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| issue date = 11/26/1980 | | issue date = 11/26/1980 | ||
| title = Interim Deficiency Rept Re Inadequacy of Sway Brace Brackets Mfg by Power Piping Co,Initially Reported on 800820.Caused by Undersized Welds & Poor Weld quality.In-plant Insp of Brackets Performed.Next Rept Is Scheduled for 810202 | | title = Interim Deficiency Rept Re Inadequacy of Sway Brace Brackets Mfg by Power Piping Co,Initially Reported on 800820.Caused by Undersized Welds & Poor Weld quality.In-plant Insp of Brackets Performed.Next Rept Is Scheduled for 810202 | ||
| author name = | | author name = Matlock R | ||
| author affiliation = WASHINGTON PUBLIC POWER SUPPLY SYSTEM | | author affiliation = WASHINGTON PUBLIC POWER SUPPLY SYSTEM | ||
| addressee name = | | addressee name = Engelken R | ||
| addressee affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V) | | addressee affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V) | ||
| docket = 05000397 | | docket = 05000397 | ||
Line 16: | Line 16: | ||
=Text= | =Text= | ||
{{#Wiki_filter:REGULATOR'NFORHATION DISTRIBUTIONi TEH (RIDS)ACCESSION NBR: 8012030728 DOC~DATE: 80/11/26 NOT'ARIZEOo NO | {{#Wiki_filter:REGULATOR'NFORHATION DISTRIBUTIONi TEH (RIDS) | ||
AashingtonI Pub.lic Power Supply System REC'IP~NAHE.RKCTIP1IE(4'T~ | ACCESSION NBR: 8012030728 DOC ~ DATE: 80/11/26 NOT'ARIZEOo NO tirPPSS Nuclear Pr oject~ Unit,. 2i Nashington Public Powe 05000397 DOCKKtl'ACIL:50-397 AUTH'AHE, HE AUTHOR AFFiILrIATION HATLOCKER.G.. AashingtonI Pub.lic Power Supply System REC'IP ~ NAHE. RKCTIP1IE(4'T~ AFFILIATION ENGELKENER ~ , Region 5E- San Franc:iscor Office of the Directo.r g rl | ||
AFFILIATION ENGELKENER | |||
==SUBJECT:== | ==SUBJECT:== | ||
Interlim def i c1i ency rept re inadequacy of0 sway br ace brackets mfg b',y Power Piping Co,iinitially reported on 800820.Caused by undersized welds&poor weld quality,In~plant insp of brackets performed;Next rept is:-scheduled for 810202..DISTRIBUTION CODE': BO ISO COPIES RECEIVED:LITR L<ENCLI J SIZE'I TLE: Const r uc t i on De f i c i ency Repo r t (10CFR50,55KI) | Interlim def i c1i ency rept re inadequacy of0 sway br ace brackets mfg b',y Power Piping Co,iinitially reported on 800820.Caused by undersized welds & poor weld quality,In~plant insp of brackets performed;Next rept is:- scheduled for 810202.. | ||
NOTES:PH: 2 copies oif al,l mater:i el.05000397 REC'IP IENTi | DISTRIBUTION CODE': BO ISO COPIES RECEIVED:LITR L< ENCLI J SIZE'I TLE: Const r uc t i on De f i c i ency Repo r t (10CFR50,55KI) | ||
~, 06 INTERNALi: | NOTES:PH: 2 copies oif al,l mater:i el. 05000397 REC'IP IENTi COPIES RECIPIENT COPIES ID CODE'/N AHE i" LlTTR ENCl ID, CODE/NAHEl LiTTR ENCl) | ||
AD/RCI/IEi 1,7 ASLBP/Ju HARD KDO&STAFFr 19 HYD/GKOI BR.22 LiIC QUALI BR | ACTION: A/D LrICENSNGT 04 1. 1 YOUNGBLOODrB'5 1 RUSHBROOKgH ~ , 06 1 1 LiYNCHeD ~ 07 1 INTERNALi: AD/RCI/IEi 1,7 1 1 AEOD 18 1 1 ASLBP/Ju HARD 1 1 D/DIR HUii F'ACii 5 1 1 KDO & STAFFr 19 1 1 EQUIP QUALl BR1.1 1 1 HYD/GKOI BR. 22 1. 1 I &EI 09 1 LiIC QUALI BR NRC PDR KV 12 02. | ||
13 1"- | |||
1 l. | |||
Director" Nucl'ear, Regulatory Commission Regi'on | 1 1 | ||
Blvd.Wal nut Creek,.CA'.94596 | 1 OELD'1 HP A. | ||
QA BR 20 14 1 | |||
1 1 | |||
1 1 | |||
1 EG FiII.E" 01, 1 1 RUTHERFORDErJ. IK 1 1 DKV 21 1. | |||
NSIC'6 EXTERNALt: ACRS 08 16 1: | |||
16 1 | |||
LPDR. 03 1 1 TOTALS NUHBER OFI COPiiKS RKQUIRED: LiTTR ENCLl | |||
r 0 | |||
,1 I W | |||
wl Washington Public Power. Supply, System A JOINT OPERATING AG)PCY-P.O. BOX 966-'000 GEO. WASHINGTON WAY RICHLANO, WASHINGTON 99352 PHONE'I509I 372.5000 Docket. No. 50.-39T November 26,. 1980 G02-80-271'I Hr;. R'. H "Ehgelken:.. Director" Nucl'ear, Regulatory Commission Regi'on 202, Walnut Creek. Plaza V'uite, 1900 N. Cal'ifornia. Blvd. | |||
Wal nut Creek,. CA'. 94596 | |||
==Subject:== | ==Subject:== | ||
.WPPSS NUCLEAR'ROJECT'O.. | . WPPSS NUCLEAR'ROJECT'O.. 2 DOCKET'O.. 50-39T, CPPR-93 REPORTABLE DEFICIENCY - 10CFR50.55 e | ||
2 DOCKET'O.. | |||
50-39T, CPPR-93 REPORTABLE DEFICIENCY | |||
-10CFR50.55 e | |||
==Reference:== | ==Reference:== | ||
(a). Telecon .(A2-80-309 dated 8/20/80, | |||
==Subject:== | ==Subject:== | ||
Notification: | Notification: of Reportable- 10CFR50.55(e) | ||
of Reportable-10CFR50.55(e)(b): G02-80-'08.'ated-9/19/80, | (b): G02-80-'08.'ated- 9/19/80, | ||
==Subject:== | ==Subject:== | ||
.Reportabl'e Deficiency | . Reportabl'e Deficiency 'I | ||
' | |||
==Dear Hr. Engelken:== | |||
In accordance. with the, provisions of 10CFR50.55(e), your staff was informed. by references (a) and. (b) of a, reportable deficiency relative to.- sway brace brackets. | |||
Attached is our follow-up report which provides the status of the program initiated to resolve this deficiency. | |||
A final report will be- submitted, when- the program is completed'nd evaluated. | |||
II | |||
~H UJ Vv) P), | |||
<oe gI | |||
&4J | |||
t 0 | |||
~ | |||
t | |||
Please: contact us if you have. additional questions.. | |||
Very truly yours;RGM/RPS/im. | Very truly yours; R'. MATLOCK WNP-2. Pr ogram Director RGM/RPS/im. | ||
I ~ | |||
Mr'..ND, Lewis,, EFSEC,,'Olympiat Mr.;.RE:: Snaith, B&R'w/1.~Mr:., V;.Stello,.NRC.w/1'r;RD Toth,, NRC.'w/,1 Mr;JJ'erderber., B&R" w/I.Mr;B..Wood, NVS;Corp.w/1 WNP-Z.Files | cc: Mr. JR'ewi's'Pk,w/1. e Mr'.. ND, Lewis,, EFSEC,,'Olympiat w/1 Mr.;. RE:: Snaith, B&R'w/1. | ||
~Mr:., V;. Stello,. NRC. w/1'r; RD Toth,, NRC.'w/,1 Mr; JJ'erderber., B&R" w/I. | |||
Mr; B.. Wood, NVS;Corp. w/1 WNP-Z. Files | |||
Attachment. | Attachment. | ||
REPVPf'ABLE DEFICIENCY AND CORRECTIVF RPFION: Page.1 of'2 WPPSS NUCLEAR" PROJECT.'O': | REPVPf'ABLE DEFICIENCY AND CORRECTIVF RPFION: Page. 1 of'2 WPPSS NUCLEAR" PROJECT.'O': | ||
SWAY=BRACE BRACKET'S'S-1'42,. | SWAY= BRACE BRACKET'S'S-1'42,. MANUFACTUREDt BY POWER'. PIPING; CO; | ||
MANUFACTUREDt BY POWER'.PIPING;CO;" P OR WELDMENT..UNDERSI D.ELDS.'LACK OF FUSION}'ASHINGTON PUBLIC POWER': SUPPLY | " P OR WELDMENT .. | ||
that;standardy weld'abricated beam attachments | UNDERSI D. ELDS .'LACK OF FUSION}'ASHINGTON PUBLIC POWER': SUPPLY NO'.- 50-'.397 SYSTEM'OCKET LICENSE: NO.'- CPPR-93 Descri tion of. Deficienc It has:, been determined. that; standardy weld'abricated beam attachments | ||
'that are used in-rigid;sway..brace assemblies, were.supplied with welds smal'ler than the, sizes: required.by: ASME.SectionT II'I'DZV.. | 'that are used in- rigid; sway.. brace assemblies, were. supplied with welds smal'ler than the, sizes: required. by: ASME.SectionT II'I'DZV.. 1,, Mandatory Appendix AIIL'able::XIII. 1740:.1: (Mfnten.1073:Addhnda)...j These weldments~', | ||
1,, Mandatory Appendix AIIL'able::XIII. | were obseryedl tol:lieve. undersi'ted,. ftllet wel'ds and. exhibitedpoor weld: qua1ity... | ||
1740:.1: (Mfnten.1073:Addhnda)...j These weldments~', were obseryedl tol:lieve. | Using.ASME: Cbdei A'1:lowables, an. analysfs. has.determined'. that. a design'deficie'ncy exists. for'hese" brackets; when- loadsa ares appl-'ied; at: an: angle. greater than:15 off the. perpendicular., | ||
undersi'ted,. | Safet Si ni fi'cance" t Failure. of these: beam attachments-woul'd.render the rigid sway. brace ineffec: | ||
ftllet wel'ds and.exhibitedpoor weld: qua1ity... | tive and: coul'd.result: in piping; system failure-. This woul'd adversely- affect the safe: operation of the-- plant: and: personnel'afety.. | ||
Using.ASME: | Corrective Acti'on-A':prel'iminary test: of. the- size.. 15 bracket. was: performed on October 24;1980. | ||
Cbdei A'1:lowables, an.analysfs.has.determined'. | The;- primary purpose-of'hi's-.. test. was; to. verify- the- test apparatus- and. procedure. | ||
that.a design'deficie'ncy exists.for'hese" brackets;when-loadsa ares appl-'ied; at: an: angle.greater than:15 off the.perpendicular., Safet Si ni fi'cance" t Failure.of these: beam attachments-woul'd.render the rigid sway.brace ineffec: | that will'e. used..in'-an overal'1.'. test programi to: demonstrate by proof load tests that the. brackets. are. adequate;- for the intended. service. During this. preliminary test" of'wenty. (20); size* 15;: brackets, 19.. of.- 20'.-satisfactorily passed. the proof load.'equirements of'F-3233;. Metal,l'ographic: examination- has. been performed on. | ||
in piping;system failure-.This woul'd adversely-affect the safe: operation of the--plant: and: personnel'afety.. | the welds of- randomly sel'ected- brackets of varying sizes. This evaluation con'- | ||
Corrective Acti'on-A':prel'iminary test: of.the-size..15 bracket.was: performed on October 24;1980.The;-primary purpose-of'hi's-.. | firmed'he existance'of undersized welds and also identified, various'eld. | ||
test.was;to.verify-the-test apparatus-and.procedure. | defects (e.,g ''ack. oftfusion,, poor penetiati'on)., | ||
that will'e.used..in'-an overal'1.'. | An in-plant inspection by qualified welding engineers. of all brackets was; in-itiated on November 4,, 1980, and, is complete. as= of this date. The intent of 'this inspection was. to establish weld. sizes visual defect distribution, angular load position,. and to establish the basis for- selection of test samples. Pre-liminary results indicate that undersize-weldments of generally poor weld quality exist. | ||
test programi to: demonstrate by proof load tests that the.brackets.are.adequate;- | A test. program will be. initiated approximately December 12, 1980 to proof test representative samples in accordance with NF-3233. The process to select samples for the test program will be. determined by consideration of the following: | ||
for the intended.service.During this.preliminary test" of'wenty.(20);size*15;: brackets, 19..of.-20'.-satisfactorily passed.the proof load.'equirements of'F-3233;. | a) Selection by minimum size welds determined by field inspection. This selection for a statistical evaluation would be considered conservative-ly biased. | ||
Metal,l'ographic: | |||
examination-has.been performed on.the welds of-randomly sel'ected-brackets of varying sizes.This evaluation con'-firmed'he existance'of undersized welds and also identified, various'eld. | Docket Ho. 50-397 Page 2 of 2 GQ-80-271 b) Selection. by visual inspection to. identify poor quality This selection for a." statistical evaluation would of'eldments.. | ||
defects (e.,g''ack.oftfusion,, poor penetiati'on)., An in-plant inspection by qualified welding engineers. | be considered conservatively biased; The random. variable- in this selection process= wi'll be the fusion of the, weldments. and. its quality, which is not visible during inspection. The sample. size will be-sufficient. to insure that. the brackets tested will be: | ||
of all brackets was;in-itiated on November 4,, 1980, and, is complete.as=of this date.The intent of'this inspection was.to establish weld.sizes visual defect distribution, angular load position,. | representative of brackets of minimum quality. The design of the test fixture, due to a, predetermined; angular load,. will induce. a maximum stress condition in- the bracket weldment. If any brackets fail to meet the oroof load, the results wilT be reported, in a statistical format with the possibility of the. following. actions: | ||
and to establish the basis for-selection of test samples.Pre-liminary results indicate that undersize-weldments of generally poor weld quality exist.A test.program will be.initiated approximately December 12, 1980 to proof test representative samples in accordance with NF-3233.The process to select samples for the test program will be.determined by consideration of the following: | a)>> If'he.,results afithe.'est: program indicate an rate~, the. brackets, even with. the undersize weld andi insignificant,'ailure. | ||
a)Selection by minimum size welds determined by field inspection. | gerrera1lTy poor..weld! qual',ity,, wiTT be consideredl adequate for their intendedi senvice~. | ||
This selection for a statistical evaluation would be considered conservative-ly biased. | b) If- the results. of'he test program indicate- a significant failure rate a: new derated'oad capacity will be used Oerating may be applied to the load. rating or by limiting'he angle at which the load is- applied.. | ||
Docket Ho.50-397 GQ-80-271 | c) When a support. is defined to be deficient in accordance with the test derated. capacity,, the bracket will be repaired or replaced. | ||
by visual inspection to.identify poor quality | A final report. or an interim report will be; provided by february 2, 1981.}} | ||
This selection for a." statistical evaluation would be considered conservatively biased;The random.variable-in this selection process=wi'll be the fusion of the, weldments. | |||
and.its quality, which is not visible during inspection. | |||
The sample.size will be-sufficient. | |||
to insure that.the brackets tested will be: representative of brackets of minimum quality.The design of the test fixture, due to a, predetermined; angular load,.will induce.a maximum stress condition in-the bracket weldment.If any brackets fail to meet the oroof load, the results wilT be reported, in a statistical format with the possibility of the.following. | |||
actions: a)>>If'he.,results afithe.'est: | |||
program indicate an | |||
rate~, the.brackets, even with.the undersize weld andi gerrera1lTy poor..weld! | |||
qual',ity,, wiTT be consideredl adequate for their intendedi senvice~.b)If-the results.of'he test program indicate-a significant failure rate a: new derated'oad capacity will be used Oerating may be applied to the load.rating or by limiting'he angle at which the load is-applied..c)When a support.is defined to be deficient in accordance with the test derated.capacity,, the bracket will be repaired or replaced.A final report.or an interim report will be;provided by february 2, 1981.}} |
Latest revision as of 07:41, 16 November 2019
ML17275A720 | |
Person / Time | |
---|---|
Site: | Columbia |
Issue date: | 11/26/1980 |
From: | Matlock R WASHINGTON PUBLIC POWER SUPPLY SYSTEM |
To: | Engelken R NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V) |
References | |
10CFR-050.55E, 10CFR-50.55E, G2-80-271, GO2-80-271, NUDOCS 8012030728 | |
Download: ML17275A720 (8) | |
Text
REGULATOR'NFORHATION DISTRIBUTIONi TEH (RIDS)
ACCESSION NBR: 8012030728 DOC ~ DATE: 80/11/26 NOT'ARIZEOo NO tirPPSS Nuclear Pr oject~ Unit,. 2i Nashington Public Powe 05000397 DOCKKtl'ACIL:50-397 AUTH'AHE, HE AUTHOR AFFiILrIATION HATLOCKER.G.. AashingtonI Pub.lic Power Supply System REC'IP ~ NAHE. RKCTIP1IE(4'T~ AFFILIATION ENGELKENER ~ , Region 5E- San Franc:iscor Office of the Directo.r g rl
SUBJECT:
Interlim def i c1i ency rept re inadequacy of0 sway br ace brackets mfg b',y Power Piping Co,iinitially reported on 800820.Caused by undersized welds & poor weld quality,In~plant insp of brackets performed;Next rept is:- scheduled for 810202..
DISTRIBUTION CODE': BO ISO COPIES RECEIVED:LITR L< ENCLI J SIZE'I TLE: Const r uc t i on De f i c i ency Repo r t (10CFR50,55KI)
NOTES:PH: 2 copies oif al,l mater:i el. 05000397 REC'IP IENTi COPIES RECIPIENT COPIES ID CODE'/N AHE i" LlTTR ENCl ID, CODE/NAHEl LiTTR ENCl)
ACTION: A/D LrICENSNGT 04 1. 1 YOUNGBLOODrB'5 1 RUSHBROOKgH ~ , 06 1 1 LiYNCHeD ~ 07 1 INTERNALi: AD/RCI/IEi 1,7 1 1 AEOD 18 1 1 ASLBP/Ju HARD 1 1 D/DIR HUii F'ACii 5 1 1 KDO & STAFFr 19 1 1 EQUIP QUALl BR1.1 1 1 HYD/GKOI BR. 22 1. 1 I &EI 09 1 LiIC QUALI BR NRC PDR KV 12 02.
13 1"-
1 l.
1 1
1 OELD'1 HP A.
QA BR 20 14 1
1 1
1 1
1 EG FiII.E" 01, 1 1 RUTHERFORDErJ. IK 1 1 DKV 21 1.
NSIC'6 EXTERNALt: ACRS 08 16 1:
16 1
LPDR. 03 1 1 TOTALS NUHBER OFI COPiiKS RKQUIRED: LiTTR ENCLl
r 0
,1 I W
wl Washington Public Power. Supply, System A JOINT OPERATING AG)PCY-P.O. BOX 966-'000 GEO. WASHINGTON WAY RICHLANO, WASHINGTON 99352 PHONE'I509I 372.5000 Docket. No. 50.-39T November 26,. 1980 G02-80-271'I Hr;. R'. H "Ehgelken:.. Director" Nucl'ear, Regulatory Commission Regi'on 202, Walnut Creek. Plaza V'uite, 1900 N. Cal'ifornia. Blvd.
Wal nut Creek,. CA'. 94596
Subject:
. WPPSS NUCLEAR'ROJECT'O.. 2 DOCKET'O..50-39T, CPPR-93 REPORTABLE DEFICIENCY - 10CFR50.55 e
Reference:
(a). Telecon .(A2-80-309 dated 8/20/80,
Subject:
Notification: of Reportable- 10CFR50.55(e)
(b): G02-80-'08.'ated- 9/19/80,
Subject:
. Reportabl'e Deficiency 'I
Dear Hr. Engelken:
In accordance. with the, provisions of 10CFR50.55(e), your staff was informed. by references (a) and. (b) of a, reportable deficiency relative to.- sway brace brackets.
Attached is our follow-up report which provides the status of the program initiated to resolve this deficiency.
A final report will be- submitted, when- the program is completed'nd evaluated.
II
~H UJ Vv) P),
<oe gI
&4J
t 0
~
t
Please: contact us if you have. additional questions..
Very truly yours; R'. MATLOCK WNP-2. Pr ogram Director RGM/RPS/im.
I ~
cc: Mr. JR'ewi's'Pk,w/1. e Mr'.. ND, Lewis,, EFSEC,,'Olympiat w/1 Mr.;. RE:: Snaith, B&R'w/1.
~Mr:., V;. Stello,. NRC. w/1'r; RD Toth,, NRC.'w/,1 Mr; JJ'erderber., B&R" w/I.
Mr; B.. Wood, NVS;Corp. w/1 WNP-Z. Files
Attachment.
REPVPf'ABLE DEFICIENCY AND CORRECTIVF RPFION: Page. 1 of'2 WPPSS NUCLEAR" PROJECT.'O':
SWAY= BRACE BRACKET'S'S-1'42,. MANUFACTUREDt BY POWER'. PIPING; CO;
UNDERSI D. ELDS .'LACK OF FUSION}'ASHINGTON PUBLIC POWER': SUPPLY NO'.- 50-'.397 SYSTEM'OCKET LICENSE: NO.'- CPPR-93 Descri tion of. Deficienc It has:, been determined. that; standardy weld'abricated beam attachments
'that are used in- rigid; sway.. brace assemblies, were. supplied with welds smal'ler than the, sizes: required. by: ASME.SectionT II'I'DZV.. 1,, Mandatory Appendix AIIL'able::XIII. 1740:.1: (Mfnten.1073:Addhnda)...j These weldments~',
were obseryedl tol:lieve. undersi'ted,. ftllet wel'ds and. exhibitedpoor weld: qua1ity...
Using.ASME: Cbdei A'1:lowables, an. analysfs. has.determined'. that. a design'deficie'ncy exists. for'hese" brackets; when- loadsa ares appl-'ied; at: an: angle. greater than:15 off the. perpendicular.,
Safet Si ni fi'cance" t Failure. of these: beam attachments-woul'd.render the rigid sway. brace ineffec:
tive and: coul'd.result: in piping; system failure-. This woul'd adversely- affect the safe: operation of the-- plant: and: personnel'afety..
Corrective Acti'on-A':prel'iminary test: of. the- size.. 15 bracket. was: performed on October 24;1980.
The;- primary purpose-of'hi's-.. test. was; to. verify- the- test apparatus- and. procedure.
that will'e. used..in'-an overal'1.'. test programi to: demonstrate by proof load tests that the. brackets. are. adequate;- for the intended. service. During this. preliminary test" of'wenty. (20); size* 15;: brackets, 19.. of.- 20'.-satisfactorily passed. the proof load.'equirements of'F-3233;. Metal,l'ographic: examination- has. been performed on.
the welds of- randomly sel'ected- brackets of varying sizes. This evaluation con'-
firmed'he existance'of undersized welds and also identified, various'eld.
defects (e.,g ack. oftfusion,, poor penetiati'on).,
An in-plant inspection by qualified welding engineers. of all brackets was; in-itiated on November 4,, 1980, and, is complete. as= of this date. The intent of 'this inspection was. to establish weld. sizes visual defect distribution, angular load position,. and to establish the basis for- selection of test samples. Pre-liminary results indicate that undersize-weldments of generally poor weld quality exist.
A test. program will be. initiated approximately December 12, 1980 to proof test representative samples in accordance with NF-3233. The process to select samples for the test program will be. determined by consideration of the following:
a) Selection by minimum size welds determined by field inspection. This selection for a statistical evaluation would be considered conservative-ly biased.
Docket Ho. 50-397 Page 2 of 2 GQ-80-271 b) Selection. by visual inspection to. identify poor quality This selection for a." statistical evaluation would of'eldments..
be considered conservatively biased; The random. variable- in this selection process= wi'll be the fusion of the, weldments. and. its quality, which is not visible during inspection. The sample. size will be-sufficient. to insure that. the brackets tested will be:
representative of brackets of minimum quality. The design of the test fixture, due to a, predetermined; angular load,. will induce. a maximum stress condition in- the bracket weldment. If any brackets fail to meet the oroof load, the results wilT be reported, in a statistical format with the possibility of the. following. actions:
a)>> If'he.,results afithe.'est: program indicate an rate~, the. brackets, even with. the undersize weld andi insignificant,'ailure.
gerrera1lTy poor..weld! qual',ity,, wiTT be consideredl adequate for their intendedi senvice~.
b) If- the results. of'he test program indicate- a significant failure rate a: new derated'oad capacity will be used Oerating may be applied to the load. rating or by limiting'he angle at which the load is- applied..
c) When a support. is defined to be deficient in accordance with the test derated. capacity,, the bracket will be repaired or replaced.
A final report. or an interim report will be; provided by february 2, 1981.