ENS 56957
ENS Event | |
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18:22 Feb 9, 2024 | |
Title | Unanalyzed Condition - Inadequate Fuses for Fuel Pool Cooling |
Event Description | The following information was provided by the licensee via email:
On 2/9/24 at 1322 EST, it was determined that the unit was in an unanalyzed condition. A review of DC feeder circuit protection schemes identified a circuit for the fuel pool cooling system is uncoordinated due to inadequate fuse sizing. This results in a concern that postulated fire damage in one area could cause a short circuit without adequate protection, leading to the unavailability of equipment credited for in 10 CFR 50 Appendix R, Fire Safe Shutdown. This condition is not bounded by existing design and licensing documents; however, it poses no impact to the health and safety of the public or plant personnel. Therefore, this event is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(ii)(B). The postulated event affects the following fire zones: fire areas 6S and 6N (within the Unit 2 reactor building). Compensatory actions for affected fire areas have been implemented. An extent of condition review is being performed. The NRC Senior Resident Inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: Fire watches have been established in the affected areas. These will be maintained until the protection scheme is revised.
The following updated information was provided by the licensee via email and phone call: On 03/08/24 at 1418, extent of condition reviews identified circuit(s) in the Units 2 and 3 Reactor Protection Systems (RPS) which are also uncoordinated due to improper fuse sizing. These circuits are not bounded by existing design and licensing documents for 10 CFR 50 Appendix R Fire Safe Shutdown and, therefore, this event is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(ii)(B). This event poses no impact to the health and safety of the public or plant personnel. The postulated event affects the following fire areas: 32, 33, 38 and 39 (Units 2 and 3 Switchgear Rooms). In accordance with procedural requirements, compensatory actions for the affected fire areas have been implemented and will remain until the condition is resolved. The NRC Senior Resident Inspector has been notified. Notified R1DO (Arner)
On March 13, 2024, at 1350 EDT, extent of condition reviews identified a circuit in the Unit 2 reactor protection system (RPS) which is also uncoordinated due to improper fuse sizing. This circuit is not bounded by existing design and licensing documents for 10 CFR 50, Appendix R, Fire Safe Shutdown, therefore, this event is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(ii)(B). This event poses no impact to the health and safety of the public or plant personnel. The postulated event affects fire area 57 (Switchgear Corridor, common to Units 2 and 3). In accordance with procedural requirements, compensatory actions for the affected fire areas have been implemented and will remain until the condition is resolved. Additionally, it was previously reported that fire area 6N contained a circuit which was not bounded by the Fire Safe Shutdown analysis; however, after further review it has been determined that compliance is maintained in this fire area and is therefore retracted from the scope of this report. The NRC Senior Resident Inspector has been notified. Notified R1DO (Jackson)
The following information was provided by the licensee via email: On 03/21/24 at 1211, extent of condition reviews identified an annunciator circuit for the Unit 3 emergency service water (ESW) and high pressure service water (HPSW) pump structure heating and ventilation panel that is also uncoordinated due to improper fuse sizing. This circuit is not bounded by existing design and licensing documents for 10 CFR 50 Appendix R Fire Safe Shutdown and, therefore, this event is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(ii)(B). This event poses no impact to the health and safety of the public or plant personnel. The postulated event affects fire area 47 (Unit 3 pump structure for `B' ESW and `3A'-`3D' HPSW pumps) and the yard fire area (Manhole 026D). In order to restore immediate compliance, the cable has been de-energized to eliminate the possibility of the event of concern. This circuit will remain de-energized or other measures will be implemented until the condition is permanently resolved. The NRC Senior Resident Inspector has been notified. Notified R1DO (Ford) |
Where | |
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Peach Bottom Pennsylvania (NRC Region 1) | |
Reporting | |
10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition | |
LER: | 05000277/LER-2024-002 Uncoordinated DC Circuits Cause Unanalyzed Condition |
Time - Person (Reporting Time:+-3.25 h-0.135 days <br />-0.0193 weeks <br />-0.00445 months <br />) | |
Opened: | Bill Linell 15:07 Feb 9, 2024 |
NRC Officer: | Thomas Herrity |
Last Updated: | Mar 21, 2024 |
56957 - NRC Website
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Unit 2 | |
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Reactor critical | Critical |
Scram | No |
Before | Power Operation (100 %) |
After | Power Operation (100 %) |
WEEKMONTHYEARENS 569572024-02-09T18:22:0009 February 2024 18:22:00
[Table view]10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition Unanalyzed Condition - Inadequate Fuses for Fuel Pool Cooling ENS 532652018-03-15T19:24:00015 March 2018 19:24:00 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition Failure to Meet Appendix R Requirements ENS 524782017-01-09T20:30:0009 January 2017 20:30:00 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident, 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition Emergency Diesel Generators Non-Conforming with Licensing Basis for Tornado Generated Missiles ENS 501282014-05-21T15:00:00021 May 2014 15:00:00 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition Unanalyzed Condition Involving Fire Safe Shutdown Capability ENS 474422011-11-16T00:52:00016 November 2011 00:52:00 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition High Pressure Coolant Injection Steam Supply Valve Cable Unprotected During Postulated Fire 2024-02-09T18:22:00 | |