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Category:DEFICIENCY REPORTS (PER 10CFR50.55E & PART 21)
MONTHYEARML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers ML20205N8341999-04-0101 April 1999 Part 21 Rept Re Automatic Switch Co Nuclear Grade Series X206380 & X206832 Solenoid Valves Ordered Without Lubricants That Were Shipped with Std Lubrication to PECO & Tva.Affected Plants Were Notified ML20236N6751998-07-0909 July 1998 Part 21 & Deficiency Rept Re Notification of Potential Safety Hazard from Breakage of Cast Iron Suction Heads in Apkd Type Pumps.Caused by Migration of Suction Head Journal Sleeve Along Lower End of Pump Shaft.Will Inspect Pumps ML20217D5701998-03-20020 March 1998 Part 21 Rept 40 Re Governor Valve Stems Made of Inconel 718 Matl Which Caused Loss of Governor Control.Control Problems Have Been Traced to Valve Stems Mfg by Bw/Ip.Id of Carbon Spacer Should Be Increased to at Least .5005/.5010 ML20198Q6961998-01-12012 January 1998 Part 21 Rept Re Failed Operation of Agastat EGPI004 Relay on 971129,as Reported by Limerick Station.Caused by Insufficient Soldering.Will Notify Customers Who Purchased EPI004 & ETR14XXX004 Relays During June 1996 ML18038A8971994-09-0707 September 1994 Part 21 Rept Re Defect in Latching Mechanism of Potter & Brumfield Relay on C&D High Voltage Shut Down Alarm Assembly Printed Circuit Boards.Pull Test on Relay Reset Button Incorporated Into Receiving Insp Procedures ML20059F2631994-01-0707 January 1994 Part 21 Rept Re Air Start Distributor Cam Mfg by Fairbanks Morse.Mfg Suggests That Site Referenced in Encl App I Inspect Air Start Distributor Cam as Soon as Practical ML20058G5981993-11-17017 November 1993 Part 21 Rept Re Westronics Recorders,Model 2100C.Signal Input Transition Printed Circuit Board Assembly Redesigned to Improve Recorder Immunity to Electromagnetic Interference.List of Affected Recorders & Locations Encl ML20059L9861993-11-11011 November 1993 Part 21 Rept Re Deviation Wherein Fully Open Butterfly Valve Located 15 Pipe Diameters Upstream of Sensors Was Disturbing Flow Profile Enough to Cause Ultrasonic Meter to Indicate 3 to 4% Low.Customers Notified & Valve Removed ML20125C7161992-12-0707 December 1992 Part 21 Rept Re Possibility for Malfunction of Declutching Mechanisms in SMB/SB-000 & SMB/SB/SBD-00 Actuators. Malfunction Only Occurs During Seismic Event.Balanced Levers May Be Purchased from Vendor.List of Affected Utils Encl ML20127P5861992-11-23023 November 1992 Followup to 921005 Part 21 Rept Re Potential Defect in SB/SBD-1 Housing Cover Screws.Procedure Re Replacement of SBD-1 Spring Cover Bolts Encl.All Fasteners Should Be Loosened & Removed.List of Affected Utils Encl ML20118B4391992-09-11011 September 1992 Part 21 Rept Re Degradation in ABB Type 27N Undervoltage Relays Used in Electrical Switchgear.Recommends That Users Review Applications Requiring Exposures Greater than 1E03 Rads TID W/Time Delay Function Option ML20090L8801992-03-18018 March 1992 Part 21 Re Cracked Piston Castings Received from Acme Foundry,Fairbanks Morse & General Casting.Magnetic Particle Insp of All Pistons Will Be Performed.List of Affected Plants Encl ML20059M1751990-09-24024 September 1990 Supplemental Part 21 Rept 1 Re Defect in Coltec Industries, Inc Connecting Rod Assemblies Nuts/Bolts on Model 38TD8-1/8 Emergency Generators.Initially Reported on 851120.Nuts/bolts for Assemblies at Stated Plants Inspected & Replaced ML20006A7141990-01-19019 January 1990 Updated Final Significant Deficiency Rept 107 Re Defective Agastat GP Relays.Initially Reported on 831129.Use of Subj Relays Does Not Represent Safety Concern & Not Reportable as Operational Concern.Test Program Developed ML20005G6831990-01-0505 January 1990 Part 21 Rept Re Installation Instructions for Grommet Use Range for Patel Conduit Seal P/N 841206.Conduit Seals in Environ Qualification Applications Inspected for Proper Wire Use Range & Grommets Replaced ML20245G0411989-08-0808 August 1989 Advises That Corrective Actions for Significant Deficiency & Part 21 Rept Re Unqualified Nupro Valve Seals Completed & Resolved,Per 890707 Rept.Only 98 Nupro Test Valves Furnished on GE Racks & Addl 17 Valves Provided for Other Racks ML20246J6411989-07-0707 July 1989 Supplemental Part 21 & Deficiency Rept L2-89-44 Re Nupro Test Valves,Installed on Instrument Line Racks Furnished by Ge,Not Remaining Leak Tight During DBA Conditions.Initially Reported on 890608.Root Cause Analysis Will Be Performed ML20245K9061989-06-30030 June 1989 Significant Deficiency Repts L2-89-08,38,43 & 45-48 Re Safe Shutdown Analysis.Corrective Actions Completed & Significant Deficiencies Considered Resolved ML20244A5101989-06-0707 June 1989 Final Significant Deficiency Rept SDR-L2-89-39 Re Failure of Stainless Steel Midlock Ferrules.Caused by Isolated Stress Corrosion Cracking Not Affecting Other Penetration Ferrules in Penetration 20JX222 Replaced ML20247Q7341989-05-31031 May 1989 Significant Deficiency Rept L2-89-34 Re Tavis Pressure Differential Transmitters Installed W/O Connecting Internal Heaters.Initially Reported on 890418.Heaters Will Be Connected on All Tavis Pressure Differential Transmitters ML20247N7731989-05-31031 May 1989 Supplemental Significant Deficiency Rept Re Safe Shutdown Analysis self-assessment ML20246F9051989-05-15015 May 1989 Significant Deficiency Rept L2-89-23 Re Essential Equipment Located in Unanalyzed Environ.Installation of Conduit Seals or Reorientation of Conduit Runs Planned to Avoid Moisture Intrusion Into Electrical Equipment Prior to Startup ML20246M3681989-05-0808 May 1989 Significant Deficiency Rept L2-89-06 Re Unavailability of Suppression Pool Indication Due to App R Fire.Caused by Design Error Resulting from Lack of Procedural Guidance. Reportability Evaluation Initiated ML20248F6101989-04-13013 April 1989 Interim Significant Deficiency Rept L2-88-11 Re Inadequate Degraded Grid Undervoltage Relay Setpoints.Event Discussed W/Engineer Involved to Ensure Procedural Adherence & New Undervoltage Relays Will Be Installed ML20248F3571989-04-0303 April 1989 Interim Significant Deficiency Rept SDR-L2-89-17 Re Unavailability of Feedwater Maint Isolation Valve to Support RCIC Operation in Event of App R Fire.Initially Reported on 890303.Cause Under Investigation.Rept to Be Submitted ML20248F9451989-03-28028 March 1989 Part 21 Rept Re Replacement of Circuit Boards for Safeguard Battery Chargers.Initially Reported on 890323.C&D Power Sys Provided Instructions to Change Out 600 Ohm Fixed Resistor w/500 Ohm Variable Resistor in Charger Circuitry ML20246H0951989-03-10010 March 1989 Significant Deficiency Rept L2-88-10 Re Improper Installation of Temporary Support Brackets in safety-related 4 Kv Switchgear.Support Brackets Removed from Switchgear Cubicle Prior to Startup & Procedures Revised ML20235F8601989-02-17017 February 1989 Interim Significant Deficiency Repts SDR-L2-89-03,04 & 05 Re Unavailability of HPCI & RCIC Sys Due to App R Fire. Initially Reported on 890117.Corrective Actions Under Review & Will Be Reported by 890531 ML20196B8281988-12-0202 December 1988 Final Significant Deficiency Rept 250-2 Re Use of Insulated Wire by Westinghouse in safety-related Motor Starters. Initially Reported on 881020.Defective Components Reworked & Corrected.Action to Prevent Recurrence Not Necessary ML20206C1571988-11-0404 November 1988 Interim Deficiency Rept 249-2 Re Nonavailability of Safe Shutdown Capabilities from Outside Control Room in Event of Fire.Initially Reported on 881006.Design Change Will Be Performed.Root Cause of Condition Still Under Evaluation ML20154Q4541988-09-28028 September 1988 Final Significant Deficiency Repts 230-2 & 231-2 Re Failures of Aluminum Vertical Bus & Belleville Washers in Cutler-Hammer Motor Control Ctrs.Aluminum Vertical Bus Replaced W/Tin Plated Copper Bus ML20153B6841988-08-25025 August 1988 Final Significant Deficiency Rept 238-2 Re Use of 600 Volt Type Thhn,Thwn or Thw Wire in 120 Volt Ac Convenience Receptacles & Lighting Circuits for Control Panels.Initially Reported on 880729.Panels,load Ctrs & Switchgear Inspected ML20151F3321988-07-0808 July 1988 Interim Significant Deficiency Rept 219-2 Re Discrepancies in Pgcc Wiring.Approx 130 Addl Minor Errors Out of 10,000 Terminations Discovered During Reinsp.Final Rept Will Be Submitted by 880815 ML20195B7641988-06-15015 June 1988 Final Deficiency Rept 232-2 Re Westinghouse Type Ds Fused Disconnect Switch.Initially Reported on 880415.Mechanical Connectors Integral to Fuse Mounting Assembly Would Not Adequately Secure Some 8 Awg Wires ML20155C3401988-06-0606 June 1988 Significant Deficiency Rept 137-2 Re Potentially Defective Type Hma Auxiliary Relays.Ge Notification Per 10CFR21 Encl. Potentially Defective Equipment Inspected & Corrected Per Field Disposition Instructions from GE ML20154E6381988-05-13013 May 1988 Interim Deficiency Rept Re Aluminum Vertical Bus Failures in Cutler Hammer Motor Control Ctr.Initially Reported During 880415 Telcon W/Nrc Regional Ofc.Evaluating Condition W/ Mfg.Next Rept Will Be Submitted by 880715 ML20154E6561988-05-13013 May 1988 Interim Deficiency Rept Re Use of Mechanical Cable Connectors on Westinghouse Type Ds Fused Disconnect Switches.Initially Reported on 880415.Determination of Extent That Both Wires Terminated W/Connectors Underway ML20154E4641988-05-13013 May 1988 Part 21 & Deficiency Rept Re Belleville Washer Failures in Cutler-Hammer Motor Control Ctrs.Initially Reported During 880415 Telcon.Exam of Failed Washers Showed Failure Due to Intergranular Decohesion.Detailed Rept Expected by 880715 ML20151A7511988-04-0404 April 1988 Final Significant Deficiency Rept 215 Re App R Safe Shutdown Capability for Fire Area 75.Diesel Generator Control Circuits Redesigned & re-reviewed Electrical Schematics & Application of Class 1E Isolation Relay ML20147G3671988-02-23023 February 1988 Final Significant Deficiency Rept 221-2 Re Westinghouse Dc Motor Control Ctrs.All Deficient Wiring in 20D201,20D202 & 20D203 Dc Motor Control Ctr Compartments Reworked to Approved Wiring Drawings ML20149N0931988-02-23023 February 1988 Final Deficiency Rept 221-2 Re Discrepancy Between Internal Control Wiring on Three Westinghouse Dc Motor Control Ctrs & Vendor Supplied Wiring on Schematic Drawings.Initially Reported on 871103.Wiring Compartments Reworked ML20234F5781987-12-31031 December 1987 Interim Deficiency Rept 219-2 Re Wiring within Power Control Complex Found in Configurations Not Specified in Connections Diagrams 865E214TR & 807E560TR.Initially Reported on 871204.Analysis Should Be Completed by 880601 ML20236V6051987-12-0202 December 1987 Interim Deficiency Rept 215 Re Fire Safe Shutdown Commitments as Documented in Section 3.2.1,Item 17 of Fire Protection Evaluation Rept.Initially Reported on 871022. Diesel Generator Control Circuits Redesigned ML20149M0971987-09-18018 September 1987 Final Deficiency Rept 213 Re High Acceleration Values for PSA-10 Snubbers.Initially Reported on 870819.All Snubber Installations That Use Size PSA-10 Snubbers Identified & Snubbers Mfg After June 1985 Will Be Installed ML20238C6301987-09-0101 September 1987 Significant Deficiency Rept 157 Re Asco Solenoid Valves on Velan air-operated Valves.Initially Reported on 840905. Completion Date for Corrective Actions Rescheduled to May 1989 Due to Const Schedule Changes.Model Number Corrected ML20238A2121987-08-24024 August 1987 Significant Deficiency Evaluation Rept 209 Re Limitorque Motor Operators W/Hydraulic Locking.Initially Reported on 870626.Limitorque Motor Operators Being Processed Through Rework Program.Item Not Reportable Per 10CFR50.55(e) ML20236P4971987-08-0505 August 1987 Advises That Corrective Actions Described in Util 870402 Deficiency Rept Complete Except for third-level Util Engineering Review & Util QA Findings.Completion of Review & Findings Anticipated by 871001 ML20236N7091987-07-31031 July 1987 Informs That Paul Munroe Actuators Have Not Been Installed to Correct Actuators Contrary to Statement in 840913 Final Significant Deficiency Rept 120.Other Mfg Being Used ML20206D0971987-04-0202 April 1987 Final Significant Deficiency Rept 198 Re Computer Aided Design & Drafting (Cadd) Conversion of P&ID & QA Diagrams. Initially Reported on 870303.Recheck of CADD-generated P&Ids Completed & Corrected P&Ids Reissued 1999-09-22
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217D1211999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Lgs,Units 1 & 2. with ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers 05000353/LER-1999-010, :on 990820,manual Actuation of Main CR Chlorine Isolation Mode Was Noted.Caused by Faint Chlorine Odor in Reactor Encl.Conducted Investigation & Was Unable to Locate Source of Odor1999-09-16016 September 1999
- on 990820,manual Actuation of Main CR Chlorine Isolation Mode Was Noted.Caused by Faint Chlorine Odor in Reactor Encl.Conducted Investigation & Was Unable to Locate Source of Odor
ML20212A8861999-09-13013 September 1999 Safety Evaluation Authorizing First & Second 10 Yr Interval Inservice Insp Plan Requestss for Relief RR-01 05000352/LER-1999-009, :on 990802,maint Was Performed That Required Disabling Certain Monitoring Capabilities on Safeguard Sys. Caused by Failure to Properly Use Plant Procedure.Monitoring Capability Was Restored to Svc & Tested1999-09-0101 September 1999
- on 990802,maint Was Performed That Required Disabling Certain Monitoring Capabilities on Safeguard Sys. Caused by Failure to Properly Use Plant Procedure.Monitoring Capability Was Restored to Svc & Tested
ML20212A4481999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Limerick Generating Station,Units 1 & 2.With ML20211E9891999-08-20020 August 1999 LGS Unit 2 Summary Rept for 970228 to 990525 Periodic ISI Rept Number 5 05000353/LER-1999-005-02, :on 990712,PCIV Isolation & Esfa Occurred Due to Blown Fuse.Caused by Mechanical Failure of Cold Solder Joing.Reset Isolation within Three Hours & 22 Minutes & Replaced Fuse1999-08-10010 August 1999
- on 990712,PCIV Isolation & Esfa Occurred Due to Blown Fuse.Caused by Mechanical Failure of Cold Solder Joing.Reset Isolation within Three Hours & 22 Minutes & Replaced Fuse
ML20210L7051999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Limerick Generating Station,Units 1 & 2.With ML20210H7391999-07-29029 July 1999 Safety Evalution Supporting Amends 136 & 101 to Licenses NPF-39 & NPF-85,respectively 05000353/LER-1999-004-02, :on 990701,determined That Thirteen MSRVs Failed to Meet 1% Setpoint Tolerance Due to Setpoint Drift.Caused by Corrosion Induced Bonding Between Pilot Disc & Seat.All Fourteen Srvs Pilot Valves Were Replaced1999-07-23023 July 1999
- on 990701,determined That Thirteen MSRVs Failed to Meet 1% Setpoint Tolerance Due to Setpoint Drift.Caused by Corrosion Induced Bonding Between Pilot Disc & Seat.All Fourteen Srvs Pilot Valves Were Replaced
05000352/LER-1999-007, :on 990617,inadvertent Emergency Svc Water Start During Test Equipment Installation Occurred.Caused by Personnel Error.Procedure Revised.With1999-07-14014 July 1999
- on 990617,inadvertent Emergency Svc Water Start During Test Equipment Installation Occurred.Caused by Personnel Error.Procedure Revised.With
05000352/LER-1999-005, :on 990611,RPS & ESF Actuations Were Noted. Caused by Personnel Error During Turbine Routine Testing. Revised Backup Overspeed & Power/Load Unbalance Test Routine Test Procedure.With1999-07-0909 July 1999
- on 990611,RPS & ESF Actuations Were Noted. Caused by Personnel Error During Turbine Routine Testing. Revised Backup Overspeed & Power/Load Unbalance Test Routine Test Procedure.With
05000353/LER-1999-003-02, :on 990607,bypass of RW Cleanup Sys Leak Detection Sys Isolation Functions on Three Separate Occasions Was Noted.Caused by Inadequate Review & Approval of Change to Sys Procedure.Procedure S44.7.C Revised1999-07-0707 July 1999
- on 990607,bypass of RW Cleanup Sys Leak Detection Sys Isolation Functions on Three Separate Occasions Was Noted.Caused by Inadequate Review & Approval of Change to Sys Procedure.Procedure S44.7.C Revised
05000352/LER-1999-004-01, :on 990606,ADS Was Inoperable During Planned Maint & Applicable TS Was Not Met.Caused by Inadequate Review Operability Requirements.Clearance Was Removed from Backup ADS Gas Bottles & Sys Was Returned to Service1999-07-0101 July 1999
- on 990606,ADS Was Inoperable During Planned Maint & Applicable TS Was Not Met.Caused by Inadequate Review Operability Requirements.Clearance Was Removed from Backup ADS Gas Bottles & Sys Was Returned to Service
ML20209G0211999-06-30030 June 1999 GE-NE-B13-02010-33NP, Evaluation of Limerick Unit 2 Shroud Cracking for at Least One Fuel Cycle of Operation ML20209D7741999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Limerick Generating Station,Units 1 & 2 ML20207H8331999-05-31031 May 1999 Non-proprietary Rev 0 to 1H61R, LGS - Unit 2 Core Shroud Ultrasonic Exam ML20195G4651999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Lgs,Units 1 & 2 ML20209D7791999-05-31031 May 1999 Revised Monthly Operating Repts for May 1999 for Limerick Generating Station,Units 1 & 2 ML20209F2381999-05-24024 May 1999 Safety Evaluation Supporting Amends 135 & 100 to Licenses NPF-39 & NPF-85,respectively 05000352/LER-1999-003-01, :on 990420,RPS & PCRVICS Actuations Were Noted, Due to Loss of FW Transient.Caused by Spuriously Opening Breaker.Deep Bed Condensate Deminerlizer Sys Was Replaced1999-05-19019 May 1999
- on 990420,RPS & PCRVICS Actuations Were Noted, Due to Loss of FW Transient.Caused by Spuriously Opening Breaker.Deep Bed Condensate Deminerlizer Sys Was Replaced
ML20206U6911999-05-19019 May 1999 Safety Evaluation Supporting Amend 99 to License NPF-85 05000353/LER-1999-002-03, :on 990419,various ESF Actuations Due to Loss of Power to 2A Rps/Ups Distribution Panel,Occurred.Caused by Loose Bus Bar Connection in RPS Breaker panel.Bus-bar Connection Inspected,Cleaned & re-tightened1999-05-18018 May 1999
- on 990419,various ESF Actuations Due to Loss of Power to 2A Rps/Ups Distribution Panel,Occurred.Caused by Loose Bus Bar Connection in RPS Breaker panel.Bus-bar Connection Inspected,Cleaned & re-tightened
ML20206U4991999-05-17017 May 1999 Safety Evaluation Supporting Amend 98 to License NPF-85 ML20206P8871999-05-14014 May 1999 Safety Evaluation Supporting Amend 97 to License NPF-85 ML20206N5761999-05-13013 May 1999 Safety Evaluation Supporting Amends 134 & 96 to Licenses NPF-39 & NPF-85,respectively ML20195B3021999-05-0606 May 1999 Rev 0 to PECO-COLR-L2R5, COLR for Lgs,Unit 2 Reload 5 Cycle 6 ML20206N2901999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Limerick Generating Station,Units 1 & 2.With ML20195G4761999-04-30030 April 1999 Revised Monthly Operating Repts for Apr 1999 for Lgs,Units 1 & 2 ML20206D8971999-04-22022 April 1999 Rev 2 to PECO-COLR-L1R7, COLR for Lgs,Unit 2 Reload 7, Cycle 8 ML20205N8341999-04-0101 April 1999 Part 21 Rept Re Automatic Switch Co Nuclear Grade Series X206380 & X206832 Solenoid Valves Ordered Without Lubricants That Were Shipped with Std Lubrication to PECO & Tva.Affected Plants Were Notified 05000352/LER-1999-002-01, :on 990303,failure to Perform TS Surveillance Required Locked Valve Insp Occurred.Caused by Personnel Error.Procedures Revised.With1999-04-0101 April 1999
- on 990303,failure to Perform TS Surveillance Required Locked Valve Insp Occurred.Caused by Personnel Error.Procedures Revised.With
ML20205N9311999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Limerick Generating Station,Units 1 & 2.With 05000352/LER-1999-001-02, :on 990217,old Rev of LGS PSP Was Discovered on Hard Drive of self-contained Computer in Security Ofc Area. Caused by Less than Adequate Ac.Security Force Was Placed on Heightened Awareness to Compensate for Compromise of SG1999-03-16016 March 1999
- on 990217,old Rev of LGS PSP Was Discovered on Hard Drive of self-contained Computer in Security Ofc Area. Caused by Less than Adequate Ac.Security Force Was Placed on Heightened Awareness to Compensate for Compromise of SGI
ML20204G9851999-03-11011 March 1999 Safety Evaluation Re Revised Emergency Action Levels for Limerick Generating Station,Units 1 & 2 ML20207J7461999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Limerick,Units 1 & 2.With ML20199G2371999-01-31031 January 1999 Rev 0 to NEDO-32645, Limerick Generating Station,Units 1 & 2 SRV Setpoint Tolerance Relaxation Licensing Rept ML20199L5301999-01-19019 January 1999 Special Rept:On 981214,seismic Monitor Was Declared Inoperable.Caused by Spectral Analyzer Not Running.Attempted to Reboot Sys & Then Sent Spectral Analyzer to Vendor for Analysis & Rework.Upgraded Sys Will Be Operable by 990331 ML20206R7881999-01-12012 January 1999 Safety Evaluation Supporting Amend 94 to License NPF-85 05000353/LER-1998-008-02, :on 981209,plant Personnel Identified That Unit 2 RCIC Turbine Steam Supply Line warm-up Bypass Valve Had Been in Partially Open Condition.Caused by Intermittment Control Circuit Anomaly.Control Circuit Replaced1999-01-0707 January 1999
- on 981209,plant Personnel Identified That Unit 2 RCIC Turbine Steam Supply Line warm-up Bypass Valve Had Been in Partially Open Condition.Caused by Intermittment Control Circuit Anomaly.Control Circuit Replaced
ML20205K0381998-12-31031 December 1998 PECO Energy 1998 Annual Rept. with ML20199F9611998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Limerick Generating Station.With 05000352/LER-1998-019, :on 981202,noted Unescorted Access to Contract Employee Who Had Tampered with Drug Test Specimen.Caused by Incorrect Computer Data Entry for pre-access Drug Screening. Will Develop Formal Training Program for Data Entry Clerk1998-12-23023 December 1998
- on 981202,noted Unescorted Access to Contract Employee Who Had Tampered with Drug Test Specimen.Caused by Incorrect Computer Data Entry for pre-access Drug Screening. Will Develop Formal Training Program for Data Entry Clerk
ML20198A3871998-12-10010 December 1998 Safety Evaluation Supporting Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power- Operated Gate Valves ML20198C7151998-12-10010 December 1998 Rev 1 to COLR for LGS Unit 1,Reload 7,Cycle 8 ML20206N4061998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Limerick Generating Station,Units 1 & 2.With ML20199E3281998-11-23023 November 1998 Rev 2 to PECO-COLR-L2R4, COLR for Lgs,Unit 2,Reload 4,Cycle 5 ML20195C9771998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Limerick Generating Station,Units 1 & 2.With ML20154J0311998-10-0101 October 1998 Safety Evaluation Supporting Amends 130 & 91 to Licenses NPF-39 & NPF-85,respectively 1999-09-30
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. PHILADELPHIA ELECTRIC COMPANY-2301 MARKET STREET P.O. BOX 8699 PHILADELPHIA A. PA.19101 (215)841 450o JOHN S. KEMPER 83NtOR VICE. PRESIDENT - NUCLE AR 10CFR50.55Ce)
May 31, 1989 U. S. Nuclear Regulatory Conmission Attn:- Docunent Control Desk Docket No.:
50-353 Washington, DC-20555 CPPR-107
SUBJECT:
Limerick. Generating Station, Unit 2 Supplemental Significant Deficiency Report, Safe Shutdown Analysis
REFERENCES:
See Enclosure 1 FILE:
. QUAL 2-10-2 (SDR-L2-88-07, SDR-L2-89-03,04,05,06,17, and SDR 249-2)
Gentlemen:
By those letters listed in Enclosure 1, we Indicated that.as
'part, of a self-assessment we were performing a root cause evaluation :
of the suspected deficiencies with the Limerick. safe shutdown analysis.
In each of the referenced letters, we further Indicated that we would provide a response discussing our assessment results and the proposed corrective actions. Enclosure 2 to this letter provides this' infonna-tion and closes.out that portion of each of the referenced significant deficiency letters concerning the safe shutdown self-assessment and corrective actions.
In addition, Enclosure 2' addresses the corrective-
. actions taken in response to SDRs L2-89-03, 04, and 05. This sup-plemental report represents PECo's final closure of those referenced SDRs related to safe shutdown analysis deficiencies.
If you have any further questions at this time, please contact us.
Since rel y, Y f /cgi -
7 Enclosures MAM/mv/05238901 cc:
W. T. Russell, USNRC, Administrator, Region I T. J. Kenny, USNRC, LGS Senior Resident Inspector R. J. Clark, USNRC, LGS Project Manager f
8906060022 890531 PDR ADOCK 05000353 S
PDC l g
_ = _ _ _ - - _
bec: S. J.'Kowalski G..M.
Leitch L. B. Pyrih
.R. J. Lees
.G. A. Hunger, Jr.
C. J. McDermott E. J. Bradley W. J. < Boye r, J r.
A. S. MacAinsh M. S. Iyer (Bechtel)
J. F. O'Rourke H. D. Honan G. J. Reid P. J. Duca M. A. Miller (TENERA)
N. Floravante (TENERA)
DAC (NG-8)
I m---------
f a.
REFERENCES 1)
Letter from S. J. Kowalski (PECo) to W. T. Russell (NRC) entitled,
" Interim Report [on] Nonavailability of Safe Shutdown Capabilities from Outside the Control Room in the Event of a Fire," dated February 1, 1989 (SDR-249-2) 2)
Letter from S. J. Kowalski (PECo) to W. T. Russo11 (NRC) entitled,
" Interim Significant Deficiency Report, Loss of the Emergency Diesel Generators Due to a Fire on the Control Complex," dated February 2, 1989 (SDR-L2-88-07) 3)
Letter from L. B. Pyrth (PECo) to W. T. Russell (NRC) entitled,
" Interim Significant Deficiency Report, Unavailability of the HPCI and RCIC Systems Due to an Appendix R Fire," dated February 17, 1989 (SDR-L2-89-03,04,05) 4)
Letter from S. J. Kowalski (PECo) to W. T. Russell (NRC) entitled,
" Interim Significant Deficiency Report, Unavailability of the Feedwater Maintenance Isolation Valve to Support RCIC Operation in the Event of an Appendix R Fire," dated April 3, 1989 (SDR-L2-89-17) 5)
Letter from S. J. Kowalski (PECo) to W. T. Russell (NRC) entitled, "Significant Deficiency Report, Unavailability of Suppression Pool Indication Due to an Appendix R Fire," dated May 8, 1989 (SDR-L2-89-06) i MAM/mv/05238902 4
1 i
1 _
LIMERICK SAFE SHUTDOWN ANALYSIS SELF-ASSESSMENT INTRODUCTION PECo's decision to initiate a self-assessment program of the Limerick safe shutdown (SSD) analysis was brought about by two concurrent events. First, Peach Bottom had reanalyzed its SSD analysis from which we obtained lessons learned and reviewed these lessons learned against the Limerick SSD analysis. Second, we conducted a series of reviews (not necessarily safe shutdown reviews) in preparation for Unit 2 startup which identified deficiencies. The Peach Bottom activity resulted in a bro der understanding of the fire protection requirements and the necessary supporting documentation. With the experience gained during these activities, a concern was raised with respect to root cause and adequacy of corrective actions. Thus, a Limerick self-assessment program was initiated in December 1988.
A number of safe shutdown analysis deficiencies were identified and reported under 10CFR50.55Ce) for Unit 2.
In each deficiency report IIsted in Enclosure 1, we Indicated that as part of a self-assessment we were performing a root cause evaluation of Limerick SSD analysis deficiencies. Upon completion of the analysis we would provide a response discussing assessment results and the proposed corrective actions. The discussion in the following sections provides this Information as corrmitted.
The status of the ongoing effort portion of the improvement program which will be complete prior to Unit 2 licensing is also provided.
LIMERICK SAFE SHUTDOWN ANALYSIS SELF-ASSESSMENT PROGRAM The self-assessment was conducted in two parts.
First, Bechtel, the architect / engineer for the project, performed an internal review.
This review included a progrartmatic and documentation overview of the safe shutdown analysis and a review of the documentation and evaluation of a sample fire area. Second, PECo performed a programmatic overview of the safe shutdown analysis. This two-part assessment program resulted in the determination of the overall root cause of the various deviations identified and specified the scope and schedule for corrective actions.
The topics evaluated by the self-assessment were as follows:
shutdown model/ assumptions, shutdown systems, shutdown components, shutdown circuits, shutdown procedures, and fire area evaluations and deviations from NUREG-0800 guidelines related to the post-fire shutdown capability.
The self-assessment efforts identified issues for correction and showed that the root cause of the SSD analysis deviations was two-fold:
(1) a lack of detailed procedures utilized in performing the safe shutdown analysis and (2~) a misunderstanding and misapplication of the detailed regulatory requirements, due in part to the changes in Interpretations over the course of IIcensing the Limerick Generating Station.
To address the root cause and assessment results, PECo initiated an improvement program for the Limerick safe shutdown analysis: the Limerick Safe Shutdown Analysis Improvement Program. The improvement program addresses the root cause through studies which broaden the evaluation of specific issues identified in the self-assessment. This improvement program also addresses the root cause through studies which provide a reverification of key aspects of the safe shutdown analysis. Upon completion of this program, detailed procedures for performing a safe shutdown analysis will be in place to prevent recurrence of similar SSD analysis concerns. The improvement program consists of an ongoing effort and an enhancement effort.
The root cause and the project plan for the Limerick Safe Shutdown Analysis Improvement Program were presented to the NRC in a meeting on January 23, 1989. The results of the assessmc t and the scope of the improvement program were discussed in subsequent meetings with the NRC on March 15, and April 6, 1989.
ONGOING EFFORT OF THE SSD ANALYSIS IMPROVEMENT PROGRAM The ongoing effort includes studies, modifications, and evaluations with the objective of providing verification of compliance to safe shutdown requirements and increasing the overall confidence in the program.
The ongoing effort is comprised of completed and ongoing studies, completed and ongoing modifications, and completed and ongoing evaluations to resolve concerns. Each aspect is discussed below.
Completed Studies Breaker Coordination Study - provided the calculation to support the Fire Protection Evaluation Report (FPER) statements that associated circuits which share a cormon power source were protected by coordination.
Procedure /Timelines Study (Preliminary) - provided preliminary (a) time-lines which dennnstrated that operator staffing and response times are appropriate for the safe shutdown procedure and (b) plant transient information to support the shutdown methodology.
High/ Low Pressure Interface Study - provided a re-identification and assessment of interfaces with the reactor coolant system.
Multiple High Impedance Faults Study (Restoration Procedures) - provided Identification of the breakers that would need to be restored in the event a fire that resulted in multiple faults on safe shutdown power supplies.
I Safe Shutdown Component Selection Criteria Study - provided a verification of the safe shutdown components.
Unit 2 Startup Interaction on Unit 1 Operation Evaluation - evaluated shared system interfaces between the two units with respect to the i
capability of shutting down Unit 1 in the interim period before Unit 2 I
operation.
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Remote Shutdown Panel (RSP) Halon System Evaluation - evaluated the effects of fire-induced spurious actuation of "ie Halon systen in the floor section of the RSP roan.
Limerick Core Uncovery Analysis - provided evaluation of the core con-ditions for safe shutdown nethods that utilize rapid depressurization and low pressure injection systens.
Fuse Control Study (Procedure Revision) - provided a methodology to control replacement of the fuses which are relied upon in the
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1 post-fire safe shutdown condition.
Fire Danage Prior to Transfer Evaluation - provided verification of the transfer switch designs with respect to the latest criteria.
Loss of Connunications Study - evaluates the ability of the existing connunication systen to address the needs of the post-fire safe shutdown procedures.
Ongoing Studies Procedures /Tinelines Study (Final) - provides final tinelines which demonstrate that operator staffing and response Lines are appropriate I
for the safe shutdown procedures and finalizes the plant transient Infonnation to support the shutdown methodology.
Valid Process Paraneters Study - evaluates the safe shutdown systens with respect to the plant's expected parameters (i.e.,
water level, j
pressure, and roan temperature).
l Ventilation Assessment - evaluates the temperature conditions for roons containing safe shutdown components.
Multiple High Impedance Faults Study (Final) - evaluates the effects of fire-induced, multiple high impedance faults on the safe shutdown power supplies.
Loss of Drywell Cooling Evaluation - evaluates the effects of a loss of the drywell cooling systems.
HPC1/RCIC Baronetric Condenser Evaluation - The original SSD analysis did not evaluate the HPCI/RCIC barometric condenser subsystens for safe shutdown.
Because of issues raised outside the scope of the SSD analysis, canponents are being re-evaluated for consideration in the SSD analysis.
The performance of these ongoing studies using the current interpreta-tions and appilcations of the regulatory reautrenents and guidance will result in the verification of Linerick regulatory compliance. As these studies and evaluations are completed, the potential exists to identify additional concerns with the Linerick design. These additional concerns would not necessarily represent deficiencies with respect to the fire pro-tection requirements.
Each additional concern has been or will be evaluated
c for deportability. These concerns nay require further evaluation and nay result in either modifications to the plant, procedural revisions, or updates to the supporting documentation. Any additional concerns will be addressed for safe shutdaan compliance prior to Unit 2 fuel load.
Completed Modification DC Power for RSP - The original safe shutdown analysis did not credit start of the diesel generators for some tine period following a fire-Initiated shutdown.
For this situation, poner for the reactor vessel level and pressure Indicators at the RSP would not have been available.
A modification has been completed to provide de power for this instrumentation.
(Modification Design Change Package (MDCP) 5950-2)
Ongoing Modifications RCIC Isolation Valve Closure - Division 3 powered RCIC steam containment isolation valve HV-49-12F007 can be closed by fire-caused danege to Division 3 steam leak detection circuits before these circuits are isolated by transfer switches at the RSP. Division 3 power is not available from the RSP. The RCIC steam containment isolation valve is being provided with an alternate Division 1 power supply which is available from the RSP. This modification corrects the deficiency identified in SDR L2-89-05.
(MDCP 5994-2) (Installation complete. Testing in progress.)
HPCI Trip Switch - Fire-caused start or valid process paraneter start of the HPCI could occur with fire danage to the HPCI trip circuits or
- unavailability of the HFe' trip switch.
If the autanatic trip on Level 8 does not stop the turbine, then HPCI would overfill the vessel to the nain steam lines. An electrical HPCI trip switch is being installed at the RSP which will pennit prompt operator action at Level 8.
This modification corrects the deficiency identified in SDR L2-89-04.
(MDCP 5995-2) (Installation in progress.)'
RCIC Flow Controller - Fire damage to circuits of the RCIC system prior to Isolation of these circuits by transfer switches at the RSP could result in danage to the RCIC speed controller and flow transmitter.
Thus, the RCIC systen vould not be controllable fran the RSP. Additional isolation for the RCIC circuitry is being provided.
(MDCP 5962-2)
(Installation conplete. Testing in progress.)
HPCI/ Core Spray Interface - Valve HV-52-12F037 was not included in the list of safe shutdown canponents. Spurious opening of the valve could affect the ability of HPCI to inject into the reactor vessel.
Cable protection is being provided to eliminate the possibility for fire-Induced spurious opening of the valve.
(MDCP 5989-2) (Installation complete. Testing in progress.)
RWCU Isolation - A fire in the control complex or Fire Area 70 East could result in spurious opening of the high-low pressure Interface j
valves located in the 4-inch RWCU blowdown line.
Spurious opening of
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three valves (HVC-44-2F033, HV-44-2F031, and either HV-44-2F034 or HV-44-2F035) would create a flow path from the pressurized reactor vessel to either the condenser or the radwaste equipnent drain
collection tank via low pressure piping. A disconnect switch will be provided to one of the three valves (HV-44-2F031), thereby ensuring that'a fire could not spuriously open all three valves. (MDCP 5998-2)
(Installation complete. Testing in progress.)
RSP Room Snoke Dampers - In accordance with the FPER, the supply and exhaust airflow rates for.the remote shutdown room are balanced so as to maintain a positive pressure with the room for both the nornal recircu-lation and outside air purge room. However, a fire to the auxiliary equipnent any render the ventilation systen inoperable, thereby allowing for the possibility of snoke infiltration into the renote shutdown panel roan.. The barriers, ducts, and doors between the auxiliary equipnent room and rennte shutdown panel are being nodified to restrict the passage of snoke. (MDCP 6007-0) (Installation in progress.)
Comro.'. cation Upgrade - In the event of a fire in one of several plant areas, the plant's connunication systens could be rendered inoperable.
The connunication system is being upgraded, including additional isolation cnd power supplies, to ensure its availability in the event of a fire.
(MDCPs 949 and 5993-0) (Installation in progress.)
Additional Energency Lighting - As part of the ongoing effort studies, the need for additional post-fire operator actions has been identified.
Energency lighting units are being provided for these actions, including the access and egress paths.
(Startup Change Request 2E5074)
(Installation in progress.)
Suppression Pool Instrumentation - In the event of a fire in the control complex, suppression pool level and temperature instrumentation ney not be available at the renote shutdown panel, The;e instruments are being provided at the remote st
.ch manel.
(Design Change Packages 2041 and 2043) (Installation complete. Testing in progress.)
Conpleted Evaluations The following concerns have been resolved without a plant modification.
HPCI Steam Leak Detection - Fire-caused danage prior to isolation of the steam leak detection circuits could cause the HPCI steam isolation valves to close.
For fire areas whe"e HPCI will be relied upon for safe shutdown, the procedures direct th'e operator to verify that the Isolation valve is open or to take action to open the valve. This evaluation resolves the deficiency identified in SDR L2-89-03.
Feedwater Isolation Valves - For post-fire safe shutdown, the credited
.flaa path for RCIC was through the noin feedwater lines. The feedaater isolation valves' circuits were not analyzed; therefore, a fire could potentially result in closure of these valves. Procedure GP-2 has been revised to remove power to these valves ducir.g power operation. Removing power to these valves precludes spurious operation.
i Ongoing Evaluations It is anticipated that the following concerns will be resolved without a plant modification.
RHR Pump Dead Heading - Valid process parameter start or spurious actuation of the RHR pump on reactor Level 1 in conjunction with fire-caused damage to the minimun flow valve circuits could lead to a situation where the punp is running without an open flow path (dead-headed).
Plant transient evaluations are being reviewed to determine if a fire would result in a Level 1 automatic start of the punp.
Currently, a safety evaluation is being developed to change the minimum flow valve from normally closed to normally open.
RHR Shutdown Cooling Valves - The RHR shutdown cooling suction valves HV-51-F008 and HV-51-F009 have been identified in the FPER as high/ low pressure interface valves. A safety evaluation is being developed to support removing power to one of the shutdown valves during paver operation. Removing power to one valve precludes spurious operation.
ENHANCEMENT EFFORT OF THE SSD ANALYSIS IMPROVEMENT PROGRAM The second step of the improvement program is a long-term enhancement program.
Immediately following completion of the ongoing studies, this enhancement program will be developed to reformat the safe shutdown analysis documentation and provide for long-term configuration management of the safe shutdown analysis. The enhancement effort is expected to provide:
Safe Shutdown Component Reverification Spurious Operation Reverification Safe Shutdown Cable Reverification Safe Shutdown Capability Reverification Part of the enhancement effort will be to format the safe shutdown analyses for Peach Bottom and Limerick into similar documentation.
Sunmary Due to an increasing incidence of reportable issues regarding the Limerick safe shutdown analysis, PECo conmitted to undertake an assessment of the root
'cause of these issues. We have identified the root cause and developed a two-phase program to ensure Limerick's compilance with applicable safe shutdown analysis requirements. The ongoing effort will ensure compliance at time of Unit 2 licensing. The enhancement effort will reverify aspects of the safe shutdown analysis and improve documentation to provide higher confidence in the analysis and better maintainability.
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MAM/mv/05238903
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