ML21120A155

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Integrated Inspection Report 05000280/2021001 and 05000281/2021001
ML21120A155
Person / Time
Site: Surry  Dominion icon.png
Issue date: 04/30/2021
From: Stewart Bailey
NRC/RGN-II
To: Stoddard D
Virginia Electric & Power Co (VEPCO)
References
IR 2021001
Download: ML21120A155 (20)


See also: IR 05000280/2021001

Text

April 30, 2021

Mr. Daniel G. Stoddard

Senior Vice President and Chief Nuclear Officer

Innsbrook Technical Center

5000 Dominion Boulevard

Glen Allen, VA 23060-6711

SUBJECT: SURRY POWER STATION - INTEGRATED INSPECTION REPORT

05000280/2021001 AND 05000281/2021001

Dear Mr. Stoddard:

On March 31, 2021, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection

at Surry Power Station. On April 12, 2021, the NRC inspectors discussed the results of this

inspection with Mr. Doug Lawrence, Surry Site Vice President and other members of your staff.

The results of this inspection are documented in the enclosed report.

One finding of very low safety significance (Green) is documented in this report. This finding

involved a violation of NRC requirements. We are treating this violation as a non-cited violation

(NCV) consistent with Section 2.3.2 of the Enforcement Policy.

If you contest the violation or the significance or severity of the violation documented in this

inspection report, you should provide a response within 30 days of the date of this inspection

report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN:

Document Control Desk, Washington, DC 20555-0001; with copies to the Regional

Administrator, Region II; the Director, Office of Enforcement; and the NRC Resident Inspector at

Surry Power Station.

If you disagree with a cross-cutting aspect assignment in this report, you should provide a

response within 30 days of the date of this inspection report, with the basis for your

disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk,

Washington, DC 20555-0001; with copies to the Regional Administrator, Region II; and the NRC

Resident Inspector at Surry Power Station.

D. Stoddard 2

This letter, its enclosure, and your response (if any) will be made available for public inspection

and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document

Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public

Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

Stewart N. Bailey, Chief

Reactor Projects Branch 4

Division of Reactor Projects

Docket Nos. 05000280 and 05000281

License Nos. DPR-32 and DPR-37

Enclosure:

As stated

cc w/ encl: Distribution via LISTSERV

ML21120A155

X Non-Sensitive X Publicly Available

X SUNSI Review

Sensitive Non-Publicly Available

OFFICE RII: DRP RII: DRP RII: DRP RII: DRP

NAME DJackson LMcKown BTowne SBailey

DATE 4/28/2021 4/28/2021 4/30/2021 4/30/2021

U.S. NUCLEAR REGULATORY COMMISSION

Inspection Report

Docket Numbers: 05000280 and 05000281

License Numbers: DPR-32 and DPR-37

Report Numbers: 05000280/2021001 and 05000281/2021001

Enterprise Identifier: I-2021-001-0076

Licensee: Virginia Electric and Power Company

Facility: Surry Power Station

Location: Surry, VA

Inspection Dates: December 07, 2020 to March 31, 2021

Inspectors: L. McKown, Senior Resident Inspector

B. Towne, Resident Inspector

B. Caballero, Senior Operations Engineer

K. Kirchbaum, Operations Engineer

Approved By: Stewart N. Bailey, Chief

Reactor Projects Branch 4

Division of Reactor Projects

Enclosure

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees

performance by conducting an integrated inspection at Surry Power Station, in accordance with

the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for

overseeing the safe operation of commercial nuclear power reactors. Refer to

https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

Failure to Perform Fire Protection Program Surveillances

Cornerstone Significance Cross-Cutting Report

Aspect Section

Mitigating Green [P.2] - 71111.05

Systems NCV 05000280,05000281/2021001-01 Evaluation

Open/Closed

The inspectors identified a finding of very low safety significance (Green) and an associated

non-cited violation (NCV) of License Condition 3.I, Fire Protection, concerning Dominion

Energys failure to implement and maintain in effect the provisions of the approved fire

protection program as described in the Updated Final Safety Analysis Report. Multiple

examples of tests and inspections of fire protection components were not performed in

accordance with the Technical Requirements Manual which resulted in the discovery of

adverse conditions requiring corrective maintenance on December 29, 2020.

Additional Tracking Items

None.

2

PLANT STATUS

Unit 1 operated at or near rated thermal power for the entire inspection period.

Unit 2 began the inspection period at rated thermal power. On March 3, 2021, Unit 2 reduced to

approximately 70 percent in support of planned main condenser maintenance and returned to

rated thermal power the same day. The unit remained at or near rated thermal power for the

remainder of the inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in

effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with

their attached revision histories are located on the public website at http://www.nrc.gov/reading-

rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared

complete when the IP requirements most appropriate to the inspection activity were met

consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection

Program - Operations Phase. The inspectors reviewed selected procedures and records,

observed activities, and interviewed personnel to assess licensee performance and compliance

with Commission rules and regulations, license conditions, site procedures, and standards.

Starting on March 20, 2020, in response to the National Emergency declared by the President

of the United States on the public health risks of the Coronavirus Disease 2019

(COVID-19), resident inspectors were directed to begin telework and to remotely access

licensee information using available technology. During this time, the resident inspectors

performed periodic site visits each week; conducted plant status activities as described in IMC 2515, Appendix D, Plant Status; observed risk-significant activities; and completed onsite

portions of IPs. In addition, resident and regional baseline inspections were evaluated to

determine if all or portions of the objectives and requirements stated in the IP could be

performed remotely. If the inspections could be performed remotely, they were conducted per

the applicable IP. In some cases, portions of an IP were completed remotely and onsite. The

inspections documented below met the objectives and requirements for completion of the IP.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

Seasonal Extreme Weather Sample (IP Section 03.01) (1 Sample)

(1) The inspectors evaluated readiness for seasonal extreme weather conditions prior to

the onset of seasonal cold temperatures for the following systems on

January 25, 2021:

  • Fire Protection
  • Emergency AC Power

3

Impending Severe Weather Sample (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated the adequacy of the overall preparations to protect risk-

significant systems from impending severe weather including heavy snow, hail, and

ice on February 11, 2021.

71111.04 - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (5 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following

systems/trains:

(1) #1 emergency diesel generator air start system on January 4, 2021.

(2) Unit 2 'A' and 'B' high head safety injection and charging pumps during 'C' pump

restoration on January 6, 2021.

(3) Unit 2 high pressure main steam and turbine controls including electro-hydraulic

control system during spontaneous closure of #4 governor and stop valves on

January 25, 2021.

(4) Units 1 and 2 spent fuel pool cooling closed cooling water alignment on

February 17, 2021.

(5) Unit 1 normal switchgear on February 22, 2021.

71111.05 - Fire Protection

Fire Area Walkdown and Inspection Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated the implementation of the fire protection program by conducting a

walkdown and performing a review to verify program compliance, equipment functionality,

material condition, and operational readiness of the following fire areas:

(1) Unit 1 cable spreading room on January 4, 2021.

(2) Unit 1 cable tunnel on January 19, 2021.

(3) Unit 2 high head safety injection and charging pump cubicles preceding 'A' pump

motor planned maintenance on February 1, 2021

(4) Units 1 and 2 normal switchgear room fire dampers on March 2, 2021.

Fire Brigade Drill Performance Sample (IP Section 03.02) (2 Samples)

(1) The inspectors evaluated the onsite fire brigade training and performance during an

unannounced fire drill inside of the radiologically controlled area at the Unit 2 'B'

refueling water storage tank chillers February 16, 2021.

(2) The inspectors evaluated the onsite fire brigade training and performance during an

actual vehicle fire in the owner-controlled area nearby a protected area vehicle

access point on February 22, 2021.

71111.06 - Flood Protection Measures

Inspection Activities - Internal Flooding (IP Section 03.01) (1 Sample)

The inspectors evaluated internal flooding mitigation protections:

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(1) Multiple roof leaks into the Unit 1 normal switchgear room around and about risk-

significant equipment including control rod drive motor-generators, reactor coolant

pump motor breakers, and condensate pump motor breakers on March 17, 2021.

71111.11B - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Requalification Program (IP Section 03.04) (1 Sample)

Licensed Operator Requalification Program (IP Section 03.04) (1 Sample)

The inspectors completed an inspection to verify the licensees ability to evaluate the

performance of their licensed operators during the conduct of examinations, to assess their

ability to properly develop and administer requalification annual operating tests and biennial

written examinations, to evaluate the performance of the control room simulator and their

testing and maintenance of the simulator, to ensure that licensed individuals satisfy the

conditions of their licenses, and to assess their effectiveness in ensuring that operator

license conditions are satisfied.

(1) Biennial Requalification Written Examinations

The inspectors evaluated the quality of the licensed operator biennial requalification

written examination administered in February and March 2020.

Annual Requalification Operating Tests

The inspectors evaluated the adequacy of the facility licensees annual requalification

operating tests.

Administration of an Annual Requalification Operating Test

The inspectors evaluated the effectiveness of the facility licensee in administering

requalification operating tests required by 10 CFR 55.59(a)(2) and that the facility

licensee is effectively evaluating their licensed operators for mastery of training

objectives.

Requalification Examination Security

The inspectors evaluated the ability of the facility licensee to safeguard examination

material, such that the examination is not compromised.

Remedial Training and Re-examinations

The inspectors evaluated the effectiveness of remedial training conducted by the

licensee, and reviewed the adequacy of re-examinations for licensed operators who

did not pass a required requalification examination.

Operator License Conditions

The inspectors evaluated the licensees program for ensuring that licensed operators

meet the conditions of their licenses.

5

Control Room Simulator

The inspectors evaluated the adequacy of the facility licensees control room

simulator in modeling the actual plant, and for meeting the requirements contained in

10 CFR 55.46.

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01)

(1 Sample)

(1) The inspectors observed and evaluated licensed operator performance in the control

room during Unit 2 high pressure main steam and turbine control challenges

associated with spontaneous closure of #4 governor and stop valves on

January 25, 2021.

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

(1) The inspectors observed and evaluated a Licensed Operator Requalification

Examination that included loss of offsite power with a failed emergency diesel

generator output breaker, followed by a small break loss of coolant accident on

February 3, 2021.

71111.12 - Maintenance Effectiveness

Maintenance Effectiveness (IP Section 03.01) (2 Samples)

The inspectors evaluated the effectiveness of maintenance to ensure the following

structures, systems, and components (SSCs) remain capable of performing their intended

function:

(1) Unit 2 'A' charging pump alternate discharge valve following observation of unusual

operation on March 15, 2021.

(2) Auxiliary feedwater booster pumps following discovery of discolored oil in lubricating

reservoirs on March 10, 2021.

Aging Management (IP Section 03.03) (1 Sample)

The inspectors evaluated the effectiveness of the aging management program for the

following SSCs that did not meet their inspection or test acceptance criteria:

(1) 'B' emergency service water pump intake piping aging management inspection using

an underwater drone on March 10, 2021.

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (6 Samples)

The inspectors evaluated the accuracy and completeness of risk assessments for the

following planned and emergent work activities to ensure configuration changes and

appropriate work controls were addressed:

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(1) Units 1 and 2 elevated risk due to lower level intake transformer 2G phase alignment

challenges on January 5, 2021.

(2) Unit 2 'B' reactor coolant system (RCS) flow loop channel #3 (2-RC-FI-2426)

troubleshooting and restoration following flow oscillations during process control

performance testing on 'B' steam generator (S/G) channel #3 (2-MS-PI-2485)

pressure sensing circuit (CR1164149) on January 20, 2021.

(3) Unit 2 high pressure main steam and turbine control challenges associated with

spontaneous closure of #4 governor and stop valves on January 25, 2021.

(4) Units 1 and 2 elevated risk due to #3 emergency diesel generator overspeed trip

testing on February 7, 2021.

(5) Units 1 and 2 elevated risk during 0-IPT-CNL-LGC-8.8 Intake Canal Level Logic

Testing on March 2, 2021.

(6) Unit 1 elevated risk following discovery #3 high pressure turbine governor valve

spring tower failure concurrent with safety injection system void verification checks

and Unit 2 reactor protection system testing on March 9, 2021.

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 03.01) (7 Samples)

The inspectors evaluated the licensee's justifications and actions associated with the

following operability determinations and functionality assessments:

(1) CR1163311, 'C' emergency service water pump discharge filter hold down bolt

configuration concern on January 5, 2021.

(2) CR1160271, CR1160470, and CR1163099, and CR1166724 multiple challenges to

low-pressure carbon dioxide fire suppression and fire protection 10 CFR Appendix R

barrier functionality at the Units 1 and 2 cable spreading areas and mechanical

equipment room #1 on January 7, 2021.

(3) CR1164149, Unit 2 'B' RCS flow loop channel #3 (2-RC-FI-2426) troubleshooting and

restoration following flow oscillations during process control performance testing on

'B' S/G channel #3 (2-MS-PI-2485) pressure sensing circuit on January 20, 2021.

(4) CR1164302, Unit 1 approximately 45 gallons per day leakage from the refueling

water storage tank on January 21, 2021.

(5) CR1165268, Unit 2 high head safety injection pump discharge alternate injection path

isolation valve unexpected operation and noise during surveillance testing on

February 10, 2021.

(6) CR1166329, Unit 2 'B' auxiliary feedwater booster pump contaminated oil in the pump

bearing oil bubbler on February 23, 2021.

(7) CR1168011, Unit 1 apparently degraded mounting and exposed environmental

qualification conduit junction box for turbine driven auxiliary feedwater pump steam

admission valves on March 18, 2021.

71111.19 - Post-Maintenance Testing

Post-Maintenance Test Sample (IP Section 03.01) (6 Samples)

The inspectors evaluated the following post-maintenance test activities to verify system

operability and functionality:

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(1) 2-OPT-CH-003, Unit 2 'C' charging pump post-maintenance operability and

performance test following motor stator replacement on January 6, 2021.

(2) Units 1 and 2 repair and inspection of upper cable spreading area NRC-identified

degraded fire barriers (CR1160271 & CR1160470) on January 14, 2021.

(3) Unit 2 'B' RCS flow loop channel #3 (2-RC-FI-2426) troubleshooting and restoration

following flow oscillations during process control performance testing on 'B' S/G

channel #3 (2-MS-PI-2485) pressure sensing circuit (WO 38204233907) on

January 21, 2021.

(4) Unit 2 high pressure main steam and turbine control challenges associated with

spontaneous closure of #4 governor and stop valves (WO 38204234255,

38204234257, 38204234254) on January 25, 2021.

(5) 0-OPT-EG-009, Number 3 Emergency Diesel Generator Major Maintenance

Operability Test, following preventive maintenance window on February 8, 2021.

(6) Units 1 and 2 'B' emergency service water pump performance test following

maintenance (WO 38204215273) on March 10, 2021.

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance tests:

Surveillance Tests (other) (IP Section 03.01) (5 Samples)

(1) 1-OPT-EG-001, #1 emergency diesel generator monthly start exercise test on

January 4, 2021.

(2) 1-OPT-FW-002 for 3B motor driven auxiliary feedwater pump testing performed on

January 20, 2021.

(3) 0-IPT-CNL-LGC-8.8 for intake canal level logic testing performed on March 2, 2021.

(4) 0-LSP-FP-046, HVAC Fire Damper Operability inspections performed on

March 2, 2021.

(5) 0-OPT-FP-009 for diesel driven fire pump testing performed on March 26, 2021.

OTHER ACTIVITIES - BASELINE

71151 - Performance Indicator Verification

The inspectors verified licensee performance indicators submittals listed below:

IE01: Unplanned Scrams per 7000 Critical Hours Sample (IP Section 03.01) (2 Samples)

(1) Unit 1 (January 1 to December 31, 2020)

(2) Unit 2 (January 1 to December 31, 2020)

IE03: Unplanned Power Changes per 7000 Critical Hours Sample (IP Section 03.02)

(2 Samples)

(1) Unit 1 (January 1 to December 31, 2020)

(2) Unit 2 (January 1 to December 31, 2020)

8

IE04: Unplanned Scrams with Complications (USwC) Sample (IP Section 03.03) (2 Samples)

(1) Unit 1 (January 1 to December 31, 2020)

(2) Unit 2 (January 1 to December 31, 2020)

71152 - Problem Identification and Resolution

Annual Follow-up of Selected Issues (IP Section 02.03) (2 Samples)

The inspectors reviewed the licensees implementation of its corrective action program

related to the following issues:

(1) Operating Experience IN 86-14: PWR Auxiliary Feedwater Pump Turbine Control

Problems based upon known leakby at the unit 1 and 2 auxiliary feedwater turbine

driven pump (TDAFW) steam admission valves initially identified in 2020.

(2) During system walkdown on 12 December 2020, 2-CS-36, Refueling Water Storage

Tank (RWST) Cooler 2B inlet valve, was found to be leaking from the body-to-bonnet

connection. This resulted in tritium containing liquid reaching the soil and a voluntary

notification to state and local agencies.

INSPECTION RESULTS

Failure to Perform Fire Protection Program Surveillances

Cornerstone Significance Cross-Cutting Report

Aspect Section

Mitigating Green [P.2] - 71111.05

Systems NCV 05000280,05000281/2021001-01 Evaluation

Open/Closed

The inspectors identified a finding of very low safety significance (Green) and an associated

non-cited violation (NCV) of License Condition 3.I, Fire Protection, concerning Dominion

Energys failure to implement and maintain in effect the provisions of the approved fire

protection program as described in the Updated Final Safety Analysis Report. Multiple

examples of tests and inspections of fire protection components were not performed in

accordance with the Technical Requirements Manual which resulted in the discovery of

adverse conditions requiring corrective maintenance on December 29, 2020.

Description: On December 29, 2020, during a walkdown of the Surry Unit 1 Upper Cable

Spreading Room (CSR), the inspectors discovered multiple indications of degraded and

missing fire protection seals at the north, exterior, wall which supports carbon dioxide

suppression system functionality. Upon assessment, and lacking technical justification for

continued functionality, the station declared Unit 1 CSR low-pressure carbon dioxide (CO2)

suppression non-functional and entered the 14-day technical requirements manual action

statement (TRMAS) 3.7.3.A.2. During evaluation of the reported conditions and in response

to further inspector concerns, licensee engineering identified several additional degraded

conditions in penetrations along the wall between the Unit 1 CSR and mechanical equipment

room #1. These conditions adversely impacted the 3-hour rating of this Appendix R concrete

block fire wall. Lacking technical justification for continued functionality, the station entered

the 7-day TRMAS 3.7.8.A.2 to restore the CSR fire barrier.

9

TRM 3.7.8 assures functionality of fire protection program fire barriers including seals, doors,

and dampers. Licensee reviews found that three additional fire barriers within the scope of

TRM surveillance requirement (TSR) 3.7.8.1, located in the Unit 1 CSR and the adjacent Unit

2 CSR had been omitted from TRM fire barrier inspection surveillance procedures on

January 13, 2021. The licensee entered TRMAS 3.7.8.A.2 for multiple newly identified

degraded conditions associated with immediate inspections at these locations. TSR 3.7.8.1

verifies approximately 20 percent of fire-rated barriers and fire-rated penetration seals will be

functional by detailed inspection every 12 months and 100 percent of fire-rated barriers and

fire-rated penetration seals shall be inspected every five years. These omissions were

associated with several fire protection procedure changes occurring over two years beginning

on December 2, 2003. As the licensee evaluation continued, the inspectors observed that

although new concerns appeared to be identified in discussions with the staff and reviews of

condition reports and logs, the inspectors were unable to accurately track the expanded

scope of the review, those concerns that were truly adverse, and how all of the adverse

conditions were being corrected. Following inspector discussions with station leadership on

February 4, 2021, the licensee informed the inspectors that their assessment would be

incorporated into a programmatic level of effort evaluation (LEE), CA8354712.

During performance of a fire protection system self-assessment which immediately followed

the extent of condition assessment from CA8354712, the licensee reported nine fire dampers

were not inspected and exercised on March 1, 2021. The limited initial scope of CA8354712

failed to identify other fire protection systems, structures, and components within the scope of

TSR 3.7.8.2 which had also been omitted from their fire protection program implementing

procedures. TSR 3.7.8.2 verifies that associated fire doors and fire dampers will be functional

based upon inspection within every 18 months. Immediate surveillance of these locations

revealed exactly one damper, 01-VS-FDMP-53-DAMPER, the Service Building AC Unit 152A

Outlet Fire Damper, which did not close completely. All other locations were satisfactory.

Inspection of 01-VS-FDMP-53-DAMPER found foreign material resulting in misalignment of

the damper closure mechanism. The location was cleaned, exercised, and restored to

satisfaction. It should be noted, there are no cables or equipment important to safe shutdown

in the affected fire areas associated with 01-VS-FDMP-53-DAMPER.

Corrective Actions: A detailed licensee assessment of low-pressure CO2 suppression

capacity based upon system testing found that the cumulative effect of all discovered

degradation was within the margin of system functionality. Expedited corrective maintenance

at these locations restored Units 1 and 2 CSR 3-hour fire barrier functionality. Based upon the

expanded scope of identified missed and omitted TRM fire protection surveillances, the

licensee has established a complete review of implementation of all TRM surveillances.

Corrective Action References: CR1163099, CR1163112, CR1163563, CA8354712,

CA8369409

Performance Assessment:

Performance Deficiency: The inspectors found that Dominion Energys failure to implement

fire protection program inspection requirements specifically associated with TSR 3.7.8.1 &

3.7.8.2 was a performance deficiency reasonably within the licensees ability to foresee and

prevent.

Screening: The inspectors determined the performance deficiency was more than minor

because it was associated with the Protection Against External Factors attribute of the

Mitigating Systems cornerstone and adversely affected the cornerstone objective to ensure

10

the availability, reliability, and capability of systems that respond to initiating events to prevent

undesirable consequences. The NRC-identified barrier degradation requiring corrective

maintenance, as well as the licensee identified degradation discovered due to the missed

TSR 3.7.8.1 and TSR 3.7.8.2 inspections are examples of adverse effects to the cornerstone

objective. The inspectors used IMC 0612, Appendix E, Examples of Minor Issues, dated

January 1, 2021, to inform answers to the more than minor screening questions finding this

condition consistent with more than minor example 4.l.

Significance: The inspectors assessed the significance of the finding using Appendix F, Fire

Protection Significance Determination Process. This finding was determined to be of very

low safety significance (Green). All degraded barriers and dampers except for 01-VS-FDMP-

53-DAMPER screened to a low degradation grading in accordance with IMC 0609 Appendix

F Attachment 2 and, therefore, their safety significance was Green. While 01-VS-FDMP-53-

DAMPER screened to high degradation this example screened to Green based upon

Qualitative Screening Questions for Individual Fire Finding Categories - Fire Containment

Question 1.4.4-C in that there were no cables or equipment important to safe shutdown in the

affected fire area.

Cross-Cutting Aspect: P.2 - Evaluation: The organization thoroughly evaluates issues to

ensure that resolutions address causes and extent of conditions commensurate with their

safety significance. Upon identification of missed fire protection seal inspections within the

scope of TRM 3.7.8, Dominion Energy failed to thoroughly evaluate other potentially omitted

fire protection program TRM 3.7.8 surveillances to ensure that resolutions addressed extent

of conditions commensurate with their impact upon the fire protection program. This was

consistent with their failure to evaluate the scope of historic fire protection procedure changes

circa 2003.

Enforcement:

Violation: License Condition 3.I, Fire Protection, states in part, The licensee shall

implement and maintain in effect the provisions of the approved fire protection program as

described in the Updated Final Safety Analysis Report The UFSAR section 9.10.5, Tests

and Inspections, states in part, Tests and inspections of fire protection systems are

performed in accordance with the Technical Requirements Manual.

Contrary to the above, from December 2, 2003, until discovery on December 29, 2020,

Dominion Energy failed to implement and maintain in effect the provisions of the approved

fire protection program as described in the Updated Final Safety Analysis Report such that

multiple examples of tests and inspections of fire protection systems were not performed in

accordance with the Technical Requirements Manual.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with

Section 2.3.2 of the Enforcement Policy.

11

Minor Performance Deficiency 71152

Minor Performance Deficiency: During a system walkdown to investigate lowering RWST

level on December 12, 2020, 2-CS-36, RWST Cooler 2B Inlet Valve was found by the

licensee to be leaking approximately 0.04 gallons per minute (gpm) from the body-to-bonnet

connection to ground. Total Leakage was estimated to be greater than 100 gallons and tritium

concentration determined to be 4.5E07 picocuries per liter (pCi/L), requiring report in

accordance with the industry voluntary groundwater protection program and 10 CFR 50.72(b)(2)(xi) (Event Notification #55035). The inspectors determined that the licensee's

failure to implement the correct torque specification on the 2-CS-36 body-to-bonnet bolts in

accordance with vendor recommendations which led to loosening and leakage was a

performance deficiency reasonably within the licensee's ability to foresee and prevent.

Screening: The inspectors determined the performance deficiency was minor. Due to the

relatively large volume of the RWST, the leakage was not sufficient to challenge the capability

of the system. Therefore, in accordance with Inspection Manual Chapter 0612 Appendix B,

the performance deficiency could not be reasonably viewed as a precursor to a significant

event; if left uncorrected would not have led to a more significant safety concern; and did not

adversely affect a cornerstone objective.

Observation: Annual Follow-up of Operating Experience IN 86-14: PWR 71152

Auxiliary Feedwater Pump Turbine Control Problems

The inspectors performed an annual follow-up of selected issues associated with IN 86-14:

PWR Auxiliary Feedwater Pump Turbine Control Problems, based upon known leakby at the

Units 1 and 2 TDAFW steam admission valves initially identified in 2020. The inspectors

reviewed preventive maintenance records, procedures, corrective action program documents,

station logs, and condition monitoring.

During a field walkdown the inspectors observed an apparent increase in Unit 2 TDAFW

casing leakage which directs condensation from the steam leakby at the admission valves to

the main steam valve house floor drains. Inspectors discovered that this leakage had

changed from drops per minute during the previous quarter to a steady pencil stream.

IN 86-14 provides operating experience at multiple stations wherein condensed steam leakby

in TDAFW steam admission lines resulted in turbine overspeed trips and auxiliary feedwater

start failures. Surry internal operating experience captured similar events in the early 1990s.

The inspectors found that though the station was experiencing TDAFW steam admission

leakby, they had not established any additional tracking actions to periodically assess

changes in casing leakage. Upon being informed of the apparent increase in casing leakage,

the licensee performed troubleshooting to validate that the rise in condensation rate with the

steam admission lines was within the capacity of the system to mitigate and drain. The station

bypassed steam traps within the TDAFW steam admission lines and observed casing

leakage to the floor drain. Changes in casing leakage to the floor drain would indicate that the

capability of the system to capture and drain steam admission valve leaky was challenged.

The licensee did not observe any adverse indication during this troubleshooting activity

indicating that the increased leakage is within the capacity of the system to mitigate and

remove.

The inspectors found that the licensee had not established additional specific actions within

work control or corrective action programs to assess and evaluate increased leakby or

condensation within the TDAFW steam admission lines which could result from further

12

degradation of the known leakby at the steam admission valves. However, the current leakby

is within the capacity of the TDAFW casing drainage system to prevent adverse impact upon

TDAFW controls. The licensee has incorporated this observation into operator rounds

turnover and system engineering condition monitoring activities to identify any changes in

TDAFW casing drain leakage to the main steam valve house floor drains. Corrective actions

on the TDAFW steam admission valves have been scheduled for the Units 1 and 2 refueling

outages in spring and fall of 2021 as the required valve maintenance cannot be performed

online.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On April 12, 2021, the inspectors presented the integrated inspection results to Mr. Doug

Lawrence, Surry Site Vice President and other members of the licensee staff.

  • On January 27, 2021, the inspectors presented the licensed operator requalification

inspection results to Mr. Doug Lawrence, Surry Site Vice President and other members

of the licensee staff.

13

DOCUMENTS REVIEWED

Inspection Type Designation Description or Title Revision or

Procedure Date

71111.01 Procedures OP-ZZ-021 Severe Weather Preparation 27

71111.04 Corrective Action CR1165994

Documents CR1166249

Resulting from

Inspection

Drawings 11448-MKS- Component Cooling Water to Spent Fuel Pit - Isometric 4

112AR1

11548-FM-088B Flow/Valve Operating Numbers Diagram Chemical and 49

SH-2 of 3 Volume Control System

4160 Volt System 11448-FE-1A1 33

Unit 1 & 2

Miscellaneous SDBD-SPS-EG Emergency Diesel Generator System Design Basis 21

Document

SDBD-SPS-MS Main Steam and Ancillary System Design Basis Document 20

Work Orders 38204202497

71111.05 Corrective Action CR1165866, Unannounced Fire Drill Condition Reports

Documents CR1166286,

CR1166288,

CR1166291,

CR1167188,

CR1167708,

CR1167957

Fire Plans 1-FS-FP-102 Unit 1 Cable Vault Tunnel Elevation 9 feet - 6 inch 003

1-FS-FP-127 Unit 1 Cable Spreading Room Elevation 45 feet - 3 inch 005

2-FS-FP-157 Charging Pumps - Unit 2 Auxiliary Building Elevation 13 feet 3

- 0 inches and 2 feet - 0 inches

71111.06 Corrective Action CR1167826,

Documents CR1167810,

CR1167797,

CR1167796

71111.11B Corrective Action CR1164400 NRC concern of question duplication between validation and 01/22/2021

Documents actual administered biennial written exams.

14

Inspection Type Designation Description or Title Revision or

Procedure Date

Resulting from CR1164522 NRC concern with the number of operators validating 01/25/2021

Inspection biennial written exam.

Miscellaneous 38.12A, 23.03B, 2021 Annual Operating Test JPMs 01/20/2021

99.06A, 35.11A,

88.65, 52.03B,

99.04D, 88.66,

23.02D, 26.12

C4 SE-2, SE-4, 2021 Annual Operating Test Scenarios 01/20/2021

SE-7, SE-8

XB-2 Biennial Written Exam 02/21/2020

XB-4 Biennial Written Exam 03/06/2020

71111.11Q Procedures 1-OP-CH-023 Boration Followed by Manual Make-up Using the Blender 012

1-OSP-TM-001 Turbine Inlet Valve Freedom Test 043

71111.12 Corrective Action CR1165268

Documents

Corrective Action CR1166329

Documents

Resulting from

Inspection

Miscellaneous 3131846 2-FW-P-4B Oil Sample Analysis 03/04/2021

PRA-SPS- Surry Maintenance Rule Ranking and Performance Criteria 5

RA.PR.2

Procedures 2-OSP-FW-002 Auxiliary Feedwater Booster Pumps 11

Work Orders 38103094695,

38103336426

71111.13 Miscellaneous PHOENIX Scheduler's Evaluation for Surry Power Station, 01/05/2021

Units 1 and 2

PHOENIX Scheduler's Evaluation for Surry Power Station, 01/20/2021

Units 1 and 2

PHOENIX Scheduler's Evaluation for Surry Power Station, 01/25/2021

Units 1 and 2

PHOENIX Scheduler's Evaluation for Surry Power Station, 02/07/2021

Units 1 and 2

PHOENIX Scheduler's Evaluation for Surry Power Station, 03/09/2021

15

Inspection Type Designation Description or Title Revision or

Procedure Date

Units 1 and 2

SPS-CR.3 Rev.35 Surry Power Station Unit 1&2 Probabilistic Risk Assessment Rev 35

Model Notebook

Work Orders Work Order ESW Pump 1B Discharge Expansion Joint: Inspect 24" 03/10/2021

  1. 38204198119 Expansion Joint and 3" Flange (Drone)

71111.22 Procedures 0-IPT-CNL-LGC- Intake Canal Level Logic Testing 03/02/2021

8.8

0-OPT-FP-009 Diesel Driven Fire Pump Test 03/26/2021

1-OPT-FW-002 3B Motor Driven AFW Pump Test 01/20/2021

71151 Miscellaneous Surry Units 1 and 2 Plant Process Computer Calorimetric

Power January 1, 2020 through December 31, 2020

71152 Corrective Action CR1151760,

Documents CR1157069

CR1162330

CR1166724,

CR1166839,

CR1166898,

CR1166919,

CR1166929,

CR1166932,

CR1166944,

CR1167770,

CR1167867

Corrective Action CR1163330,

Documents CR1163345,

Resulting from CR1163563,

Inspection CR1163727,

CR1163917,

CR1164214,

CR1164268

Miscellaneous Surry Updated Final Safety Analysis Report 9/30/2020

Surry Power Station Technical Requirements Manual 12/31/2020

16

Inspection Type Designation Description or Title Revision or

Procedure Date

Turbine Driven Auxiliary Feedwater Pump Troubleshooting 03/03/2021

Control Form

EN#55035 NRC Form 361 Reactor Plant Event Notification Worksheet 12/12/2020

ET-CEP-06-0018 Results of Low Pressure CO2 Leakage Test Rev. 2

Procedures 0-MCM-0402-01 ITT Industries (Grinnel) Diaphragm Valve Maintenance 35

Self-Assessments CA8263622

17