ML20247L272

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Insp Rept 50-298/98-02 on 980308-0418.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support
ML20247L272
Person / Time
Site: Cooper Entergy icon.png
Issue date: 05/15/1998
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20247L227 List:
References
50-298-98-02, 50-298-98-2, NUDOCS 9805220355
Download: ML20247L272 (36)


See also: IR 05000298/1998002

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ENCLOSURE 2

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket No.: 50-298

License No.: DPR-46

Report No.: 50-298/98-02

Licensee: Nebraska Public Power District

Facility: Cooper Nuclear Station

Location: P.O. Box 98

Brownville, Nebraska

Dates: March 8 through April 18,1998

Inspectors: Mary Miller, Senior Resident inspector

Chris Skinner, Resident inspector

Approved By: Elmo Collins, Chief, Branch C

Division of Reactor Projects

ATTACHMENT: Supplemental Information

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9805220355 980515

gDR ADOCK 05000298 I

PDR

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EXECUTIVE SUMMARY

Cooper Nuclear Station

NRC Inspection Report 50-298/98-02 l

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Ooerations

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Plant management demonstrated intrusive involvement in successfully demanding focus i

on and resolution of priority issues, allocating and directing engineering resources to l

reduce operator work-arounds, and understanding plant anomalies. Plant management

raised standards for staff performance in response to a snowstorm which blocked routine l

access to the site for over 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> and in the installation of the Z-sump modification l

(Section 01.1). l

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During a reactor startup and power operations, control room crews' operations evidenced

strong safety focus. They successfully implemented strong command and control,  !

awareness and assessment of plant conditions, questioning attitude, Technical I

Specification adherence, configuration control, and procedural adherence. Management

involvement was strong. Minor weaknesses were promptly corrected (Section 01.2). l

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Operations response to a snowstorm with limited plant access was excellent

(Section 01.3).

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Operations demonstrated a questioning attitude regarding operability of a safety-related

heat exchanger and successfully obtained engineering focus to address the operability

controls (Section O2.1).

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When a crew did not meet operations and training management expectations during

dynamic simulator training, a remediation was initiated. Inspectors observed that the

remediation process was self-critical and was based on many specific observations of

crew behaviors during simulator training. Operations management demonstrated strong

self-critical standards and continued close involvement with crew performance over the

training cycle (Section 05.1).

Maintenance

During observations of routine maintenance, inspectors observed procedural adherence,

radiation protection, and ALARA practices and found them generally good. Acceptance

criteria were properly referenced and followed. Cases in which data were not within

acceptance criteria, or anomalies were found, were dispositioned with problem

identification reports and/or documentation on a discrepancy sheet. The appropriate

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standards for initiation of problem identification reports appeared to have been met when

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problems were encountered (Section M1.1).

- Maintenance response to a snowstorm which blocked routine access to the site for over

24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> was outstanding. Two shifts of emergency response organization were formed

onsite as well as two shifts each of operations, security, and maintenance staff to

address plant operations, outage work, and effects of the snowstorm. For the majority of

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activities, maintenance and the outage organization took on a leadership role and

properly prioritized and coordinated site activities (Section M1.2).

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. Several examples of material condition were identified. In general, material condition is

good (Section M2.1).

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Maintenance responded promptly and provided a repair to a failed circulating water

valve. However, the valve was repaired with a modification without appropriate

administrative controls. Maintenance did not promptly verify safety-related valves with

similar designs. Also, similar essential valves were not promptly verified to determine if

the same mechanism may be a concern until after inspector involvement (Section M2.2).

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The licensee failed to properly implement corrective actions for inadequate torquing

instructions which had caused safety system inoperability. Administrative controls were

not implemented to ensure the word tight or tighten would be used appropriately in new

or revised procedures, the licensee failed to identify all maintenance procedures affected

by the concern, and no permanent corrective action for uncontrolled fastener installations

were addressed (Section M8.1).

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A violation for the failure to require verification of Technical Specification operability

requirements before increasing operating modes was not property corrected. The

licensee did not identify all operability verification requirements during the corrective

action process (Section M8.2).

Enaineerina

- The length of fuel had been increased from 144 to 150 inches. However, calculation

changes to implement the design change failed to change the reference point for the top j

of active fuel on fuel range levelindicators and emergency operating procedure

parameters. This caused a nonconservative bias in the fuel range indication of 6 inches.

The licensee evaluation concluded that, although this bias was nonconservative, it did i

not exceed the existing design margin (Section E2.1).

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Procedures for use during a loss of coolant accident and loss of offsite power directed

that core spray be throttled to 4750 gpm per pump, although 6100 gallons were required i

for core coverage, by the Updated Safety Analysis Report accident analysis I

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(Section E2.2).

- Engineering failed to implement clear instructions for controlling the electrical load profile

in emergency operating procedures. This profile is the basis for the Technical

Specification 7-day diesel fuelinventory requirement. Operations had not been

instructed that this profile must be used if the design basis loss-of-coolant accident

occurred (Section E2.3).

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The licensee did not recognize that paint applied in the reactor building contained an

unacceptably high percentage of volatile organics. The initial evaluation and restrictions

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on the painting, as well as the evaluation of the effect of this painting on standby gas

treatment, did not accurately address the technical issue or the iodine release profile,

and the control room was not informed of later developments (Section E2.4).

- For a modification to the Z-sump, engineering did not IS.itify all affected operating

procedures. Inspectors found that, if the nonessential power to the essential heat trace I

was lost due to electrical component failure, no requirements or actions were provided to

operators in abnormal or alarm response procedures to respond to this loss

(Section E2.5).

. The licensee failed to reconcile the design requirements for torus level to remain below

2 inches and the emergency operating procedures which allow a torus level up to

37 inches (Section E2.7).

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Engineering demonstrated weak support of an issue regarding a small amount of water

found in diesel fuel oil day tank. After discovery of water in one train of the diesel fuel oil

day tank, the licensee did not promptly check for water in the redundant train until after

inspector questioning a day later (Section E2.9).

- The licensee failed to evaluate the extent of condition of a violation for improper

incorporation of design modifications in emergency procedures (Section E8.1).

Plant Sucoort

- The work control staff initiated interdepartmental dose reduction efforts, found dose

reduction opportunities, and documented the results in weekly lessons teamed reports to

inform and provide expectations for site staff (Section R1.1).

  • During the snowstorm when routine access to the site was cut off for over 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />, the I

emergency response organization promptly contacted state officials and assessed

personnel onsite to evaluate emergency response to fulfill requirements for two shifts of

an emergency response organization (Section P1.1).

comparing past drill performance observations during the critique, due to ownership by

the technical support center director (Section P7.1).

- Security responded appropriately to indications of a broken seat on a diesel fuel tank

inlet (Section S1.2). l

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Egoort Details

Summarv of Plant Status

The plant was shut down at the beginning of this report period for a midcycle outage. The plant I

achieved criticality on March 13,1998, connected to the grid on March 14, and reached

100 percent power on March 16. On March 21, a circulating water motor-operated valve failed.

Operations reduced power to 71 percent as required by procedures. The plant was retumed to

100 percent power on March 23. On April 13, the lube oil pump for Reactor Feedwater Pump B

seized, causing a momentary feedwater pump trip signal and brief reduction of the feedwater

pump flow. Operators reduced power to 75 percent for troubleshooting and repairs. The lube oil

pump was replaced and full power was restored on April 15.

l. Operations

01 Conduct of Operations

01.1 Plant Manaaement involvement in Licensed Activities

a. Insoection Scoce (71707)

Inspectors observed several routine licensed activities, such as plan-of-the-day

meetings, shift turnovers, condition review groups, corrective action review board closure !

reviews, outage meetings, modification project management meetings, and station

operations review committee meetings.

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b. Observations and Findinas  !

During the inspection scope activities, multiple instances of strong plant management

action were observed. Plant management successfully demanded focus of resources on

l resolution of problems. Inspectors observed plant management performing plant

walkdowns several times per week. Several examples were observed where plant

management demanded and successfully raised standards for improving questioning

attitudes toward anomalous conditions, identification and final resolution of problems,

maintenance of plant equipment, housekeeping, presence of supervision in the field, and

a stronger questioning attitude by plant staff. Plant management successfully demanded

higher standards by the operations organization in interfacing with the work control

organization and implementing plant scheduling requirements in a more thoughtful and

timely manner.

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l Plant management demonstrated strong involvement and demands to focus plant staff to

resolve key plant issues. Examples include resolution of Z-Sump modification

installation, response to a heavy snowstorm blocking roads for 24-hours, understanding

and improving plant thermal performance, involvement and resolution of the fuel bundle

length versus reactor vessel water level indication parameters associated with

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emergency operating procedures, strong demands for engineering support to address

long-term operator work-arounds, and multiple housekeeping and radiation practice

improvements.

Plant management demonstrated leadership of the corrective action program by leading

a generally successful initiative to raise corrective action standards by review of closure

packages for significant conditions adverse to quality. This initiative resulted in rejection

of several closure packages and reopening of several condition reports to further define

problem scope and implement more effective corrective action. Plant management has

also demonstrated a strong positive standard for the station operations review

committee, for both improving a questioning attitude and successfully raising standards

for station operationsireview committee approval actions. Similar effectiveness has been

demonstrated in approximately weekly attendance of condition review group meetings.

c. C_onclusion

Plant management demonstrated intrusive involvement in successfully demanding focus

on and resolution of priority issues, allocating and directing engineering resources to

reduce operator work-arounds, and understanding plant anomalies. Plant management  !

raised standards for staff performance in response to a snowstorm which blocked routine

access to the site for over 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> and in the installation of the Z-sump modification. l

O1.2 Strona Crew Performance in Startuo and Routine Ooerations

a. Insoection Scooe (71707)

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Inspectors observed control room crew performance during a midcycle outage, a reactor

startup and return to full power, and routine full power operations. Inspectors held

discussions with licensed and nonlicensed operators and operations management.

b. Observations and Findinos

inspectors observed strong, positive control of plant conditions during all portions of this

inspection scope and many examples of a strong questioning attitude and refusal to

allow schedule pressure to affect plant startup and control room operations. Shift

technical engineers identified problems and coordinated with shift management and

operations management to resolve several issues requiring engineering and licensing

evaluations. Communication between operators was complete, clear, and directed

toward appropriate prioritized activities. Inspectors observed multiple crews coordinate

with work control to minimize control room distractions, particularly during infrequent

evolutions such as reactor startup and power ascension. This indicated correction of a

past vulnerability which caused an event during the last startup. The following examples

provided are indicative of operations performance.

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Inspectors observed Surveillance Procedure 6.1RPS.307, " Reactor Vessel Low-High

Water Level Calbration and Functional Test," Revision 2, scheduled during shutdown

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activities shortly after plant shutdown. The reactor operator in charge of the evolution

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questioned the appropriateness of performing a reactor levelinstrument surveillance i

during this evolution which has the potential to cause a Group 2 isolation of shutdown

cooling. The licensee documented the concern in Problem Identification Report 2-28381

which noted that the test affected Primary Containment isolation System Group 2 and

should not have been perfornied under the current plant conditions. The surveillance ,

was postponed until after the decay heat generation rate had been reduced  !

considerably. This demonstrated a strong questioning attitude and good plant i

knowledge.

On March 21, Circulating Water Valve CW-MOV-103 failed, isolating the circulating water

in the Condenser B2 water box, causing condenser maximum increase of 3 inches

mercury absolute. Operations reduced power to 71 percent as required by procedures.

The vacuum reestablished at former levels as power was decreased. Maintenance and

engineering support were called into the site. Reactor engineering provided control rod

adjustment procedures to ensure rod line remained below the 105 percent required by

analysis. During the downpower transient and feedwater heating transition, rod line

reached 108.9 percent. Reactor engineering and the control room staff concluded that

the transient value had been previously analyzed and was acceptable. The required

chemistry analysis was performed. The inspector observed the control room activities

shortly after the transient. The shift supervisor reviewed the plant conditions and status

of the evaluations, solicited input from each licensed crew member, and emphasized

procedure adherence, communications, and attention to detail. The shift technical

engineer coordinated activities with reactor engineering and maintenance. Subsequent

return to full power was also coordinated with reactor engineering.

Shift technical engineers demonstrated strong performance in resolving issues affecting

plant operations and demanding resources and technical support when required. For

example, a shift technical engineer initiated a problem identification report documenting  !

that the new engineering process for conveying equipment operability information had l

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not assured adequate or timely information to the control room for an equipment issue.

On a separate NRC issue regarding a potential bias of the vessel fuel zone level

indication, operations support staff and shift technical engineers found indications that

the concern may be valid contrary to the conclusion reached by engineering. Operations

management and a shift technical engineer concluded that the facts and potential scope

of the concern should be researched over the weekend by available shift resources. 1

Shift technical engineers evaluated and documented a seven-page contingency and

scope matrix. When the issue was confirmed, operations promptly implemented the

contingency matrix. i

Generally, turnovers were very well organized. They were complete, formal, and concise

at all crew levels. Turnover meetings were crisp and complete, with strong positive

control of the meeting by the shift supervisor and control room supervisor. Two minor

observations of reduced formality were observed, which were not recognized and

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l corrected by the operations supervisor. After discussion with the inspector, operations

management re-emphasized standards. No further reductions in the level of formality

were observed.

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The licensee implemented a method of controlling shutdown cooling by using the

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residual heat removal heat exchanger outlet valve (RHR-MO-128). This is a

nonthrottleable valve controlled by a keylock switch on control room panel. The valve is

maintained in position by opening its power supply breaker at the motor control center.

The position is changed by closing the breaker for a specified number of seconds,

calibrated to percent of full stroke. Original plant design had the service water heat

exchanger outlet valves (SW-MO-89A and -B) used for controlling shutdown cooling, but

the valves did not work due to river water corrosion effects and the heat exchanger

bypass valves do not have adequate capacity. Operations management identified this

condition as an operator work-around and has added this to the engineering work

assignments to resolve work-arounds. Inspectors also observed that this breaker, which

is out of normal position, is not controlled by a tagging order, but by procedure.

However, the position of the breaker for the residual heat removal pump valve

(RHR-MO-168) was controlled by a tagging order when it was out of its normal position

in the same procedure. This aspect of valve control will be reviewed by operations.

A station operator demonstrated good observation skills when he identified that, when

Service Water Pump C was started, the pump slightly moved on its foundation.

Maintenance technicians performed troubleshooting actions and determined that three of )

the eight foundation bolts were loose. Operations requested that the other service water {

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pump foundation bolts be verified tight, and no other bolts were found loose.

During the outage and subsequent power operations, no violations of Technical

Specifications or procedural adherence were observed. Configuration control was i

excellent. Management presence and involvement was observed on a daily basis.

c. Conclusion

During a reactor startup and power operations, control room crews operations evidenced

strong safety focus. They successfully implemented strong command and control,

awareness and assessment of plant conditions, questioning attitude, Technical

Specification adherence, configuration control, and procedural adherence. Management

involvement was strong. Minor weaknesses were promptly corrected.

01.3 Resoonse to Difficult Site Access Conditions Caused by Snowstorm

a. Insoection Scoce (71707)

Inspectors observed licensee activities during blizzard conditions which significantly

impaired access to the site over 24-hours.

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b. Observations and Findinas  ;

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On March 8,1998, during the midcycle outage, with the plant in a shutdown, vented ,

condition, a heavy snowfall and strong wind condition occurred. Plant access was l

difficult because of a heavy winter snowstorm accompanied by strong shifting winds,

causing massive drifting over east-west roads and highways of the area. The licensee

contacted the Nemaha County Sheriff's department and was informed that some major

roads providing access to the site were closed by snow. The licensee contacted the

state officials from both Nebraska and Missouri regarding assessment of site access

requirements. State officials determined that, although some roads were passable by

specialty vehicles, travel of the major east-west highways was not possible. The

licensee initiated a report in accordance with 10 CFR 50.72 informing the NRC that

access to the site was impaired by snowstorm and that state and county officials had

been contacted regarding the difficult access and evacuation conditions. A resident

inspector was on site and observed the licensee's response.

Operations assessed onsite staff and found adequate shift staffing, with the exception of

a second shift supervisor. The licensee provided speciality ground transportation and

brought another shift supervisor to the site. Operations also assessed and determined

that the off-site grid was stable and verified no abnormal plant condition existed.

Operations coordinated with security and emergency planning to assure adequate site i

staffing for two shifts.

Operations coordinated with maintenance to conduct outage activities at a rate

appropriate to the staffing onsite, assuming that relief would not be available within

24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. Meals were provided for personnel on shift. Further, licensee speciality

vehicles transited major routes to the nearby towns of Auburn and Nemaha, Nebraska,

for the transportation of some licensee staff to and from their homes.

On March 10, Nebraska and Missouri state officials had determined that roads were

sufficiently cleared to allow site evacuation commensurate with emergency plan

requirements. By this time, licensee staffing was returned to normal.

c. _Gpnclusions

Operations' response to a snowstorm with limited plant access was excellent.

O2 Operational Status of Facilities and Equipment

O2.1 Operability of Reactor Eauioment Coolina Heat Exchanoer Run in Backwash

a. Insoection Scooe (71707)

Inspectors reviewed licensee's activities associated with operations' questioning

operability controls for running the reactor equipment cooling heat

exchanger in a backwash configuration.

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b. Observations and Findinos

The shift supervisor questioned the adequacy of the procedure giving instructions to

perform a backwash of a reactor equipment cooling heat exchanger. The procedure did

not specify whether the system was operable. The shift supervisor requested an

engineering evaluation and delayed the backwash evolution. The shift supervisor

declared the reactor equipment cooling heat exchanger inoperable while being

backwashed. The licensee initiated Problem identification Report 2-27269 to question if

, the quarterly backwash of the reactor equipment cooling heat exchanger involved an

operability concern.

Engineering's evaluation concluded that parallel flow in backwash removed less heat

than counter flow in normal operation; the backwashed heat exchanger should be

declared inoperable during the evolution.

The inspectors noted that under design basis conditions the maximum river temperature

would not support removal of design basis heat loads from the backwashed reactor

equipment cooling heat exchanger since the service water first ran through the operable

heat exchanger and then reversed through the inoperable heat exchanger, having

removed heat from the first exchanger in line. The evaluation did not address river water

temperature limit when the backwash heat exchanger could no longer perform its design

basis function or qualifications of piping in use to perform backwash operations.

The licensee also did not address past operability of performing this activity under high

river temperature conditions or the vulnerability of a lack of operational controls to

preclude this con'iguration with high river temperatures. This is an inspector followup

item (50-298/98002-01).

c. Conclusions

Operations demonstrated a good questioning attitude regarding operability of a safety-

related heat exchanger and successfully obtained engineering focus to address the

operability controls.

02.2 Station Ooerators identification of Problerns

a. Insoection Scoce (71707)

During a routine tour in the reactor building, the inspectors identified that a manual valve

hand wheel was in contact with safety-related electrical conduit. Discussions were held

with operations and engineering staffs.

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b. Observations and Findinos

On March 29,1998, during a routine walkdown the inspector identified that the

handwheel on Reactor Core Isolation Cooling Valve RCIC-96 was in contact with a

2-inch electrical conduit leading to the reactor core isolation cooling starter rack. The -

inspectors also observed four scribe marks at approximately 1/8-inch intervals below the

contact point of the valve indicating that, as the valve had been opened and closed in the

past, it had scribed the conduit in multiple locations during its travel.

l Station operators had not questioned the acceptability of the handle for a manual valve

L contacting electrical conduit. Engineering evaluation concluded the condition would not

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Tne inspectors identified a minor plant configuration issue that was not questioned by

station operators.

05 Operator Training and Qualification

05.1 Remediation of Ooeratina Crew Durina Trainino Process

a. Insoection Scone (71707)

Inspectors observed the licensed operator training and remediation process for a crew

which did not meet management expectations during dynamic simulator training.

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b. Observations and Findinas  ;

On April 6,1998, a crew in training performed a dynamic simulator scenario. Their i

l actions to obtain important parameters to allow diagnosis of plant conditions were not

l timely enough to meet management expectations. Also, coordination between the shift

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supervisor and the shift technical engineer was not implemented in a sufficiently strong

manner to meet management expectations. The licensee concluded that the crew would

have carried out licensed responsibilities during an event in an adequate manner, but i

that they failed to meet maagement expectations. Therefore both training and l

operations management concluded remediation of the crew performance was warranted.

l inspector review of crew performance found this conclusion to be appropriate.

The inspector observed some of the remediation activities, including a dynamic simulator

scenario evaluation by operations and training staff. The inspector observed self-critical

standards by both the crew and operations management. The evaluation was

comprehensive, specifically addressing several examples of strengths and weaknesses.

The inspector identified several observations, many of which were identified by the crew,

trainers, and operations evaluators. The inspector's observations which were not

originally addressed by the licensee focused on reactivity management and sensitivity to

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the effects of plant conditions and equipment failures on reactor power. Operations

management acknowledged these observations and re-emphasized a need for high crew

sensitivity to reactivity management and effects on reactor power.

During the critique, operations management required that the crew performance be

evaluated with respect to the past performance evaluations to allow the crew to evaluate

their performance and conclude if they considered the remediation adequate. This

indicated a demand for crew members to internalize a strong standard of fact-based,

self-critical performance eva.'uation.

The licensee concluded that the remediation had corrected the majority and severity of

the performance concems. However, operations management concluded that followup

in future training weeks would be performed for this crew to determine if an adverse trend

in any of these areas occurred.

c. Conclusions

When a crew did not meet operations and training management expectations during

dynamic simulator training, a remediation was initiated inspectors observed that the

remediation process was self-critical and was based on many specific observations of

crew behaviors during simulator training. Operations management demonstrated strong

self-critical standards and continued close involvement with crew performance over the

training cycle.

08 Miscellaneous Operations issues

08.1 (Closed) Violation 50-298/96031-01: Failure to provide procedures for expected

abnormal conditions. The control room had mitigated a slush buildup in the circulating

water bay. No guidance had been provided by procedures, although this condition had

occurred in the past. The licensee found that several abnormal or unusual conditions not

always generally known by plant personnel would be expected during the life of the plant.

These conditions had not been addressed in plant references or operations procedures.

To correct this situation, the licensee initiated a collection of unusual or not generally

known information (such as unusual relay arrangements and ventilation system effects)

in a database. This database is available for review throughout the site. A person

assigned by operations has reviewed submittals from all site staff for inclusion and it has

been used repeatedly in the continuing operations training cycles. During instances of

database review, operators identified some examples of information which should be

more properly included in system operating procedures, and they modified procedures to

include the information. Inspectors observed contents of the database, found it to have

collected obscure but potentially usefulinformation, and noted that the purpose of the

corrective action was served by the continuing review and identification of information

which was then incorporated into operations procedures.

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11. Maintenance

M1 Conduct of Maintenance

M1.1 General Comments

a. Insoection Scooe (71707)

The inspectors observed and reviewed the following work activities and associated work

orders, tagout orders, and other related documents:

6.1(2)RPS.307 Reactor Vessel Low High Water Level Calibration and Functional

15. PAS.301 Post-Accident Sampling Area Radiation Monitor Functional Test

6.RHR.306 Reactor High Pressure Calibration and Functional

6.1 ADS.301 ADS Reactor Pressure Permissive Calibration and Functional and

Logic Tests 6.1SW.101 Service Water Surveillance Operation

MWR 98-1097 Replacement of Flow Switch PC-FS-11 on Division ll H2/02

analyzer

PM 01113 Oil Sample for Service Water Pump A

PM 01115 Oil Sample for Service Water Pump C

c. C_onclusions

inspectors observed procedural adherence, radiation protection, and ALARA practices

and found them generally good. Acceptance criteria were properly referenced and

followed. Cases in which data were not within acceptance criteria, or anomalies were

found, were dispositioned with problem identification reports and/or documentation on a

discrepancy sheet. The appropriate standards for initiation of problem identification

reports appeared to have been met when problems were encountered.

M1.2 Coordination of Midevele Outaoe and Resoonse Durina Snowstorm

a. insoection Scoce (71707)

During the midcycle outage, inspectors observed maintenance coordination of outage

activities, including response to an occurrence of heavy snowfall and wind which closed

routine access to the site for over 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> and a complex modification of Z-sump, which

affects the standby gas treatment system.

b. Observations and Findinas

Maintenance, outage, and construction departments coordinated the midcycle outage.

Scheduling provided plant activity information and coordination. Outage management

responded well to challenges and changes to expected conditions.

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Throughout the outage, maintenance and plant management intervened with

i

engineering to implement required modifications to the Z-sump, a sump located under

'

the elevated release point which can cause standby gas system inoperablity if it is not

properly drained. Engineering was challenged to implement the modification in a timely l

manner due to changes in scope and requirements. Maintenance management provided

direct, proactive project leadership of the modification installation and identified several l

potential safety and scheduled issues and drove them to resolution. Generally strong l

problem resolution standards were demonstrated. Construction and outage

management were also involved in assisting with implementation of the modification.

l

On March 8, the licensee experienced heavy snowfall and high winds. The severity of

the weather conditions are described earlier in Section O1.3. The maintenance, outage,

scheduling and construction departments demonstrated strong proactive involvement

and coordination of all departments on tite to ensure adequate staff.

Plant, outage, maintenance, and construction management demonstrated strong,

proactive involvement in assuring personnel safety and logistic support for staff on site,

shifts were property assigned, priorities for work activities were appropriate, and offsite '

state and county officials were contacted.

c. Conclusions

Maintenance response to a snowstorm which blocked routine access to the site for over

24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> was outstanding. Two shifts of emergency response organization were formed

onsite as well as two shifts each of operations, security, and maintenance staff to

address plant operations, outage work, and effects of the snowstorm. For the majority of

activities, maintenance and the outage organization took on leadership roles and

properly prioritized and coordinated site activities.

M2 Maintenance and Material Condition of Facilities and Equipment

M2.1 Plant Material Condition

a. Insoection Scoce (62707)

Inspectors assessed plant material condition.

b. Observations and Findinas

During plan of the day meetings, plant management identified specific areas, of the plant

where housekeeping did not meet management expectations and focused staff attention

l

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on continued diligence on improving housekeeping in various areas of the plant.

Inspectors had observed these areas during routine plant tours and found housekeeping

to be only adequate and therefore the plant manager issues were valid. None of these

areas included safety systems or components.

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l A 96-inch butterfly valve in the circu!ating water system failed in the closed position vehen

a set-screw failed, allowing the shaft key to translate and the valve shaft to become

l disengaged from the motor operator.

A station operator identified that, when Service Water Pump C was started, the pump ,

slightly moved on its foundation. Maintenance technicians performed troubleshooting i

actions and determined that three of the eight foundation bolts were loose. Operations

requested that the other service water pump foundation bolts be verified tight, and no

other bolts were found loose.

The licensee implemented a method of controlling shutdown cooling by using the

residual heat removal heat exchanger outlet valve (RHR-MO-128). This is a

nonthrottleable valve controlled by a keylock switch on the control room panel. The

valve is maintained in position by opening its power supply breaker at the motor control

center. The position is changed by closing the breaker for a specified number of

seconds, calibrated to percent of full stroke. Original plant design had the service water )

heat exchanger outlet valves (SW-MO-89A and -B) used for controlling shutdown 1

cooling, but the valves did not work due to river water corrosion effects, and the heat

exchanger bypass valves do not have adequate capacity.

c. Conclusions

in general, plant material condition was good.

M2.2 Circulating Water Valve Failure

a. Inspection Scooe (62707)

I

inspectors reviewed maintenance actions in response to a valve failure. I

b. Observations and Findinos

On March 21,1998, a 96-inch circulating water valve failed. Maintenance responded  ;

promptly and identified that the valve stem had become disengaged from the motor

operator due to a set screw failure and the associated key backing out of the shaft.

Maintenance repositioned the valve and reassembled the spline on the shaft. They

added two set screws on the valve shaft to more securely attach the spline to the va!ve

l stem. Maintenance determined that the failure had occurred due to a combination of

l vibration of the open butterfly disk in a flow stream and installation practice by

l maintenance. The other similar valves on the circulating water supply were inspected

I and found in good condition.

l On March 23, after following up the licensee's activities, the inspector identified two l

concerns: that the set screws installed on the valve spline and shaft appeared to fit the

licensee's definition of a modification, but did not appear to have been evaluated and

documented as such; and the cause of the problem, vibration of the disk in the flow

1

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stream coupled with the improper installation of the key and setscrew, may extend to i

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safety-related valves of similar design, such as the butterfly valves in the service water,

l reactor equipment cooling, and residual heat removal systems. The licensee had not

inspected the safety-related valves of similar design and installation characteristics for a

! similar vulnerability. The licensee promptly inspected several butterfly valves in safety- 1

related systems which may be vulnerable to this failure and documented the

unauthorized modification on a problem identification report. The extent of condition

evaluation and inspections found no similar vulnerability on similar design safety related

valves. Engineering management noted that resolution of the condition report had not

yet concluded. Therefore, appropriate bounding of the extent of condition was not

expected before conclusion of the 30 days.

c. Conclusions

Maintenance responded promptly and provided a repair to a failed circulating water

valve. However, the valve was repaired with a modification without appropriate

administrative controls. The licensee did not verify safety-related valves with similar

designs until after inspector involvement.

M8 Miscellaneous Maintenance issues (92902)

M8.1 (Closed) Licensee Event Reoort 50-298/96-013-00 and -01: Inoperable high pressure ,

coolant injection system due to control oil leak on turbine stop valve actuator. Upon l

investigation, the licensee determined that the leakage originated from the bolted flange. l

The licensee concluded that the apparent cause was overtorquing in 1991. The

overtorquing resulted from a lack of adequate guidance in the procedure used to l

reassemble the hydraulic actuator. The procedure directed the bolts be tightened as

opposed to being torqued to the vendor specified value.

The licensee implemented the following corrective actions: (1) reviewed maintenance

procedures and identified 114 procedures which used the word tighten; (2) based on i

reviews of the procedures, vendor manuals, and using experienced maintenance

personnel, the list was narrowed to seven procedures that needed to be revised; l

(3) placed the seven procedures on administrative hold until revised to include a torque

value; and (4) visually examined the accessible components of the seven procedures for i

signs of overtorquing or looseness.

The inspectors reviewed these corrective actions and determined that no process had

been put in place to ensure revised or new procedures correctly used the word tighten.

Also, the criteria used to determine if the word tighten was appropriate was not

documented. Through interviews with the maintenance personnel who performed the

review, the inspectors determined that, if the vendor manual did not call out a specific ,

l

( torque valve, the word tighten was considered appropriate. The inspectors performed a

word search and identified 12 additional maintenance procedures beyond the 114

identified by the licensee that used the word tighten. The inspectors reviewed two of

f these procedures and identified that Procedure 7.2.47, "MSIV Air Manifold Removal,

l

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Overhaul, Testing, and installation, " Revision 8, used the word tighten, but the vendor

manual recommended a torque valve of 15 ft/lbs.

The licensee did not follow up on verification that the inaccessible components affected

by the seven procedures were visually examined, nor that a long-term action was put in

place to replace the fasteners requiring controlled torque values.

In summary, although the !icensee performed corrective actions, only maintenance

procedures were reviewed and inspectors found 12 additional affected procedures.

Administrative controls had not been implemented to preclude future inappropriate

guidance for tightening fasteners. Permanent corrective action or controlled fastener

installation in the plant were not scheduled or performed.

The failure to implement procedural guidance with appropriate torque values to prevent

overtorquing and causing the high pressure coolant injection system to become

inoperable is a violation of 10 CFR Part 50, Appendix B, Criterion V, which requires that

activities affecting quality be prescribed by procedures and instructions appropriate to the

circumstances (50-298/98002-02). This licensee-identified violation is being cited,

because the inspectors identified that the licensee's corrective actions were not

adequate.

Conclusion

The licensee failed to properly implement corrective actions for inadequate torquing i

instructions which had caused safety system inoperability. Administrative controls were

not implemented to ensure the word tight or tighten would be used appropriately in new

or revised procedures, the licensee failed to identify all maintenance procedures affected

by the concern, and no permanent corrective action for uncontrolled fastener installations

were addressed.

M8.2 (Ocen) Violation 50-298/97006-01: Failure to follow Technical Specifications and

inadequate procedure for re-inerting. This violation consisted of two examples of

inadequate procedures. In the first example, no procedure allowed the use of installed

24-inch valves for inerting. The second example involved Procedure 2.1.1, "Startup

Procedure," and allowed the operators to place the mode switch in the startup/ hot-

standby position prior to performing the daily jet pump operability check contrary to the

Technical Specifications. This review only addressed the second example associated

with Procedure 2.1.1.

One of the corrective actions associated with the second example was performance of a

review of the Technical Specifications to identify all operability verifications required prior

to a mode change consistent with Technical Specifications. This action was to be

completed by September 2,1997. Procedure 2.1.1.2, " Technical Specification Pre-

Startup Checks," was to be revised to incorporate all of the operability verifications

identified by the Technical Specification review by October 15,1997. Condition

Report 97-1075 documented and tracked the corrective actions for this violation.

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On March 11,1998, the licensee identified that Procedure 2.1.1.2 required the average

power range monitors to be tested monthly, although Technical Specifications required a

weekly test. The licensee initiated Condition Report 98-0214. On April 6,1998, the I

'

licensee issued Problem identification Report 2-27100 to document inadequate

corrective actions associated with Condition Report 97-1075. The problem identification

report was closed as a trend item with no actions required. In the evaluation section of

Condition Report 98-0214, a discussion on the failure of Condition Report 97-1075 was

given, but no corrective actions were listed to address why Condition Report 97-1075 l

I

missed the average power range monitors surveillance requirements or to address the

potential extent of condition.

The failure to identify and correct procedures to test the average power range monitors

prior to a mode change as stated in the licensee's response to the Notice of Violation for i

Violation 238/97006-01 is a violation of 10 CFR Part 50, Appendix B, Criterion XVI, which

requires for significant conditions adverse to quality that actions be taken to prevent

recurrence (50-298/98002-03).

This item remains open pending verification of actions for the inadequate procedure for

re-inerting primary containment with the 24-inch valves.

Conclusion

Corrective actions for a violation for the failure to require verification of Technical

Specification operability were not comprehensive. The licensee did not identify all

operability verification requirements during the corrective action process.

M8.3 (Closed) Licensee Event Reoort 50-298/98-C04: Average power range monitors were

not tested as a result of failure to implement a Technical Specification amendment. This

issue is related to the concern described above. On March 11,1998, a problem

identification report (Condition Report 98-0214) was written to determine if the applicable

surveillance requirements were being met for average power range monitors prior to

placing the mode switch in run. The investigation determined that during the December

1995 startup from Refueling Outage 16 and the May 1997 startup from Refueling Outage

17 the mode switch was placed in the run position prior to testing the average power

range monitors within the required one week.

The corrective action section of the licensee event report stated that as immediate

corrective action the procedure was placed on administrative hold pending revision to be

completed by June 2. The discovery date was March 11, but the procedure was not

placed on administrative hold until April 9. The inspectors confirmed that the procedure

was not used from March 11 to April 9. The inspectors questioned the adequacy of the

corrective actions documented in the licensee event report since it indicated that only the

specific problem was fixed, and no actions were identified to prevent a similar problem

from recurring.

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The inspectors reviewed the licensee's Condition Report 98-0214 to determine if more

corrective actions were planned. ' It documented several actions that, when completed,

!- would prevent the problem from recurring. For example, operations would be required to -

I perform a comprehensive review of procedures to identify all operability verifications

required prior to a mode change, the work control center would be required to review

plant records associated with Technical Specification surveillance required for plant l

startup to verify no other requirements were missed, and operations management would

be required to conduct a lessons-learned briefing for each shift. Corrective actions are

scheduled in the licensee action tracking list, with appropriate administrative controls.

These actions and others documented a strong seif-critical review of the condition which

was not documented in the licensee event report. These actions have been completed

l or are in the licensee's action item tracking system.

The failure to perform surveillance testing on the average power range monitors prior to

placing the mode switch to run in December 1995 and May 1997 is a violation. This

nonrepetitive, licensee-identified and corrected violation is being treated as a noncited

violation, consistent with Section Vll.B.1 of the NRC Enforcement Policy

(50-298/98002-04).

M8.4 (Closed) Violation 50-298/97011-02: Failure to follow procedure and inadequate

procedure. Inspectors identified that the standby gas surveillance testing procedures

allowed nonconservative testing to determine if the system was operable. Other j

inadequacies were found. The licensee corrected these specific findings, but further

work to identify the extent of condition was not performed. Subsequently, an NRC

inspection found further problems, which were cited separately. Also in this violation,

inspectors identified that the licensee failed to follow procedure requirements to promptly

evaluate problem identification reports by condition review groups in that 23 reports were

not evaluated within about a month. These reports were part of a specific initiative to

address problem identification, and were collected as a group over time. Since this

occurrence, the licensee has re-emphasized the need to promptly evaluate reports.

Additional examples have not been noted.

111. Engineering

E2 Engineering Support of Facilities and Equipment

. E2.1 Nonconservative Bias in the Fuel Ranae Level Indicators

a. lasoection Scooe (37551)

Inspectors evaluated the parameters used by operators during ernergency operating

procedures to determine vessel level in the fuel range and make decisions on when

reactor vessel depressurization should be performed.

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b. Observations and Findinas

On March 31,1998, the inspector questioned if the fuel range level parameters

accurately reflected the vessel level with respect to the top of active fuel. Original

procedures assumed a fuel height of 144 inches and the length of active fuel had been

changed from the original 144 inches to 150 inches. The inspector questioned if the

reactor vessel level parameters had been altered to reflect the changed height of the top

of active fuel. Technical Specification Figure 2.2.1 identified a height of active fuel as

144.00 inches and the core spray permissive setpoint as -39 inches as relative to top of

active fuel. Also, Level Indicator Ll-91 measured the reactor vessel level above active

fuel and has not been altered since installation. The inspector noted that, although this

would provide 6 inches less submergence over active fuel, the licensee had verified that

the design basis accident analysis had evaluated core uncovery at the -29-inch level

consistent with the lower edge of the jet pump nozzles regardless of fuel height in i

General Electric accident analysis.

On April 2, the inspector questioned if the correct reference point for top of active fuel in

the plant was zero on Level Indications Ll-91 A, -B, and -C. The application of these

reactor vessel water level parameters are provided in Emergency Operating

Procedure 2A RC/L-14. Operators must wait to depressurize the vessel until reactor

water level drops to the top of active fuel; if reactor vessel injection is available,

emergency pressurization occurs. If reactor vesselinjection is not available, steam

cooling is required and the reactor vessel remains pressurized while water level is

allowed to drop to -40 inches (0 inches is top of active fuel). This value of -40 inches

appeared to be dependent on the General Electric-provided fraction of 150-inch fuel

which must remain covered by liquid in order to assure peak centerline temperature

remains below 1800 F.

Operations review of Emergency Operating Procedure Calculation NEDC 89-1843,

Revision 1, stated that 150-inch fuel had been considered during the calculation. This

calculation stated that it determined various reactor vessel pressure level variables to be

used in emergency operation procedures, including minimum core flooding interval, the

maximum core uncovery time limit, the minimum steam cooling reactor vessel pressure

level water level, and the minimum no injection reactor vessel pressure water level. This

calculation noted that the water level of the reactor vessel pressure level at the top of

active fuel was that listed in Technical Specification Figure 2.1.1, and that water level,

considered zero on Level Indicator LI-91, is based on a 144-inch fuel length. Current fuel

length is 150 inches and this length is reflected as the minimum length of active fuel in

this calculation. The linear heat generation rate of 14.4 kw/ft is referenced by Calculation

DC 90-152, CNS Cycle 14, Reload 13, Design and Safety Analysis.

The generic parameters associated with BWR Owner's Group, emergency planning

guides, were listed in the calculation. Specifically, the minimum active fuel length fraction

which must be covered to maintain peak center line temperature less than 1800 F

without injection in percentage was 70.83 percent. The calculation to determine the

l length of fuel which may be uncovered relative to water level from the top of active fuel

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concluded that, given a ratio of this percentage relative to 150-inch fuel, a water level of

-43.8 inches would be the lowest level i.n which peak centerline temperature would

remain less than 1800 F. Emergency Operating Procedure 2A allowed steam cooling in

the core in absence of injection until water level drops to -40 inches.

On April 3, design engineering concluded that the several inches of inactive uranium

reflector added to the top of the fuelin the new design could be credited as margin.

Based on this, the licensee concluded the issue was not significant.

In response to these issues, operations generated a problem resolution matrix

documenting several outstanding questions and contingencies to be taken upon answers

received for each of those questions. These questions included the inspectors'

'

questions, plus several others. Further, the shift technical engineers identified the need

to review the basis for other reactor vessel water level parameters and other water level

dependent considerations. Examples would be low and high water level trips and

minimum core reflooding interval.

On April 7, engineering stated that when zero was indicated on Level Indicators Ll-91 A,

-B, and -C, the actual water level in the reactor was 6 inches lower than the top of active

fuel as defined in emergency operating procedure calculations. The licensee stated that,

because the 150-inch fuel had 6 inches of reflector on both top and bottom of fuel, this

distance was not significant. The inspector raised the issue that, for the case of the

1800*F peak centerline temperature limit, the required fuel coverage was 70.89 percent.

A 6-inch bias applied in the negative direction would result in fuel becoming uncovered.

The licensee stated that the issue of exceeding 1800 F peak centerline temperatures

involves an event beyond design basis.

The licensee did not address: (1) the nonconservative aspect of the plus or minus l

calibration tolerances on Level Indicator LI-91 manual action points, nor was I

nonconservatism associated with instrument error or calibration instrument error l

addressed; (2) the calculation of core uncovery time which had changed due to the i

relative change of top of active fuel to wide range level zero; and (3) the calculations

associated with volume required at specific vessel levels for boron dilution during an

anticipated transient without scram event and subsequent boration or emergency l

boration, as well as commitments to the NRC regarding implementation of BWR Owner's '

Group Emergency Operating Procedure Guidelines associated with 1800*F fuel

l temperature limits.

l Other areas the licensee did not address included parameters used in generic vendor

calculations. General Electric Service information Letter 529, Supplement 1, dated

l

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! March 14,1997, described the need for fuel design specific input parameters to be used

i for Appendix C to Emergency Procedure Guidelines, Revision 4, for General Electric 8x8

and 9x9 fuel designs. The service information letter describes steam cooling-related 1

parameters to emergency operating procedure calculations including: (1) the minimum i

length for active fuel which must be covered to maintain peak critical temperature less l

than 1800*F without injection into the reactor pressure vessel, (2) minimum bundle j

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steam flow required to maintain peak critical centerline temperature less than 1500'F for

an uncovered core, (3) maximum time before peak centerline temperature exceeds

l 1500*F for an uncovered core referenced to POHGH equal 13.4 kw/ft, (4) the cold

l shutdown boron concentration requirements, and (5) the hot shutdown boron

concentration requirement. The emergency operating procedure parameters ultimately

effected by these concems were listed as the boron injection initiation temperature, cold

shutdown boron wait, peak capacity level limit, heet capacity temperature limit, hot

shutdown boron weight, minimum alternate reactor pressure vessel flooding pressure, l

minimum core flooding interval, maximum core uncovery time limit, minimum number of

safety relief valves required for emergency depressurization, minimum reactor pressure

vessel flooding pressure, minimum steam cooling reactor pressure vessel water level, j

minimum zero reactor pressure vessel water level, peak centerline temperature,

pressure-suppression pressure, and peak linear heat generation rate. The licensee had

addressed only the top of active fuel parameter.

The licensee issued Problem Identification Report 2-27287 to document that an apparent

discrepancy existed with the 0-inch level assumed as the top of active fuel in the vessel.

The licensee noted that 150-inch fuel potentially extended to above the zero level.

The licensee evaluated the safety significance of the 6-inch nonconservative bias.

Vendor testing had found that fuel peak centerline temperatures of 1800"F would not be

reached until vessel water level dropped below -70 inches (below top of active fuel). The

licensee performed an evaluation which considered various instrument errors, including

errors expected in a harsh equipment qualification environment. They found that the

1800*F limit would not be reached even with the 6-inch nonconservativa instrument bias.

The failure to incorporate the correct fuel length design requirements in plant emergency

operating procedures is an example of a violation of 10 CFR Part 50, Appendix B,

Criterion ill, which requires, in part, that the design basis correctly translated into

procedures (50-298/98002-02).

Additional questions which remain to be resolved include: (1) Technical Specification

Interpretation 96-003 which documented that the fuel length indicated in Technical

Specification was 144 inches, although the Updated Safety Analysis Report stated that

active fuellength was 150 inches. The resciution associated with the interpretation

concluded that the conversion to improved Technical Specifications would remove the

associated figure which showed the top of active fuel relative to the 144-inch active fuel ;

length. The recalculation of setpoints for improved Technical Specification would be l

done in accordance with General Electric setpoint methodology and instrument zero l

would be redefined as a fixed point above the fuel which will be defined for the purposes I

of level monitoring as top of active fuel. The interpretation stated that the reference in j

the Technical Specification bases was not a basis for the limiting safety system setting I

and that safety margin for transient and accident analysis was maintained through ,

administrative controls such as higher trip setpoints and emergency operating j

procedures. This Technical Specification request dated June 8,1996, stated that the '

safety limit was maintained regarding General Electric setpoint methodology. Inspectors

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noted the bases for the top of active fuel measurement in the emergency operating

procedures appears to be based on Level Indicators LI-91 with the top of active fuel

equal to zero. Also, the licensee's emergency operating procedure calculation process

failed to properly consider the change in fuel length.

Inspectors reviewed Surveillance Procedure 6.RHR.305, "RHR Reactor Vessel Shroud

Level Indication Calibration," Revision 1, which required the zero point for Level

Indicator Li-91 A to be set at 381 inches. Technical Specification noted that the zero level

for this indicator was 351 inches. This indicates approximately 30 inches of water over

the top of active fuel when Level Indicator Ll-91 A reads zero. This issue will also be

followed in the closure of the violation.

c. Conclusions

The length of fuel had been increased from 144 to 150 inches. The licensee failed to

change the reference point for the top of active fuel on fuel range level indicators and

improperly performed changes to emergency operating procedure parameters. This

caused a nonconservative bias in the fuel range indication of 6 inches. The licensee

evaluation concluded that, although this bias was nonconservative, it did not exceed the

existing design margin.

E2.2 Imorocer Requirement to Throttle Core Sorav Flow Durina Loss of Coolant Conditions

a. Insoection Scoce (37551)

Inspectors followed the licensee's actions to correct procedures which had required

improper throttling of core spray flow under accident conditions.

b. Observations and Findinos

A licensee engineer identified that an emergency procedure specified that core spray

flow should be throttled back to 4750 gpm per pump (total of 9500 gpm). The Updated

Safety Analysis Report required total core spray flow of 12,000 gpm (two pumps) under

design bases conditions. The licensee issued Prcunm Identification Report 2-26684

documented by Significant Condition Adverse to Quality 98-0197 to address this issue.

The licensee identified that flow had been throttled to adcress diesel fuel consumption

concerns and keep the fuel consumption rate below that specified by a load study. The

safety analysis requked that, for the first 400 minutes of a design basis accident, full core

spray flow of at least 12,200 gpm be prcvided for core reflood. The licensee corrected

the procedure to require operators to ensure full core spray flow to the core for the first

10 minutes of an event and to stipulate that flow be throttled back after that only if core

reflood had successfully occurred.

The licensee reported this issue in accordance with 10 CFR 50.72, as a potential

unanalyzed condition. This issue will be followed in the closure of the licensee event

report.

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l c. Conclusion

Procedures for use during a loss of coolant accident and loss of offsite power directed

that core spray be throttled to 4750 gpm per pump, although 6100 gallons were required

for core coverage by the Updated Safety Analysis Report accident analysis.

E2.3 Inaccuracies in Emeraency Procedure for Diesel Generator Loading

a. Insoection Sepoe (37551)

Inspectors reviewed Procedure 5.2.5, " Lose of All Site AC Power - Use of Emergency AC

Power," Revision 31, and held discussions v/ith operations and engineering personnel.

b. Observations and Findings

The inspectors reviewed the instructions in Procedure 5.2.5, regarding electrical load

controls. Engineering had provided load profile line items so the diesel generator loads

could be outside design calculations. One instruction in the procedures indicated that

diesel generators could be run at 4,000 kw (nameplate rating) for up to 22 hours2.546296e-4 days <br />0.00611 hours <br />3.637566e-5 weeks <br />8.371e-6 months <br /> and up

to 4400 kw for up to 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> every 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> without exceeding design requirements.

However, an attachment indicated that diesel generators could be run only within

particular load limits it listed all motor control centers with letter designators and, further,

referenced a table to indicate how long each particular load was allowed to be run and

for what times during the accident. This attachment referred to the loads being used as

" Load Study for Diesel Generators." Further evaluation found that this load study

represented the design basis condition where only one diesel generator was running and

loads were maintained in a manner to ensure Technical Specifications 7-day fuel

inventory requirements and diesel loading limits were followed.

1

The inspectors considered that under the design basis event for which the design 7-day  !

Technical Specification fuel inventory was based (loss-of-coolant accident with loss of

'

one diesel), operators were not likely to follow Procedure 5.2.5 until about 20 minutes

into the event. Further, operations considered these design basis diesel loading limits to

be guidelines, as stated in the procedure, rather than a limit or procedure which must be

followed. On the other hand, engineering stated that the basis for the validity of the

7-day fuel inventory requirement was the implementation of the diesel loading profile as

stated in Procedure 5.2.5.

The inspectors questioned if engineering had provided adequate instructions to

operators to ensure diesel loading would remain within fuel consumption assumptions in

design basis conditions. Operations acknowledged that, in an event situation, following

the table and load study may be cumbersome. The inspector considered the

26 specified chronolegy requirements for each load, and the use of a single dieselload

i

profile for a particular accident, as a basis for allload profile requirements and accidents j

l to be cumbersome and potentially confusing. Operations agreed that a more favorable

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format would be helpful.-These :: uce '.;"! be revice :d !a fe!!cefup c/mssassue This

issue is unresolved (50-298/98002-05).

c. Conclusions

Engineering failed to implement clear instructions for controlling the electrical load profile

in emergency operating procedures. This profile is the basis for the Technical

Specification 7-day diesel fuelinventory requirement. Operations had not been

instructed that this profile must be used if the design basis loss-of-coolant accident

occurred. I

E2.4 Paintina Without Procer Evaluation of Effect on Standbv Gas Treatment System

a. Insoection Scoce (37551)

Inspectors questioned the effects of paint fumes on the standby gas treatment system.

Discussions were held with operations and engineering personnel.

b. Observations cnd Findinos

On February 11,1998, the inspector identified that painting activities in the reactor i

building caused significant fumes. Examination of the paint can labelidentified several

ether and acrylate-based compounds which would indicate volatile components.

Discussions with the systems engineer indicated that water-based painting was allowed

for about 10 gallons of paint in a drying status. The inspector questioned if the standby ,

gas treatment charcoal was vulnerable to effects from the volatile components of the l

water-based paint in use.

On March 9, the licensee stated that, since the majority of the organics were light-weight,

these organics would enter and then clear the standby gas treatment system in a

relatively rapid fashion, whereas the smaller fraction of large organics would have a

longer-term effect. Therefore, engineering determined that the total effect was not

significant.

On March 18, in response to inspection questions, the licensee identified that the fraction

of larger organics and the affect on standby gas treatment system operability may have

been greater than previously anticipated. When informed of this condition, the inspector

asked why a problem identification report had not been generated several days prior

when the condition was initially discovered and why the control room had not been

informed that the original operability evaluation was no longer valid.

To address operability concerns, engineering evaluated ventilation flow paths which had

occurred during the painting evolution and found that predominantly, normal ventilation

had removed organic fumes. Engineering determined that a small fraction of organics

may have been entrained in the standby gas treatment system charcoal. Engineering

issued Problem Identification Report 2-19345 after discussing these concerns with the

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inspectors. To date, the licensee had not documented a basis for standby gas treatment

operability had a design basis event occurred during painting activities in the reactor

building.

l

On February 11, the painting was reduced to limits bounded by oil painting. Later

painting in the reactor building was suspended pending results of the charcoal sample

review.

The failure to incorporate controls for paint with a significant fraction of organics,

potentially affecting the standby gas treatment system, is an example of a violation of

10 CFR Part 50, Appendix B, Criterion V, which requires in part that activities affecting

quality be prescribed by procedures appropriate to the circumstances

(50-298/98002-02).

c. Conclusions

Controls for painting inside the reactor building were inadequate. The licensee did not

recognize that some paints contained an unacceptably high percentage of volatile

organics. The initial evaluation and restrictions on the painting, as well as the evaluation

of the effect of this painting on standby gas treatment, did not accurately address the

technical issue or the iodine release profile, and the control room was not informed of

later developments.

E2.5 Z-Sumo Modification Concerns

a. Insoection Scoce (71707)

Inspectors reviewed portions of the Z-sump modification procedures changes and

problem identification reports, attended station operations review committee meetings

associated with these procedure changes, and held discussions with operations, t

engineering, and management.

b. Observations and Findinas

The licensee had identified that the Z-sump and equipment required modification

because it did not meet seismic design requirements. For the modification to correct the

system design weakness, several mechanical, electrical, and instrument and control

installations were performed to support redundant sump pumps and level indications.

Several operating procedures were changed. Under freezing temperatures, absence of

heat trace for over 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> would make the standby gas treatment system inoperable.

The heat trace is normally powered by a nonessential bus. After the procedure changes

were approved, the inspectors noted that no alarm response procedures, abnormal

procedures, night orders, or system operating procedures had directed operators to

respond to a loss of the nonessential power to the essential heat trace providing an

essential power source.

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Operations acknowledged this lack of guidance and initiated changes to night orders, l

abnormal procedures, system operating procedures, and annunciator response

procedures. The inspector observed that, for these examples, engineering had failed to

identify these procedures affected by the modification.

Discussions with operations management indicated that they recognized the concern )

that operations demand more effective action from engineering regarding installation

modifications. No problein identification report was initiated to address engineering

failure to correct all procedures affected by the heat trace requirement. ,

The failure of engineering to identify procedures affected by the Z-sump modification is

contrary to Procedure 3.4.3, Revision 14, which requires that affected procedures be

identified by the modification package. This concern, along with findings by an

engineering inspection team reviewing this modification, and the licensee's corrective

actions for this concern, will be followed by an unresolved item (50-298/98002-06).

The inspector also identified that, although soil compaction testing was scheduled for

areas of excavation for the conduit, in order to confirm that rain and water table moisture

had not degraded the soil compaction over time, no testing was planned to verify if the

soil near the Z-sump, under the elevated release point, had remained compacted. The

area under the elevated release point is flooded for days at a time in high river level

conditions. Engineering promptly ordered this testing, which concluded satisfactory

compaction.

c. Conclusions

For a modification to the Z-sump, engineering did not identify all affected operating

procedures. Inspectors found that, if the nonessential power to the essential heat trace

was lost due to electrical component failure, no requirements or actions were provided to

operators in abnormal or alarm response procedures to respond to this loss.

E2.6 Portion of Service Water Pioino for Residual Heat Removal System Not Analyzed For

Air-Filled Condition

a. Insoection Scoce (37551)

,

inspectors evaluated the engineering response to portions of the essential service water j

system and residual heat exchanger being found filled with air instead of water. )

.

b. Observations and Findinos

The residual heat removal service water system is provided with service water flow from

service water pumps. Service water booster pumps boost flow through the residual heat I

removal heat exchanger to the outfall. Discharge check valves are installed at the

discharge of each booster pump. On December 18,1997, the licensee identified that the i

piping downstream of the service water booster pump discharge check valve

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(SW-CV-19CV) was not filled with water, i.e., air was found when drains and vents were

opened to determine the condition of the piping. The licensee postulated that the check

valve had become stuck and did not allow flow through the piping via the service water

booster pumps. Disassembly of the check valve did not identify the reason for the check

valve to have stuck shut, nor did it confirm that the check valve was stuck shut. The

licensee initiated twice-weekly thermal acoustical monitoring of the piping to determine if

the condition repeated. The licensee concluded that the service water piping and the

heat exchanger were operable while filled with air.

Based on the inspectors' questioning of the licensee's conclusion, the licensee

determined that no analysis was in place to substantiate that the piping and system were l

operable when filled with air downstream of the check valve. On March 4, the licensee I

initiated engineering information document EFOM 98-005 to document the need to verify l

operability of the downstream piping by twice weekly acoustical monitoring. On l

March 12, the inspectors identified that engineering had not updated the operability

evaluation and that the control room was unaware that monitoring was required to assure

operability.

On April 6, the inspector questioned why the piping being in an unanalyzed condition

was not reportable. The licensee concluded that a contractor evaluation would show the

piping had been operable. This issue will be followed by an inspector followup item to

review the licensee's conclusion of operability of the system in the air-filled condition (50-

298/98002-07).

c. Conclusions

A portion of the service water piping and the residual heat removal heat exchanger was

found filled with air rather than water during power operation. The licensee concluded

the piping was operable. Operability of the system piping was not demonstrated by

analysis or calculation. Compensatory actions to demonstrate operability were not

provided to the control room in a timely fashion and the operability evaluation was not

corrected to reflect the operability assessmerit of the as-found condition of the piping

until 3 weeks later.

E2.7 Potential Effect of Hich Torus Level Allowed by Emeraency Operatina Procedures Not

Addressed

a. Insoection Scoce (37551)

inspectors reviewed the basis for torus level with respect to the design limits of critical

components. Inspectors reviewed procedures, corrective action documentation, and

design information; observed simulator scenarios; and held discussions with engineers,

operators, and rnanagers.

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b. Observations and Findinas

l On March 30,1988, the inspector questioned procedural controls for the torus level with

l respect to the design requirements for critical components. Engineering had identified

that the torus strainer penetrations had nonconservatisms in their calculations and that

the hydrodynamic loading was analyzed only when torus level was 2 inches or less. The

j inspector noted that emergency operating procedures allowed a torus level to increase of

37 inches before an emergency depressurization was required. This indicated that the

plant could be vulnerable when the torus level was high.

On March 31, the inspector held discussions with operations, emergency operating

procedures staf' and structural engineering staff. Emergency operations procedure staff

l stated that the 37-inch limit was based on the limit of hydrodynamic loading on the

l safety-relief tail pipe T-quenchers for a manual blowdown via the safety relief valves.

l

'

The engineering staff was unaware that the emergency operating procedures allowed

increase of the torus level to 37 inches, before plant depressurization was required.

On February 7, the licensee stated that the hydrodynamic loading on the strainer

penetrations had been addressed by General Electric and documented in proprietary

information regarding the details of the limiting components of the torus structure.

According to the licensee, the BWR Owner's Group committee stated that large loss-of-

coolant-accident loads would be acceptable for high torus water levels not exceeding the

bottom ring header in Mark I containments. Therefore, the decision that loading on the

T-quenchers was more limiting at high torus levels than loading on the strainer

penetration was based on proprietary information held by the vendor. The licensee did

not provide documentation of this conclusion.

I

No rigorous, dynamic, or hydrodynamic load calculations beyond the Mark I program

l assessments had been performed by the licensee. The licensee stated that probabilistic

risk analysis had typically not considered hydrodynamic loading. The licensee's

evaluation to resolve the issue addressed three scenarios associated with high torus

level: a design basis loss-of-coolant-accident, a reactor pressure vessel breach, and an

l

anticipated transient without scram greater than 6 percent power. The inspector asked if

the emergency procedure scenarios run on March 18,1998, as well as the licensee's

event in early August 1988, involving an increase in torus level above analyzed level,

were bounded by these 3 analyses. The licensee acknowledged this should be

addressed.

l A conference call on April 24 discussed these concerns among the licensee, General

Electric, and the BWR Owners Group. The participants concluded that further evaluation

was required. This resolution of the issue will be followed by an inspector followup item

I' (50-298/98002-07),

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c. Conclusions

The licensee failed to reconcile the design requirements for torus level to remain below

2 inches and the emergency operating procedures which allow a torus level up to l

37 inches.

E2.8 Inadequacies Associated with Plant Temocrarv Modifications to Feed Pumo Controller

a. Insoection Scoce (37551)

The inspectors reviewed the engineering evaluation and proposal for temporary plant

modification and the associated station operations review committee approval.

Inspectors held discussions with engineers and engineering management. l

l

b. Observations and Findinas l

On March 27,1998, the inspectors observed review and approval of a plant temporary I

modification to monitor a controller circuit on the Feedwater Pump B controller. The  !

inspectors noted that several potential vulnerabilities had been addressed and properly

evaluated with the following exceptions:

1. The heat generation due to the temporary equipment in the cable spreading room l

had not been addressed under abnormal or emergency conditions in which

ventilation would be changed.

2. Power sources had not been evaluated with respect to the effect on vital or

nonvital circuits and the resultant effect on power consumption.

3. Radio frequency interference from cellular phones was not addressed. The

temporary modification had considered the radio frequency interference from

plant security radios, and guidance had been made to make jumper connections

as short as possible to minimize the chance of interference.

In response to these concerns, the engineers identified that heat generation and power

consumption were not an issue, since this was well within design margins. Engineers

identified that the cellular phones operated at a frequency of 900 megahertz. This

corresponded to an optimum antenna length of approximately 30 cm. Since this length

was similar to the length of jumper wires, and engineers had not evaluated the use of

cellular phones near the recorders, the inspector raised a concern that no specific

instructions or bounding analysis had been done to ensure cellular phone interference

would not affect feed pump control circuitry.

The plant manager directed a review of the cellular phone radio frequency testing to

determine if routine surveillance testing using test equipment and jumpers had been

addressed. Engineering concluded that the radio frequency testing had not addressed

jumper configurations expected in routine surveillance testing and that vulnerabilities ,

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jumper configurations expected in routine surveillance testing and that vulnerabilities

existed if cellular phones were placed in contact or in near contact with unshielded

jumpers. The licensee is developing specific calculations and administrative controls for

the concern. Problem Identification Report 2-01365 addresses this issue.

c. Conclusions

1

The inspector identified failures to consider potential vulnerabilities of temporary

modification to design basis and radio frequency challenges. The plant manager

demonstrated ownership and a questioning attitude to also require engineering

evaluation of potential cellular phone radio frequency effects on jumpers used in routine

'

surveillance testing, q

l

E2.9 Enaineerina Evaluation of Water in a Diesel Fuel Od Dav Tank l

l

a. Insoection Scoce (37551) {

inspectors followed the licensee's response to finding water in the diesel fuel oil day tank.

Inspectors reviewed procedures and held discussions with operators, engineers, and '

managers.

b. Observations and Findinas

On ' March 23,1998, the licensee had identified that Diesel Fuel Oil Day Tank 2 had

collected approximately 90 ml of water. The licensee initiated Problem identification

Report 2-27175, dated March 24, to document the concern. The licensee took no action

to check the redundant fuel tank to determine if a similar condition existed until after the

inspector raised questions on March 24. Operations promptly added procedural

guidance to consider checking the alternate fuel tank for generic effects, performed a

check, and found no water in the alternate fuel oil tank. Operations issued Problem

Identification Report 2-27177 to document a need to be sensitive to the potential that a

generic concern may exist on the opposite diesel generator fuel oil day tank.

System engineering determined that the water was less than 0.5 percent of the volume

of the day tank and therefore within specifications of dissolved water and suspended

solids associated with the larger tanks and incoming fuel. Inspectors determined that l

engineering did not understand the difference between dissolved and suspended water

'

in fuel oil. They were unable to provide a basis for concluding that the fuel in the day

tank did not exceed the 0.5 percent limit. Inspectors concluded that suspended water,

rather than dissolved water, was being measured, based on use of a centrifuge testing

method. Therefore the inspector was able to conclude that a reasonable basis existed

for the operability of the fuel in both the day tank and the 2,000 gallon tank. The licensee

did not identify the source of water. i

l

When operations found the water in the fuel, the system engineer was informed in l

accordance with the procedure. Operations requested engineering to provide an  !

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operability acceptance criteria with respect to the amount of water found. The system

l engineer declined to provide an acceptance criteria stating that informing system

l engineering would provide adequate technical support to make an operability decision.

!

Since water had been found in only three cases over the past several years, the system

engineer concluded that a detrimental effect on the fuel was unlikely. The engineer was

unable to provide a basis for this conclusion,

c. Conclusions

Engineering demonstrated weak support of an issue regarding a small amount of water

found in the diesel fuel oil day tank. After discovery of water in one train of the diesel fuel

oil day tank, the licensee did not promptly check for water in the redundant train until

after inspector questioning a day later.

l E4 Engineering Staff Knowledge and Performance

E4.1 Enaineerina Evaluation of Fluctuating Safety Relief Valve Tail Pioe Temperatures

a. Insoection Scoce (37551)

l

Inspectors reviewed engineering actions and evaluations responding to a plant request

to evaluate the cause of a fluctuating safety relief valve tailpipe temperature. Inspectors

held discussions with operators, engineers, and construction personnel.

1

b. Observations and Findinas

On February 12,1998, the plant requested engineering to evaluate fluctuating safety

relief valve tailpipe temperatures. Review of this evaluation found that the engineer had

compared tailpipe temperature profiles during a downpower with a different plant having

leaking relief valves. The profiles did not match. Therefore the engineer ruled out the

potential of a leaking valve.

The inspector noted that the engineer assumed the leakage mechanism was the same

as another plant's mechanism, based on checking a single type of manifestation of l

leakage. The conclusion was based on comparison with one mechanism, without  ;

independent confirmation of other parameters, such as trending torus temperature over i

l tirne. The engineer had not interviewed containment coordinators or looked at drawings

to determine if nearby equipment airflow or other artifacts of the containment mechanical 3

or electrical arrangement could have caused this e'fect. The engineer lacked an

understanding of the adiabatic expansion mechanism which could cause leaking steam

temperatures to rise or fall.

During the midcycle outage, a ventilator was found to be blowing directly on the

temperature sensor. This condition was corrected. j

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c. Cpoclusions

Engineering provided weak support in identifying and bounding the potential causes of

fluctuating safety relief valve tailpipe temperatures.

E8 Miscellaneous Engineering issues

E8.1 (Closed) Violation 50-298/96024-07: Multiple violations concerning implementation of

design changes in plant procedures. Inspectors identified examples where emergency

operating procedures did not properly implement design assumptions. The licensee

stated that design and licensing assumptions had not been properly implemented in

procedures. Specifically, the licensee identified that, before 1991, design changes had

not required review by operations and, therefore, some of the violations had occurred.

Inspectors identified that the licensee had not taken corrective action to identify the

extent of condition of those design changes which had not been properly implemented ,

due to the vulnerability of the process before 1991. The failure to identify whether other I

design modifications had been properly reflected in procedures is an indication that the

licensee did not take actions to preclude recurrence of this significant condition adverse

to quality. This is an example of a violation of 10 CFR Part 50, Appendix B,

Criterion XVI, which requires that conditions adverse to quality be corrected and the root

cause of significant conditions adverse to quality be identified and corrected to preclude )

repetition (298/98002-03).

Conclusions

The licensee failed to evaluate the extent of the condition of a violation for improper

incorporation of design modifications in emergency procedures.

E8.2 (Closed) Licensee Event Reoort 50-298/96-003-00 and -01: The reactor isolation cooling

system was declared inoperable due to a failed monthly operability surveillance test.

Upon the pump turbine start, speed initially increased to approximately 4500 rpm (normal

speed) but subsequently decreased and stabilized at approximately 2000 rpm.

Troubleshooting determined an erroneous output from the Woodward EGM control box.

The control box was replaced and the reactor isolation cooling system was satisfactory

tested.

The control box was sent to the vendor for examination and repair. The vendor

performed terts on the control box under the observation of a licensee quality assurance

inspector. The vendor was unable to determine a cause for the failure of the control box.

but did note that a varistor for input power protection only was missing. The vendor

stated that not having the varistor installed would not have caused the control box failure,

The licensee concluded that the root cause was unknown due to a lack of available

evidence or due to evidence unintentionally destroyed.

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The inspectors concluded that the reactor core isolation system failure was an isolated

event since no similar failures have occurred before or since this failure (March 20,

j

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1996). The inspectors identified an example of a weak root cause analysis, because the

licensee failed to evaluate the missing varistor as a loose part and a potential cause of '

the failure or additional failure vulnerability until questioned by the inspectors. Through

discussions with the current system engineer, the inspectors discovered that if the

varistor became loose it could have caused the control box failure. The varistor was

never found, nor does the licensee know when or how the varistor became missing.

Through discussions between the system engineer and the inspectors, the system

engineer stated that the varistor was most likely never installed, since the varistor was

l soldered in place (would not have fallen out), the control box was refurbished (removed

i during refurbishment and not replaced), and the varistor was never found (during

I troubleshooting maintenance or by the vendor),

i

!

IV. Plant Support

j R1 Radiological Protection and Chemistry Controls

R1,1 Interdeoartmentai Coordination to Reduce Dose

l a. Insoection Scone (7175Q)

i

l

l Inspectors reviewed work control initiatives to reduce radiation dose,

b. .Qb33rvations and Findinas

inspectors found that the work control group had initiated review of work activities to

determine if dose reductions could be obtained. Activities where potential reductions

l could be identified in planning stages were discussed with technicians and health

i physics personnel. These initiatives were implemented at the job site. Work control staff

'

j included these practices in the weekly lessons learned documentation to inform other

l

site personnel and document the progress of dose reduction efforts. Savings generally

amounted to a few millirem on each job.

I

c. Conclusions  !

l l

The work control staff initiated interdepartmental dose reduction efforts, found dose

reduction opportunities, and documented results in weekly lessons leamed reports to

inform and provide expectations for site staff. I

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P Conduct of Emergency Preparedness (EP) Activities

P1.1 Resoonse to Severe Snowstorm

a. Insoection Scoce (71750)

inspectors observed EP organization response to severe snowstorm conditions.

b. Observations and Findinos

The emergency response organization responded to a severe snowstorm within minutes

after local sheriffs offices declared portions of a highway near the plant to be closed.

The licensee assessed the emergency response capability onsite and found that two

shifts of individuals were available onsite who could staff the response organization.

Most of the individuals held formal qualification in the emergency response organization

positions, the remainder were sufficiently qualified with interim qualifications.

c. Conclusions

During the snowstorm when routine access to the site was cut off for over 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />, the

emergency response organization promptly contacted state officials and assessed

personnel onsite to evaluate emergency response to fulfill requirements for two shifts of

an emergency response organization.

P7 Quality Assurance in EP Activities

P7.1 Quality Assurance in EP Activities

a. Insoection Scooe (71750)

Inspectors observed over 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> of technical support center (TSC) performance in a drill

and the subsequent debrief.

b. Observations and Findin.qS

The response during the drill appeared appropriate. Several weaknesses were

observed, none of which would preclude proper event response. During debrief after the

drill, the facilitatory provided and encouraged staff to discuss specific observations.

During the debrief, the TSC team reviewed past debrief strengths and weaknesses to

determine if improvements were being made from one drill to the next. During several

l prior debriefs observed, the emergency response staff did not refer to documentation of

! past emergency response team performance observations. This self-critical review of

lessons learned was led by the TSC director. When the inspector asked the EP staff

why this practice was not typical, they indicated facilitatory would encourage this practice

in the future.

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I c. Conclusions

After a drill response, the TSC conducted a self-critical review by comparing past drill

performance observations during the critique.

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Si Conduct of Security and Safeguards Activities

S1.1 Security Resoonse to Severe Weather Conditions

a. Insoection Scooe (71750)

The inspector observed security response to reduced staffing and severe weather

conditions during a snowstorm.

b. Observations and Findings

Security entered into the security plan procedure appropriate to reduced staffing, heavy

weather conditions, and reduced visibility due to heavy blowing snow. Staffing

evaluation found they had approximately one and one-half security shifts. This was

adequate to provide staffing over 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. During the event, guards appeared alert and

demonstrated appropriate responses and activities. Security coordinated effectively and

proactively with maintenance and operations to address conditions and put

contingencies in place to respond to potential challenges.

c. Conclusions

Security responded well to a severe snowstorm, reduced staffing, low visibility, and

isolated access conditions. Coordination with other site organizations was outstanding.

S1.2 Broken Lead Seal on Diesel Generator Fuel Tank A

a. Insoection Scooe (71750)

The inspectors observed licensee activities when a security officer reported a broken

seal on Diesel Generator Fuel Tank A. Discussions were held with security and

operations staff.

b. Observations and Findinas

On April 16,1998, a security officer reported to the control room that the seal for the

Diesel Generator Fuel Tank A inlet cover was broken. The control room supervisor

immediately had the seal replaced. The broken seal was retained for evaluation.

Chemistry performed a visual inspection, water test, and particulate test on the fuel.

Also, another sample was shipped to a laboratory to have the broader requirements of

Technical Specification testing performed.

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The security officer who found the broken seal reported to the control room that he may -

have caused the seal to break. The security officer explained that he felt the wire pull  :

away from the seal as he tugged on the lead seal. 1

I

Based on the security officer's statement and the tests conducted, on site, the control l

room considered the diesel generators operable. I

c. Conclusion

Security responded appropriately to indications of a broken seal on a diesel fuel tank

inlet. )

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X1 Exit Meeting Summary

The inspectors presented the inspection results to members of licensee management at the exit

meeting on April 20,1998. The licensee acknowledged the findings presented.

The inspectors asked the licensee whether any materials examined during the inspection should

be considered proprietary. No proprietary information was identified.

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SUPPLEMENTAL INFORMATION

PARTIAL LIST OF PERSONS CONTACTED

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Licensee

L. Dewhirst, Licensing Engineer

C. Gaines, Maintenance Manager

M. Holmes, Shift Supervisor

B. Houston, Licensing Manager

J. Lewis, Acting Reactor / Fuel Engineering Manager

J. Long, Engineering Support Manager

L. Newman, Operations Manager

O. Olson, Containment Engineering Supervisor

M. Peckham, Plant Manager

J. Pellitier, Senior Manager of Engineering

E. Plettner, Engineering Supervisor

D. VanDerkamp, Assistant Operations Manager

INSPECTION PROCEDURES USED

IP 37551: Onsite Engineering

IP 61726: Surveillance Observation

IP 62707: Maintenance Observation

IP 71707: Plant Operations

IP 71750: Plant Support Activities

IP 92901: Followup - Plant Operations

IP 92902: Followup e Maintenance

IP 92903: Followup - Engineering

ITEMS OPENED, OPENED AND CLOSED, CLOSED AND REVIEWED

Ooened

298/98002-01 IFl Reactor equipment cooling heat exchanger operability in backwash

(Section O2.1)

298/98002-02 VIO Three examples of inadequate procedures or instructions (Sections M8.1, E2.1,

and E2.4)

298/98002-03 VIO Two examples of inadequate corrective actions (Sections M8.2, E8.1,)

298/98002-05 URI Failure to implement 7-day diesel fuel inventory design requirements in

emergency procedures (Section E2.3)

298/98002-06 URI Concerns in implementation of Z-sump modification (Section E2.5)

298/98002-07 URI Operability evaluation of service water system in air filled condition (Section E2.6)

298/98002-08 IFl Inconsistent controls on torus level regarding design requirements for limiting

components (Section E2.7)

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Ooened and Closed

298/98002-04 NCV Average power range monitors not tested when required (Section M8.4).

Closed

298/96031-01 VIO Failure to provide procedures for expected abnormal conditions (Section 08.1)

298/97011-02 VIO Failure to follow procedure and inadequate procedure (Section M8.4)

298/96-013-00

298/96-013-01 LER inoperable high pressure coolant injection system due to a control oil leak

(Section M8.1)

298/96-003-00

298/96-003-01 LER Inoperable reactor isolation cooling system due to a failed operability test

(Section E8.2)

298/98-004-00 LER Average power range monitors not tested when required (Section M8.4)

298/96-024-07 VIO Examples of inadequate implementation of design changes in procedures

(Section E8.1)

Status

298/97006-01 VIO Failure to follow Technical Specifications (Section M8.2).

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