed.by references (a)and.(b)of a, reportable deficiency relative to.-sway brace brackets.Attached is our follow-up report which provides the status of the program initiated to resolve this deficiency.
t
A final report will be-submitted, when-the program is completed'nd evaluated.
 
II~H&4J Vv)P), UJ<oe gI 0~t t Please: contact us if you have.additional questions..
Please: contact us     if you have. additional questions..
Very truly yours;RGM/RPS/im.
Very truly yours; R'. MATLOCK WNP-2. Pr ogram Director RGM/RPS/im.
Attachment cc: Mr.JR'ewi's'Pk,w/1.
I ~
Mr'..ND, Lewis,, EFSEC,,'Olympiat Mr.;.RE:: Snaith, B&R'w/1.~Mr:., V;.Stello,.NRC.w/1'r;RD Toth,, NRC.'w/,1 Mr;JJ'erderber., B&R" w/I.Mr;B..Wood, NVS;Corp.w/1 WNP-Z.Files I 4~e w/1 R'.MATLOCK WNP-2.Pr ogram Director
cc: Mr. JR'ewi's'Pk,w/1.                 e Mr'.. ND, Lewis,, EFSEC,,'Olympiat w/1 Mr.;. RE:: Snaith, B&R'w/1.
~Mr:., V;. Stello,. NRC. w/1'r; RD   Toth,, NRC.'w/,1 Mr; JJ'erderber., B&R" w/I.
Mr; B.. Wood, NVS;Corp. w/1 WNP-Z. Files


Attachment.
Attachment.
REPVPf'ABLE DEFICIENCY AND CORRECTIVF RPFION: Page.1 of'2 WPPSS NUCLEAR" PROJECT.'O':
REPVPf'ABLE DEFICIENCY AND CORRECTIVF RPFION:                                               Page. 1 of'2 WPPSS NUCLEAR" PROJECT.'O':
SWAY=BRACE BRACKET'S'S-1'42,.
SWAY= BRACE   BRACKET'S'S-1'42,. MANUFACTUREDt BY                                   POWER'. PIPING; CO;
MANUFACTUREDt BY POWER'.PIPING;CO;" P OR WELDMENT..UNDERSI D.ELDS.'LACK OF FUSION}'ASHINGTON PUBLIC POWER': SUPPLY SYSTEM'OCKET NO'.-50-'.397 LICENSE: NO.'-CPPR-93 Descri tion of.Deficienc It has:, been determined.
                                            " P OR WELDMENT ..
that;standardy weld'abricated beam attachments
UNDERSI   D. ELDS .'LACK OF FUSION}'ASHINGTON PUBLIC   POWER': SUPPLY NO'.- 50-'.397 SYSTEM'OCKET LICENSE: NO.'- CPPR-93 Descri tion of. Deficienc It has:, been determined. that; standardy weld'abricated beam attachments
'that are used in-rigid;sway..brace assemblies, were.supplied with welds smal'ler than the, sizes: required.by: ASME.SectionT II'I'DZV..
'that are used in- rigid; sway.. brace assemblies, were. supplied with welds smal'ler than the, sizes: required. by: ASME.SectionT II'I'DZV.. 1,, Mandatory Appendix AIIL'able::XIII.         1740:.1: (Mfnten.1073:Addhnda)...j These weldments~',
1,, Mandatory Appendix AIIL'able::XIII.-
were obseryedl tol:lieve. undersi'ted,. ftllet     wel'ds and. exhibitedpoor weld: qua1ity...
1740:.1: (Mfnten.1073:Addhnda)...j These weldments~', were obseryedl tol:lieve.
Using.ASME: Cbdei A'1:lowables, an. analysfs. has.determined'. that. a design'deficie'ncy exists. for'hese" brackets; when- loadsa ares appl-'ied; at: an: angle. greater than:15 off the. perpendicular.,
undersi'ted,.
Safet     Si ni fi'cance"                                                                                           t Failure. of these:     beam attachments-woul'd.render         the rigid sway. brace ineffec:
ftllet wel'ds and.exhibitedpoor weld: qua1ity...
tive   and: coul'd.result: in piping; system failure-. This woul'd adversely- affect the safe: operation of the-- plant: and: personnel'afety..
Using.ASME:
Corrective Acti'on-A':prel'iminary test: of. the- size.. 15 bracket. was: performed on October 24;1980.
Cbdei A'1:lowables, an.analysfs.has.determined'.
The;- primary purpose-of'hi's-.. test. was; to. verify- the- test apparatus- and. procedure.
that.a design'deficie'ncy exists.for'hese" brackets;when-loadsa ares appl-'ied; at: an: angle.greater than:15 off the.perpendicular., Safet Si ni fi'cance" t Failure.of these: beam attachments-woul'd.render the rigid sway.brace ineffec:-tive and: coul'd.result:
that will'e. used..in'-an overal'1.'. test programi to: demonstrate by proof load tests that the. brackets. are. adequate;- for the intended. service. During this. preliminary test" of'wenty. (20); size* 15;: brackets, 19.. of.- 20'.-satisfactorily passed. the proof load.'equirements of'F-3233;. Metal,l'ographic: examination- has. been performed on.
in piping;system failure-.This woul'd adversely-affect the safe: operation of the--plant: and: personnel'afety..
the welds of- randomly sel'ected- brackets of varying sizes. This evaluation con'-
Corrective Acti'on-A':prel'iminary test: of.the-size..15 bracket.was: performed on October 24;1980.The;-primary purpose-of'hi's-..
firmed'he existance'of undersized welds and also identified, various'eld.
test.was;to.verify-the-test apparatus-and.procedure.
defects (e.,g ''ack. oftfusion,, poor penetiati'on).,
that will'e.used..in'-an overal'1.'.
An   in-plant inspection     by qualified welding engineers. of all brackets was; in-itiated     on November 4,, 1980, and, is complete. as= of this date.                                     The intent of 'this inspection     was. to establish weld. sizes visual defect distribution, angular load position,. and to establish the basis for- selection of test samples.                                               Pre-liminary results indicate that undersize-weldments of generally poor weld quality exist.
test programi to: demonstrate by proof load tests that the.brackets.are.adequate;-
A test. program will be. initiated approximately December 12, 1980 to proof test representative samples in accordance with NF-3233. The process to select samples for the test program will be. determined by consideration of the following:
for the intended.service.During this.preliminary test" of'wenty.(20);size*15;: brackets, 19..of.-20'.-satisfactorily passed.the proof load.'equirements of'F-3233;.
a)   Selection by minimum size welds determined by field inspection. This selection for a statistical evaluation would be considered conservative-ly biased.
Metal,l'ographic:
 
examination-has.been performed on.the welds of-randomly sel'ected-brackets of varying sizes.This evaluation con'-firmed'he existance'of undersized welds and also identified, various'eld.
Docket Ho. 50-397                                                                     Page 2              of 2 GQ-80-271 b)   Selection. by visual inspection to. identify poor quality This selection for a." statistical evaluation would             of'eldments..
defects (e.,g''ack.oftfusion,, poor penetiati'on)., An in-plant inspection by qualified welding engineers.
be considered conservatively biased; The random. variable- in this selection process= wi'll be the fusion of the, weldments. and. its quality, which is not visible during inspection.                                       The sample. size will be-sufficient. to insure that. the brackets tested will be:
of all brackets was;in-itiated on November 4,, 1980, and, is complete.as=of this date.The intent of'this inspection was.to establish weld.sizes visual defect distribution, angular load position,.
representative of brackets of minimum quality. The design of the test fixture, due to a, predetermined; angular load,. will induce. a maximum stress condition in- the bracket weldment.         If any brackets fail to meet the oroof load, the results wilT be reported, in a statistical format with the possibility of the. following. actions:
and to establish the basis for-selection of test samples.Pre-liminary results indicate that undersize-weldments of generally poor weld quality exist.A test.program will be.initiated approximately December 12, 1980 to proof test representative samples in accordance with NF-3233.The process to select samples for the test program will be.determined by consideration of the following:
a)>> If'he.,results afithe.'est:     program indicate an rate~, the. brackets, even with. the undersize weld andi insignificant,'ailure.
a)Selection by minimum size welds determined by field inspection.
gerrera1lTy poor..weld! qual',ity,, wiTT be consideredl adequate for                             their intendedi senvice~.
This selection for a statistical evaluation would be considered conservative-ly biased.
b)   If- the results. of'he test program indicate- a significant failure rate a: new derated'oad capacity will be used Oerating may be applied to the load. rating or by limiting'he angle at which the load is- applied..
Docket Ho.50-397 GQ-80-271-2-Page 2 of 2 b)Selection.
c)   When a   support. is defined to be deficient in accordance with the test   derated. capacity,, the bracket will be repaired or replaced.
by visual inspection to.identify poor quality of'eldments..
A final   report. or an interim report will be; provided by february 2, 1981.}}
This selection for a." statistical evaluation would be considered conservatively biased;The random.variable-in this selection process=wi'll be the fusion of the, weldments.
and.its quality, which is not visible during inspection.
The sample.size will be-sufficient.
to insure that.the brackets tested will be: representative of brackets of minimum quality.The design of the test fixture, due to a, predetermined; angular load,.will induce.a maximum stress condition in-the bracket weldment.If any brackets fail to meet the oroof load, the results wilT be reported, in a statistical format with the possibility of the.following.
actions: a)>>If'he.,results afithe.'est:
program indicate an insignificant,'ailure.
rate~, the.brackets, even with.the undersize weld andi gerrera1lTy poor..weld!
qual',ity,, wiTT be consideredl adequate for their intendedi senvice~.b)If-the results.of'he test program indicate-a significant failure rate a: new derated'oad capacity will be used Oerating may be applied to the load.rating or by limiting'he angle at which the load is-applied..c)When a support.is defined to be deficient in accordance with the test derated.capacity,, the bracket will be repaired or replaced.A final report.or an interim report will be;provided by february 2, 1981.}}

Latest revision as of 07:41, 16 November 2019

Interim Deficiency Rept Re Inadequacy of Sway Brace Brackets Mfg by Power Piping Co,Initially Reported on 800820.Caused by Undersized Welds & Poor Weld quality.In-plant Insp of Brackets Performed.Next Rept Is Scheduled for 810202
ML17275A720
Person / Time
Site: Columbia Energy Northwest icon.png
Issue date: 11/26/1980
From: Matlock R
WASHINGTON PUBLIC POWER SUPPLY SYSTEM
To: Engelken R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
References
10CFR-050.55E, 10CFR-50.55E, G2-80-271, GO2-80-271, NUDOCS 8012030728
Download: ML17275A720 (8)


Text

REGULATOR'NFORHATION DISTRIBUTIONi TEH (RIDS)

ACCESSION NBR: 8012030728 DOC ~ DATE: 80/11/26 NOT'ARIZEOo NO tirPPSS Nuclear Pr oject~ Unit,. 2i Nashington Public Powe 05000397 DOCKKtl'ACIL:50-397 AUTH'AHE, HE AUTHOR AFFiILrIATION HATLOCKER.G.. AashingtonI Pub.lic Power Supply System REC'IP ~ NAHE. RKCTIP1IE(4'T~ AFFILIATION ENGELKENER ~ , Region 5E- San Franc:iscor Office of the Directo.r g rl

SUBJECT:

Interlim def i c1i ency rept re inadequacy of0 sway br ace brackets mfg b',y Power Piping Co,iinitially reported on 800820.Caused by undersized welds & poor weld quality,In~plant insp of brackets performed;Next rept is:- scheduled for 810202..

DISTRIBUTION CODE': BO ISO COPIES RECEIVED:LITR L< ENCLI J SIZE'I TLE: Const r uc t i on De f i c i ency Repo r t (10CFR50,55KI)

NOTES:PH: 2 copies oif al,l mater:i el. 05000397 REC'IP IENTi COPIES RECIPIENT COPIES ID CODE'/N AHE i" LlTTR ENCl ID, CODE/NAHEl LiTTR ENCl)

ACTION: A/D LrICENSNGT 04 1. 1 YOUNGBLOODrB'5 1 RUSHBROOKgH ~ , 06 1 1 LiYNCHeD ~ 07 1 INTERNALi: AD/RCI/IEi 1,7 1 1 AEOD 18 1 1 ASLBP/Ju HARD 1 1 D/DIR HUii F'ACii 5 1 1 KDO & STAFFr 19 1 1 EQUIP QUALl BR1.1 1 1 HYD/GKOI BR. 22 1. 1 I &EI 09 1 LiIC QUALI BR NRC PDR KV 12 02.

13 1"-

1 l.

1 1

1 OELD'1 HP A.

QA BR 20 14 1

1 1

1 1

1 EG FiII.E" 01, 1 1 RUTHERFORDErJ. IK 1 1 DKV 21 1.

NSIC'6 EXTERNALt: ACRS 08 16 1:

16 1

LPDR. 03 1 1 TOTALS NUHBER OFI COPiiKS RKQUIRED: LiTTR ENCLl

r 0

,1 I W

wl Washington Public Power. Supply, System A JOINT OPERATING AG)PCY-P.O. BOX 966-'000 GEO. WASHINGTON WAY RICHLANO, WASHINGTON 99352 PHONE'I509I 372.5000 Docket. No. 50.-39T November 26,. 1980 G02-80-271'I Hr;. R'. H "Ehgelken:.. Director" Nucl'ear, Regulatory Commission Regi'on 202, Walnut Creek. Plaza V'uite, 1900 N. Cal'ifornia. Blvd.

Wal nut Creek,. CA'. 94596

Subject:

. WPPSS NUCLEAR'ROJECT'O.. 2 DOCKET'O..50-39T, CPPR-93 REPORTABLE DEFICIENCY - 10CFR50.55 e

Reference:

(a). Telecon .(A2-80-309 dated 8/20/80,

Subject:

Notification: of Reportable- 10CFR50.55(e)

(b): G02-80-'08.'ated- 9/19/80,

Subject:

. Reportabl'e Deficiency 'I

Dear Hr. Engelken:

In accordance. with the, provisions of 10CFR50.55(e), your staff was informed. by references (a) and. (b) of a, reportable deficiency relative to.- sway brace brackets.

Attached is our follow-up report which provides the status of the program initiated to resolve this deficiency.

A final report will be- submitted, when- the program is completed'nd evaluated.

II

~H UJ Vv) P),

<oe gI

&4J

t 0

~

t

Please: contact us if you have. additional questions..

Very truly yours; R'. MATLOCK WNP-2. Pr ogram Director RGM/RPS/im.

I ~

cc: Mr. JR'ewi's'Pk,w/1. e Mr'.. ND, Lewis,, EFSEC,,'Olympiat w/1 Mr.;. RE:: Snaith, B&R'w/1.

~Mr:., V;. Stello,. NRC. w/1'r; RD Toth,, NRC.'w/,1 Mr; JJ'erderber., B&R" w/I.

Mr; B.. Wood, NVS;Corp. w/1 WNP-Z. Files

Attachment.

REPVPf'ABLE DEFICIENCY AND CORRECTIVF RPFION: Page. 1 of'2 WPPSS NUCLEAR" PROJECT.'O':

SWAY= BRACE BRACKET'S'S-1'42,. MANUFACTUREDt BY POWER'. PIPING; CO;

" P OR WELDMENT ..

UNDERSI D. ELDS .'LACK OF FUSION}'ASHINGTON PUBLIC POWER': SUPPLY NO'.- 50-'.397 SYSTEM'OCKET LICENSE: NO.'- CPPR-93 Descri tion of. Deficienc It has:, been determined. that; standardy weld'abricated beam attachments

'that are used in- rigid; sway.. brace assemblies, were. supplied with welds smal'ler than the, sizes: required. by: ASME.SectionT II'I'DZV.. 1,, Mandatory Appendix AIIL'able::XIII. 1740:.1: (Mfnten.1073:Addhnda)...j These weldments~',

were obseryedl tol:lieve. undersi'ted,. ftllet wel'ds and. exhibitedpoor weld: qua1ity...

Using.ASME: Cbdei A'1:lowables, an. analysfs. has.determined'. that. a design'deficie'ncy exists. for'hese" brackets; when- loadsa ares appl-'ied; at: an: angle. greater than:15 off the. perpendicular.,

Safet Si ni fi'cance" t Failure. of these: beam attachments-woul'd.render the rigid sway. brace ineffec:

tive and: coul'd.result: in piping; system failure-. This woul'd adversely- affect the safe: operation of the-- plant: and: personnel'afety..

Corrective Acti'on-A':prel'iminary test: of. the- size.. 15 bracket. was: performed on October 24;1980.

The;- primary purpose-of'hi's-.. test. was; to. verify- the- test apparatus- and. procedure.

that will'e. used..in'-an overal'1.'. test programi to: demonstrate by proof load tests that the. brackets. are. adequate;- for the intended. service. During this. preliminary test" of'wenty. (20); size* 15;: brackets, 19.. of.- 20'.-satisfactorily passed. the proof load.'equirements of'F-3233;. Metal,l'ographic: examination- has. been performed on.

the welds of- randomly sel'ected- brackets of varying sizes. This evaluation con'-

firmed'he existance'of undersized welds and also identified, various'eld.

defects (e.,g ack. oftfusion,, poor penetiati'on).,

An in-plant inspection by qualified welding engineers. of all brackets was; in-itiated on November 4,, 1980, and, is complete. as= of this date. The intent of 'this inspection was. to establish weld. sizes visual defect distribution, angular load position,. and to establish the basis for- selection of test samples. Pre-liminary results indicate that undersize-weldments of generally poor weld quality exist.

A test. program will be. initiated approximately December 12, 1980 to proof test representative samples in accordance with NF-3233. The process to select samples for the test program will be. determined by consideration of the following:

a) Selection by minimum size welds determined by field inspection. This selection for a statistical evaluation would be considered conservative-ly biased.

Docket Ho. 50-397 Page 2 of 2 GQ-80-271 b) Selection. by visual inspection to. identify poor quality This selection for a." statistical evaluation would of'eldments..

be considered conservatively biased; The random. variable- in this selection process= wi'll be the fusion of the, weldments. and. its quality, which is not visible during inspection. The sample. size will be-sufficient. to insure that. the brackets tested will be:

representative of brackets of minimum quality. The design of the test fixture, due to a, predetermined; angular load,. will induce. a maximum stress condition in- the bracket weldment. If any brackets fail to meet the oroof load, the results wilT be reported, in a statistical format with the possibility of the. following. actions:

a)>> If'he.,results afithe.'est: program indicate an rate~, the. brackets, even with. the undersize weld andi insignificant,'ailure.

gerrera1lTy poor..weld! qual',ity,, wiTT be consideredl adequate for their intendedi senvice~.

b) If- the results. of'he test program indicate- a significant failure rate a: new derated'oad capacity will be used Oerating may be applied to the load. rating or by limiting'he angle at which the load is- applied..

c) When a support. is defined to be deficient in accordance with the test derated. capacity,, the bracket will be repaired or replaced.

A final report. or an interim report will be; provided by february 2, 1981.