ML20237A622

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Insp Rept 50-298/98-04 on 980531-0711.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support
ML20237A622
Person / Time
Site: Cooper Entergy icon.png
Issue date: 08/10/1998
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20237A613 List:
References
50-298-98-04, 50-298-98-4, NUDOCS 9808140215
Download: ML20237A622 (27)


See also: IR 05000298/1998004

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ENCLOSURE 1

- U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket No.:

50-298

License No.:

DPR 46

Report No.:

50-298/98-04

Licensee:

Nebraska Public Power District

Facility:

Cooper Nuclear Station

Location:

P.O. Box 98

Brownville, Nebraska

Dates:

May 31 through July 11,1998

Inspectors:

Mary Miller, Senior Resident inspector

Chris Skinner, Resident inspector

Charles Marschall, Senior Project Engineer

Jim Melfi, Project Engineer

Approved By:

Charles Marschall, Acting Chief, Branch C

Division of Reactor Projects

ATTACHMENT:

Supplemental Information

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9808140215 980610

PDR

ADOCK 05000298

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EXECUTIVE SUMMARY

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Cooper Nuclear Station

NRC Inspection Report 50-298/98-04

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Ooerations

Plant management continued to demonstrate intrusive involvement in plant activities and

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successfully demanded resolution of safety issues as well as increased site performance

on high profile issues both within and outside of the plant organization (Section 01.1).

Operators demonstrated generally strong standards, responded promptly to challenges,

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and successfully demanded engineering support for these challenges (Section 01.2).

Inspectors identified an operability determination which had not documented the basis for

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its conclusion, although its conclusion was accurate (Section 02.1).

inspectors determined that corrective action for enforcement of past inadequate

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corrective action was not formal and that the licensee performed narrow evaluations of

very recent past corrective actions. These selections of past corrective actions were not

based on programmatic or systematic criteria. In response, the licensee initiated a

sampling process which included a broader scope of past corrective action issues and

involved systematic evaluation of the findings of those assessments (Section 07.1).

Operators routinely initiated a large number of insightful and self-critical problem

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identification reports both within and outside of the operations area, demonstrating a

strong focus on safety (Section O7.2).

Cooper Operations and Maintenance organizations had only recently (January 1998)

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begun to develop a process for systematic self-assessment. The operations and

maintenance departments had not yet demonstrated the ability to improve performance

using results of their self-assessments. The Radiation Protection department had

performed good annual self-assessments for several years (Section 07.3).

inspectors identified that the licensee closed commitment action items without obtaining

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the associated performance improvements. As a result, the commitment tracking system

did not effectively monitor corrective actions for identified deficiencies, and inspectors

could not determine whether the licensee had completed actions to address the

deficiencies identified in NRC Inspection Reports 50-298/97-07 and -97-12

(Section 07.4).

Maintenance

Maintenance during this inspection period was generally good. Supervisors were at the

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work sites, and technicians used appropriate radiological practices. Maintenance

rnanagers imposed a stand down after two instances of improper work practices

(Section M1.1).

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Despite troubleshooting performed at intervals over a month, maintenance failed to

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identify the cause of unexplained reductions in oil level for an essential service water

booster pump. Engineering identified the cause and demonstrated strong ownership and

good safety focus by deciding to immediately replace the pump (Section M1.2).

Some examples of poor rnaterial condition existed, including leakage through the

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residual heat removal heat exchanger outlet valves, resulting in silt buildup in essential

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service water piping and erosion of nonessential service water piping, resulting in

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through-wall leakage (Section M2.1).

Licensed operators assigned to the work control staff demonstrated strong safety focus

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control of plant configuration and communications with both control roorr md

maintenance work crews. Plant configuration was continually monitored by the work

control staff, resulting in improved work flow, scheduling, and safety (Section M4.1).

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Maintenance demonstrated an appropriately low threshold of identification of problems

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regarding equipment failures, lack of procedural acceptance criteria, and other quality

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administrative concerns in problem identification reports. This safety conscience regard

for identification of problems appeared to be an improvement over past performance in

this area (Section M7.1).

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Enaineerina

Significant sitt buildup was observed in residual heat removal service water booster

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pumps' suction and discharge lines. Inspections and evaluations determined that weekly

runs of the pumps would properly clear silt from the lines. This issue will be followed with

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the corrective actions associated with the violation regarding the residual heat removal

heat exchanger tube plugging (Section E2.1).

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The replacement component evaluation and procedures associated with an equivalent

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component replacement of safety-related relays did not insure adequate testing. The

equipment used to test the old design relays caused false failure indications when testing

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the replacement relays (Section E3.1).

Plant Succort

The inspectors identified that procedural guidance for controlling access and egress for

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satellite areas outside the radiological controlled area was weak. The radiological

protection personnel had already recognized this procedural deficiency independently

and had a partially completed revision when the inspector identified the concern

(Section R3.1).

No as-low-as-reasonable-achievable (ALARA) staff were observed to be present, nor

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was a systematic ALARA focus demonstrated for plant activities which were considered

one time. interim, or temporary processes in lower level radiation areas up to about

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35 millirem per hour. The inspector pointed out examples of these types of activities

without ALARA reviews which had been sustained for months or years and still

considered temporary.

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Report Details

Summary of Plant Status

The plant operated at 100 percent power at the beginning of this report period. A scheduled

power reduction to 70 percent power for turbine testing occurred June 12,1998.

1. Operatisns

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Conduct of Operations

O1.1

Plant Manaaement involvement in Plant Activities

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a.

Insoection Scoce (71707)

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Inspectors observed plant management involvement in plant activities and multiple

formal and informal meetings during the inspection period,

b.

Observations and Findinas

Management raised issues and set expectations for ownership and accountability for

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improved site performance. For example, during plan-of-the-day meetings, plant

management successfully demanded the following: more effective planning for power

reductions, reduced numbers of individuals with overdue training, proactive maintenance

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on intake structure screens (to preclude accumulation of debris during seasonal

flooding), and stronger performance of condition review group members and station

operations review committee members. Also, plant management successfully obtained

timely resolution of several design issues affecting plant procedures, including resolution

of concerns regarding the bases for some operator action points in the emergency

operating procedures, inspectors noted that, for those issues described in this report as

findings and concems, strong management involvement had typically not been

observed.

Plant management tracked completion of corrective actions and commitments within

scheduled due dates. Tracking and articulation of plant management expectations

throug'h this inspection period resulted in a significant reduction of overdue items in every

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site department. For example,6 months ago several departments had 30 or more

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overdue items. During this inspection period, the highest number of overdue items was

nine. Several departments had no overdue items. However, findings indicated that

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some items had been closed out when almost completed on or just before the due dates.

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Issues associated with these standards for closure of open items are discussed in

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Section 07.4 of this report.

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Plant management successfully demanded resolution of Updated Safety Analysis Report

discrepancies and poorly defined bases for operability. Standards for control room

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coordination with dispatchers regarding off-site power conditions and vulnerabilities were

improved regarding potential faults and vulnerabilities on off-site power lines, such as

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degraded electrical poles. Shift crews have successfully intervened with dispatchers

regarding scheduling of off-site power grid maintenance. Plant management

demonstrated intrusive involvement in Check Valves RCIC-42, -40, and -12 issues

described in Section M2.1 of this report, particularly in the scheduling of reactor core

isolation coolant system surveillance prior to resolution of the check valve issue.

Management intervention resulted in more effective resolution of valve operability,

reducing the time an essential system was inoperable.

c.

Conclusiomi

Plant management continued to demonstrate a strong safety focus and intrusive

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involvement in plant activities. Plant management successfully demanded resolution of

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high profile issues as well as increased site performance on issues both within and

outside of the plant organization.

01.2 Control Room Staff Activities and Resoonse to Plant issues and Events

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a.

Insoection Scoce (71707)

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inspectors observed multiple control room activities, including routine maintenance and

surveillance control, problem identification and resolution, and implementation of

abnormal and emergency procedures.

b.

Observations and Findinas

Control room crews demonstrated generally strong, proactive response to plant

conditions and activities. The control room supervisor or shift supervisor maintained

awareness and positive control of activities performed. Crew standards were generally

strong, with exceptions noted elsewhere in this report. The shift technical engineer

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typically provided strong intrusive evaluation of problems. The crew appropriately

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entered emergency procedures upon recognition of entry conditions. On July 6, before a

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weather front traveled across the area, the centrol room staff had discussed expected

conditions with the National Weather Service. When the reactor building vacuum

momentarily indicated a positive pressure of 0.03 inches of water, the operators

immediately entered Emergency Operating Procedure S.A," Containment Control"

Similarly, operators entered tornado alert procedures upon the declaration of tomado

watch conditions by the National Weather Service. Loss of offsite power procedures

were briefed to the crew under these conditions.

On June 14,1998, a station operator identified a leak in service water system discharge

from the nonessential turbine equipmerit cooling heat exchanger. Plant staff found a

through-wall leak and wall thickness degraded to as low as 0.16 inch for approximately a

6-inch diameter elliptical area inside an elbow. There was no isolation valve between the

leak and the river. A pipe patch was applied to stop leakage.

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Operators, with assistance from engineering, developed contingencies for loss of pipe

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integrity. The contingencies addressed flooding of the turbine building basement and

expected equipment losses under those conditions, such as feed pumps, condensate

booster pumps, some fire protection equipment, and other nonessential gear. Each crew

reviewed, updated, and added further detail to the contingency plans during their watch.

Inspectors observed as many as three engineers continuously assisting operators in the

control room in development of the contingency plans, such as identification of affected

circuitry, affected procedure steps, and equipment requirements under a flooding

condition.

The inspector and licensee were unable to locate a flood analysis that described the

expected effects of a turbine building flood. Engineers planned to determine if an

analysis was required to demonstrate that a turbine building flooding event was

appropriately analyzed. The inspectors walked down the accessible barriers between

the reactor building and the turbine building and did not identify apparent leakage paths

or po'ential circuit interaction. Since secondary containment forms the barrier for vital

equipment in the reactor building, and no leakage paths were apparent, the lack of an

analysis for turbine building flooding will be followed by an inspector followup item (50-

298/98004-01).

c.

Conclusions

Operators demonstrated generally strong standards, responded promptly to challenges,

and successfully demanded engineering support for these challenges.

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Operational Status of Facilities and Equipment

O2.1

Lack of Documentation for Operability Determination

a.

Insoection Scoce f71707)

The inspectors reviewed and followed the resolution of a problem identification report

that documented that test equipment failures nonconservatively affected relay settings.

Discussions were held with operations, maintenance, and engineering personnel.

b.

Observations and Findinos

inspectors identified an issue associated with replacement relays during routine review of

plant problem reports. Problem identification Report 2-28983 described several relays

that had failed testing. The problem identification report identified that the relays were

installed in multiple emergency core cooling systems. The operability determination

concluded that the relays were operable but did not describe the basis for the operability

conclusions.

Further inquiry found that existing relays had been replaced by a different model. The

new model had been evaluated as appropriate for service in a replacement component

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evaluation performed by engineering. The replacement component evaluation had

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evaluated the characteristics associated with the safety function of the relay, but had not

evaluated the test equipment used to test the relays. Electricians generated the problem

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identification report, when several replacement relays failed testing. The control room

had concluded that the relays remained operable based on knowledge of the acceptable

replacement component eva!uation; however, the inspectors noted that operators did not

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include or reference the component evaluation as the basis for operability. The lack of

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documentation of a basis for the operability conclusion was a weakness, although the

conclusion that the relayc were operable appeared valid. The cause of the test failures

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will be discussed in Section E3.1 of this report.

c.

Conclusions

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Inspectors ideritified an operability determination that had not documented the basis for

its conclusion, although its conclusion was accurate.

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Quality Assu.ance in Operations

07.1

Site-Wide Corrective Action Prooram Activities

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Lrisoection Scoce (71707)

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Inspectors observed corrective action program activities, including review of closed

problem identification reports and performance assessment group activities to appraise

the adequacy of corrective actions.

b.

Conclusions

inspectors determined that corrective action for enforcement on past inadequate

corrective action was not formal and that the licensee performed narrow evaluations of

very recent past corrective actions. These selections of past corrective actions were not

based on programmatic or systematic criteria. In response, the licensee initiated a

sampling process which included a broader scope of past corrective action issues and

involved systematic evaluation of the findings of those assessrnents.

07.2 Ooerations Problem identification and Corrective Action

a.

Insoection Scoce (71707)

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Inspectors reviewed problem identification reports init ated by the operations staff as well

as corrective actions for problems in the operations area.

b.

Observations and Findincs

During routine review of problem identification reports, inspectors noted that operations

problem identification reports continued to be insightful and self-critical. For example,

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operators questioned the length of time required for maintenance to provide an

evaluation of the operationalimpact of repeated service water booster pump oillevel

problems. This example demonstrated a questioning attitude and operator insistence on

engineering support. Control room operators and station operators also documented

more thm a dozen additional degraded conditions in problem identification reports during

a 3-day period.

Operators also demonstrated aggressive corrective action in initiating stop-work for

inadequate industrial safety work practices. Operator response to a nonessential service

water piping leak is an example. The response to the througn-wall leak is described in

more detail in Section 01.2 of this report.

c.

Conclusions

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Operators routinely initiated a large number of insightful and self-critical problem

identification reports both within and outside of the operations area, demonstrating a

strong focus on safety.

07.3 Self-Assessment

a.

Insoection Scoce (40500)

Inspectors evaluated the effectiveness of the licensee's self-assessment capability in the

operations, maintenance, and radiation protection areas by reviewing self-assessment

reports, audits (including audits of both onsite and offsite safety committee activities),

and evaluations. Engineering self-assessment was not within the scope of the

inspection.

b.

Observations and Findinas

The licensee's self-assessment program was in the early stages of development and

implementation. Departments had begun a monthly self-assessment program in January

1998. Only the radiation protection department had been performing annual self-

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assessments. Administrative Procedure 0-CNS-25, "Self-assessment," Revision 0,

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established the requirement for departments to assess their performance.

The operations department began to produce monthly reports in January. The monthly

reports contain good broad based performance information, including problem

identification reports, observations from outside organizations, and quality assurance

audit findings. Inspectors noted that, although the reports included observations by shift

mentors, the reports relied heavily on observations frun other organizations, such as

NRC inspection reports. These contributions do not constitute self-assessment, and the

operations staff has performed little assessment based on direct observation. rhe

reports do, however, include some analysis of problem identification repcrte. Tr'e reports

for January, February, and March 1998 presented a collection of information similar to

performance indicators, but did not furnish an evaluation of the data. Operations staff

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also produced a quarterly report on June 18,1998, for the first quarter of calendar year

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1998. The report compiled the results of the monthly reports for January through March

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1998 and documents performance strengths and five areas for improvement.

Additionally, a section of the report documented planned actions to address the areas for

improvement. Although the report identified actions to address many of the areas

needing improvement, in some cases areas for improvement remained unaddressed.

For example, the report documented planned action to address low numbers of

management observations, but oid not address operations emergency preparedness

training deficiencies. The assessment report aim documents plant status and

configuration control as the " biggest problem area for Operations." The report included

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actions to improve performance, but did not describe the problem. As a result, the

reader cannot determine whether the operations staff has addressed the problem

appropriately. The report also provided very little tre 'd information, possibly due to the

very small number of monthly reports. Since the due dates for the planned actions for

improvement were after the end of the inspection period, the inspectors could not assess

the overall effectiveness of the operations self-assessment.

The maintenance department had not yet begun to produce monthly reports.

Department personnel had, however, performed an assessment of their performance

based on information existing iri NRC inspection reports, quality assurance audits and

assessments, performance assessment by independent reviewers, and observations of

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managers and supervisors based on historical observations. Based on this information,

the maintenance staff developed the Maintenance improvement Plan, which identified

valid areas for improvement. The maintenance staff intended to use the plan to perform

focused performance assessments in the identified areas that require improved

performance. The inspectors found that the initial performance assessment had

identified valid areas requiring performance improvement and considered this approach

sound. The inspectors could not assess the effectiveness of raaintenance self-

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assessment, since no basis existed for determining whether implementation of the

program will result in performance improveinents.

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jnspectors found that the radiation protection department had an existing program of

annual self-assessment that had been ongoing since 1995. As documented in NRC

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inspection Report 50-298/98-18 the existing process was a good example of a critical

review that demonstrated good management oversight. The assessment made good

use of industry peers to identify problems and potential areas of improvement. As

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required by Administrative Procedure 0-CNS-25, the radiation protection staff has also

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initiated development of a monthly self-assessment report. At the time of the inspection,

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however, no reports had been completed.

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Inspectors also noted that the Safety Review and Audit Board (SRAB) has performed a

meaningful self-assessment and made changes to improve SRAB effectiveness. In

addition, inspectors considered the practice of individual SRAB member involvement in

quality assurance and engineering activities a positive indication of their involvement in

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improving plant performance. Inspectors found that quality assurance audits were

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appropriately scoped and that the reports contained meaningful findings. Inspectors

noted some repetitive quality assurance findings, an indication that some portions of the

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line organization did not implement corrective actions based on the findings.

c.

Conclusions

Cooper operations and maintenance organizations had only recently (January 1998)

begun to develop a process for systematic self-assessment. The operations and

maintenance Apartments had not yet demonstrated the ability to improve performance

using results of their self-assessments. The radiation protection department had

performed good annual self-assessments for several years.

07.4 Licensee Resoonse to inadeouate Corrective Action

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a.

Insoection Scoce (40500)

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inspectors reviewed licensee action to address the inadequate corrective actions

identified in NRC Inspection Reports 50-298/97-07 and 97-12 (EA 97-424).

b.

Observations and Findinos

inspectors noted that plant staff had performed substantial effort to address the identified

concerns, however, the inspectors could not determine that plant staff had completed

sufficient action to permit closing this item. In addition, the inspectors identified some

problems with the monitoring of corrective actions.

The licensee tracks action items, including commitments to the NRC in the nuclear

power group action item tracking system (NAITS). In reviewing the NAITS and the

associated documentation, the inspectors found that the licensee had closed some

NAITS items by reference to the corrective action program and the strategy for achieving

engineering excellence, without a corresponding cross-reference to the closed NAITS

item. Items, in some cases representing licensee commitments to the NRC in response

to the violation (EA 97-424), were not tracked further despite lack of completion of the

committed actions. For example, the licensee committed to implement Nuclear Safety

Advisory Group (NSAG) to provide additional oversight of engineering activities. The

licensee closed the NAITS item tracking this commitment, based on development of

administrative requirements for the NSAG, yet the three-member NSAG was not fully

staffed. The licensee also closed the NAITS item associated with engineering support

personnel training, although four people had not completed the training. In addition,

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plant staff closed a NAITS item to improve work standards associated with preventive

maintenance activity based on a project underway to upgrade the program despite not

completing the upgrades for all systems.

Inspectors also fcund NAITS items closed with no indication that performance had

changed. For example, one item required development of initial testing parameters and

determination of as-found leakage rates at the end of each operating cycle for torus to

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drywell vacuum breakers. The closure package contained no evidence of initial testing

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parameters or data or procedures associated with as-found leak rates. Another item

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required that operations management reinforce high standards for operator performance,

including procedure use and adherence. The closure package contained no evidence of

improved procedure use and adherence or other indications of improved performance.

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An additional NAITS item required that supervisors re-emphasize standards for conduct

and adequacy of prejob briefs. Inspectors noted that, although plant staff had revised

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Operations Instruction 8, dealing with prejob briefs, no evidence existed to support a

conclusion that prejob briefs improved.

The inspectors also reviewed licensee action in response to the residual heat removal

heat exchanger fouling documented in the previously mentioned NRC inspection reports.

In Nebraska Public Power District letter from G. R. Horn, Senior Vice President, Energy

Supply, to the Director, Office of Enforcement, NRC, dated December 31,1997, the

licensee committed to develop a formal Generic Letter 89-13 (Service Water System

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Problems Affecting Safety-related Equipment) program document with defined

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ownership, roles and responsibilities, and program criteria. Engineering Procedure 3.34,

Heat Exchanger Program, Revision 0, Section 1, states that the procedure defines the

ownership, roles, organization responsibilities, and program criteria for implementing the

Cooper Nuclear Station heat exchanger program. Section 4.4, implementing Action 111,

states, " Ensure by establish:.ng a routine inspection and maintenance program for open-

cycle service water system piping and components that corrosion, erosion, protective

coating failure, silting, and biofouling cannot degrade the performance of the safety-

related systems supplied by service water." Surveillance Procedure 6.SW.102, Service

Water System Post-LOCA Flow Verification, Revision 4, stated that it "can be used to

monitor silt accumulations to detect degraded system performance." The licensee could

not furnish evidence, however, that plant staff had used the procedure for that purpose.

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As of the end of the inspection, the licensee had riot furnished evidence that a program

existed to inspect for silting in service water system components. Ine NAITS item

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remained open, however, it contained a January 27,1998, entry that stated,

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" Engineering Procedure 3.34, ' Heat Exchanger Program,' has been approved and meets

the intent of the commitment." The inspectors concluded that the licensee had not yet

completed the action necessary to effectively monitor degradation of service water

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system components, despite the entry in the NAITS.

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c.

Conclusiqos

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Inspectors identified that the licensee chmd commitment action items without obtaining

the associated performance improvemeou. As a result, the commitment tracking system

did not effectively monitor corrective actions for identified deficiencies, and inspectors

could not determine whether the licensee had completed actions to address the

deficiencies identified in NRC Inspection Reports 50-298/97-07 and -97-12.

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08

Miscellaneous Operations issues

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08.1

(Closed) Violation 50-298/97011-01: Technical Specification violation for sample line

isolation. The licensee was in two limiting condition for operations that had the same

action for reactor sample valves. One of the limiting conditions of operation allowed the

isolation valves to be opened under administrative controls, and the other one did not.

The valves were opened under administrative control. The inspector identified that the

other limiting condition of operation was violated.

The licensee's reply to the Notice of Violation, dated April 8,1998, corrective action

taken was narrowly focused on the specific problem and the licensee did not indicate any

corrective steps to avoid further violations. The inspectors reviewed Condition Report

97-1541 to identify additional corrective actions. The condition report documented

several actions which would prevent the problem from recurring. For example, both the

scheduling and work control process were modified to contain a review of inoperable

Technical Specification equipment with respect to the weekly and daily schedule. The

inspectors considered the corrective actions acceptable.

08.2 (Ocen) Violation 50-298/97012-01 (EA 97-424): Inadequate corrective actions. The

NRC took escalated enforcement for several examples of inadequate corrective actions

in multiple areas. Review of the licensee's process to correct this condition found, for

assessment of the extent of condition, the actions were narrow and, in samples of past

concerns, small. Results were not evaluated in a systematic fashion. In response to the

concerns raised by the inspector, the licensee broadened this assessment. This issue is

described in Sections 07.1 and 07.4 of tnis report.

08.3 (Closed) Licensee Event Reoort 50-298/97-017: Inadequate original design did not meet

primary containment isolation requirements. On July 24,1996, the licensee discovered

that the motors and operators for the residual heat removal system heat exchanger vent

valves (RHR-MOV-M0166A, -B and RHR-MOV-M0167A, -B) did not meet the applicable

primary containment isolation requirements. The licensee determined that the inboard

isolation valves were powered from the same electric source and there was not an

automatic closure signal to the valves from the primary containment isolation function.

The valves were designed to vent noncondensable gases from the residual heat

exchanger during the steam condensing mode of operation.

The licensee identified that the apparent cause was an inadequate original design which

failed to consider the primary containment isolation requirements and electrical

separation requirements associated with these valves. As corrective actions the steam

condensing mode of operation was deleted from all procedures and the valves were

closed and de-energized.

The failure to meet primary containment isolation requirements for the residual heat

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removal system heat exchanger vent valves is a violation of 10 CFR Part 50,

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L_._____._____.__.__

f.

_ _ _

.

-to-

I .

l

Appendix B,

Criterion III.

This nonrep3titiva, licanssa

idsntificd and corrected violation is bsing trsated as c

-noncited violation, consistant with Saction VII.B.1 of ths

NRC Enforcement Policy (50-298/98004-02).

?

(

II. Maintenance

'

M1

Conduct of Maintenance

M1.1 General Comments

a. Insnection Scone (62707 and 61726)

The following maintenance activities were observed:

Maintenance Work Request 97-1385

Replacement of Service

Water Booster Pump A

L

Maintenance Work Request 98-1665

Inspection of Service

l-

Water Booster Pump C for

Silting

l

Maintenance Work Request 98-1697

Inspection of Service

Water Booster Pump B for

Silting

Maintenance Work Request 98-1698

Inspection of Service

Water Booster Pump D for

Silting

' Maintenance Work Request 98-1919

Troubleshooting Service

Water Booster Pump A

low

outboard 011 bearing

Level

'

Maintenance Work Request 98-1967

Troubleshooting and

Correction of Service

Water Booster Pump A

]

Surveillance Procedure 6.PC.302

Suppression Chamber Water

Level Calibration Test

and Functional Test

Instrument and Controls Procedure 14.4.4

Instrument

Sensing Line

Backflush/Backf

ill

Maintenance Procedure 7.2.14

Service Water Booster

Pump Overhaul and

l

Replacement

L

b.

Observations and Findinas

Maintenance personnel conducted good prejob briefings and

implemented management expectations for performing

maintenance.

Inspectors observed engineering presence

during many of the activities and saw strong maintenance

adherence to procedure and good practices for control of

y

work packages.

Maintenance personnel stopped work

'

immediately

_ _

_ _ _ _ _ - _ _ _ _ _ _ _

- - . _ _ _ - _ _ _ _ _

- _ _ - _

_ _ _ _ _ - _ _ _

. _ _ _ _ _ _ .

__

_ _ _ _ _

_ _ _ _ _ _ .

.

.

-11-

immediately and informed supervision when they encountered unexpected conditicns.

Maintenance supervisors and managers were often at job sites, and workers observed

appropriate radiological practices.

On June 10, the maintenance department conducted a stand down to address

performance concerns identified by maintenance managers. The concerns involved two

improper work practices; in one case workers did not have the maintenance instruction in

active use during the work. In the other, a mechanic changed a valve position within a

clearance boundary without informing operators or work control. Neither activity resulted

in a direct effect on plant safety. Maintenance craft were reminded of management

expectations in these areas.

c.

Conclusions

Maintenance during this inspection period was generally good. Supervisors were at the

work sites, and technicians used appropriate radiological practices. Maintenance

managers imposed a stand down after two instances of improper work practices.

M 1.2 Troubleshooting and Correction of Service Water Booster Pumo A Oil Level Droo

a.

J.cspection Scone (62707)

Inspectors observed licensee's activities associated with troubleshooting and

replacement of Service Water Booster Pump A after repeated oillevel decreases,

b.

Observations and Findinos

)

On June 1,1998, the licensee replaced Service Water Booster Pump A as part of

scheduled maintenance. Seven days later operations initiated a problem identification

report documenting that the thrust bearing oil level had dropped to the low level at a rapid

rate. Maintenance staff made several unsuccessful attempts to correct the problem. On

June 30, the licensee disassembled the pump and found that the shaft was undersized

as a result of an overhaul about a year earlier at a qualified pump overhaul facility.

Engineering determined that further troubleshooting and testing might not resolve the

degraded condition, and plant staff replaced the pump.

Engineering actively supported the troubleshooting on June 28-30, and took an active

role in determining whether to replace the pump. Maintenance sent the pump to the

vendor for a complete evaluation and initiated a quality assurance assessment of the

vendor's pump rebuilding program. Engineering determined that the oillevel reduction

resulted from an improperly high oil operating band. This was not identified during

I

receipt inspection. Engineering determined that the high oillevel resulted in formation of

an oil mist that flowed out of the bearing housing and deposited on the pump housing

i

and local area. This occurred until the level was reduced to the lower third of the bearing

race, where misting was significantly reduced and the oillevel stabilized. The pump

l

t

l

.

l

.

_ _ _ , _ _ _ _ _ - _ _ _ _ _ _

_ _ _ - _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _

.

.

-12-

)

l

shaft was also undersized, but engineering determined it had no effect on safety. The

.

undersized pump shaft and the improperly marked oil operating band were the basis for

I

engineering requiring pump replacement.

During these activities, maintenance identified that some technicians had demonstrated

poor workmanship, and critical parameters may not have been checked properly during

receipt and acceptance testing. These technicians were also involved in the stand down

described in the previous section of this report. As an interim corrective measure, these

maintenance technicians were subsequently decertified for supervisory and quality

control activities and sent to retraining after counseling with management.

When maintenance managers recognized that the incorrect overhaul of the pump had

not been properly diagnosed, they initiated a problem identification report. Inspectors will

track the possibly generic issue of installation of an undersized shaft during overhaul,

and the resolution of performance by the maintenance staff using inspector followup item

(50-298/98004-03),

c.

Conclusions

Despite troubleshooting performed at intervals over a month, maintenance failed to

identify the cause of unexplained reductions in oil level for an essential service water

booster pump. Engineering identified the cause and demonstrated strong ownership and

]

good safety focus by deciding to immediately replace the pump.

j

M2

Maintenance and Material Condition of Facilities and Equipment

4

M2.1 Examoles of Plant Material Condition

a.

Scone (62703.71707.61726)

Inspectors observed several indications of plant material condition, summarized in this

section.

b.

Observations and Findinos

Inspectors observed the following indications of material condition of the plant.

I

Significant silt accumulation was found in the suction and discharge lines of service

water booster pumps and in the residual heat removal heat exchanger head

(Section E2.1).

Residual Heat Removal System Heat Exchanger Outlet Valves SW-MO-89A and -B leak

past the seats, allowing significant transport of silt into the essential service water

system.

'

.

I

lL_.-------

,

- -

_ _ _ __

_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

.

!

i

-

,

,

-13-

Service Water Booster Pump A was found to have been improperly rebuilt by a Part 21

vendor (Section M1.3).

Through-wall leakage occurred on an eloow in the nonessential service water portion of

the turbine equipment cooling system. This was determined to have been caused by

f

erosion of piping by service water sitt (Section E2.2).

l

c.

Conclusion

Some examples of poor material condition existed, including leakage through the

l

residual heat removal heat exchanger outlet valves, resulting in silt buildup in essential

service water piping and erosion of nonessential service water piping, resulting in

]

through-wall leakage.

M4

Maintenance Staff Knowledge and Performance

,

M4.1 Ooerator Involvement in the Work Control Process

a.

Insoection Scoce (71707)

Inspectors observed operator and work control staff implementation, completion, and

processing of several work orders.

b.

Observations and Findinas

in general, operators in control of work demonstrated very effective interaction with

maintenance and operating crews to insure proper control of plant conditions, resulting in

a significant improvement in safety and coordination of work flow. Communications were

detailed, accurate, timely, and properly conveyed the priorities associated with each

scheduled activity. Licensed operators performed many of the tasks associated with

planning and implementation of the work control process. Clearances were determined

and discussed with technicians and control room crew members, work packages and

postmaintenance testing were reviewed, work schedules were coordinated with the

control room, limited condition for operation entry conditions associated with work

packages were properly recognized and recommended, and clearances and plant

configuration were controlled and maintained with close, effective coordination with the

I

control room. Problem identification reports were reviewed by licensed operators in the

work control center, resulting in several examples of safety focused evaluation of

concerns.

c.

Conclusions

Licensed operators assigned to the work control staff demonstrated strong safety focus,

good control of plant configuration, and effective communications with corurol room and

i

l

maintenance crews. The work control staff continually monitored plant configuration,

resulting in improved safety, work flow, and scheduling.

_ _ _ _ _ _ _ _ _ _ _ _

_ _ - - - _ _ - _ _ _ _ _ _ _ _ _ _ _

_ _ _ - _ _ _ _ _ _ _ _ _ _ _ _

_

_ _ _

_ - _ _ - _ _ -

._

.

.

l

- 14-

l

l

M7

Quality Assurance in Maintenance Activities

M7.1 Problem identification in Maintenance

a.

Insoection Scoce (62707)

Inspectors reviewed problem identification reports initiated during the inspection period

and observed maintenance performance in the area of problem recognition and

documentation.

b.

Observations and Findinas

During this inspection period, over 30 problem identification reports initiated by

maintenance personnel demonstrated an appropriately low threshold for equipment

problem and problems in the area of administrative and programmatic issues. One

example was failures of relays in test devices discussed in Section E3.1. Other reports

clearly described equipment that had not responded as expected, procedures or work

instructions that did not adequately address the job requirements, or administrative

requirements had not been met. Interviews with maintenance technicians indicated a

higher standard for proper maintenance and an improved understanding of the process

and purpose of problem identification reports.

c.

Conclusions

Maintenance demonstrated an appropriately low threshold of identification of problems

regarding equipment failures, lack of procedural acceptance criteria, and other quality

administrative concerns in problem identification reports. Inspectors considered this

safety conscience regard for identification of problems an improvement over past

performance.

M8

Miscellaneous Maintenance issues (92902)

M8.1 (Closed) Licensee Event Reoort 50-298/98-007: Missed surveillance testing of main

turbine stop valve closure. Technical Specification Table 4.1.1 requires that the main

turbine stop valve closure scram function be tested once per month. During shutdowns,

the surveillance cannot be performed. With the valves inoperable, Technical

Specification Table 3.1.1, Note 1.b, requires that operators reduce power below

30 percent. Testing of the main turbine stop valve prior to exceeding 30 percent power

was not performed during startups from the December 1995 refueling outage and the

May 1997 refueling outage.

This item was identified during completion of corrective actions for Licensee Event

Report 50-298/98-004 and Violation 50-298/98002-03. The licensee's corrective action

will be reviewed during the closure of Violation 50-298/98002-03.

_ _ _ _ _ _

_ _ _ _ _

_ _ _ _ _ _ _ _ _

_ _ _ _ _ _ _ _ _ _ _ _ _ _

____

.

.

-15

The failure to test the main turbine stop valves prior to exceeding 30 percent power is a

violation of Technical Specification 4.1.1. This nonrepetitive, licensee identified and

corrected violation is being treated as a noncited violation, consistent with Section Vll.B.1

of the NRC Enforcement Policy (50-298/98004 04).

M8.2 (Closed) Licensee Event Reoort 50-298/97-016: Diesel generator test did not meet

minimum Technical Specification time requirements. Technical Specification

Surveillance Requirement 4.5.F.1 required the redundant operable diesel generator be

. demonstrated operable by a run time greater than or equal to 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> following the

declaration that the other diesel generator was inoperable. On December 10,1996, the

operable diesel generator was run fcr only 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />,9 minutes.

The licensee event report stated that the cause of the Technical Specification violation

was due to a past interpretation regarding the applicability of the surveillance procedures

(6.1DG.102 and 6.2DG.102, " Diesel Generator Demonstration of Operability Test"). As

corrective actions the procedures were placed on administrative hold until revised to

specifically state the purpose of the procedures. The inspectors considered the

ambiguous understanding of the purpose of the procedure to have been a contributing

factor, but concluded that the root cause was poor operator standards for clear

understanding and precise implementation of the Technical Specification requirements.

The licensee did not address inadequate operator understanding and implementation of

Technical Specifications in the licensee event report. Since the root cause of this

problem is similar to that of Violation 50-298/98002-03, documenting that Technical

Specification amendments were not rigorously implemented, the corrective actions will

be reviewed during the closure of that violation.

The failure to run the operable diesel generator for greater than or equal to 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> is a

violation of Technical Specification 4.5.F.1 which required that the operable diesel

l

generator be demonstrated operable by running it for greater than or equal to 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />.

This nonrepetitive, licensee identified and corrected violation is being treated as a

noncited violation, consistent with Section Vll.B.1 of the NRC Enforcement Policy (50-

298/98004-05).

111. Enaineerina

E2

Engineering Support of Facilities and Equipment

E2.1

Identification of Sil' Builduo in Residual Heat Removal Service Water Booster Pumos

a.

Insoection Scoce (93702. 37551)

Inspectors responded to the finding of significant silt buildup in service water booster

pump piping. Inspectors observed the conditions which the licensee encountered,

observed boroscope inspections, reviewed evaluations and sitt inspection findings, and

held discussions with maintenance technicians, engineers, and managers.

_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ . -

_

i

-

.

-16-

b.

Observations and Findings

l

On May 26,1998, during maintenance on Service Water Booster Pump A, technicians

'

reported that the suction and discharge lines had accumulated significant sitt. The inlet

was found 75 percent clogged and the outlet about 50 percent clogged. A problem

identification report was initiated, as well as significant engineering involvement and a

problem resolution matrix. Plant staff examined the other three pumps and both of the

residual heat removal heat exchangers by boroscope inspection. They found Service

Water Booster Pump B suction line about 50 percent full of sitt and found approximately

one inch of sitt in the outlet. The remaining pumps (C and D), and the two heat

exchangers contained minimal silt (approximately one inch). Service Water Booster

Pumps A and C had last been run in March, while B and D had been run more recently

to provide torus cooling.

I

,

An evaluation determined that running the Service Water Booster Pump B with silt in the

inlet would cause no adverse effects. Operators ran the pump without incident. A

boroscope examination conducted immediately afterward found that the silt in the inlet

had been removed, and no sitt was present in the outlet or in the heat exchanger.

Technicians completed replacement of Service Water Booster Pump A, returned the

pump to service, and performed a boroscope inspection. No silt was observed in the

inlet, outlet, or heat exchanger. After approximately 3 weeks of boroscope inspections

and pump runs, an engineering evaluation concluded that weekly pump runs would keep

silt properly controlled.

Silt ao umulation in service water systems will be addressed with the corrective actions

for Violution 50-298/97012-01, fouling of the residual heat removal heat exchanger,

c.

Conclusions

Significant silt buildup was observed in residual heat removal service water booster

pumps' suction and discharge lines. Inspections and evaluations determined that weekly

runs of the pumps would properly clear silt from the lines. This issue will be followed with

the corrective actions associated with the violation regarding the residual heat removal

heat exchanger tube plugging.

E2.2

Engineering Supoort of Through-Wall Leak in Nonessential Service Water System

a.

Scooe (37551. 93702)

Inspectors reviewed the engineering response to operations identification of through-wall

leakage on the nonessential service water piping. Inspectors participated in conference

calls, reviewed analyses, inspected the system, and held discussions with engineers and

managers.

\\

.

-_

_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ .

._.

_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

-

I

l

-

i

.

!

17

I

b.

Conclusions

As described in Section 01.2 of this report, engineering response to a through-wallleak

in the nonessential service water system was prompt, but was not comprehensive

regarding analysis of piping integrity or flooding analysis.

E3

Engineering Procedures and Documentation

E3.1

Lack of Evaluation of Test Eauioment in Replacement Comoonent Process

a.

Icipection Scoce (37551)

Inspectors reviewed a problem identification report which indicated a vulnerability in the

replacement component evaluation process.

b.

Observations and Findinos

Problem Identification Report 2-28983 described indications of multiple failures of

equivalent replacement relays during pre-installation testing. As described in

Section O2.1, the relays were equivalent replacement relays that engineering had

accepted in a replacement component eva:uation. This evaluation had not considered

whether the existing test equipment would provide valid testing of the replacement

components. Further, Procedure 3.25, " Replacement Component Evaluation, and

Procedure 3.4, " Configuration Change Control", Revision 22, did not require evaluation of

test equipment to assure that testing of replacement equipment would result in valid

conclusions. The licensee initiated Problem identification Report 2-26318 in response to

the inspector's concerns regarding lack of procedure adequacy. The licensee had not

concluded the scope of the concern and to date considers that, since the testing failed in

a conservative manner, no corrective actions were necessary. The licensee's conclusion

and final corrective actions will be followed by an inspector followup item (50-298/98004-

06)

c.

Conclusions

The replacement component evaluation and procedures associated with an equivalent

component replacement of safety-related relays did not insure adequate testing. The

equipment used to test the old design relays caused false failure indications when testing

the replacement relays.

,

Miscellaneous Engineering issues (92903)

E8

l

'

E8.1

(Ocen) Insoector Followuo item 50-298/98002-07: Potential effect of high torus level

allowed by emergency operating procedures. On March 30,1998, the inspectors

questioned procedural controls for the torus level with respect to the design requirements

for cntical torus components. Engineering had identified that the torus strainer

penetration calculations were nonconservative, and that penetrations were still operable,

.

L _ -- _ _

_

__

_ _ - _ _ _ _ _ _ _

________-__- __ ______ _ _ _ _ _ - - _

.

.

-18-

hydrodynamic loads associated with a loss-of-coolant accident blowdown from the

downcomers. The hydrodynamic loading is bounded by analysis only when torus levelis

2 inches or less. The inspector noted that emergency operating procedures allowed a

torus level to increase to a level of 37 inches before an emergency depressurization was

required. This indicated that the plant could remain at full pressure and therefore be

vulnerable to a loss-of-coolant accident in conditions where the torus level and

associated hydrodynamic forces could cause the strainer penetrations to be in an

unanalyzed condition. Licensee evaluation for the following few weeks was inconclusive,

and licensee management involvement was requested based on potential safety

significance.

During a briefing on June 16 after significant management involvement, licensing,

engineering, and operations staff presented a thorough and integrated evaluation of this

issue. Engineers concluded that the vendor's emergency procedure guidelines (EPGs)

l

and the severe accident management guidelines (SAGS) had not considered

hydrodynamic loading effects on torus strainers in determining an acceptable torus level

for implementation of the guidelines during accidents.

'

The licensee modeled a reactor coolant system breech with higher torus level r id found

that, under typicalloss-of-coolant accident simulator scenarios, no core damage was

predicted. However, with torus level elevated and modeling of a breech of primary

containment as a result of torus hydrodynamic loading on suction strainer penetrations,

the resulting torus failure would cause a higher core damage probability than a loss-of-

coolant accident event without containment damage. This aspect of probabilistic risk had

not been modeled in EPGs or licensee-specific individual plant evaluation.

The licensee reviewed the SAGS to determine if torus level had been properly

considered in their development. The licensee found that torus hydrodynamic loading as

a result of torus level had not been modeled and that, under severe accidents resulting in

reactor coolant system breech, a containment failure subsequent to reactor coolant

system breech should be considered if torus level resulted in exceeding hydrodynamic

loading limits on primary containment suction strainer penetrations. The licensee noted

that further conservatism may be available in calculations for hydrodynamic loads.

I

However, the licensee also considered this aspect of severe accidents to require review

from a generic standpoint by the Boiling Water Reactor Owner's Group (BWROG) in

development of severe accident guidelines and presented these issues to the BWROG

SAG working group on June 24.

l

The BWROG SAG working group concluded that torus level guidelines had not been

evaluated with respect to hydrodynamic loading of torus internals, such as strainers, for

l

any BWR containment design. The issue was assigned a BWROG EPG issue number

l

(EPG 9817) and had been assigned to various licensees for technical evaluation and

recommendations.

The licensee noted that current emergency operating procedures require torus level to

be promptly reduced if it should rise above 2 inches. This would be an immediate action

i

'

i

.

_ _ _ _ _ _ - - _ _ _ _ _ _ _

l

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l

l

.

19

be promptly reduced if it should rise above 2 inches. This would be an immediate action

unless a group isolation had isolated the pathway from the torus to radwaste. In that

case, a plant trip would have been anticipated, and emergency operating procedurec do

not allow reset of that isolation without first fully understanding the causes of plant

conditions. This pathway would remain isolated and the torus level would not be

reduced until further diagnosis had occurred. To address this concern, operations

determined that a prompt plant cooldown and depressurization would be required to

reduce the potential for hydrodynamic loading. This expectation was promptly provided

t

to crews and evaluated in simulator scenarios. This item will remain open to follow up

l

resolution of generic concerns.

c.

Conclusions

After significant inspector and plant management involvement, engineering performed

l

thorough and complete technical evaluation of a complex issue, and effectively

integrated operations and licensing staff in the evaluation and interim resolution.

l

Engineering assessed the potential effects of hydrodynamic loading on torus strainers,

[

caused by high torus levels allowed by emergency operating procedure and severe

'

accident guidelines. The licensee concluded that the guidelines had not considered

these effects, implemented interim compensatory actions, and presented the issue to the

BWROG.

IV. Plant Suonort

!

'

R3

Radiological Protection and Chemistry Procedures and Documentation

R3.1

Weak Guidance for Access to and Exit from Radiologically Controlled Satellite Areas

a.

Inspections Scoce (71750)

The inspectors observed posting and control of radiological controlled areas and

technician implementation of controls, reviewed Procedure 9.RADOP.3, " Area Posting

,

'

and Access Control," Revision 0, and held discussions with radiological protection

i

personnel and management.

b

Observations and Findinos

During the review of Procedure 9.RADOP.3, the inspectors identified that access and

I

exit requirements for radiologically controlled satellite areas were not well defined in the

procedure. Satellite areas were defined to be areas within the restricted area that require

,

posting by 10 CFR Part 20. The procedure clearly described the requirements for

I

access and exit for the radiological controlled area. Step 4.4 stated that access and exit

requirements for satellite areas will not be as extensive as those established for the

radiological controlled area. The procedure did not clearly state what the requirements

'

were for a satellite area nor did the procedure state how the requirements for the two

areas were different.

.

._____________. _ _ _

. _ -

'

.

o

-20-

Based on discussion with radiation protection, the inspectors discovered that the

guidance for access and exit from satellite areas had already been recognized

radiation protection staff and a procedure revision was partially developed. Until the;

procedure change is implemented, the radiation protection staff will control the acce

and exit of the satellite areas.

c.

Conclusion

The inspectors identified that procedural guidance for controlling access and exit f

satellite areas outside the radiological controlled area was weak. The radiologica

and had a partially completed revision when the inspec

!

R4

Radiological Protection Staff Knowledge and Perfor;aance

R4.1 At>>AA Procram Deficiencies

h

Inspections Scone (71750)

a.

Inspectors reviewed the ALARA program efforts for one time, interim, or temp

changes to plant activities in radiation areas. Inspectors held discussions with

maintenance, engineering, planning, and radiological protection staff.

b.

Observations and Findinos

inspectors noted that the ALARA staff had not been involved in a review to determ

the radiation exposure could be reduced for the inspections of the residual heat re

heat exchanger silt buildup discussed in Section E2.1 of this report. The radiatio

in the heat exchanger rooms vary from 5 to 20 millirem per hour, with 35 millire

hour on contact. Since the inspections were initiated to respond to recent events n

determination had been made rqardino how many more inspections were expect

,

The licensee performed more inspections v,'he heat exchangers over the fo

weeks, and the interviews with plant staff identified that no ALARA reviews we e

performed to reduce exposure.

The inspector had observed that ALARA personnel were usually involvec in re

activities in radiation areas and in one-time tasks in the higher radiation areas. Site

personnelgenerally used basic radiation protection and ALARA practices. However n

involvement of ALARA personnel or systematic ALARA focus was observed in s

,

as they prepared for interim, potentially repetitive, or emergent tasks in low radiation

areas of up to about 35 millirem per hour.

An additional example is the chemistry control measures for addition of oxygen

feedwater. The long-term plan of piping gas from outside the turbine building ha

been accomplished, so chemistry performs the interim measure of regularly b

feedwater chemistry control gas bottles into a radiologically controlled area of the

.

_ _ _ - _ _ _ _

_

_-__- __ _ _ _ _ _ - _ _ - _ _ _ _ - - . _ - _ _ .

_ _ _ _

. -__

.- .__- _ _-

.

l

e

-20-

l

!

Based on discussion with radiation protection, the inspectors discovered that the lack of

guidance for access and exit from satellite areas had already been recognized by the

radiation protection staff and a procedure revision was partially developed. Until the

procedure change is implemented, the radiation protection staff will control the access

and exit of the satellite areas.

j

c.

Conclusion

The inspectors identified that procedural guidance for controlling access and exit for

satellite areas outside the radiological controlled area ; as weak. The radiological

protection personnel had already recognized this procedural deficiency independently

'

and had a partially completed revision when the inspector identified the concern.

R4

Radiological Protection Staff Knowledge and Performance

R4.1

ALARA Proaram Deficiencies

a.

Lrlspfctions Scoce (71750)

Inspectors reviewed the ALARA program efforts for one time, interim, cr temporary

changes to plant activities in radiation areas. Inspectors held discussions with

maintenance, engineering, planning, and radiological protection staff.

b.

Observations and Findinas

Irispectors noted that the ALARA staff had not been involved in a review to determine if

the radiation exposure could be reduced for the inspections of the residual heat removal

heat exchanger silt buildup discussed in Section E2.1 cf this report. The radiation levels

in the heat exchanger rooms vary from 5 to 20 millirem per hour, with 35 millirem per

hour on contact. Since the inspections were initiated to respond to recent events, no

determination had been made regarding how many more inspections were expected.

The licensee performed more inspections of the heat exchangers over the following

weeks, and the interviews with plant staff identified that no ALARA reviews were

performed to reduce exposure.

1

The inspector had observed that ALARA personnel were usually iavolved in repetitive

activities in radiation areas and in one-time tasks in the higher radiation areas. Site

personnel generally used basic radiation protection and ALARA practices. However, no

involvement of ALARA personnel or systematic ALARA focus was observed in site staff

as they prepared for interim, potentially repetitive, or emergent tasks in low radiation

areas of up to about 35 millirem per hour.

An additional example is the chemistry control measures for addition of oxygen to

feedwater. The long-term plan of piping gas from outside the turbine building has not

been accomplished, so chemistry performs the interim measure of regularly bringing

feedwater chemistry control gas bottles into a radiologically controlled area of the turbine

l

0

_..__________.__._.___-_-_w

- _ __- _ - _ _ __-__- _____

_ _ - _ _ _ _ _ _ _ _ _ _ _ - - _ _ _ - _ _ _ _ - _ _ _ _ - _ _ _ - - _ _ _ _ _ _ _ _ _ _ _ _ _ .

.

e

-21-

building. The radiation area is low. This practice had not been evaluated by ALARA to

determine if radiation exposure could be reduced or a higher priority could be placed on

the final modification for chemistry control to reduce the number of bottle replacements

required.

c.

Conclusions

No ALARA staff were obsewed to be present, nor was a systematic ALARA focus

demonstrated for plant activities which were considered one time, interim, or temporary

processes in lower level radiation areas up to about 35 millirem per hour. The inspector

pointed out examples of these types of repetitive activities without ALARA reviews that

had been sustained for months or years and were still considered temporary.

X1

Exit Meeting Summary

The inspectors presented the inspection results to members of licensee management at

the Corrective Action Program exit meeting on June 4,1998, and at the routine exit

j

meeting on July 7,1998. The licensee acknowledged the findings presented.

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The inspectors asked the licensee whether any materials examined during the inspection

should be considered proprietary. Proprietary information had been provided, and the

inspectors agreed that it was to be controlled consistent with existing memoranda of

understanding and NRC policy. The information will be retumed to the licensee.

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PARTIAL LIST OF PERSONS CONTACTED

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Licensee

" Mark Bohling, Senior Auditor, Quality Assurance

    • Mike Boyce, Plant Engineering Manager
    • Joe Burton, Performance Analysis Manager
    • Paul Caudill, Senior Engineering Manager
  • Tim Chard, Assistant Radiological Manager
  • Linda Dewhirst, Licensing Engineering
  • Roman Estrada, Corrective Action Program Supervisor
  1. Charles Fidler, Assistant Maintenance Manager
    • Chuck Gaines, Maintenance Manager
  1. Ted Gifford, Design Engineering Manager
  1. Paul Gritton, Employee Communications
  1. Andy Jacobs, NSAG
  1. David Madson, Licensing Engineer
  1. Mike Peckham, Plant Manager
    • Jennifer Peters, Licensing Secretary
  1. Andy Sessoms, Senior Quality Assurance Manager
    • Alan Shiever, Operations Manager
  • Sara Stiers, Administrative Services Manager
    • Jim Sumpter, Lice.1 sing
  • Bruce Toline Quality Assurance Audit Supervisor

NEG

  • Charles Marschall, Project Engineer
  • Attended Corrective Action Program exit meeting on June 4,1998
  1. Attended routine exit meeting on July 7,1998

INSPECTION PROCEDURES USFO

IP 37551: Onsite Engineering

IP 61726: Surveillance Observation

IP 62707: Maintenance Observation

IP 71707. Plant Operations

IP 71750: Plant Support Activities

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IP 92902: Followup - Maintenance

IP 92903: Followup - Engineering

IP 93702: Prompt Onsite Response to Events at Operating Power Reactors

IP 40500: Effectiveness of Licensee Controls in Identifying, Resolving and Preventing Problems

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9

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ITEMS OPENED, OPENED AND CLOSED, CLOSED, AND DISCUSSED

Opened

50-298/98004-01

IFl

No analysis for turbine building flooding (Sections 01.2 and E

50-298/98004-03

IFl

.

Problems associated with service water booster pump vendor an

maintenance (Section M1.2).

50-298/98004-06

IFl

Replacement component evaluations failed to address test

equipment (Section E3.1).

Opened and Closed

50-298/98004-02

NCV

Inadequate original design did not meet primary containment -

isolation requirements (Section 08.3).

h

50-298/98004-04

NCV

}

Failure to test the main turbine stop valves prior to exceeding

30 percent power (Section M8.1),

50-298/98004-05

NCV

Diesel generator test did not meet minimum Technical

Specification time requirements (Section M8.2).

C1019.d

50-298/97011-01

VIO

Technical Specification violation for sample line isolation

(Section 08.1).

50-298/97-017

LER

inadequate original design did not meet primary containment

isolation requirements (Section 08.3).

50-298/98-007

LER

Missed surveillance testing of main turbine stop valve closure

(Section M8.1).

50-298/97-016

LER

Diesel generator test did not meet minimum Technical

Specification time requirements (Section M8.2).

Qiscussed

50-298/98002-03

VIO

Inadequate corrective actions in identifying the extent of condition

(Sections M8.1, and M8.2).

50-298/97012-01

VIO

Inadequate corrective action (Sections 07.1,08.2, and E2.1).

50-298/98002-u,

IFl

Potential effect of high torus level allowed by emergency oper

procedures (Section E8.1).

.

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_ - __ _ _________-___ _ __ _ _ _ _ _ _

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ITEMS OPENED, OPENED AND CLOSED, CLOSED. AND DISCUSSED

Ooened

50-298/98004-01

IFl

No analysis for turbine building flooding (Sections 01.2 and E2.3).

50-298/98004-03

IFl

Problems associated with service water booster pump vendor and

maintenance (Section M1.2).

50-298/98004-06

IFl

Replacement component evaluations failed to address test

equipment (Section E3.1).

Ooened and Closed

50-298/98004-02

NCV Inadequate original design did not meet primary containment '

isolation requirements (Section 08.3).

50-298/98004-04

NCV Failure to test the main turbine stop valves prior to exceeding

30 percent power (Section M8.1).

50-298/98004-05

NCV Diesel generator test did not meet minimum Technical

Specification time requirements (Section M8.2).

Closed

50-298/97011-01

VIO

Technical Specification violation for sample line isolation

(Section 08.1).

50-298/97-017

LER

Inadequate original design did not meet primary containment

isolation requirements (Section 08.3).

50-298/98-007

LER

Missed surveillance testing of main turbine stop valve closure

(Section M8.1).

I

50-298/97-016

LER

Diesel generator test did not meet minimum Technical

Specification time requirements (Section M8.2).

Discussed

50-298/98002-03

VIO

Inadequate corrective actions in identifying the extent of condition

(Sections M8.1, and M8.2).

50-298/97012-01

VIO

Inadequate corrective action (Sections 07.1,08.2, and E2.1).

50-298/98002-07

IFl

Potential effect of high torus level allowed by emergency operating

procedures (Section E8.1).

.