IR 05000336/2006003: Difference between revisions

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| issue date = 07/28/2006
| issue date = 07/28/2006
| title = IR 05000336-06-003, 05000423-06-003; on 04/01/2006 - 06/30/2006; Millstone, Units 2 and Unit 3; Equipment Alignment, Operability Evaluations, Event Followup
| title = IR 05000336-06-003, 05000423-06-003; on 04/01/2006 - 06/30/2006; Millstone, Units 2 and Unit 3; Equipment Alignment, Operability Evaluations, Event Followup
| author name = Krohn P G
| author name = Krohn P
| author affiliation = NRC/RGN-I/DRP/PB6
| author affiliation = NRC/RGN-I/DRP/PB6
| addressee name = Christian D A
| addressee name = Christian D
| addressee affiliation = Dominion Resources, Inc
| addressee affiliation = Dominion Resources, Inc
| docket = 05000336, 05000423
| docket = 05000336, 05000423
| license number = DPR-065, NPF-049
| license number = DPR-065, NPF-049
| contact person = Krohn P G, RI/DRP/PB6/610-337-5120
| contact person = Krohn P, RI/DRP/PB6/610-337-5120
| document report number = IR-06-003
| document report number = IR-06-003
| document type = Inspection Report, Letter
| document type = Inspection Report, Letter
Line 18: Line 18:


=Text=
=Text=
{{#Wiki_filter:
{{#Wiki_filter:July 28, 2006Mr. David A. ChristianSr. Vice President and Chief Nuclear Officer Dominion Resources 5000 Dominion Boulevard Glenn Allen, VA 23060-6711SUBJECT:MILLSTONE POWER STATION - NRC INTEGRATED INSPECTIONREPORT 05000336/2006003 AND 05000423/2006003
[[Issue date::July 28, 2006]]
 
Mr. David A. ChristianSr. Vice President and Chief Nuclear Officer Dominion Resources 5000 Dominion Boulevard Glenn Allen, VA 23060-6711
 
SUBJECT: MILLSTONE POWER STATION - NRC INTEGRATED INSPECTIONREPORT 05000336/2006003 AND 05000423/2006003


==Dear Mr. Christian:==
==Dear Mr. Christian:==
On June 30, 2006, the US Nuclear Regulatory Commission (NRC) completed an inspection atyour Millstone Power Station Unit 2 and Unit 3. The enclosed inspection report documents theinspection results, which were discussed on July 11, 2006, with Mr. A. Skip Jordan and other members of your staff.The inspection examined activities conducted under your license as they relate to safety andcompliance with the Commission's rules and regulations and with the conditions of your license.
On June 30, 2006, the US Nuclear Regulatory Commission (NRC) completed an inspection atyour Millstone Power Station Unit 2 and Unit 3. The enclosed inspection report documents theinspection results, which were discussed on July 11, 2006, with Mr. A. Skip Jordan and other members of your staff.The inspection examined activities conducted under your license as they relate to safety andcompliance with the Commission's rules and regulations and with the conditions of your license.


The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.This report documents three NRC-identified findings of very low safety significance (Green). Two of these findings were determined to involve violations of NRC requirements. However,because of their very low safety significance and because are entered into your corrective action program, the NRC is treating these issues as non-cited violations (NCVs), in accordancewith Section VI.A.1 of the NRC's Enforcement Policy. If you contest any NCV in this report, youshould provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN.: Document Control Desk, Washington DC 20555-0001; with copies to the Regional Administrator, Region I; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-
The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.This report documents three NRC-identified findings of very low safety significance (Green). Two of these findings were determined to involve violations of NRC requirements. However,because of their very low safety significance and because are entered into your corrective action program, the NRC is treating these issues as non-cited violations (NCVs), in accordancewith Section VI.A.1 of the NRC's Enforcement Policy. If you contest any NCV in this report, youshould provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN.: Document Control Desk, Washington DC 20555-0001; with copies to the Regional Administrator, Region I; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at the Millstone Power Station.In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, itsenclosure, and your response (if any) will be available electronically for public inspection in theNRC Public Document Room or from the Publicly Available Records (PARS) com ponent ofNRC's document system (ADAMS). ADAMS is accessible from the NRC Website at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
0001; and the NRC Resident Inspector at the Millstone Power Station.In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, itsenclosure, and your response (if any) will be available electronically for public inspection in theNRC Public Document Room or from the Publicly Available Records (PARS) com ponent ofNRC's document system (ADAMS). ADAMS is accessible from the NRC Website at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
 
Sincerely,/RA/
Paul G. Krohn, ChiefReactor Projects Branch 6 Division of Reactor Projects Mr. D. A. Christian2Docket Nos.:50-336, 50-423License Nos.:DPR-65, NPF-49
 
===Enclosure:===
Inspection Report 05000336/2006003 and 05000423/2006003


===w/Attachment:===
Sincerely,
Supplemental Informationcc w/encl:J. A. Price, Site Vice President, Millstone StationC. L. Funderburk, Director, Nuclear Licensing and Operations Support D. W. Dodson, Supervisor, Station Licensing L. M. Cuoco, Senior Counsel C. Brinkman, Manager, Washington Nuclear Operations J. Roy, Director of Operations, Massachusetts Municipal Wholesale Electric Company First Selectmen, Town of Waterford B. Sheehan, Co-Chair, NEAC E. Woollacott, Co-Chair, NEAC E. Wilds, Director, State of Connecticut SLO Designee J. Buckingham, Department of Public Utility ControlG. Proios, Suffolk County Planning Dept.
/RA/
Paul G. Krohn, ChiefReactor Projects Branch 6 Division of Reactor Projects Mr. D. A. Christian2Docket Nos.:50-336, 50-423License Nos.:DPR-65, NPF-49Enclosure:Inspection Report 05000336/2006003 and 05000423/2006003w/Attachment: Supplemental Informationcc w/encl:J. A. Price, Site Vice President, Millstone StationC. L. Funderburk, Director, Nuclear Licensing and Operations Support D. W. Dodson, Supervisor, Station Licensing L. M. Cuoco, Senior Counsel C. Brinkman, Manager, Washington Nuclear Operations J. Roy, Director of Operations, Massachusetts Municipal Wholesale Electric Company First Selectmen, Town of Waterford B. Sheehan, Co-Chair, NEAC E. Woollacott, Co-Chair, NEAC E. Wilds, Director, State of Connecticut SLO Designee J. Buckingham, Department of Public Utility ControlG. Proios, Suffolk County Planning Dept.


R. Shadis, New England Coalition Staff G. Winslow, Citizens Regulatory Commission (CRC)S. Comley, We The People D. Katz, Citizens Awareness Network (CAN)
R. Shadis, New England Coalition Staff G. Winslow, Citizens Regulatory Commission (CRC)S. Comley, We The People D. Katz, Citizens Awareness Network (CAN)
Line 207: Line 196:
No findings of significance were identified.
No findings of significance were identified.


===Cornerstone:===
===Cornerstone: Emergency Preparedness [EP]1EP6Drill Evaluation (71114.06 - One Unit 2 Sample and One Unit 3 Sample)
Emergency Preparedness [EP]1EP6Drill Evaluation (71114.06 - One Unit 2 Sample and One Unit 3 Sample)


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors observed one sample of the conduct of Unit 2 licensed operatorsimulator training during a drill conducted on April 12, 2006, and one sample of theconduct of Unit 3 licensed operator simulator training on May 30, 2006. The inspectors evaluated the Operations crew activities related to evaluating the scenario and makingproper emergency action level classification determinations. Additionally, the inspectors 13Enclosureassessed the ability of Dominion's evaluators to adequately address operatorperformance deficiencies identified during the exercise. Documents reviewed during the inspection are listed in the Attachment.
The inspectors observed one sample of the conduct of Unit 2 licensed operatorsimulator training during a drill conducted on April 12, 2006, and one sample of theconduct of Unit 3 licensed operator simulator training on May 30, 2006. The inspectors===
 
evaluated the Operations crew activities related to evaluating the scenario and makingproper emergency action level classification determinations. Additionally, the inspectors 13Enclosureassessed the ability of Dominion's evaluators to adequately address operatorperformance deficiencies identified during the exercise. Documents reviewed during the inspection are listed in the Attachment.


====b. Findings====
====b. Findings====
Line 296: Line 286:
Opened and  
Opened and  
===Closed===
===Closed===
: [[Closes finding::05000423/FIN-2006003-01]]NCVDid Not Evaluate and Correct aSignificant Condition Adverse to
05000423/2006003-01NCVDid Not Evaluate and Correct aSignificant Condition Adverse to
: Quality Associated with Gravity Feed
Quality Associated with Gravity Feed
: Boration Lines (1R04)
Boration Lines (1R04)05000336/2006003-02FINDid Not Identify or Evaluate AirVoids Located in Auxiliary
: [[Closes finding::05000336/FIN-2006003-02]]FINDid Not Identify or Evaluate AirVoids Located in Auxiliary
Feedwater System (1R15.1)
: Feedwater System (1R15.1)
A-2Attachment05000423/2006003-03NCVDid Not Adequately Evaluate aReactor Protection System Setpoint
: A-2Attachment
Modification (4OA3.2)
: [[Closes finding::05000423/FIN-2006003-03]]NCVDid Not Adequately Evaluate aReactor Protection System Setpoint
: Modification (4OA3.2)
===Closed===
===Closed===
: [[Closes finding::05000423/FIN-2006003-01]]NCVDid Not Evaluate and Correct aSignificant Condition Adverse to
05000423/2005-004-00LERPressurizer Spray Nozzle WeldIndications (4OA3.1)05000423/2005-005-00, 01LERAutomatic Reactor Trip of MillstoneUnit 3 Due to Low-Low Steam
: Quality Associated with Gravity Feed
Generator Level (4OA3.2)
: Boration Lines (1R04)
: [[Closes finding::05000336/FIN-2006003-02]]FINDid Not Identify or Evaluate AirVoids Located in Auxiliary
: Feedwater System (1R15.1)
: A-2Attachment
: [[Closes finding::05000423/FIN-2006003-03]]NCVDid Not Adequately Evaluate aReactor Protection System Setpoint
: Modification (4OA3.2)
 
==LIST OF DOCUMENTS REVIEWED==
==LIST OF DOCUMENTS REVIEWED==
Section 1R01: Adverse Weather ProtectionAOP-2560, Revision 010-01, Storms, High Winds, and High TidesSP-2615, Revision 006-01, Flood Level Determination
Section 1R01: Adverse Weather ProtectionAOP-2560, Revision 010-01, Storms, High Winds, and High TidesSP-2615, Revision 006-01, Flood Level Determination
: C
: OP 200.6, Revision 002, Storms and Other Hazardous Phenomena
: MP-2721C, Revision 007-01, Protection and Restoration of Service Water Pump Motor Duringa Hurricane
==Section 1R04: Equipment Alignment==
: OP-2346A, Revision 026-04, "A" Emergency Diesel GeneratorDWG
: EM-104A, Revision 30, Chemical and Volume Control System
: DWG
: EM-104C, Revision 46, Chemical and Volume Control System
: CR-06-04511, Very Loud High Pitched Harmonic Coming from RBCCW Piping
: OP-2330A, Revision 023-00, RBCCW System
: DWG
: EM-133A, Revision 44, Service Water
: SP-3604C.8, Revision 000, Gravity Feed Boration Line Gas Accumulation Monitoring
: SP-3604C.8-001, Gravity Feed Boration Line Gas Volume Calculation for Mode 1, 2, and 3dated September 9, 2004, and April 17, 2006.CR-01-12135, Document and Track Closure of Recommendations Provided in TechnicalEvaluation M3-EV-98-0126 Revision 1, Gas Accumulation in Gravity Feed Boration PipingOP-3304A, Revision 029-07, Charging and Letdown
: MP-EV-98-0126, Revision 1, Technical Evaluation for Gas Accumulation in Gravity FeedBoration PipingReportability Determination for
: CR-06-03730, Found "B" Gravity Boration Line Essentially EmptyUnit 3 Final Safety Analysis Report Unit 3 Control Room Log
: CR-06-03730, Found "B" Gravity Boration Line Essentially Empty as Followup to CR-06-03712
: CR-04-08235, Train "A" Gravity Feed Boration Line Gas Accumulation Monitoring Surveillance 3604C.8 Failed
: A-3Attachment
==Section 1R05: ==
: Fire ProtectionMillstone Unit 2 Fire Hazards Analysis, Revision 9Millstone Unit 2 Individual Plant Examination of External EventsMillstone Unit 3 Fire Hazard Analysis Boundary Drawing, RevisionMillstone Unit 3 Fire Protection Evaluation Report, Revision 17.3Suppression Effects Analysis, January 1998
: Unit 2 Fire Fighting Strategy
: MP-PROG-OPS-SFP18, Revision 001-02, Establishing Ventilation for East West 480VAC125VDC Switchgear RoomCR-06-05029, Drumming Area and Railway Access Sprinkler Failed Design Function TestEPM Calc. No. 186, Revision 1, Combustible Loading Re-Analysis
==Section 1R06: Flood ProtectionMillstone Unit 2 Final Safety Analysis Report, Change 8 Millstone Unit 2 Internal Flooding Evaluation, Revision 0Millstone Unit 2 Individual Plant Examination of External EventsSuppression Effects Analysis, January 1998==
: SFP-17, Revision 002-00, Fire Penetration Seal and Barrier Inspections
: AOP-2559, Revision 007-04, Millstone Unit 2 FireUnit 2 Fire Fighting Strategy, Updated on July 15, 2002
==Section 1R11: ==
: Licensed Operator Requalification Program Lesson Plan C06306L, Operability Works heetsMP-26-EPI-FAP06-02, Revision 004-01, Millstone Unit 2 EAL TablesMP-26-EPI-FAP07-001, Revision 001-01, Incident Report Form Drill Exercise Sequence of Events, Revision 2, Dated April 12, 2006
==Section 1R12: Maintenance Effectiveness==
: CR-06-00243, Entered TSAS 3.0.3 for Loss of Second Facility of Charging PumpsCR-06-03350, 3RHS-HC607 Position Indicator did not Return to Original Position duringPortions of Valve StrokingMP-24-MR-FAP710, Revision 001, Maintenance Rule Functional Failure and Evaluations Maintenance Rule Functional Failure Evaluation Performed on 2/10/2006
==Section 1R13: Maintenance Risk Assessments and Emergent Work Control==
: MP-20-WM-FAP02.1, Revision 011, Conduct of On-Line MaintenanceMP-13-PRA-FAP01.1, Revision 001, Performing Risk Reviews
: CR-06-04628, Unit 3 SBO Diesel Alarms on SBO D/G Control Panel - Section 3
: SP-2619G, Revision 000-04, TS 3.8.1.b.4, One EDG Inoperable for Extended MaintenanceOutage Performed 0033, 5/15/2006AWO M2-05-09256, 2-CH-512 Freeze Seal Contingency Plan
: A-4AttachmentNRC Inspection Manual Part 9900 Technical Guidance, Mechanical Freeze PlugsControl Room and Maintenance Logs Unit 2 Work Week Schedule for 5/15/2006
==Section 1R14: Operator Performance During Non-Routine Evolutions and EventsCR-06-06124, Unplanned==
: TS, TRM Entries, Minor SWP Brazed Joint Leak on
: SWP-003-05-3(A-)RECO for
: CR-06-06124, A Minor Leak was Discovered in Line 3SWP-003-003-86-3 in theSupply to 3HVR*ACU1A (CR-06-06124)Engineering Record of Correspondence (ERC) 25212-ER-06-0041, Evaluation of FlawResulting from Loss of Braze in SW Blowdown Line Leak (CR-06-05056)
==Section 1R15: Operability EvaluationsCR-06-03441,==
: MP2 P4 Terry Turbine Pump Outboard Bearing Vibration in the Vertical Directionis Acceptable But is Outside the IST Normal RangeCR-06-03578, 2-MS-342 Leaks by Seat
: CR-06-03730, Found "B" Gravity Boration Line Essentially Empty as Followup to CR-06-03712
: CR-06-03712, Abnormal Discharge Pressure While Starting 3CHS*P2B for SP-3604C.1-001
: CR 06-03276, 3CCE*37B Charging Pump Cooler 3CCE*E1B Temperature Control Valve FailedStroke Time TestCR-06-03265, Unplanned LCO, Both Control Building Filters Inoperable Due to Tagging
: CR-06-03840, Difficulty Venting Flow Transmitters FT-5278A/B
: CR-06-04047, UT of AFW Piping in Aux Bldg East and West Penetration (38'6") RevealedPiping Volume not 100% Flooded in Some SectionsCR-06-03718, Control Room Panel Deficiency #2451.
: F5278B-1, #2 Steam Generator AuxFeed Flow Indication, Fluctuating with Aux Feedwater SecuredCR-06-04500, Add Additional AFW Flow Indication to the PPC
: CR-06-04677, Lessons Learned.
: Recent CRs on Problems with MP2 AFW Flow IndicationCould Have Used RECO/OD to Document Operability DiscussionsCR-06-04538,
: FT-5278A/B Observations, Regarding Oscillations on AFW Flow MeterCR-06-00140, Aux Feedwater Flow Transmitters
: FT-5277B and
: FT-5278B as Found DataFound Out of Spec.
: Cal'd per Procedure as Date Within Spec.CR-06-03588, F5278 S/G Aux Feedwater Flow Indication Erroneous.
: This is Control PanelDeficiencyCR-06-01796, Reactor Trip Due to a Loss of Instrument Air
: CR-06-03250, Charging Pulsation Dampeners May Have Been Adversely Impacted ByChattering During CooldownCR-06-03442, "A" Charging Pulsation Dampener Bladder Has Failed
: CR-06-05318, EBFS Control Dampeners not Rated to MOPD
: CR-06-05202, Larger Wattage Bulbs Installed in DC Lighting than Called for in Drawing
: CR-06-05355, After Adjusting Air Regulators for EBFS Fan Discharge Dampeners, 2-EB-42and 52, the Dampeners Would Not Close on DemandCR-06-05351, Unplanned Entry into Tech Spec 3.0.3 for Enclosure Building Filtration
: OP-2314G, Revision 014-03, Enclosure Building Filtration System
: A-5AttachmentRegulatory Guide 1.52, Revision 3, June 2001, Design, Inspection, and Testing Criteria for AirFiltration and Adsorption Units of Post-Accident Engineered-Safety-Feature Atmosphere Cleanup Systems in Light-Water-Cooled Nuclear Power PlantsNRC Information Notice 88-24, Failures of Air Operated Valves Affecting Safety-RelatedSystems Dated May 13, 1988M2-EV-04-0018, Revision 00, Precharge Requirements for MP2 Charging Pump DampenersBladders for Low Pressure OperationDWG 25203-20150, Sheet 516, Unit 2 AFW Isometric Drawing
: DWG 25203-26005, Sheet 3 of 4, Revision 62, P&ID Condensate Storage and Aux FeedMP3 TS, Section 3/4.7, Plant Systems Unit 2 FSAR, Section 10.4.5, Revision 21, Condensate and Feedwater System
: DCR M2-99005, Revision 0, Auxiliary and Main Feedwater Control and Isolation IssuesM2-EV-99-0046, Revision 0, Motor Driven AFW Pump Cycling Requirements During TurbineBuilding HELB
==Section 1R19: Post-Maintenance Testing==
: AWO M2-06-03408, Inspect 2-RC-001 Packing at NOP/NOTAWO M2-06-03208, Adjust Packing and Perform Flowscan Testing
: AWO M2-05-06191, Overhaul Terry Turbine Outboard Mechanical Seal
: AWO M2-06-03091, Replace Turbine-Driven Auxiliary Feedwater Pump Outboard BearingAWO M2-06-04291, "B" Control Room Air Conditioning Compressor Assembly
: AWO M3-06-04349, Active Steam Leak on TDAFW Pump Steam Trap
: AWO M3-06-04363, M33EGS*EGB Replace O-rings/Gaskets for #10 Cylinder Water Jumper
: AWO M3-04-07920, RHR Hx Cooling Outlet isolation Pilot ReplacementAWO M3-03-00495, RHR Hx Cooling Outlet Insolation Bettis Actuator Over haulSP-3646A.2-1, Revision 018-02, Emergency Diesel Generator "B" Operability TestsSP-3630A.7-008, Revision 000-02, "B" Train RPCCW Valve Stroke Time Test Troubleshooting Sheet Associated with AWO M2-06-04291
: DWG 25203-32023, Sheet 56, Revision 5, Control Room A/C Air Cool Condenser MF36B
: DBS-2315A, Revision 0, Control Room Air Conditioning Design Bases Summary
==Section 1R20: Refueling and Outage Activities==
: OP-2203, Revision 017-01, Plant StartupOP-2202, Revision 021-00, Reactor Startup IPTE
: OP-2205, Revision 014-02, Plant Shutdown
: OP-2206, Revision 011-00, Reactor Shutdown
==Section 1R22: Surveillance TestingSP-3603D.3, Revision 006-01, Charging Pump Cooling System Valve Operability TestSP-2610BO-002, Revision 000-00,==
: TDAFW and Recirculation Check Valve IST
: SP-2613B, Revision 021-01, Periodic DG Operability Test, Facility 2 (Fast Start, Loaded Run)Performed on 5/17/2006SP-3610A.1-001, Revision 010-03, 3RHS*P1A Operational Readiness Test in Mode 1, 2, 3 or 4 
: A-6AttachmentCR-06-03276, 3CCE*37B Charging Pump Cooler 3CCE*E1B Temperature Control Valve FailedStroke Time Test
==Section 1EP6: Drill Evaluation==
: MP-26-EPI-FAP06-02, Revision 004-01, Millstone Unit 2 EAL TablesMP-26-EPI-FAP07-001, Revision 001-01, Incident Report Form Drill Exercise Sequence of Events, Revision 2, Dated April 12, 2006MP-26-EPI-FAP04, Revision 003, Emergency Operation Facility Activation OperationCR-06-04173, A SERO Rehearsal Drill was Conducted During Which a Number of Areas forImprovement were IdentifiedCR-06-03548, Millstone Paging Application FailureCR-06-04371, A Rehearsal Drill was Conducted on 4/12/06 During Which a Number ofInformation Technology (IT) Related Comments Were ReceivedCR-06-04220, Field Team Air Sample Could Not Obtain Flow Rate Specified inMP-26-EPI-FAP15-003LORTSE58, Operational Exam 58, Simulator Guide Approval Sheet
==Section 4OA1: Performance Indicator (PI) Verification==
: NEI 99-02, Revision 2, Regulatory Assessment Performance Indicator Guidance
==Section 4OA2: ==
: Identification and Resolution of ProblemsMP-14-OPS-GDL400, Revision 007-01, Operations Administrative ProceduresUnit 2 and Unit 3 Shift Turnover Reports Unit 2 and Unit 3 Operator Work-arounds, Burdens, and Distraction database
: CR-06-00372, Transient Combustible Fire Load did not have a Permit
: CR-06-04691, Combustible Material Storage not Appropriate for Area or No Permit Provided
: CR-06-00805, Trend in Poor Housekeeping/Combustible Permit Process Adherence
: CR-06-00984, Poor Housekeeping and Lack of Combustible Permits for the MP2 Aux -45'
: CR-05-07551, Review of Compensatory Measures for a Fire Protection Permit
: CR-06-06890, Classification Needed on What Constitutes Compensatory Measures in Operability Determination Process
: WC-7, Revision 005-03, Fire Protection ProgramSection 4OA3 Event Followup
: LER 2005-004-00, Pressurizer Spray Nozzle Weld IndicationsLER 2005-005-00 and
: LER 2005-005-01, Automatic Reactor Trip of Millstone Unit 3 Due toLow-Low Steam Generator LevelCR-05-13356, Millstone Unit 3 Reactor TripDesign Change Notice
: DM3-00-0077-02, RPS, ESF and AMSAC Low Steam Generator LevelTrip Setpoint Change, Dated January 28, 2002CR-05-11047, 3RCS*TK1 6" Spray Line has 2 Linear Indications that are Rejectable by ASMESection XI
: A-7AttachmentCR-05-11382, Automated Ultrasonic Examination of the Pressurizer Spray Nozzle hasIdentified 3 Flaw IndicationsCR-05-11521, Indications in the Pressurizer Spray Nozzle to Safe End Weld Exceed ASMESection XI Allowable SizeCR-06-04788, Inadequate Screen for DCN
: DM3-00-0077-02CR-02-01362, SG Mid-Deck Plate Pressure Loss That May Affect SG Low-Low Water LevelReactor Protection Setpoints Unresolved Indication Report
: MP3-05-009, Spray Nozzle to Safe End Weld Flaw
: M3-EV-05-0035, Evaluation of Unresolved Indication Report MP3-05-009
: Dominion 60 day Response to NRC Bulletin 2004-01, Dated July 27, 2004Dominion Clarification to the 60 day Response to NRC Bulletin 2004-01, Dated March 31, 2005NRC Issuance of Relief from Code Requirements for Millstone Unit 3, Dated January 23, 2006M3-05-14477, Pressurizer Spray Nozzle to Safe End Weld Overlay
: NRC Bulletin 2004-01, Inspection of Alloy 82/182/600 Materials Used in the Fabrication ofPressurizer Penetrations and Steam Space Piping Connections at Pressurized Water Reactors, Dated May 28, 2004Westinghouse Nuclear Safety Advisory Letter,
: NSAL-02-3, Revision 1, Steam GeneratorMid-deck Plate Pressure Loss issueUnit 3 Final Safety Analysis Report
==Section 4OA5: Other ActivitiesAOP-2580, Revision 003-02, "Degraded Voltage"ARP-2590J, Revision 001-01, "Alarm Response for==
: RFL Supervisory Panel, C909"
: ARP-2590F, Revision 008-00, "Alarm Response for Control Room Panel, C-08"
: ARP-2592E, Revision 001-00, "Alarm Response for RSST, 15G-22S"
: CR-04-09302,
: AOP 2580, "Degraded Voltage" Needs Additional Tech Spec ApplicabilityGuidance on Switchyard VoltageCR-04-09304, Recommended Change to Procedure to Add Tech Spec Applicability Guidanceon Switchyard VoltageCR-05-05487, Alarm on the Warning I-Dent-A-Tech at the South Access Point will not AlarmWhen Taking the Devices Designed to Make it Alarm Through the DetectorCR-05-09287, Tracking CR for
: ISO-New England Procedure Revision
: MP-13-PRA-FAP01.1, Revision 001, "Performing Risk Reviews"
: MP-14-OPS-GDL600, Revision 004-01, "Plant Status and Configuration Control"MP-20-OM-FAP02.1, Revision 001-04, "Shutdown Risk Management"
: MP-20-WM-FAP02.1, Revision 010-01, "Conduct of Online Maintenance"
: OP-2351, Revision 010-01, "CONVEX 345 KV Switchgear"
: OP-3353.MB8A, "Main Board 8A Annunciator Response"
==LIST OF ACRONYMS==
AFWauxiliary feedwaterAOPabnormal operating procedure
AMSACATWS mitigating system actuation circuitry
A-8AttachmentATWSanticipated transient without scramCFRCode of Federal Regulations
CRcondition report
CVCSchemical and volume control systemDCNdesign change notice
DRPDivision of Reactor Projects
DRSDivision of Reactor Safety
EDGemergency diesel generator
FINfinding
FSARFinal Safety Analysis Report
HXheat exchanger
IMCInspection Manual Chapter
ISTin-service testing
LERlicensee event report
MCCmotor control center
MRmaintenance rule
NCVnon-cited violation
NEINuclear Energy Institute
NRCNuclear Regulatory Commission
NTSnominal trip setpoint
ODoperability determinationOPoperating procedure
PIperformance indicator
PMTpost-maintenance testing
RBCCWreactor building closed cooling water
RCSreactor coolant system
RECOreasonable expectation of continued operabilitySDPsignificance determination process
SGsteam generator
SPsurveillance procedure
TDAFWturbine-driven auxiliary feedwaterTItemporary instruction
TRMTechnical Requirements Manual
TStechnical specification
: [[UT]] [[ultrasonic test]]
}}
}}

Revision as of 15:16, 13 July 2019

IR 05000336-06-003, 05000423-06-003; on 04/01/2006 - 06/30/2006; Millstone, Units 2 and Unit 3; Equipment Alignment, Operability Evaluations, Event Followup
ML062090543
Person / Time
Site: Millstone  Dominion icon.png
Issue date: 07/28/2006
From: Paul Krohn
NRC/RGN-I/DRP/PB6
To: Christian D
Dominion Resources
Krohn P, RI/DRP/PB6/610-337-5120
References
IR-06-003
Download: ML062090543 (35)


Text

July 28, 2006Mr. David A. ChristianSr. Vice President and Chief Nuclear Officer Dominion Resources 5000 Dominion Boulevard Glenn Allen, VA 23060-6711SUBJECT:MILLSTONE POWER STATION - NRC INTEGRATED INSPECTIONREPORT 05000336/2006003 AND 05000423/2006003

Dear Mr. Christian:

On June 30, 2006, the US Nuclear Regulatory Commission (NRC) completed an inspection atyour Millstone Power Station Unit 2 and Unit 3. The enclosed inspection report documents theinspection results, which were discussed on July 11, 2006, with Mr. A. Skip Jordan and other members of your staff.The inspection examined activities conducted under your license as they relate to safety andcompliance with the Commission's rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.This report documents three NRC-identified findings of very low safety significance (Green). Two of these findings were determined to involve violations of NRC requirements. However,because of their very low safety significance and because are entered into your corrective action program, the NRC is treating these issues as non-cited violations (NCVs), in accordancewith Section VI.A.1 of the NRC's Enforcement Policy. If you contest any NCV in this report, youshould provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN.: Document Control Desk, Washington DC 20555-0001; with copies to the Regional Administrator, Region I; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at the Millstone Power Station.In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, itsenclosure, and your response (if any) will be available electronically for public inspection in theNRC Public Document Room or from the Publicly Available Records (PARS) com ponent ofNRC's document system (ADAMS). ADAMS is accessible from the NRC Website at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Paul G. Krohn, ChiefReactor Projects Branch 6 Division of Reactor Projects Mr. D. A. Christian2Docket Nos.:50-336, 50-423License Nos.:DPR-65, NPF-49Enclosure:Inspection Report 05000336/2006003 and 05000423/2006003w/Attachment: Supplemental Informationcc w/encl:J. A. Price, Site Vice President, Millstone StationC. L. Funderburk, Director, Nuclear Licensing and Operations Support D. W. Dodson, Supervisor, Station Licensing L. M. Cuoco, Senior Counsel C. Brinkman, Manager, Washington Nuclear Operations J. Roy, Director of Operations, Massachusetts Municipal Wholesale Electric Company First Selectmen, Town of Waterford B. Sheehan, Co-Chair, NEAC E. Woollacott, Co-Chair, NEAC E. Wilds, Director, State of Connecticut SLO Designee J. Buckingham, Department of Public Utility ControlG. Proios, Suffolk County Planning Dept.

R. Shadis, New England Coalition Staff G. Winslow, Citizens Regulatory Commission (CRC)S. Comley, We The People D. Katz, Citizens Awareness Network (CAN)

R. Bassilakis, CAN J. M. Block, Attorney, CAN P. Eddy, Electric Division, Department of Public Service, State of New York P. Smith, President, New York State Energy Research and Development Authority J. Spath, SLO Designee, New York State Energy Research and Development Authority Mr.

SUMMARY OF FINDINGS

IR 05000336/2006-003, 05000423/2006-003; 04/01/2006 - 06/30/2006; Millstone PowerStation, Unit 2 and Unit 3; Equipment Alignment, Operability Evaluations, Event Followup.The report covered a 3-month period of inspection by resident inspectors and announcedinspections by regional inspectors. Two (Green) non-cited violations (NCVs) and one (Green)

finding were identified. The significance of most findings is indicated by their color (Green,

White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, "Significance Determination Process" (SDP). Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRC's program for overseeing the safeoperation of commercial nuclear power reactors is described in NUREG-1649, "ReactorOversight Process," Revision 3, dated July 2000.A.

NRC-Identified and Self-Revealing Findings

Cornerstone: Initiating EventsUnit 3!

Green.

The inspectors identified a Green NCV of 10 CFR 50, Appendix B,Criterion III, "Design Control," for an inadequate design change review for asteam generator low-low water level setpoint modification. Specifically,

Dominion did not fully consider the impact of the modification on the ability of the steam generator to accommodate operational transients without exceeding a parameter threshold which would require automatic or manual protective action.

This led to a reactor trip on December 1, 2005, while conducting a rapid downpower in response to a reactor coolant system leak from the packing of aloop maintenance stop valve that was collected in a drain tank inside primary containment. At 38 percent power, main turbine vibrations increased above allowable values and the turbine was manually tripped. Following the turbine trip, the reactor unexpectedly automatically tripped on the "C" steam generator low-low level trip setpoint. Dominion entered this condition into their corrective action program as CR-06-04788. Corrective actions for this issue included plans to conduct an engineering analysis to determine the new steam generator low-low level trip setpoints and revision of the design change notice and the 10 CFR 50.59 screening.This finding is more than minor because it is associated with the Initiating EventsCornerstone and affects the cornerstone objective to limit the likelihood of those events that upset plant stability. Specifically, an inadequate design changereview led to an unanticipated reactor trip. This issue is of very low safety significance because it did not contribute to both the likelihood of a reactor trip and the likelihood that mitigation equipment or functions would not be available. This finding is related to the cross-cutting aspect of human performance in that Dominion's review and decision making process was not effective at identifying possible unintended consequences when making assumptions for a risk significant design change. (Section 4OA3.2)

iv

Cornerstone: Mitigating SystemsUnit 2!

Green.

The inspectors identified a finding when Dominion did not recognize thata portion of the auxiliary feedwater (AFW) discharge header contained air voidsafter they determined that AFW flow instrumentation was behaving erratically as a result of air in the instrument line. Specifically, Dominion initiated a condition report after identifying that AFW flow instrumentation was air bound but closed out operability concerns based on air only affecting instrumentation and not thepotential that air could exist in the discharge portion of the system. As a result,

Dominion did not identify existing voids in AFW discharge piping or assess these air voids for impact on AFW operability. Dominion entered this condition intotheir corrective action program as CR-06-04677. Corrective actions for this issue included conducting ultrasonic testing of the discharge piping, quantifying the air voids in the system, and evaluating operability of the system with these airvoids left in place.This finding is more than minor because it is associated with the MitigatingSystems Cornerstone and affects the cornerstone objective of ensuring the reliability of systems that respond to initiating events to prevent undesirableconsequences. Specifically, Dominion did not investigate or evaluate the existence of air voids in the AFW system discharge piping when air wasidentified in t he system. This finding was determined to be of very low safetysignificance (Green) because it did not result in a loss of function once the existing air voids were identified and evaluated. This finding is related to the cross-cutting aspect of problem identification and resolution in that Dominion did not fully investigate the existence of air voids in other parts of the AFW systemand as a result did not fully evaluate the impact of existing air voids in the AFW system discharge piping. (Section 1R15.1)Unit 3!Green. The inspectors identified a Green NCV of 10 CFR 50, Appendix B,Criterion XVI, "Corrective Action," for the failure to fully evaluate and correct a significant condition adverse to quality which led to a repeat occurrence of air introduction in the gravity feed boration line. Specifically, following identification and documentation of air in the "A" gravity feed boration line on September 9,2004, Dominion did not evaluate and correct the cause which then led to a repeat occurrence of air introduction in the "B" gravity feed boration line on April 13, 2006. The inspectors determined that the cause of both events wasdue to an inadequate chemical and volume control system (CVCS) f ill and ventprocedure. Dominion entered this condition into their corrective action program as CR-06-03730. Corrective actions for this issue included venting the air from the gravity feed boration line and plans to revise the CVCS f ill and ventprocedure.

vThis finding is more than minor because it is associated with the MitigatingSystems Cornerstone and affects the cornerstone objective of ensuring the availability of systems that respond to initiating events to prevent undesirableconsequences. Specifically, excessive air in the gravity feed lines has the potential to damage the operating charging pump if an emergency boration event were to occur. This finding was determined to be of very low safety significance (Green) since full mitigation credit was given for the availability of r edundantemergency boration paths. This finding is related to the cross-cutting aspect of problem identification and resolution in that Dominion did not fully evaluate and correct an identified degraded condition discovered in September 2004, which then recurred in April 2006. (Section 1R04).

B.Licensee-Identified Violations

None.

Enclosure

REPORT DETAILS

Summary of Plant StatusUnit 2 operated at essentially 100 percent power for the duration of the inspection period withthe following exceptions. On April 1, 2006, the plant was shutdown after the turbine-drivenauxiliary feedwater (TDAFW) pump was determined to be inoperable. The TDAFW pump wasrepaired and retested on April 7, and a reactor startup commenced on April 9. The reactor was returned to 100 percent power on April 10, 2006.Unit 3 operated at essentially 100 percent power for the duration of the inspection period.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity1R01Adverse Weather Protection (71111.01)Seasonal Site Inspection (One Site Sample)Unit 2 and Unit 3

a. Inspection Scope

The inspectors performed a review of severe weather preparations during the onset ofthe hurricane season to evaluate the site's readiness for seasonal susceptibilities. Theinspectors reviewed Dominion's preparations for severe weather and the impact on the protection of safety-related systems, structures and components. The inspectionensured that the selected equipment, instrumentation, and supporting structures were configured in accordance with Dominion's procedures and that adequate controls were in place to ensure functionality of the systems. The inspectors reviewed the Unit 2 andUnit 3 Final Safety Analysis Report (FSAR) and Technical Specifications (TS) and compared the analysis with procedure requirements to ascertain that procedures were consistent with the FSAR. The inspectors performed partial walkdowns of the Unit 2 and Unit 3 intake structures, service water systems, intake structure traveling screensand emergency diesel generators to determine the adequacy of equipment protection from the effects of hurricanes. The inspectors verified that operator actions defined in the adverse weather procedures maintained readiness of essential systems and thatadequate operator staffing was specified. Documents reviewed during the inspection are listed in the Attachment.

b. Findings

No findings of significance were identified.

2Enclosure1R04Equipment Alignment (71111.04)Partial System Walkdowns (71111.04 - Two Unit 2 Samples and Two Unit 3 Samples)

a. Inspection Scope

The inspectors performed four partial system walkdowns during this inspection period. The inspectors reviewed the documents listed in the Attachment to determine the correct system alignment. The inspectors conducted a walkdown of eac h system toverify that the critical portions of selected systems were correctly aligned in accordancewith these procedures and to identify any discrepancies that may have had an effect on operability. The inspectors verified that equipment alignment problems that could causeinitiating events, impact mitigating system availability or function, or affect barrier functions, were identified and resolved. The following systems were reviewed based ontheir risk significance for the given plant configuration:Unit 2*Partial equipment alignment of "A" and "C" reactor building closed cooling water(RBCCW) heat exchangers (HXs) with the "B" RBCCW HX out-of-service, May 9, 2006; and*Partial equipment alignment of the "B" emergency diesel generator (EDG) during"A" EDG maintenance, May 18, 2006.Unit 3*Partial equipment alignment of "A" gravity feed boration line, April 18, 2006; and*Partial equipment alignment of "A" service water train during a "B" service watertrain outage, May 10, 2006.

b. Findings

Unit 2No findings of significance were identified.

Unit 3Introduction. The inspectors identified a Green non-cited violation (NCV) of 10 CFR 50,Appendix B, Criterion XVI, "Corrective Action," for the failure to fully evaluate and correct a significant condition adverse to quality which led to a repeat occurrence of air introduction in the gravity feed boration line. Specifically, following identification and documentation of air in the "A" gravity feed boration line on September 9, 2004,Dominion did not evaluate and correct the cause which led to a repeat occurrence of air introduction in the "B" gravity feed boration line on April 18, 2006. The inspectors determined that both events were due to an inadequate chemical and volume controlsystem (CVCS) fill and vent procedure.

3EnclosureDescription. On April 17, 2006, during a routine monthly operational readiness test ofthe "B" boric acid transfer pump, Operations observed erratic indications on the pump discharge pressure gage. Operations investigated the following day and determinedthat approximately 29 liters of air was introduced into the "B" gravity feed boration line. Operations determined that the air was introduced following the f ill and vent of the "B"charging pump on April 13, 2006. In accordance with Surveillance Procedure(SP)-3604C.8, "Gravity Feed Boration Line Gas Accumulation Monitoring," this amount of air made the "B" gravity feed line inoperable. Operations entered Technical Requirements Manual (TRM) action statement 3TRM-7.6.1, "Safety Grade Cold Shutdown," and vented the "B" gravity feed boration line to restore operability.The inspectors reviewed Operating Procedure (OP)-3304A, "Charging and Letdown",the control room logs, and associated CRs and technical evaluations. The inspectors identified that a similar event had occurred in September 2004. Specifically, onSeptember 9, 2004, following maintenance on the "A" charging pump, the CVCS systemwas filled and vented. Approximately nine hours after restoring the "A" charging pump to an operable status, an ultrasonic test revealed that piping on the downstream side of the gravity feed boration valve was zero percent full (3.5 liters of air). In accordance with SP-3604C.8, this amount of air made the "A" gravity feed line inoperable.

Operations entered TRM action statement 3TRM-7.6.1, "Safety Grade Cold Shutdown"and removed the air by venting the "A" gravity feed boration line. The inspectors determined that Dominion did not recognize the September 2004 eventas a significant condition adverse to quality. The issue was considered a significant condition adverse to quality since damage to an operating charging pump (a safety-related component) would have occurred during a gravity boration event while the excessive air was in the gravity feed lines. The inspectors determined that the failure to take corrective action to preclude repetition from the September 2004 event led to a repeat occurrence of air introduction in the "B" gravity feed boration line on April 13, 2006. The inspectors determined that the cause of both events was due to aninadequate CVCS f ill and vent procedure. Because the cause of the September 2004event was similar to the April 2006 event, the inspectors concluded that the April 2006 event was within Dominion's ability to foresee and correct, and should have beenprevented. The performance issue associated with this finding is that Dominion failed to identify and correct the cause of air introduction into the "A" gravity feed line in September 2004. This then led to a repeat occurrence of air introduction into the "B" gravity feed line in April 2006.Analysis. This finding is more than minor because it is associated with the MitigatingSystems cornerstone and affects the objective of ensuring the availability of systemsthat respond to initiating events to prevent undesirable consequences. Specifically, the air volume identified in the boration lines in 2004 and 2006 resulted in their unavailabilityto perform the intended safety function. The inspectors evaluated this finding in accordance with IMC 0609, Appendix A, "Significance Determination of Reactor Inspection Findings for At-Power Situations." The Significance Determination Process (SDP) Phase 1 screening identified that a SDP workbook Phase 2 evaluation was needed because the inoperable "B" gravity feed line represented a potential loss of 4Enclosuresafety function of one or more non-technical specification trains of equipmentdesignated as risk-significant per 10 CFR 50.65 for greater than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. In Phase 2, the inspectors determined that the event of interest was an anticipated transient withoutscram (ATWS). The gravity boration feed line is referenced in the ATWS emergency operating procedure as a backup method of emergency boration and selected 10 CFR Part 50, Appendix R, scenarios to achieve cold shutdown conditions. Because redundant trains of emergency boration were available, the inspectors determined that full mitigation credit was appropriate and concluded that this finding is of very low safety significance (Green). This finding is related to the cross-cutting aspect of problem identification and resolution in that Dominion did not fully evaluate and correct an identified degraded condition discovered in September 2004, which then recurred in April 2006.Enforcement. Code of Federal Regulations 10 CFR Part 50, Appendix B, Criterion XVI,"Corrective Action," requires, in part, that measures shall be established to assure that conditions adverse to quality, such as failures, malfunctions, deficiencies, deviations, defective material and equipment, and non-conformances are promptly identified and corrected. In the case of significant conditions adverse to quality, the measures shall assure that the cause of the condition is determined and corrective action taken to preclude repetition. Contrary to the above, following documentation of air introductioninto the "A" gravity feed boration line on September 9, 2004, Dominion did not fullyevaluate the cause of this condition. This led to a recurrence of air introduction into the "B" gravity feed boration line on April 13, 2006. This issue has been entered in Dominion's corrective action program as CR 06-03730. Corrective actions for this issue included venting the air from the gravity feed boration line and plans to revise the CVCS fill and vent procedure. This issue is being treated as a non-cited violation consistentwith Section VI.A of the Enforcement Policy (NCV 05000423/2006003-01, Did NotEvaluate and Correct a Significant Condition Adverse to Quality Associated with Gravity Feed Boration Lines).

1R05 Fire Protection (71111.05)Quarterly Sample Review (71111.05Q - Three Unit 2 Samples and Three Unit 3Samples)

a. Inspection Scope

The inspectors performed six walkdowns of fire protection areas during the inspectionperiod. The inspectors reviewed Dominion's fire protection program to determine the required fire protection design features, fire area boundaries, and combustible loading requirements for the selected areas. The inspectors walked down these areas to assess Dominion's control of transient combustible material and ignition sources. In addition, the inspectors evaluated the material condition and operational status of fire detection and suppression capabilities, fire barriers, and any related compensatorymeasures. The inspectors then compared the existing conditions of the areas to the fire protection program requirements to ensure that selected program requirements were 5Enclosurebeing met. The inspectors also interviewed fire protection engineers and otherDominion staff, and evaluated the impact of fire suppression systems on adjacent plantareas. Documents reviewed during the inspection are listed in the Attachment. The fire protection areas reviewed included:Unit 2*Auxiliary Building Cable Vault, 25'6" Elevation (Fire Area A-24);*West DC Switchgear Room, 14'6" Elevation (Fire Area A-21); and

  • Railroad Bay Area, 14'6" Elevation (Fire Area A-14).Unit 3*Cable Spreading Area, 24'6" Elevation (Fire Area CB-8);*Floor Area, Auxiliary Building, 43'6" Elevation (Fire Area AB-1); and
  • Floor Area, Auxiliary Building, 66'6" Elevation Fire Area AB-1).

b. Findings

No findings of significance were identified.

1R06 Flood Protection Measures (71111.06 - One Unit 2 Sample)Internal Flooding Inspection

a. Inspection Scope

During the week of April 3, 2006, the inspectors reviewed one sample of flood protectionmeasures for equipment in the Unit 2 Auxiliary Building Cable Vault. This review was conducted to evaluate Dominion's protection of the enclosed safety-related systemsfrom internal flooding conditions. The inspectors performed a walkdown of the area and reviewed the Final Safety Analysis Report, the internal flooding evaluation, and related documents. The inspectors examined the as-found equipment and conditions to ensure that they remained consistent with those indicated in the design basis documentation,flooding mitigation documents, and risk analysis assumptions. The inspectors also interviewed Dominion engineers and other staff. Documents reviewed during the inspection are listed in the Attachment.

b. Findings

No findings of significance were identified.

6Enclosure1R11Licensed Operator Requalification Program (71111.11)Resident Inspector Quarterly Review (71111.11Q - One Unit 2 Sample and One Unit 3Sample)

a. Inspection Scope

The inspectors observed one sample of Unit 2 licensed operator simulator training onApril 12, 2006. The inspectors also observed one sample of Unit 3 licensed operator requalification (operability determination) training on April 21, 2006. The inspectorsverified that the training evaluators adequately addressed that the applicable trainingobjectives had been achieved, operator performance was adequate, and evaluators were identifying and documenting crew performance problems. Documents reviewed during the inspection are listed in the Attachment.

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness (71111.12)Routine Maintenance Effectiveness Inspection (71111.12Q - One Unit 2 Sample andOne Unit 3 Sample)

a. Inspection Scope

The inspectors reviewed two samples of Dominion's evaluation of degraded conditions,involving safety-related structures, systems and/or components for maintenanceeffectiveness during this inspection period. The inspectors reviewed licensee implementation of the Maintenance Rule (MR), 10 CFR 50.65, and verified that theconditions associated with the referenced condition reports (CRs) were appropriately evaluated against applicable MR functional failure criteria as found in licensee scoping documents and procedures. The inspectors also discussed these issues with the system engineers and maintenance rule coordinators to verify that they wereappropriately tracked against each system's performance criteria and that the systemswere appropriately classified in accordance with MR implementation guidance.

Documents reviewed during the inspection are listed in the Attachment. The following conditions were reviewed:Unit 2*Loss of Second Facility of Charging Pumps (CR-06-00243).Unit 3*"B" Residual Heat Removal Flow Control Valve Stroke Failed (CR-06-03350).

b. Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13 - Three Unit 2Samples and Four Unit 3 Samples)

a. Inspection Scope

The inspectors reviewed seven samples of the adequacy of maintenance riskassessments for emergent and planned activities during the inspection period. The inspectors utilized the Equipment-Out-of-Service quantitative risk assessment tool toevaluate the risk of the plant configurations and compared the results to Dominion'sstated risk. The inspectors verified that Dominion entered appropriate risk categories and implemented risk management actions as necessary. Documents reviewed during the inspection are listed in the Attachment. The inspectors verified the conduct and adequacy of scheduled maintenance risk assessments for plant conditions affected by performance of the following maintenance and testing activities:Unit 2*Emergent work control during week of April 2, 2006, due to failure of theturbine-driven auxiliary feedwater pump;*Risk assessment during "A" EDG two-year overhaul, May 15-20, 2006; and

  • Risk assessment during "B" EDG maintenance, June 1, 2006.Unit 3*Risk assessment during turbine-driven auxiliary feedwater pump steam trapmaintenance, April 13, 2006;*Risk assessment due to scheduled "A"EDG maintenance, April 25, 2006;
  • Risk assessment due to containment pressure relay replacement, May 5, 2006; and*Risk assessment during "B" EDG sequencer slave relay testing, May 8, 2006.

b. Findings

No findings of significance were identified.

1R14 Operator Performance During Non-Routine Evolutions and Events (71111.14 - One Unit3 Sample)

a. Inspection Scope

The inspectors reviewed one sample of events that demonstrated personnelperformance in coping with non-routine evolutions and transients. The inspectors observed operations in the control room and reviewed applicable technical 8Enclosurespecifications, operability determination basis documents, and technical evaluations toevaluate the adequacy of Dominion's response to this event. The inspectors also verified the event was entered into the corrective action program to resolve identified adverse conditions. Documents reviewed during the inspection are listed in the

.Unit 3*On June 30, 2006, with the Unit at 100 percent power, Unit 3 operatorsquestioned whether isolation of room cooling to the "A" rod control motor control center (MCC) room also affected safety-related MCCs in this room. Operators declared the affected switchgear inoperable and entered Technical Specification 3.8.3.1, "Onsite Power Distribution." Engineering personnel reviewed theconfiguration and established a basis for operability based on existing structuralsupports, service water cooling margin assuming a maximum leak size for the affecting piping, and ultrasonic examination of upstream and downstream piping.

Operators accepted the reasonable assurance of continued operability (RECO),unisolated service water cooling to the room, and exited the technical specification action statement. The inspectors responded to the site and reviewed the basis of the RECO and the adequacy of operator actions.

b. Findings

No findings of significance were identified.

1R15 Operability Evaluations (71111.15 - Six Unit 2 Samples and Five Unit 3 Samples)

a. Inspection Scope

The inspectors reviewed eleven operability determinations associated with degraded ornon-conforming conditions to ensure that operability was justified and that mitigatingsystems or those affecting barrier integrity remained available and no unrecognizedincrease in risk had occurred. The inspectors also reviewed compensatory measures to ensure that the measures were in place and were appropriately controlled. The inspectors reviewed licensee performance to ensure all related TS and FSAR requirements were met. Documents reviewed during the inspection are listed in the

. The inspectors reviewed the following degraded or non-conforming conditions:Unit 2*Turbine-Driven Auxiliary Feedwater (TDAFW) Pump Vibration in Alert Status(CR-06-03441);*Air in AFW Discharge Piping (CR-06-03840);

  • Instrument Air to AFW Flow Control Valve Bottles (CR-06-01796);
  • Charging System Bladder Failure at Reduced Pressure (CR-06-03250);

9Enclosure*Reasonable Expectation of Continued Operability Enclosure Building FiltrationSystem Solenoids Related to NRC Information Notice 88-24 (CR-06-05351);*Incorrect Wattage DC Lighting and TSAS 3.0.3 Entry (CR-06-05202).Unit 3*Charging Pump Cooling System Temperature Control Valve (CR-06-03276);*Control Building Emergency Air Filtration System Configuration (CR-06-03265);

  • TDAFW Header Drain Valve Leaking (CR-06-03578);
  • "B" Train Charging due to Air in "B" Gravity Boration Line (CR-06-03730);

b. Findings

Unit 2.1Introduction. The inspectors identified a finding when Dominion did not recognize that aportion of the auxiliary feedwater (AFW) discharge header contained air voids after theydetermined that AFW flow instrumentation was behaving erratically as a result of air in the instrument line. Specifically, Dominion initiated a condition report after identifying that AFW flow instrumentation was air bound but closed out operability concerns basedon air only affecting instrumentation and not the potential that air could exist in thedischarge portion of the system.Description. On April 18, 2006, Operations determined that the Unit 2 AFW flowinstrumentation associated with the #2 steam generator was fluctuating with AFWsecured. Indicated AFW flow for the instrument was cycling between 0 and 75 gallons per minute (gpm) from control room, remote shutdown, and primary plant computer indications. Dominion determined that there was no TS required action based on the availability of redundant instrumentation. Dominion initiated a work order to vent theinstrumentation but had difficulties establishing flow through the low side instrumentationsensing line. Subsequently, a pressurized water source was used to establish flow through this line. Dominion considered recent maintenance performed on the turbine-driven auxiliary feedwater pump as a possible source for the air in theinstrumentation line and focused on how the air affected the flow transmitters. Dominion did not investigate whether air voids were present in AFW system discharge piping and,as a result, did not evaluate the impact of discharge piping air voids on the operability ofthe system.On April 24, 2006, the inspectors questioned whether or not Dominion had consideredthe possibility that air voids could be present in other portions of the AFW system and the subsequent effects on the AFW system's capability to deliver the required flow. OnApril 25, 2006, Dominion conducted ultrasonic testing on various portions of the AFW system and discovered that two sections of the AFW discharge header containedvoiding. Specifically, Dominion determined that a 20 foot AFW discharge piping run for the #2 steam generator was 90 percent flooded (approximately 12.68 cubic feet of air). In addition, Dominion determined that a 30 foot length of AFW discharge piping run for 10Enclosurethe #1 steam generator was 95 percent flooded (approximately 0.16 cubic feet of air). Operations subsequently determined that this amount of air would not affect AFWsystem operability based on the volume of air identified in t he system, the location of theair and relevance to a previously accepted Millstone Unit 3 Technical Evaluation (M3-EV-05-008), "ECCS Gas Accumulation in Support of Surveillance". The performancedeficiency is that Dominion did not recognize the air binding of the AFW feed flow instrument as an indication of the potential for air in the discharge portion of the systemand, as a result, did not identify or evaluate air voids that were located in two sections ofdischarge piping.Analysis. The finding is more than minor because it is associated with the MitigatingSystems Cornerstone and affects the cornerstone objective of ensuring the reliability ofsystems that respond to initiating events to prevent undesirable consequences. Thisfinding was determined to be of very low safety significance (Green) by using Phase 1 of Inspection Manual Chapter (IMC) 0609, "Significance Determination Process."

Specifically, the finding did not result in a loss of function per NRC Part 9900 TechnicalGuidance, "Operability Determination Process for Operability and FunctionalAssessment" and was not related to a seismic, flooding, or severe weather event. This finding is related to the cross-cutting aspect of problem identification and resolution in that Dominion did not fully investigate the existence of air voids in other parts of theAFW system and as a result did not fully evaluate the impact of existing air voids in theAFW system discharge piping.

Enforcement.

No violations of regulatory requirements occurred. On April 18, 2006,Dominion did not recognize air binding of the AFW feed flow instrument as an indication for the potential for air in the discharge portion of the system. As a result, Dominion did not identify or evaluate air voids in two sections of discharge piping until questioned by the inspectors on April 24, 2006. This is considered a finding of very low safety significance (Green). This issue has been entered in Dominion's corrective action program as CR-06-05202, CR-06-04677, and CR-06-05318. Corrective actions for this issue included conducting ultrasonic testing of the discharge piping, quantifying the air voids in the system, and evaluating operability of the system with these air voids left inplace. Because this finding does not involve a violation of regulatory requirements andhas very low significance, it is identified as (FIN 05000336/2006003-02), Did NotIdentify or Evaluate Air Voids Located in Auxiliary Feedwater System.Unit 3No findings of significance were identified.

1R19 Post-Maintenance Testing (71111.19 - Four Unit 2 Samples and Three Unit 3 Samples)

a. Inspection Scope

The inspectors reviewed seven samples of post-maintenance tests (PMT) during thisinspection period. The inspectors reviewed these activities to determine whether the 11EnclosurePMT adequately demonstrated that the safety-related function of the equipment wassatisfied given the scope of the work specified and that operability of the system wasrestored. In addition, the inspectors evaluated the applicable test acceptance criteria to verify consistency with the associated design and licensing bases, as well as TS requirements. The inspectors also verified that conditions adverse to quality were entered into the corrective action program for resolution. Documents reviewed during the inspection are listed in the Attachment. The following maintenance activities and their post-maintenance tests were evaluated:Unit 2*Adjust Packing on Reactor Coolant System #1 Hot Leg Sample Line IsolationValve (M2-06-03408);*Overhaul TDAFW Pump Outboard Mechanical Seal (M2-05-06191);

  • TDAFW Pump Outboard Bearing Replacement (M2-06-03091); and
  • "B" Control Room Air Conditioning Fuse Replacement Retest (M2-06-04291).Unit 3*Repair Leak on TDAFW Pump Steam Trap (M3-06-04349);*Replace O-rings/Gaskets for #10 Cylinder Water Jumper on Unit 3 "B"Emergency Diesel Generator (M3-06-04363); and*"B" Residual Heat Removal Heat Exchanger Cooling Outlet Isolation PilotReplacement and Bettis Actuator Overhaul (M3-04-07920).

b. Findings

No findings of significance were identified.

1R20 Refueling and Outage Activities

(71111.20 - One Unit 2 Sample)

a. Inspection Scope

The inspectors reviewed one sample of a forced outage following a Unit 2 shutdownassociated with the turbine-driven auxiliary feedwater pump failure on April 1, 2006, forcompliance with Technical Specification requirements and approved procedures, conduct of outage risk evaluations, configuration control, and maintenance of key safety functions. Documents reviewed during the inspection are listed in the Attachment.

During this forced outage, the inspectors monitored Dominion's control of the outage activities listed below:*Shutdown risk evaluations;*Startup scheduling;

  • Reactor startup and criticality;
  • Plant startup; and
  • Power ascension.

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing (71111.22 - Two Unit 2 Samples and Two Unit 3 Samples)

a. Inspection Scope

The inspectors reviewed four samples of surveillance activities to determine whether thetesting adequately demonstrated equipment operational readiness and the ability toperform the intended safety-related function. The inspectors attended pre-job briefs, verified that selected prerequisites and precautions were met and that the tests were performed in accordance with the procedural steps. Additionally, the inspectors evaluated the applicable test acceptance criteria to verify consistency with associated design bases, licensing bases, and TS requirements and that the applicable acceptance criteria were satisfied. The inspectors also verified that conditions adverse to quality were entered into the corrective action program for resolution. Documents reviewed during the inspection are listed in the Attachment. The following surveillance activities were evaluated:Unit 2*Turbine-Driven Auxiliary Feedwater and Recirculation Check Valve In-serviceTesting (IST) (SP-2610BO-002); and*"B" Emergency Diesel Generator Fast Start, Load Run (SP-2613B).Unit 3*Charging Pump Cooling System Valve Operability Test for Temperature ControlValve 37B (SP-3603D.3); and*"A" Residual Heat Removal Pump Operational IST (SP-3610A.1).

b. Findings

No findings of significance were identified.

===Cornerstone: Emergency Preparedness [EP]1EP6Drill Evaluation (71114.06 - One Unit 2 Sample and One Unit 3 Sample)

a. Inspection Scope

The inspectors observed one sample of the conduct of Unit 2 licensed operatorsimulator training during a drill conducted on April 12, 2006, and one sample of theconduct of Unit 3 licensed operator simulator training on May 30, 2006. The inspectors===

evaluated the Operations crew activities related to evaluating the scenario and makingproper emergency action level classification determinations. Additionally, the inspectors 13Enclosureassessed the ability of Dominion's evaluators to adequately address operatorperformance deficiencies identified during the exercise. Documents reviewed during the inspection are listed in the Attachment.

b. Findings

No findings of significance were identified.4.OTHER ACTIVITIES [OA]

4OA1Performance Indicator (PI) Verification (71151 - Three Unit 2 Samples and Three Unit 3Samples)

a. Inspection Scope

Cornerstone: Initiating Events The inspectors reviewed six samples of Dominion submittals for the PIs listed below toverify the accuracy of the data reported during that period. The PI definitions andguidance contained in NEI 99-02, "Regulatory Assessment Indicator Guidelines",

Revision 2, were used to verify the basis for reporting each data element.Unit 2*Unplanned Scrams per 7000 Critical Hours;*Unplanned Scrams with Loss of Normal Heat Removal; and

  • Unplanned Power Changes per 7000 Critical Hours.Unit 3*Unplanned Scrams per 7000 Critical Hours;*Unplanned Scrams with Loss of Normal Heat Removal; and
  • Unplanned Power Changes per 7000 Critical Hours.The inspectors reviewed portions of the operations logs and initial PI data developedfrom monthly operating reports and discussed the methods for compiling and reportingthe PIs with cognizant licensing and engineering personnel. The inspectors compared graphical representations from the most recent PI report to the initial data to verify thatthe data was correctly reflected in the report. Documents reviewed during this inspection are listed in the Attachment.

b. Findings

No findings of significance were identified.

14Enclosure4OA2Identification and Resolution of Problems (71152).1Review of Items Entered into the Corrective Action ProgramAs required by Inspection Procedure 71152, "Identification and Resolution of Problems",and in order to help identify repetitive equipment failures or specific human performance issues for followup, the inspectors performed a daily screening of items entered into Dominion's corrective action program. This was accomplished by reviewing the description of each new CR and attending daily management review committee meetings..2Semi-Annual Review to Identify Trends

a. Inspection Scope

The inspectors performed a semi-annual review to identify trends that might indicate theexistence of a more significant safety issue. The inspectors reviewed Unit 2 and Unit 3 performance indicator monthly reports, condition reports, system health reports, qualityassurance audits, self-assessment reports, maintenance reports, and NRC inspectionreports and interviewed key personnel to evaluate if a trend existed.

b. Findings and Observations

Operability DeterminationsNo findings of significance were identified. The inspectors continue to evaluateDominion's improvement initiatives in the area of Operability Determination quality andprocess implementation. For example, on June 2, 2006, the inspectors reviewedDominion's response when Operations determined that several non-Appendix R lightingfixtures had higher wattage light bulbs than assumed in the station's DC battery loading calculations. Operations took action to restore operability by opening various breakersassociated with the lighting fixtures, thereby, restoring margin to both vital batteries.

Dominion did not consider the action to open the breakers supplying the lighting fixtures as a compensatory measure governed under their Operability Determination process. The inspectors discussed with Dominion over the next several weeks the basis for why the action should have been considered a compensatory measure until full systemqualification is restored. As a result, Dominion entered CR-06-06890, "Classification needed on what constitutes compensatory measures in Operability DeterminationProcess" into the corrective action program (CAP).The inspectors have noted some effective corrective actions, particularly in the areas ofoperations and engineering personnel training. However, the inspectors have determined that sustained performance improvement on the part of both Units needs tobe demonstrated in order to evaluate the success of Dominions recent initiatives.

Therefore, the residents will continue to follow these issues, including what constitutescompensatory measures, within the framework of the baseline inspection program and re-visit the Operability Determination trend in subsequent reports.

15Enclosure.3Annual Sample Review Operator Work-arounds (One Site Sample)

a. Inspection Scope

The inspectors reviewed the current listing of operator work-arounds for Unit 2 andUnit 3. The review was conducted to verify that Dominion procedures and practices provided necessary guidance to plant personnel, that the cumulative effects of the known operator work-arounds were addressed, and that the overall impact on the affected systems were assessed. The inspectors independently assessed thecumulative impact of known operator work-arounds to determine if they adversely affected the ability of plant operators to implement emergency operating procedures,respond to plant transients, or perform normal functions within the expectations of the established Dominion risk models. In support of this assessment, the inspectors reviewed various condition reports regarding operator work-arounds and verified that work-arounds were being identified, tracked, and resolved in Dominion's corrective action program.

b. Findings and Observations

No findings of significance were identified. The inspectors determined that operatorwork-arounds are adequately classified, tracked, and assessed in accordance with Dominion's procedures..4Cross-References to PI&R Findings Documented Elsewhere in this ReportSection 1R04 describes a finding for the failure to identify and correct the cause of theair introduction into the "A" boric acid transfer pump gravity feed line in September 2004.

This led to a repeat occurrence of air introduction into the "B" boric acid transfer pump gravity feed line in April 2006. This finding is related to the cross-cutting aspect of problem identification and resolution in that Dominion did not fully evaluate and correct an identified degraded condition discovered in September 2004, which then recurred in April 2006.Section 1R15 describes a finding for the failure to adequately investigate and assess airvoids in the Auxiliary Feedwater System. This finding is related to the cross-cuttingaspect of problem identification and resolution in that Dominion did not fully investigate the existence of air voids in other parts of the AFW system and as a result did not fullyevaluate the impact of existing air voids in the AFW system discharge piping. 4OA3Event Followup (71153 - One Unit 2 Sample and One Unit 3 Sample).1(Closed) LER 05000423/2005-004-00, Pressurizer Spray Nozzle Weld IndicationsOn December 16, 2005, Dominion reported the discovery of flaws in the pressurizerspray nozzle to safe-end bimetallic region. The inspectors reviewed this LER with its 16Enclosureassociated condition reports to verify that the cause and corrective actions related to theevent described in the LER were adequate. In addition, the inspectors reviewed commitments made with regard to NRC Bulletin 2004-01 to ensure these wereappropriately addressed. No findings of significance were identified. This LER is closed..2(Closed) LER 05000423/2005-005-00 and LER 05000423/2005-005-01, AutomaticReactor Trip of Millstone Unit 3 Due to Low-Low Steam Generator Level

a. Inspection Scope

The inspectors interviewed Dominion personnel and reviewed this LER with itsassociated condition reports to verify that the root cause and corrective actions related to the event described were adequate.

b. Findings

Introduction.

The inspectors identified a Green NCV of 10 CFR 50, Appendix B,Criterion III, "Design Control," for an inadequate design change review for a steamgenerator low-low water level setpoint modification which led to a reactor trip on December 1, 2005, while conducting a rapid downpower in response to a reactor coolant system (RCS) leak.Description. On December 1, 2005, with the plant in Mode 1 at 38 percent power, anautomatic reactor trip occurred on a "C" steam generator low-low level (S/G low-low level) protection signal. At the time of the reactor trip, a rapid downpower to 30 percent was in progress to facilitate a containment entry to locate and repair a RCS leak fromthe packing of a loop maintenance stop valve that was collected in a drain tank inside primary containment. As turbine load and reactor power were reduced, main turbine vibrations increased above the allowable limits and the main turbine was manually tripped in accordance with procedures. After the turbine was manually tripped, the reactor tripped unexpectedly on "C" S/G low-low level. At the time of the trip, the reactor protection system S/G low-low level trip setpoint was being maintained at 27 percentversus the original value of 18 percent to address nuclear steam supply system vendor identified S/G level inaccuracies associated with the S/G mid-deck plate differential pressure.Based on a review of the event, interviews, the LER, associated CRs and otherapplicable documents, the inspectors determined the design change review in April 2002 for the S/G low-low level setpoint change was inadequate. The review did not take into account the impact of the S/G low-low level setpoint modification on the margin to accommodate S/G level changes due to operational transients. Unit 3 Final Safety Analysis Report, Chapter 15, Section 15.0.1.1, "Accident Analysis," states, "Condition Ioccurrences are accommodated with margin between any plant parameter and the value of that parameter which would require either an automatic or manual protectiveaction." The inspectors determined that the Condition I occurrences under consideration for the S/G low-low setpoint change included, in part, operational 17Enclosuretransients defined in FSAR, Chapter 15 such as step load changes (+/- 10 percent),ramp load changes (up to 5 percent/minute), and load rejection up to and including a design full load rejection transient. The design change review (DCN DM3-00-0077-02,"RPS, ESF, AMSAC Low Steam Generator Level Trip Setpoint Change") and associated 10 CFR 50.59 screening concluded that there was no impact on the nuclear steam supply system and balance of plant design bases. The design change had noevaluation or discussion of FSAR, Chapter 15 operational transients. However, as discussed in the LER, the direct cause of the trip was a low-low level in the "C" S/G that resulted from the shrink in S/G water level created by the manual turbine trip and that operation at the increased S/G low-low level setpoint (27 percent) reduced the marginavailable to accommodate S/G level transients that occur following a turbine trip at power. In addition, the inspectors identified that a license amendment should have beensubmitted for the S/G low-low level setpoint change pursuant to 10 CFR 50.59, "Changes, Tests, and Experiments." Specifically, a change to the S/G low-low setpoint Technical Specification (TS 2.2.1, Table 2.2-1, "Reactor Trip Instrumentation TripSetpoints") is required because the actual setting of the nominal trip setpoint (NTS)(27 percent) is not consistent with the Technical Specification stated value of the NTS(18 percent). The change to the S/G low-low NTS was made in April 2002 with no action identified to initiate a Technical Specification change. The performance deficiency associated with this finding is that Dominion did not conduct an adequate design change review associated with a S/G low-low level trip setpoint modification.

This led to a reduction in automatic protective action margin available to accommodate steam generator level changes for operational transients and resulted in an unintended reactor trip.Analysis. This finding is more than minor because it is associated with the DesignControl attribute of the Initiating Events cornerstone and affects the objective to limit the likelihood of those events that upset plant stability and challenge critical safety functionsduring shutdown as well as power operations. The finding is associated with an increase in the likelihood of initiating events in that a reactor trip actually occurred. The inspectors determined that the finding was of very low safety significance (Green)through performance of a Phase 1 SDP in accordance with IMC 0609, Appendix A, "Significance Determination of Reactor Inspection Findings for At-Power Situations."

Specifically, this finding did not involve a loss-of-coolant accident or external event initiators or contribute to both the likelihood of a reactor trip and the likelihood that mitigation equipment or functions will not be available. All safety systems performed asdesigned following the reactor trip. This finding is related to the cross-cutting aspect of human performance in that Dominion's review and decision making process was not effective at identifying possible unintended consequences when making assumptions for a risk significant design change.Enforcement. Code of Federal Regulations 10 CFR Part 50, Appendix B, Criterion III,"Design Control," states, in part, "design control measures shall provide for verifying or checking the adequacy of design, such as by the performance of design reviews, by the use of alternate or simplified calculational methods, or by the performance of a suitable 18Enclosuretesting program." Contrary to this requirement, in April 2002, Dominion did not conductan adequate design review of the S/G low-low level setpoint modification which led to an unanticipated reactor trip on December 1, 2006. This issue has been entered into Dominion's corrective action program as CR-06-04788. Corrective actions for this issue included plans to conduct an engineering analysis to determine new S/G Low-Low level setpoints and revision of the design change notice and the 10 CFR 50.59 screening. This issue is being treated as a non-cited violation consistent with Section VI.A of theEnforcement Policy (NCV 05000423/2006003-03, Did Not Adequately Evaluate aReactor Protection System Setpoint Modification).4OA5Other ActivitiesImplementation of Temporary Instruction (TI) 2515/165 - Operational Readiness of Offsite Power and Impact on Plant Risk

a. Inspection Scope

The objective of TI 2515/165, "Operational Readiness of Offsite Power and Impact onPlant Risk," was to gather information to support the assessment of nuclear power plant operational readiness of offsite power systems and impact on plant risk. The inspectorsevaluated Dominion procedures against the specific offsite power, risk assessment and system grid reliability requirements of TI 2515/165. They also discussed the attributeswith Dominion personnel.The information gathered while completing this TI was forwarded to the Office ofNuclear Reactor Regulation for further review and evaluation on April 3, 2006.

b. Findings

No findings of significance were identified.4OA6Meetings, Including ExitIntegrated Report Exit Meeting SummaryOn July 11, 2006, the resident inspectors presented the overall inspection results toMr. A. Skip Jordan and other members of his staff, who acknowledged the findings. The inspectors asked Dominion whether any of the material examined during the inspection should be considered proprietary. No proprietary information was identified.ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee personnel

J. Armstrong, Unit 2 Fire Protection Engineer
B. Bartron, Licensing
B. Burnham, I&C Engineer
G. Closius, Licensing
K. Cortis, AOV Program Coordinator
D. Dodson, Licensing
R. Fuller, Configuration Control
R. Griffin, Director, Nuclear Station Safety and Licensing
T. Ickes, IST Coordinator
A. Jordan, Director, Nuclear Station Operations and Maintenance
M. Kai, Safety Analysis
R. MacManus, Director, Nuclear Engineering
J. Mangeno, Unit 3 Fire Protection Engineer
A. Price, Site Vice President - Millstone
N. Sacco, Configuration Control
J. Semancik, Unit 3 Assistant Operations ManagerNRC pers onnel
J. C. Benjamin, Resident Inspector, Division of Reactor Projects (DRP)
J. A. Bobiak, Reactor Inspector, Division of Reactor Safety (DRS)
G. Johnson, Reactor Inspector, DRS
S. R. Kennedy, Resident Inspector, DRP
S. M. Schneider, Senior Resident Inspector, DRP
N. S. Sieller, Reactor Engineer, DRP

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and

Closed

05000423/2006003-01NCVDid Not Evaluate and Correct aSignificant Condition Adverse to

Quality Associated with Gravity Feed

Boration Lines (1R04)05000336/2006003-02FINDid Not Identify or Evaluate AirVoids Located in Auxiliary

Feedwater System (1R15.1)

A-2Attachment05000423/2006003-03NCVDid Not Adequately Evaluate aReactor Protection System Setpoint

Modification (4OA3.2)

Closed

05000423/2005-004-00LERPressurizer Spray Nozzle WeldIndications (4OA3.1)05000423/2005-005-00, 01LERAutomatic Reactor Trip of MillstoneUnit 3 Due to Low-Low Steam

Generator Level (4OA3.2)

LIST OF DOCUMENTS REVIEWED

Section 1R01: Adverse Weather ProtectionAOP-2560, Revision 010-01, Storms, High Winds, and High TidesSP-2615, Revision 006-01, Flood Level Determination