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| number = ML17223A359 | | number = ML17223A359 | ||
| issue date = 10/16/1989 | | issue date = 10/16/1989 | ||
| title = NPDES Noncompliance Notification:On 890803 & 04, | | title = NPDES Noncompliance Notification:On 890803 & 04,plant Discharge Canal Temp Exceeded 113 F Limit.Unit 1 down- Powered to Clean Condenser Water Boxes | ||
| author name = | | author name = Sager D | ||
| author affiliation = FLORIDA POWER & LIGHT CO. | | author affiliation = FLORIDA POWER & LIGHT CO. | ||
| addressee name = | | addressee name = | ||
Line 13: | Line 13: | ||
| document type = NPDES NONCOMPLIANCE NOTIFICATION, TEXT-ENVIRONMENTAL REPORTS | | document type = NPDES NONCOMPLIANCE NOTIFICATION, TEXT-ENVIRONMENTAL REPORTS | ||
| page count = 7 | | page count = 7 | ||
}} | }} | ||
=Text= | |||
{{#Wiki_filter:ACCELERATED DI BUTION DEMONSTRATION SYSI'EM REGULAT INFORMATION DISTRIBUTION STEM (RIDS) | |||
ACCESSION NBR:8910240217 DOC.DATE: 89/10/16 NOTARIZED: NO DOCKET FACIL:50-335 St. Lucie Plant, Unit 1, Florida Power 6 Light Co. 05000335 AUTH. NAME AUTHOR AFFILIATION SAGER,D.A. Florida Power & Light Co. | |||
RECIP.NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk) | |||
==SUBJECT:== | |||
NPDES noncompliance notification:on 890803 6 04,plant discharge canal temp exceeded 113 F limit.Util down-powered. | |||
DISTRIBUTION CODE: IE25D COPIES RECEIVED:LTR ENCL SIZE: | |||
TITLE: Environmental Monitoring Rept (per Tech Specs) | |||
NOTES: | |||
RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME L'gTR ENCL .ID .CODE/NAME LTTR ENCL PD2-2 LA 3 3 PD2-2 PD 1 1 NORRISiJ, 1 ' h INTERNAL: ACRS 1 1 AEOD/DSP/TPAB 1 1 IRM TECH ADV 1 1 NRR ROTHMANgR 1 1 | |||
~REP RPB 10 2 2 NUDOCS-ABSTRACT 1 1 RE XT 01 1 1 RGN2 DRSS/RPB 1 1 LE 02 1 1 EXTERNAL EGSG S IMPSON i F 2 2 LPDR 1 1 NRC PDR 1 1 h | |||
TOTAL NUMBER OF COPIES REQUIRED: LTTR 19 ENCL 19 | |||
P.O. Box14000, Juno Beach, FL 33408-0420 oCTOBHR i6 19B9 L-89-368 U. S.'uclear Regulatory Commission Attn: Document Control Desk Washington, D. C. 20555 Gentlemen: | |||
Re: St. Lucie Unit 1 Docket No. 50-335 Environmental Protection Plan Report National Pollutant Dischar e Elimination S stem NPDES Re ortable Event In accordance with Section 3.2.1. of the St. Lucie Unit 1 Environmental Protection Plan, attached is a copy of the Discharge Monitoring Report (DMR) required by the St. Lucie Plant NPDES Permit with respect to a reportable event. Additionally, a description of the event is provided. | |||
Very truly yours, | |||
<ad D. A. ger Vice sident St. Lucie Plant DAS/MSD/gp Attachments cc: Stewart D. Ebneter, Regional Administrator, Region Senior Resident Inspector, USNRC, St. Lucie Plant II, USNRC I | |||
se>02O02>7 S9iOib PDR ADOCK 05000335'q g PNu an FPL Group company | |||
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PERMITTEE NAMEIADDRESS llnklnch NATIONALPOLLUTANTDISCHARGE ELIMINATIONSYSTF M (NPDES J Form Apptovrd NAME ADDREss Q ~t~rl | |||
~~tati lre~i~t | |||
~~~ | |||
Fnrirlrie lenrkk/Lorn rion ffdjffkrknrl | |||
- ~ol e A+I-A+I?S L!L n DISCHARGE MONITORING REPORT(DER) | |||
FL0002200 (2-)6J 001 | |||
((7-)9) 1 F FINAL CONU t; AUX COOLING 'yf'A~V~. | |||
ail ~eM PERMIT NUMBER DISCHARGE NUMBER t" ~cj.i FL, 334 0d MONITORING PERIOD FACILITY YEAR MO DAY Y 0 D Y LOCATION FROM y u v TO MAJOR (SU&i? JA) | |||
'TTN: To Ro FAIR (20.2!) (22-23J (2C-25) (26.27) (2(f-29) (3M(J NOTE: Read Instructions before completing this form. | |||
(3 Card OrtlTJ QUANTITYOR LOADING (C Crrrd Only) OUALITYOR CONCENTRATION PARAMETER (C6.53J (jdidlJ (3(f45) (Cd 53) (5C4) J NO. FREQUENCY SAMPLE EX OF TYPE (32-3T) ANALYSIS AVERAGE MAXIMUM UNITS MINIMUM AVERAGE MAXIMUM UNITS 6MB (dd J58J (69.Tft) | |||
TEMP ERATURL'-v>>A1 f-.t, SAMPLE Ar rrV AA ~ Y Phr~ | |||
A rA vv AA rvvv Yv r | |||
~L( FAH,'? Eidlii. 1 1 MEASUREMENT ./( Hc | |||
'30011 1 0 0 PERMIT OOPVVA VtpffteXhtv r'ip p rpv REQUIREMENT AJ INST,HX DEAF UENT GR(ISu VALUE. | |||
I LHP ~ DIFF ~ ULI I(ELif AA YY AA 'Y A YV vvh h AA v rv AA | |||
'P YYYV'PA 4 SAMPLE | |||
~AN o t UP iT ILf'i UE-- ~ f- MEASUREMENT uoV13 1 ) 0 PERMIT 4 P'Ir L FF ULeN1 dict)SS V ALUI. | |||
REQUIREMENT AAAA vvv r INST'X DLGoF 3I?ON TIJTAI r YAAAA AA rv.r 'PPVP hAAJ AAAAAA vvvv rff 9 SAMPLE ~ ~ e (AS: ) MEASUREMENT JttetA J y A A h | |||
..I 1022 2 4 PERMIT ~ 0 | |||
' Ar Ni I V.nL Jtr REQUIREMENT Vh 'rff INST, MX HG/L BATCH VX IL',EINTS s TOTAL YVVAA AA YVV 4A A A A Jr AAAA Yvv rvff vfr A Ar SAMPLE | |||
.Ai=SIDUAL MEASUREMENT | |||
<, o Q 1A.OM 94044 P 0 PERMIT VV Per P P YC POOha 0~ 3 REQUIREMENT J'Y V' 4 A V INST'HX XG/L UOUS U)CIDENlst Tt)TAL SAMPLE 4 AJ A lf 'pep hA e ff h AAA ~ AAAA YVAV P JP'P A AAVfftAA p per4 ftt.SI DUAL MEASUREMENl'ERMIT I4t)44 Q 0 0 AA ff AAA VVY er ~ vrr AA qietrh JeA A Onl Ol IN 0 0 I 'i ~ | |||
REQUIREMENT ArvvAA Y INST MX . HG/L VOUS OX10ENTSv FRE'- SAMPLE r 4AAA p erff ~ | |||
AAAA A VrVVeff A AAAv ff'vvv e s\VAI LAUL- MEASUREMENT ,o% | |||
34045 I? 0 0 PERMIT AAJIA vAAA AA p r "p lk' A AAA 0~2 Oe5; EEKL REQUIREMENT A lr YV Ie DAILY AV INST-(AX . XG/L 4A AAA VYMYVY vp A J AAA f3XI t)FI4TS v FRI:= | |||
AVAILAt)L~ | |||
SAMPLE MEASUREMEN'r J A JeAAA l p ~ N | |||
,p4 | |||
)4045 S 0 0 PERMIT ~ ff'ff P'P Y VVYffVh t V'AA ht II OY ~ P Oo2 Oe'5 EEKL REQUIREMENT rvv r DAILY AV INST HX HG/L NAMBTITLEPRINCIPALEXECUTIVEOFFICER TELEPHONE DATE I certify under penalty of law that this document and all attachments were prepared under my direction or supervision in accordance with system designed to assure that qualified personnel propedy gslher anda evafuate the information submitted. Based on my inquiry of the perSOn Or persons who manage the system. or those persons directly responsible for gathering the information, the Intorrnatfon submined Is. to the best ol SIGNA REOF PRINCIPAL CUTIVE knowledge and belief. true. sccursle.snd complete. I sm aware thai my TYPED OR PRINTED are signiticant penalilies lor submitting false information. includingthere the OFFICER OR AUTHORIZEDAGENT NUMBER YEAR Mo DAY possibility of fine and Imprisonment for knowing violations. | |||
COMMENT AND EXPLANATIONOF ANYVIOLATION: | |||
+ SE.V 4't'ItiCW~'L VCt c C-. | |||
AUXIL I Alv Y e 'i)ill)iliStth' UISCHA?Gt 9 H.=UN I f 1s S=UD IT 2 BORON HUNITORINb R'i='LJUIREO;v'HL:N I'ICTUS | |||
'Ail'i r | |||
Ik;)I-"Cti.'al.:.~ I'"t.i'-'"0 tr I FU, 44 'HATLf? S TUr? A ~ ~ r ISO NOi'f Ai RATEi) Iv AT<:I HULO I Nio TANK~ .p)r hr - t>ay $ g... rr EPA Form 3320.1 (Rev.10-79) PREvtous EDITloN Yo BEUsED IREPLACES EPA FORM T ao WHICH MAYNOT BE USED.) OF UNTILSUPPLY IS EXHAUSIED. | |||
01135/061409-045't PAGE 1 | |||
4 | |||
'V rQ | |||
DESCRIPTION OF THE EVENT The following is a description of an event which occurred at the St. Lucie Plant on August 3 and 4, 1989. This information was reported to Steve Scholfield of EPA by Ron Hix of FPL Environmental Affairs on August 7, 1989. Mr. Scholfield requested that this written report be submitted with the appropriate DMR. | |||
On the dates and times listed below, the St. Lucie Unit 1 discharge canal temperature exceeded the 113'F limit allowed for normal operation. | |||
Au ust 3 1989 Au ust 4 1989 Time ~Tem Time ~Tem 1300 hrs 114'F 1400 hrs 115'F 1400 114 1500 114 1500 114 1600 114 1600 115 1700 114 1700 115 1800 114 1900 115 During these periods, St. Lucie Unit 1 was experiencing severe condenser fouling. The St. Lucie Plant. NPDES Permit allows 117'F at the discharge terminus under these conditions. Unit 1 was down-powered the evenings of August 4, 1989 and August 5, 1989 to clean condenser water-boxes. Since that time discharge canal temperatures have returned to below 113'F. | |||
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Latest revision as of 21:56, 29 October 2019
ML17223A359 | |
Person / Time | |
---|---|
Site: | Saint Lucie |
Issue date: | 10/16/1989 |
From: | Sager D FLORIDA POWER & LIGHT CO. |
To: | NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM) |
References | |
L-89-368, NUDOCS 8910240217 | |
Download: ML17223A359 (7) | |
Text
ACCELERATED DI BUTION DEMONSTRATION SYSI'EM REGULAT INFORMATION DISTRIBUTION STEM (RIDS)
ACCESSION NBR:8910240217 DOC.DATE: 89/10/16 NOTARIZED: NO DOCKET FACIL:50-335 St. Lucie Plant, Unit 1, Florida Power 6 Light Co. 05000335 AUTH. NAME AUTHOR AFFILIATION SAGER,D.A. Florida Power & Light Co.
RECIP.NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)
SUBJECT:
NPDES noncompliance notification:on 890803 6 04,plant discharge canal temp exceeded 113 F limit.Util down-powered.
DISTRIBUTION CODE: IE25D COPIES RECEIVED:LTR ENCL SIZE:
TITLE: Environmental Monitoring Rept (per Tech Specs)
NOTES:
RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME L'gTR ENCL .ID .CODE/NAME LTTR ENCL PD2-2 LA 3 3 PD2-2 PD 1 1 NORRISiJ, 1 ' h INTERNAL: ACRS 1 1 AEOD/DSP/TPAB 1 1 IRM TECH ADV 1 1 NRR ROTHMANgR 1 1
~REP RPB 10 2 2 NUDOCS-ABSTRACT 1 1 RE XT 01 1 1 RGN2 DRSS/RPB 1 1 LE 02 1 1 EXTERNAL EGSG S IMPSON i F 2 2 LPDR 1 1 NRC PDR 1 1 h
TOTAL NUMBER OF COPIES REQUIRED: LTTR 19 ENCL 19
P.O. Box14000, Juno Beach, FL 33408-0420 oCTOBHR i6 19B9 L-89-368 U. S.'uclear Regulatory Commission Attn: Document Control Desk Washington, D. C. 20555 Gentlemen:
Re: St. Lucie Unit 1 Docket No. 50-335 Environmental Protection Plan Report National Pollutant Dischar e Elimination S stem NPDES Re ortable Event In accordance with Section 3.2.1. of the St. Lucie Unit 1 Environmental Protection Plan, attached is a copy of the Discharge Monitoring Report (DMR) required by the St. Lucie Plant NPDES Permit with respect to a reportable event. Additionally, a description of the event is provided.
Very truly yours,
<ad D. A. ger Vice sident St. Lucie Plant DAS/MSD/gp Attachments cc: Stewart D. Ebneter, Regional Administrator, Region Senior Resident Inspector, USNRC, St. Lucie Plant II, USNRC I
se>02O02>7 S9iOib PDR ADOCK 05000335'q g PNu an FPL Group company
f t
PERMITTEE NAMEIADDRESS llnklnch NATIONALPOLLUTANTDISCHARGE ELIMINATIONSYSTF M (NPDES J Form Apptovrd NAME ADDREss Q ~t~rl
~~tati lre~i~t
~~~
Fnrirlrie lenrkk/Lorn rion ffdjffkrknrl
- ~ol e A+I-A+I?S L!L n DISCHARGE MONITORING REPORT(DER)
FL0002200 (2-)6J 001
((7-)9) 1 F FINAL CONU t; AUX COOLING 'yf'A~V~.
ail ~eM PERMIT NUMBER DISCHARGE NUMBER t" ~cj.i FL, 334 0d MONITORING PERIOD FACILITY YEAR MO DAY Y 0 D Y LOCATION FROM y u v TO MAJOR (SU&i? JA)
'TTN: To Ro FAIR (20.2!) (22-23J (2C-25) (26.27) (2(f-29) (3M(J NOTE: Read Instructions before completing this form.
(3 Card OrtlTJ QUANTITYOR LOADING (C Crrrd Only) OUALITYOR CONCENTRATION PARAMETER (C6.53J (jdidlJ (3(f45) (Cd 53) (5C4) J NO. FREQUENCY SAMPLE EX OF TYPE (32-3T) ANALYSIS AVERAGE MAXIMUM UNITS MINIMUM AVERAGE MAXIMUM UNITS 6MB (dd J58J (69.Tft)
TEMP ERATURL'-v>>A1 f-.t, SAMPLE Ar rrV AA ~ Y Phr~
A rA vv AA rvvv Yv r
~L( FAH,'? Eidlii. 1 1 MEASUREMENT ./( Hc
'30011 1 0 0 PERMIT OOPVVA VtpffteXhtv r'ip p rpv REQUIREMENT AJ INST,HX DEAF UENT GR(ISu VALUE.
I LHP ~ DIFF ~ ULI I(ELif AA YY AA 'Y A YV vvh h AA v rv AA
'P YYYV'PA 4 SAMPLE
~AN o t UP iT ILf'i UE-- ~ f- MEASUREMENT uoV13 1 ) 0 PERMIT 4 P'Ir L FF ULeN1 dict)SS V ALUI.
REQUIREMENT AAAA vvv r INST'X DLGoF 3I?ON TIJTAI r YAAAA AA rv.r 'PPVP hAAJ AAAAAA vvvv rff 9 SAMPLE ~ ~ e (AS: ) MEASUREMENT JttetA J y A A h
..I 1022 2 4 PERMIT ~ 0
' Ar Ni I V.nL Jtr REQUIREMENT Vh 'rff INST, MX HG/L BATCH VX IL',EINTS s TOTAL YVVAA AA YVV 4A A A A Jr AAAA Yvv rvff vfr A Ar SAMPLE
.Ai=SIDUAL MEASUREMENT
<, o Q 1A.OM 94044 P 0 PERMIT VV Per P P YC POOha 0~ 3 REQUIREMENT J'Y V' 4 A V INST'HX XG/L UOUS U)CIDENlst Tt)TAL SAMPLE 4 AJ A lf 'pep hA e ff h AAA ~ AAAA YVAV P JP'P A AAVfftAA p per4 ftt.SI DUAL MEASUREMENl'ERMIT I4t)44 Q 0 0 AA ff AAA VVY er ~ vrr AA qietrh JeA A Onl Ol IN 0 0 I 'i ~
REQUIREMENT ArvvAA Y INST MX . HG/L VOUS OX10ENTSv FRE'- SAMPLE r 4AAA p erff ~
AAAA A VrVVeff A AAAv ff'vvv e s\VAI LAUL- MEASUREMENT ,o%
34045 I? 0 0 PERMIT AAJIA vAAA AA p r "p lk' A AAA 0~2 Oe5; EEKL REQUIREMENT A lr YV Ie DAILY AV INST-(AX . XG/L 4A AAA VYMYVY vp A J AAA f3XI t)FI4TS v FRI:=
AVAILAt)L~
SAMPLE MEASUREMEN'r J A JeAAA l p ~ N
,p4
)4045 S 0 0 PERMIT ~ ff'ff P'P Y VVYffVh t V'AA ht II OY ~ P Oo2 Oe'5 EEKL REQUIREMENT rvv r DAILY AV INST HX HG/L NAMBTITLEPRINCIPALEXECUTIVEOFFICER TELEPHONE DATE I certify under penalty of law that this document and all attachments were prepared under my direction or supervision in accordance with system designed to assure that qualified personnel propedy gslher anda evafuate the information submitted. Based on my inquiry of the perSOn Or persons who manage the system. or those persons directly responsible for gathering the information, the Intorrnatfon submined Is. to the best ol SIGNA REOF PRINCIPAL CUTIVE knowledge and belief. true. sccursle.snd complete. I sm aware thai my TYPED OR PRINTED are signiticant penalilies lor submitting false information. includingthere the OFFICER OR AUTHORIZEDAGENT NUMBER YEAR Mo DAY possibility of fine and Imprisonment for knowing violations.
COMMENT AND EXPLANATIONOF ANYVIOLATION:
+ SE.V 4't'ItiCW~'L VCt c C-.
AUXIL I Alv Y e 'i)ill)iliStth' UISCHA?Gt 9 H.=UN I f 1s S=UD IT 2 BORON HUNITORINb R'i='LJUIREO;v'HL:N I'ICTUS
'Ail'i r
Ik;)I-"Cti.'al.:.~ I'"t.i'-'"0 tr I FU, 44 'HATLf? S TUr? A ~ ~ r ISO NOi'f Ai RATEi) Iv AT<:I HULO I Nio TANK~ .p)r hr - t>ay $ g... rr EPA Form 3320.1 (Rev.10-79) PREvtous EDITloN Yo BEUsED IREPLACES EPA FORM T ao WHICH MAYNOT BE USED.) OF UNTILSUPPLY IS EXHAUSIED.
01135/061409-045't PAGE 1
4
'V rQ
DESCRIPTION OF THE EVENT The following is a description of an event which occurred at the St. Lucie Plant on August 3 and 4, 1989. This information was reported to Steve Scholfield of EPA by Ron Hix of FPL Environmental Affairs on August 7, 1989. Mr. Scholfield requested that this written report be submitted with the appropriate DMR.
On the dates and times listed below, the St. Lucie Unit 1 discharge canal temperature exceeded the 113'F limit allowed for normal operation.
Au ust 3 1989 Au ust 4 1989 Time ~Tem Time ~Tem 1300 hrs 114'F 1400 hrs 115'F 1400 114 1500 114 1500 114 1600 114 1600 115 1700 114 1700 115 1800 114 1900 115 During these periods, St. Lucie Unit 1 was experiencing severe condenser fouling. The St. Lucie Plant. NPDES Permit allows 117'F at the discharge terminus under these conditions. Unit 1 was down-powered the evenings of August 4, 1989 and August 5, 1989 to clean condenser water-boxes. Since that time discharge canal temperatures have returned to below 113'F.
I t
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