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 Start dateReport dateSiteReporting criterionSystemEvent description
ENS 571159 May 2024 12:00:00Beaver Valley10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition
10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
The following information was provided by the licensee via phone and email: At 0800 EDT on May 9, 2024, it was identified during leak rate testing that through-wall flaws existed on reactor plant river water piping inside the containment building. This determination resulted in a containment bypass condition such that a gaseous release could have occurred at a location not analyzed for a release in the loss of coolant accident dose consequence analysis. This condition is not bounded by existing design and licensing documents. Evaluation of the condition of the piping is ongoing to support repair prior to startup. With the plant currently in cold shutdown, the containment, as specified in Technical Specification 3.6.1, is not required to be operable. There was no impact on the health and safety of the public or plant personnel. This event is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(ii)(A), 10 CFR 50.72(b)(3)(ii)(B), and 10 CFR 50.72(b)(3)(v)(C). The NRC Resident Inspector has been notified.
ENS 5709225 April 2024 21:55:00Perry10 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionResidual Heat RemovalThe following information was provided by the licensee via phone and email: On April 25, 2024, it was determined that between March 25, 2024, 2015 (EDT) and March 30, 2024, 2024 (EDT), the condensate transfer and storage system was employed as a method of alternate keepfill in place of the installed residual heat removal (RHR) systems waterleg pump for RHR system loops `B and `C. This condition is not bounded by existing design and licensing documents. Therefore, this condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(ii)(B). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 569579 February 2024 18:22:00Peach Bottom10 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionService water
Reactor Protection System

The following information was provided by the licensee via email: On 2/9/24 at 1322 EST, it was determined that the unit was in an unanalyzed condition. A review of DC feeder circuit protection schemes identified a circuit for the fuel pool cooling system is uncoordinated due to inadequate fuse sizing. This results in a concern that postulated fire damage in one area could cause a short circuit without adequate protection, leading to the unavailability of equipment credited for in 10 CFR 50 Appendix R, Fire Safe Shutdown. This condition is not bounded by existing design and licensing documents; however, it poses no impact to the health and safety of the public or plant personnel. Therefore, this event is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(ii)(B). The postulated event affects the following fire zones: fire areas 6S and 6N (within the Unit 2 reactor building). Compensatory actions for affected fire areas have been implemented. An extent of condition review is being performed. The NRC Senior Resident Inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: Fire watches have been established in the affected areas. These will be maintained until the protection scheme is revised.

  • * * UPDATE ON 03/08/24 FROM PAUL BOKUS TO TOM HERRITY * * *

The following updated information was provided by the licensee via email and phone call: On 03/08/24 at 1418, extent of condition reviews identified circuit(s) in the Units 2 and 3 Reactor Protection Systems (RPS) which are also uncoordinated due to improper fuse sizing. These circuits are not bounded by existing design and licensing documents for 10 CFR 50 Appendix R Fire Safe Shutdown and, therefore, this event is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(ii)(B). This event poses no impact to the health and safety of the public or plant personnel. The postulated event affects the following fire areas: 32, 33, 38 and 39 (Units 2 and 3 Switchgear Rooms). In accordance with procedural requirements, compensatory actions for the affected fire areas have been implemented and will remain until the condition is resolved. The NRC Senior Resident Inspector has been notified. Notified R1DO (Arner)

  • * * UPDATE ON 3/13/2024 AT 1538 FROM TROY RALSTON TO SAM COLVARD * * *

On March 13, 2024, at 1350 EDT, extent of condition reviews identified a circuit in the Unit 2 reactor protection system (RPS) which is also uncoordinated due to improper fuse sizing. This circuit is not bounded by existing design and licensing documents for 10 CFR 50, Appendix R, Fire Safe Shutdown, therefore, this event is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(ii)(B). This event poses no impact to the health and safety of the public or plant personnel. The postulated event affects fire area 57 (Switchgear Corridor, common to Units 2 and 3). In accordance with procedural requirements, compensatory actions for the affected fire areas have been implemented and will remain until the condition is resolved. Additionally, it was previously reported that fire area 6N contained a circuit which was not bounded by the Fire Safe Shutdown analysis; however, after further review it has been determined that compliance is maintained in this fire area and is therefore retracted from the scope of this report. The NRC Senior Resident Inspector has been notified. Notified R1DO (Jackson)

  • * * UPDATE ON 3/21/2024 AT 1525 FROM PAUL BOKUS TO IAN HOWARD * * *

The following information was provided by the licensee via email: On 03/21/24 at 1211, extent of condition reviews identified an annunciator circuit for the Unit 3 emergency service water (ESW) and high pressure service water (HPSW) pump structure heating and ventilation panel that is also uncoordinated due to improper fuse sizing. This circuit is not bounded by existing design and licensing documents for 10 CFR 50 Appendix R Fire Safe Shutdown and, therefore, this event is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(ii)(B). This event poses no impact to the health and safety of the public or plant personnel. The postulated event affects fire area 47 (Unit 3 pump structure for `B' ESW and `3A'-`3D' HPSW pumps) and the yard fire area (Manhole 026D). In order to restore immediate compliance, the cable has been de-energized to eliminate the possibility of the event of concern. This circuit will remain de-energized or other measures will be implemented until the condition is permanently resolved. The NRC Senior Resident Inspector has been notified. Notified R1DO (Ford)

ENS 5692818 January 2024 20:04:00Columbia10 CFR 50.72(b)(3)(v)(B), Loss of Safety Function - Remove Residual Heat
10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition
Service water
Residual Heat Removal
Spray Pond

The following information was provided by the licensee via email: On January 18, 2024, at 0030 PST, diesel generator 2 (DG2) was shut down following a monthly surveillance run. Subsequently, a leak was discovered in the DG2 building. Service water pump '1B' was secured at 0117, effectively stopping the leak. The leak was determined to be service water coming from a diesel generator mixed air cooling coil. Service water system 'B' and DG2 were subsequently declared inoperable at 0135. After discussion with engineering, it was identified that the amount of service water leakage from the cooling coil was assumed to be greater than the leakage allowed by the calculation to assure adequate water in the ultimate heat sink to meet the required mission time of 30 days. At 1204, it was determined that entry into Technical Specification 3.7.1 condition D was warranted since the assumed leakage from the cooling coil could exceed the calculated allowed value. At 1238, the control power fuses for service water pump '1B' were removed. DG2 and service water system 'B' were declared unavailable, and the technical specification condition for the inoperable ultimate heat sink was exited. With the control power fuses removed, the pump is kept from auto starting, effectively preventing the leak and ensuring the safety function of the ultimate heat sink is maintained while the cooling coil is repaired or replaced. Due to the leakage assumed greater than the calculated allowable value this condition is reportable per 10 CFR 50.72(b)(3)(ii)(B) as an unanalyzed condition and per 10 CFR 50.72(b)(3)(v)(B) as an event or condition that could have prevented fulfillment of the safety function of structures or systems that are needed to remove residual heat. There was no impact to the health and safety of the public. The NRC Resident has been notified.

  • * * RETRACTION ON 3/18/24 AT 1923 FROM VALERIE LAGEN TO KAREN COTTON * * *

The following information was provided by the licensee via email: On January 18, 2024 at 2138 EST, Columbia Generating Station notified the NRC under 10 CFR 50.72(b)(3)(ii)(B) of an unanalyzed condition on the available capacity of the ultimate heat sink (UHS) and under 10 CFR 50.72(b)(3)(v)(B) of an event or condition that could have prevented fulfillment of the safety function of structures or systems needed to remove residual heat. On January 18, 2024, following monthly surveillance of the diesel generator DG2, a DG2 room cooler flow alarm was received at 0115. A leak was discovered in the diesel mixed air (DMA) air handler unit. Service Water Pump '1B' was secured and the leakage was stopped at 0117. The service water system 'B' and diesel generator system 'B' were declared inoperable at 0135. The leak was assumed to be greater than that allowed to ensure adequate water in the UHS required to meet the 30-day mission time, and the UHS was declared inoperable at 1204. Control power fuses for the service water pump '1B' were removed to fully eliminate the leakage path from the cooler, and the UHS was declared operable at 1238. Following the event, engineering performed an analysis based on the size and location of the leak, and concluded it would have taken 1.4 days to deplete the available excess water in the UHS to below the minimum technical specification required water level of the spray pond. Operations were able to secure the service water subsystem of the UHS prior to exceeding the volumetric margins in the spray ponds to ensure the 30-day mission time was met. The condition did not represent a safety significant unanalyzed condition nor a loss of safety function. The NRC Resident Inspector has been notified. Notified R4DO (Gepford).

ENS 5691028 December 2023 16:29:00Watts Bar10 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionThe following information was provided by the licensee via email: Plant alignment caused an unanalyzed condition regarding unit 1 and unit 2 Appendix R procedures. (Watts Bar Nuclear) (WBN) unit 1 and unit 2 Appendix R procedures require manual operator action times including (volume control tank) (VCT) isolation. They are calculated with an assumed hydrogen cover gas constant at 20 psig. This is to preclude hydrogen ingestion into the charging pumps with an operator action time of 70 minutes. Due to recent lower hydrogen concentration in the (reactor coolant system) (RCS), (unit 2) VCT hydrogen regulator set point was increased to 28 psig. This increased pressure set point invalidated the initial assumptions made in the Appendix R calculations for manual operator action times. WBN unit 1 VCT hydrogen regulator was also verified high out of band at 22 psig. WBN has restored unit 1 and unit 2 VCT hydrogen regulators to the required specification. The NRC Resident Inspector has been notified of this condition.
ENS 5684910 November 2023 21:45:00Waterford10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition

The following information was provided by the licensee via email: At 1545 CST on November 10, 2023, personnel at Waterford Steam Electric Station Unit 3 determined that 19 conduits in the engineered safety features actuation system (ESFAS) auxiliary relay cabinets A and B did not have the required fire seals for bay separation. This condition meets the criteria involving an unanalyzed condition that significantly affects plant safety. The plant is currently defueled. Decay heat is being removed by normal spent fuel cooling system operations. ESFAS is not required to be operable in the current plant mode. This event is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(ii)(B) as an unanalyzed condition that significantly degrades plant safety. There was no impact to the health and safety of the public or plant personnel. The NRC Region 4 Branch Chief (Dixon) has been notified.

  • * * RETRACTION ON 1/8/2024 AT 1222 EST FROM PETER RAMON TO ERNEST WEST * * *

On November 10, 2023, Waterford Steam Electric Station Unit 3 reported in EN 56849 that 19 conduits in engineered safety features actuation system (ESFAS) auxiliary relay cabinets A and B did not have the required fire seals for bay separation. This condition met the criteria involving an unanalyzed condition that significantly affects plant safety. Waterford 3 has determined that the ESFAS auxiliary relay cabinets A and B jumper conduits do not require fire seals based on review of an engineering specification that specifies the size and length of conduits which require fire seals to be installed. None of the nineteen affected conduits meet the size and length criteria that would necessitate installation of a fire seal. Based on this, the condition described in EN 56849 is not considered to be an unanalyzed condition that significantly affects plant safety as described in 10 CFR 50.72(b)(3)(ii)(B) and therefore is not reportable. The licensee notified the NRC Resident Inspector. Notified R4DO (Gaddy)

ENS 566106 July 2023 16:32:00Millstone10 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionSteam Generator
Main Steam Isolation Valve
Auxiliary Feedwater
Main Steam Line
The following information was provided by the licensee via email: On July 6, 2023, at 1232 EDT, while operating in Mode 1 at 100 percent power, the supply check valve from the number 2 steam generator to the turbine driven auxiliary feedwater pump was determined during troubleshooting that it is not able to perform its isolation function. This failure would have resulted in the blowdown of both steam generators during a main steam line break in the number 2 steam generator main steam line upstream of the main steam isolation valves until the operators could isolate the faulted steam generator. Previous evaluation has determined that this condition constituted an unanalyzed condition that could impact containment pressure. There was no radioactive release to the environment. The steam line from the steam generator to the turbine driven auxiliary feedwater pump was isolated by use of a motor operated valve in the discharge line of the number 2 steam generator. There was no impact to Unit 3 which remains at 100 percent power. The NRC Senior Resident Inspector was notified. This condition is being reported pursuant to 10 CFR 50.72(b)(3)(ii)(B) as a condition that resulted in the nuclear power plant being in an unanalyzed condition that significantly degrades plant safety.
ENS 5656911 June 2023 05:30:00Beaver Valley10 CFR 50.72(b)(3)(v)(B), Loss of Safety Function - Remove Residual Heat
10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition
The following information was provided by the licensee via email: At 0130 EDT on June 11, 2023, it was discovered that the Beaver Valley Power Station, Unit No. 2 auxiliary building door A-35-5A, credited for tornado missile protection of the primary component cooling water system, was open and unlatched. Upon discovery, the door was shut and latched. This event is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(ii)(B) and 10 CFR 50.72(b)(3)(v)(B). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 5654125 May 2023 17:45:00Watts Bar10 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionEmergency Diesel GeneratorThe following information was provided by the licensee via phone and email: At 1345 EDT on May 25, 2023, it was determined that a fire barrier for area 737-A1B was not installed, and would render the 2A Emergency Diesel Generator (EDG) not operable in the event of a fire on the Unit 2 side of elevation 737 in the Auxiliary Building. The 2A EDG is the credited power source for fire safe shutdown for a fire located in this area. Without the credited source of power, this places WBN U2 (Watts Bar Nuclear Unit 2) in an unanalyzed condition. A fire watch has been established in the area until the issue is resolved. Therefore, this event is being reported as an eight-hour non-emergency notification per 10 CFR 50.72(b)(3)(ii)(B). The NRC Resident Inspector has been notified.
ENS 564556 April 2023 20:46:00Perry10 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionMain Steam Isolation Valve
Main Steam Line
The following information was provided by the licensee via phone and email: On March 4, 2023, it was determined that the main steam line (MSL) local leak rate test results for MSL 'B' were in exceedance of technical specification (TS) surveillance requirement (SR) 3.6.1.3.10 limits. Additionally, the leakage at the outboard main steam isolation valve (MSIV) 'B', was indeterminate due to a gross packing gland leak. An engineering calculation dated April 6, 2023, showed that this leakage, in conjunction with a design basis loss of coolant accident, would result in the radiological dose exceeding Updated Safety Analysis Report limits to the exclusion area boundary, the low population zone, and the control room. Therefore, this condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(ii)(B) as a condition that results in the power plant being in an unanalyzed condition that degrades plant safety. Both inboard and outboard 'B' MSIVs have been reworked and are within the TS SR limits. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 5635012 February 2023 13:00:00Beaver Valley10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition
Control Room Emergency Ventilation

The following information was provided by the licensee via phone call and email: At 0800 on February 12, 2023, it was discovered that both trains of control room emergency ventilation system were simultaneously inoperable due to a safety injection relief valve discharging to a Unit 1 sump. This leakage in conjunction with design basis loss of coolant accident may result in radiological dose exceeding limits to the exclusion area boundary and to the control room, which is common to both Unit 1 and Unit 2. Therefore, this condition is being reported as an eight-hour, nonemergency notification per 10 CFR 50.72(b)(3)(ii)(B) and 10 CFR 50.72(b)(3)(v)(D) as an 'Unanalyzed Condition and a Condition that Could Have Prevented Fulfillment of a Safety Function.' There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.

  • * * RETRACTION FROM ROBERT TAYLOR TO DONALD NORWOOD AT 0530 EDT ON 3/17/2023 * * *

Retraction of EN56350, Control Room Emergency Ventilation System Inoperable: Based on subsequent evaluation, it was determined that the control room emergency ventilation system remained operable due to the maximum measured leak rate being within the bounds of the analysis. The maximum measured leak rate of 32,594 cc/hr from the safety injection system did not challenge the calculated maximum engineered safety features leak rate of 45,600 cc/hr and remained within the current dose analysis limits. As such, this was not an unanalyzed condition and did not prevent the fulfillment of a safety function to mitigate the consequences of an accident. The NRC Resident Inspector has been notified. Notified R1DO (Bickett).

ENS 5589613 May 2022 16:11:00Monticello10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition
Steam Jet Air Ejector
Control Room Envelope
The following information was provided by the licensee via email: On 5/13/22 at 1111 CDT the station entered LCO 3.7.4 Condition B for Control Room Envelope being inoperable. This was due to results from an inspection in the Steam Jet Air Ejector room that identified steam leakage exceeding the leakage rate assumptions made in the Alternate Source Term (AST) dose analysis calculation. Therefore, this is being reported in accordance with 10CFR50.72(b)(3)(ii)(B) for an unanalyzed condition that significantly degrades plant safety and 10CFR50.72(b)(3)(v)(D) for any event or condition that at the time of discovery could have prevented fulfillment of the safety function of structures or systems that are needed to mitigate the consequences of an accident. There is no impact to the health and safety of the public. NRC Resident has been notified.
ENS 5557614 November 2021 16:50:00Millstone10 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionSteam Generator
Main Steam Isolation Valve
Auxiliary Feedwater
Main Steam Line
On November 14, 2021, at 1150 EST, while operating in Mode 1 at 100 percent power, the supply check valve from the Number 2 steam generator to the turbine driven auxiliary feedwater pump was determined during troubleshooting that it is not able to perform its isolation function. This failure would have resulted in the blowdown of both steam generators during a main steam line break in the Number 2 steam generator main steam line upstream of the main steam isolation valves until the operators could isolate the faulted steam generator. Previous evaluation has determined that this condition constituted an unanalyzed condition that could impact containment pressure. There has been no radioactive release to the environment. The steam lines from the steam generators to the turbine driven auxiliary feedwater pump have been isolated by use of a motor operated valve in the discharge line of the Number 2 steam generator. There has been no impact to Unit 3 which remains at 100 percent power. The NRC Senior Resident has been notified. This condition is being reported pursuant to 10 CFR 50.72(b)(3)(ii)(B) as a condition that resulted in the nuclear power plant being in an unanalyzed condition that significantly degrades plant safety.
ENS 555656 November 2021 15:00:00Millstone10 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionSteam Generator
Feedwater
Main Steam Isolation Valve
Auxiliary Feedwater
Main Steam Line
During a Unit 2 refueling outage valve overhaul activity on the steam supply check valve from the number 2 steam generator to the turbine driven auxiliary feedwater pump, 2-MS-4B, the check valve was found with its disc separated from the disc arm. This failure would have resulted in the blowdown of both steam generators during a main steam line break in the steam generator number 2 main steam line upstream of the main steam isolation valves until the operators could isolate the faulted steam generator. On November 6, at approximately 1100 EDT evaluation determined that this condition constituted an unanalyzed condition that could impact containment pressure. There has been no radioactive release to the environment. The valve has been repaired. The check valve in the steam supply from the number 1 steam generator to the turbine driven auxiliary feedwater pump was inspected and found to be satisfactory. There has been no impact to Unit 3 which remains at 100% power. The Senior Resident has been notified. This condition is being reported pursuant to 10 CFR 50.72(b)(3)(ii)(B) as a condition that resulted in the nuclear power plant being in an unanalyzed condition that significantly degrades plant safety.
ENS 5545913 September 2021 22:22:00Surry10 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionEmergency Diesel GeneratorOn September 13, 2021, at 1822 EDT, an apparent non-compliance with 10 CFR 50, Appendix R, section III.G.2 (separation of redundant fire safe shutdown equipment) was identified. Specifically, it was determined that some Emergency Diesel Generator (EDG) cables may be susceptible to a hot short/spurious operation to the close circuit. A spurious closure of the emergency bus normal supply breakers after the EDG is powering the bus could result in non-synchronous paralleling, EDG overloading, or EDG output breaker tripping due to faulted power cable from normal supply breaker. The spurious closure of the normal supply breakers is not currently addressed in the Appendix R Report or previous Multiple Spurious Operations (MSO) analysis. This condition is associated with the Appendix R safe-shutdown function of the Emergency Power System. The Emergency Power System is considered operable but not fully qualified for its safety-related design function. The following fire areas are impacted: 1) Fire Area 13, Unit 1 Normal Switchgear Room 2) Fire Area 46, Unit 1 Cable Tray Room 3) Fire Area 3, Unit 1 Emergency Switchgear and Relay Room 4) Fire Area 2, Unit 2 Cable Vault and Tunnel Until this condition is analyzed, Surry has implemented mitigating actions in the above fire areas. This condition is being reported pursuant to 10 CFR 50.72(b)(3)(ii)(B). This is also reportable as a 60-day written report pursuant to 10 CFR 50.73(a)(2)(ii)(B). This event was entered into the licensee's Corrective Action Program as CR (condition report) 1180502. The NRC Resident Inspector has been notified of this event. Mitigating actions include posting fire watches in the affected areas.
ENS 5542724 August 2021 18:06:00FitzPatrick10 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionDuring an extent of condition review of DC control circuits, it was identified there are additional unprotected DC control circuits which are routed between separate Appendix R fire areas. A postulated fire in one area can cause a short circuit and potentially result in secondary fires or cable fires in other fire areas where the cables are routed. The secondary fires or cable failures degrade the degree of separation for redundant safe shutdown trains and are outside the assumptions of the 10 CFR 50 Appendix R Safe Shutdown Analysis. This condition is reportable in accordance with 10 CFR 50.72(b)(3)(ii)(B). Compensatory actions for affected fire areas have been implemented. Design modifications in the affected control circuits are being developed and will be scheduled to correct this condition.
ENS 5537522 July 2021 21:51:00North Anna10 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionEmergency Diesel GeneratorOn July 20, 2021, at 1707 EDT, an apparent non-compliance with 10 CFR 50, Appendix R, section III.G.2 (separation of redundant fire safe shutdown equipment) was identified. This issue was initially categorized as not affecting train separation or the ability of the equipment to perform their Design Basis functions. The original concern was entered into the licensee's Corrective Action Program as CR1177199. Subsequently, on July 22, 2021, at 1751 EDT, a further review of the affected control circuits for the Unit 1 and Unit 2 Emergency Diesel Generator (EDG) output breakers and emergency bus feeder breakers identified a concern that breaker position interlocks routed to or through non-safety related components or spaces may affect the ability to provide emergency power on the affected unit due to impacts on the control power circuits during an Appendix R fire associated with a loss of offsite power. The following are the affected fire areas: - Unit 1 and Unit 2 Turbine Buildings - Unit 1 and Unit 2 Cable Spreading Rooms - Unit 1 and Unit 2 Normal (307) Switchgear Rooms This condition is being reported pursuant to 10 CFR 50.72(b)(3)(ii)(B). This is also reportable as a 60-day written report pursuant to 10 CFR 50.73(a)(2)(ii)(B). This event was entered into the licensee's Corrective Action Program as CR 1177399. The NRC Resident Inspector has been notified of this event.
ENS 5532122 June 2021 16:08:00Davis Besse10 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionAuxiliary FeedwaterAt 1208 (EDT) on 6/22/2021, the high-energy line break door separating Auxiliary Feedwater Train Rooms 1 and 2 was not able to be latched following normal usage. The door was able to be closed, protecting Train 1 equipment from a break in Room 2. However, it is assumed a break in Room 1 would push the unlatched door open and allow high-energy fluids to enter Room 2. This condition is not bounded by existing design and licensing documents; however, it poses no impact to the health and safety of the public or plant personnel. The door was able to be latched at 1215 (EDT) on 6/22/2021 following repairs to the door latch interlocking mechanism. Therefore, this event is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(ii)(B). No other equipment was inoperable during this event. The NRC Resident Inspector has been notified.
ENS 552313 May 2021 13:30:00Fermi10 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionAt 0930 EDT on 5/3/2021, it was determined that during entries into the Fermi 2 Reactor Building Steam Tunnel (RBST) on 4/17/2021, 4/18/2021, and 4/21/2021 that the door was not controlled according to site procedures. The RBST door is credited as a hazard barrier for various high-energy line break (HELB) scenarios. On the identified dates, the RBST door was left open for brief periods during maintenance related activities in the RBST. This condition is not bounded by existing analyses as the door is assumed to be closed throughout a HELB event. The time period that the door was open was less than one hour in each case, as stay times in the room are inherently limited by industrial and radiological conditions. Individuals remained in the area to close the door if needed, but existing analyses do not address the ability to perform those actions under all HELB scenarios. There is no impact to the health and safety of the public or plant personnel as the door is currently closed and latched and access into the area has been restricted to normal ingress and egress per site procedures, which ensures consistency with existing analyses. Therefore, this event is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(ii)(B). Investigation into the cause is ongoing. Preliminary review of the extent of this condition identified entries into the RBST on other occasions during the past three years where the conditions may also have not been bounded by existing analyses. The additional occasions where the door may have been held open were on 9/22/2018 (MODE 3), 10/26/2018 (MODE 1 ), 11/2/2018 (MODE 1), and 3/21/2020 (MODE 3). Each of these instances was also less than one hour with the exception of the occurrence beginning on 10/26/2018 which lasted approximately 10 hours to support packing leak repairs on a HPCI (High Pressure Coolant Injection) Outboard Isolation Valve. The licensee notified the NRC Resident Inspector.
ENS 5480630 July 2020 13:15:00Callaway10 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionEmergency Core Cooling System

EN Revision Imported Date : 8/18/2020 EMERGENCY PROCEDURE ERROR POTENTIALLY PREVENTING TIMELY COMPLETION OF EMERGENCY CORE COOLING SYSTEM RECIRCULATION ALIGNMENT At 0815 CDT on 7/30/2020, it was determined that a procedural error in emergency procedure ES1.3, Transfer to Cold Leg Recirculation, could delay realignment from emergency core cooling system (ECCS) injection phase to recirculation phase under lower plant operational modes. It is noted this scenario is postulated to occur only when the boron dilution mitigation system is operable in lower modes of operation as per Technical Specification 3.3.9 (required operable in Mode 2 (below P-6), 3, 4 and 5). Current plant conditions require this feature nonfunctional so this issue does not impact current plant conditions. This condition is not bounded by existing design and licensing documents; however, it poses no current impact to the health and safety of the public or plant personnel. Therefore, this event is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(ii)(B). The NRC Resident Inspector has been notified.

  • * * RETRACTION ON 8/17/2020 AT 1603 EDT FROM JOSH COPELAND TO KERBY SCALES * * *

Event Notification (EN) 54806, made on 7/30/2020, is being retracted because re-evaluation performed subsequent to the notification has demonstrated that the error in Emergency Operating Procedure ES1.3 would not have resulted in a condition outside of the current licensing basis analyses of record for the Callaway Plant. This re-evaluation addressed core effects, containment pressure-temperature and radiological consequences analyses, documented in the plant's corrective action program. The re-evaluation has led to the conclusion that the procedural error in ES1.3 would not have prevented any system required to be OPERABLE by the Technical Specifications from performing its specified safety functions. With all systems capable of performing their specified safety functions, the current licensing basis analyses of record for Callaway Plant remain valid and bounding. Based on these considerations, it has been determined that the condition reported in EN 54806 did not result in the plant being in an unanalyzed condition that significantly degraded plant safety. Consequently the condition did not meet the criteria for an 8-hour notification per 10 CFR 50.72(b)(3)(ii)(B) for an unanalyzed condition that significantly degrades safety. The NRC Resident Inspector has been notified of this Event Notification retraction. Notified R4DO (Taylor)

ENS 5453320 February 2020 17:40:00FitzPatrick10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition(On February 20, 2020, at 1240 EST, the Licensee determined the following information:) This notification is in reference to reports EN 54130 and LER 2019-002, which were retracted. James A. FitzPatrick Nuclear Power Plant received additional information on the technical basis for the retraction. Further review, including testing of the terminal blocks, demonstrated that the short circuit current would result in heat levels in excess of cable insulation ratings. Unprotected DC control circuits for non-safety related DC motors are routed between separate fire areas. A postulated fire in one area can cause a short circuit and potentially result in secondary fires or cable fires in other fire areas where the cables are routed. The secondary fires or cable failures degrade the degree of separation for redundant safe shutdown trains and are outside the assumptions of the 10 CFR 50 Appendix R Safe Shutdown Analysis. This condition is reportable in accordance with 10 CFR 50.72(b)(3)(ii)(B). Compensatory actions per the Technical Requirements Manual (TRM) for affected fire areas have been implemented. A modification to install fuses in the control circuits for 94P-2(M), 31P-7A(M), 31P-7B(M), and 94P-13(M) has been scheduled and shall correct this condition. The NRC Resident Inspector has been notified.
ENS 5448722 January 2020 03:18:00Sequoyah10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition

EN Revision Imported Date : 2/21/2020 CONTAINMENT RELIEF VALVES INOPERABLE At 22:18 (EST) on 1/21/20, it was discovered that all Unit 1 containment vacuum relief isolation valves were closed and all vacuum relief lines were simultaneously inoperable; therefore, this condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v). The isolation valves were opened and the vacuum relief valves were restored to operable. There is no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.

  • * * UPDATE ON 02/20/2020 AT 1626 EST FROM FRANK SCHULTE TO BRIAN P. SMITH * * *

At 1549 (EST), February 20, 2020, a completed engineering evaluation of the condition initially reported on January 22, 2020 determined that the inoperability of the Sequoyah Unit 1 Containment Vacuum Relief System affected the ability to protect containment against an external pressure event. This condition is not bounded by existing design and licensing documents; however, it poses no impact to the health and safety of the public or plant personnel. The condition was resolved when isolation valves were opened on January 21, 2020 and the vacuum relief lines were restored to an operable status. Therefore, this event is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(ii)(B), "an unanalyzed condition that significantly degrades plant safety. Subsequent to the initial notification, continued evaluation of the reported condition has concluded that the isolation of the containment vacuum relief function did not prevent the fulfillment of a safety function that is needed to control the release of radioactive material; nor mitigate the consequences of an accident therefore this event is not reportable under 10 CFR 50.72(b)(3)(v), "Event or Condition that could have prevented fulfillment of a safety function. The NRC Resident has been notified. Notified R2DO (Musser)

ENS 5443711 December 2019 18:56:00Surry10 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionService water
Auxiliary Feedwater
Main Steam
On December 11, 2019, at 1356 EST, it was concluded that certain safety-related equipment is vulnerable to design basis tornado missiles which could render the equipment inoperable and not able to perform its design function. This applies to the following Technical Specification equipment: 1. Component cooling water piping for the 'A' spent fuel cooling water system heat exchanger. This heat exchanger is vulnerable to a horizontal missile traveling through the roll-up door, which would challenge operability of the Technical Specification required component cooling system equipment. 2. All three (3) emergency service water pumps and their diesel fuel oil supply tank. The emergency service water pumps and diesel fuel oil tank are vulnerable to a horizontal missile penetrating the missile screens. 3. Certain component cooling water system pump discharge piping is vulnerable from a vertical missile penetrating the auxiliary building roof. 4. The Unit 1 auxiliary feedwater (AFW) system pumps and the pump suction and discharge piping are vulnerable to a missile traveling through the screens on the sides and roof of the main steam valve house. This vulnerability also exists for the Unit 2 AFW. This condition puts Unit 1 and 2 into Technical Specification 3.01 which requires the units to be in hot shutdown within 6 hours and in cold shutdown within the following 30 hours. The NRC Resident Inspector has been notified.
ENS 544255 December 2019 14:10:00Cooper10 CFR 50.72(b)(3)(v)(B), Loss of Safety Function - Remove Residual Heat
10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition
The following was received via email from Cooper Nuclear Station: At 0810 (CST), on 12/5/19, Operations personnel discovered BLDG-DOOR-R209, FIRE DOOR BETWEEN CRITICAL SWITCHGEAR ROOMS F & G, was unlatched. The door was immediately latched upon discovery. Based on door logs, the door separating the two critical switchgear rooms was inadvertently left unlatched for approximately 5 minutes. This door is a Steam Exclusion Boundary (SEB) door. It is required to be closed and latched when the Auxiliary Steam Boiler is in service due to Auxiliary Steam piping passing through Critical Switchgear Room 'G'. If a steam line break was to occur with the door unlatched, steam could render both Critical Switchgear busses inoperable. This is being reported under 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition, and 10 CFR 50.72(b)(3)(v), Any event or condition that at the time of discovery could have prevented the fulfillment of the safety function of structures or systems that are needed to (B) remove residual heat and to (D) mitigate consequences of an accident. There was no impact on the health and safety of the public or plant personnel. The door closes automatically and appeared to have been left unlatched by the last person passing through. The door was tested and latches as required. The licensee notified the NRC Resident Inspector.
ENS 5441730 November 2019 19:00:00Diablo Canyon10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition
Containment SprayOn November 30, 2019, at 1100 PST, with Unit 2 in Mode 4, Operations identified that both trains of containment spray had been removed from service earlier at approximately 0217 hours as part of preparations for a planned Mode 5 entry. The containment spray pumps are required to be operable (along with the containment fan cooler units) in Modes 1 through 4 in accordance with Technical Specification 3.6.6. With both containment spray pumps inoperable, TS 3.6.6 Action F requires the Unit to be shut down in accordance with TS 3.0.3. At 1125 hours, both trains of containment spray were returned to operable and the required actions of TS 3.6.6 and TS 3.0.3 were exited. The five containment fan cooler units remained operable for the duration of the occurrence. This notification is being made in accordance with the requirement of 10 CFR 50.72(b)(3)(v) as an event or condition that could have prevented fulfillment of a safety function, and 10 CFR 50.72(b)(3)(ii) as an event or condition that may have resulted in the plant being in an unanalyzed condition. The NRC Senior Resident Inspector has been notified.
ENS 543662 November 2019 19:15:00Beaver Valley10 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionAt 1515 on November 2, 2019, the Refueling Water Storage Tank (RWST) was declared inoperable due to a Low Head Safety Injection relief valve discharging to the Safeguards Sump during routine surveillance testing. The leakage from the Low Head Safety Injection system in conjunction with a postulated Design Basis Accident (DBA) Loss of Coolant Accident (LOCA) with transfer to Safety Injection Recirculation may result in dose exceeding the Dose Analysis of the Exclusion Area Boundary (EAB) and the Control Room, which is common to both Unit 1 and Unit 2. This condition may not be bounded by existing design and licensing documents; however, it poses no impact to the health and safety of the public or plant personnel. The Low Head Safety Injection relief valve has been isolated to prevent further leakage, and makeup to the RWST completed. At 1602 on November 2, 2019 the RWST was declared Operable. This event is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(ii)(B) and 10 CFR 50.72(b)(3)(v)(B), (C), (D) as an Unanalyzed Condition and a condition that could have prevented the Fulfillment of a Safety Function." The licensee notified the NRC resident inspector.
ENS 5426611 September 2019 00:34:00Browns Ferry10 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionRemote shutdownA lightning strike occurred at approximately 1502 CDT on 09/10/2019, and a resulting power surge damaged some of the security door card reader system equipment. However, this did not affect access to plant areas for personnel who were already within protected area. At 1830 on 09/10/2019, it was discovered that some of the oncoming night shift personnel could not access particular areas that required the use of security card readers. Extent of condition check at 1934 on 09/10/2019 determined that access to 1A and 3A Electric Board Rooms, which contain remote shutdown panels and Fire Safe Shutdown equipment. was prohibited for the night shift personnel. This condition is reportable under 10 CFR 50.72(b)(3)(ii)(B) - Any event or condition that results in the nuclear power plant being in an unanalyzed condition that significantly degrades plant safety. Access was restored to all plant areas at 2106 on 9/10/2019. No plant events occurred during the time frame that the 1A & 3A Electric Board Rooms inaccessible that would have required access to these areas. The NRC Resident Inspector has been notified.
ENS 542576 September 2019 02:15:00South Texas10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Reactor Coolant System

EN Revision Text: CONTAINMENT PENETRATION DISCOVERED NOT ISOLATED At 2115 CDT on 9/5/2019, an inside containment test connection and inoperable outside containment isolation valve were discovered to be open for a containment air sample penetration. This resulted in the containment penetration not being isolated. The inside containment test connection was closed at 2322 CDT on 9/5/2019.

This event is being reported under 10 CFR 50.72(b)(3)(v)(C) and (D) and 10 CFR 50.72(b)(3)(ii)(B).

There was no impact to the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.

  • * * UPDATE FROM PAUL BURTON TO HOWIE CROUCH AT 1342 EST ON 11/7/19 * * *

This event was originally reported on September 6, 2019 under 10 CFR 50.72(b)(3)(v)(C) and (D) and 10 CFR 50.72(b)(3)(ii)(B). Upon completion of the investigation of the event, it was determined that the event had insignificant safety consequences because the containment breach was disconnected from the Reactor Coolant System by a series of closed valves for the duration of the event. Additionally, the lines to the inside containment connection and the outside inoperable containment isolation valve that was found to be open as well as the main line connecting and passing through the penetration were one-inch diameter lines. Analysis determined that containment breaches that are less than a three-inch diameter do not lead to a large radiation release. The event did not place the plant in an unanalyzed condition that significantly degrades plant safety. Therefore, 10 CFR 50.72(b)(3)(ii)(B) did not apply to this event and this notification is to retract reporting under that criterion. The licensee notified the NRC Resident Inspector. Notified R4DO (Drake).

ENS 5413024 June 2019 22:15:00FitzPatrick10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition

EN Revision Text: POTENTIAL UNANALYZED CONDITION DUE TO UNPROTECTED CONTROL CIRCUITS RUNNING THROUGH MUTILPLE FIRE AREAS During a review of industry Operating Experience it was identified that there were unprotected DC control circuits for non safety-related DC motors which are routed from the Battery Charger Rooms to other separate fire areas. Circuit Breakers used to protect the motor power conductors appear to be inadequate to protect the control conductors. The concern is that under fire safe shutdown conditions, it is postulated that a fire in one area can cause short circuits potentially resulting in secondary fires or cable fires in other fire areas where the cables are routed. The secondary fires or cable failures are outside the assumptions of the 10 CFR 50 Appendix R Safe Shutdown Analysis. This condition is reportable as an 8-hour ENS report in accordance with 10 CFR 50.72(b)(3)(ii)(B) as an unanalyzed condition. Requirements of the Technical Requirements Manual (TRM) for the affected fire areas will be implemented." The licensee has notified the NRC Resident Inspector.

  • * * RETRACTION FROM ROBERT GRAHAM TO HOWIE CROUCH AT 2045 EDT ON 9/30/19 * * *

In accordance with NUREG-1022, Sections 2.8 and 5.1.2, James A. FitzPatrick Nuclear Power Plant is retracting (formally withdrawing) Licensee Event Report (LER) Number 2019-002. LER 2019-002 was transmitted to the NRC via letter JAFP-19-0080 dated August 23, 2019. The LER reported, under 10 CFR 50.73(a)(2)(ii)(B), the nuclear power plant being in an unanalyzed condition that significantly degraded plant safety. Subsequent to submittal of LER 2019-002, FitzPatrick Engineering completed analyses using more accurate input conditions. This analysis has determined no credible hot short scenario will result in damage to adjacent cables in other fire zones, showing that the postulated condition would not degrade plant safety. Therefore, James A. FitzPatrick Nuclear Power Plant is retracting LER 2019-002 (and this event notification). The licensee will notify the NRC Resident Inspector and the New York State Public Service Commission. Notified R1DO (DeFrancisco).

ENS 5411111 June 2019 16:32:00Monticello10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Primary containmentAt 1132 CDT on 6/11/2019, both manual primary containment isolation valves in a one-inch service air line were found open. This resulted in an open primary containment penetration. Both valves are required to be closed for Primary Containment Isolation Valve Operability. Both valves were closed and independently verified closed at 1149 CDT on 6/11/2019. This is being reported under 10 CFR 50.72(b)(3)(v)(C) and (D), and 10 CFR 50.72(b)(3)(ii)(B). There was no impact to the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. The licensee also notified the State of Minnesota State Duty Officer.
ENS 5399712 April 2019 23:15:00Monticello10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition
Core Spray
Low Pressure Coolant Injection

EN Revision Text: HIGH ENERGY LINE BREAK DOOR FOUND IN INCORRECT POSITION RESULTING IN LPCI AND CORE SPRAY BEING INOPERABLE At approximately 1815 CDT on April 12, 2019, High Energy Line Break (HELB) Door-410A in the Reactor Building was discovered in the closed position. HELB Door-410B was previously closed for maintenance. Either Door-410A or Door-410B must be open to support the current HELB analyses. With both doors closed, this is considered an unanalyzed condition resulting in the loss of a post-HELB safe shutdown path. With Door-410A and Door-410B closed, LPCI (Low Pressure Coolant Injection) and Core Spray injection valves in both divisions are no longer considered available. This condition is being reported under 10 CFR 50.72(b)(3)(ii) as an unanalyzed condition that significantly degrades plant safety and 10 CFR 50.72(b)(3)(v) as an event or condition that could have prevented the fulfillment of a safety function. The condition was resolved at approximately 1845 CDT on April 12, 2019 when Door-410A was blocked open. The health and safety of the public was not affected by this condition. The NRC Resident has been notified.

  • * * RETRACTION FROM JESSE TYGUM TO HOWIE CROUCH AT 1330 EDT ON 5/24/19 * * *

Event Notification (EN) #53997, made on 4/13/2019, is being retracted. An engineering evaluation completed subsequent to this event analyzed the discovered condition with both Door-410A and Door-410B being closed. The engineering evaluation determined that the environmental conditions present with both Door-410A and Door-410B closed would not have impacted the availability of both divisions of the LPCI (Low Pressure Coolant Injection) and Core Spray injection valves nor would it have resulted in the loss of a post-HELB safe shutdown path. Therefore, this condition did not meet the criteria for an 8-hour notification per 10 CFR 50.72(b)(3)(ii) as an unanalyzed condition that significantly degrades plant safety or per 10 CFR 50.72(b)(3)(v)(D) as an event or condition that could have prevented the fulfillment of a safety function. The NRC Resident Inspector has been notified. The licensee also notified the Minnesota State Duty Officer. Notified R3DO (Cameron).

ENS 539681 April 2019 03:06:00Palo Verde10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Emergency Core Cooling System

At 2006 (MST), on 3/31/2019, the Palo Verde Nuclear Generating Station Unit 1 Shift Manager was informed that leakage was measured from the Train A Emergency Core Cooling System (ECCS) piping at approximately 100 ml/minute through a High Pressure Safety Injection (HPSI) A drain valve. This value exceeds the assumed 3000 ml/hour ECCS leakage for a large break loss of coolant accident analysis. At 0230 (MST) on April 1, 2019, the valve was flushed and the leakage reduced to 10 ml/minute (600 ml/hour) and was no longer above the limit of the safety analysis. This condition is being reported as an unanalyzed condition per 10 CFR 50.72(b)3)(ii)(B) and a condition that could have prevented the fulfillment of a safety function to the control the release of radioactive material per 10 CFR 50.72(b)(3)(v)(C). This event did not result in an abnormal release of radioactive material. Notification received by Caty Nolan and emailed to HOO.HOC@NRC.GOV The NRC asked a followup question: Why was the criterion for Control of Radioactive Material selected? per the PVNGS Unit 1 Shift Manager, this criterion was selected due to the potential of exceeding offsite dose projections, post recirculation, following a Design Basis Accident. The resident inspector has been notified.

  • * * UPDATE ON 05/15/19 AT 1417 EDT FROM SEAN DORNSEIF TO BETHANY CECERE * * *

An engineering evaluation concluded that the as-found ECCS leakage would not have degraded the performance of the Pump Room Exhaust Air Cleanup system; therefore, it remained operable. The evaluation also concluded that the as-found leakage was within the analysis margins for HPSI pump hydraulic performance and containment flood level following a Large Break Loss of Coolant Accident; therefore, the ECCS also remained operable. Based on the above information, the condition identified on March 31, 2019, was an unanalyzed condition per 10 CFR 50.72(b)(3)(ii)(B), but did not prevent the fulfillment of the safety function of the structures or systems that are needed to control the release of radioactive material per 10 CFR 50.72(b)(3)(v)(C). The NRC resident inspectors have been informed. Notified R4DO (Proulx).

ENS 5380120 December 2018 05:00:00Watts Bar10 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionAt 1642 Eastern Standard Time (EST) on December 20, 2018, it was determined that both trains of Containment Air Return Fan (CARF) were simultaneously INOPERABLE from 0817 (EST) to 1129 (EST) on November 20, 2018. This condition is not bounded by existing design and licensing documents; however, it poses no impact to the health and safety of the public or plant personnel. Therefore, this event is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(ii)(B). The NRC Resident Inspector has been notified.
ENS 537121 November 2018 04:00:00Fermi10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition

EN Revision Text: UNANALYZED CONDITION DUE TO MODIFICATION NOT ADDED TO PROCEDURE On November 1, 2018, at approximately 1300 EDT, Fermi 2 identified that a Station Blackout (SBO) procedure was deficient as a result of a modification installed during a recent refueling outage. A review identified that the performance of the SBO procedure could have resulted in a challenge to having an alternate AC source available within one hour as outlined in the Updated Final Safety Analysis Report (UFSAR) 8.4.2. The alternate AC source was always available to be manually aligned in accordance with other standard operating procedures. The modification did not affect the function for Appendix R alternative shutdown. Immediate actions are underway to revise the impacted procedure. The health and safety of the public was not affected as offsite power has remained available since the modification was installed. Investigation into the cause and corrective actions is ongoing. Fermi 2 is reporting this event as an unanalyzed condition pursuant to the requirements of 10 CFR 50.72(b)(3)(ii)(B). The licensee notified the NRC Resident Inspector.

  • * * RETRACTION ON 12/28/18 AT 1228 EST FROM JEFFREY MYERS TO JEFFREY WHITED * * *

The purpose of this notification is to retract a previous report made on November 1, 2018 (EN 53712) under 10 CFR 50.72(b)(3)(ii)(B). Subsequent to the initial notification, the event, site procedures, and the NRC guidance in NUREG-1022 pertaining to 10 CFR 50.72(b)(3)(ii)(B) were reviewed further. The evaluation determined that at the time of the event, there were multiple methods defined in existing station procedures to establish an available alternate AC source within one hour as outlined in the Updated Final Safety Analysis Report (UFSAR) 8.4.2. Under these circumstances, the event does not represent an unanalyzed condition under 10 CFR 50.72(b)(3)(ii)(B). Therefore, EN 53712 can be retracted and no Licensee Event Report (LER) under 10 CFR 50.73(a)(2)(ii)(B) is required to be submitted. The licensee has notified the NRC Resident Inspector. Notified R3DO (Riemer).

ENS 5367519 October 2018 04:00:00Perry10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition

During extent of condition review of a previously identified fire induced hot-short (Ref. EN#53644) an unfused circuit associated with the 0M23C0002A, Miscellaneous Switchgear Recirculation Fan was discovered. This condition is not bounded by existing design and licensing documents. This results in an unanalyzed condition due to the possibility for a postulated fire induced hot-short to cause a secondary fire in a different fire area, which would be outside the boundaries analyzed for safe shutdown in the Appendix R Evaluation, Safe Shutdown Capabilities Report, due to an unfused circuit. Without overcurrent protection for this circuit, the potential exists that an initial fire event affecting this circuit could cause a short circuit that would cause excessive current through the circuit beyond the capacity rating of the conductors. This could lead to a secondary fire in another plant area where this circuit is routed, challenging the ability to achieve and maintain safe shutdown. The postulated event would affect multiple fire zones in the control complex. This condition is being reported in accordance with 10 CFR 50.72(b)(3)(ii)(B). Interim compensatory measures (i.e., fire watches) have been implemented for affected areas of the plant. The licensee has notified the NRC Resident Inspector.

  • * * UPDATE ON 10/19/2018 AT 1454 EDT FROM EDWARD CONDO TO ANDREW WAUGH * * *

Further extent of condition reviews have discovered another unfused circuit. The circuitry is related to 0M24C001A, Battery Room Exhaust Fan. This condition is not bounded by existing design and licensing documents. This results in an unanalyzed condition due to the possibility for a postulated fire induced hot-short to cause a secondary fire in a different fire area, which would be outside the boundaries analyzed for safe shutdown in the Appendix R Evaluation, Safe Shutdown Capabilities Report, due to an unfused circuit. This condition is being reported in accordance with 10 CFR 50.72(b)(3)(ii)(B). Interim compensatory measures (i.e., fire watches) have been implemented for affected areas of the plant. The licensee has notified the NRC Senior Resident Inspector. Notified R3DO (Hills).

ENS 5367419 October 2018 04:00:00Fermi10 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionOn 10/19/2018, at approximately 0400 EDT, during an investigation into a failed surveillance test for a Loss of Offsite Power (LOP) coincident with a Loss of Coolant Accident (LOCA), it was identified that the Engineered Safety System Bus degraded voltage relay scheme contained a time delay setting that could inhibit all Low Pressure Core Injection (LPCI) pumps from automatically starting and operating during a LOP/LOCA, thus making LPCI incapable of meeting its functional requirement of automatic startup and operation regardless of the availability of offsite power supply (UFSAR Section 6.3.1.4 and Tech. Spec. Surveillance Requirement 3.8.1.17). The condition was identified during the first-time performance of a revised surveillance procedure for a LOP coincident with a LOCA signal. Fermi is currently in Mode 4 (Cold Shutdown) and LPCI auto start on a LOP/LOCA signal is not required. However, the initial investigation identified the condition likely existed in the past during modes of operation where LPCI auto start on LOP/LOCA was required. Investigation into the cause and corrective actions is ongoing. Since LPCI auto start is not required at the time of discovery (Mode 4), this event is being reported pursuant to 50.72(b)(3)(ii)(b). The NRC Resident Inspector has been notified.
ENS 5366311 October 2018 04:00:00Calvert Cliffs10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition
During a post maintenance start of the 1B diesel generator, the air start solenoid valves did not close as expected. This resulted in lowering air pressure in the common air start headers causing inoperability of the 2A and 2B diesel generators at time 23:03. The 1B diesel generator was isolated from the common air start header, which restored the air start header pressure to the 2A and 2B diesel generators. The 2A and 2B diesel generators were declared operable at 23:34. The NRC Resident Inspector was notified.
ENS 536444 October 2018 04:00:00Perry10 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionDegraded or unanalyzed condition due to the possibility for a postulated fire induced hot short to cause a secondary fire in a different fire area, which would be outside the boundaries analyzed for safe shutdown in calculation SSC-001 due to an unfused circuit associated with the 1M43C0001A, Diesel Generator Building Ventilation Fan. This condition is not bounded by existing design and licensing documents. Without overcurrent protection for this circuit, the potential exists that an initial fire event affecting this circuit could cause a short circuit without protection that would cause excessive current through the circuit beyond the capacity rating of the conductors. This could lead to a secondary fire in another plant area where this circuit is routed challenging the ability to achieve and maintain safe shutdown. The postulated event would affect the following fire zones: 1CC-3c (Unit 1, Division 1 4160V and 480V Switchgear Room, 620 feet 6 inch elevation), 1CC-3e (Unit 1 West Corridor North of Elevator, 620 feet 6 inch elevation), DG-1d (Hallway Diesel Generator Building 620 feet 6 inch elevation), and 1DG-1c (Unit 1, Division 1 Diesel Generator Building 620 feet 6 inch elevation). This condition is being reported in accordance with 10 CFR 50.72(b)(3)(ii)(B). Interim compensatory measures (i.e., fire watches) have been implemented for affected areas of the plant. The licensee has notified the NRC Senior Resident Inspector.
ENS 5362225 September 2018 05:00:00River Bend10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition
At 1200 CDT on September 25, 2018, while the plant was in MODE 1 at 90 percent power, it was identified that an additional condition existed which had not previously been considered in developing the compensatory measures implemented for design flaws and single point vulnerabilities associated with the Control Building Chilled Water System. Specifically, a 20 minute 'quick restart timer' on Control Building Chillers that have analog control systems (HVK-CHL1A & 1B) would prevent the chillers from starting in specific scenarios. The recommended compensatory actions to address the new condition were implemented at 1235 CDT on September 25, 2018. Currently the Chilled Water System is otherwise operating as designed. Operator actions are in place to ensure the plant meets all required design safety system functions. Work is currently underway to identify and correct all design vulnerabilities. The (NRC) Senior Resident Inspector has been notified. This was identified by engineering during an extended condition search.
ENS 5359711 September 2018 05:00:00Monticello10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Core Spray
Emergency Core Cooling System
On 9/10/2018, the 11 Core Spray (CSP) loop was placed in service to support quarterly surveillance testing. With the 11 CSP pump in service it was identified that the check valves isolating the 11 CSP system from the keep fill supply were leaking by. At 1129 CDT on 9/11/2018, it was identified that this leakage may have exceeded the leakage rate assumptions made in the dose analysis calculation for emergency core cooling system (ECCS) leakage outside containment following a loss of coolant accident (LOCA). Therefore, this is being reported in accordance with 10 CFR 50.72(b)(3)(ii)(B) for an unanalyzed condition that significantly degrades plant safety and 10 CFR 50.72(b)(3)(v) for any event or condition that at the time of discovery could have prevented the fulfillment of the safety function of structures or systems that are needed to: (C) Control the release of radioactive material; or (D) Mitigate the consequences of an accident. The potential ECCS leak pathway has been isolated. There is no impact to health and safety of the public. The NRC Resident Inspector has been notified.
ENS 5354812 August 2018 04:00:00Beaver Valley10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown
Emergency Diesel Generator

EN Revision Text: TECHNICAL SPECIFICATION REQUIRED SHUTDOWN - LOSS OF 480 VOLTAGE EMERGENCY BUS On 8-12-18 at 0158 EDT, Beaver Valley Unit 2 experienced a loss of 480 Volt 2P Emergency Bus. This resulted in a Loss of Safety Function due to the 2-2 Emergency Diesel Generator (EDG) being Inoperable coincident with the Residual Heat Release Valve (2SVS-HCV104). A Technical Specification shutdown is required per LCO 3.0.3. The Licensee also stated they were in an unanalyzed condition due to the EDG and Residual Heat Release Valve being inoperable at the same time. The Licensee is shutting down to Mode 5 (Cold Shutdown). The Licensee is notifying the Resident Inspector. The Licensee will be making a Press Release about the unplanned shutdown.

  • * * UPDATE ON 08/16/2018 AT 1424 EDT FROM BLASE BARTKO TO KEN MOTT * * *

On 8-12-18 at 0158 (EDT) Beaver Valley Unit 2 experienced a loss of 480 Volt 2P Emergency Bus. Per operational guidance, this was determined to be a Loss of Safety Function due to the Unit 2 Emergency Diesel Generator (EDG) being INOPERABLE coincident with the Residual Heat Release Valve (2SVS-HCV104) 10 CFR 50.72(b)(3)(v)(B) and (D). This was also reported as an Unanalyzed Condition 10 CFR 50.72(b)(3)(ii)(b). No Press Release was performed for this event. The NRC Resident Inspector was notified. At 0410 (EDT) a Technical Specification Shutdown was commenced 10 CFR 50.72(b)(2)(i). At 2011 (EDT) the 480 Volt 2P Emergency Bus was restored and energized. Further evaluation of the event has determined that this event was not an Unanalyzed Condition and did not result in a Loss of Safety Function. The classifications of Unanalyzed Condition and Loss of Safety Function are being retracted. The accuracy of the existing guidance relative to Safety Function has been entered in the Corrective Action Program and interim actions have been taken to provide accurate guidance. Notified R1DO (Young) via email.

ENS 534853 July 2018 05:00:00Callaway10 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionService water
Auxiliary Feedwater

EN Revision Text: DISCOVERY OF AN UNANALYZED CONDITION THAT SIGNIFICANTLY DEGRADES PLANT SAFETY On July 3, 2018, while performing a review of Emergency Operating Procedures, a concern was identified regarding the potential for excessive loss of ultimate heat sink inventory (UHS) through the auxiliary feedwater (AFW) system mini-flow recirculation pathway. This condition would have the potential to prevent the ultimate heat sink from providing an adequate inventory of water for a 30-day mission time.

The normal water supply for the Callaway AFW system is the condensate storage tank (CST). The CST is a non-safety grade component. The safety-grade supply for AFW is the essential service water (ESW) system. The ESW system is supplied by the UHS. The UHS thermal performance analysis accounts for a loss of UHS inventory to the AFW system up until the point of the accident sequence that the AFW pumps would be secured. The analysis did not include an allowance for loss of UHS inventory through the AFW mini-flow recirculation pathway following the AFW pumps being secured. The EOP guidance that secures the AFW pumps does not isolate the mini-flow recirculation pathway.

Initial estimates indicate that loss of UHS inventory through the mini-flow recirculation pathway, if not isolated, would preclude the UHS from completing its 30-day mission time. This potential for depletion of the UHS placed the plant in an unanalyzed condition that significantly degraded safety.

Callaway has issued interim guidance to the on-shift personnel regarding this concern to ensure that the ultimate heat sink water level is maintained at a level that will be adequate to mitigate the potential loss of inventory.

This condition is reportable per 10 CFR 50.72(b)(3)(ii)(B) for an unanalyzed condition that significantly degrades safety. The NRC Resident Inspectors have been notified of this condition.

  • * * RETRACTION ON 07/31/2018 AT 1430 EDT FROM LEE YOUNG TO ANDREW WAUGH * * *

Event Notification (EN) 53485, made on July 3, 2018, is being retracted because re-evaluation performed subsequent to the notification has demonstrated, based on actual plant equipment and environmental conditions, that the unanalyzed inventory losses previously reported by EN 53485 would not have depleted the UHS inventory to an unacceptable level during its 30-day mission time. The re-evaluation has led to the conclusion that the previously unanalyzed losses of UHS inventory would not have prevented the UHS from performing its specified safety functions and meeting its 30-day mission time requirements. With the UHS capable of performing its specified safety functions and meeting its 30-day mission time requirements, the systems supported by the UHS would have remained capable of performing their specified safety functions. Based on these considerations, it has been determined that the condition reported in EN 53485 did not result in the plant being in an unanalyzed condition that significantly degraded safety. Consequently, the condition did not meet the criteria for an 8-hour notification per 10 CFR 50.72(b)(3)(ii)(B) for an unanalyzed condition that significantly degrades safety. The NRC Resident Inspector has been notified of the Event Notification retraction. Notified R4DO (Gaddy).

ENS 534381 June 2018 04:00:00Salem10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition
Service water
Auxiliary Feedwater

During the period of evaluation of tornado missile vulnerabilities and the potential impacts to technical specification (TS) plant equipment, it was determined that the power cables to a safety related motor control center (MCC) in the service water (SW) intake structure are not adequately protected from tornado generated missiles. During walk downs, it was identified that the installed SW pipe tunnel barrier is not adequate. A tornado could generate missiles capable of striking the power cables and rendering a SW MCC inoperable. These conditions are reportable per 10 CFR 50.72(b)(3)(ii)(B) and per 10 CFR 50.72(b)(3)(v)(D). This condition is being addressed in accordance with NRC enforcement guidance provided in Enforcement Guidance Memorandum (EGM) 15-002, 'Enforcement Discretion for Tornado-Generated Missile Protection Noncompliance,' Revision 1, and DSS-ISG-2016-01, 'Clarification of Licensee Actions in Receipt of Enforcement Discretion per Enforcement Guidance Memorandum EGM 15-002, Enforcement Discretion for Tornado- Generated Missile Protection Noncompliance,' Revision 1. Compensatory measures have been implemented in accordance with these documents. The NRC Resident Inspector has been notified. The licensee will be notifying the Lower Alloways Creek Township.

  • * * UPDATE ON 6/18/2018 AT 1604 EDT FROM JUSTIN HARGRAVE TO RICHARD SMITH * * *

During subsequent walk downs, PSEG (Public Service Enterprise Group) identified that both the Unit 1 and Unit 2 turbine driven auxiliary feedwater pumps are also not adequately protected from tornado generated missiles. The steam exhaust pipe could be potentially impacted and cause crimping that could reduce steam exhaust flow and pump capacity. EN 53438 is updated to include both Salem units and these additional components. This condition is being addressed in accordance with NRC enforcement guidance provided in enforcement Guidance Memorandum (EGM) 15-002, 'Enforcement Discretion for Tornado-Generated Missile Protection Noncompliance,' Revision 1, and DSS-ISG-2016-01, 'Clarification of Licensee Actions in Receipt of Enforcement Discretion per Enforcement Guidance Memorandum EGM 15-002, Enforcement Discretion for Tornado-Generated Missile Protection Noncompliance,' Revision 1. Compensatory measures have been implemented in accordance with these documents." The NRC Resident Inspector has been notified. The licensee will be notifying the Lower Alloways Creek Township. Notified R1DO (Burritt).

ENS 5341922 May 2018 04:00:00Beaver Valley10 CFR 50.72(b)(3)(v)(B), Loss of Safety Function - Remove Residual Heat
10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown

EN Revision Text: GAS VOIDS DISCOVERED IN BOTH TRAINS OF LOW HEAD SAFETY INJECTION On 5/22/2018, while operating at approximately 100 percent power, Ultrasonic Testing of the Beaver Valley Power Station (BVPS) Unit 1 Low Head Safety Injection (LHSI) pump suction piping identified gas voids in excess of the acceptable limit for void volume. Both trains of LHSI were declared inoperable. Technical Specification (TS) 3.5.2 for both trains of the LHSI system was entered along with TS 3.0.3 which requires the initiation of a plant shutdown. Time of TS entry was 12:56 (EDT). Plant shutdown was commenced at 15:56 (EDT) in accordance with plant procedures. At 15:59 (EDT) Train 'A' LHSI was restored to operable status, TS 3.0.3 Action was exited and the power reduction was stopped at approximately 99 percent. At 17:43 (EDT) Train 'B' LHSI was restored to operable status, TS 3.5.2 Actions were exited. This is reportable per 10 CFR 50.72(b)(3)(ii) Unanalyzed Condition, 10 CFR 50.72(b)(3)(v) Event or Condition that Could Have Prevented the Fulfillment of a Safety Function and 10 CFR 50. 72(b )(2)(i) TS Required Shutdown. The NRC Resident Inspector has been notified.

  • * * RETRACTION ON 6/21/18 AT 1535 EDT FROM SHAWN KEENER TO RICHARD SMITH * * *

Further engineering evaluation has determined that the gas voids that existed at the time of discovery would not have rendered the LHSI (Low Head Safety Injection) system inoperable if it were required to actuate. The engineering evaluation concluded that filling of the containment sump during a Design Basis Accident would result in a void volume reduction such that the void in the LHSI suction piping would not be large enough to significantly impact the operability of the system. Therefore, the system remained operable but degraded. No TSs (Technical Specifications) were required to be entered and no shutdown was required. As such, all three reporting criteria do not apply and are being retracted. The NRC Resident Inspector has been notified. Notified R1DO (Burritt).

ENS 5340114 May 2018 17:05:00Calvert Cliffs10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition
On May 14, 2018, during evaluation of protection for Technical Specification (TS) equipment from the damaging effects of a tornado generated missile, Calvert Cliffs identified a non-conforming condition in the plant design such that specific TS equipment is considered to not be adequately protected from a tornado generated missile. A tornado could generate a missile that could strike the Unit 1 Saltwater system header and associated piping. This could result in damage to the unit 1 Saltwater system header which could affect the ability of the Unit 1 Saltwater subsystems to perform their design function if such a tornado would occur. This condition is reportable per 10 CFR 50.72(b)(3)(ii)(B) for any event or condition that results in the nuclear power plant being in an unanalyzed condition that significantly degrades plant safety, and per 10 CFR 50.72(b)(3)(v)(D) for any event or condition that at the time of discovery could have prevented the fulfillment of the safety function of structures or systems that are needed to mitigate the consequences of an accident. This condition is being addressed in accordance with NRC enforcement guidance provided in EGM 15-002 and DSS-ISG-2016-01. Compensatory measures have been implemented in accordance with these documents. The NRC Resident Inspector has been informed of this notification.
ENS 533928 May 2018 04:00:00Farley10 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionReactor Coolant System
Control Room Emergency Filtration System
On May 7, 2018 at 1041 CDT, Unit 1 performed an RCS (reactor coolant system) leakrate procedure that calculated an unidentified RCS leakrate of 0.202 gpm. The leak source investigation concluded at 2150 that the packing for the charging flow control valve (FCV) was the source of the RCS leakage when it was bypassed, which isolated the leakage. A second RCS leakrate calculation was performed after the charging flow control valve was isolated which calculated an acceptable leakrate of 0.00 gpm. The packing leakage from the charging flow control valve represented leakage external to containment which would result in a greater that 5 Rem dose projection to control room personnel during accident conditions which does not satisfy the GDC19 criteria described in Technical Specification Bases 3.7.10. Therefore the control room emergency filtration system would not be able to fulfill its design function resulting in an unanalyzed condition. This condition is being reported pursuant to 10CFR50.72(b)(3)(ii) for a 'condition that results in the nuclear power plant being in an unanalyzed condition that significantly degrades plant safety'. The packing leak from the charging flow control valve will remain isolated until repaired under work order SNC944374. The NRC Resident Inspector has been notified.
ENS 533824 May 2018 16:29:00River Bend10 CFR 50.72(b)(3)(v)(A), Loss of Safety Function - Shutdown the Reactor
10 CFR 50.72(b)(3)(v)(B), Loss of Safety Function - Remove Residual Heat
10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition
During performance of an extent of condition evaluation of protection for Technical Specification (TS) equipment from the damaging effects of tornados, River Bend Station identified non-conforming conditions in the plant design such that specific TS equipment is considered to not be adequately protected from tornado missiles. The reportable condition is postulated by tornado missiles entering the Diesel Generator Building through conduit and pipe penetrations. A tornado could generate multiple missiles capable of striking Division 1, Division 2, and Division 3 Diesel Generator support equipment rendering all Safety Related Diesel Generators inoperable. This condition is reportable per 10 CFR 50.72(b)(3)(ii)(B) for any event or condition that results in the nuclear power plant being in an unanalyzed condition that significantly degrades plant safety, and per 10 CFR 50.72(b)(3)(v) for any event or condition that at the time of discovery could have prevented the fulfillment of the safety function of structures or systems that are needed to (A) Shut down the reactor and maintain it in a safe shutdown condition, (B) Remove residual heat, or (D) Mitigate the consequences of an accident. This condition was identified as part of an on-going extent of condition review of potential tornado missile related site impacts. Enforcement discretion per Enforcement Guidance Memorandum EGM 15-002 has been implemented and required actions taken. Corrective actions will be documented in a follow-on licensee event report. The licensee has notified the NRC Resident Inspector.
ENS 5334919 April 2018 23:44:00Watts Bar10 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionResidual Heat RemovalOn April 19, 2018 at 1944 EDT, Watts Bar Nuclear Plant (WBN) determined that a preliminary analysis shows current acceptance criteria for gas accumulation in the WBN Unit 1 and Unit 2 Safety Injection System (SIS) and Residual Heat Removal System (RHRS) discharge piping may be non-conservative. The surveillances that check void values and allow venting of the systems are to be performed utilizing conservative criteria at more frequent intervals to ensure gas void volumes remain under acceptable limits. Additional analysis is being performed to determine final actions. The NRC Resident Inspector has been notified.
ENS 5332411 April 2018 06:50:00River Bend10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition
At time 0150 CDT on April 11, 2018, a condition was identified that could impair the ability of the Control Building Air Conditioning System to perform its design function. Engineering determined that the time delay relays HVKA11-80YB or HVKA11-80YD (Division II chilled water LOW FLOW relays) could fail in a manner that challenges the design safety function of the Control Building Chilled Water System during a Loss of Offsite Power (LOP) Event. A failure of the time delay relay HVKA11-80YB or HVKA11-80YD (Division II chilled water LOW FLOW relays) to provide the time delay function would cause both the Division I and Division II HVK chilled water pumps to start after a LOP, which in turn could hinder the auto start of either Division I or Division II chillers. Currently the Chilled Water System is otherwise operating as designed. All operator actions are in place to ensure the plant meets all required designed safety system functions. Work is currently underway to correct this design vulnerability. The NRC Resident Inspector has been notified of this condition.
ENS 5330029 March 2018 18:44:00Browns Ferry10 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionEmergency Equipment Cooling WaterAt 1344 on March 29, 2018, it was determined (engineering evaluation) that an unanalyzed condition that significantly degraded plant safety previously existed. During a postulated control room abandonment due to a fire, and concurrent with a Loss of Offsite Power (LOOP), the required number of Emergency Equipment Cooling Water (EECW) pumps would not have been available from 10/28/2015 to 3/10/2018. On March 8, 2018, during relay functional testing it was discovered that the C3 Emergency Equipment Cooling Water (EECW) pump closing springs did not recharge with the breaker transfer switch in emergency. On August 23, 2012, a wire modification was performed that contained a drawing error resulting in wire placement on the incorrect connection points for the C3 EECW pump. On March 10, 2018, the C3 EECW pump breaker wiring was corrected and subsequent testing was completed satisfactorily. Prior to 10/28/2015, Brown's Ferry Nuclear Plant (BFN) adhered to Appendix R fire protection requirements which did not credit the C3 EECW pump for fire protection from the backup control location. On 10/28/2015, BFN transitioned to National Fire Protection Association (NFPA) 805 fire protection requirements which takes credit for the C3 EECW pump from the backup control location. This condition is being reported pursuant to 10 CFR 50.72(b)(3)(ii)(B), 'Any event or condition that results in the nuclear power plant being in an unanalyzed condition that significantly degrades plant safety'. This is also reportable as a 60-day written report in accordance with 10 CFR 50.73(a)(2)(ii)(B). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified of this event.