ML20210S886

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Insp Repts 50-245/97-202,50-336/97-202 & 50-423/97-202 on 970520-0721.Violations Noted.Major Areas Inspected: Operations,Maint,Engineering & Plant Support Re Performance in Emergency Preparedness & Control of FP Activities
ML20210S886
Person / Time
Site: Millstone  Dominion icon.png
Issue date: 08/29/1997
From:
NRC (Affiliation Not Assigned)
To:
Shared Package
ML20210S864 List:
References
50-245-97-202, 50-336-97-202, 50-423-97-202, NUDOCS 9709120179
Download: ML20210S886 (92)


See also: IR 05000245/1997202

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U.S. NUCLEAR REOULATORY COMMISSION

] OFFICE OF NUCLEAR REACTOR F.EGULATION

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8PECIAL PROJECTS OFFICE

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, Docket Nos.: 50 245 50 330 50 423

Report Nos.: 97 202 97 202 97 202

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License Nos.: DPR 21 DPR 65 NPF 49

Licensee: Northeast Nuclear Energy Company

P. O. Box 120

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Waterford, CT 06385

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Facility: Millstone Nuclear Power Station, Units 1,2, and 3

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Inspection at: Waterford, CT

Dates: May 20,1997 July 21,1997

inspectors
T. A. Easlick, Senior Resident inspector Unit 1

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D. P. Beaulleu, Senior Resident inspector, Unit 2

A. C. Corne, Senior Resident inspector, Unit 3

A. L. Burritt, Resident inspector, Unit 1

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R. J. Arrighi, Resident inspector, Unit 3 .

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J. W. Andersen, Project Manager, Unit 3

R. S. Bhatia, Reactor Engineer

J. E. Carrasco, Reactor Engineer

D. A. Dempsey, Reactor Engineer

1 J. T. Furia, Senior Radiation Specialist

I- L. M. Harrison, Reactor Engirieer

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J. H. Lusher, Health Physicist

D. T. Moy, Reactor Engineer

L. L. Scholl, Reactor EnD i neer

M. A Blamonte, NRR

R, Pelton, NRR

, M. Kotzalas, NRR

J. B. O'Brien, NRR

P. Berler, NRC Contractor

J. C. Higgins, NRC Contractor

S. M. Wong, NRC Contractor

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' Approved by: Jacque P. Durr, Chief

Inspections, Special Projects Office, NRR

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9709120179 970829

DR ADOCK 050002 5

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TABLE OECONTEN1B

E X EC UTlW S U M M ARY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . iv

U1.1 Operations ..................................................1 l

U101 Conduct of Operations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1 '

U 1.Il M ain t o n ' n c e . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 5

U1 M3 Maintenance Procedures and Documentation ............... 5  :

U1 M8 Miscellaneous Maintenance lasues . . . . . . . . . . . . . . . . . . . . . . . 6

U 1 Ill E nginee ring . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 7

U1 El Conduct of Engineering . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 7

U1 E3 Engineering Procedures and Documentation ................ 9

U2.1 Operations .................................................10

U2 01 Conduct of Operations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 10

U2 03 Operations Procedures and Documentation . . . . . . . . . . . . . . . . 12 ,

U 2.ll M aint enanc e . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 13

U2 M8 Miscellaneous Maintenance issues . . . . . . . . . . . . . . . . . . . . . . 13

U 2.lli Enginee rin g . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 15

U2 E8 Miscellaneous Engineering issues . . . . . . . . . . . . . . . . . . . . . . . 15

U3.1 Operations .................................................22  !

U3 01 Conduct of Operations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 22

U3 07 Quality Assurance in Operations . . . . . . . . . . . . . . . . . . . . . . . 24

U3 08 Miscellaneous Operations issues (92700) . . . . . . . . . . . . . . . . . 26 -

U 3.li M ainte nance . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 2 9

U3 M1 Conduct of Maintenance . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 29

U3 M3 Maintenance Procedures and Documentation ..............34

U3 M4 Maintenance Staff Knowledge and Performance .......,,,,.41

U3 M8 Miscellaneous Maintenance issues . . . . . . . . . . . . . . . . . . . . . . 43

U 3.Ill Engineering . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 4 7

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U3 E2 Engineering Support of Facilities and Equipment ............ 47

U3 E3 Engineering Procedures and Documentation ............... 49 .

U3 E8 Miscellaneous Engineering issues . . . . . . . . . . . . . . . . . . . . . . . 57

IV Plant Support .................................................66

R1 Radiological Protection and Chemistry Controls . . . . . . . . . . . . . 66

R5 Staff Training and Qualification in Radiological Protection and

Chemistry Controls ................................,69

P4 Staff Knowledge and Performance in Emergency Preparedness . . 69

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P8 Miscellaneous Emergency Preparedness issues . . . . . . . . . . . . . 74

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F1 Control of Fire Protection Activities . . . . . . . . . . . . . . . . . . . . . 74

F4 Fire Protection Staff Knowledge and Perforrnance . . . . . . . . . . . 70

F7 Quality Assurance in Fire Protection Activities . . . . . . . . . . . . . . 77

V. M an agement M ee ting s . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 7 8

X1 Exit Meeting Summary . . . . . . . . . . . . . . . . . . . . . . . . . . . . , . 78

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EXECUTIVE SUMMARY

Millstone Nuclear Power Station

Combined Inspection 245/97 202; 336/97 202;423/97 202

Operations

  • At Unit 1, recent changes within the operations department require the shif t

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managers to report to the assistant operations manager, a now reporting

requirement and a change from the previous responsibility of the assistant.

Following a review of the concerns raised by the inspector, operations management

has taken steps to ensure that the roles of the operations manager and the assistant

operation manager are clearly defined, including the new reporting structure.

(U1.01.2)

  • During a review of the restoration process for the Unit 1 service water system, the

operations staff was not initially using a new operation departmentalinstruction,1-

OPS 0.32 " Millstone Unit 1 System Readiness Review," which would have

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enhanced the restoration by providing a formal process for returning a system to an

l operable or available status. Additionally, an Individual assigned as the overall

i management lead for the evolution did not function in that capacity. The reactor

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operator assigned to control and monitor the restoration activities from the control

room, did an excellent job coordinating the step by step activities with the field

operators, and kept the unit supervisor informed of each step of the restoration.

There was also good coordination between operations, the test engineer, and the

management test lead, The service water normal operating procedures did not

contain appropriate guidance fer determining normal system operating parameters

following the system restoration. (U1.01.3)

  • Overall, operator performance at Unit 2 was good in evaluating shutdown risk by

maintaining awareness of plant conditions and equipment availability. In particular,

on July 14,1997, operators exhibited a good questioning attitude regardng the

planned removal from service of the spent fuel pool area ventilation supply f an.

(U2.01.1)

  • At Unit 2, the licensee initiated effort in removing 10 non-conservative technical

specification clarifications from the technical requirements manual was good.

(U2.01.2)

  • At Unit 2, the total backlog of 780 condition reports (CRs) that are greater than 120

days old indicates that timeliness for completing corrective actions continues to be a

concern. The new management planned to demonstrate a higher standard by

dispositioning newly generated CRs in a timely manner while establishing a plan for

working off the CR backlog that existed when they arrived. However, the backlog

of 200 CRs greater than 120 days old that were generated in 1997 indicates that

the new management is also ineffective in addressing the corrective action

timeliness issue which is considered a significant weakness. (U2.01.3)

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  • At Unit 2, although the licensee determined that there would be sufficient net .

positive suction head available to the reactor building closed cooling water (RBCCW)

pumps, the f ailure to evaluate and proceduralize the level band that operators should

control RBCCW surge tank level was considered a weakness. (U2.03.1)

e Although the loss of spent fuel pool cooling at Unit 3 was not significant from a

de ign basis or safety related viewpoint, it was significant not only with respect to

the adequacy of current operational and configuration control but also

management's expectation for operational standards. The former appears to have

been addressed by the licensee's Event Review Team (ERT) report, while the latter

was in the process of being assessed at the close of this inspection period. The

NRC will continue to monitor the licensee's assessment of this event,its generic

implications on the adequacy of other programs, and the implementation of effective

corrective actions. (U3.01.1)

e At Unit 3 the Nuclear Oversight organization appeared to be actively involved in

quality assurance and assessment activities directed toward effective corrective

actions for identified problem areas and program enhancements to improve future

operations. The initiatives reviewed this period attest to a more active role by

Nuclear Oversight in dealing with line performance. However, while the routine OA

and oversight reports document cognizance of the areas which represent the most

significant challenges to Iruproving performance, the ability of Nuclear Oversight to

effect positive changes has not yet been fully demonstrated. (U3.07.1)

e NRC review of several LERs established that while the licensee's operational

activities were proper evolutions, literal compliance with the plant TS had not been

maintained. Based on the appropriate corrective actions and the low safety

significance of the issues, these licensee identified and corrected violations are

being treated as non cited violations. The closure of the LERs does not address the

generic concern for TS compliance. A review of LERs issued as of April 1996

revealed that there have been a number of LERs that have dealt with TS compliance

problems relating to questionabic interpretations. This area is of current interest for

further NRC review. (U3.08.1)

Maintenance

e A review was conducted of the preparation and planning activities associated with

the retrieval of a hatch bolt from the Unit 1 standby liquid control (SBLC) tank.

Nuclear oversight (performance evaluation (PE) group) became aware of the plans to

retrieve a hatch bolt from the SBLC tank and raised a number of questions

concerning the uen of an automated work order in place of a special procedure. The

lack of clear guidance on when a special procedure is required resulted in significant

resistance from the line personnel to PE concerns about using a work order to

perform the work. The decision was made by plant management to develop a

special procedure for the bolt retrieval. (U1.M3.1)

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l. * At Unit 1, the licensee's corrective actions were appropriate to address concerns

with the adequacy of procedural guidelines for determining quality control

involvement in safety related work activities. This closes a previous unresolved

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item concerning this issue. As feedback to the package development process, the

- open item package had most of the requisite information. -(U1.M8.1) -

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e Contrary to Unit 2 technical specifications, during preparations for a surveillance,

operators mistakenly aligned all three high pressure injections to the reactor cooiant

system. This licensee identified concern was characterized as a non cited violation.

(U2.M8.2)

e A comprehensive self assessment of the Millstone 3 IST program documented broad

scope problems that constituted a violation of 10 CFR 50.55alf). The licensee-

- identified violation was not cited because the causes for the program f ailures were

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being addressed adequately, and individual test discrepaneles were being tracked

and resolved appropriately.- (U3.M1.2)

-In accordance with Code requirements. A followup item was opened regarding the

potential that relief valve testing to the valve " simmer" point may be

, nonconservative. For other Code Class 2 and 3 relief valves, set pressure

adjustments made to account for differences in bench test and normal operating

ambient temperatures need to be justified by test per OM 1 (U3.M3.1)

e Unit 3 acceptance criteria established for IST of safety related pumps met or I

exceeded Code requirements. Equipmerit or procedure changeu will be needed to

meet Code requirements for repentability of test reference values, or NRC relief to

use broader tolerance bands will be needed. (U3.M3.2)

e The Unit 3 power operated valve exercise tests met or exceeded Code

requirements, and use of the motor power monitor diagnostic system was

commendable. Nonintrusive testing of check valves also was noteworthy, but more

documentation was needed to meet GL 89-04 requirements. Additional manual

valves may need to be added to the IST program, even if their safety functions are

passive. (U3.M3.3)

e A review of ARCOR coating application work orders revealed that on six separate

occasions the recoat window was exceeded. The collective procedural

noncompliance indicates both an individual and departmental control performance

problem in that it demonstrates a low standard for following procedures and a lack

of management oversight for this critical evolution. This f ailure to follow procedures

is a violation of technical specifications. (U3.M1.4)

e An apparent violation was identified for Units 1,2, and 3 pertaining to the

Mplementation of the systematic approach to training for technical training

p igrams We found the overallimplementation of these programs to be generally

inadequate to ensure continued qualification of technical and non licensed personnel

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to perform in plant work. Specifically, the licensee f ailed to properly evaluate .

trainee mastery of tasks and conduct training program effectiveness evaluations.

(U3.M4.1)

Engineering

cubicles f ailed to identify discrepancies with pipe supports in the areas. The

licensee's initiative to access and inspect normally inaccessible areas is an important

mechanism to monitor the material condition of the plant. However, clear

expectations need to be developed concerning who conducts these inspections and

how the inspections are to be performed and documented. This issue is unresolved

pending NRC review of the corrective actions and completion of the preventative

maintenance program development for normally inaccessible areas. (U1.E1.1)

e The testing of the Unit 1 emergency diesel generator (EDG) was well controlled with

an appropriate level of station management involvement. As issues arose they were

assessed and handhd in accordance with station procedures and policies. At the

end of the inspection period, the EDG testing was continuing. With respect to the

preparation and procedure development, plant management's intervention early in

the process resulted in improvements in the overall restoration process for the

diesel. (U1.E1.2)

e Unit 1 has approximately 38,000 components currently in the production

maintenance management system (PMMS) database. As part of the NU

Performance Enhancement Program (PEP) in the early 1990's, a contractor to NU

reviewed these components and through the material, equipment, and parts lists

(MEPL) program downgraded about 1450 from safety related (SR) to non safety-

related (NSR) in late 1994. It was later determined that this downgrade process had

not been properly performed. Thus about 350 of the downgraded components were

reverted back to SR on an emergency MEPL evaluation. Unit 1 currently has plans

to redo all the system level MEPLs before plant startup, but due to lack of resources

has not begun this effort yet. As outage work is ongoing in Unit 1, individual

component and part MEPL evaluations are being performed as necessary to support

the work and issuance of parts. (U1.E3.1)

  • Since 1993 at Unit 2, numerous licensee events reports, adverse condition reports,

and NRC enforcement actions have discussed concerns whether air operated valve

actuator springs are adjusted to apply sufficient force for the valve to perform its

intended safety function. Escalated Enforcement item (EEI) 50 336/96 20125 was

created to address inadequate licensee corrective action regarding the issue. NRC

review of the eel revealed that licensee corrective actions continue to be inadequate

in that the scope of the review was limited to containment isolation valves rather

than all safety related air operated valves. This eel remains open. (U2.E8.1)

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  • At Unit 2, the licensee has satisfactorily resolved the potential for leakage of the fire

protection piping joints in the vital switchgear rooms during a seismic event by

replacing the Vitaulic couplings on the piping with welded flanges. (U2 E8.4)

  • Review of the MEPL program implementation at Unit 2 indicated that two unit-

specific items require followup inspectiom (1)In 1994,998 components were

downgraded from safety related (Category 1) to non safety related. After a number

of these downgrades were found to be inappropriate,in 1995 and 1990 all of the

downgt,aded components were upgraded back to safety related. The licensee

reviewed the work performed while the components were downgraded and found 7

examples where non safety related parts were installed. The licensee is currently

dispositioning these items; and (2) The licensee is also in the process of evaluating

whether parts classified as ' Undetermined' and non safety related which have no

MEPL have been inappropriately installed. (U2.E8.5)

non safety related was found to be acceptable. However, concerns regarding

recurrent inservice testing f ailures of these check valves is considered unresolved.

(U2.E8.6)

  • Four issues were identified during a review of the Millstone MEPL program. These

items pertained to 1) potential for non safety related parts to be installed in safety

related components,2) potential f ailure to assess the impact of downgrading a

component in the quality assurance program,3) potential not to considor normal

operations and abnormal operational occurrences as part of safety related

classifications, and 4) an incomplete PMMS database. (U3.E3.1)

  • Unit 3 has approximately 60,000 components in the PMMS database, of which

about 19,000 are safety-related and 3,000 are augmented quality. During PEP

reviews a number of components were originally identified for downgrade, however

this action was stopped in Unit 3 beforo being implemented as a result of lessons

learned on Units 1 and 2. In 1996, Unit 3 began MEPL bill of material evaluations

for all safety related components that have ever had any work performed on them.

As part of this effort, whenever non safety related or undetermined parts are

reclassified to safety related, a full work history is performed to ensure acceptable

quality of parts in these components. Five additionalissues were identified during a

review of specific MEPL components and the CVCS system. (U3.E3.3 and E3.4)

  • The inspector reviewed a Unit 3 adverse condition report that addresses the RHR

heat exchanger bolting susceptible to boric acid attack and the actions taken by the

licensee to remove an unsecured structural member installed above safety related

components and to prevent future !nstallations of this nature. The inspector

concluded that the licensee's corrective and preventive actions were adequate.

(U3.E8.1 and E8.2)

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e An apparent violation was identified for Unit 3 pertaining to recirculation spray .

l system design errors which resulted in operation outside the design basis and

system inoperability. (U3.E8.4)

Plant Support

  • The licensee has created a framework at Units 1 and 2 to implement an effective

ALARA program. The lack of an effective work control and planning process.

together with the absence of a unit ALARA committee still exists at Unit 3.

(IV.R12)

e Unit 1 management sponsored plant " supervisors walk arounds" in order to raise the

health physics awareness of supervisors observing day to day work activities in the '

field. The walk around tour was extremely informstive arid provided good insights

into radiological waste reduction. The initiative was well roceived by the Unit 1

supervisors and will be expanded to included additional areas such as Security and

Nuclear Oversight. (IV.R5.1)

e Significant improvement was found regarding oversight and organization of the fire

protection program. Although planned corrective actions were found to be

comprehensive, further NRC review is necessary to verify implementation. (IV.F1.1)

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e The fire brigade functioned effectively during the observed fire drill and was well

prepared to combat fires. Significant improvements were demonstrated by the

Training and Site Fire Protection departments, including robust command and

control, teamwork, support provided by Operations, and a good drill critique.

(IV.F4.1)

e An improvement in the quality of assessment provided for the fire protection

program was noted. (IV.F7.1)

e Overall, performance of the Site Emergency Response Organization (SERO) was

good. Simulated events were accurately diagnosed, proper mitigation actions were

performed, emergency declarations were timely and accurate, and offsite agencies

were notified promptly. Protective action recommendations to the State of

Connecticut were correct and timely. Additionally, the information presented during

the management meeting was informative and indicates that the corrective

measures being taken are appropriate. No exercise weaknesses, safety concerns, or

violations of NRC requirements were observed. (IV.P4.1)

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Report Details

Summarv of Unit i Status

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Unit 1 remained in an extended outage for the duration of the inspection period. The

licensee continues to implement configuration management program (CMP) activities,

j engineering reviews, and docketed correspondence assessments to verify compilance with

the established design and licensing basis of the unit. The successful completion of these

activities is required by NRC order prior to restart of the unit While there is a reduction of

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restart activities at Unit 1, through the end of this year, configuration management program

activitled continue. Following a major reduction.of the contractor work force for the CMP

project, approximately 35 plant personnel from operations, engineering, and maintenance

were temporarily assigned work on the CMP,

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U101 Conduct of Operations l

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01.1 General Comments (71707)

i Using Inspection Procedure 71707, the inspectors conducted frequent reviews of ongoing

i plant operations During this period the inspectors reviewed activities associated with the . ,

! restoration of the service water system and the emergency diesel generator, both of which

i were being restored following an extended outage for maintenance and plant modification

- work. There was a significant effort on the part of the Unit 1 staff to return these systems

safety and efficiently to an available status for shutdown risk considerations. This effort is

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discussed in detailin Sections U1.01.3 and U1.E1.2 below.

! 01.2 Ooerations Denartment Command and Control

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a. insoection Scoce (717071

l The position of assistant operations manager was eliminated following the implementation

of the recovery organization at Unit 1 in October 1996. Subsequently, the recovery team

re instituted the position and required that the shif t managers report directly to the

. assistant operations manager. Currently, the operations manager holds a Unit 1 senior

i reactor operator (SRO) license, fulfilling the requirement of Technical Specification (TS)

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6.3.1.a., Facility Staff Qualifications. The inspector observed unit operations and

j conducted interviews with a number of shift managers in order to determine if there were

clear expectations for command and control within the department. This was particularly

Important since the shift managers report to the assistant operations manager and the

! operations manager holds the TS required SRO license.

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b. Observations and Findinos

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On June 26,1997, ths inspector informed the Director, Unit Operations that there

l appeared to be a problem with command and control within the Unit 1 operations

department. This was based on observing unit operations and interviews with a number of

shif t managers, who expressed a concern with the day to day direction for departmental  ;

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operation. There was confusion around the operations manager fulfilling the TS SRO

license requirement, and the role of the assistant operations manager they were now

required to report to. This was a new reporting requirement, and a change from the

previous responsibility of the assistant, which was more of an administrative position.

The Director, Unit Operations was unaware of the concerns of the shift managers. By the

end of June, the operations manager, at the request of the Director, interviewed each of

the shif t managers and confirmed that there was a problem in the operation department

with respect to command and control. The operations manager determined that some shif t

managers expressed a concern about the operations manager not being included in the

decision making process and policy making for the department. Some shift managers

complained of receiving contradicting direction in the simulator and during classroom

training, from the operations manager and the assistant operations manager Shift

managers were not clear on management's expectations, how they were communicated,

and the implications if they were not met.

in response to this concern, the operations department performed a "new reporting

relationship review," and discussed all of the issues and concerns identified by the

inspector and the operations manager, The Director, Unit Operation, operations manager,

assistant operations manager, and the five on shift shift managers were present for this

review. A plan was developed following the discussions, which included: 1) revising

Operations Manual,1 OM.3.1, to clearly define the role of assistant operations manger: 2)

solicit feedback from shif t managers routinely to determine if issues are being effectively

addressed; and 3) continue improving cornmunications to assure alignment within the

department.

The inspector conducted follow up interviews with the shift managers and received positive

comments about the new reporting relationship review," and the resolution of the issues.

The operations staff was responsive to the inspector's concems, performed their own

review, and arrived at an adequate solution to the problems. A condition report (CR M1-

971770) was initiated to document the concems and track the corrective actions,

c. Conclusion

Recent changes within the operations department required the shift managers to report to

the assistant operations manager, a new reporting requirement and a change from the

previous responsibility of the assistant, which was more of an administrative position.

Following concerns raised by the inspector, operations management has taken steps to

ensure that the roles of the operations manager and the assistant operation manager are

clearly defined, including the new reporting structure.

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01.3 Service Water Sv11em Restoration

a. inanection Scone (71707)

The inspector reviewed the restoration process for the service water system following an

extended maintenance outage. The restoration included the completion of special

procedure, SPROC 95126, ' Service Water System Outage (IPTE).* The special procedure

was required to establish plant conditions to support the maintenance of the service water

system piping to the reactor building closed cooling water heat exchangers and the turbine

building service water piping.

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b. Observation and Findings

During a review of the restoration process for the service water system, the inspector

determined that the operations staff was not using a new operation departmental

instruction,1 OPS 6.32 " Millstone Unit 1 System Readiness Review," which would have

enhanced the restoration process. This instruction was developed to define the process for

assessing and doeurnenting the restoration of a system and provide guidance on

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documenting and resolving discrepancies identified during the system walkdown process.

The instruction was developed in response to earlier NRC concerns with the lack of a

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methodology the returning aystems to service. The instruction provided a formal process

for returning a system to an operable or available status.

Operations management had formed a team to oversee the operations' portion of the

service water system restoration. Lacking guidance on how to accomplish this task, the

team choose to use the * equipment return to service" departmentalinstruction, which was

a two page instruction applicable to returning a piece of equipment to operable status.

Further inspection identified that a service water restoration plan had been developed,

which identified responsibilities for a project sponsor and departmentalleads from

operations, engineering, maintenance, and planning. The project sponsor was given the

responsibility of providing management oversight of the system restoration activities.

Discussions with the project sponsor, a maintenance manager, indicated that this person

was not aware of his overall responsibility as defined in the plan, but rather considered

himself a management support lead. He considered his responcibility to be the completion

of the physical work and turn over of the system to operations. While a restoration plan

was developed, it doesn't appear that it was implemented. A CR (M1971686) was -

initiated to document the lack of clearly defined roles and responsibilities, and the lack of

an identified point of contact to coordinate all the required activities to restore the system.

A meeting was held between operations and engineering department management to

assign responsibility for performing the specific steps within 1 OPS 6.32 Additionally, a

self assessment was conducted following the service water restoration to identify several

areas for improvement. The individuals involved in the upcoming emergency diesel

- generator (EDG) recovery activities were also present during the self-assessment meeting,

to gain some insight into the planned EDG recovery work. The self assessment

recommendations were documented in a CR (M1971723).

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The inspector observed the service water system recovery activities from the control room.

Pre start briefings were well coordinated and assignments and responsibilities were

discussed with the plant staff. A half hour into the evolution, the shif t manager identified

that the management test lead (MTL) was not on site, when he tried to contact the MTL

with a question concerning the system restoration. The shift manager suspended the

evolution until the MTL was on site. The restoration activities were controlled under

administrative procedure ACP OA 2,27, ' Infrequently Performed Test or Evolution (IPTE)."

While ACP OA 2,27 states that the MTL la responsible for continuous responsibility

(whether on sito or off site) for IPTE oversight, the shif t manager deterrnined that it was

appropriate for the MTL to be on site for the dynamic portion of the evolution.

Additionally, during this time nuclear oversight questioned the adequacy of termination

criteria in the restoration procedure. This issue was evaluated and SP 023.13A " Service

Water Pump Performance Test" was added to ensure that the service water system was

performing its intended function, once it was placed back in service. This later caused a

problem since test conditions specified in the performance test could not be met because

the test was normally performed during normal operating conditions. The restoration

activities resumed the following day.

Operations management assigned a reactor operator (RO) to control and monitor the

activities from the control room. The RO did an excellent job coordinating the step by step

activ!tles with the field operators via the radio, and keeping the unit supervisor Informed of

each step of the restoration. There was also good coordination between operations, the

test engineer, and the MTL, The evolution was also observed by the assistant operations

manager and nuclear oversight. Following the completion of the evolution the termination

criteria was again revised to remove the service water pump performance test and in its

place service water operating parameters such as pump amperes, vibration, and discharge

pressure were added to ensure that the system was operating properly. The inspector

noted that the service water system normal operating procedures did not contain

appropriate guidance for determining normal system operating parameters. This issue was

identified during the development of the termination criteria stated above. A CR (M197-

1713) was initiated to document this concern.

c. Conclusion

During a review of the restoration process for the service water system, the operations

staff was not initially using a new operation departmentalinstruction,1 OPS 6.32

" Millstone Unit 1 System Readiness Review," which would have enhanced the restoration

by providing a formal process for returning a system to an operable or available status.

Additionally, an individual assigned as the overall management lead for the evolution did

not function in that capacity. The reactor operator assigned to control and monitor the

activities from the control room did an excellent job coordinating the step-by step activities

with the field operators, and kept the unit supervisor informed of each step of the

restoration. There was also good coordination between operations, the test engineer, and

the management test lead. The inspector noted that the service water normal operating

procedures did not contain appropriate guidance for determining normal system operating

parameters following the system restoration.

- _ -- - - .- . . - - - . -

_ _ _ _ _ _ . _ _ _ _. _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _

.

.

.

5

U1.11 Mainianant

U1 M3 Maintenance Procedures and Documentation

M 3.1 Standbv Llould Control Tank

a. Insoection Scone _(02707)

The inspector reviewed the preparation and planning activities associated with the retrieval

of a hatch bolt from the standby liquid control (SDLC) tank. While sampling the SBLC tank

on June 19,1997, the threaded rod that holds the tank cover in place unscrewed and

dropped into the tank (CR M1971520).

!

b. Observations and Findinas

Unit 1 nuclear oversight (performance evaluation (PE) group) became aware of the plans to

retrieve a hatch bolt from the SBLC tank at the 6:30 morning work control meeting, on

June 24,1997. Af ter some discussion with the chemistry supervisor, it was apparent that j

the work was going to be performed under an automated work request (AWO),in a day or I

two, with no pre job briefing up to that point, no system engineering involvement, and no

nuclear oversight involvement. PE suggested that a meeting be set up to bring all

interested parties together and discuss the evolution. A number of questions were raised

by PE at that meeting concerning the use of an AWO in place of a special procedure,

foreign material exclusion (FME) control, material compatibility, and possible chemical

interactions between the contents of the SBLC tank and all equipment being used for

retrieving the hatch bolt.

Subsequent to the initial meeting, the inspector noted significant resistance from the line

personnel to PE concerns about using an AWO to perform the work. PE's concerns

included the f act that this was an infrequently performed activity. DC 1, * Administration

of Procedures and Forms," states that special procedures are prepared as necessary to

support infrequently performed activities which are not to be included in the permanent list

of station procedures. There were discussions about whether or not this activity was

infrequently performed, e.g., removing something from a tank. PE was concerned that

since this was a category 1, safety system, and the tank contained heater coils and air

spargers, special precautions were needed to address these issues, which would require

involvement by system engineering. The line personnelinsisted on using an AWO and PE

provided a large number of comments following a review of the draft AWO At that time,

the line planned to perform the work using a revised AWO, which inchaded PE's comments.

After continued dialogue between the line personnel and nuclear oversight that lasted

approximately two weeks, the decision was made to open the tank and determine the

exact scope of the recovery activities. The inspector observed the activity, which was

appropriately controlled, FME controls were in place. Following that activity, plant

management determined that a special procedure would be written, and work would be

performed in August 1997.

_ _ . _ _. . _ . _ _ _ _ _ _ _ _ _ _ _ _ _ - - _ _ _

c

.

6 , ,

c. Conclualon l

The inspector reviewed the preparation and planning activities associated with the retrieval

of a hatch bolt from the standby liquid control (SBLC) tank. Nuclear oversight

(performance evaluation (PE) group) became aware of the plans to retrieve a hatch bolt

from the SBLC tank and raised a number of questions concerning the use of an automated

work order in place of a special procedure. The lack of clear guidance on when a special '

procedure is sequired resulted in significant resistance from the line personnel to PE

concems about using a woik order to perform the work. The decision was made by plant

management to develop a special procedure for the bolt retrieval. *

U1 M8 Miscellaneous Maintenance issues

M8.1 (Closed) Unresolved item (URll 50 245/94 014 13; Qualitv Control involvement in

i

Safetv related Work Actlylijst (SIL 108 UPDATE)

a. insoection Scone 162707)

-

-

The inspectors reviewed the licensee's findings and corrective actions associated with the

,

.

determination of quality controlinvolvement in safety related work activities and for

l

determining when inspection hold points were required,

b. Dhagrvations and Findinas ,

i. The unresolved item concerned maintenance on EDG air start system solenoid-operated

valves (SOV). The maintenance was a rebuild activity and the inspector found that the

work was performed without a PORC approved procedure, and there was a violation issued

for that finding. In addition, the procedure in place at the time, ACP OA 2.02C, Work

Control, provided guidelines for determining quality controlinvolvement in safety related ,

work activities and for determining whether inspection hold points were required...The

planner's conclusion that no quality services department involvement was required for the

SOV maintenance appeared to have been consistant with those guidelines. At the time of i

the inspection, the inspector was concemed with the adequacy of those procedural

guidelines. Nuclear oversight needed to reevaluate the policies and guidelines set forth in f

ACP OA 2.02C A URI was initiated to document this concern,

The reevaluation was completed and the licensee implemented a new procedure, WP 8003,

" Unit 1 Work Package Planning," which included a step that provided definitive guidance -

on when work orders required a quality assurance (OA) review. The guidance was.-

= changed from listing six activities that need QA involvement, which is open to

interpretation, to a " management by exception" concept, listing the 23 activities that do

not require OA' involvement, with all others requiring a OA review. - Additionally, as part of

the recovery plan for nuclear oversight, two procedures were developed that gave nuclear

l . oversight ownership of the hold point program and responsibility for assigning hold points _

on all AW0s. A OC tech support group was established to provide this function, with all

l AW0s being reviewed by this group prior to implementation.

1

,

4

e- -N, , ,w----e" - - - - - ym~~ --

,, ,,s-w-s,-,r.e--s-,,,n,-e,e,e-v.wweem-m-

-

w----,-w -,-,N--~ .-w,r&~e,-,,w,-- , rw - - .-ms- vn,-y m, sm e m -r -'

-

._ _ _ _ _

, __ . _ . . _ _

.

'

7

c. Conclusions

. The NRC concluded that the licensee's corrective actions would address the adequacy of

procedural guidelines for determining quality control involvement in safety related work

activities. This item is closed. As feedback to the package development process, the

inspector concluded that the open item package had most of the requisite information,

however, the inspector needed to consult the preparer of the package to understand how

the information addreseed the issue. ,

.

Q1.lli Enoineering

U1 E1 Conduct of Engineering

E 1.1 A and B Reactor Water Cleanuo Svstem Filter Cubicles

a. Insoection Scone (375511

The inspector rev owed a video tape record of an inspection that was conducted in the A

and B reactor '.<ater cleanup (RWCU) system filter cubicles. On June 1617,1997, the A

and B RWCU filter entrance floor plugs were removed for an inspection of the areas. The

inspection was part of the licensee's program for entering normally inaccessible areas,

b Observations and Findings

The work activity was performed under an AWO with a system engineering sign off for the

completed inspections. A video tape record of the inspection was completed and the

inspector requested a copy for review. While reviewing the tape, the inspector noted an

object wedged between two pipes in a pipe sleeve in the 8 filter cubicle. The system

engineer was contacted and the inspector was informed that the discrepancy had not been

identified or documented in a condition report. Tt e inspector also reviewed the completed

AWO that stated that two pieces of wood and one pen were removed from the floor of the

'B' cubicle; no additional discrepancies were noted. The system manager, his supervisor,

and the inspector reviewed the video tape and identified some additional discrepancies of

the same type, wedges in pipe sleeves. A CR (M1971678) was initiated as a result of

that review to document the discrepancies and corrective actions, and an assignment was

added to the CR to determine why the initial inspection failed to identify the discrepancies. .

Discussions with the system manager rerponsiblo for developing a strategy for the

inspection of normally inaccessible areas, indicated that a prever.tive maintenance program

was being established to ensure that these areas are inspected on regular basis. All but

one of the sixteen areas designated as normally inaccessible at Unit 1, are inside structures

considered within the NRC Maintenance Rule 10 CFR 50.65, in-scope population.

Therefore, these areasi are subject to a structuralinspection to be conducted every two

refueling cycles to ensure compliance with the structural monitoring provisions of the

maintenance rule.

.

. .

.

4

8

'

c. Conclusions

The inspector concluded that the licensee's initiative to access and inspect normally

inaccessible areas is an important mechanism to monitor the material condition of the

plant. However, clear expectations need to be developed concerning who conducts these

inspections and how these inspections are to be performed and documented. This issue is

unresolved (URI 245/97 202 01) pending NRC review of the CR corrective actions and

completion of the PM program development.

E1.2 Emeroencv Diesel Generator Testina

e, insoection Scone (375B1)

The inspector reviewed the restoration process for the emergency diesel generator (EDG)

following maintenance and modification work.

i

b. Observations and Findinas

During a PORC meeting conducted on June 4,1997, four different special procedures were

proposed for the restoration of the EDG following maintenance and modification work. At

that point, plant management determined that the staff would need to perform a review of

all the EDG post maintenance testing, to identify any overlapping testing that was required

for the EDG restoration. This was needed to prevent duplication of the testing and provide

an efficient methodology to complete the required testing. A special procedure was

created following the review under administrative procedure ACP-Q'A 2,27, " Infrequently

Performed Test or Evolution (IPTE)," to encompass all the work required for restraation.

,_ The special procedure consisted of six phases including monitoring, testing, and data

gathering steps. The test included post maintenance and modification testing and limited

the number of EDG test starts by performing the testing in a logical, efficient manner.

The inspector observed the initial briefing for the test conducted on July 15,1997, by the

management test lead (MTL) and the test engineer, and found that it was comprehensive

and provided an good overview of the IPTE. The termination criteria and responsibilities for

plant personnel were explicitly stated. A number of issues that were raised at the briefing

and were reviewed and appropriately added to the procedure. For example, the reactor-

operator (RO) suggested adding a step to line up the in service systems to the S1 power

supply prior to the start of the test. This had been discussed during the briefing, but the

RO noted that it was not part of prerequisite steps in the IPTE.

The inspector noted that the lessons learned from the earlier service water restoration were

included in this evolution, including identifying a management lead individual responsible for

the oversight of the system restoration activities, and the use of 1 OPS 6.32 " Millstone

Unit 1 System Readiness Review."

_ _ _ - _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

. _ _ _ _ _ . .

.

. .

..

.

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9

c. Conclusions

The testing of the emergency diesel generator was well controlled with an appropriate level

of station management involvement. As issues arose, they were assessed and handled in

accordance with station procedures and policles. At the end of the inspection period, the

l EDG testing was continuing. With respect to the preparation and procedure development,

the inspector found that management's intervention early in the process resulted in

improvements in the overall restoration process for the diesel.

U1 E3 Engineering Procedures and Documentation

E3,1 Unit 1 MEPL Status Uodate

,

The overall site material, equipment, and parts lists (MEPL) program was reviewed;

comments and discussion that apply to all three units are provided in Section U3 E8.1.

This section provides Unit 1 specific discussions only.

Unit 1 has approximately 38,000 components currently in the production maintenance '

management system (PMMS) database. As part of the NU Performance Enhancement

Program (PEP) in the early 1990's, a contractor to NU reviewed these components and

I

through the MEPL pro 0 ram downgraded about 1450 from safety related (SR) to nc,n safety-

f related (NSR)in late 1994, it was later determined that this downgrade process had not

been properly performod. Thus about 350 of the downgraded components were reverted

back to SR on an emergency MEPL evaluation. The other 1100 were each given a full

MEPL evaluation with the following results. About 20% were converted back to SR and

the remaining 80% were determined to be appropriately downgrsded to NSR.

Unit 1 currently has plans to redo all the system level MEPLs before plant startup, but due

to lack of resources has not begun this effort yet. As outage work is ongoing in Unit 1,

'

individual component and part MEPL evaluations are being performed as necessary to

support the work and issuance of parts. Unit 1 has not decided on the level of MEPL

evaluations to be performed for component Bill of Materials (BOM) Currently, full BOMs

are not being completed even for components that are being worked on AWOs. Unit 1 is

performing full historical reviews of work history for components ur parts that are upgraded

from NSR to SR but not for items upgraded from Undetermined (U) to NSR.

-

,

.

Reoort Detalla -

Summarv of Unit 2 Stalus

Unit 2 entered the inspection period with the core off loaded. The unit was initially shut

down on February 20,1990, to address containment sump screen concerns and has

remained shut down to address an NRC Demand for Information (10 CFR 50.54(f)) letter

requiring an assertion by the licensee that future operations are con' ducted in accordance

with the regulations, the license, and the Final Safety Analysis Report.

U2.1 Ooerations

U201 Conduct of Operations

01.1 General Comments (71707)

Using Inspection Procedure 71707, the inspectors conducted frequent reviews of ongoing

plant operations, in general, the conduct of operations was professional and safety-

conscious. Operator performance was good in evaluating shutdown risk by maintaining

awareness of plant conditions and equipment availability. In particular, on July 14,1997,

operators exhibited a good questioning attitude regarding the planned removal from service

of the spent fuel pool area ventilation supply fan, F 20. Operators noted that procedure OP

2264, " Conduct of Outages," was unclear whether the shutdown risk " Key Safety

I

Function *' for spent fuel pool area ventilation boundary would remain " Green" with f an F 20

removed from service. A condition report was generated to address the concern,and

procedure OP 2264 was changed before proceeding with planned maintenance activities on

f an F 20. Other noteworthy observations are detailed in the sections below.

01.2 Removal of Non-conservative Technical Soecification Clarifications from the

Technical Reauirements Manual

a. Insanction Scone (71707)

The inspector evaluated the licensee's efforts to remove non conservative technical

specification (TS) clarifications from the technical requirements manual (TRM).

b. Observations and Findings

T% licensee performed an evaluation the 27 technical specification clarifications and

ca.egorized 7 of them as more conservative,10 as less conservative, and 10 of them being

neutral as compared to the corresponding technical specification. On July 15,1997, the

licensee completed their effort of removing from the TRM all 10 technical specification

clarifications that were categorized as less conservative. The inspector verified that each of

the non conservative TS clarifications that could be considered a TS non compliance was

appropriately reported to the NRC in accordance with 10 CFR 50.73,

c. ConcluslQD

The licensee initiated offort in removing 10 non conservative technical specification

clarifications from the TRM was good.

.

_ - _ _ _ _ _ _ _

.-

11

l4

01.3 Timeliness of Corrective Ac' ans Condition Reoort Backlog

a. lasagstion Scoce (717'

The NRC evaluated the timelint s in which the licensee completed corrective actions

i associated with Unit 2 conditior sports (CRs).

I b. Observations and Findinos

'

l Timeliness for completion of corrective actions has been a longstanding concern at

Millstone. Having a CR backlog in itself is not a reflection of poor performance because as

the threshold for writing CRs decreases, the CR backlog willincrease accordingly. The

concern is the number of CRs that are not closed in a timely manner. To help provide the

NRC some sense of the licensee's progress in addressing the timeliness concern, the

licensee was asked to provide the number of CRs having outstanding corrective actions

that are greater than 120 days old. Although the NRC does not consider 120 days a level

of excellence nor is it acceptable when addressing immediate safety concerns,it does

provide some understanding of licensee management effectiveness in addressing the

corrective action timeliness issue.

At the end of the current inspection period, there were 780 CRs greater than 120 days old

that have not been closed which is a decrease from 828 CRs at the end of the last

I

inspection period. Out of the 780 CRs currently greater than 120 days old,200 of them

were initiated in 1997,

DEPARTMENT CRs OLDER THAN 1997 CRs OLDER

120 DAYS THAN 120 DAYS

Operations 48 10

Design Engineering 255 62

Technical Support 182 26

Work Planning 25 8

Maintenance 54 26

l&C 28 7

Safety / Licensing 47 8

Other 141 53

TOTAL 780 200

12 ,

c. Conclusions

The total backlog of 780 CRs that are greater than 120 days old indicates that timeliness

for completing corrective actions continues to be a concern. The backlog of 1997 CRs

greater than 120 days old is of greater concern because it reflects the performance of the

new management organization. The new management planned to demonstrate a higher

standard by dispositioning newly generated CRs in a timely manner while establishing a

plan for worising off the CR backlog that existed when they arrived. However, the backlog

of 200 CRs greater than 120 days old that were generated in 1997 indicates that the new

management is also ineffective in addressing the corrective action timeliness issue which is

considered a significant weakness. As discussed in NRC Inspection Report 50 330/96-04,

timeliness and effectiveness of corrective actions is an area in which the licensee must

demonstrate sustained improved performance.

U2 03 Operations Procedures and Documentation

03.1 Reactor Buildina closed Coolino Water Suroo Tank Minimumhynj

a. IDioection Scoco (71707)

.

The inspector evaluated the licensee's administrative controls for maintaining the reactor

building closed cooling water (RBCCW) system surge tank level.

b. Observations and Findinas

The RBCCW surge tank, which is utilized by both facilities (trains), is normally maintained

at 50 percent level by an automatic makeup valve in the primary makeup water system.

The RBCCW surge tank has an internal vertical weir that rises to the 37 percent level

which allows draining of one f acility while maintaining the other f acility in service. To

support maintenance on RBCCW system components, the licensee had drained facility 1

and was maintaining level on the f acility 2 side of the RBCCW surge tank was than 32

percent. Operators were periodically opening the primary makeup water supply to f acility 2

to account for minor system leakage. However, the inspector found that the required

RBCCW surge tank level band was not proceduralized nor was it specified on the Shif t

Turnover Report. One control room operator stated that operators had been filling the

RBCCW surge tank when level reached approximately 20 percent. The inspector was

concemed that with an undefined minimum surge tank level, RBCCW system operability

could be affected due to potential net positive suction head (NPSH) concerns for the

HBCCW pumps.

The inspector discussed this concern with operations management and as an interim

measure, the licensee added a surge tank level band of 24 percent to 32 percent to the

Shif t Turnover Report. Subsequent review by plant engineering indicated that as long as

there is a visible levelin the surge tank, there would be sufficient NPSH for the RBCCW

pumps. Nevertheless, the licensee agrees that the RBCCW level band should be

proceduralized and is in the process of evaluating the necessary procedure changes.

. .. .- . - . . .- -.

l

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l

13

c. Conclusion

Although the licensee determined that there would be sufficient NPSH available to the

RBCCW pumps, the failure to evaluate and proceduralize the level band that operators

should control RBCCW surge tank level was considered a weakness.

U2.Il Ma]nttnante

U2 M8 Miscellaneous Maintenance issues

M8.1 (Closed) Insoector Follaw uo item 50 336/95 201 03: Procedure Level of Use

Desionation (SIL 8 Individual item Closed)

e, ingstion Scong.192902)

The scope of this inspection included a review of Inspector Followup Item (IFI) 50 336/95-

201 03.

b. Observations and Findinas

This item concerned the fact that most maintenance and surveillance procedures were

classified as " General Use" versus * Continuous Use." The procedure Level of Use

designations are defined in procedure DC 4, " Procedural Complience," as follows:

Continuous Level of Use Procedure

  • A procedure that controls a work activity that is critical, complex, or involves

infrequently performed evolutions or activities.

  • Requires step-by step use to prevent immediate effects on nuclear or

personnel safety and plant reliability.

General Level of Use Procedure

  • A procedure that involves evolutions or work activities on plant equipment or

has multiple actions required to perform a task or tasks.

  • Procedure must be referred to as necessary during the performance of the

work activity to erwure the evolution is performed correctly.

  • The level of detail u. .vs the user to read an entire sequence and perform it

before referring to the procedure again to confirm the complete task and

prepare for the next task or sequence.

Information Level of Use

  • A procedure that involves administrative or technical evolutions or processes.
  • Procedure requires periodic review for familiarity but is not required in the

field.

The inspector found that only five mechanical and electrical procedures had been changed

from " General Use" to " Continuous Use" during the past two years which reflects licensee

management's view that the " General Use" category is adequate for most procedures.

14

'

Procedure DC 4 specifies that the Level of Use Indicates the minimum required degree of

reference to the procedure during portions of the work activity and does not alter

expectations for procedure adherence,

c. Conclusion

The NRC considers IFl 50 336/95 20103 to be closed based on: (1) There is no specific

regulatory requirement that defines or mandates procedure Level of Use classification: (2)

Although there have been examples of procedural adherence issues documented in NRC

inspection reports since this IFl was opened, there were no documented examples of where

the procedural noncompliance could be attributed to the Level of Uso designation; and (3)

inspector observations indicate that surveillance procedures are generally referred to on a

step by step basis even though most surveillances are " General Use." Even though this

item is being closed, the NRC considers procedure Level of Use to be an area where

management standards and expectations should be promulgated, particularly with

surveillance procedures to ensure understanding by the licensee's staff.

M8.2 (Closed) Licensee Event Reoort 50 336/97 04: Hlah Pressure Safetv inlection (HPSI)

Pumo Allonment

a. Insoection Scone (92902)

The inspectors reviewed the corrective actions taken by the licensee to prevent recurrence

of the event described in the subject LER.

b. Observations and Findinos

On January 23,1997, th, scensee discovered that three HPSI pumps were aligned such

that they were all capable of injecting water into the reactor coolant system. The plant

was in the refueling mode (Mode 6) with the reactor vessel head removed. In that mode

plant technical specifications only permit two charging pumps and two HPSI pumps to be

,

capable of injecting into the reactor coolant system (RCS) to prevent an inadvertent RCS

overpressurization. The three HPSI pumps were inadvertently aligned, due to personnel -

error, for approximately 36 minutes during preparations for surveillance testing. The -

condition was immediately corrected upon discovery. .

Additional corrective actions included the revision of all affected surveillance test

procedures to include pump alignment requirements. A detailed briefing of the event and

causal factors was given the operating shift crews. The inspector reviewed the revised

test procedures and the briefing provided to the operators,

c, Conclusions

The licensee's corrective actions associated with this LER were determined to be

acceptable. The safety significance of this event was minimal because: 1) With the reactor

__ vessel head removed, the inadvertent injection by three pumps could not overpressurize the

reactor coolant system; and 2) If operators had not discovered the HPSI pump alignment

,

._.-1.- - ..,._..._...=._--,mm__.-_ _ _ , , - - , _ m - , , , . .. ...-,_-<-,.-m ,_w__. --

- - . _

__-_ _ __ . .

._ .

.

16

during the shif t, the condition would have been identified during the shif tly performance of

the control room operator logs per procedure OPS Form 2614A 2, * Control Room Daily

Surveillance, Mode 6 and Defueled.* This licensee identified technical specification non-

compliance is being treated as a Non Cited Violation, consistent with section Vll.B.1 of the

NRC Enforcement Poliev. This LER is closed.

l

U2.lli En91ntidng  ;

U2 E8 Miscellaneous Engineering Issues

,

E8.1 LClosed) IFl 50 336/93 20-05 & LER 50 336/9711-and (Undatel eel 50 336/96-

20125: Testina of Dual Function Valves (Update Significant item List No. 30)

a. insoection Scone (92903)

The inspector reviewed the corrective actions taken by the licensee to address questions

regarding testing of dual function air operated valves. The licensee defines dual function

, valves as those valves that have an isolation function at containment design pressure and

at the normal system operating pressure.

b. Observations and Findinos

As discussed in Licensee Event Report 60-336/93 23,in June 1993, the licensee

experienced problems with leakage past the letdown isolation valves 2 CH 089 and 2 CH-

615 while attempting to establish isolation to support repairs to a manual stop valve in the

line. The plant was at normal operating pressure (2250 psig) at that time. The cause of

the leakage was found to be improper adjustment of the spring preload on the air operators

during prior maintenance. The LER documented the immediate corrective actions taken

which included the adjustment of the affected valve operator spring preloads and

verification of the isolation capability at normal reactor coolant system pressure. The LER

also noted that a maintenance procedure had been developed for the actuator type used on

the af fected valves. This procedure included detailed spring bench setting requirements.

Procedures for all dual function valves were to be completed prior to the next refueling

outage and retest requirements involving verification of isolation against normal system

pressure for the valves were also to be defined,

in February 1994, a violation was cited for the performance of the work on the air

actuators without written procedures. At that time, the inspector noted that the violation

could have reasonably been prevented by corrective action for a previous licensee finding

concerning valve 2 EB-99. The licensee's violation response specified that procedures for

pneumatic actuators would be completed prior to May 6,1994. Additionally, the licensee

committed to specifying retest requirements to verify valve isolation capability against

normal system pressure for all valves that function in a dual role.

.

e

16

in June 1995, Adverse Condition Report (ACR) 1935 was written to identify that actions

had not yet been taken to implement the commitment to ensure the required isolation af

dual function valves against normal system pressure.

In response to an NRC inspection finding that the licensee's commitment had still not been

completed, in March 1996, ACR 9623 was written to identify the potential that 23 dual

function valves may not be set to isolate against normal system pressure, The licensee

planned to perform as found testing of the valves following the core off load, Escalated

Enforcement item (EEI) 50 336/96 20125 documented an apparent violation for the

licensee f ailure to implement prompt corrective action to resolve the dual function valve

testing concern,

in March 1997, Condition Report (CR) M2 97 0412 was written to document the results of

the as found testing. The testing method involved measuring the pressure needed to

operate the valva and then using the air pressure results to determine the seating force the

valve operator sving was transmitting to the valve disc,

Following the completion of testing and evaluation of test results,in May 1997, LER 50-

336/97 011 reported that 11 of the 23 valves tested were not capable of closing to a leak

tight condition against normal system operating pressure, The corrective actions specified

in the LER were to: (1) revise the appropriate procedures prior to entering Mode 4 to

ensure that the proper valve control parameters are specified and verified af ter

maintenance that could affect dual function valve closing forces; and (2) adjust the

affected valves to ensure they properly close against containment pressure and normal

operating system pressure prior to entering Mode 4. The licensee also stated that these

actions satisfied the commitment to specify the retest requirements for dual function

valves.

The inspector reviewed the licensee actions taken to date to resolve the issue of

inadequate testing of dual function valves, Since the cwse of the original problems was

attributed to the lack of adequate procedures for performing maintenance on valve air

actuators, the inspector questioned why the concern for adequate closing force would not

apply to all air actuators in the plant, not only valves with dual functions. The licensee had

not reviewed other air operated valves, in particular those valves that have safety

functions, to assess the valve operability, The licensee acknowledged this concern and

prepared Memorandum MM2 97 043, dated July 2,1997, which discusses planned actions

to screen, evaluate, and test additional air operated valves to ensure that valves that are

critical to the safe operation of the plant are set up properly,

c, Conclusions

The NRC concluded that the licensee has established adequate methods for testing the air

operated valves to ensure that adequate force is applied by the actuator springs for the

valve to perform its function. However, despite numerous LERs, ACRs and NRC

enforcement actions that have documented the air operated valve concerns since 1993,

licensee corrective actions continue to be inadequate in that the scope of the review was

limited to the * dual function" valves even though other safety related air operated valves

i

!

4

17

'

could have the same setup problems. eel 50 330/96 20125 (and Significant items List

No. 30) remain open pending:

  • NRC review of the completed licensee corrective actions committed to in LER 50-

330/97 11;

e NRC review of the licensee findings and corrective actions relative to non dual

function air operated valves; and,

o NRC review of any additionallicensee actions that may result from the resolution of

eel 50 330/96 20125. Because eel 50 330/96 201 25 encompasses the technical

issues and corrective actions discussed in LER 50 330/9711, the NRC will use this

eel to track those issues; LER 50 330/9711 is considered administratively closed.

Inspector Followup item (IFI) 50 330/93 20-05 identificJ e concern that reduced pressure

testing of 10 CFR 50, Appendix J, may not adequately assure the leak tight integrity of

valves that may be required to close at full reactor coolant system pressure. The inspector

noted that the Appendix J testing verifies the valve seating capability at containment

design pressure. This testing, combined with additional testing to ensure adequate closing

force at full system pressure, demonstrates the ability of the valves to function at full

system pressure. Since the actions being taken to implement the additional testing are

being tracked as discussed above,IFl 50 330/93 20-05 is considered closed.

E8.4 [Vodate) Escalated Enforcement item 50-330/96 201 36: Inadeauste Corrective

Action Concernina a Seismic Deslan Deficiencv of a Vital Switchaear Room CantcI

(Closed Significant items List No. 33)

a. Insntetion Scoce (92903)

The inspector reviewed the licensee's modification to the fire protection piping in the cable

spreading area of the turbine building for precluding potentialleakage of the Fire Protection

(FP) class 2 piping over class 1 components and the design basis for precluding the

unwanted seismic class 2 over 1 interaction in this cable spreading area,

b. Observations and Findinas

On September 29,1995, the licensee's Service Water System Operational Performance

(SWSOPI) identified a concern with Vitaulic couplin9s in a 3" fire protection (FP) pipe

located over chiller X 182 in the cable spreading area of the turbine building at elevation

45' 0", The possibility existed that the Vitaulic coupling could have leaked during a

seismic event, thus, actuating the moisture detector in the coffer dam around the X 182

chiller which then would close the service water flow to the coolers.

The inspector reviewed the licensee's records, interviewed the cognizant personnel, and

performed a walkdown to ensure that the corrective action that replaced the Vitaulic

couplings with welded flanges to assure leak tightness of the fire protection system pipe

joints was properly implemented. During the walkdown, the inspector observed that the

_ _

.

18 ,

Vitaulic couplings on the 3" fire protection piping over chiller X 182 located in the cable

spreading area of the turbine building had been replaced with welded flanges es prescribed

by the corrective action. The rest of the FP piping appeared to be well supported to

withstand a postulated seismic event.

During the walkdown, the inspector noted that a segment of thit. FP piping (elbow) has a

1/4" of clearance from a safety related a cable tray, thereby creating a possible

nonconformance with the seismic 2 over 1 Interaction criterion. The licensee initiated a

condition rep' ort to prepare a calculation to evaluate the as found configuration during a

postulated seismic event. The inspector reviewed the licensees' calculation No. 97 ENG-

01819C2, Revision 0, and concluded that the licensee has performed a detall caleMation

with a finite element computer model of ths subject pipe t :Ing a standard computer

program. The analysis was performed using the correct parameters from the design basis.

The results showed that the maximum relative displacement between the FP pipe and the

cable tray in question is 0.078 which is less than 1/4". Therefore, the existing 1/4"

clearance is adequate,

c. Conclusion

. The licensee has satisf actorily resolved the potential for leakage of the fire protection

piping joints during a seismic event by replacing the Vitaulic couplings on the piping with

welded flanges. The proposed violation and potential escalated enforcement action for this

item is still under review by the NRC.

EB.5 luodm) Escalated Enforcement items 50 336/96 201 42 & 43 Material.

Eguinment and Parts List Prooram (Update Significant items List No.18)

a. Jr aoection Scone (92903)

The overall site material, equipment, and parts lists (MEPL) program was reviewed;

comments and discussion that apply to all three Millstone units are provided in Unit 3

Section U3 E8.1. This section provides Unit 2 specific discussions only,

b. Observations and Findinus

!

Unit 2 has approximately 60,000 total components in the plant, of which about 12,000

are safety related. As part of the Performcnce Enhancement Program (PEP)in the early

1990's, the licensee reviewed the quality classification of about 28,000 components, in

late 1994, the MEPL program was utilized to downgrade 998 components from safety-

related (Category 1) to non safety related, it was later determined that a number of these

downgrades were not correct. Thus, in 1995 and 1996 all of the downgraded components

were upgraded back to safety related. During the time period that the components were

'

improperly classified, work was performed on them as non safety related components,

creating the possibility ths,t substandard parts may have been installed. To address this

concern, the licensee reviewed each of the 400 to 500 automated work orders (AWOs)

that had been performed during this time period on these components to determine if non-

safety related replacement parts had been installed. Seven instances were identified that

-

_ _ _ _ _ _ _ _ - - - - - _ - - - _ - _ _ - - _ _

. _ _ _ _ _ _ _ - _ _ _ _ _ - - _ _ _ - _ _ _ _ -

-

. .

. 19 i

required that nonconformance reports (NCRs) to be issued and various corrective actions to

be taken. As of the end of this inspection report period, not all of the NCRs had been fully

dispositioned.

As one action to adda,ss the various concerns associated with classification of

components and the MEPL pre vam, Unit 2 is performing a MEPL re review of all systems

and all safety related components. This is being done at the component level and is

scheduled for completion in the Fall of 1997.

MEPL' evaluations are not only performed at the component level but also the part level

because parts that are not critical for the component to perform its intended safety

function may be classified as non-safety related. For each unit, a number of condition

reports (CRs) have documented that some parts listed on the Bill of Materials (BOMs) for a

safety-related component were either classified as ' Undetermined' or non safety related.

This raises the question of whether non-safety related parts have been inappropriately

installed in safety related components. At Unit 2, licensee corrective actions to address

this concern included: (1) performing BOM MEPLs prior to working on components during

the current mid cycle outage, and (2) performing a full historical review of work orders of

any part or component that has its MEPL classification upgraded from ' Undetermined' or

non safety related to safety related. The inspector asked the licensee why it was

appropriate to limit the historical review to only those parts that have been upgraded

because components that have not been worked during the mid cycle outage, whose BOM

MEPL has not been performed, may have had non safety related parts installed. At the

close of the inspection period, the licensee was still gathering information to justify their

plans,

c. Conclu1}DD

Escalated Enforcement items 50 336/96-201-42 & 43 remain open to allow further NRC

inspection of the nite-specific and programmatic MEPL concerns that are summarized in

in Unit 3 Section U3 E8.1.

E8.6 (Ocen) Unresolved item 50-336/97-202-02) Main Steam Check Valves Deslan

Adeauaev (Closed - Significant items List No. 45)

a. Insoection Scoce (929021

This inspection involved a review of Adverse Condition Report (ACR) M2 96-0542, which

questioned whether the non-safety-related classification of the main steam check valves

was appropriate. The check valves are credited in the accident analysis for preventing the

blowdown cf the intact steam generator in the event of a main steam line break (MSLB)

upstream of the main steam isolation valves (MSIVs).

- . ,

_ _ - _ _ _ _ _ _ _ _ _ __

.

20

.

b. Observations and Findinos

in addressing the ACR, the licensee provided a detailed licensing basis history regarding the

main steam check valves. There is no licensing basis documentation that specifies

explicitly whether the check valves are considered safety related or non safety related.

However, the seismic classification of the check valves that is explicitly stated in the Final

Safety Analysis Report (FSAR) combined with NRC guidance documentation issued after

Millstone 2 was licensed, provides a sufficient basis to conclude that the non-safety-related

classification of the check valves is acceptable. The original FSAR, Section 10.3.2.1,

states that main steam line up to and including the MSIVs are required to be Seismic Class

I and all downstream components (which includes the main steam check valves) are

considered seismic Class ll.

Although the following information is contained in NUREGs that were issued af ter Millstone

7 was licensed, they still provide insights on the staff's position regarding the issue. The

NRC discusses and generically accepts the use of non safety >related main steam check

valves in NUREG-0138, " Staff Discussion of 15 Technicalissues Listed in Attachment to

November 3,1976 Memo from Director, NRR to NRR Staff." NUREG 1038, Issue No.1,

discusses the treatment of non-safety-grade equipment in evaluations of postulated steam

line break accidents. Although the main steam checks valves were not the focus of the

evaluation, NUREG-0138 stated that "for the purposes of this discussion, a safety grade

component is defined as one which is designated as seismic category I.... The remaining

Valves in the rnain steam and main feedwater lines are designated as non-safety grade

components...." The NRC notes that for accidents involving spontaneous f ailures of the

secondary system piping, that are not part of the primary system boundary, less stringent

requirements are imposed on the quality and design of systems needed to cope with the

secondary system ruptures.

Due to their use as a backup to safety-related components in the safety analyses, the

inspector also reviewed the Inservice Testing (IST) and Inservice Inspection (ISI)

requirements associated with the main steam check valves. The IST program requires that

the licensee verify during each cold shutdown that the valve travels smoothly and

completely to the closed position as steam plant load is reduced. The inspector reviewed

the following:

-

IST surveillance test SP 21134, " Main Steam System Valves Operational Readiness

Test," Rev.10, and the Surveillance Cover Sheet ENG. Form 21134, Rev. 4, which

contains the acceptance criteria and which records the data, test acceptability, and

approvals:

The inspector noted two errors in Rev. 4 of ENG. Form 21134 with respect to the position

of the valves during the test as being fully open or fully closed. The licensee concurred and

initiated a procedure change. The inspector also selected recent tests and noted that there

have been difficulties with the valves passing the test. The maintenance history for the

vcives was also reviewed and the inspector noted a moderate amount of work required to

l

l

.. ...

. . . . - . . . . _ . . . - . - - . . . . - - . . . _ - - . . - . - . . - - . . . - . . . - . - . _ . - - . . - . = - . . -

.,

,

4

4

21

. .

maintain the valves. The inspector reviewed procedure EN 21221, liev. O, " Check Valve

Examination and Testing," which places these check valves in the Priority 3 Group for

examination once every five refueling outages. This procedure was placed in a "Do Not

Use" status as of September,1993,

c. Conclusion

The licensee's basis for determining that the main steam check valves are non-safety-

related was found to be acceptable and Significant items List No. 45 is considered closed.

The area of inspection, maintenance, and testing associated with these check valves is

unresolved and will be further reviewed to ensure that appropriate activities are being

accomplished to ensure reliable functionality of the valves. (Unresolved item 50 336/97-

202 02)

.

.,a , , + =- -

.a,, aas-u a +. . ~ . , - -- .u --.. ~ - a ~-o - --~ -

.

Unit 3 Renort DetaHA .

Summarv of Unit 3 StalMA

Unit 3 remained in cold rhutdown (mode 5) status throughout the. inspection period. The

licensee continued to implement unit recovery activities, while continuing to develop an

Operational Readiness Plan directed toward the objectives and milestones leading to both

the physical readiness of the Unit 3 restart and the preparedness for the NRC operational

readiness inspection conduct.

On July 16,1997 the licensee notified the NRC that the problem identification phase of its

Configuration Management Program (CMP) was complete for all 88 plant systems,

comprising all Maintenance Rule "in scope" group 1 and 2 systems. As delineated in the

NRC Confirmatory Order governing the Independent Corrective Action Verification Program

(ICAVP), this pronouncement by the licensee declared all 88 systems available for review

and inspection as part of the ICAVP process. During the previous inspection period, the

licensee line management had declared readiness for the start of ICAVP activities. Af ter

concurrence from the licensee's Nuclear Oversight organization, the ICAVP process at -

Millstone Unit 3 commenced on May 27,1997.

As of the end of this inspection period, the NRC had selected all five systems tnat will be

subject to the ICAVP contractor (four "in-scope" systems) and NRC team (one "out-of-

scope" system) review. The last two of the four "in-scope" systems were selected by

random drawing at a public meeting held on July 18,1997 by the Connecticut Nuclear

Energy Advisory Council. The results of the ICAVP review process are made public via the

protocol established with the ICAVP contractor and plan approval; and therefore will not

routinely be documented in the Millstone Special Projects Office combined inspection

reports.

U3.1 Onorationt

U3 01 . Conduct of Operations

01.1 Loss of Scent Fuel Pool Coolina Event Followuo

a. insoection Scoce (71707. 92901)

On June 25,1997, cooling water flow to the spent fuel pool was inadvertently stopped

when the component cooling water and service water systems supporting the in service

("A" train) spent fuel pool cooling heat exchanger were taken out of service as part of

planned outage maintenance activities. With the cessation of forced cooling, the spent fuel

pool water temperature increased approximately 10*F over the following 28 hours3.240741e-4 days <br />0.00778 hours <br />4.62963e-5 weeks <br />1.0654e-5 months <br />. Based

upon the higher pool temperature reading, observed by a plant equipmcnt operator (PEO)

during routine operations shift rounds, the abnormal equipment lineup was recognized and

spent fuel pool cooling (SFPC) was restored using the in-service components of the

redundant "B" SFPC train. During event followup subsequent to the recovery from the

abnormal spent fuel pool heatup, the NRC inspector reviewed the licensee's root cause

investigation process and independent review team (IRT) interim (draft) report. The

inspector attended an IRT working meeting and discussed findings and facts with both unit

.

.

.

.

23

line management and nuclear oversight personnel. The inspector also reviewed the

operating procedure for the spent fuel pool cooling and purification system.

b. Observations and Findinos

Routine NRC resident inspection of the control room on June 25,1997 identified a spent I

fuel pool tempbrature of less than 90'F. The normal operating procedure directs routine

operation of the SFPC system to maintain pool temperature below 125'F. Since a slight

rise in temperature is anticipated with a train swap, the spent fuel pool temperature

increase that occurred during the remainder of the day and swing shif ts on June 25 would

not have been expected to be recognized as an abnormal condition by the plant operators.

A review of the logs for the Mode 5/6 Daily and Shiftly Control Room Rounds for the period

in question noted that the mid shift on June 26 documented a spent fuel pool temperature

of 90'F on both control board temperature indicators, SFC*Tl27A&B. Since the

documented acceptance criteria for a temperature less than 125'F was met, only operator

cognizance of a rising temperature trend would have identified the loss of spent fuel pool

cooling before it was identified by the PEO on radwaste rounds on the morning of June 26.

Control room operator recognition of such a rising trend was impeded by the practice that a

,

'

new log theet is issued daily for all thrae shifts, commencing on the mid shift. Therefore,

the mid shif t operator did not have the benefit of a visual aid indicating to him when he

filled out the Control Room Rounds sheet for June 26 that the temperature had risen to

l 90*F from the mid-80's temperature indications documented on the previous day's log

l sheet.

The inspector reviewed the Control Room Rounds logs, the computer generated spent fuel

pool temperature plots, the alarm response procedures, the SFPC operating procedure (OP

3305, Revision 15), and examined the control board temperature indicators, discussing

with operators on shif t both the conduct of shift log keeping and the degree of accuracy to

which temperature indications would be recorded. The inspector noted that SFC*Tl27A&B

were marked in 5'F increments, which by common instrumentation and control convention

would limit the degree of accuracy for any temperature readings to step intervals of

approximately 2.5 degrees each. The inspector confirmed that the main control board

alarm for spent fuel pool temperature annunciates at greater than 135'F. It was noted that

the operators appropriately used the emergency operating procedure, EOP 3505A, for

" Loss of Spent Fuel Pool Cooling" to restore an operable cooling flow path once it was

recognized that the system was not correctly aligned. The maximum temperature to which

the spent fuel pool rose during this event was approximately 98'F.

The Unit 3 line management initiated an Event Review Team (ERT) to investigate the root

cause and contributing factors to this event. The Nuclear Oversight organization also

chartered an independent Review Team (IRT) at the request of senior station management

to assess the event, its causes, and the conduct of the ERT. The inspector reviewed the

completed ERT Root Cause Investigation, monitored the IRT conduct of a meeting to

discuss preliminary results of their review, and examined a copy of the IRT interim report.

it was determined that the interim nature of the IRT analysis, findings, and conclusions was

based upon the intent to perform a follow-up assessment of the larger programmatic

aspects of the " Conduct of Operations" at Millstone Station. Both the ERT report and IRT

assur

_ _ _ . _ . . . . ___ . _ . ._ __. _ _ _ . _ . _ _ . _ __ __ _ ._.-. ___

.

d

24 ,

!

interim report documented several corrective action recommendations on specific (e.g., log

keeping) and generic (e.g., configuration control issues) measures that could be

implemented to r' event problem recurrence and enhance future process controls, including

those affecting human performance issues, While some of these corrective actions are

-

directed toward longer term (e.g., corrective action effectiveness, conduct of operations

standards) enhancements, most recommendations appear that they should be implemented

prior to the restart of the unit.

,

c. Conciusioni

(

The Unit 3 spent fuel poolis designed from a structural standpoint to withstand a

'

temperature of 200'F, has a design limit of 140'F from the standpoint of preservation of

4

the purification components (e.g., resin), has an annunciator alarm setpoint of 135'F, and

is controlled administratively to operate at a temperature of less than or equal to 125'F.

, Therefore, this event, involving the loss of SFPC for approximately 28 hours3.240741e-4 days <br />0.00778 hours <br />4.62963e-5 weeks <br />1.0654e-5 months <br /> and resulting

1- in the heatup of the pool to approximately 98'F, was not significant from a safety related

or design basis considerations. However, given the configuration management

'

ramifications (i.e., the shut down risk impact with a cross train connected system lineup,

the " train swap" control considerations, and the loss of continuity of operator cognizance

.

of how safety related equipment was aligned), this event has significance not only with

respect to the adequacy of current operational and configuration controls but also

management's expectations for operational standards. The former appears to have been

addressed by the licensee's ERT report, while the latter is in the process of being assessed

'

by the IRT oversight. Several corrective measures have been recommended and a

i

programmatic review of the conduct of operations is planned as an IRT follow up activity.

The NRC will continue to monitor licensee progress in the assessment of this event, its

4 generic implications upon the adequacy of other programs (e.g., corrective actions, conduct

, of operations), and the implementation of effective corrective measures. This overallissue

will be tracked as an inspector followup item. (IFl 50 423/97 202-03)

U3 07 Quality Assurance in Operations

07.1 Ooerational Oversiaht Activities (SIL ltems 73 & 86)

The inspector continued to routinely meet with Nuclear Oversight personnel to discuss

activities and initiatives in the areas of the corrective action program enhancement, self

'

4

assessments, priorities for unit restart readiness,10 CFR 50.54(f) involvement, and the .

2

conduct of Nuclear Safety Assessment Board (NSAB) meetings. Where appropriate,

Nuclear Oversight surveillance, audit, and special reports were reviewed to assess the level

of QA involvement in the performance of routine activities by the Unit 3 line management,

as well as to determine progress in the corrective measures taken for known problem

areas. Specfically during this inspection, the inspector reviewed the following documents

-

and performance of assessment / evaluations, that provided evidence of continued

management attention to strengthening the Nuclear Oversight function at Millstone Station.

4

e Dissemination of site briefing information on the conduct of an Independent
Assessment of Nuclear Oversight by a review team of industry consultants and

n. e ~ w

. 25

personnel from other nuclear utilities. This team performed a two-week, onsite

assessment commencing on June 19,1997 and conducted a preliminary exit

briefing with senior NU management before departing the station. This exit meeting

was observed by an NRC Special Projects Office Branch Chief.

  • Issuance of a self assessment report for the first quarter of 1997, documenting the

Nuclear Oversight Performance Evaluation (PE) Department's strategic plan

development and assessment of organizational effectiveness. Since the PE group

,

was formed in December 1996, this selfessessment evaluated the infrastructure

and organizational effectiveness of the department using interviews, bench marking,

and criticalinternal assessments.

  • Documentation of a Nuclear Oversight Operational Readiness Assessment Plan for

Urlt 3. This document discusses the approach and process by which verification

activities will be conducted to ensure safe operution of the unit, the effective

functioning of the line organizations, and the adequacy of preparations for the

resumption of power operatior.s after the extended shutdown.

  • Publishing Northeast Utilities Nuclear Safety Standards and Expectations by the

President and Chief Executive Officer of the NU Nuclear Group. The principles

discussed in this document appear directed to providing Nuclear Group personnel

with management's focus on the safety of operations and other critical, mission-

driven organizational requirements.

  • Establishment of the Independent Review Team concept, including IRT staff

organization and resources, goals, and the use of processes in event evaluations.

The IRT process was utilized to further assess the loss of spent fuel pool cooling

discussed in Section 01.1 of this inspection report.

  • lssuance of a significant number of condition reports (CRs), along with appropriate

use of its stop-work authority, by the Nuclear Oversight Organization during this

report period. An increasing level of Nuclear Oversight involvement in both problem

identification and recommendations for improvement is evident not only in the CRs,

but also in audit and surveillance reports, as well as routine and special management

meeting participation,

in addition to review of the above program initiatives and assessment activities, the

inspector specifically evaluated Nuclear Oversight and senior licensee management actions

to address concerns with personnel overtime controls. The inspector noted that some

overtime program violations had been recurring at Unit 3 smce early 1996. The Nuclear

Safety Engineering Group conducted an evaluation of the overtime controls at Millstone

Station to determine if changes to Nuclear Group Procedure, NGP 1.09, " Overtime Controls

for All Personnel at Millstone Station," were necessary. Based upon this review and

issuance of a Level 1 CR to collectively address the identified overtime violations, the

licensee determined that a revision to NGP 1.09 was required. On .luly 23,1997, the

station operations review committeo (SORC) approved revision 8 to NGP 1.09 and the new

overtime control provisions became effective on July 25,1997.

. _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ - - -

26

.

The inspector questioned when an updated Millstone Unit 3 Operational Readiness Plan

(ORP) would be issued, since the existing revision 3 had been issued in November 1996

and appeared to be outdated. The inspector noted that d NSAB had also commented at a

board meeting conducted in May 1997 about the " obsolete" nature of the current ORP. It

was recognized by the NRC that since November 1996, an interim "Re::overy Plan * has

been published; however, the protracted length of time since the last ORP revision

encompassed a number of management changes and corresponding adjustments to the

plan. On July 24,1997, a new Unit 3 ORP (revision 4) was issued, bringing up to date the

current licensee philosophy on the restart issues management and restart eternents

recognized to prepare Unit 3 for operational readiness and subsequent startup and power

ascension activities.

Overall, the Nuclear Oversight organization appeared to be actively involved in quality

assurance and assessment activities directed toward effective corrective actions for

i identified problem areas and program enhancements to improve future operations. The

initiatives noted above attest to a more active role by Nuclear Oversight in dealing with line

performance. However, while the routine QA and oversight reports document cognizance

of the areas which represent the most significant challenges to improving performance, the

ability of Nuclear Oversight to effect positive changes has not yet been fully demonstrated.

, While examples of success, as noted above, do exist, significant challenges were noted by

I the NRC to remain in such areas as corrective action effectiveness, training enhancements,

and plant configuration management controls, as are discussed in technical details in other

sections of this report, Progress in the areas of QA/ Oversight program improvement will

continue to be tracked by the NRC as part of SIL ltem 73, while needed training program

enhancements, discussed further in Section M4.1 of this inspection report, will be reviewed

as part of SIL ltem 86.

U3 08 Miscellaneous Operations issues (92700)

08.1 Technical Soecification (TS) Noncomoliance

a, ID30ection Scoce

Several recently issued licensee event reports (LERs) have dealt with TS noncompliance

issues. The inspector reviewed the LERs for root cause and safety significance

determinations and adequacy of corrective actions. The inspector also verified that the

reporting requirements of 10CFR 50.73 had been met,

b. Observations and Findinas

(Closed) LER 50-423/96-34

This LER documented that the residual heat removal (RHR) pump suction relief valves were

not set in accordance with TS 3.4.9.3. The TS required the RHR reliefs be set at 450 psig

in order to provide over pressure protection when the reactor coolant system cold leg

temperature was less than 350*F. The actual lift pressure for the RHR suction reliefs is

440 psig. The lif t pressure for the valves, as documented in the original design change and

_ _ _ _ - _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ .

a

2 7 .-

.

the subsequent set point calculation, is 440 psig. A TS change request was processed and

submitted to the NRC for review to change the value to between 426.8 and 453.2 psig,

The inspector verified the licensee had entered the applicable TS action statement and had

not credited the RHR suction reliefs as a means to satisfy TS 3.4.9.3. In addition, the

licenseo had issued proposed technical specification change request (PTSCR) 314 96 to

change the RHR suction relief setpoint. This request was approved on July 10,1997.

(Closed) LER 50 423/97 14

This LER documents that both trains of the control room envelope pressurization system

(CREPS) were inoperable due to instrument air valves 3 IAS V644/V725 being found out of-

position. These valves supply air to solenoid operated valves which control air operated

dampers in the control building. The solenoids are not qualified as category 1 equipment

and therefore, it must be postulated that they fall in the most adverse position. This

creates the potential for a breach of the control room envelope which would render the

CREPS inoperable. The air valves had been opened to allow purging of the cable spreading

room and apparently had not been closed after completion of the evolution.

The licensee promptly restored the air valves to their required position and revised the

procedure to correct the deficiencies. The inspector verified that procedure OP 3314F

was revised to restore the valves to their normally closed position.

(Closed) LER S0-423/97 23

This LER documents that the main steam isolation valves had not been tested in

accordance with the literal requirements contained in the TS. The Technical specifications

require that the valves be demonstrated operable by verifying full closure within 10

seconds in modes 1, 2, and 3 when tested pursuant to TS 4.0.5. Relief from the

requirement to perform a full stroke test during power operation had,been granted by the

NRC in the licensee's inservice test program; however, the licensee had not submitted a TS

change request to delete this requirement from TS. The inspector verified the licensee had

initiated a PTSCR to eliminate the requirement for full stroke testing the MSIVs in modes 1

and 2.

(Closed) LER 50-423/97-24

This LER documents that the engineered safeguards building noble gas activity monitor

(3HVQ'RE49) was inoperable and that best efforts to repair the monitor had not been

initiated in accordance with TS 3.3.3.10. The radiation monitor was declared inoperable

since it was incapable of measuring an effluent concentration as low as 1.0 E 06 uCi/cc.

The instrument had been purged by operations personnel due to the receipt of spurious

alarms. The radiation monitor design contains a feature where, upon completion of a

purge, a new background level is automatically measured and entered into the circuitry.

Review of the database entries indicated that a background value of 1.01 E 06 uCi/cc was

entered. Background readings at this location are normally 1.0 E 08 to 1.0 E-07 uCi/cc.

The high background level was attributed to electromagnetic interference from welding

. . - _ _ - - .. .-

.

.

28

.

activities in the general area. The incorrect background level prevented the monitor from

meeting the sensitivity requirements specified in the TS bases.

Interim corrective actions included revising operations procedure OP 3250.62 to enter a

zero background level reading after purging the radiation monitor, and chemistry procedure

SP 3867 to verify zero background after completion of surveillance activities. Long term

corrective actions include a review to evaluate the removal of the automatic background

subtraction feature associeed with 3HVQ'RE49 and other radiation monitors.

The inspector verified that procedural changes had been made to the operations and

chemistry procedures to zero the background level after purging and completion of the

surveillance in addition, an engineering work request was initiated to delete the automatic

background subtraction feature from applicable radiation monitors.

(Closed) LER 50-423/97-26

This LER documents that ASME Section XI required examinations on some service water

supports had not been re performed during the subsequent refueling outage, for supports

that initially f ailed inservice inspection (ISI) examinations during 1989. The licensee had '

originally assumed that the supports were located in areas where performance of the

examinations was impractical.10CFR 50.55a provides for relief, when justified. However,

relief was not spec'.fically requested to allow excluding the examination of these

component supports. The f ailure to perform these examinations is a condition prohibited

by TS 4.0.5. Subsequent inspections by the licensee revealed that the supports were

acceptable.

As corrective action, the licensee revised the ISI program documents to include ASME

Section XI requirements for performing additional and successive examinations, and

included guidance for requesting relief in accordance with 10CFR 50.55a. The inspector

verified that the ISI Program Manual was revised to capture these requirements,

c. Conclusions

The LERs discuss conditions prohibited by TS. Further NRC review of each LER established

that while the licensee's operational activities were proper evolutions, literal compliance

with the plant TS had not been maintained. Based on the above corrective actions and the

low safety significance of the issues, these licensee-identified and corrected violations are

being treated as Non-Cited Violations, consistent with Section Vll.B.1 of the NBC

Enforcement Poliev. The listed LERs are closed.

However, the closure of the LERs does not address the generic concern for TS compliance.

A review of LERs issued as of April 1996 revealed that there have been a number of LERs

that have dealt with TS compliance problems relating to questionable interpretations. This

area is of current interest for further NRC review and is included as an NRC followup

activity; documented as Significant items List (SIL) item 70.

.. .

..

_ - _ _ _ _ _ _ _ _

_____

.

.

29

U3.Il Maintenance

U3 M1 Conduct of Maintenance

M 1.1 General Comments

The inspectors' determined that the maintenance and surveillance activities observed were

properly performed.

M1.2 inservice Test Prooram Review

a. insoection Scone (73756. Tl 2515110)

The inspectors evaluated the effectiveness of Northeast Nuclear Energy Company's

(NNECO) inservice test program for safety related pumps and valves at Millstone Unit 3.

The inspectors focused primarily on components in the auxiliary feedwater (AFW),

interrnediate head safety injection (IHSI), and reactor plant component cooling water

systems. These risk significant systems are needed to prevent or to mitigate the dominant

core damage frequency events identified in the Millstone Unit 3 Individual Plant

Examination.

The)urposes of inservice testing (IST) are to assess the operational readiness of pumps

and valves, to detect degradation that might affect component operability, and to maintain

safety margins with provisions for increased surveillance and corrective action. The

requirements for IST are contained in Millstone Unit 3, TS 4.0.5, which requires testing in

accordance with 10 CFR 50.55a, " Codes and Standards," and Section XI of the American

Society of Mechanical Engineers (ASME) Boiler and Pressure Vessel Code (the Code). The

inspectors reviewed administrative and surveillance procedures, engineering evaluations

and calculations, test rest,lts, and LER's germane to the Millstone Unit 3 IST program.

b. Observations and Findinos

Millstone 3 Unit is implementing the first 10-year interval of the IST program, which is

based on Section XI of the Code (1983 Edition). However, pursuant to 10 CFR

50.55a(f)(4)(iv), NNECO is currently upgrading its program for the second 10-year interval >

to the 1989 Code Edition which includes ASME/ ANSI OMa-1988, " Inservice Testing of

Pumps and Valves in Light Water Reactor Power Plants," Part 6 (OM 6) for pumps, Part 10

(OM 10) of ASME/ ANSI OMa-1988 for valves, and ASME/ ANSI OM-1,1987 for pressure

relief devices.

M1.3 IST Prooram Scoce -

a. insoection Scone

The inspector used NNECO's IST program submittals, the Updated Final Safety Analysis

Report (UFSAR) and technical specifications, design basis documents, system drawings,

_ ~_ _ _ ._

.

30 .

and surveillance procedures to verify that the pumps and valves in the selected systems

that perform a safety function were included in the IST program.

b. Observations and Findinas

During an IST program review conducted in June 1996 on part of their response to a 10

CFR 50.54f letter, the licensee identified 75 valves that were not included in the program,

end 45 instances involving valves in which all the safety functions were not tested

periodically. Components in thirteen safety-related systems were involved, including the

reactor coolant safety injection, service water, containment recirculetion spray, and

emergency diesel generator systems. The licensee reported the condition to the NRC in

Licensee Event Reports 50-423/96-21 and 50-423/96 24. The inspector conducted a

detailed review of the selected systems to confirm that the licensee had changed the

program scope to include all of the required components and tests. The inspector found

that with the exception of tesidual heat removal pump seal cooler relief valves

3CCP*RV239A/B and resioual heat removal heat exchanger relief valves 3CCP'RV64A/B,

the revised IST program satisfied the scope statements of Article IWV-1100, and Section

1.1 of OM 10 and OM-1,

The licensee determined that the program scope discrepancies had been due to lack of

management commitment to the program, and inadequate program monitoring and self-

assessment. Corrective actions included staff augmentation, development and

implementation of detailed administrative procedures and project instructions, and

compilation of a component level design-basis document detailing the bases for decisions

regarding program scope and test requirements, in the document, the safety functions of

each component are traced back to the TS, UFSAR, and design documents and

calculations. The design-basis scope document is not required by the Code and was a

good licensee initiative. The inspector also noted that a new project instruction for periodic

IST program suif-cssessments was included in the new program. The inspector found that

the licensee's corrective actions addressed the root causes of the program deficiencies.

Resolution of specific test discrepancies were being tracked under Action Request

96036464. Twenty-nine major items encompassing 143 action items were being tracked.

The inspector reviewed approximately half of the major items covering 112 components

and tests. Most of the action items involving surveillance procedure and test schedule

revisions were completed. However, due to the operating condition of the plant, few tests

had been performed at the time of the inspection. The inspector determined that no test

failures had yet occurred, and that the outstanding tests were being tracked adequately.

The licensee has committed to update LER 96-21 with the results of the new tests.

c. Conclusions

The IST program scope problems constituted a violation of 10 CFR 50.55a(f), which

requires inservice testing of ASME Code Class components as defined in Article IWV-1100

and Section 1.1 of OM-10 and OM-1. The causes for the program failures were being

addressed adequately, and individual test discrepancies were being tracked and resolved

l

l

'

l

'

. 31

appropriately. Therefore, this licensee identified and corrected violation will not be cited

since the criteria of Section Vll.B.1 of the NRC Enforcement Policy were met.

M 1.4 (Uodatel SIL ltem 53 - ARCOR Coatino

a. Insoection Scone (627071 l

The licensee developed special procedure SPROC 97 3-4, "SpecialInspection and Testing

of Se,rvice Water Piping Previously Lined with ARCOR Epoxy," to verify the quality of the

ARCOR coating applied to the internal surf ace of the service water (SW) piping. This

testing was being performed to establish baseline adhesion values for the ARCOR coating,

and to determine the condition of the existing ARCOR coating within the SW system. The

inspector witnessed portions of the testing on the ARCOR test plates and inspection of

selected SW spool pieces.

b. Observations and Findinos

The test program to establish the baseline adhesion value for ARCOR coatings consisted of

performing pull-tests to failure of the various ARCOR test plates. The plates were

fabricated with proper intercoat, heated intercoat, contaminated intercoat, and a releasing

agent intercoat. Testing revealed that the ARCOR coating could withstand a force of 2000

psiif the ARCOR coatings were properly applied; whereas contaminated surf a':es could

only withstand a force of approximately 500 psi before the ARCOR coating delaminated.

Based on these bounding values, the licensee performed pull tests (a non-destructive test

method) on the ARCOR coated spool pieces installed in the field to 1000 psi to

demonstrate that the ARCOR coatings were properly applied. Each ARCOR coated spool

piece was tested at each end and at the approximate mid-point of the spool at the 90,180,

270, and 360 radial degree locations.

Testing of the "B" train SW revealed no ARCOR delamination from the pull testing to 1000

psi. However, during the removal of one of the pull tabs, a small piece of the ARCOR top

coat delaminated. The licensee was subsequently able to remove an area of approximately

one square foot from this area indicating that it was not properly bonded. Condition Report

(CR) M3-97-1729 was written to document this condition. A couple of days later, another

coating failure occurred during the removal of a pull tab for a spool that had recently been

coated.

Investigation into the f ailure for the newly applied ARCOR coating revealed that the cure

time had been exceeded, in addition, one of the environmental conditions (humidity)

specified in maintenance procedure MP 3710C, " Application of Linings to Plant Systems

Subject to Salt Water immersion," was not maintained. A review of maintenance records

of other recently coated spool pieces revealed that the cure time had been exceeded for

five other SW spools. A voluntary stop work was initiated on all Unit 3 SW coating

application due to these application errors.

The SW spool pieces identified as having application errors were re-tested by "X-CUT" (a

destructive test method) to determine the quality of the ARCOR coating. No additional

_ - - _ _ _ _ _ - _ - - - .

32

'

problems were noted. As a result of the failures of the ARCOR coating during removal of

the pull tabs, the licensee concluded that they could not demonstrate that the ARCOR

coating on the SW spools tested by the pull test methodology had been properly applied.

All but one ARCOR coated spools in the "B" train of SW have since been tested by "X-

CUT;" no other delsmination failures occurred.

The licensee concluded that the root cause for the suspected improper application of the

ARCOR coating was procedure non-compliance. The procedure for application was not

followed as written due to incorrect assumptions made by the painters and contractor

inspectors. The ARCOR re-coat window time was incorrectly assumed to be seven hours

or thumb nail (check for ability to cause indentation in product indication not fully cured).

The environmental condition control was recognized as being lost, however the craft

reestablished the conditions and continued the coating application without obtaining any

further guidance.

The inspector reviewed procedure MP 3710C and the maintenarice records for ARCOR

coating application and noted that severalindividuals had not followed the procedure,

i

investigation revealed that the SW spools in question all exceeded the 7 hour8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br /> maximum

overcoat time by 45 minutes to 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> and 41 minutes. Procedure step 4.5.2 states that

the re-coat window is determined from the product specific technique sheet (PSTS). The

PSTS maximum acceptable overcoat condition is 7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br /> or thumb nail test with no

indentation, whichever is less. The collective procedural noncompliance indicates both an

individual and departmental control performance problem. The f ailure to follow procedures

constitutes a violation of technical specification 6.8.1. (VIO 50-42397 202-04)

c. Conclusions

A review of ARCOR coating application work orders revealed that on six separate

occasions the recoat window was exceeded, These examples demonstrate a low standard

for following procedures and a lack of management oversight for this critical evolution.

The condition of existing ARCOR coating within the SW system and the potential effect of

ARCOR delamination on safety-related components is under NRC review an is included as

an Independent Corrective Action Verification Program followup activity; this is

documented as Significant items List (SIL) Item 53.

M1.5 Service Water Class ill Pioina Retest

a. Insoection Scooe (62707)

The inspector reviewed maintenance activity M3-96-18746, replacement of service water

(SW) piping to ventilation unit 3HVO*ACU2A, to ensure that proper retest requirements

were specified.

__

,

33

b. Observations and Findinajl

The work activity consisted of the replacement of the SW ventilation piping; a 1 1/2 inch

nominal pipe size (NPS), ASME Code Class lll pipe. A review of the work order and ASME

Section XI repair and replacement plan revealed that the licensee had invoked the use of

code case N-4161, " Alternative Pressure Test Requirements for Weld Repairs or

Installation of Repitce. ment item by Welding, Class 1,2,3,Section XI, Decision 1." The

work activity required only a visual examination (VT 2) of the affected mechanical joints at

normal operating pressure and temperature.

Code case N-4161 specifies that a system leak test, in lieu of a hydrostatic pressure test,

may be performed provided that a non-destructive examination (NDE) is performed in

accordance with Section XI with a VT-2.

ASME Section XI requires that after welding repairs on the pressure retaining boundary of

Class lll piping, either a hydrostatic test or non-destructive testing be performed. In a

memorandum, dated January 18,1995, the NRC approved the use of code case N-4161

for Unit 3 as an alternative to the provisions of ASME Code Section XI, thus eliminating the

'

requirement to perform a hydrostatic pressure test. The NRC authorized the use of this

code case provided that additional surface examinations were performed on the root (pass)

layer of butt and socket welds on the pressure retaining boundary of Class 3 components

_

when the surface examination method is used in accordance with Section til of the ASME

Code.

NU memorandum, CES 95163, dated 2/16/95 attempted to clarify the guidance provided

by the NRC. The guidance indicated that a surf ace examination would be required on

Class 3 piping when Section XI required surface examinations of the welds.Section XI

Section ND 5222 states that a surface examination is not required on two inch NPS or

less. The welds in question were for piping of 1 1/2 inches.

The inspector discussed with the licensee the interpretation of the use of the code case

provision. The licensee stated that their interpretation was based on discussions with the

NRC in 1995. The inspector contacted NRR for clarification of this issue to determine what

was the intent of the 1995 letter. The NRC reviewed this issue and concluded that a

system leak check was adequate for Class lil NPS two inches or less.- The NRC staff did

not intend that the licensee apply additional surface examination of the root pass to weld

joints two inch NPS and smaller as a condition for approval of the code case.

c. Conclusion

Code case N 4161 was approved for use at Unit 3 by the NRC in a letter dated January

.18,1995. The licensee's interpretation and use of the code case for Class ll1 piping was

proper. The retest specified for work activity M3 96-18746 was adequate.

.

34

.

U3 M3 Maintenance Procedures and Documentation

M3.1 Testino of Safetv/ Relief Valves

a. insoection Scone

The IST program invoked the requirements of ANSI /ASME PTC 25.3, Safety and Relief

Valves / Performance Test Codes, for testing safety / relief valves. As permitted by 10 CFR

50.55a(f)(4)(iv), however, the licensee's procedures also referenced Operation and

Maintenance (OM) 1 1987. The inspector reviewed licensee and vendor procedures

against the scope, test methodology, and corrective action requirements contained in these

documents.-

b. Observations and Findinos

The licensee categorized pressurizer power operated relief valves (PORVs) 3RCS*PCV455A

and 3RCS*PCV456 as Category B/C valves in their IST program, and tested the valves in

accordance with TS 4.4.4.1, Relief Valves,4.4.9.3.1, Overpressure Protection System,

and Section 7.3.1.2 of OM 1. The tests involved determination of operability of pressure

sensing and valve actuation equipment, and verification of the operation and electrical

characteristics of the valve position indicators. Calibration of the PORV actuation

instrument channels was performed once per refueling interval, and the PORVs were

operated through one complete cycle of full travel with the blocking valves open while the

plant was in hot standby or hot shutdown.

NRC Information Notice 89-32, Surveillance Testing of Low Temperature Overpressure

Protection (LTOP) Systems, documented that some licensees did not translate the PORV

stroke times assumed in their LTOP analyses into IST surveillance requirements. Licensee

calculation NM 027 ALL, Active Valve Response Times, assigned a PORV open stroke time

limit of two seconds based on safety grade cold shutdown system requirements. However,

the licensee's' cold overpressure mitigation (COM) system analysis assumed a more

restrictive stroke time limit. Westinghouse memorandum NSD SAE ESI 97-167, dated

March 19,1997, specified an opening requirement of 0.85 seconds. Surveillance

procedure SP 3601B.2, Reactor Coolant System Vent Path Operability Check, specified an

acceptance criterion of one second. The inspector verified that the acceptance criterion

satisfied Section IWV-3413(b) of the Code, which requires PORV stroke times of ten

seconds or less to be measured to the nearest second. The licensee will need to update

calculation NM-027 ALL to reflect the more restrictive criterion.

The inspector reviewed procedure SP 3712A, Pressurizer Code Safety Valve Surveillance

Testing, and Wyle Laboratories Report No. 44656-0, Recertification Test Program For

Millstone Nuclear Plant, Unit 3, dated June 4,1995. The acceptance criteria for "as-

-

found" and "as-lef t" set pressure tests were plus or minus 3 percent and plus or minus 1

-

percent, respectively. The criteria conformed to TS 3.4.42 requirements and met or

exceeded the requirements of the Code. The inspector noted that step 2.1.2(b) of

procedure SP 3712A specified a five minute waiting period between consecutive valve lifts

instead of the minimum 10 minute period required by Section 8.1.1.8 of OM-1. The

_ _ _ _ _ .

.

35

licensee provided an NRC approved relief request for the deviation. The licensee's

surveillance procedure and the vendor tests conformed with the requirements of PTC 25.3

and OM 1.

The licensee tests the main steam safety valves in place using a hydraulic lift assist

i

(hydroset) device per procedure SP 3712G, Main Steam Code Safety Valve Surveillance

Testing. This 1nethod is sanctioned in PTC 25.3 and OM 1. A sample of main steam

safety valves also were tested at Wyle Laboratories in 1997. The inspector reviewed test

results and Wyle Laboratories Procedure No.1071, Testing of Dresser Spring-Operated

Main Steam Safety Relief Valves, and found that the requirements of TS 3.7.1.1 and OM 1

were met. The licensee properly evaluated system operability when "as found" tests failed

to meet the specified acceptance criteria.

Step 4.1.16 of procedure SP 3712G specifies that hydroset pressure be increased until the

safety valve begins to simmer. A preceding note cautions that the valves not be allowed

to " pop". The licensee noted that Section 2.7 of PTC 25.3 defines " simmer" as an audible

or visible escape of fluid at an inlet static pressure below the popping pressure and at no

measurable capacity. Thus, if the actual difference between the valve's simmer point and

set pressure were great enough (e.g. greater than one percent of set pressure), the current

<

test method would be nonconservative. The licensee initiated condition report M2-97-

0955/M3 971758 to evaluate the condition. The inspector did not consider it likely that

the difference would hate a significant effect on valve performance during a rapid

overpressure transient. However, the issue was relevant to literal compliance wi;h the

Code, and had potentially generic consequences regarding the validity of the test method.

The licensee's observation evidenced a good questioning attitude towards safety and Code

compliance, inspection followup item (IFl 50 423/97 202-05) is opened to review the

results of the licensee's evaluation of this matter.

Other Code Class 2 and 3 relief valves were tested periodically in accordance with

maintenance procedure MP 3762WD, Setting and Testing Relief Valves. The inspector

reviewed the procedure and found that it satisfied the requirements of OM 1 overall. The

procedure stated that no set pressure corrections for ambient temperature were needed

when normal system operating temperature was less than 250 degrees Fahrenheit ('F),

while the set pressure setting was to be increased by three percent where system

operating temperature was between 250'F and 1000*F. Section 8.1.3.5 of OM-1 requires

the ambient temperature of a relief valve's operating environment to be simulated during

the set pressure test, if the effect of ambient temperature on set pressure can be

established for a particular valve type, then the valve may be pressure tested using an

ambient temperature different from the operating ambient temperature. Correlations

between the operating and testing ambient temperatures must be established by test per-

Sections 8.3.2 and 8.3.3 of OM-1. The ASME has found that some relief valve

manufacturers have no engineering or test bases for the correlations that they provide, and

has established a task force to determine standardized criteria for the correlations. The -

licensee ultimately will need to establish a technical basis for its set pressure adjustment to

be in full compliance with OM-1. However, since the difference between the " cold" (i.e.

bench test) and operating set pressures typically is small, the inspector concluded that the

licensee's approach was not an immediate safety concern.

___. . _ _ - _ - _ _ _ _ _ _ _ - _ _ _ - _ - _ _ -

36 .

c. Conclusions

Pressurizer safety / relief valves and main steam safety valves were tested in accordance

with Code requirements. However, a followup item was opened regarding the potential

that relief valve testing to the valve " simmer" point may be nonconservative. For other

Coda Class 2 and 3 relief valves, set pressure adjustments made to account for differences

in bench test and normal operating ambient temperatures need to be justified by test per

OM 1. .

M3.2 Eump Testina

a. Insoection Scom

The inspectors reviewed surveillance procedures and performance records against OM-6

requirements for test periodicity, quantities measured, and allowable ranges. The review

l included pumps in the auxiliary feedwater, intermediate and low pressure safety injection,

L and reactor plant component cooling water systems,

b. Observations and Findinas

.

Procedure EN 31121, IST Pump Operational Readiness Evaluation, contained the

acceptance criteria for the safety-related pumps at Millstone 3. The inspector verified that

I the hydraulic and vibration criteria established by the licensee conformed to the limits in

Table 3 of OM-6. The licensee's vibration monitoring program exceeded Code

requirements by including the pump drivers, which are explicitly excluded from the program

scope in Section 1.2(a) of OM-6. The procedure also contained guidance pertaining to the

required corrective actions if a pump entered the alert or required action ranges. A note

preceding step 4.4.4 of the procedure stated that new reference values could be

. established as corrective action for a pump that was operating in the alert range. This

guidance was inconsistent with Sections 4.3 and 4.5 of OM 6, which state, respectively,

that reference values shall only be established when a pump is known to be operating

acceptably, and that additional reference values may be established only if IST of the

existing' set of reference values is acceptable. The licensee agreed with the inspector's

observation and initiated a procedure change to delete the note from the procedure. The

inspector noted that the provision had not been invoked for any pumps at Millstone 3.

The inspector noted that the charging and intermediate head safety injection pump

performance curves contained in Attachment 4 of procedure EN 31121 differed from the-

curves (Figures 6.3-4 and 6.3-5, respectively) in the UFSAR. The licensee explained that

the UFSAR figures were based on system flow calculations used in the accident analyses,

while the curves in the engineering procedures were actual pump performance curves

developed during pre-service testing. The inspector had no further questions regarding the

curves.

For IST of pumps, Section 5.2 of OM-6 requires that the resistance of the system shall be

varied until either the flow rate or [ differential] pressure equals the reference value. Where

system resistance cannot be varied, flow rate and pressure shall be determined and

-__

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. . . .

.

.. . .

.

.

37

compared to their respective reference values. Clarification provided in Section 5.3 of

NUREG 1482 states that the Code does not nilow for variance from a fixed reference

value. In order to ensure that periodic tests are performed under repeatable conditions, the

NRC has determined that a tolerance of +/ 2 percent (%) of the reference value may be )

used without NRC approval. For a tolerance greater than +/ 2%, compensatory i

adjustments may be made to the acceptance criteria, or an evaluation may be performed, I

justifying the greater tolerance. Where resistance cannot be varied, it is acceptable to use I

the broader criteria in Table 3b of OM 6 as the tolerance.

'

Most of the safety-related pumps at Millstone 3 are tested through fixed resistance

minimum flow lines that are capable of, but were not designed for, adjusting the flow rates.

The licensee identified that for the charging, intermediate head safety injection, and

feedwater pumps it could not meet the tolerance band prescribed in the NUREG due to

large instrument fluctuations. In pump-specific evaluations, the licensee justified reference

value ranges of up to 7.2%/+ 10% of the reference values based on the minimum flow

lines being fixed resistance flow paths. Also, since the reference values were close to the

minimum flow rates required for pump protection, the licensee determined that throttling to

attain a tighter tolerance band would be imprudent.

The inspector agreed that throttling the minimum flow rate may be undesirable. However,

l it did not appear that the licensee had considered fully the options to reduce the instrument

fluctuations discussed in Section 4.6.1.5 of OM-6, including use 01 symmetrical damping

devices, instrument line snubbers, or throttling small gage valves in the instrument lines.

The inspector concluded that since it was possible to adjust the flow rates through the

minimum flow lines, although undesirable, the licensee needed to request NRC relief to use

the broader tolerance bands for these pumps.

The inspector also found that the licensee had changed the IST procedure for the

emergency diesel generator fuel oil transfer pumps to no longer adjust pump discherge flow

to attain the required tolerance. The change was made to reduce operator burden and to

avoid having to declare the diesel generators inoperable during IST. As discussed in GL 87-

09, Sections 3.0 and 4.0 Of The Standard Technical Specifications On The Applicability Of

Limiting Conditions For Operation and Surveillance Requirements, and Section 3.1.2 of

NUREG 1482, entry into a TS limiting condition for operation is not itself adequate

justification for deviating from Code requirements.- The licensee will need to provide

additional justification for using a broader reference value tolerance in a relief request to the

NRC, or take other actions to meet the tolerance band required by the Code. The licensee

agreed to evaluate means to reduce the instrument fluctuations, or to request relief from

the Code requirement,

c. Conclusions

Acceptance criteria established for IST of safety-related pumps met or exceeded Code

requirements. Equipment or procedure changes will be needed to meet Code requirements

for repeatability of test reference values, or NRC relief to use broader tolerance bands will

be needed.

_ _ - _ _ _ _ _ _ - - _ _ .

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. . . . .. .

.

1

38 ,

M3.3 Valve Testing

a. Insoection Scooe

The inspector reviewed surveillance procedures, methods, and acceptance criteria for

several types of valves in the IST program. In addition, the inspectors reviewed the

licensee's treatment of reactor coolant system pressure isolation valves,

b. Observations and Findinas

Power-Ocerated Valve Exercise Tests

Articles IWV 3413(a) and Section 4.2.1.4(a) of OM 10 require limiting values of full stroke

time to be established. The inspector reviewed surveillance procedure acceptance criteria

for power-operated valve stroke times against calculation NM-027 ALL, Active Valve

Response Times: Technical Requirements Manual 3TRM 3.6.3, Containment Isolation

Valves; and UFSAR Table 6.2-65, Containment isolation Valves and verified that the

limiting values selected by the licensee were appropriate. Where not specified in accident

analyses or other design / licensing basis documents, limiting values were assigned based on

a multiple of the reference value stroke time and the physical characteristics of the valve.

The licensee's method in these cases was technically justified and satisfied the Code

requirement. The inspector noted a discrepancy involving charging pump safety injection

isolation valves 3SlH*MV8801 A/B in which the close stroke time limits in the TRM and the

UFSAR table differed. The licensee also had identified the error and was processing a

change to the UF3AR to correct the condition,

The licensee established stroke time reference values based on the average of three stroke

times taken when the valves were known to be in good condition. This method was

consistent with industry practice and Section 3.3 of OM 10. The IST program was in

transition from S9ction XI of the 1983 Code Edition to OM 10. The inspector verified that

the reduction in the stroke time limit for electric motor-operated valves with stroke times

greater than 10 seconds was being implemented in the surveillance procedures.

The inspector noted during review of procedure SP 3608.6, Safety injection System Valve

Operability Test, that the licensee exercised and timed both the open and closed strokes of

many valves that had safety functions in only one direction. This practice exceeded Code

requirements and provided additionalinformation for performance trending of power-

operated valves.

The stroke time tests of motor-operated valves 3SlH*MV8801 A/B were performed using a

motor power monitoring diagnostic system that is installed temporarily at the remote motor

control centers. This method differs from the customary IST practice of using remote valve

position indicating lights, and provides additional information regarding valve performance.

Stroke time was defined in the procedure as the period between maximum motor inrush

current and torque switch trip. The inspector noted that the method could result in longer

stroke times than those derived from valve position indication lamps that are actuated by

- _ _ _ _

_

39

limit switches. However, this f actor likely is offset by the elimination of the operator

response time lag inherent in using a stop watch.

Article IWV-3300 and Section 4.1 of OM 10 require remote valve position indicators to be

verified by local observation of valves at least once every two years. In Section 4.2,6 of

NUREG 1482, the NRC clarified that the requirement applies only to remote indicators that

are used !n exercising and stroke timing power operated valves. The inspector considered

that the requirement applied to the motor power monitor as well, and noted that the

surveillance procedure provided for the verification.

Check Valve Testina

Check valves in the selected systems were categorized properly in the licensee's program

as Category A or A/C valves. Full flow testing of check valves was performed where

practical under verified accident flow conditions contained in the TS, UFSAR, or other

design documents, as specified in Position 1 of Generic Letter 89-04, Guidance On

Developing Acceptable Inservice Test Programs. Quarterly partial flow tests were followed

up during cold shutdowns or refueling outages with full flow tests, disassembly and

inspection, or nonintrusive techniques. For disassembly and inspection, the licensee

followed the guidance contained in Position 2 of GL 89-04 for grouping and corrective

action. The licensee's methods for verifying check valve closure on cessation of flow met

the requirements of Article IWV 3522(a) for verification by positive means.

Procedure SP 3608.6, Refuel Full Stroke Testing of SlH Header Check Valves, was utilized

to exercise the intermediate head safety injection system injection header check valves.

The procedure measured flow only in the main headers vice through the individual branch

lines, Thus, flow rate through the branch line check valves was not verified, and

nonintrusive test techniques were used to verify valve obturator position. The inspector

reviewed procedures SA 97718, Acoustic and Magnetic Non-intrusive Check Valve

Analysis, SA 95923, Non-Intrusive Check Valve Testing Data Collection, and data traces

recorded during the performance of procedure SP 3608.6 in May 1995. The traces clearly

showed the check valves hitting their backstops, and seating after cessation of flow.

,

As discussed in Section 4.1.2 of NUREG-1482, the NRC has determined that use of

nonintrusive techniques is acceptable as another " positive means" of verifying that check

valves are full stroke exercised within the meaning of the Code. To substantiate the

validity of the method, the licensee must address and document the items enumerated in

Position 1 of GL 89-04 in its IST program, including: (1) The impracticality of performing a

full flow test; (2) A description and summary of the alternative technique used; (3) A

description of the method and results of the program used to qualify the method to Code ,

requirements; (4) A description of the basis used to verify that the baseline data has been

generated when the valve is known to be in good working order; and, (5) A description of

the basis for the acceptance criteria for the alternate method, and the corrective action to

be taken if the acceptance criteria are not met. While the licensee's procedures and the

quality of the data supported their use of nonintrusive test methods, the licensee will need

to address explicitly the items listed in Position 1 of GL 89-04 in their IST program

document. The inspector noted that the licensee also identified this issue during their

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40

1996 review of the Millstone 3 IST program, tracked in Condition Report item

9603646405, and initiated action to complete the required items.

Reactor Coolant Pressure Isolation Valve Testing

The operational and functional requirements of the pressure isolation valves at Millstone 3

are contained in TS 3.4.6.2.f. The TS imposes maximum leakage rates on the check

valves located between the reactor coolant system and contiguous low pressure systems in

order to ensure that the leakage rates will not exceed the pressure relief capacity of the

relief valves. Overpressurization and rupture of the low pressure systems would result in a

loss of coolant accident outside of the primary containment.

The pressure isolation valves were classified properly in the IST program as Category A/C

valves, and leakage rates were tested at least once every refueling interval in accordance

with procedure SP 3601F.4, Reactor Coolant System Pressure Isolation Test, and results

were trended in accordance with Article IWV 3427(b) of the Code. For applied pressure

less than the maximum functional differential pressure (2250 +/- 20 psla), the measured

leakage rate was adjusted by the square root of the ratio between the maximum functional

differential pressure and the test differential pressure. This method comported with the

requirement of Article IWV-3423(e). The inspector found a minor discrepancy in the

,

licensee's calculation in that test pressures measured in pounds per square inch gage were

not correct < d to absolute pressure. Since the error resulted in slightly overestimating

valve leakage rates, no adverse safety consequences ensued.

Manual Valves

The Code requires IST of Category B manual valves that fall within the scope of 10 CFR

50.55a. The inspector noted that there were very few manual valves included in the

Millstone 3 IST program. For example, chemical addition isolation valves 3CCP'V303,

'V304, 'V349, and 'V350 that provide safety class boundary isolation for the reactor

plant component cooling water system were not included in the program or exercised

periodically in accordance with Article IWV-3412 or Section 4.2.1 of OM-10. Per operating

procedure CP-38071, the normally shut valves are opened and left unattended for

approximately 30 minutes when adding chemicals to the system. The licensee explained

the exclusion by citing Section 2.4.2 of NUREG 1482, which states that valves need not

be considered " active" (requiring periodic exercise testing) if they are only temporarily

removed from their safety positions for a short period of time under administrative controls.

The inspector agreed with the licensee's position regarding these valves. However, the

licensee will need to include these, and similar valves, in its IST program as " passive"

Category B valves, as applicable.

c. Conclusions

Power-operated valve exercise tests met or exceeded Code requirements, and the

licensee's use of the motor power monitor diagnostic system was commendable.

'

Nonintrusive testing of check valves also was noteworthy, but more documentation was

needed to meet GL 89-04 requirements. Additional manual valves may need to be added

_ _ _ _ _ _ - - - _ _ - _ _ _ - _ _ _ _ - _ _ _ _ _ - _ _ _ _ _ - -

.

41

to the IST program, even if their safety functions are only passive. Pressure isolation

valves were leakage rate tested in accordance with the Millstone Unit 3 TS and the Code.

U3 M4 Maintenance Staff Knowledge and Performance

M4.1 (Ocen) eel 245/97-202-06. 336/97 202-06.423/97 202-06: Ineffeeliya

MainteAance and Technical Trainino Proaram Evaluation

a. insoection Scoce (41500)

The programs reviewed were non-licensed operator; electrical maintenance personnel;

mechanical maintenance personnel; instrument and control technician; chemistry

technician; radiation protection technician; and engineering support personnel.

10 CFR 50.120 requires that training programs be established, implemented, and

maintained using a systems approach to training (SAT) as defined in 10 CFR 55.4. A SAT-

based program requires 1) Systematic analysis of the jobs to be performed, 2) Learning

objectives derived from the analysis which describe desired performance after training, 3) .

Training design and implementation based on the loaming objectives, 4) Evaluation of

l trainee mastery of the objectives during training, and 5) Evaluation and revision of the

l training based on the performance of trained personnelin the job setting.

The inspectors evaluated 18 of 25 characteristics of a SAT as described in NUREG 1220.

The evaluation involved assessing the SAT characteristics related to systematic analysis of

training requirements, training program design and implementation, trainee evaluation, and

training program evaluation. Unless specifically noted otherwise, the results obtained apply

to each of the training programs reviewed.

b. Observations and findings

An assessment of the programs and processes related to the systematic analysis of the

jobs to be performed indicated the tasks were selected for continuing training based

primarily on the workers' and supervisors' desires to expand their knowledge into new

technical areas. Although appropriate for increasing the level of technical knowledge, this

method would not ensure that on the-job performance was maintained at the level needed

to support safe day-to-day plant operations. Changes to equipment and procedures were

assessed by the licensee to determine their impact on training. Personnel interviewed felt

that changes identified from these assessments were incorporated into training. However,

reorganization of workers and changes in their responsibilities when transferring from the

Connecticut Yankee site were not assessed to ensure that personnel had the appropriate

Millstone site-specific knowledge. Overall, the systematic analysis of the jobs to be

performed was functioning adequately but with weaknesses.

Interview results suggested that workers felt the training they had received was of good

quality. The inspectors observed effective interaction between students and instructor,

and good use of visual aids and job aids during classroom training sessions. The lesson

materials were of good quality and the trainees indicated that the instructor presentations

. ..

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42

.

were generally good. However, many of the plant personnelinterviewed indicated that

instructors needed to spend more time in the plant to improve their credibility by obtaining

first-hand knowledge of the uses of the training they were providing. Overall, training

design and implementation was functioning well.

Information gathered in interviews suggested that the evaluation of trainees during training

had weaknesses. Non-licensed operators noted that the examinations they were given

were not a good assessment of the information they received in training and, in at least

one case, were given several months after completion of the training. Additionally,

methods used to remediate non-licensed operators, primarily self study of the lesson plans,

were not sufficient to prevent repeat f ailures, in all reviewed programs, the task selection

process and training methods used in continuing training do not ensure maintenance of task

proficiency. The use of 'significant notices', while timely, does not require any evaluation

to determine the extent to which the information was understood by the workers or to

ensure that newly hired workers will receive the information as part of their initial training.

Interview results also indicated that most people believe the on the-job training and

evaluation (OJT/E) programs should be changed due to known weaknesses. Those

interviewed indicated that the OJT/E process was not formal enough and is not high on the

'

list of management priorities. Additionally, the lack of management emphasis on OJT/E

has resulted in workers not being fully knowledgeable about the status of their own

qualifications, in the maintenance and technical training programs some task qualifications

do not expire and others require periodic renewal, i.e., renewal every year, every two

years, or every five years. However, those tasks that require periodic renewal do not

always require that task proficiency be demonstrated but rather use the opinion of the

supervisor as the basis for continued qualification / renewal of qualification without

consideration of individual task assessment. The weaknesses in the implementation of the

OJT/E process is offset, at least in part, by the apparent willingness of workers to ask for

assistance in task performance or to inform their supervisor if they feel unable to perform a

task even if they are fully qualified to perform the task. Overall, the evaluation of trainee

mastery of objectives during training was inadequate.

The task qualification matrix for engineering support personnel is the notable exception

related to task qualification status. Extensive revisions to the engineering qualification

standards has been undertaken to ensure that qualifications are consistent across all

engineering disciplines. The update to the matrix is viewed as positive by engineers and

their supervisors.

In the area of program evaluation, interview results indicated that although trainee critiques

of training are encouraged and are collected they are not being used to identify potential

deficiencies in the training program. There is also no program to gather job incumbent

performance data related to degraded task abilities, on-the-job experiences, and input from

supervisors regarding performance-based training needs.

The licensee has a number of curriculum advisory committees (CACs) that are specifically

designed to provide site-wide oversight of each of the technical training programs.

However, interview results indicated that the site-wide perspective is frequently lost by

- _ - _ - -

43

holding one-on-one meetings between a training representative and a plant supervisor.

Their discussions, although focused on unit specific issues, may have unexplored site wide

implications that are not being addressed as part of the program effectiveness evaluation.

The notable exception is the health physics technical advisory counsel (TAC). The TAC is

comprised of technician representatives from each unit that meet regularly with the specific

task of discussing task proficiency issues, in general, technical training program evaluation

was found to function inadequately.

The significance of the training program deficiencies identified by the inspectors were I

evalubted against the problems previously identified in the Nuclear Training Department

" Top Ten" List. The " Top Ten" list was developed as part of a corrective action plan

addressing recent problems in the operator training program. However, the inspectors

found that implementing the appropriate corrective actions for each of the eleven items on

the list would not prevent recurrence of the those specific problems nor prevent similar

problems from developing in other training areas because none of the items specifically

addressed the SAT process weaknesses underlying each of the issues.

Although the inspection focused on Unit 3 training programs, the SAT processes are

common to all units at the site. Therefore, the problem g are considered also applicable to

Units 1 and 2. The failure to maintain training programs derived from a systems approach

to training, as described in 10 CFR 55.4 was evidenced by the failure to evaluate trainee

mastery and conduct effective training program evaluation and is considered an apparent

violation of 10 CFR 50.120. (eel 50 245/97 202-06; 50 336/97 202-06; 50-423/97 202-

06).

c. Conclusion:

The overallimplementation of the systematic approach to training (SAT) for the technical

training programs at the Millstone site was generally inadequate to ensure continued

qualification of technical and non-licensed personnel to successfully perform in plant work.

As described above, one violation was identified concerning a failure to properly evaluate

trainee mastery of tasks and conduct training program effectiveness evaluations.

U3 M8 Miscellaneous Maintenance issues

M 8.1 (Closed) Unresolved item 50-423/96-08-18: Adequacy of the IST Program

The results of the licensee's assessment of the Millstone Unit 3 IST program, the corrective

actions planned and implemented, and NRC findings are discussed in Sections U3.M1 and

U3.M3 of this inspection report. An additional NRC concern documented by this item

involved the licensee's failure to perform timely operability determinations for the

components for which IST had not been performed. To correct this condition, the licensee

revised the IST program manual to require a condition report to be initiated if a component

is determined to be within the scope of the Code. The condition report will require that an

operability determination be performed. The inspector concluded that the licensee's

corrective actions addressed the IST program deficiencies.

- . . .

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.

.. ..

. . ..

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44

Additionally, the inspector reviewed the licensee's disposition and corrective action for CR

M3 97 0866 which documented the identification of valves inappropriately left out of the

IST prot, am. Programmatic corrective measures, already in progress, appeared to be

.

adequately directed to the resolution of the documented concerns.

M8.2 (Closed) LER 50-423/96 50:

This LER documented that the range of control building chilled water pump suction

pressure gages used for surveillance were not in accordance with ASME Section XI

requirements. On December 11,1996, the licensee identified that the control building

chilled water pump suction pressure gages did not meet the requirement of Section

5.4.1.2(a) of OM 6 that the full scale range of each analog instrument shall not exceed

three times the reference value. The licensee concluded that pump operability was not

impaired since the gages' full scale range only exceeded the Code requirement by 4 psig,

but otherwise met Code accuracy requirements. The inspector agreed with the licensee's

assessment. The licensee substituted the gages with process computer points that met

the range and accuracy requirements of the Code for digitalinstruments.

The licensee performed a review of other instruments used for IST and documented the

results in memorandum CBM 97-114, dated March 24,1997. Gages and computer points

utilized during testing of pumps in seven other systems, including component cooling

water, auxiliary feedwater, intermediate head safety injection, quench spray, and

recirculation spray, also were found not to conform to OM 6 requirements. As corrective

action, the licensee changed procedures to use substitute gages, changed the calibrated

ranges of the computer points, replaced instruments, and/or revised pump reference flow

rates. At the time of the inspection, many of the substitutions and recalibrations had been

performed, and a design change request to implement other corrective actions had been

developed and was being reviewed.

The licensee determined that the condition was caused by the informality of the IST

program and lack of provisions for periodic assessment of program compliance with the

Code. To prevent recurrence, a comprehensive administrative program document was

written and approved. The guidance contained in the program document comported with

Code requirements, and the new program contained provisions for periodic program

assessments.

The inspector found that the condition would not reasonably have been expected to have

been prevented by corrective actions for previous violations or findings, and the licensee's

corrective actions and actions to prevent recurrence were comprehensive and acceptable.

This licensee identified and corrected violation of the instrument range requirements of OM-

6 is being treated as a Non Cited violation, consistent with Section Vll.B.1 of the NRC

Enforcement Policy.

M8.3 (Closed) LER 50-423/97-22:

This LER documented that testing of the control room emergency air filtration system had

not been performed after routine filter replacement in violation of technical specification

- _ _ _ - _ _ _ _ .

.

.

45

(TS) surveillance requirement 4.7.7(f). Two historicalinstances were identified, one in

each train. Each filter train was subsequently tested satisfactorily during normal

surveillance testing. The licensee attributed these events to a lack of a prompting I

mechanism within the applicable maintenance procedures or work orders. Missed TS

surveillances were previously cited as a violation at Unit 3. As part of the corrective

actions for that violation, the licensee will review surveillance procedures to ensure

prompts exist for conditional surveillances. The corrective action is scheduled to be  !

completed by September 30,1997.

The inspector reviewed the work orders and maintenance procedures and noted that they

had incorporated the TS surveillance requirement. A'dditional corrective actions are being

performed as part of the previously cited violation. Based on the above corrective actions

and the low safety significance of the issues, this IMensee-ideatified and corrected violation

is being treated as a Non Cited Violation, consistent with Section Vll.B.1 of the NRC

Enforcement Policy. This LER is closed.

M8.4 (Closed) ACR M3-940159 (Partial SIL ltem 151

l

l a. Insoection Scoco (92902)

The inspector reviewed the corrective actions taken by the licensee to resolve the issue

, docurnented in ACR M3 96-0159, the associated purchase order and design calculations

1

for the needed replacement component, and the component design drawings,

b. Observations and Findinas

Letdown heat exchanger 3CHS*E2 had exhibited leakage at the lower flange for a long

period of time. The leaking fluid caused corrosion of the carbon steel flange bolts and

represented a constant source of contamination. The licensee considered corrective

actions to address the leak as early as 1989, as documented in Nonconformance Report

(NCR) 389 239 (dated 7/12/89). However, due to unexpected difficulties, alternate

correction approaches and changing circumstances, the final resolution was still pending in

1996. The proposed corrective action, at that time, was replacement of 21 of the 28

flange bolts with corrosion resistant stainless steel bolts. The design adequacy of the

bolted joint, using only 21 bolts, was based on the use of the new bolts' certified material

tensile properties, inspector review of this proposed corrective action concluded that the

design represented an apparent conflict with ASME code requirements.

The licensee documented this discrepancy in Adverse Condition Report (ACR) M3 96-0159.

The corrective actions to resolve the ACR include replacement of the heat exchanger and

the training of design engineers on code requirements.

The licensee had an available heat exchanger that was essentially identical to the original

leaking unit. To improve the leak tightness integrity and performance characteristics of this

replacement, the unit was returned to the original manufacturer, Holtec International, for

modification, code qualification and testing. The inspector reviewed the vendor prepared

design drawings and code qualification calculations and the licensee's vendor surveillance

_ _ _ _ _ _ _ _ _ _ - - - - - - - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ __

,

46

.

records for the replacement unit, it was noted that the licensee will provide the necessary

documentation to satisfy the ASME Code Data Report and the ASME Code Reconciliation

during the close out of maintenance modification (MMOD) M3 97512, after successful

acceptance testing at operating temperature and pressure, it was also noted that the

Holtec drawings listed the flange bolt torque as 250 ft lbs instead of the 350 ft-Ibs found

to be necessary to achieve leak tightness during the hydro test. Following the document

review, the heat exchanger was inspected in the field by the inspector, and it was verified

that a refurbishment plate was installed and correctly stated the new shell design pressure

of 165 psig.

The inspector discussed the purchase and installation effort with the responsible licensee

project engineer. The engineer provided documents to show that the paperwork to achieve

ASME Code compliance was in place and confirmed that a design change notbe (DCN) to

revise the flange torque values to 350 ft-Ibs on the component drawing had been issued.

To assess the corrective action regarding training, the inspector reviewed the lesson plan

and interviewed several engineers who had received the training. Most of the interviewed

engineers were responsible for stress computations and had a clear understanding of the

issue and correct design procedures for bolting. The lesson plan was concise,

c. Conclusions

Replacement of the 3CHS*E2 heat exchanger resolved the flange leakage problem. With a

new, larger sealing gasket, it could be a permanent solution. Interviews with design

engineers confirmed their understanding of ASME Code requirements for flange bolting.

The inspector concluded that the licensee's corrective actions were appropriate and ACR

M3-96-0159 is considered closed. The NRC will review, as inspector follow up item (IFl

50-423/97 202-07), the results of the heat exchanger performance tests and the

associated completion of documentation to show ASME Code compliance when the plant

achieves normal operating temperature and pressure.

M8.5 (Closed) ACR M3-96-0563 (Partial Sll item 33)

a. Insoection Scoce (92902)

The inspector reviewed the corrective actions taken by the licensee to resolve the issue

documented in ACR M3-96-0563 regarding the access manholes to the Normal and

Reserve Station Service Transformer fire protection water valve pits,

b. Observation and Findinas

Manholes provide acce s to the Normal and Reserve Station Service Transformer fire

protection water valve pits. Several Adverse Condition Reports (ACR's) were issued to

request relief from the inspection and surveillance burdens associated with making access

to the pits. When the access manholes are covered, the pit air spaces must be sampled

before entry. When the manholes are left open, only a daily sampling is required but the

openings present a fall hazard which must be protecteo against. To accommodate frequent

_ ____ - ___ - - ---

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. 47

access, the manholes had been lef t open and temporary guards had been installed.

However, due to their temporary nature, the guards required constant surveillance. The

deficiency of the temporary guard and the burden of frequent sampling was noted in

several ACR's. To resolve this concern, permanent protective guard rails were insta'ind at

the two manholes. They were designed to meet OSHA strength and dimensional

requirements and to accommodate ready access.

-

1

An inspection of the Normal and Reserve Station Service Transformer fire protection water

valve pit access manholes was made by the inspector. Stainless steel tallings, bolted to i

the concrete pads and walls, with drop chains at the entry points, were installed at each I

manhole. The inspector discussed the ACRs with their originator who was satisfied that

the railings resolved his concern. When queriod why there were multiple ACRs for the

same issue, he stated that there were some initial misunderstandings of his concern,

c. Conclusio_nB

The permanent railings at the Normal and Reserve Station Service Transformer fire

protection water valve pit access manholes appeared structurally sound and met OSHA

dimensional and design requirements. The inspector concluded they were an appropriate

resolution of the reported concern. Based on their installation, ACR M3 96 0503 is

considered closed.

1)).lli Engineering

U3 E2 Engineering Support of Facilities and Equ;pment

E2.1 [Uodato - Slklitm 57) ACR M3 96-0080: Inadeouste Seoaration BetvitpD

Redundant Electrical Circuits, and ACR M3 96-0081: Potential Electrical Seoaration

Violations with Solid State Protection System

e, insoection Scoop (92903)

ACR M3 96 0080 identified potential noncompliances with electrical separation

requirements for the reactor trip switch on Main Control Room (MCR) Board MB4 (MCB-

MB4), and the safety injection switches on MCB MB2 and MCB MB4. These conditions

have existed since unit startup in 1985. A root cause of the elecPical separation

noncompliances was identified as inadequate job skills for maintaining electrical separation

during maintenance and modifications.

ACR M3 96-0081 identified potential electrical separation violations associated with

electrical wire bundles for the two trains of the Solid State Protection System (SSPS). The

power cable supplying power to the opposite SSPS train:, was less than one inch from the

internal backplane wiring in the logic cabinets.

The inspector reviewed the licensee's corrective actions to address the above concerns.

.

48 .

b. Observations and Findlys

Following the discovery of the noncompliance with electrical separation requirements for

redundant protection equipment trains on June 10,1996, the licensee staff performed

additional system walkdowns to sarch for discrepancies in electrical separations of: (i)

installed wiring in other MCR Panel Boards, and (ii) electric cables on cable trays in various

)

plant areas. These additionalinspections identified numerous electrical separation 1

noncompliances on various MCR panel boards and electrical cable installations in general

plant and protected areas. (Reference LERs 96 015 01 and 96-015 02). The licensee's

corrective actions were: (il modifications to install electrical separation barriers and *re- )

train" cables as necessary, i.e., redundant cable trains tie wrapped to minimum separation

distancet, (ii) develop training module on electrical separation and implement continuing l

training for applicable personnel, and (iii) revise applicable work planning process i

'

procedures to incorporate guidance for electrical separation inspection plan development.

l

Separation barriers made of QA 18 gauge galvanized sheet metal have been installed on

the inside of the MCR panel boards MB4 and VP1 to correct the discrepant conditions.

Based on field walkdowns of the MCR panel boards, the inspector verified that the installed

'

barriers were in compliance with Ron. Guide 1.75 and IEEE Std. 384 1974 requirements.

. The barriers were found to be securely mounted on the panel boards with no air gaps

observed. The Control Building Isolation pushbutton (PB13HVC CB1) located on

3HVS'PNLVP1 has been returned to service after successful functional retest results per

surveillance procedure SP 3614F.3.

On the insides of several MCR panel boards identified on the Unit 3 electrical separation

discrepancy list, electrical wire bundles have been tie wrapped to maintain acceptable

separation distances. The licensee's OC inspection results for AWO M3 97 03509

indicated that the completed re training of electrical wire bundles on the internal MCR

panelboards, MB1 to MB6 and VP1, met the acceptance criteria for electrical separation.

Based on field walkdown of the affected MCR panel boards, the inspector aid not find any

operabluty concerns.

LER 96-015 02 (an update of LER 96 015-00 and LER 96-015 01) identified electrical

separation noncompliances in specific areas of the MCR panel boards. Interviews with the

licensee staff indicated that work is in progress to correct the identified noncompliances.

The inspector also conciucted field walkdowns in other plant areas, e.g., cable spreading

room, diesel generator room *A", and electrical switchgear room "A", to assess whether

cable arrangements are in compliance whh separation requirements. The inspector did not

find any new noncompliances which were not identified by the licensee's electrical

separation inspection program. LER 96 049 01 has identified 976 deviations of minimum

separation distances between a Class 1E and a non-Class 1E cable in the cable spreading

and instrument rack rooms. The licensee indicated that about 160 noncompliance items

have been corrected through re training of the cables, and repair of Sil temp protective

wraps. Another 540 noncompliance items are related to inadequate separate distances

between cable trays. The licensee is in the process of issuing DCNs for the installation of

cable wraps to meet the regulatory requirements. However, the proposed modifications are

not fully implemented yet. Since the work on correcting electrical separation

_ _ _ .

. .

49

noncompliances is ongoing and expected to be completed prior to plant startup, this issue

will remain open.

One corrective action for ACRs M3 96 0080 and M3 96 0081 is the adequate training of ,

applicab!c personnelin the Engineering Department and General Technical Services who are

responsible f or neaintaining electrical separation requirements. A training program on

electrical separation requirements was developed. Classroom treining on separation criteria

for electrical wiring in electrical panels and cabinets, and for cables and raceways in

general plant areas and cable spreading areas were provided to applicable personnel from

l November,1990 through April,1997. The inspector found that the training course

contents (in ES CONT C098) adequately identified the regulatory requirements and * thumb

rules" for electrical separation to the students. However, minor comments on the exact

definitions of technical terms (e.g., common cause initiating events) were provided to the

licensee training staff to enhance the training course materials. The licensee agreed to

incorporate these comments in the classroom training materials.

l The Millstone Station Procedures U3 WC1, " Unit 3 Work Management," and U3 WP2,

" Unit 3 Work Planning," have been revised to include guidance for development of

electrical separation inspection plans when electrical maintenance on safety related or non-

safety related cables, conduits, or raceways are required. These procedural revisions were

effective as of June 1,1997.

c. Conclusions

The licensee has developed a training program on electrical separation requirements, and

classroom training has been provided to applicable personnelin the Engineering Department

and General Technical Services. The licensee has also completed revisions to work

planning procedures to include guidance for development of electrical separation inspection

plans. However, work on correcting electrical separation noncompliances in the MCR panel

boards and other plant areas are ongoing to meet the plant startup deadline For example,

installation of separation barriers in other MCR panel boards hav:; not been completed.

Since corrective activities are ongoing, this issue will remain open.

U3 E3 Engineering Procedures and Documentation

E3.1 Site level MEPL Proaram Review

The overall site material, equipment, and parts lists (MEPL) program was reviewed;

comments and discussion that apply to all three units are provided here.

The inspector reviewed the following MEPL related documents:

. NGP 6.01 Material, Equipmen;, and Parts Lists for in-Service Nuclear Generation

Facilities, Rev.'9, 8/13/94.

.

NGP 6.05 Processing and Control of Purchased Material, Equipment, Parts, and

Services, Rev. 8.

_

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l

50

  • Specification SP ST ME 944, Lists for in Service Nuclear Generation Facilities (MEPL

Program), Rev. O,7/12/95 through Rev. 4, 4/20/97.

  • Production Maintenance Mana0ement System (PMMS) Training Manual.

+ PMMS User's Guido Volumes 1 & 2.

  • PI 29, Development of Millstone Unit 3 Design Bases Summary Documents, Rev.1,

Effective date 3/11/97.

  • Northeast Utilities Quality Assurance Program (NUQAP) Topical Report, Appendix A,

Rev.18, 8/15/95.

  • Engineering Self Assessment of the Material, Equipment, and Parts List (MEPL)

Program, Millstone Unit No. 3, ESAR PES 97 009,4/12/97.

  • Selected MEPL evaluations, and MEPL related ACRs and CRs.
  • NGP 0.10, Use of the PMMS ID. System and BOM Database, Rev. 8.

At the time of tl. iinitial MEPL Program difficulties (discussed under MEPL Program status),

the controlling document was NGP 0.01. This has subsequently been replaced by the

improved Specification 944. Specification 944 has also undergone improvements and

revision over the last two years. The new Specification provides detailed guidance for the

MEPL process in Figures 7.3 and 7.4, which are used to document the evaluations and

subsequent reviews. The Spec. addresses both component level MEPL evaluations and

l parts Bill of Materials (BOM) MEPLs. Section 5 provides instructions on the safety

l classification process, in particular: determination of the licensing basis and the safety

function at the plant, system, component, and part level, it covers safety related,

augmented quality, and non-safety-related determinations. Figures 7.3 and 7.4 provide for

a safety evaluation and USQ determination for changes in classification. The licensee has

l

also established added controls over any changes to the system where the parts

classification information resides (namely, NGP 6.10 to control the PMMS System).

The MEPL program is now receiving significant resources and attention at the site level and

in Units 2 and 3. Unit 1 ef forts will begin in earnest when the work on Unit 3 is

completed. Four issues were identified with respect to the site level program, as follows:

1. There continues to be a historical question of the potential to have non safety-

related (NSR) parts installed in safety related (SR) components. This has been

I documented on a number of ACRs and CRs for each unit. The plans to address this

l concern for U3 appear comprehensive (but are not fully implemented yet). For U1

! and U2, the plans are currently less comprehensive and implementation is not as f ar

along. The licensee has not yet fully justified the plans for Units 2 & 3.

2. Specification 944 does not check for the impact on NUQAP, Appendix A when

downgrading a component from SR to NSR. Any changes to the NUQAP that

_ _ .

. . - . . . . - . , .

.

.

51

reduce commitments (e 0., the list of SR items) require prior NRC approval per 10

CFR 50.54(a).

3. NRC previously (Inspection Reports 95 07 and 95 09) raised a concern that the

MEPL procedures did not adequately consider normal operations and anticipated

operational occurrences (AOOs) as part of the " design basis events" to be

considered when making safety related classifications under the MEPL program.

Discussions with NU managers responsible for the MEPL program stated that the

intent of the current program, under Spec. 944,is that engineers performing MEPL

evaluations must consider normal operations and AOOs as part of the * design basis

events"in making safety related classifications. Step 5.2.2.4 of Spec. 944 states

that guidance can be found in EPRI NP 6895. Page 4 2 of NP 6895 contains a

definition of Design Basis Events that includes normal operations and AOOs, as well

as other items. This indirectly addresses the concern, however personnel

performing evaluations will not usually have or reference the EPRI document.

4. The PMMS database is not complete. Some SR components are not in the

database, e.g., snubbers. Many augmented QA and NSR parts and components are

also not in the database. The impact on site programs of these gaps in the

database needs to be evaluated.

E3.2 (Uodate PartiaLSLLite_m 25) ACR M3 96 0912: Acoarent Violations and Escalated

EQtomement items from NRC Insoection Reoort 96 201. Items No. 18.19. & 43

This ACR addresses three apparent violations from NRC inspection report 90 201. These

items are also under consideration for escalated enforcement action, which has not been

completed yet. The items relate to the MEPL program, which is reviewed in this section of

the report. Issues associated with the MEPL program are identified herein. The licensee is

still actively working on MEPL evaluations that must be completed before startup. Also,

there are other areas of inspection review on the program that will be performed over the

next reporting period. SIL ltem 25 remains open.

E3.3 Unit 3 MEPL Status Uodate

Unit 3 has approximately 60,000 components in the PMMS database, of which about 19K

are safety related (SR) and 3,000 are augmented quality (due to fire protection, radwaste,

station blackout, or ATWS commitments). During the Performance Enhancement Program

(PEP) reviews a number of components were originally identified for downgrade, however

this action was stopped in Unit 3 before being implemented as a result of lessons loamed

on Units 1 and 2. Over the 1995 and 1996 time frame Unit 3 performed system level

MEPL evaluations of all systems and hence all components in the database. As a result of

these efforts a number of changes in component classification were implemented, and are

generally summarized here:

  • About 3,000 duplicate items were identified and removed from the database.
  • About 2,000 items were downgraded from eugmented quality to NSR.
  • About 1,000 items were upgraded from NSR to augmented quality.

_ _ - - - - -

,

.

52

,

  • About a dozen items were upgraded from NSR to SR, but did not require physical

changes to the components.

  • About another dozen items were identified where NSR components had to be

upgraded to SR, but these items required design modifications to change out

equipment. These modifications are stillin progress.

  • About 2,000 to 3,000 items were down0raded from SR to NSR. These items were

all either database errors or downgrades of items that had been classified as SR due

to utility convenience rather than regulatory requirements.

The above activities were all at the component level. For each component, the MEPL

prcgram also evaluates the parts of the components and establishes the classification for

each part on the Bill of Materials (BOM). In early 1997, Unit 3 performed an operability

determination (OD No: MP 010 971 that satisf actorily evaluated all safe shutdown, SR

components with one or more NSR parts in their BOM. This included an engineering

evaluation, " Acceptability of Installed Parts / Material Associated with Active Components

Credited for Defense in Depth." In 1996 and 1997 Unit 3 began MEPL BOM avaluations

for all SR components that have ever had any work performed on them. As part of this

effort, whenever NSR or Undetermined (U) parts are reclassified to SR, a full work history

examination is being performed to ensure acceptable quality of parts installed the

components.

E 3.4 UDL13 MEPL Proaram imolementation (Uodate Partialjlkitem 25)

The 6.:spector selected a system MEPL evaluation (for the CVCS S) stem) and a few

indivioual component MEPLs for review to determino if classification determinations were

reasonable and properly documented. The MEPLs were compared with drawings, FSAR

descriotions, and components in the plant. Additionally, a number of components and

compoi ent identification were noted in the plant and compared to the MEPL and PMMS

systems to ensure that the components were properly classified and were properly entered

into PMMS. The parts issuance portion of the program was not reviewed due to ongoing

issues identified by the licensee in that area.

The inspector noted the following five issues, which will be tracked with SIL item 25.

1, in order to properly classify an item in the MEPL Program, the safety function must

be clearly understood. The latest revision of Spec 944 requires this to be

determined and documented in the MEPL evaluation. The earlier versions of the

Spec. also recognized the importance of determination of safety function, but were

not as specific in the procedure. The MEPL evaluations reviewed did not always

clearly document all of the safety functions Examples include: the overall CVCS

System, the CVCS function with respect to the Reactor Coolant Pump seals, and

valves CHS * V501, 'V505, 'V436, 'V437, AND 'V303.

2. The MEPL evaluations reviewed did not list all of the pertinent design documents

and FSAR references on the MEPL determination, Figures 7,3 or 7,4 (example,

identify CVCS System MEPL).

)

l

__

s

,

53

3. The numbering scheme for PMMS results in differences between the identity for

components in the field and in the PMMS database when the number of characters

exceeds 15.

4. FSAR Figure 3.2.2 states that an asterisk (') indicates that equipment is quality

assurance category 1 (i.e., SR). However, the inspector noted that not all SR

components use the * as noted in the FSAR, e.g., SR snubbers; there is some j

ambiguity in the use of the ' for relays; and some identification tags and signs in

plant do not use the *, even though the component is SR and the * is used in

PMMS,

5. - While performing the MEPL related plant tours, the inspector noted that some

orango or A Train components are being newly painted purple (the color of the B

train), e.g., OSS pump and AFW pump. This creates an increased potential for

" wrong train" type of human errors.

E3.5 (Undatel Unresolved item 50 423/95 07 10: Containment Hatch Downaradina SR

eauloment throuah the MEPL orocram

Through the early 1990s, NU had a program to review, and where possible, downgrade

components from safety related to non safety related. This item addressed the issue of

improper downgrades. The generic or programmatic aspects of the downgrades are being

addressed under the Eels and SIL 25 noted herein. One particular component identified

with this unresolved item was the containment personnel hatch and its interlocking system.

MEPL Evaluation No. MP-CD 132 downgraded a number of parts associated with the

containment batch. As a result of concerns raised, the licensee re evaluated the pressure

retaining parts of the hatch and raised their classification from NSR to SR. This action then

required a design change (PDCR MP 95 025) that was implemented to upgrade these parts

to SR. 'There are currentiv 231 parts on the hatch BOM. Over the last two years, a

number of MEPL evaluations have been performed on the containment hatch parts. One

particular aspect in question was whether the hatch interlock mechanism served a SR

function. The MEPLs determined that it did not; and, the inspector verified this by a review

of the design drawings and discussions with the pertinent engineers. During this review-

the inspector noted the following issues:

1. - The most recent MEPL (CD-789) for the hatch did not clearly specify which of the

previous MEPLs had been superseded and thus it was not clear which of the

multiple MEPLs were still effective.

2. The PMMS system incorrectly notes that CD 789 is the pertinent MEPL for all

containment batch BOM parts in PMMS.

3. The acceptance criteria (on Maint. Form 3712X+1, Rev. 2) for the Technical

,

Specification surveillance test do not accurately verify that the hatch interlocks

function properly. However, the steps and the note within the procedure itself (SP

3712X, Rev. 5) do properly test the interlocks.

_ ___-___ __ - _

.

54 .

This unresolved item remains open pending resolution of the above notad issues.

E3.6 RHR System Control Valves

As an example of a SR component with associated NSR parts and components, the

inspector selected the residual heat removal (RHR) system flow control valves for the RHR

heat exchanger (HX). 3RHS*HCV606 &G07 (HX outlet valves), and 3RHS'FCV618 & 619

(HX bypass yalvest. These valves were identified in ACR 13427 on 6/15/96, as having a

design problem whereby their f ailure position on loss of control air would give maximum

cooling. This is apprcpriate for the RHR system but could cause an over temperature

condition in the reactor plant component cooling water system (CCP). This resulted in a

design change (EWR M3 96097, DCN No. DM3 S 0662 96, DCR M3 96005) and a new

l MEPL evaluation MP3 CD 0947. This design change makes several modifications,

including: limiting the full open position of the HX outlet valves, failing open the RHR HX

bypass valves on loss of air, and adding a SR solenoid valve between the valve positioners

and the actuators to ensure a vent path to place the control valves in their safety position

when required. The inspector reviewed the associated documentation and observed the

modification work in progress in the plant. The MEPL evaluation appropriately classified

the various items in accordance with the new design.

.

During the review of these valves, the broader question of SRINSR Interactions (particularly

l as it concerns interactions between control grade and SR components) was raised. The

f licensee presented an Engineering Report M3 ERP 97 0008, Rev. O, dated 6/19/97, titled

" Assessment of Safety Related Valves with Nonsafety Related Controls." This report

'

analyzes 101 valves and associated controls in Unit 3. This is a comprehensive study

which establishes design criteria and groups, analyzes each of the valves, and recommends

changes where needed. In general the analysis of the control grade components assumes

f ailure in the adverse direction if it may be in a harsh environment (such as post LOCA or

HELB). If in a mild environment, the analysis is performed for two cases, with the control

grade components operating as designed and with them failed "as is." Random or spurious

failures of these components may be an initiating event, but are not assumed to occur

concurrent with a design basis accident. This position was verified to be consistent with

NRC review positions noted in: the Standard Review Plan (SRP), NUREG-0800, Section

7.7; Resolution of USl A47, Generic letter 8919, and NUREG 1217; and issues

surrounding Information Notice 79 22.

No unresolved issues were identified as part of this review.

U3.E7 Quality Assurance in Engineering Activities

E7.1 Review of items to be Comoleted Af ter Restart

a. Insoection Scoce 192903)

In a letter dated April 16,1997, the NRC superseded the " Demand for Information" of

earlier letters and requested that the licensee provide, in part, the following information

pursuant to 10 CFR 50.54(f):

- _ _ _ _ - _ _

. _ _ _ _ _ _ _ _ _ _ _ . _ _ _ _ _ _ - _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _- ___ _ - _ ____

55

e For each unit, the list of significant items that are needed to be accomplished prior

to restart;

e For each unit, the list of items to be deferred until af ter restart; and,

e For each unit, the process and rationale used to defer items until af ter restart.

The letter also requested updates approximately every 45 days for the fi;;t two items. On

May 29,1997, the licensco provided the initiallists for Units 2 and 3 in responto to this

letter. On July 14,1997, the licensee provided'the initlat lists for Unit 1 and updates for

Units 2 and 3.

The inspectors reviewed the information provided for Unit 3 to assess the content of the

list and whether the deferrals were appropriate. Specifically, the inspectors reviewed a

sample of deferred items to ensure issues that could affect equipment operability or the

ability of equipment to perform its intended design basis function were not deferred. The

inspectors also reviewed the licensee's process for identification of significant items for

restart and items which could be deferred.

b. Observations and Findinas

Sianificant item For Ru$ tart List

To develop the significant items for restart list the licensee reviewed all adverse condition

reports (ACRs) open as of January 1,1996, and all ACRs and condition reports (CRs)

initiated after that date. Significance level A or B ACRs and level 1 CRs were included as

significant items. The lower significance level ACRs/Crs were screened further and those

issues that questioned the operability or design basis function of maintenance rule group 1

or 2 systems were included as significant items, (Maintenance rule group 1 and 2 systems

include safety related systems and risk significant systems.) The licensee noted that there

are also many other non significant items that are planned to be completed prior to plant

restart. The inspectors concluded that the licensee significant items for restart list

provided the information requested in paragraph 1 of the revised 10 CFR 50.54(f) letter

dated April 16,1997.

Def erred items J. int

'

- The licensee provided the screening criteria used to defer items in their May 29,1997,

response letter. Similar criteria are also provided in Project instruction (PI) 20, * Unit 3

Startup item Administrative Instructions." Items screened to determine if they could be

deferred included unresolved item reports (UIRs), non significant ACRs and CRs, non-

conformance reportu (NCRs), engineering work requests (EWRs) and automated work

orders (AWOs). An item was classified as startup required if it was necessary to

accomplish one of the following actions:

e implement or support a change to plant technical specifications,

.

56 ,

e Correct a licensing or design basis deficiency,

e Accomplish a restart license commitment,

I

e Resolve an operability concern associated with a maintenance rule group 1 or 2

system.

If the item did not fit any of these categories it was considered for deferral, subject to

management concurrence.

A total of approximately 1500 items were included on the deferred issues list at the time of

the licensee's update on July 14,1997. The inspectors reviewed the one line description

of all of these items and selected approximately 30% for additional review, in selecting the

items for further review the inspectors considered those items in safety significant systems

where the one line description indicated the potential for equipment operability questions or

other operational concerns. The inspectors reviewed supporting documentation for these

items and discussed the issues with the licensee staff as necessary to obtain sufficient

information on each of the items. The inspectors had the following findings:

  • Open item reports (OIRs), which document potential testing deficiencies, were not

included in the initial (May 29,1997) submittal of deferred items. However, when

questioned by the NRC, OIRs were included on the deferrallist in the July 14,1997,

update,

o The NRC's April 16,1997, letter specifically requested that bypass jumpers and

control room deficiencies be included in the deferred items list. The licensee did not

originally review these items for inclusion in the list. However, when questioned by

the NRC, the licensee reviewed these items and found that all but one of the bypass

jumpers and control room deficiencies had been included as deferred issues as a

result of another associated document, such as an EWR or AWO The item that

was not included was a recorder associated with a non safety system and would

- not have affected safe operation,

o The licensee's July 14,1997, update added items to the deferred list that existed

well before the time the initial list was submitted, but these items were not included

on either the original deferred list or the significant items for restart lict, it was not

evident to the inspectors or discussed in the update letter whether the initial

screening addressed these items or if they were initially screened as non significant

restart issues,

e The inspectors identified twenty two items on the deferred list that the licensee did

not intend to defer For ten of the items, the individual actions necessary to resolve

the issue were scheduled for completion prior to restart. In nine cases all actions

necessary to close the issue were already complete. The licensee reclassified three

items that were questioned by the inspectors. Two items were AWOs to repair

three emergency lights and were placed on the startup schedule because the

affected lights were included in the 10 CFR Part 50, Appendix R program. The

-. _

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_

.

l. 57

other item that was reclassified to be required for startup was an EWR to replace a

-level recorder in the auxiliary feedwater system.

The inspectors found that the licensee did not have a consistent method for coding

restart actions in the Action item Tracking and Trending System (AITTS). Some

l _ actions were coded to a schedule reference to clearly indicate that the action was

! required to be completed prior to startup. Other items required before restart did

l not have a schedule reference entered and were tied to startup only by having the

requested action completion date precede the expected startup date. The licensee

1

documented this concern on CR M3 97 2265

In addition, the inspectors discussed with the licensee the status of the corrective actions

recommended in self assessments, independent third party reviews, nuclear oversight

reviews, and on site review organization reviews (ie, ACR 7007, Root Cause Evaluation -

Effectiveness of the Oversight Organization, Joint Utilities Management Association _ report,

etc.) and if any were to be deferred. The licensee stated that they are currently reviewing -l

all of these reports and will address what actions they have taken or will be taking in their -i

response to item (4) of the NRC's April 16,1997, letter. Specifically, item (4) requested 1

. the licensee to submit what actions they have taken to ensure that future operation of each

unit will be conducted in accordance with the licensee, regulations, and Final Safety

Analysis Report (FSAR). l

c. Conclusions

The inspectors found that the licensee's determination for which items could be deferred

was generally appropriate. The three items that were removed from the deferred items list

as a result of this inspection would not hr.ve had a significant impact on plant operations if

they had not been resolved prior to startup.

However, the inspectors concluded that the deficiencies discussed above constitute a

violation of paragraph (a) of 10 CFR 50.9 which requires licensees to provide complete and

accurate information. (VIO 50-423/97 202 08)

Also, in resolving CR M3 97 2265 the licensee should ensure adequate controls are in

place to ensure that actions required prior to startup do not get inadvertently dsferred as a

result of changes to action due dates in AITTS. This is particularly important for those

items that have some actions required for startup and other actions that may be deferred.

U3 E8 Miscellmnus Engineering leeues

E8.1 Residual heat Removal (RHR) Heat Exchanaer Boltina Susceotible to Boric Acid

Attack (Sil. Item 47)

a. insoection Scone (92903)

The inspector reviewed the licensee's adverse condition report (ACR) No. M3 96-0391 that

addresses the RHR heat exchanger bolting susceptibly to boric acid attack (SIL ltem 47)

=_

.

4

l 58

.

b. Observations and Findings

, During a 10 CFR 50.54(f) walkdown of the RHR system, the licensee identified that the

i RHR host exchangers have high strength carbon steel (B7) studs installed in the shell/ head

flange and, therefore, may be susceptible to boric acid attack since these flanges have

been leaking. As a part of the ACR's disposition, the licensee performed operability and

reportability determinations. The inspector reviewed the licensee's records with the

following observations discussed below.

To determine the extent of a potential boric acid attack of the studs, the licenses removed

five studs with evidence of boric acid stains. The visualinspection performed on these

studs revealed them to be in good physical condition; the studs exhibited good metal

condition, full thread form and no pitting attack below the minor diameter of the studs, in

addition, the licensee performed a magnetic particle (MT) surface examination of the studs

and did not identify any circumferential flaws on the examined studs. There was no loss in

material that would detrimentally affect the strength of the studs or impact the integrity of

the joint. The structuralintegrity of the A and B RHR heat exchangers was never

compromised. Therefore, the A and B heat exchangers were found operable. This

operability determination was based on the good condition of the removed studs and the

results of the MT performed on the studs. Further, reportability was not required because

degradation of the pressure boundary did not occur, and the plant was not operated outside

the design bases,

c. Conclusion

The inspector concluded that the licensee's actions to address ACR No, M3 96 0391 were

adequato. The licensee's documentation and interviews conducted by the inspector with

the cognizant personnel showed sufficient evidence which demonstrated that the RHR heat

exchangers were operable in their as found condition due to the good condition of the

examined studs. As a preventive action, the licensee will continue to monitor these studs

by removing and examining five bolts every five years. SIL ltem 47 is closed,

E8.2 Unsecured 1 Beam Above Safetv Related Comoonents (SIL ltem 37)

a. Insoection Scone (92903)

The inspector reviewed the actions being taken by the licensee to remove an unsecured

structural member installed above safety-related components and the actions to prevent

future installations of this nature,

b. Obiervations and Findings

During a walkdown of Millstone Unit 3 on March 12,1996, an NRC inspection team found

a temporary l beam installed above three of the four recirculation spray system (RSS) heat

exchangers. The licensee reported this condition to the NRC on March 13,1996, in -

accordance with 10 CFR 50.72, after determining that the I beam had the potential to

render both trains of the RSS inoperable during a seismic event. The licensee initiated ACR

!

I

- - _ = =

- - . _ . - . _ _

.

'. 59

No.10382 to remove the l beam and to perform an engineering review of the historical

impact on plant operations. The inspector walked down the areas and verified that the l-

beam had been removed. An NRC team inspection determined that this l beam removal

was adequate corrective action. However, the team was concerned about the lack of

instructions or procedures to prevent recurrence; documented as eel 423 20121, and part

of SIL ltem 37.

.

In response to this NRC concern, the licensee revised Maintenance and House Keeping

Procedure No. OA8, Revision 0, which emphasized the proper storage, use and restraint of

temporary structures or equipment installed above safety related equipment. The inspector

i reviewed the procedure and found that it adequately addressed the NRC's concern and

l

provided some clear guidelines for the restraint and Installation of temporary structures

above safety related components. 'l

! - c. Conclusion

The inspector concluded that the licensee's corrective action was adequate. In addition,  ;

the licensee revised their maintenance and housekeeping procedure to provide engineering

'

and maintenance personnel with a clear guidance for the restraint and installation of

temporary structures above safety related components. Therefore, the technicalissues

involved with this item are closed, and SIL ltem 37 is partially closed. eel 423/96 20121

remains administratively open pending completion of enforcement actions.

E8.3 (Undate) eel 423/96 20124: Concrete Spalling of Service Water (SW) Pump

Pedestal

(Partial Closure) SIL ltem 37: Corrective Action Effectiveness

a. Insoettion Scoce R2103J

The inspector reviewed the licensee's actions taken to resolve the issues documented in

eel 423/96 20124; spalling of SW booster pump,3SWP'3B, concrete pedestal. Spalling

of the pedestal resulted in the pump being declared inoperable since the anchor bolts

holding down the pump did not extend past the pedestalinto the concrete floor; thus the

ability of the pump to withstand a seismic event could not be guaranteed. This condition

had existed for an extended period of time and had not been identified and corrected by the

licensee,

b. Observations and Findinas

As corrective action, the SW booster pump pedestal was repaired and a protective coating

was applied to the pump pedestal. The licensee concluded that the pedestal damage was

caused by condensation entering cracks in the concrete, causing the rebar to rust and

expand Other SW system components were inspected for similar conditions. Walkdowns

revealed that several other pump pedestals were cracked; however, the licensee

determined that none of the cracks affected the seismic capability of the components. The

anchor bolts for these components extended into the concrete floor. To prevent

--

.

60 .

recurrence, the licensee revised procedure EN 31094, " Millstone Unit 3 System Engineer

Walkdowns," to ensure that other equipment foundations are inspected during system

reviews. In addition, procedure EN 31098, 'MP3 Condition Monitoring of Structures," had

been put in place under the Maintenance Rule to monitor safety related structures for

structural degradation.

The inspector reviewed the work orders and design change notices that were issued to

repair the damaged components. Pedestals that were Identified as cracked were repaired

with Five Star Structural Concrete, and a protective coating was applied to the pedestals to

minimize water intrusion into cracks. A review of the m::nuf acturer's instructions revealed

that the concrete used for the repairs had a higher compressive strength than the concrete

used for the original concrete pads, in addition, a walkdown of the auxiliary building

, revealed that all degraded pump pedestals had been repaired or were identified and

l scheduled to be repaired by the licensee,

c. Conclunon

The inspector concluded that the technicalissue resolution and corrective actions for this

particular concern were good. However, the closure of this issue does not address the

'

overall effectiveness of the licensee's corrective action program. Continued inspection of

-the corrective action program will bs reviewed as followup to SIL ltem 37. SIL ltem 37 la

partially closed. eel 96 20124 remains open due to ongoing NRC considerations of

potential escalated enforcement action involving this issue.

E8.4 (Ocen) eel 423/97 202-09: RSS Dosion Deficienev

j (Closed) LER 50-423/97-03, Potential RSS Water Hammer

LER 50-423/9715. Potential RSS Vortexing,

LER 50-423/97 28, Potential Loss of RSS Pump NPSH,

luodatel Sllitem 85 Other RSS and Related Design Basis Concerns

On January 13,1997, a licensee engineering evaluation determined that the recirculation

spray system (RSS) heat exchangers and piping may be susceptible to water column

'

separation, and subsequent water hammer events, if the RSS pumps are restarted during

design basis accident conditions. On February 4,1997, a licensee review of design

calculations identified that the calculated minimum water levelin the containment sump at

the time of the start of the RSS pumps following a large break loss of cooling accident

(LOCA) would be below the containment sump vortex suppression gratings. It was

determined that cavitation of the operating RSS pumps could result from the air

entrainment which would accompany the postulated vortex formatioriin the sump coolant.

On April 10,1997, another review of the design calculations for the not positive suction

head (NPSH) for the RSS pumps identified the potential for steam flashirig and partial

voiding of the coolant from the containment sump based upon suction line head losses in

excess of the calculated availability of saturated coolant head conditions.

. _ _ _ _ _ _ _ . ._ _

---_.-_._--_d

61

l.

All three of these licensee identified design deficiencies were reported to the NRC

(respectively, LERS 97 03, 97 15, & 97 28), within the required time framos delineated in

10 CFR 50.72 and 50.73, as conditions outside the design basis of the plant and,in the

case of the NPSH concern, also as a loss of safety function. The cause for all three events

,

was determined by the licensee to relate to inadequate initial RSS design scope and to

l Inadequate engineering review and process control during plant construction, i.e., prior to

l the issuance of the initiallow power operating license, NPF 44, in November 1985.

I Additionally, the above noted problems with the RSS design relate to a concern

l documented in LER 96-97, as supplemented, involving the RSS piping and supports being

exposed to temperatures in excess of those for 'which stress analysis had been conducted

prior to initial licensing. NRC inspection follow up of this latter concern (i.e., LER 96-07) is

documented in inspection report 50-423/96 06, concluding that the operation of the unit

with the existence of such a design deficiency constitutes an apparent violation (eel

423/96 06 13) of regulatory requirements. The inspection documented in IR 96 06 also

represents an update of Sllitem 1.

In establishing the cause of the event documented in LER 96 07, the licensee determined

that the identified " conditions have existed as part of the original plant design of the RSS

(and other affected) systems." Also, LER 96-07 documents a condition in which the plant

operated outside its design basis, resulting in the inoperability of, along with other analyzed

systems, the RSS. The commonality of cause (initial design errors), effect (unit operation

outside the analyzed design conditions), and specific system impact (RSS inoperability),

that connects LER 96 07 with the other three LERs also supports the conclusion that the

design deficiencies discussed in LERs 97 03,9715, and 97 28 collectively represent an

additional apparent violation (eel 423/97 202 09) of regulatory requirements.

The technical details, corrective measure impicmentation, and design changes intended to

address the problems discussed in these three LERs will be tracked with the apparent

violation, as well as with this Update of SIL ltem 85. Therefore, LERs 97 03,9715, and

97 28 are herewith individually closed.

E8.5 1 Closed) URI 96 20140 (Partial SIL litmll)

a. Insoection Scoce (92903)

The inspector reviewed the engineering calculations and corrective actions taken to resolve

deficiencies in the engineering calculations to validate the operability of the turbine-driven

auxiliary feedwater pump (TDAFWP). The licensee had initiated, but was unable to finalize,

these evaluations during the specialinspection of engineering and licensing activities, and

review of the final calculations was identified as an unresolved item,

b. Observations and Findings

i

ACR 13426, dated May 22,1996, was initiated to address deficiencies noted in the

NUSCO engineering calculation 91074 324M3, Rev. 0 (dated March 26,1983) used to

validate the operability of the TDAFWP The corrective actions to resolve the ACR l

included the acquisition of additional performance data for the turbine, the preparation of l

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62

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new engineering calculations, revision of the associated component specifications and the

l FSAR. The inspector reviewed the new engineering calculations (Proto Power Calculation  ;

j 97 014 for TDAFWP performance and Proto Power calculation 97 000 for pressure loss) *

l- and found them appropriate and comprehensive. They were based on the new turbine

performance data and included detailed estimates of pressure losses in the intet and

exhaust piping for the pump turbine. The calculations addressed the deficiencies noted, l

'

superseded the calculations in question, and demonstrated the capability of the TDAFW to

satisfy design requirements. The inspector reviewed the procuroment specification (SWEC

l specification No. 2275.200 041) and the vendor specification (Terry Turbine specification {'

l No OIM 041003A) and verified that they and the Design Basic Document Package MP3-

i FWA for the AFW System, were modified to reflect the corrected performance

l requirements. Since the corrective actions include the performance of a flow test to

assess the potential for flow induced vibrations, the inspector discussed the proposed test

with the technical support engineer responsible for its performance. The engineer showed -

a clear understanding of test objectives, +

i

c. Conclusions  ;

l

l

The inspector concluded that the new calculations prepared by the licensee for ACR 13456

l correct the deficiencies noted in the original calculation and provide the basis for evaluation ,

i of the TDAFWP overall performance. The revised estimates of performance parameters

show that the turbine / pump unit can meet design flow / power requirements. The affected

unit performance specifications were corrected to reflect the revised performance

parameters. Based on these findings, URI 96 201-40 is considered closed. -

E8.0 (Closed) Sll item 16: Dual Function Valve Control and Testina 4

a. Insoection Scoce (92903)

In 1993 Millstone. Unit 2 identified a problem with the operation of air operated valves in

the letdown line. Specifically, the air actuator spring preload was not properly set such

that adequate closing force was not available to close the valve against full reactor coolant

system pressure. The inspector reviewed the licensee's evaluation for the applicability of

this issue to Unit 3.-

b. Observations and Findinos

The cause of the problem on Unit 2 was attributed to a lack of procedures for performing

maintenance on the valve actuators which resulted in the incorrect actuator spring preload .

_

. adjustment,

l

A review of this event by Unit 3 personnel concluded that this issue was not a concern on

Unit 3. . This conclusion was based on the following:

e When the valves were purchased, a valve specific specification sheet was provided

for each Unit 3 air operated valve. The specification sheet included the maximum

required shutoff pressure for the valve,

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63

e The valve actuators were set up by the vendor to operate at the maximum shutoff

pressure and the valve nameplates specify the air pressure bench settings that will

result in the proper actuator spring preload,

e Unit 3 maintenance procedures contain provisions for controlling the actuator

settings and for post maintenance testing to verify the actuator operates at the

bench settings on the valve nameplate,

c. CDDChtSLons

The inspector reviewed valve specification sheets, maintenance procedures and a sample

work order that performed rnaintenance on an air operated valve. Based on these reviews

and discussions with licensee engineers, the inspector concluded that the licensee had

adequately evaluated the event for applicability to Unit 3. Controls in place on Unit 3

should prevent a similar event on Unit 3. SIL ltem 16 is closed.

E8.7 [C1gicd) Insoection Fajlowuo item No. 50-423/96 0817. (SIL 76): Fuse Ferrule

Cracks

'

a. Insocction Scone (37551-10)

The fuse ferrule cracks became a concern when on September 11,1996, the

licensee found several fuses (Shawmut Amptrap Cat # A2Y10) with axial cracks on

their ferrules, that has been drawn from the warehouse for installation in Millstone

Unit 3 (MP3). At that time, the licensee had developed a detailed plan to segregate

i

all suspect fuses in the warehouse; to perform a 10 CFR Part 21 evaluation, and to

perform an operability determination of fuses installed in all units, in addition, the

licensee, af ter consultation with fuse manuf acturers and other utilities, had

determined that the fuses with hairline cracks on the ferrule were capable of

,

performing the intended design function based on the available industry experience.

However, the licensee decided to perform an additionalindependent test to verify

this industry position,

b. Observation and Findina_ s

The inspector noted that the fuses manuf actured with brass ferrule material are

suspectable to stress corrosion cracking, due to the brass ferrule material relieving

internal stresses built up during the forming and crimping process. Both the fuse

manufacturers (Gould Electronics by 1994 and Bussmann by 1985) had addressed

this issue by changing the ferrule material design to a bronze or pure copper.

The inspector determined that the licensee had performed an operability analyses on

installed fuses and concluded that all fuses installed in the station were operable.

The fuses with cracked ferrules met the required resistance values, cuvent carrying

capacity, clearing time-current requirements at 200% and 500% for the time delay

fuses, and interrupting capability higher than expected values.

.

.

The inspector also reviewed the licensee's engineering evaluation of Millstone

Station (Unit Nos.1,2 and 3) concerning cracked fuses ferrule defects and noted *

that the licensee had appropriately issued a 10 CFR 21 notification report to the

NRC on December 13,1990. The report lodicated that the cracked fuse ferrule

problem existed in a variety of fuses from different manufacturers and indicated that

fifteen different type of fuses from three different manufacturers (Gould Shawmut,

Bussmann, and CEFCO) had axial cracks, as a result of the brass ferrule relieving its

internal stress as described above. The inspector noted that the licensee had

completed the following planned corrective actions:

1. Procurement and warehouse groups had completed inspecting all fuses for

cracked ferrules and replaced suspect fuses with newly procured fuses.

2. A metallurgical ana!ysis on defective fuses was performed to determine the

cause of the ferrule cracks. The analysis was found consistent with industry

l data.

l 3. Conducted an indeperdent functional testing on defective fuses. The results

! from the testing indicated that the fuses met their intended function of

maintaining electrical continuity and interruptinD the current during overload

and electrical f ault.

4. Established an appropriate certificate of conformance material type of

requirements in their procurement documentation to purchase new fuses to

ensure fuses being ordered were of new construction design either brass

pure copper. Procurement also notified the manufacturer of this defect and

confirmed determined that they had taken corrective measure to address this

concern.

5. Completed the operability determinations on each Millstone unit and their

evaluation concluded that the fuses installed were operable. Engineering

, departments of each unit has established a listing of safety related

distribution fuses to include affected fuses. The license found that no

defective style fuses were installed in Millstone 3. The licensee has elected

to replace the defective style fuses in other units by an attrition basis as per

their established routine preventive maintenance program.

6. Enhanced the procedure (NPM1-003, Rev. 2, by adding a note in it that if the

material appears defective, material should be provided to the procurement

engineering group for evaluation.

The inspector randomly verified fuses stored in the warehouse and found that all

fuses were free from above concern. The inspector also inspected fuses installed in

electrical distribution equipment, such as switchgear, control power centers, motor

control centers, and electrical distribution panels and verified that fuses installed in

Unit 3 were not of a defective style fuses and exhibited no concern. The inspector

noted that the fuses were properly labeled and easily identifiable.

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5

c. Conclusion

l

The inspector concluded that the licensee had done an excellent job to resolve the

fuse ferrule crack concerns at the station. Specifically,in Millstone Unit 3, most of

the electrical distribution system fuses has been inspected and replaced with

appropriate size new one with no cracks. The licensee en0ineering staff has

conducted a through analysis to verify the industry position on fuse ferrule cracking

to assure that the fuses installed in the station meet its intended design function.

This item is closed.

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66 ,

jy Pla_nt Runnort

(Common to Unit 1 Unit 2, and Unit 3)

R1 Radiological Protection and Chemistry Controls

R 1,1 Review of ALARA Pagam

a. insoection figspe (83728 and 92904)

The inspector reviewed the licensee's program for maintaining occupational exposures

ALARA, including work control and planning, pre job ALARA reviews, post Job ALARA

reviews and management involvement in the ALARA program. The Inspector also reviewed

actions taken to address previously identified violations of NRC requirements in the area of

radworker performance.

b, Observations and Findinag

Unit 1

Unit 1 established an ALARA Council through the implementation of procedure RPM 1,4.3,

Rev 0, " Unit 1 ALARA Council." Council membership consists of the Directors for

Operations, Work Management, Maintenance and I&C, Engineering and Support Services,

together with thu Radiation Protection Manager (RPM). The inspector reviewed the

activities of the council by discussion with members of the Unit ALARA staff and review of

the Council meeting minutes Prior to the establishment of this council, unit management

involvement in ALARA activities was minimal, and thus creation of the council and

participation at the director's level represents an improvement in the program.

For 1997, the unit ALARA goal was recently lowered by 200 person-rem to 198 person-

rem, to reflect'the very limited amount of work still to be performed during the remainder

of 1997. Through July 10th, unit occupational exposure was just above 164 person-rem

and was tracking well against licensee projections. Following the decision to defer most

work in'the unit until 1998, the ALARA staff began closing most ALARA review packages,.

obtaining worker comments , and compiling lessons learned. When work recommences,

,

these reviews will aid in establishing appropriate ALARA controls on these unfinished jobs.

During the last specialist inspection in this area (NRC Inspection 50 246/97 02), several

examples of improper radworker practices were identified. Subsequent to that incpection,

the licensee undertook a Common Cause analysis, documented as " Adverse Trend in

Personnel Performance Across Millstone Site." This analysis concluded that there were-

four primary root causes, three related to management. Of significance was the

recognition in the analysis that radworker practice problems were not solely a Radiation '

Protection Department issue but was a site wide problem requiring actions be taken by all

radiological workers and their supervisors. While many of the corrective actions required to

address the findings were not implemented at the time of this inspection, the heightened

awareness by radworkers and their supervisors was evidenced by the significant reduction

in the number of documented instances of improper radworker practices. This was

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67

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confirmed by the results of the inspector's observations of radworkers in the Radiologically

Controlled Areas iRCA). Actions taken in Unit 1 included training sessions and unit

walkdowns conducted by the RPM, and a reduction in the number of access points into the

unit RCA.

Unit 2

Unit 2 has established an ALARA Committee which includes representatives from each of

the major departments and is chaired by the Uni.t Director. Meetings are held every two

months at a minimum, and the directors of the major unit functional areas are required to

attend at least two of the Committee meetings in person As part of this inspection, the

inspector attended the ALARA Committee meeting held on July 10,1997. The inspector

noted the scope and depth of discussions held during the meeting as being appropriate.

Committee mernbers were observed being proactive in their discussions and actions to

address personnel exposure issues and to plan for improvements in the ALARA program.

The annual exposure goal for the unit remains at 182 person rem, and a summary of daily

exposures is presented daily at the Unit Director's morning staff meeting and reviewed in

detail. Exposures were on track with the licensee's predictions, and the unit goal continues

to appear attainable.

Unit 2 had experienced the largest number of documented instances of improper radworker

t

practices, three each cited in NRC InspectiN Reports 60 336/97 01 and 50 336/97 02.

Since the last specialist inspection in this area, however, no additionalinstances have been

identified. As part of this inspection, the inspector toured the containnient and auxlhary

buildings observing work areas and radworkers. No radworker discrepancies were

identified by the inspector. Enhanced controls included the closing of some satellite RCA

access areas, the continued assignment of a health physics technician to check workers

dosimetry prior to RCA entrance and more effective posting of the main RCA access door.

Unit 3

Unit 3 had the largest amount of work and workers in the RCA at the time of this

inspection. The unit ALARA goat remained at 134 person rem, and exposures were

tracking well with the predicted values. Significant radiological work still to be completed

included the replacement of all four reactor coolant pumps. Activities in support of the

ALARA area remained weak, especially those actions outside of the Health Physics

Department. No ALARA Committee has been formed at Unit 3, which was identified as a

weakness in a recently completed Nuclear Oversite Audit, MP 97 A06-02, * Radiation

Protection," dated June 27,1997. In addition, work control and planning remain very

arratic and incomplete at the unit with respect to advanced planning and scheduling. An -

earlier attempt at creation of a 12 week planning schedule was suspended in the spring in

f avor of an outage planning and management system. That too was abandoned after only

two months, with the, unit again looking at a 12 week planning schedule, in general,

occupational exposures at Unit 3 have remained low due to the very low dose rates found

at the unit, not because of any efforts in support of an ALARA program. Discussions held

with the Unit Vice President / Recovery Manager indicated that the ALARA program

. - _ - _ _ _

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68

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weaknesses were clearly recognized as needing management attention, and that the

creation of an ALARA Committee was also to be addressed.

Improper radworker practices were identified in NRC Inspection Report 50 423/97 02.

Since that specialist inspection, the Unit has significantly upgraded the level of interaction

and briefings given to radworkers prior to entrance to the RCA through the main RCA

controi point, located at the entrance to the auxiliary building. The entrance was also

recently equipped with a turnstile that could only be activated if the redworker placed both

his electronic dosimeter (ED) and thermoluminescent dosimeter (TLD) in it. This is utilized

to reduce the chances of a worker accessing the RCA without having the appropriate

dosimetry with him. The inspector observed workers entering and exiting from this area,

and also observed a number of workers in the RCA, including the ESF, spent fuel and

auxiliary building. All workers observed had proper dosimetry and were aware of their area

dose rates.

The inspector also attended a training committee meeting hosted by Unit 3 involving

radworker training. At the time of this meeting, all station training was suspended, and the

major theme of this meeting was to identify and resolve allissues related to radworker

training so that this program could recommence as soon as possible (Radworker training

recommenced on July 10,1997). The inspector noted that the Training department staff

present served as facilitators, but that ownership of the training program clearly rested

with the units. Good coordination and communications between the three unit RPMs was

also observed.

Site Health Physics

The inspector reviewed parts of the site radiation protection program under the direction of

the Site Health Physics Manager and his staff. The inspector reviewed Condition Reports

(CRs) and other records maintained by this staff for compliance with NRC rules and

requirements. Allincidents and events requiring a CR by station procedure were found to

be so documented. The inspector also discussed with the Site RPM and his staff an event

involving the discovery of an unlocked door to the trailer located at the radweste bunker on

May 5,1997. This event was not documented as a CR, nor was a CR required. The event

was documented in the Site Health Physics Support Groups daily log book. Following

conversations with the inspector, the Site RPM determined that, although not required, for

tracking and trending purposes, a CR should be written to document the event.

Subsequently CR M1971685 was written on July 9,-1997,

c. Conclusions

The program for maintaining occupational exposures ALARA at each of the three units

remains weak. While the framework for an ALARA program has been implemented at

Units 1 and 2, with the creation of an ALARA Committee and the implementation of an

operational work control and work planning group, neither have been established for a long-

enough period to fully evaluate their effectiveness. The continuing lack of an effective work

control and planning process together with the lack of a unit ALARA Committee at Unit 3

continues to be of concem, however. Licensee actions to address radworker practice

issues have been generally effective, although long term actions are still being

implemented.

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R5 Staff Training and Qualification in Radiological Protection and Chemistry

Controls

R5.1 Health Physics " Supervisors Walk Around",

a. lnsoecilon Scone (71760j

On June 25,1997, the inspector participated in a health physics (HP) " supervisors walk-

,

'

around" with the radiation protection manager (RPM). Plant management sponsored the

plant walk arounds in order to raise the HP awareness of supervisors observing day to day

l work activities in the field. The walk arounds were (nandatory of all Unit i supervisors,

b. Observations and Findinas

The walk around was conducted by the RPM and began outside the radiological controlled

area (RCA) with a review of the radiological work permit system and the proper use of

electronic dosimetry. Once inside the RCA, the RPM discussed the operation and use of

the small article monitor (SAM) and personnel contamination monitor. A primary focus area

'

for the walk around was the use of reusable materials in the plant, particularly in the area

of FME control. The RPM stressed the fact that limiting the amount of disposable material

brought lato the plant, results in a reduction in radiological waste (RW). Plans for a " hot

tool" locker in the plant were also discussed.

The tour was extremely informative and provided good insights into RW reduction. The

walk arounds received very good response from the plant staff and as of the end of June,

78 of 80 Unit 1 supetvisors attended, and 79 additional personnel participated in the

activity, including individuals from Unit 3. The inspector was informed that additional

walk arounds are planned for other HP areas, for example HP posting and boundaries, as

well as, walk arounds in the areas of security and nuclear oversight.

4

c. Conclusions

Plant management sponsored the plant supervisors walk arounds in order to raise the HP

awareness of supervisors observing day to day work activities in the field. The walk-

around tour was extremely informative af.d provided good insights into radiological waste

reduction. The initiative as well received by the Unit 1 supervisors and will be expanded to

included additional ares such as security and nuclear oversight.

PA Staff Knowledge and Performance in Emergency Preparedness

P4.1 Dfill Evaluation Scoce

a. - insoection Scapg

During this inspection, the NRC inspectors observed and evaluated the performance of the

-licensee's site emergency response organization (SERO) during the drill in the simulator

control room (SCR), technical support center (TSC), opcrations support center (OSC), and

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70 .

the emergency operations f acility (EOF). The inspectors assessed licensee recognition of

abnormal plant conditions, classification of emergency conditions, notification of offsite

agencies, devdopment of protective action recommendations, command and contrul,

communications, and the overallimplementation of the emergency plan. In addition, the

inspectors attended the post exercise critique to evaluate the licensee's self assessment of

the drill,

b. Qhtetystions and Findings

Emergency Resoonse Facilitv Observations and Crittaus

Simulator ControLBoom (SCR)

During this drill, the shif t manager demonstrated excellent command and control of the

operations crew Good internal communications were evident between the unit supervisor

and the control board operators, to include strong ' repeat back techniques, good use of

the alarm master silence" feature, and proper use of the emergency operating procedures.

The shif t manager conducted initial classificatior of the event at the " Alert" level in a

timely manner and with proper consideration of the criteria delineated in the event

assessment procedure, EPIP 4400. Communications with the technical support center

(TSC) was established and maintained effectively. However,it was noted that the shift

manager transferred the responsibility for emergency classification to the assistant director

of technical support before full TSC functional capability had been verified and that this

transfer of duties was not announced to the control room staff at the earliest opportunity.

Once a direct communications link was established with the TSC, frequent briefings and

discussions took place on plant conditions, equipment status, and the analysis of this -

event. The control room staff was particularly effective in discussing options and operating

decisions with TSC personnel before commencing or altering planned evolutions. This

deliberative coordination was found to be in evidence in the decisions to start and then

secure the *C" charging pump, to not reopen the accumulator isolation valves af ter

resetting the initial safety injection signal, and to start and secure quench spray pump

operation as necessary. Also, the shif t manager performed wellin assessing and projecting

the potential for further radiation barrier ' degradation and in discussing the appropriate

recommendations with the TSC staff. One area where coordination between the control

room and the TSC could have improved was the control and tracking of various support

personnel (e.g., chemistry, health physics, field teams) that were dispatched for work

activities from either of these two locations without the clear and direct knowledge of all

concerned managers and/or coordinators.

The control room staff had a good focus on maintaining a safe'and stable unit, given the

changing plant conditions and equipment abnormalities. The unit supervisor conducted

appropriate critical safety function reviews and worked with the shift manager in

prioritizing control room activities and evolutions and in attempting to provide "real time"

information to both the.TSC and the Emergency Operations Facility (EOF). Anomalous

plant conditions (e.g., increasing containment pressure indications an6 iadiation levels)

were diagnosed and discussed by the licensed control room operators with input from the

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71

shif t technical advisor and station duty officer, to provide both the TSC and EOF with the

best collective analysis of what might be causing any observed worsening emergency

conditions.

One area where better external control room communications and coordination could have

been provided was that of the " turnover" of functional responsibilities to designated

personnelin the other facilities, in addition to the possibly premature transfer of event

classification duties discussed above,it was noted that the station duty officer delegated

the responsibility for initially notifying NRC headquarters of the " Alert" to the EOF

information officer before the shif t manager had turned over command and control of the

emergency to the Director of Station Emergency Operations (DSEO). It is routinely

expected that the initial telephone communications with the NRC duty officer would

originate from the control room, vice the EOF. Also, the shift manager's turnover of

command and control to the DSEO appears to have occurred prior to actual activation of

the EOF.

While some turnover and coordination problems involving the control room's interaction

with both the TSC and EOF were observed, the overall response of the licensed operators,

shif t management, and the entire control room crew were determined to be good, with

positive impact upon both the assessment and steps taken to mitigate the emergency

conditions.

Technical Succort Center (TSC) Ooerational Sucoort Center J.QSQ

The TSC was staffed and activated in a timely manner. The Assistant Director of

Technical Support (ADTS) exhibited strong command and control, and maintained good

communications with the simulator control room throughout the drill. The ADTS conducted

a good turnover from the shift manager and ensured that his staff was briefed prior to

activation. However, the ADTS accepted responsibility for emergency classification from

the simulator control room prior to officially activating the TSC. Additionally, the inspector

noted that there was some confusion as to when the TSC was activated.

Event classifications were correct and timely, and notifications of offsite officials were

'

appropriately initiated. Although, after the declaration of the Site Area Emergency (SAE)

and the General Emergency (GE), the declarations were not announced to plant personnel

via the public address system. In evaluating the Emergency Action Levels (EALs) for

escalating from a SAE to a GE, the ADTS was noticeably focused on the barrier failure

portion of the EALs, and the barrier failure reference table. The apparent difficulty in the

use of this portion of the EAL distracted the ADTS from other applicable EALs. As the drill

progressed, the ADTS was reminded by the Director of Site Emergency Operations (DSEO)

in the EOF, that a GE can be declared directly from the in-plant radiation EAL regardless of

barrier failure criteria,

During regular and frequent briefings, the ADTS ensured that priorities were properly

established and understood by both the TSC and OSC members. The Manager, Operational

Support Center (MOSC) and the Manager, Technical Support Center (MTSC) were both

given the opportunity to provide a status of reports at each of the briefings. This allowed

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for the close coordination of activities between the TSC and the OSC. Three way

communications (repeat backs) were consistently and effectively used by all TSC/OSC

'

members. The ADTS kept the TSC staff thinking ahead in anticipation of changing plant

conditions by the use of a white board and continually asking the question, "What can go

wrong?" The use of backup ADTSs during this drill was excellent in that it removed some ,

of the administrative and communication burdens from the ADTS.

'

The MTSC coordinated with the accident management team to evaluate potential adverse

consequences of the events, keeping the ADTS advised of the changing priorities. The

accident management team played an important role in assessing the scenario in light of

erroneous information (containment radiation levels) from the simulator control room.

'

The ADTS appropriately established and adjusted the priorities of emergency repairs. The

MOSC maintained a good command and control over the OSC. Team activities were

closely monitored and teams were dispatched in an orderly f ashion depending on changing

priorities. All OSC teams were briefed by HP prior to being dispatched.

Emercenev Ooerations Fad 1RyEREl

'

Good command and control was demonstrated by the Director of Site Emergency '

Operations (DSEO) and the Assistant Director of the Emergency Operations Facility

(ADEOF). The DSEO gave thorough briefings to the EOF staff. The DSEO effectively used

the team leads to provide information to the other staf f members during the briefings in the

emergency operations center. However, it appeared that the DSEO was having problems

getting the plant status information through the open link used to transfer information from

the simulator control room and the technical support center. This lack of information could

have been a hindrance in some of the decision making in formulation of the protective

action recommendations provided to the state of Connecticut.

The technical information coordinators did a very good job in maintaining the status boards

and informing the DSEO of plant conditions as they changed, through di_ rect-

communications from the simulator control or from the Offsite Facility Information System

(OFlS).

The ADEOF's performance in preparing the PAR for the DSEO using the new, approved

PAR procedure in formulating the initial PAR on plant conditions at the general emergency

and the PAR upgrade which was caused by a change in plant conditions later in the drill

was good. Because the new PAR procedure is the same for Haddam Neck, and it was

adequately demonstrated during this drill, the Haddam Neck violation on formulation of

PARS is closed.

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Dose Assessment

I The radiological dose assessment team monitored plant parameters and calculated the

number of the curles of noble gases in the containment based upon the containment -

radiation monitor reading. The dose assessment team informed the Assistant Director

Emergency Operations. Facility (ADEOF) of the dose consequences which may occur if the

o

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entire containment source term was released from the worst release point. This

information was used in providing a worst case estimate of potential consequences, but

could cause inappropriate protective action recommendations (PARS) to be issued if the

recommendations were based upon this information. The ADEOF considered this

information, but properly based his PAR upon the current plant conditions as a release was

not ongoing nor predicted to occur. It would have been beneficial for the dose assessment

team to provide adoitional what if" calculations for other release points and other release

magnitudes.

Although the radiological dose assessment team was able to make dose projections and

position field teams to monitor the release, the following at.pects of the radiological dose

assessrnent was not well performed:

  • Dose assessment personnel were not proficient in the use of the Offsite Facility

Information System (OFIS). OFIS can be used to monitor containment radiation

levels and vent stock monitor readings.

  • When it was discovered that the OFlS readings legged the actual plant readings, the

dose assessment team did not aggressively pursue obtaining more timely radiation

rnonitor data from another source.

  • The start of the release was not quickly identified by the dose assessment staff and

was not clearly communicated among the EOF staff and field monitoring teams.

  • Dose projection calculation sheets were not properly filled out. One of the dose

assessment sheets contained an error and other calculational sheets did not have all

the pertinent data entered. Sheets were not signed and dated. Very little hard copy

dose projection data was printed out. This data could have been usefulin tracking

the update in dose projections during the event and would have been useful in

evaluating the dose projections af ter the event / drill.

Licensee Drill Critiaug

The licensee's critique was very comprehensive and thorough. It identified all of the

observations identified by the NRC inspection team,

c. Overall Drill ConglyMons

Overall performance of the SERO was good. Simulated events were accurately diagnosed,

proper mitigation actions were performed, emergency declarations and protective action

recommendations were timely and accurate, and offsite agencies were notified promptly.

No drill weaknesses, safety concerns, or violations of NRC requirements were observed.

i

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4

P8 Miscellaneous Emergency Properedness issues

a. Inspection SAQDa

On Tuesday, June 17,1997, the inspector and Emergency Preparedness and Safeguards

Branch Chief met with the Northeast Utilities Director of Ernergency Preparedness and his

staff and were presented with the " Millstone Station Emergency Planning Status."

The presentation included past issues, issue resolution, emergency planning elements that

-were in progress, milestones completed, and milestones remaining. A copy of the

presentation handout is attached. The corrective measures being taken are appropriate,

b. Observations and Findings

The inspector' observed a test of the new dialogic callout systems that is scheduled to I

replace the present system that is currently in use. The pagers were activated at

approximately 7:00 p.m. on June 18,1997. It was demonstrated to the inspector by

calling into the system that the initial call backs seemed to overload it initially, but within 2

to 3 minutes we were able to callinto the system. Within about 20 minutes, the callout

was complete.

>

.A message was displayed on the beepers that if there were any problems getting into the

system that personnel were to contact the emergency preparedness services department.

There were several instances where the PIN number for the beeper holder did not work

properly and that was to be corrected.

The system appeared to function and made timely notification to the site emergency

response organization.

Further tests of the system are to be performed before placing it into operation.

F1 Control of Fire Protection Activities

F1.1 Program Oversicht

a. Innocction Scone (64704)

The inspector reviewed fire protection program policy changes made by licensee

management to improve program oversight. This review was performed as a result of

previous NRC inspection findings, as documented in inspection Report No. 96 08,

Section F.

b. Observations and Findinos

The inspector found that the licensee continued development of the Fire Protection Program

Manual. Although lacking supervisory approval of the manual, the inspector reviewed the

licensee's documented efforts for integrating design features, personnel requirements,

,

_ _ _ _ _ _ ___.

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75

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equipment, and procedures to ensure fire protection requirements are met. Following

document approval, the licensee plans to develop supplemental guidance documents,

project instructions, to the manual for controlling fire hazards analyses and 10 CFR Part 50,

Appendix R analyses.

l

The inspector found the manuel improved over Nuclear Group Procedure (NGP) 2.14, I

Revision 9, ' Nuclear Plant Fire Protection Program / and reflected the program

organizational changes to date, better defined individuals responsibilities, and appropriately

established a single point of et trol and contact for improved program implementation, in

addition, the inspector noted tl.at information pertaining to the design and licensing

requirements for the three Millstone plants was contained within the draft manual. The

inspector noted that the manual presented an expanded view of fire protection comrw-

the NGP. More specifically, the inspector found that the manual applied to fire

structures, systems, and components important-to safety in t,ddition to safe w

safety related equipment. Although fWlimplementation of the licensee's cc a

had not been completed, and subsequently the inspector could not evaluate

effectiveness of such actions. the inspector concluded that positive measures were taken

by a competent staff foi establishing a good fire protection program and consistent

approaches for maintaining the prograta in accordance with NRC requirements. The

inspector noted that the manual was approved without any changes from the draft version

reviewed during the inspection on July 2,1997, by the Site Operations Review Committee

(SORC) and on July 9,1997, by each Millstone unit Plant Operations Review Committee

'

(PORC).

Corrective actions taken by the licensee to improve the effectiveness of engineering

i

support for the fire protection program, as discussed in Inspection Report 96-08, Section

F.1, were not evaluated during this inopection and will be the subject of future NRC review

prior to restart of any Millstone unit. (IFl 97 202 10) The acceptability of the licensen's

corrective actions will be used to subnantiate closure nf NRC safety issues list (SIL) issues

Nos 65,21, and 42 for Millstone Units 1,2, and 3 respectively.

The inspector found that corrective action taken by Northeast Utilities included the

performance of an engineering self assessment (ESAR) No. PES-97-0006, Revision 0, for

evaluating the licensing commitment control, configuration management, technical

adequacy, and effectiveness of the Unit 3 fire protection / Appendix R program. This

assessment was conducted by on independent team and resulted in numerous deficiencies

and corrective actions. The licensee stated that ESARs were planned for Units 1 and 2

also. The inspector determined that the ESAR w:.s comprehensive for verifying compliance

with regulatory requirements and qualitative for recommending corrective actions that

would ansure an effective fire protection program. The inspector found that license

commitments were extensively summarized with background and reference information

sufficient to verify proper plant configuration and adequacy.

e. Conclusion

The inspector concluded that significant nusgress had been made by the licensee in

improving the overs ght and organization of the fire p ohetion program. Although planned

__ .-_ -.__ _ _ --.---- ___________ ____ _ _ _

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76

corrective a:,tions were found to be comprehensive, further NRC review is necessary to

verify the proper implementation of the planned currective actions.

F4 Fire Protection Staff Knowledge and Performance

F4.1 Fire Briaade Drill

a. Insoection Scoce (64704)

The inspectors observed an unannounced fire drill to evaluate the effectivehess of the new

centralized, fire brigade, the drill scenario, and the drill critique. This observation was made

as a follow up to previously identified drill weaknesses, as documented in NRC inspection

report 96-08, section F4.2.

b. Observations and Findings

The inspector observed a fire drill on June 24,1997, that involved a simulated motor

control center breaker fire in the turbine building of Unit 1. The inspector observed the

brigade response, dress out, simulated attack strategy, and command and control

demonstrated by the brigade captain. The inspector found that many improvements had

been implemented by the licensee. Scersario cards were utilized at the fire scene to

describe fire conditions and enable fire brigade members to size-up the situation and

[ develop their fire fighting strategy. A newly created position of fire brigade advisor was

l utilized as an Operations department liaison, communicating information between the

l control room and brigade captain. An emergency response vehicle was used to expedite

brigade arrival at the fire scene by transporting fire gear. A pre-drill meeting was held *(o

better ensum proper drill coordination and evaluation by both the Training and Site Fire

Protection departments, and a post drill caucus was held prior to the drill critique to ensure

consistent feedback was provided to the brigade regarding their performance.

. t

The inspector found that:

  • the drill scenario was realistic;
  • excel:ent support was provided to the brigade captain by the fire brigade advisor;
  • the fire captain demonstrated outstanding command and control and verified self-

checks were perfor Ted by the brigade, properly reviewed the pre-fire plan, and

made team assignmen.a accordingly;

e drillmanship and teamwork were robust; and

  • the drill critique properly reflected brigade member performance.

_ - _ _ _ - _ _ _ _ _ _ _

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c. Conclusion

The inspector concluded that the fire brigade functioned effectively and was well prepared

to combat fires. Significant improvements were implemented by the licensee that

!

contributed to overall sunerior performance displayed by the Training and Site Fire

Protection Departments associated with the fire drill. The inspector considered the drill to

be outstanding and concluded that significant improvement was displayed by both the

brigade and training departments.

F7 Quality Assurance in Fire Protection Activities

F7,1 Audits and Surveillsnees

a, insoection Scoce (64704)

The inspector reviewed the most recent audit completed by the Quality Assurance (QA) I

Nuclear Oversight Department to satisfy the technical specification requirements, The

audit evaluated the effectiveness of fire protection measures, equipment, program

implementation; and problem identification and resolutlen. This review was performed

following previously identified audit weaknesses as documented in NRC Inspection Report

No - 90-08, Section F7,1,

b, Observations and Findinos

The inspector reviewed audit no. A24057/A25119, " Triennial Fire Protection program -

Millstone," dated March 10,1997, and found that the audit;

  • was comprehensive and appropriate in scope;
  • = demonstrated good problem identification;
  • appropriately followed up on previously identified QA findings: and

e clearly communicated findings in reports.

c, Conclushn

The inspector concluded that this OA audit provided a good assessment of the fire

prctection program and satisfied the technical specification requirement for performance.

The inspector noted an improvement in the assessment quality over previous audits of the

fire protection program.

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V. Management Meetings

- X1T Exit Meeting Summary

The inspectors presented the inspection results to members of licensee management at

. separate meeti ngsi n each unit at the conclusion of the inspection. The licensee

acknowledged the findings presented.

,

- X1.2 Final Safety Analvsis Reoort Review

A recent discovery of a licensee operating their facihty in a manner contrary to the updated

final safety analysis report (UFSAR) description highlighted the need for additional

. verification that licensees were complying with UFSAR commitments. All reactor

inspections' will provide additional attention to UFSAR commitments and their incorporation

into plant practices, procedures and parameters.

While performing the inspections which are discussed in this report the inspectors reviewed

the applicable portions of the UFSAR that related to the areas inspected. The following

,

inconsistencies were noted between the. wording of the UFSAR and the plant practices,

procedures and/or parameters observed by the inspectors, as documented in Sections

U3.M1.3, U3.M3.2, and U3.E3.4.

.

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ITEMS OPENED, CLOSED, AND DISCUSSED

Ooened

URI 50 245/97 202 01 U 1.E8,1 RWCS filter cubicle inspection i

URI 50 336/97 202 02 ULE8.6 Main steam check valves design adequacy I

IFl 50 423/97 202 03 U3,01.1 Loss of spent fuel pool cooling

VIO 50-423-97 202-04 U3 M1.4 Failure to follow procedures

!Fl 50-423/97 202 05 U 3,M 3,1 Testing of safety / relief valves

eel 56 245/336/423/ U3 M4,1 Ineffective maintenance and technical training

97 202 06 evaluation

,

IFl 50-423/97-202-07 U3.M8.4 Letdown heat exchanger ASME code compliance

l~ VIO 50-423/97 202-08 U3 E7.1 Incomplete and inaccurate information

[ eel 50 423/97-202-09 U3 E8,3 RSS design deficiency

IFl 50-423/97 20210 U 3,F 1.1 Engineering support of fire protection program

Cloted

URI 50-245/94-14-03. U 1,M8,1 QA involvement in safety related work

IFl 50-336/95 201-03 U2.M8,1 Procedure level of use

IFl 50-336/93 20-05 U2,E8.2 Testing of dual function valves

URI 50 336/96-0814 U2 E8.3 Remc, val of startup rate trip

URI 50-423/96-08-18 U 3,M 8,1 Adequacy of IST program

URI 50-423/96 20140 U3,E8,5 - TDAFW calculations

- Uodated

eel 50 336/96-201-25 U2,E8,1

eel 50 336/96 20136

~

U2,E8.4

eel 50-336/96-201-42 U2 E8,5

eel 50-336/96 201-43- U2 E8,5

LER 50-423/9515 02 U3 E2,1

URI 50-423/95-07-10 U3,E3.5

eel 50-423/96-20121 U3 E8.2

eel 50-423/96-201-24 U3,E8,3

The followina LERs were also closed durina this insoection:

Docket Number 50-336

97-04

97 11

,

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80

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Docket Number 50-423

96 34

96 50

97 03

97 14

97-15

97-22

97-23

97-24

97 26

97-28

4

s

$

)

1

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LIST OF ACRONYMS USED

ACP(s) administrative control procedure (s)

ACR(s) adverse candition report (s)

ADEOF Assistant Director of.the Emergency Operations Facility

ADTS . Assistant Director of Technical Support

AFW auxiliary feedwater

AITTS action item tracking and trending system

ALARA as low as reasonably achievable

ANSI /ANS ' American National Standards institute /American Nuclear

AOO(s) anticipated operational occurrence (s)

l ASME American Society of Mechanical Engineers

l A W O(s) automated work order (s)

BOM bill of materials

CAC(s) curriculum advisory committee (s)

CCP. reactor plant component cooling

CFR Code of Federal Regulations

,

CMP configuration management plan

'

CR(s) condition report (s)

CREPS control room envelope pressurization system

DCN design change notice

DSEO Directo* of Station Emergency Operations

EAL(s) emergency action level (s)

EDG emergency diesel generator

eel escalated enforcement item

EOF Emergency Operations Facility

EOP(s) emergency operation procedure (s)

EPIP(s) emergency plan implementing procedure (s)

EPRI Electric Power Research Institute -

ERT event revie. ., team

ESAR engineering self-assessment report

EWR(s) engineering work request (s)

FME foreign material exclusion i

FP fire protection

FSAR Final Safety Analysis Report

GE General Electric

GL Generic Letter

gpm gallons per minute

HELB high energy line break

HPSI high pressure safety injection

HX- . heat exchanger

ICAVP Independent Corrective Action Verification Program

IFl inspector follow item

IHSI intermediate head safety injection

IP(s)- inspection procedure (s)

IR(s) Inspection Reports (s)

.

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82

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IRT independent review team

ISI inservice inspection

IST in-service testing

LER(s) licensee event report (s)

LOCA loss of coolant accident

LTOP low temperature overpressure protection

MCR Main Control Room

MEPL material, equipment, and parts list

MMOD maintenance modification

MOSC Manager, Operational Support Center

. MSIV main steam isolation valve

MTL management test lead

MTSC Manager, Technical Support Center

MSLB main steam line break

NCR(s) nonconformance report (s)

NCV non-cited violation

NDE non-destructive examination

NGP(s) nuclear guidance procedure (s)

NNECO Northeast Nuclear Energy Company's

NPS nominal pipe size

NPSH net positive suction head

NRC Nuclear Regulatory Commission

NRR Nuclear Reactor Regulation

NSAB nuclear safety assessment board

NSIC Nuclear Safety information Center

NSR nonsafety-related

NUGAP Northeast Utilities Quality Assurance Program

NUREG Nuclear Regulation

NUSCO Northeast Utili'.'es Servh.e Company

OCA Office of Congressional Affairs

OEDO ' Office of Executive Director for Operations =-

OFIS offsite facility information system

OlRls) open item report (s)

OJT on the job training

OJT/E on the job training / evaluation

OP(s) operating procedure (s)

ORP Operational Readiness Plan

OSC Operational Support Center

OSHA Occupational Safety & Health Administration

PAO Public Affairs Office

PDCR plant design change record

PDR- Public Document Room

PEO plant equipment operator

PGS primary grade water system

PMMS production maintenance management system

PORC plant operation review committee

PORV(s) power operated relief valve (s)

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,y

PSTS. product' specific technique sheet

PTSCR proposed technical specification change request -

QA quality assurance

OC . quality control

QSS quench spray system

RBCCW reactor building closed cooling water

RCS - seactor coolant system

RG' Regulatory Guide

RHR residual heat removal

Rt Region l-

RO reactor operator

RPM radiation protection manager

l RSS recirculation spray system

i

RW~ radiological waste

RWCU reactor water cleanup

SAT systems approach to training

SBLC standby liquid control

SCR simulator control room

SERO station emergency response organization

SFPC spent fuel pool cooling

Sll significant item list

SORC site operations review committee

SOV(s) solenoid operated valve (s)

SP(s) - surveillance procedure (s)

SPO Special Projects Office

SPROC special procedure

_SR safety related -

SRO senior reactor operator

SRP - Standard Review Plan

SSPS solid state protection system

SWEC - Stone & Webster Engineering Corporation

SWSOPl ._ service water system operational performance inspection

TAC technical advisory counsel

TDAFW turbine driven auxiliary feedwater

Tl temporary instruction

TLD(s) - thermo-luminescent dosimeter (s)

TRM Technical Requirements Manual

- TS(s) technical specification (s)

TSC Technical Support Center

_UFSAR updated final safety analysis report

UIR(s) unresols ed item report (s)

URl(s) unresolved item (s)

USO. unresolved safety question

VIO violation

.

.