ML20235E641
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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO LER)
MONTHYEARML20217G7821997-07-22022 July 1997
[Table view]Special Rept:On 970227,ECCS Sys Was Actuated & Injected Water in Rcs.Declared HPCI Subsystem Operable Following Restoration of Subsystem to Normal Standby Lineup ML20097D4661992-05-27027 May 1992 Special Rept,Reflecting Quad-Cities Nuclear Power Station, Unit 2 Summary Status of Fuel Performance at End of Cycle 11. No Sipping Performed on Reload Fuel Assemblies at End of Cycle 11 ML20066J6331991-01-31031 January 1991 Forwards Summary Status of Fuel Performance for End of Cycle 11 ML20207P1881987-01-0606 January 1987 Special Rept:Summarizes Status of Fuel Performance as of End of Cycle 8.Of 2031 Assemblies used,289 Determined to Have Failed & Discharged as Leaker Assemblies.Aug 1986 Sipping Tests Showed No Indication of Assembly Failure BECO-86-173, Partially Withheld Security Event Rept:On 861107,HVAC Duct, Penetrating Vital Area,Removed by Contracted Craft Workers Before Notifying Security.Cause Not Stated.Security Oversight of Subj Contract Work Intensified1986-11-12012 November 1986 Partially Withheld Security Event Rept:On 861107,HVAC Duct, Penetrating Vital Area,Removed by Contracted Craft Workers Before Notifying Security.Cause Not Stated.Security Oversight of Subj Contract Work Intensified BECO-86-171, Partially Withheld Security Event Rept:On 861106,temporary Vital Area Barrier Insp Found Barrier Could Be Breached. Barrier Modified & Compensatory Security Measures Released1986-11-10010 November 1986 Partially Withheld Security Event Rept:On 861106,temporary Vital Area Barrier Insp Found Barrier Could Be Breached. Barrier Modified & Compensatory Security Measures Released ML20211E0731986-09-26026 September 1986 Unplanned Operating Event Rept 85-6, Manual Reactor Trip Following MSIV Closure Due to Inadvertent Emergency Feedwater Actuation,851009 BECO-86-125, Partially Withheld Security Event Rept:On 860826,bomb Threat Received.Search Initiated.No Suspicious Objects Found1986-08-29029 August 1986 Partially Withheld Security Event Rept:On 860826,bomb Threat Received.Search Initiated.No Suspicious Objects Found ML20238E4601986-08-28028 August 1986 Partially Withheld Secrity Event Rept:On 860824,bomb Threat Received for Plants.Bomb Search Initiated.No Suspicious Objects Found ML20211K8211986-06-18018 June 1986 Special Rept:On 860521,valid Failure Occurred on Div 2 Diesel Generator During Performance of Tech Spec Surveillance 4.8.1.1.2.Caused by Failure of Jacket Water Thermostatic Control Valve to Open ML20238E4591986-06-17017 June 1986 Partially Withheld Security Event Rept:On 860612,withheld Discovery Made Re 860604 Moderate Loss of Security Effectiveness.Caused by Inadequate Post Orders & Training for Assignment.Assignments Will Be Specifically Addressed 05000000/LER-1986-009, Ro:On 860312,discovered That LER 2-86-04 & LER 86-009 Not Submitted to Nrc.Caused by Misplaced Repts.Repts Telecopied to Nrc.Procedure for Distribution of Repts Revised1986-04-14014 April 1986 Ro:On 860312,discovered That LER 2-86-04 & LER 86-009 Not Submitted to Nrc.Caused by Misplaced Repts.Repts Telecopied to Nrc.Procedure for Distribution of Repts Revised BECO-86-016, Partially Withheld Security Event Rept:On 860215 Security Officer Appeared to Be Asleep at Post at Vital Area Penetration.Unathorized Entry of Vital Area Did Not Occurr. Security Officer Relieved of Duty & Suspended1986-02-20020 February 1986 Partially Withheld Security Event Rept:On 860215 Security Officer Appeared to Be Asleep at Post at Vital Area Penetration.Unathorized Entry of Vital Area Did Not Occurr. Security Officer Relieved of Duty & Suspended BECO-85-220, Partially Withheld Security Event Rept:On 851204 Vertical Pipe Chase Not Locked.Lock Removed When Surveys Indicated Radiation Level Below Requirement for Locked High Radiation Level.Pipe Chase Will Be Secured1985-12-0909 December 1985 Partially Withheld Security Event Rept:On 851204 Vertical Pipe Chase Not Locked.Lock Removed When Surveys Indicated Radiation Level Below Requirement for Locked High Radiation Level.Pipe Chase Will Be Secured AECM-84-0204, Special Rept 84-017/0:on 840304,Fire Doors 1A401 & OC219 Blocked Open to Support Maint Activities.Fire Watches Established Until Doors Restored1984-04-0606 April 1984 Special Rept 84-017/0:on 840304,Fire Doors 1A401 & OC219 Blocked Open to Support Maint Activities.Fire Watches Established Until Doors Restored ML20082P6541983-12-0505 December 1983 Telecopy RO 50-83/20-01T:on 831202,review of Ultrasonic Test Data Obtained During Current Refuel Outage Revealed Circumferential Linear Indication in Heat Affected Zone of Weld 02B-S9.Further Info Expected within 14 Days ML20198H3691983-11-14014 November 1983 Ro:On 831003,results of as-found Tests Indicated Crosby Main Steam Relief Valves Had Lift Points Exceeding Tech Spec Limits.Valves Disassembled & Rebuilt by Mfg ML20078J8531983-10-12012 October 1983 Telecopy Ro:On 831011,during Performance of Ultrasonic Insp of Cleanup Sys Piping,Crack Indication Discovered in Heat Affected Zone of Weld 12S-S27 of Line 2-1202-6A.Further Info to Be Provided within 14 Days ML20105D2431983-06-24024 June 1983 Special Rept:Five Individuals Found to Have Received Radiation in Excess of 10CFR20.101 Limits W/O Required Documentation.Caused by computer-based Sys Feature Allowing Use of Outdated Info & Personnel Error.Procedures Revised ML20137G4501981-03-24024 March 1981 Ro:During walk-through of Operator Training Program, O-ring Seal of Filter Holder Found Not Seated Properly Causing Partial Bypass of Filter for Air Sucked Into instrument.Filter-in Lock Adjusted ML20071F0861980-09-25025 September 1980 Ro:On 800912,sample Analysis Taken from Hydrazine Addition Tank Indicated Sodium Chloride in Tank.Anonymous Telcon Indicated Salt May Have Been Added Prior to Labor Strike by Unknown Persons ML20086D5141978-01-0606 January 1978 Telecopy Ro:On 780105,discovered That One of Two Nuclear Engineering Co Model B3-1 Shipping Casks Provided w/1-inch Diameter Lid Bolts Rather than 1-1/4 Inch Size Specified in Certificate of Compliance 6058 ML20086D5201977-12-14014 December 1977 Telecopy Ro:Heating Steam Coil Leak in Reactor Bldg Ventilation Supply Unit V-AH-4A Resulted in Freezing of Condensate at Inlet to Unit & Subsequent Inoperability of Associated Secondary Containment Isolation Dampers ML20086D5371977-10-14014 October 1977 Telecopy Ro:Insp of Internal Torus Catwalk Support Structure Revealed That Catwalk Mitered Sections Not All Attached to Horizontal Catwalk Support Plates in Some Manner.Attachment Locations Will Be Upgraded ML20086D5501977-10-13013 October 1977 Telecopy Ro:On 771012,local Leak Rate Testing of MSIV AO-2-80A & Nitrogen Instrument Air Sys Isolation Valve CV-7436 Indicated That Leakage Exceeded Tech Spec Acceptance Criteria.Cause Under Investigation ML20086D5541977-10-0505 October 1977 Telecopy Ro:On 771004,local Leak Rate Testing of HPCI Sys Discharge Isolation Check Valve HPCI-9 Indicated That Leakage Exceeded Tech Spec Acceptance Criteria.Cause Under Investigation ML20086D5571977-09-29029 September 1977 Telecopy Ro:On 770929,local Leak Rate Testing of Core Spray Inboard Isolation Check Valve AO-14-13A Indicated That Leakage Exceeded Tech Spec Acceptance Criteria.Cause Under Investigation ML20086D5611977-09-14014 September 1977 Telecopy Ro:On 770913,local Leak Rate Testing of Core Spray Inboard Isolation Check Valve AO 14-13B Indicated That Leakage Exceeded Tech Spec Acceptance Criteria.Related Event on 770914 ML20086D5671977-09-12012 September 1977 Telecopy Ro:Main Steam Drain Isolation Valve MD 2373 & Main Steam Outboard Isolation Valve AO 2-86A Exceeded Tech Spec Acceptance Criteria for Local Leak Rate Tests ML20086D6421977-07-11011 July 1977 Telecopy Ro:On 770709,determined That Recombiner Sys a Offgas Flow Control Valve PCV 7489A Could Be Opened W/ Controlling Solenoid Valve Deenergized.Valve Held from Svc Pending Investigation ML20137G4461977-06-23023 June 1977 Ro:On 770621,radioactive Source Containing 200 Mci Cs-137 Recovered from Brine Well 33.Incident Described in ML20086F0801977-06-0606 June 1977 Ro:On 770506,plant Iodine & Particulate Release Rate Exceeded 4% of Facility Tech Spec Averaged Over Second Calendar Quarter of 1977.Caused by Fuel Perforations Coupled W/End of Cycle Testing & Reactor Coolant & Steam Leaks ML20084S1401977-05-13013 May 1977 Ro:On 770512,unit Experienced Sudden Turbine Control Valve Opening Resulting in Feedwater Flow Increase & Reactor Scram from APRM flux.Short-term Reactivity Increase Corresponding to Reactor Period of Less than 5s Experienced ML20084S1531977-05-0909 May 1977 Ro:On 770507,station Experienced Momentary Short Period of Less than 5s During Shutdown Margin Demonstration.Similar Experience Occurred on 770504.Addl Info Will Be Submitted in RO 50-254/77-23 ML20086D6911977-03-0202 March 1977 Telecopy Ro:On 770301,torus Water Vol Found to Be Slightly Below Min Vol Established by Tech Specs.Water Vol Restored to Normal Operating Level ML20086D7031977-02-24024 February 1977 Telecopy Ro:On 770223,while Withdrawing in-sequence Control Rod to Bring Reactor Critical,Reactor Period of Less than 5 Obtained ML20084S1901977-02-17017 February 1977 Telecopy Ro:On 770217,info Received by Station Indicated That MAPLHGR Limit Curves Given by Tech Specs Shall Be Additionally Lowered.Reduction Resulted from Review of ECCS Analysis.Maplhgr Curves Lowered Effective 770217 ML20084S2041977-01-18018 January 1977 Telecopy Ro:On 770118,info Received by Station Indicated That MAPLHGR Limit Curves Shall Be Lowered.Reduction Resulted from Review of ECCS Analysis.Curves Lowered ML20084S3501977-01-0404 January 1977 RO-50-254/76-37:on 761205,limit for Having No More than 2 Ci Activity in Radwaste Tank Farm in 24h Exceeded. Caused by Deterioration of Effectiveness of Radwaste Sys to Perform as Designed.Radwaste Sys Being Updated ML20084S3551976-12-30030 December 1976 RO 50-254/76-36:on 761202,cooling Water Suction Header Common to Both RHR Containment Cooling Loop 1A & Diesel Generator 1 Cooling Water Pump Airlocked.Caused by Procedure Inadequacy.Maint Procedures Will Be Revised ML20084S2861976-12-28028 December 1976 RO 50-254/76-38:on 761215,GE Notified Util That NRC Discovered Errors in Code Inputs to ECCS App K Analysis, Caused by GE Incorrectly Applying Data for ECCS App K Analysis.Maplhgr Curves Reduced by 4% ML20084S3611976-12-16016 December 1976 RO 50-254/76-35:on 761203,discovered Discrepancy Between Tech Spec & Nedo 20360 Rod Worth Minimizer Operable Rated Power.Orders Written in Daily Order Book Requiring Rod Worth Minimizer Operability Below 20% ML20084S3391976-12-16016 December 1976 Ro:On 761215,preliminary Info Received by Station Indicated That MAPLHGR Curves Should Be Lowered by 4%.Change Resulted from Review of ECCS Analysis.Curves Lowered ML20086F4181976-12-0909 December 1976 RO Re Plant Iodine & Particulate Release Rate Exceeding 4% of Tech Spec 3.8.C.2 Averaged Over Fourth Calendar Quarter 1976.Caused by Leaks in Reactor Water Cleanup Sys.Leaks Repaired & Equipment Modified to Reduce Leakage ML20084S3701976-12-0303 December 1976 Ro:On 761203,info Received Indicated That Rod Worth Minimizer (RWM) Operability Requirements Should Be Changed from 10% to Below 20% Rated Power.Caused by Review of Rod Drop Accident Analysis ML20084S3791976-11-22022 November 1976 Updated RO 50-254/76-33:on 761029,repairs to RCIC Pump Consisted of Rebuilding Pump Casing & Installing New Rotary Element.Pump Reassembled & Repairs Completed by 761111.Welds on Piping Acceptable ML20084S3771976-11-12012 November 1976 RO 50-254.76-34-on 761104,electromatic Relief Valves 1-203-3C & 1-203-3E Failed to Open When Actuated from Control Room.Caused by Excessive Steam Leakage Into Area Below Valve Disc.Investigation in Progress W/Manufacturer ML20084S3941976-11-10010 November 1976 RO 50-254/76-33:on 761029,while Performing RCIC Sys Pump Operability Surveillance,Discovered That Pump Could Not Achieve Flow & Pressure Required.Caused by Two of Five Stages Being Severely Damaged.Pump Being Rebuilt ML20084S5421976-10-30030 October 1976 Updated RO 50-254/76-26:on 760803,rod Worth Minimizer Not Operable for Withdrawal of First Twelve Control Rods to Fully Withdrawn Position While in Startup Mode.Caused by Burned Out Wire Runs on Relay Board.Software Modified ML20070J8681976-10-20020 October 1976 RO 76-13:on 760916,normal Boric Acid Makeup to Vol Control Tank Could Not Be Accomplished Due to Plugging of Chemical & Vol Control Sys Line 1-inch-CH-56-152.Cause Unknown.Line Will Be Inspected for Indications of Solidification 1997-07-22 Category:TEXT-SAFETY REPORT MONTHYEARML20217A9931999-09-30030 September 1999
[Table view]NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data SVP-99-204, Monthly Operating Repts for Sept 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers ML20212J0501999-09-21021 September 1999 Safety Evaluation Re Licensee Implementation Program to Resolve USI A-46 at Plant,Per GL 87-02,Suppl 1 SVP-99-179, Monthly Operating Repts for Aug 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20210L8661999-08-0202 August 1999 Safety Evaluation Accepting License 60-day Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Movs SVP-99-155, Monthly Operating Repts for July 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With SVP-99-148, Monthly Operating Repts for June 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML20195K1481999-06-16016 June 1999 Safety Evaluation Authorizing Relief Request RV-23A for Duration of Current 10 Yr IST Interval on Basis That Compliance with Code Requirements Would Result in Hardship Without Compensating Increase in Level of Quality & Safety SVP-99-123, Monthly Operating Repts for May 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20195B2591999-05-19019 May 1999 Rev 66a to CE-1-A,consisting of Proposed Changes to QAP for Dnps,Qcs,Znps,Lcs,Byron & Braidwood Stations SVP-99-104, Monthly Operating Repts for Apr 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With SVP-99-102, Summary Rept of Changes,Tests & Experiments Completed, Covering Period 990201-0430. with1999-04-30030 April 1999 Summary Rept of Changes,Tests & Experiments Completed, Covering Period 990201-0430. with ML20205Q5291999-04-16016 April 1999 SER Concluding That Quad Cities Nuclear Power Station,Unit 1,can Be Safely Operated for Next Fuel Cycle with Weld O2BS-F4 in Current Condition Because Structural Integrity of Weld Will Be Maintained ML20205J6011999-04-0707 April 1999 Safety Evaluation Accepting Proposed Merger of Calenergy Co, Inc & Midamerican Holdings Co for Quad Cities Nuclear Power Station,Units 1 & 2 SVP-99-071, Monthly Operating Repts for Mar 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With1999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20205C5671999-03-19019 March 1999 Simulator Four-Yr Certification Rept ML20207D2341999-03-0101 March 1999 Post Outage (90 Day) Summary Rept, for ISI Exams & Repair/Replacement Activities Conducted 981207-1205 ML20204B1571999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Quad Cities,Units 1 & 2.With SVP-99-021, Quarterly Summary SER of Changes,Tests & Experiments Completed, Covering Period of 981101-990131,IAW 10CFR50.59 & 10CFR50.71(e).With1999-01-31031 January 1999 Quarterly Summary SER of Changes,Tests & Experiments Completed, Covering Period of 981101-990131,IAW 10CFR50.59 & 10CFR50.71(e).With SVP-99-007, Monthly Operating Repts for Dec 1998 for Quad Cities Nuclear Power Station,Units 1 & 2,IAW GL 97-02 & TS 6.9.With1998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Quad Cities Nuclear Power Station,Units 1 & 2,IAW GL 97-02 & TS 6.9.With ML20205D1311998-12-31031 December 1998 1998 Decommissioning Funding Status Rept for Yr Ending 981231 for Quad Cities Nuclear Power Station,Units 1 & 2 ML20205M7061998-12-31031 December 1998 Unicom Corp 1998 Summary Annual Rept. with SVP-98-364, Monthly Operating Repts for Nov 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With1998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20196G1241998-11-30030 November 1998 COLR for Quad Cities Unit 1 Cycle 16 ML20196D9651998-11-30030 November 1998 Safety Evaluation Supporting Relief Requests CR-21 & CR-24, Respectively.Relief Request CR-23,proposed Alternative May Be Authorized,Per 10CFR50.55a & Relief Request CR-22 Was Withdrawn by Licensee ML20196C8731998-11-30030 November 1998 Rev 0 to GE-NE-B13-01980-30-1, Fracture Mechanics Evaluation on Observed Indications at Two Welds in Recirculation Piping of Quad Cities,Unit 1 Station ML20196C8391998-11-30030 November 1998 Rev 0 to GE-NE-B13-01980-030-2, Assessment of Crack Growth Rates Applicable to Induction Heating Stress Improvement (IHSI) Recirculation Piping in Quad Cities Unit 1 ML20196A9761998-11-20020 November 1998 Safety Evaluation Re Licensee 180-day Response to GL 95-07, Thermal Binding of Safety-Related Power-operated Gate Valves ML20196A4191998-11-19019 November 1998 Safety Evaluation Accepting QA TR CE-1-A,Rev 66 Re Changes in Independent & Onsite Review Organization by Creating NSRB SVP-98-346, Monthly Operating Repts for Oct 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With1998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With SVP-98-358, Summary Rept of Changes,Tests & Experiments Completed, Including SEs Covering Period on 980716-1031.With1998-10-31031 October 1998 Summary Rept of Changes,Tests & Experiments Completed, Including SEs Covering Period on 980716-1031.With SVP-98-326, Monthly Operating Repts for Sept 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With1998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Quad Cities Nuclear Power Station,Units 1 & 2.With ML20153D0191998-09-18018 September 1998 Part 21 Rept Re Defect in Gap Conductance Analyses for co- Resident BWR Fuel.Initially Reported on 980917.Corrective Analyses Performed Demonstrating That Current Operating Limits Bounding from BOC to Cycle Exposure of 8 Gwd/Mtu ML20153C6771998-09-17017 September 1998 Part 21 Rept Re Defect Relative to MCPR Operating Limits as Impacted by Gap Conductance of co-resident BWR Fuel at Facilities.Operating Limit for LaSalle Unit 2 & Quad Cities Unit 2 Will Be Revised as Listed ML20151T2711998-09-0404 September 1998 Safety Evaluation Accepting Licensee Response to NRC Bulletin 95-002 ML20151Y7261998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Quad Cities Nuclear Power Station ML20237E2331998-08-21021 August 1998 Revised Pages of Section 20 of Rev 66 to CE-1-A, QA Topical Rept ML20237A6251998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Quad Cities Nuclear Power Station,Unit 1 & 2 ML20151Y7301998-07-31031 July 1998 Revised MOR for Jul 1998 for Quad Cities Nuclear Power Station,Units 1 & 2 SVP-98-328, Summary Rept of Changes,Tests & Experiments Completed, Including SEs Covering Period of 971001-980715,per 10CFR50.59 & 10CFR50.71(e).With1998-07-15015 July 1998 Summary Rept of Changes,Tests & Experiments Completed, Including SEs Covering Period of 971001-980715,per 10CFR50.59 & 10CFR50.71(e).With SVP-98-249, Monthly Operating Repts for June 1998 for Quad Cities Nuclear Power Station,Units 1 & 21998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Quad Cities Nuclear Power Station,Units 1 & 2 SVP-98-215, Monthly Operating Repts for May 1998 for Quad Cities Nuclear Power Station Units 1 & 21998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Quad Cities Nuclear Power Station Units 1 & 2 ML20247N6281998-05-19019 May 1998 Rev 2 to COLR for Quad Cities Unit 2 Cycle 15 ML20216C0561998-04-30030 April 1998 Safe Shutdown Rept for Quad Cities Station,Units 1 & 2, Vols 1 & 2.W/22 Oversize Figures SVP-98-176, Monthly Operating Repts for Apr 1998 for Quad Cities Nuclear Power Station,Units 1 & 21998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Quad Cities Nuclear Power Station,Units 1 & 2 ML20217D0281998-04-22022 April 1998 Part 21 Rept Re Additive Constants Used in MCPR Determination for Siemens ATRIUM-9B Fuel by Core Monitoring Sys Were Found to Be non-conservative.SPC Personnel Notified All Customers w/ATRIUM-9B Lead Test Assemblies ML20217G3951998-04-0808 April 1998 TS 3/4.8.F Snubber Functional Testing Scope Quad Cities Unit 2 TS (Safety-Related) Snubber Population 129 Snubbers SVP-98-128, Monthly Operating Repts for Mar 1998 for Quad Cities Nuclear Station Units 1 & 21998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Quad Cities Nuclear Station Units 1 & 2 1999-09-30 |
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REFERENCE QUAD CITY NUCLEAR POWER STATION DPR29 APPENDIX A SECTION 1.0.A.2 AT 1230 AM ON 11-15-72 WITH THE REACTER AT 90 PER CENT POWER MSIV l-203-2D WOULD NOT CHECK PROPERLY USING THE TEST CIRCUIT LOAD WAS RENEWED IN ORDER TO TEST FULL CLOSURE OF THE VALVES AND TO CLOSE THE OTHER IN LINES MSIV IF NECESSARY.
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