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Category:SAFETY EVALUATION REPORT--LICENSING & RELATED ISSUES
MONTHYEARML20217B4471999-10-0707 October 1999 Safety Evaluation Supporting Amends 159 & 150 to Licenses NPF-10 & NPF-15,respectively ML20211R0571999-09-0909 September 1999 Safety Evaluation Supporting Amends 158 & 149 to Licenses NPF-10 & NPF-15,respectively ML20212A2391999-09-0707 September 1999 Safety Evaluation Supporting Amends 157 & 148 to Licenses NPF-10 & NPF-15,respectively ML20211N0511999-09-0303 September 1999 SER Approving Exemption from Certain Requirements of 10CFR50.44 & 10CFR50 App A,General Design Criterion 41 to Remove Requirements from Hydrogen Control Systems from SONGS Units 2 & 3 Design Basis ML20211H8621999-08-23023 August 1999 Safety Evaluation Accepting Licensee Requests for Relief RR-E-2-03 - RR-E-2-08 from Exam Requirements of Applicable ASME Code,Section Xi,For First Containment ISI Interval ML20211E9441999-08-19019 August 1999 Safety Evaluation Supporting Amends 156 & 147 to Licenses NPF-10 & NPF-15,respectively ML20211F2211999-08-19019 August 1999 Safety Evaluation Supporting Amends 155 & 146 to Licenses NPF-10 & NPF-15,respectively ML20209G8991999-07-12012 July 1999 Safety Evaluation Supporting Amends 154 & 145 to Licenses NPF-10 & NPF-15,respectively ML20207A0211999-05-13013 May 1999 Safety Evaluation Supporting Amends 153 & 144 to Licenses NPF-10 & NPF-15,respectively ML20206G6561999-04-27027 April 1999 SER Accepting Proposed Exemption from 10CFR50.71(e)(4) for SONGS Units 2 & 3 ML20206D1461999-04-26026 April 1999 Safety Evaluation Supporting Amend 152 to License NPF-10 ML20205Q6221999-04-19019 April 1999 Safety Evaluation Authorizing Proposed Alternative to Use Wire Penetrameters for ISI Radiography in Place of ASME Code Requirement ML20205R0371999-04-16016 April 1999 SER Approving Proposed Deviation from Approved Fire Protection Program Incorporating Technical Requirements of 10CFR50,App R,Section III.0 That Applies to RCP Oil Fill Piping ML20205N2691999-04-0909 April 1999 Safety Evaluation Supporting Amends 151 & 143 to Licenses NPF-10 & NPF-15,respectively ML20203J1981999-02-12012 February 1999 Safety Evaluation Supporting Amends 149 & 141 to Licenses NPF-10 & NPF-15,respectively ML20203J1131999-02-12012 February 1999 Safety Evaluation Supporting Amends 150 & 142 to Licenses NPF-10 & NPF-15,respectively NUREG-0800, Safety Evaluation Supporting Amends 148 & 140 to Licenses NPF-10 & NPF-15,respectively1999-02-0909 February 1999 Safety Evaluation Supporting Amends 148 & 140 to Licenses NPF-10 & NPF-15,respectively ML20206N6281998-12-16016 December 1998 Safety Evaluation Supporting Amends 145 & 137 to Licenses NPF-10 & NPF-15,respectively ML20196A6161998-11-23023 November 1998 Safety Evaluation Supporting Amend 136 to License NPF-15 ML20154B7211998-10-0101 October 1998 Safety Evaluation Approving Licensee Request to Implement Alternatives Contained in Code Case N-546 for Current Interval at Songs,Units 2 & 3 Until Code Case Approved by Ref in Reg Guide 1.147 ML20197D0161998-09-0909 September 1998 Safety Evaluation Supporting Amends 141 & 133 to Licenses NPF-10 & NPF-15,respectively ML20239A1431998-08-26026 August 1998 Safety Evaluation Supporting Amends 140 & 132 to Licenses NPF-10 & NPF-15,respectively ML20249C7361998-06-19019 June 1998 Safety Evaluation Supporting Amends 139 & 131 to Licenses NPF-10 & NPF-15,respectively ML20203E7301998-02-17017 February 1998 SER Accepting 980105 Request to Use Mechanical Nozzle Seal Assembly as Alternate Repair Method,Per 10CFR50.55a(a)(3)(1) for Plant,Units 2 & 3 ML20202J1111997-12-0303 December 1997 Safety Evaluation Supporting Amends 137 & 129 to Licenses NPF-10 & NPF-15,respectively ML20210T0631997-08-29029 August 1997 Safety Evaluation Approving Application Re Proposed Restructuring of Enova Corp,Parent Company of San Diego Gas & Electric Co by Establishment of Holding Company W/Pacific Enterprises ML20134C9261996-10-0303 October 1996 Safety Evaluation Supporting Amends 131 & 120 to Licenses NPF-10 & NPF-15 ML20128L7231996-10-0303 October 1996 Safety Evaluation Supporting Amend 158 to License DPR-13 ML20094J5991995-11-0202 November 1995 Safety Evaluation Supporting Amends 126 & 115 to Licenses NPF-10 & NPF-15,respectively ML20091R3581995-08-23023 August 1995 Safety Evaluation Supporting Amends 124 & 113 to Licenses NPF-10 & NPF-15,respectively ML20086U0231995-07-26026 July 1995 Safety Evaluation Supporting Amends 123 & 112 to Licenses NPF-10 & NPF-15,respectively ML20086M2951995-07-14014 July 1995 Safety Evaluation Supporting Amends 120 & 109 to Licenses NPF-10 & NPF-15,respectively ML20084F6591995-05-17017 May 1995 Safety Evaluation Supporting Amends 119 & 108 to Licenses NPF-10 & NPF-15,respectively ML20081J7151995-03-17017 March 1995 Safety Evaluation Supporting Amends 118 & 107 to Licenses NPF-10 & NPF-15,respectively ML20080P3171995-02-28028 February 1995 Safety Evaluation Supporting Amends 117 & 106 to Licenses NPF-10 & NPF-15,respectively ML20078Q4101995-02-13013 February 1995 Safety Evaluation Supporting Amends 115 & 104 to Licenses NPF-10 & NPF-15,respectively ML20076M3671994-10-27027 October 1994 Safety Evaluation Supporting Amends 113 & 102 to Licenses NPF-10 & NPF-15,respectively ML20063F1671994-02-0404 February 1994 Safety Evaluation Supporting Amends 110 & 99 to Licenses NPF-10 & NPF-15,respectively ML20058B1241993-11-19019 November 1993 Safety Evaluation Accepting Proposal to Leak Rate Test SI Tank Outlet Check Valves by Using Leak Test Method Described in OM-10,Paragraph 4.2.2.3(c) ML20057G3071993-10-18018 October 1993 Safety Evaluation Granting Licensee 930616 Relief Request B-12 Re Hydrostatic Testing of Certain Welds in 4 Inch Line from Main Steam Header to Auxiliary Feedwater Pump ML20056E2441993-08-0303 August 1993 Safety Evaluation Supporting Amends 108 & 97 to Licenses NPF-10 & NPF-15,respectively ML20056E0851993-08-0202 August 1993 Safety Evaluation Accepting Licensee 890308,910301 & 911217 Responses to NRC Bulletin 88-011 Re C-E Owners Group Program for Evaluation of Pressurizer Surge Line Thermal Stratification ML20056D6421993-07-27027 July 1993 SER Approving Licensee 930305 Relief Requests B-10,B-11 & Code Case N-496 ML20128P8401993-02-17017 February 1993 Safety Evaluation Supporting Amend 153 to License DPR-13 ML20125A4341992-12-0303 December 1992 Safety Evaluation Accepting Alternative Exam Methods Per 10CFR50.55a(a)(3)(i) & Addl Info Re Auxiliary Feedwater Sys Lube Oil Cooling,Per ISI Relief Requests B-7,B-8 & B-9 & Code Case N-481 ML20085K3981991-10-0909 October 1991 Safety Evaluation Supporting Amends 100 & 89 to Licenses NPF-10 & NPF-15,respectively ML20081K1821991-06-17017 June 1991 Safety Evaluation Supporting Amends 95 & 85 to Licenses NPF-10 & NPF-15,respectively ML20081F2171991-06-0303 June 1991 Safety Evaluation Supporting Amends 94 & 84 to Licenses NPF-10 & NPF-15,respectively ML20247N3731989-08-30030 August 1989 Safety Evaluation Supporting Amends 76 & 64 to Licenses NPF-10 & NPF-15 ML20246N4321989-08-25025 August 1989 Safety Evaluation Supporting Corrected Amends 74 & 62 to Licenses NPF-10 & NPF-15,respectively 1999-09-09
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217B4471999-10-0707 October 1999 Safety Evaluation Supporting Amends 159 & 150 to Licenses NPF-10 & NPF-15,respectively ML20217E3381999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Songs,Units 2 & 3 05000361/LER-1999-005-01, :on 990831,loss of Physical Separation in Control Room,Occurred.Caused by Personnel Error.Creacus Train a Was Returned to Standby on 9908311999-09-23023 September 1999
- on 990831,loss of Physical Separation in Control Room,Occurred.Caused by Personnel Error.Creacus Train a Was Returned to Standby on 990831
ML20212A1471999-09-13013 September 1999 Special Rept:On 990904,condenser Monitor Was Declared Inoperable.Difficulties Encountered During Component Replacement Precluded SCE from Restoring Monitor to Service within 72 H.Alternate Method of Monitoring Was Established ML20211R0571999-09-0909 September 1999 Safety Evaluation Supporting Amends 158 & 149 to Licenses NPF-10 & NPF-15,respectively ML20212A2391999-09-0707 September 1999 Safety Evaluation Supporting Amends 157 & 148 to Licenses NPF-10 & NPF-15,respectively ML20211N0511999-09-0303 September 1999 SER Approving Exemption from Certain Requirements of 10CFR50.44 & 10CFR50 App A,General Design Criterion 41 to Remove Requirements from Hydrogen Control Systems from SONGS Units 2 & 3 Design Basis 05000206/LER-1999-001-02, :on 990808,unattended Security Weapon Was Discovered Inside Pa.Caused by Posted Security Officer Falling Asleep.Officer Was Relieved of Duties,Pa Access Was Removed & Officer Was Placed on Investigatory Suspension1999-08-31031 August 1999
- on 990808,unattended Security Weapon Was Discovered Inside Pa.Caused by Posted Security Officer Falling Asleep.Officer Was Relieved of Duties,Pa Access Was Removed & Officer Was Placed on Investigatory Suspension
ML20211Q8201999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Songs,Units 2 & 3. with ML20211H8621999-08-23023 August 1999 Safety Evaluation Accepting Licensee Requests for Relief RR-E-2-03 - RR-E-2-08 from Exam Requirements of Applicable ASME Code,Section Xi,For First Containment ISI Interval ML20211E9441999-08-19019 August 1999 Safety Evaluation Supporting Amends 156 & 147 to Licenses NPF-10 & NPF-15,respectively ML20211F2211999-08-19019 August 1999 Safety Evaluation Supporting Amends 155 & 146 to Licenses NPF-10 & NPF-15,respectively ML20210P4791999-08-11011 August 1999 COLR Cycle 10 Songs,Unit 3 ML20210P4731999-08-11011 August 1999 COLR Cycle 10 Songs,Unit 2 05000361/LER-1999-004-01, :on 990708,automatic Tgis Actuation Occurred. Caused by Small Leak in Suction Side of Tgis Train a Sample Pump.Small Leak Repaired1999-08-0606 August 1999
- on 990708,automatic Tgis Actuation Occurred. Caused by Small Leak in Suction Side of Tgis Train a Sample Pump.Small Leak Repaired
ML20210Q6521999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Songs,Units 2 & 3 ML20210L2771999-07-30030 July 1999 SONGS Unit 3 ISI Summary Rept 2nd Interval,2nd Period Cycle 10 Refueling Outage U3C10 Site Technical Services 05000362/LER-1999-005, :on 990630,discovered LTOP Sys Relief Valve Setpoint Was Higher than Allowed by Ts.Cause Indeterminate. Subject Valve Will Be Disassembled & Inspected to Determine Caused of High Setpoint.With1999-07-28028 July 1999
- on 990630,discovered LTOP Sys Relief Valve Setpoint Was Higher than Allowed by Ts.Cause Indeterminate. Subject Valve Will Be Disassembled & Inspected to Determine Caused of High Setpoint.With
05000362/LER-1999-006, :on 990623,EDG 3G003 Was Inadvertently Made Inoperable.Caused by Operators Aligning EDG to Inoperable Automatic Voltage Regulator.Licensee Will Revise Process of Locating Tags.With1999-07-26026 July 1999
- on 990623,EDG 3G003 Was Inadvertently Made Inoperable.Caused by Operators Aligning EDG to Inoperable Automatic Voltage Regulator.Licensee Will Revise Process of Locating Tags.With
ML20209G8991999-07-12012 July 1999 Safety Evaluation Supporting Amends 154 & 145 to Licenses NPF-10 & NPF-15,respectively ML20209C9281999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Songs,Units 2 & 3. with 05000362/LER-1999-003-01, :on 990513,reactor Manually Tripped Due to Loss of Main Feedwater.Caused by Open Relay Contact in Output of Feedwater Regulation Control Sys.Faulty Relay Was Replaced1999-06-11011 June 1999
- on 990513,reactor Manually Tripped Due to Loss of Main Feedwater.Caused by Open Relay Contact in Output of Feedwater Regulation Control Sys.Faulty Relay Was Replaced
05000362/LER-1999-004, :on 990515,reactor Manually Tripped Due to Feedwater Control Valve Opening.Caused by Faulty Valve Positioner.Faulty Positioner Was Replaced1999-06-11011 June 1999
- on 990515,reactor Manually Tripped Due to Feedwater Control Valve Opening.Caused by Faulty Valve Positioner.Faulty Positioner Was Replaced
ML20195D3061999-06-0202 June 1999 Safety Evaluation of TR SCE-9801-P, Reload Analysis Methodology for San Onofre Nuclear Generating Station,Units 2 & 3. Rept Acceptable ML20195H5491999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Songs,Units 2 & 3 05000362/LER-1999-002-01, :on 990328,RWST Outlet Isolation Valve Failed to Open After Being Closed for Testing.Caused by Degradation of Valve.Rwst Oulet Valve Was Repaired.With1999-05-20020 May 1999
- on 990328,RWST Outlet Isolation Valve Failed to Open After Being Closed for Testing.Caused by Degradation of Valve.Rwst Oulet Valve Was Repaired.With
ML20207A0211999-05-13013 May 1999 Safety Evaluation Supporting Amends 153 & 144 to Licenses NPF-10 & NPF-15,respectively ML20196L3221999-05-11011 May 1999 SONGS Unit 2 ISI Summary Rept 2nd Interval,2nd Period Cycle-10 Refueling Outage ML20206H2611999-05-0505 May 1999 Part 21 Rept Re Defect Found in Potter & Brumfield Relays. Sixteen Relays Supplied in Lot 913501 by Vendor as Commercial Grade Items.Caused by Insufficient Contact Pad Welding.Relays Replaced with New Relays ML20206S7281999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Songs,Units 2 & 3 ML20206G6561999-04-27027 April 1999 SER Accepting Proposed Exemption from 10CFR50.71(e)(4) for SONGS Units 2 & 3 ML20206D1461999-04-26026 April 1999 Safety Evaluation Supporting Amend 152 to License NPF-10 ML20205Q6221999-04-19019 April 1999 Safety Evaluation Authorizing Proposed Alternative to Use Wire Penetrameters for ISI Radiography in Place of ASME Code Requirement ML20205R0371999-04-16016 April 1999 SER Approving Proposed Deviation from Approved Fire Protection Program Incorporating Technical Requirements of 10CFR50,App R,Section III.0 That Applies to RCP Oil Fill Piping ML20205N2691999-04-0909 April 1999 Safety Evaluation Supporting Amends 151 & 143 to Licenses NPF-10 & NPF-15,respectively ML20205G2611999-04-0101 April 1999 Special Rept:On 990328,3RT-7865 Was Removed from Service. Monitor Is Scheduled to Be Returned to Service Prior to Mode 4 Entry (Early May 1999) Which Will Exceed 72 H Allowed by LCS 3.3.102.Alternate Method of Monitoring Will Be Used ML20205Q0981999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Songs,Units 2 & 3 05000362/LER-1999-001-01, :on 990211,TS 3.0.3 Entered Due to Both Chilled Water Trains Being Inoperable.Warm Main Condenser Discharged Water Diverted in Salt Water Cooling (Swc)(Bs) Intake.With1999-03-12012 March 1999
- on 990211,TS 3.0.3 Entered Due to Both Chilled Water Trains Being Inoperable.Warm Main Condenser Discharged Water Diverted in Salt Water Cooling (Swc)(Bs) Intake.With
05000361/LER-1999-002, :on 990208,pressurizer Safety Valves Were Above TS Limit.Caused by Setpoint Drift.Sce Submitted License Amend Application on 980904 Requesting Tolerence Be Changed to +3/-2%.With1999-03-10010 March 1999
- on 990208,pressurizer Safety Valves Were Above TS Limit.Caused by Setpoint Drift.Sce Submitted License Amend Application on 980904 Requesting Tolerence Be Changed to +3/-2%.With
05000361/LER-1999-001, :on 990201,automatic Start of EDG Was Noted. Caused by Workers Closing Breaker 2A0418 by Discharging Closing Springs.Operators Restored SDC in Approx 26 Minutes. with1999-03-0303 March 1999
- on 990201,automatic Start of EDG Was Noted. Caused by Workers Closing Breaker 2A0418 by Discharging Closing Springs.Operators Restored SDC in Approx 26 Minutes. with
ML20204F8101999-02-28028 February 1999 Monthly Operating Repts for Songs,Units 2 & 3.With ML20203J1131999-02-12012 February 1999 Safety Evaluation Supporting Amends 150 & 142 to Licenses NPF-10 & NPF-15,respectively ML20203J1981999-02-12012 February 1999 Safety Evaluation Supporting Amends 149 & 141 to Licenses NPF-10 & NPF-15,respectively NUREG-0800, Safety Evaluation Supporting Amends 148 & 140 to Licenses NPF-10 & NPF-15,respectively1999-02-0909 February 1999 Safety Evaluation Supporting Amends 148 & 140 to Licenses NPF-10 & NPF-15,respectively ML20202F7041999-01-21021 January 1999 Special Rept:On 990106,SCE Began to Modify 2RT-7865.2RT-7865 to Allow Monitor to Provide Input to New Radiation Monitoring Data Acquisition Sys.Monitor Found to Exceeds 72 H Allowed Bt LCS 3.3.102.Alternate Monitoring Established ML20206H2101998-12-31031 December 1998 SCE 1998 Annual Rept ML20199F0771998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Songs,Units 2 & 3 ML20206N6281998-12-16016 December 1998 Safety Evaluation Supporting Amends 145 & 137 to Licenses NPF-10 & NPF-15,respectively ML20198A6731998-12-11011 December 1998 Special Rept:On 981124,meteorological Sys Wind Direction Sensor Was Observed to Be Inoperable.Caused by Loss of Communication from Tower to Cr.Sensor Was Replaced & Sys Was Declared Operable on 981204 ML20196D8901998-11-30030 November 1998 Non-proprietary Reload Analysis Methodology for Songs,Units 2 & 3 1999-09-09
[Table view] |
Text
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-t UNITEl> STATES ja j
NUCLEAR REGULATORY COMMISSION o1 t
WASHINGTON, D.C. 20555-0001 o
.... 4 SAFETY EVALUATION BY THE OFFICE OF NUCLEAR REACTOR REGULATION RELATED TO AMENDMENT NO.155 TO FACILITY OPERATING LICENSE NO. NPF-10 AND AMENDMENT NO.146 TO FACILITY OPERATING LICENSE NO. NPF-15 SOUTHERN CALIFORNIA EDISON COMPANY SAN DIEGO GAS AND ELECTRIC COMPANY l
THE CITY OF RIVERSIDE. CALIFORNIA 1
THE CITY OF ANAHEIM. CALIFORNIA l
SAN ONOFRE NUCLEAR GENERATING STATION. UNITS 2 AND 3 DOCKET NOS. 50-361 AND 50-362 l
l
1.0 INTRODUCTION
The current tech'nical specificailen (TS) 3.4.9, Pressurizer, for the San Onofre Nuclear Generating Station (SONGS) Units 2 and 3, requires that a maximum pressurizer water volume l
of 900 cubic feet be maintained during Modes 1,2, and 3. This maximum water volume is i
l approximately equivalent to 61% water level. By letter dated December 19,1997, as supplemented June 1,1998, and May 13,1999, the Southern California Edison Cornpany (the licensee) submitted license amendments to request changes to TS 3.4.9 to reduce the i
maximum ' pressurizer water volume for pressurizer operability. The maximum water volume would also be revised to a percent pressurizer water level of 57%.
The licensee stated that this change is necessary to be consistent with a revised pressurizer level instrumentation total loop uncertainty (TLU) which was developed for the replacement transmitters at SONGS Units 2 and 3. The licensee provided the results of its evaluation and reanalysis of certain events that are sensitive to pressurizer water level to support its proposed changes. The licensee also proposed chang'es to the Updated Final Safety Analysis Report (UFSAR) to incorporate the changes and revised safety analyses.
The licensee's letters dated June 1,1998, and May 13,1999, provided clarifications and additional information that were within the scope of the original Federa/ Register notice and did
- not change the U.S. Nuclear Regulatory Commission (NRC) staff's initial proposed no
. significant hazards consideration determination (63 FR 14488).
2.0 BACKGROUND
. The licensee replaced the pressurizer level transmitter instrumentation in the 1995 Cycle 8 refueling outage to improve pressurizer level instrument loop accuracy under loss-of-coolant accident (LOCA) conditions. As part of the design change package for the instrument replacement, a new TLU was calculated by using the transmitter performance specifications for 9908300275 990819 j
. DR ADOcK 0 31
. the replacement transmitters. The revised calculation used the same methodology as the original calculation in accordance whh the applicable rev;sion to SCE Standard JS-123-103C, which follows the guidance in ISA-S67.04-1994, "Setpoints for Nuclear Safety. Related instrumentation Used in Nuclear Power Plants," and Regulatory Guide 1.105 Rev 2,
" Instrument Setpoint for Safety-Related Systems," February 1986. The SCE TLU setpoint program was reviewed and found acceptable by the NRC staff in February 1991.
3.0 EVALUATION (1)
Pressurizer Water Level Setpoint The current maximum pressurizer water volume is approximately equivalent to 61% water level.
The licensee performed an analysis to determine an acceptable maximum water volume taking
- o into account the TLU resulting from the use of the replacement transmitters. The pressurizer level instrument TLU recalculation yielded a control room indicated pressurizer level maximum TLU value of 3.9%. Incorporation of this TLU value requires restricting pressurizer level to 57%, which is less than the current TS 3.4.9 value of 900 cubic feet (which corresponds to a level of approximately 61%). With a TLU value of 4%, the control room pressurizer level indicator value should be reduced to 57% in order to provide margin between the selpoint and the safety analyses that were done at 61% of pressurizer level. The normal full power pressurizer level for plant normal operation is approximately 53%. The setpoint for pressurizer water level of 57% is conservative and provides necessary margin based on the 4% TLU and therefore, is acceptable. Also, administrative controls have been implemented to ensure that the pressurizer level does not exceed 57% during normal power operation.
(2)
Reanalysis for UFSAR Chapter 15 Events The revised TLU value of 3.9% requires restricting the pressurizer level to 57% (i.e.,
approximately 860 cubic feet which is less than the current TS 3.4.9 value of 900 cubic feet) such that the assumed initial pressurizer level of 61% in the UFSAR will remain valid.
The licensee has provided the results of its reanalysis for UFSAR Chapter 15 events that are sensitive to pressurizer water level including the chemical and volume control system (CVCS) malfunction and feedwater system pipe breaks (FSPB) assuming an initial pressurizer water level of 61%.
The licensee has provided its evaluation to demonstrate that the consequences of an inadvertent actuation of the emergency core cooling system (ECCS) is bounded by the CVCS malfunction event. The design shutoff head for the high pressme safety injection (HPSI) pumps was established at a value significantly below the minimum operating pressure'for the reactor coolant system (RCS). There will be no water injected into the RCS through the HPSI pumps for the inadvertent ECCS operation event. Therefore, the injection flow to RCS during the inadvertent ECCS operation is the same as for the CVCS malfunction event, the flow from all three charging pumps. Also, the inadvertent ECCS operation will switch over the suction of the charging pumps from the volume control tank (VCT) to the boric acid makeup tank or refueling water storage tank with higher boron concentration. The higher boron concentration water will inject negative reactivity into tr.e core and cause decrease of power and coolant temperature and reduce the increase in RCS inventory caused by the operation of all charging pumps. Equivalent injection flow for both the scenarion and higher boron concentration in the m
. inadvertent ECCS actuation scenario demonstrate that the consequences of an inadvertent ECCS actuation is bounded by the CVCS malfunction event.
(a)
CVCS malfunction event The licensee performed a reanalysis of the CVCS malfunction event using an NRC-approved CESEC-Ill computer code. In its reanalysis, the licensee assumed the proposed 61%
pressurizer water level and pressurizer level control system failure which could initiate operation of all three charging pumps and isolate letdown. In this event, various pressurizer level and pressure controlindications and alarms are available to alert the operator of the event. The licensee stated that depending on the failure mode, the pressurizer level control system may not automatically terminate and manual operator action would be required. Presently, UFSAR Chapter 15 analysis of this event assumes 30-minute operator action. Based on the reanalysis with the proposed 61% pressurizer water level, the licensee determined that operator action within 15 minutes would terminate the additional charging flow and the pressurizer will not become water solid. The revised analysis indicates that 15 minutes following the event, the pressurizer water volume is 1100 cubic feet which is below the maximum pressurizer water volume of 1465 cubic feet at which the pressurizer would become solid (UFSAR Chapter 15, Figure 15.5-7).
In order to support the reduction in the operator action time required for this event from 30 minutes to 15 minutes, the licensee simulated this event on the plant simulator. Using criteria contained in NRC Information Notice 97-78, " Crediting of Operator Actions in Place of Automatic Actions and Modifications of Operator Actions, including Response Times," the NRC staff evaluated the licensee's proposed operator action times. In response to the NRC staff's request dated September 22,1998, the licensee provided additional information including emergency operating procedures to demonstrate that the assumed 15 minutes operator actions to terminate this event is achievable in its May 13,1999, response, the licensee described that the CVCS malfunction event (e.g., failure of the controlling pressurizer level transmitter) would initiate erroneous indications of low pressurizer level. Pressurizer level would actually be at the normal prograra level, but the control system would "think" level was low as a result of the instrument failure. The contrei system would autcmatically try to r'.all the pressurizer to its programmed level, which would cause the actual level to ;r.:rcae above normal. The licensee indicated that 15 rninutes would be adequate time for operators to take the necessary actions to detect and correct the CVCS malfunction event.
In its December 19,1997, submittal, the licensee stated that " Operators recognized and terminated this event on the Simulator in approximately 5 minutes." In its May 13,1999, submittal, the licensee further stated that "The simulator evaluation was performed with a normal full crew complement of licensed Operators with a mix of experience....The CVCS Malfunction event is a routine training task, which is run for all SONGS licensed operating crews on a minimum once per two year frequency. All crews have been evaluated on the simulator and have performed satisfactorily." The licensee further indicated that all crews were naive to the event before being tested, hence they had no advanced knowledge that they would be tested on this event. All operator actions required to mitigate the event are taken from the control room and are performed from a control board on one section of the control boards.
Only one operator is required to perform the actions, with a second operator cross-checking his/her actions. The change proposed by the licensee did not require any modification to procedures and thus, no new training was required. In addition, the licensee discussed the t
. consequences of operators failing to perform the required actions in the time available in its May 13,1999, submittal. They indicated that, if the operators did not take the required actions in the 15 minutes allowed, then the pressurizer would slowly fill and the VCT level would drop.
The control room would receive an additional alarm on low VCT level. Eventually, the pressurizer begins going solid and the RCS pressure begins to rise. At the high pressurizer pressure trip setpoint, the reactor will trip, resulting in a volume reductic ' in the RCS. The reduced volume would create a steam bubble in the pressurizer, promphng the operators to correct the charging / letdown mismatch. The licensee has demonstrated using NRC-approved Code and methodology that operator action within 15 rninutes would prevent the pressurizer becoming water solid. Further, the licensee performed a successful simulator evaluation and showed that operator action within 15 minutes to terminate the event is achievable. Based on its review, the NRC staff finds the reduced operator action time to be adequate for correcting the additional charging flow and terminating the CVCS malfunction event prior to filling the pressurizer, and is therefore, acceptable.
(b)
FSPB Event in the reanalysis of the FSPP event, the licensee assumed 30 minutes operator action time for accident mitigation which is consistent with the previous analysis. In its May 13,1999, submittal, the licensee indicated that the FSPB reanalysis "did not result in any adverse char ges to the expected plant response or operator response for this response. In addition, no emergency procedare changes were required to accommodate the reanalysis of this event."
The results of this analysis indicate that the peak pressurizer volume is 1396 cubic feet which is less than 1465.7 cubic feet to ensure that the pressurizer is not water solid and no water-flow through the PSV. The peak RCS pressure is less than 120% of its design pressure which is the acceptance criteria used for this event at SONGS and, therefore, the NRC staff finds the reanalysis to be acceptable.
4.0
SUMMARY
The licensee's reanalysis of the proposed pressurizer water level has demonstrated that the RCS pressure remains below 110% of its design pressure, the peak pressurizer water volume of 1100 cubic feet is less than 1465.7 cubic feet (which is the maximum volume to prevent we.ter entering into the pressurizer relief valve), and the pressurizer will not be water solid and no water will flow through the pressurizer safety valves (PSV). The licensee's proposed TS changes provide sufficient margin between the setpoint and assumed accident analysis limits.
The licensee has also demonstrated by simulator evaluation that operator action within 15 minutes to identify and mitigate the CVCS malfunction event is achievable. Therefore, the NRC staff finds the proposed change to TS 3.4.9 to revise the maximum pressurizer water level from 61% to 57% to be acceptable.
5.0 STATE CONSULTATION
in accordance with the Commission's regulations, the California State official was notified of the proposed issuance of the amendments. The State official had no comments.
i
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6.0 ENVIRONMENTAL CONSIDERATION
The amendments change a requirement with respect to the installation or use of a facility component located within the restricted area as defined in 10 CFR Part 20. The NRC staff has determined that the amendments involve no significant increase in the amounts and no significant change in the types of any effluents that may be released offsite, and that there is no significant increase in individual or cumulative occupational radiation exposure. The Commission has previously issued a proposed finding that the amendments involve no significant hazards consideration, and there has been no public c.omment on such finding (63 FR 14488). Accordingly, the amendments meet the eligibility criteria for categorical exclusion set forth in 10 CFR 51.22(c)(9). Pursuant to 10 CFR 51.22(b) no environmental impact statement or environmental assessment need be prepared in connection with the issuance of the amendments.
7.0 CONCLUSION
The Commission has concluded, based on the considerations discussed above, that (1) there is reasonable assurance that the health and safety of the public will not be <. dangered by operation in the proposed manner, (2) such activities will be conducted in compliance with the Commission's regulations, and (3) the issuance of the amendments will not be inimical to the common defense and security or to the health and safety of the public.
1 Principal Contributors: C. Liang J. Bongarra
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Date: August 19, 1999 1
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