Notice of Violation from Investigation Rept 1-94-021 on 940506-960329.Violation Noted:Between 740831-910407,licensee Made Changes to Facility Described in Safety Analysis Rept for Refueling Core Offloads Without Performing EvaluationML20207F152 |
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Millstone ![Dominion icon.png](/w/images/b/b0/Dominion_icon.png) |
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05/25/1999 |
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NRC (Affiliation Not Assigned) |
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ML20207F108 |
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References |
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EA-96-151, NUDOCS 9906080081 |
Download: ML20207F152 (4) |
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Category:NOTICE OF VIOLATION OF A REGULATION
MONTHYEARML20207F1521999-05-25025 May 1999 Notice of Violation from Investigation Rept 1-94-021 on 940506-960329.Violation Noted:Between 740831-910407,licensee Made Changes to Facility Described in Safety Analysis Rept for Refueling Core Offloads Without Performing Evaluation ML20205M7201999-04-0606 April 1999 Notice of Violation from NRC OI Case 1-96-002 & Conclusions of Millstone Independent Review Team.Violation Noted. E Debarba,Deliberately Discriminated Against Supervisor in Performance Engineering Group at Millstone Station ML20205M7351999-04-0606 April 1999 Notice of Violation from Investigation in Case Numbers 1-96-002 & 1-97-007.Violation Noted:Licensee Discriminated Against Supervisor in Performance Engineering Group at Plant Due to Involvement in Protected Activities ML20207M1131999-03-0909 March 1999 Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $88,000.Violation Noted:Employment of Two Contractor Employees Terminated in Aug 1997,in Part Because Individuals Raised Concerns Re MOV Program Manual ML20199C6381999-01-0707 January 1999 Notice of Violation from Insp on 981006-1123.Violation Noted:On or Before 981120,conduit 9-15,in Fire Area A-24,not Sealed & Tested in Accordance with Astme E-119,fire Endurance Test ML20195H6901998-11-18018 November 1998 Notice of Violation from Insp on 980818-1005.Violation Noted:Engineering Evaluations Not Performed When RCS Heatup Rate Limit Exceeded on 951217 & When RCS Cooldown Rate Limit Exceeded on Three occasions,940424,0728 & 951215 ML20155B1521998-10-23023 October 1998 Notice of Violation from Insp on 980810-0903.Violation Noted:Design Basis,As Described in FSAR Chapter 14,Accident Analyses Had Not Been Correctly Translated Into Plant Procedures & Acceptance Criteria ML20154D1151998-09-11011 September 1998 Notice of Violation from Insp on 980413-24-0511-15,27-29, 0609-11 & 23-25.Violation Noted:Program Implemented TS 6.8.4.a,failed to Include Provisions to Reduce Leakage from RSS Heat Exchangers to SW Sys ML20237B0741998-08-12012 August 1998 Notice of Violation from Insp on 980428-0629.Violation Noted:Licensee Failed to Direct Test Personnel to Close & Lock RHR Outboard Drain Valve ML20237D3041998-08-12012 August 1998 Notice of Violation from Insp on 980413-0508.Violations Noted:Two Examples Identified Where Licensee Not Performing Leakage Testing of safety-related Valves in Sys That Could Contain Highly Radioactive Fluids During Accident ML20249C6931998-06-19019 June 1998 Notice of Violations from Combined Insp on 980301-0427. Violations Noted:Prior to 980424,instrument Min Accuracy of Wind Speed Channels Were Not Measured as Required by Table 3.3-8 of Unit 2 TS 3/4.3.3.4 ML20249B0421998-06-12012 June 1998 Notice of Violations from Insp on 980413-24.Violations Noted:Only 1 RCS Loop Operable W/Plant in Mode 4 on 980407 ML20236L5381998-06-11011 June 1998 Notice of Violation from Insp on 980302-0409.Violation noted:post-mod Test Procedure Did Not Incorporate Requirements Contained in Design Documents ML20249B0811998-06-11011 June 1998 Notice of Violation from Insp on 980209-20.Violation Noted: Between 1992 & 1993,appropriate C/A Not Taken to Prevent Recurring Air Binding Problems for Boric Acid Transfer Pumps ML20249B2171998-05-26026 May 1998 Revised Notice of Violation from Insp on 980101-0228. Violations Noted:As of 980210,21 nonsafety-related SOVs in High Pressure & Low Pressure Safety Injection Sys & Four nonsafety-related SOV in RCS Not Included in EQ Program ML20248E5951998-05-26026 May 1998 Notice of Violation from Insp on 980101-0228.Violation Noted:On 980225,NRC Determined That Written Equipment Control Procedures Were Not Established to Process Revs to Sys Valve Lineups ML20248A7781998-05-22022 May 1998 Notice of Violation from Insp on 980302-31 & 980412. Violation Noted:Structural Steel Support Members Did Not Meet 3-h Fire Barrier Criterion,In That on & Before 980304, Columns D2-54,D2-53 & A4-52 Had Gaps in Fire Rated Coating ML20248F3061998-05-0808 May 1998 Notice of Violation from Insp on 980223-0306.Violation Noted:Listed Examples Were Identified Where Requirements of 10CFR50 App B,Criterion Xvi, Corrective Action, Were Not Met ML20247D8561998-05-0606 May 1998 Notice of Violation from Insp on 980223-26.Violation Noted: Between 1988 & 980226,licensee Failed to Maintain Adequate PASS Program That Ensured Capability to Obtain & Analyze Samples Under Post Accident Conditions ML20217M9091998-04-0808 April 1998 Notice of Violation from Insp on 980209-27.Violation Noted:As of 980227,measures Were Not Established to Assure That Design Basis of safety-related MOVs Was Correctly Translated Into Specifications,Drawings & Instructions ML20216F9841998-04-0303 April 1998 Notice of Violation from Insp on 980105-0206.Violation Noted:Certain Measures for Verifying Adequacy of Plant Design Inadequate ML20216G0921998-04-0101 April 1998 Notice of Violation from Insp on 971027-980128.Violation Noted:Licensee Failed to Perform & Include in Written Records,Safety Evaluations for Approx 250 Changes to FSAR Made Between mid-1996 & mid-1997 ML20196J5911998-03-0909 March 1998 Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $55,000.Violation Noted:As of Sept 1997, Condition Adverse to Quality Existed at Facility Which Had Not Been Promptly Identified & Corrected ML20203H0981998-02-25025 February 1998 Notice of Violation from Insp on 971201-31.Violation Noted: on 971222,equipment Located in safety-related Area,Unit 2 Control Room,Not Restrained in Accordance W/Attachment 3 in Procedure Oa 8 ML20198F0501997-12-30030 December 1997 Notice of Violation from Insp on 970825-29.Violation Noted: as of 970829,adequate Dose Assessment Methods Were Not in Use.Page 23 of Incoming Submittal Was Not Included ML20202J7221997-12-10010 December 1997 Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $2,100,000.Violation Noted:Licensee Did Not Translate Design Features Into Work Instructions & Did Not Verify Adequacy of Designs ML20202J7891997-12-0505 December 1997 Notice of Violation from Insp on 970818-29 & 0908-19. Violations Noted:During NRC Insp That Ended 970919,listed Instances Were Identified Where Requirements of TS 6.8.1a Were Not Met ML20202A7491997-11-21021 November 1997 Notice of Violation Form Insp on 970722-1001.Violation Noted:On 971215 Activities Affecting Quality Were Not Prescribed by Documented Instructions,Procedures or Drawings ML20216C7471997-08-29029 August 1997 Notice of Violation from Insp on 970529-0721.Violation Noted:On Several Occasions in May & June 1997,overcoat Window Was Exceeded by 45 Minutes to 2 Hours & 41 Minutes ML20210S8701997-08-29029 August 1997 Notice of Violation from Insp on 970520-0721.Violations Noted:Overcoat Window Was Exceeded by 45 Minutes to 2 H & 45 Minutes ML20141E3101997-06-24024 June 1997 Notice of Violation from Insp on 970311-0519.Violation Noted:Since Commencement of Operations at Unit 1,applicable Regulatory Requirements & Design Basis Not Correctly Translated Into Drawings & Procedures ML20140F1121997-06-11011 June 1997 Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $55,000.Violation Noted:Licensee Identified Seven Incidents Where Items Containing Safeguards Info Had Not Been Under Control of an Authorized Individual ML20140C5551997-04-11011 April 1997 Notice of Violations from Insp on 970101-0310.Violations Noted:Since Commencement of Operations,Unit 1 Failed to Determine Concentration of Nuclides in Gaseous Effluents Released from Radwaste Storage Bldg Through Exhaust Fan ML20137F3921997-03-24024 March 1997 Notice of Violation from Insp on 961222-970208.Violations Noted:When Repeatedly Depressurizing Unit 2 RHR Sys from 970123-30,operators Did Not Properly Implement Procedures as Required ML20135E6111997-02-24024 February 1997 Notice of Violation from Insp on 961026-1231.Violation Noted:Individual Gained Access to PA W/O Having Authorized or Hand Geometry Confirmed ML20134G3911997-02-0303 February 1997 Notice of Violation from Insp on 961112-22.Violation Noted: Licensee Failed to Establish & Implement Procedure to Verify That Design Basis Relative to Ventilation Air Supply Involving Radwaste Was Maintained as Described by UFSAR IR 07100128/20120021997-01-0606 January 1997 Notice of Violation from Insp on 771128-1202.Violation Noted:Licensee Did Not Test Addl 10 Snubbers for Each Found Inoperable Per Procedure 2733B,hydraulic Snubber Functional Test,Rev 0,770601 ML20135C9951996-12-0303 December 1996 Notice of Violation from Insp on 960827-1025.Violation Noted:All Valves Classified as Containment Isolation Boundaries Did Not Receive Monthly Verification to Insure They Are in Closed Position ML20128M1941996-10-0909 October 1996 Notice of Violation from Insp on 960506-10.Violation Noted; Licensee Failed to Control SGI as Required on 951105 ML20149K7331994-07-13013 July 1994 Notice of Violation & Proposed Imposition of Civil Penalties in Amount of $220,000.Violation Noted:Licensee Failed to Take Action to Address Condition Until 891117,when FWCI Was Inoperable IA-97-223, Notice of Violation & Proposed Imposition of Civil Penalties in Amount of $220,000.Violation Noted:Licensee Failed to Take Action to Address Condition Until 891117,when FWCI Was Inoperable1994-07-13013 July 1994 Notice of Violation & Proposed Imposition of Civil Penalties in Amount of $220,000.Violation Noted:Licensee Failed to Take Action to Address Condition Until 891117,when FWCI Was Inoperable ML20059G0631993-12-23023 December 1993 Notice of Violation from Insp on Stated Date.Violation Noted:Written Licensee Procedures Were Not Established or Implemented Re Testing for Drugs ML20058D3371993-11-22022 November 1993 Notice of Violation from Insp on 930818-0928.Violation Noted:Seismic Brace in Count Rate Module of Radiation Monitor RM-8156 Not Reinstalled During Instrument Calibr ML20058Q0601993-10-15015 October 1993 Notice of Violation from Insp on 920512-14.Violation Noted. Licensee Determined That Records Required to Be Maintained by Commission Regulations or License Conditions Not Complete & Accurate in All Matl Respects ML20057E2971993-09-20020 September 1993 Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $50,000.Noncompliance Noted:During 1991-1992 LORT Program,Facility Failed to Ensure Personnel Licensed Per 10CFR55 Had Completed Requalification Program ML20056H2491993-09-0101 September 1993 Notice of Violation from Insp on 930719-23.Violation Noted: Measures to Assure Conditions Adverse to Quality Not Taken to Promptly Correct Deficiency of Failure to Follow Procedures as Evidenced by Listed Actions ML20056G3681993-08-26026 August 1993 Notice of Violation from Insp on 930614-25.Violation Noted: Dynamic Tests for Seventeen safety-related MOVs Performed in Accordance W/Test Procedures That Did Not Incorporate Requirements & Acceptance Limit for Determining Operability ML20128D6071993-02-0101 February 1993 Notice of Violation from Insp on 921028-1222.Violation Noted:Bypass Jumpers Not Initiated for Scaffolding Installed for Greater than 90 Days as Required by Procedure ACP 2.19 ML20127D8451993-01-11011 January 1993 Notice of Violation from Insp on 920706-24.Violation Noted: on 920706,implementation Plan of Plant Design Change Record 2-123-91 Was Not Translated Correctly Into Work Order M2-92-06984 ML20126K0671992-12-28028 December 1992 Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $62,500.Violation Noted:Between 920711 & 0824, Two Independent Trains of Abfs Not Operable 1999-05-25
[Table view] Category:TEXT-INSPECTION & AUDIT & I&E CIRCULARS
MONTHYEARIR 05000245/19990081999-09-14014 September 1999 Insp Repts 50-245/99-08,50-336/99-08 & 50-423/99-08 on 990615-0809.Four Violations Noted & Being Treated as Ncvs. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000423/19990071999-08-27027 August 1999 Insp Rept 50-423/99-07 on 990614-0715.Violations Noted & Being Treated as Ncvs.Major Areas Inspected:Review of C/A Program Using IP 40500, Effectiveness of Licensee Controls in Identifying,Resolving & Preventing Problems IR 05000336/19990061999-07-19019 July 1999 Insp Repts 50-336/99-06 & 50-423/99-06 on 990420-0614.Ten Violations Occurred & Being Treated as non-cited Violations. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000336/19982191999-06-10010 June 1999 Insp Rept 50-336/98-219 on 981214-18,990126-29,0208-19 & 0301-05.Noncited Violations Identified.Major Areas Inspected:Exam of Licensee Corrective Action Implementation IR 05000245/19990051999-06-0404 June 1999 Errata to Insp Repts 50-245/99-05,50-336/99-05 & 50-423/99-05,consisting of Figure 1 ML20207G1211999-06-0303 June 1999 Insp Repts 50-245/99-05,50-336/99-05 & 50-423/99-05 on 990302-0419.No Violations Noted.Major Areas Inspected: Operations,Maint,Engineering & Plant Support ML20207F1521999-05-25025 May 1999 Notice of Violation from Investigation Rept 1-94-021 on 940506-960329.Violation Noted:Between 740831-910407,licensee Made Changes to Facility Described in Safety Analysis Rept for Refueling Core Offloads Without Performing Evaluation ML20196K2621999-05-24024 May 1999 EN-99-020:on 980525,notice of Violation & Exercise of Enforcement Discretion Will Be Issued to Licensee.Action Based on Severity Level III Problem Consisting of Four Individual Violations Involving Refueling Outage PNO-I-99-022, on 990509,Millstone Unit 2 Established Reactor Criticality.Nrc Staff Providing Augmented Insp Coverage of Restart Activities,Including round-the-clock Observations of Licensee Activities During Key Operational Evolutions1999-05-11011 May 1999 PNO-I-99-022:on 990509,Millstone Unit 2 Established Reactor Criticality.Nrc Staff Providing Augmented Insp Coverage of Restart Activities,Including round-the-clock Observations of Licensee Activities During Key Operational Evolutions IR 05000336/19990031999-05-10010 May 1999 Insp Rept 50-336/99-03 on 990322-26.No Violations Noted. Major Areas Inspected:Review of Actions Taken by Util to Resolve Significant Issues List Item 21,fire Protection ML20206F4601999-04-30030 April 1999 Insp Rept 50-336/99-04 on 990315-31.Violation Noted.Major Areas Inspected:Monitored Licensee Activities During Plant Transition Between Operational Modes,Both During Normal & off-normal Working Hours PNO-I-99-016, on 990406,operators Initiated Plant Cooldown from Normal Operating Pressure & Temp in Mode 3,hot Standby. Cooldown Was Necessary to Minimize Further Degradation of Bonnet Pressure Seal for Valve 2-SI-652 & to Repair Valve1999-04-0707 April 1999 PNO-I-99-016:on 990406,operators Initiated Plant Cooldown from Normal Operating Pressure & Temp in Mode 3,hot Standby. Cooldown Was Necessary to Minimize Further Degradation of Bonnet Pressure Seal for Valve 2-SI-652 & to Repair Valve ML20205M7201999-04-0606 April 1999 Notice of Violation from NRC OI Case 1-96-002 & Conclusions of Millstone Independent Review Team.Violation Noted. E Debarba,Deliberately Discriminated Against Supervisor in Performance Engineering Group at Millstone Station ML20205M7351999-04-0606 April 1999 Notice of Violation from Investigation in Case Numbers 1-96-002 & 1-97-007.Violation Noted:Licensee Discriminated Against Supervisor in Performance Engineering Group at Plant Due to Involvement in Protected Activities IR 05000245/19990021999-04-0202 April 1999 Insp Repts 50-245/99-02,50-336/99-02 & 50-423/99-02 on 990112-0301.Violations Noted.Major Areas Inspected: Operations,Maint,Engineering & Plant Support IR 05000336/19990011999-03-29029 March 1999 Insp Rept 50-336/99-01 on 990117-0217.Violations Noted.Major Areas Inspected:Licensee C/A Program Implementation Using Guidance of NRC IP 40500, Effectiveness of Licensee Controls in Identifying,Resolving & Preventing Problems ML20205J0941999-03-12012 March 1999 Rept of Review of Millstone Units 1,2 & 3:Allegations of Discrimination in NRC Ofc of Investigations Cases 1-96-002, 1-96-007,1-97-007 & Associated Lessons Learned ML20207M1131999-03-0909 March 1999 Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $88,000.Violation Noted:Employment of Two Contractor Employees Terminated in Aug 1997,in Part Because Individuals Raised Concerns Re MOV Program Manual ML20205G6161999-03-0909 March 1999 EN-99-010:on 990309,notice of Proposed Imposition of Civil Penalty in Amount of $88,000 Issued to Licensee.Action Based Upon Severity Level II Problem Involving Discrimination Against Two Contractor Employees at Millstone MOV Dept IR 05000245/19980061999-03-0101 March 1999 Insp Repts 50-245/98-06,50-336/98-06 & 50-423/98-06 on 981123-990111.No Violations Noted.Major Areas Inspected: Operations,Maintenance,Engineering & Plant Support PNO-I-99-006, on 990128,operators Inadvertently Reduced Spent Fuel Pool Water Level by Two Inches When Purification of Spent Fuel Pool Water Initiated.Operators Held Shift Briefing to Discuss Realigning Purification Sys1999-01-29029 January 1999 PNO-I-99-006:on 990128,operators Inadvertently Reduced Spent Fuel Pool Water Level by Two Inches When Purification of Spent Fuel Pool Water Initiated.Operators Held Shift Briefing to Discuss Realigning Purification Sys IR 05000245/19982171999-01-22022 January 1999 Evaluation Repts 50-245/98-217,50-336/98-217 & 50-423/98-217 Conducted on 981026-30.Areas Evaluated:Whether NNECO Has Improved Sufficiently & Has Demonstrated Sustained Performance in Maintaining safety-conscious Work Environ PNO-I-99-004, on 990115,carbon Dioxide Was Inadvertently Discharged Into Unit 3 Cable Spreading Room,Containing Electrical Wiring.Ambulance Reported to Site as Precautionary Measure.Licensee Assembled Event Review1999-01-20020 January 1999 PNO-I-99-004:on 990115,carbon Dioxide Was Inadvertently Discharged Into Unit 3 Cable Spreading Room,Containing Electrical Wiring.Ambulance Reported to Site as Precautionary Measure.Licensee Assembled Event Review IR 05000336/19980051999-01-0707 January 1999 Insp Repts 50-336/98-05 & 50-423/98-05 on 981006-1123. Violations Noted.Major Areas Inspected:Operations, Maintenance,Engineering & Plant Support ML20199C6381999-01-0707 January 1999 Notice of Violation from Insp on 981006-1123.Violation Noted:On or Before 981120,conduit 9-15,in Fire Area A-24,not Sealed & Tested in Accordance with Astme E-119,fire Endurance Test PNO-I-99-001, on 981231,Millstone Unit 2 Began Reloading Fuel Into Reactor After Extended Shutdown.Millstone Unit 3 Went Critical on 981230,after Forced Outage Due to Inadvertent MSIV Closure During Surveillance Testing at Power1999-01-0404 January 1999 PNO-I-99-001:on 981231,Millstone Unit 2 Began Reloading Fuel Into Reactor After Extended Shutdown.Millstone Unit 3 Went Critical on 981230,after Forced Outage Due to Inadvertent MSIV Closure During Surveillance Testing at Power PNO-I-98-062, on 981211,Millstone Unit 3 Tripped from 100% Reactor Power During MSIV Partial Stroke Testing.Solenoid Valve Integral to MSIV Failed to Reopen When Licensed Operator Released Test Switch1998-12-15015 December 1998 PNO-I-98-062:on 981211,Millstone Unit 3 Tripped from 100% Reactor Power During MSIV Partial Stroke Testing.Solenoid Valve Integral to MSIV Failed to Reopen When Licensed Operator Released Test Switch ML20195H6901998-11-18018 November 1998 Notice of Violation from Insp on 980818-1005.Violation Noted:Engineering Evaluations Not Performed When RCS Heatup Rate Limit Exceeded on 951217 & When RCS Cooldown Rate Limit Exceeded on Three occasions,940424,0728 & 951215 IR 05000245/19982161998-11-18018 November 1998 Insp Repts 50-245/98-216,50-336/98-216 & 50-423/98-216 on 980818-1005.Violations Noted.Major Areas Inspected: Operations,Maintenance,Engineering & Plant Support IR 05000336/19982031998-11-0505 November 1998 Insp Rept 50-336/98-203 on 980824-0904.No Violations Noted. Major Areas Inspected:Effectiveness of Configuration Mgt Plan ML20155B1521998-10-23023 October 1998 Notice of Violation from Insp on 980810-0903.Violation Noted:Design Basis,As Described in FSAR Chapter 14,Accident Analyses Had Not Been Correctly Translated Into Plant Procedures & Acceptance Criteria IR 05000336/19982131998-10-23023 October 1998 Insp Rept 50-336/98-213 on 980810-0903.Violations Noted. Major Areas Inspected:Certain Aspects of Accident Mitigation Sys IR 05000245/19982151998-10-14014 October 1998 Evaluation Repts 50-245/98-215,50-336/98-215 & 50-423/98-215 on 980824-28.Major Areas Evaluated:Whether Licensee Has Improved Sufficiently & Has Demonstrated Sustained Performance in Maintaining safety-conscious Work Environ IR 05000336/19980041998-10-0101 October 1998 Insp Rept 50-336/98-04 on 980914-18.No Violations Noted. Major Areas Inspected:Mov Program Associated with GL 89-10 IR 05000245/19982121998-09-25025 September 1998 Insp Repts 50-245/98-212,50-336/98-212 & 50-423/98-212 on 980630-0817.No Violations Noted.Major Areas Inspected: Operations,Maintenance,Engineering & Plant Support IR 05000423/19982111998-09-11011 September 1998 Insp Rept 50-423/98-211 on 980413-24,0511-15,27-29,0609-11 & 23-25.Violation Noted.Major Areas Inspected:Evaluation of Licensee C/As & Other ICAVP Process Activities ML20154D1151998-09-11011 September 1998 Notice of Violation from Insp on 980413-24-0511-15,27-29, 0609-11 & 23-25.Violation Noted:Program Implemented TS 6.8.4.a,failed to Include Provisions to Reduce Leakage from RSS Heat Exchangers to SW Sys IR 05000424/19980061998-09-10010 September 1998 Insp Repts 50-424/98-06 & 50-425/98-06 on 980628-0815.No Violations Noted.Major Areas Inspected:Aspects of Licensee Operations,Engineering,Maint & Plant Support PNO-I-98-039, 980812,Millstone Unit 3 Was Shutdown to Repair Small Leak on Afws Discharge Noted.Current Leakage Does Not Exceed Regulatory Requirements & Shutdown Not Required by Tech Specs.Licensee Issued Press Release on 9808111998-08-12012 August 1998 PNO-I-98-039:980812,Millstone Unit 3 Was Shutdown to Repair Small Leak on Afws Discharge Noted.Current Leakage Does Not Exceed Regulatory Requirements & Shutdown Not Required by Tech Specs.Licensee Issued Press Release on 980811 ML20237D3041998-08-12012 August 1998 Notice of Violation from Insp on 980413-0508.Violations Noted:Two Examples Identified Where Licensee Not Performing Leakage Testing of safety-related Valves in Sys That Could Contain Highly Radioactive Fluids During Accident IR 05000245/19982081998-08-12012 August 1998 Insp Repts 50-245/98-208,50-336/98-208 & 50-423/98-208 on 980428-0629.Violations Noted.Major Areas Inspected: Operations,Maint,Engineering & Plant Support ML20237B0741998-08-12012 August 1998 Notice of Violation from Insp on 980428-0629.Violation Noted:Licensee Failed to Direct Test Personnel to Close & Lock RHR Outboard Drain Valve IR 05000336/19982011998-08-12012 August 1998 Insp Rept 50-336/98-201 on 980413-0508.Violations Noted. Major Areas Inspected:Licensee Ability to Identify & Resolve Deficiencies Focusing,But Not Limited To,Period of CMP Implementation & ICAVP at Parsons Power Group,Inc PNO-I-98-026, on 980701,Millstone Unit 3 Criticality Update Made.Nrc Staff Continues to Provide Augmented Insp of Unit 3 Restart Activities,Including round-the-clock Coverage of Key Operational.Licensee Plans No Press Release1998-07-0101 July 1998 PNO-I-98-026:on 980701,Millstone Unit 3 Criticality Update Made.Nrc Staff Continues to Provide Augmented Insp of Unit 3 Restart Activities,Including round-the-clock Coverage of Key Operational.Licensee Plans No Press Release PNO-I-98-025, on 980630,unit 3 Established Reactor Criticality,However Reactor Was Shut Down When Control Room Operator Noticed Spiking Intermediate Range Monitor.Licensee Troubleshooting1998-06-30030 June 1998 PNO-I-98-025:on 980630,unit 3 Established Reactor Criticality,However Reactor Was Shut Down When Control Room Operator Noticed Spiking Intermediate Range Monitor.Licensee Troubleshooting IR 05000245/19982071998-06-19019 June 1998 Insp Repts 50-245/98-207,50-336/98-207 & 50-423/98-207 on 980301-0427.Violations Noted.Major Areas Inspected:Maint, Operations,Engineering & Plant Support ML20249C6931998-06-19019 June 1998 Notice of Violations from Combined Insp on 980301-0427. Violations Noted:Prior to 980424,instrument Min Accuracy of Wind Speed Channels Were Not Measured as Required by Table 3.3-8 of Unit 2 TS 3/4.3.3.4 IR 05000423/19970831998-06-12012 June 1998 Insp Rept 50-423/97-83 on 980413-24.Violations Noted. Major Areas Inspected:Readiness of Plant Hardware,Staff & Mgt Programs to Support Safe Restart & Continued Operation of Plant Unit 3 ML20249B0421998-06-12012 June 1998 Notice of Violations from Insp on 980413-24.Violations Noted:Only 1 RCS Loop Operable W/Plant in Mode 4 on 980407 IR 05000423/19970821998-06-11011 June 1998 Insp Rept 50-423/97-82 on 980209-20.Violations Noted.Major Areas Inspected:Corrective Actions Processes 1999-09-14
[Table view] |
Text
]q t1AY-25-1999L 08:02T _ USNRC RI/OFC OF, REG ADt1 blu m x41 e. u viu -
. s
' s ENCLOSURE 1 NOTICE OF VIOLATION.
- ; Northeast Nudear Energy Company Docket No. 50-245 Licenae No. DPR-21
- Millstone 1
- EA 96-151
~
During an investigation conduded by the NRC Office of Investigations from May 6,1994 to March 29,1996, violations of NRC requirements were identified.' In accordance with~ the " General Statement of Policy and Procedure for NRC Enforcement Actions," NUREG-1600, the violations are listed below- .
~A.- ;10' CFR 50.59(a) allows licensees to make changes to the facility or procedures as
-desenbod in the safety analysis report, without prior Commission approval unless the I change involves an unreviewed safety qesstion (USQ).
10 CFR 50.59(b) requires, in part, that the licensee maintain written safety evaluations that
- provide the bases for the determination that the change does not involve a USQ.
' Updated Final Safety Analysis Report (UFSAR), Section 9, stated that the normal heat load for the spent fuel pool (SFP) during a refueling outage (RFO) was based on a partial cora offload decayed for 150 hours0.00174 days <br />0.0417 hours <br />2.480159e-4 weeks <br />5.7075e-5 months <br />, and the emergency (abnormal) heat load was based on a full core omend decayed for 250 hours0.00289 days <br />0.0694 hours <br />4.133598e-4 weeks <br />9.5125e-5 months <br />. T' c UFSAR also stated that the SFP cooling heat exchangers were designed to remove the maximum normal heat load from the fuel pool, and that the SFP cooling system and the shutdown cooling (SDC) system, working together, could remove the emergency heat load. l Contrary to the above, between August 31,1974 and April 7,1991, the licensee made changes to the facility descnbed in the safety analysis report for refueling core offloads
' without performing an evaluation to provide the basis that the changes did not itivolve a
- USQ. The licensee routinely performed core offloads without assuring that the specified i
decay times in the UFSAR had been met, and the licensee did not perform an analysis to assure that the design SFP heat loads were not exceeded. Specifically,
- Full core offloads were commenced less than 250 hours0.00289 days <br />0.0694 hours <br />4.133598e-4 weeks <br />9.5125e-5 months <br /> after shutdown during RFOs 2 -4 and 7 - 13. In all but three of these RFOs, fuel transfer began before the reactor had been shutdown for 150 hours0.00174 days <br />0.0417 hours <br />2.480159e-4 weeks <br />5.7075e-5 months <br />.
- A partial core offload was commenced less than 150 hours0.00174 days <br />0.0417 hours <br />2.480159e-4 weeks <br />5.7075e-5 months <br /> after shutdown during RFO 5. (01013)
.B. - 10 CFR Part 50, Appendix B, Criterion V, requires, in part, that activities affecting quality be
=
' accomplished in accordance with documented instructions or procedures.
' Contrary to the above, between 1980 and 1991, the licensee provided augmented cooling to the SFP, an activity affecting quality, without documented instructions or procedures.
Spec;rically, the rcensee used the SDC system to augment the SFP cooling system during
\
' N 1'990525 PDR COMMS Mt(,C 7
CORRESPONDENCE PDR
r? rHY-43-Assp . co me .: . ustwv nieut L ur kco Hur'd 6104576241 P.08/10 e[
?Enclosure1 2 refueling operations with flow through the SFP cooling and SDC discharge intertie valves.
No procedure existed for operation of the SFP cooling and SDC- systems in this
- configuration. (01023); , .
C. 10 CFR 50.9(a) requires, in part, that information provided to the Commission by a licensee be complete and accurate in all material respects.
Contrary to the above, in the. submitted request for License Amendment 40 dated June 24, 1988, the licensee failed to provide the NRC complete and accurate information conceming the performance of core offloads. In an analysis submitted to the NRC to support the license amendment to increase the fuel storage capacity of the SFP, the licensee stated that l
it analyzed two scenarios for fuel offload.to the SFP. However, the licensee failed to j indicate, in that analysis, that its offload practices were different than the stated analyzed scenarios. Specifically, the licensee stated that the analysis performed to obtain the decay heat load and the bulk temperature profile for the SFP was based on conservative assumptions. These assumptions included: (1) a normal discharge, described as one third of the core discharged after 150 hours0.00174 days <br />0.0417 hours <br />2.480159e-4 weeks <br />5.7075e-5 months <br /> of decay in the reaMor; and (2) an abnormal condition, described as the full core discharged with fuel transfer beginning 250 hours0.00289 days <br />0.0694 hours <br />4.133598e-4 weeks <br />9.5125e-5 months <br /> after reactor shutdown. This description implies that those scenarios represented the actual ,
methods used by the licensee to discharge fuel from the reactor core. As such, this I information was not complete and accurate because it did not reflect that full core offloads were routinely performed with fuel transfer beginning before the reactor had been shutdown for 250 hours0.00289 days <br />0.0694 hours <br />4.133598e-4 weeks <br />9.5125e-5 months <br /> as described above. The actual conditions for the majority of the fuel offloads performed by the licensee were less conservative with respect to SFP heat load than the j conditions described in the analyzed scenarios. This information was material in that the time the fuel transfer begins is integral to the assessment of SFP heat removal capabilities.
It was assumed that the supporting analysis bounded the actual conditions that would exist in the SFP during a core offload. (01033)
D. 10 CFR 50.9(a) requires,in part, that information provided to the Commission by a licensee be complete and accuratein all material respects.
10 CFR 50.73(b)(2)(ii)(C) requires that the narrative required to be included in a Licensee Event Report shall contain the dates and approximate times of occurrences of the events ,
being reported.
Contrary to the above, on October 18,1993, in a Ucensee Event Report (LER) (No.93-011) l submitted to the NRC to report a condition outside of the design basis of the plant, the licensee failed to provide complete information conceming the performance of core offloads.
The licensee reported that conditions may have existed where the SFP cooling system may have been ir,c.psNe of rnaintaining the SFP temperature below the 150 *F design limit when I performing full core offloads and described a scenario in which fuel transfer began 150 l hours after reactor shut down. However, the information provided was not complete in that it did not report tne dates of occurrences of at least seven refueling outages (RFOs 2 -4 and i 8 - 11), prior to the submittal of the LER, when full core offloads we e actually commenced before the reactor had been shutdown for 150 hours0.00174 days <br />0.0417 hours <br />2.480159e-4 weeks <br />5.7075e-5 months <br />. This information was material in that the NRC relies on LERs to assess the significance of events, assess licensee performance, 9
MAY-25 _1999 08:03_ UbNNC Rl/DFC u_ NcG ADM 61035/:>d41 P.09/10
- 7 Enclosure 1 3 and to identify issues that may impact the health and safety of the publ'm. In this case, the
' NRC could not accurately assess the' safety significance or licensee perfonnance without the specific information that was omitted. (01043) .
T.us is a Severity Level 111 problem (Supplement 1).
.The NRC has concluded' that you have already addressed the broad, programmatic problems that leid to the violations cited in the enclosed Notice in your response to the 52,100,000 civil penalty.
However, if you choose to respond, clearly markyour response as a " Reply to a Notice of Velation," l and send it to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, D.C. 20555 with a copy to the Regional Administrator, Region I, and a copy to the NRC -
Resident inspector at the facility that is the subject of this Notice, within 30 days of the date of the letter transmitting this Notice of Violation (Notice).
If you contest this enforcement action, you should also provide a copy of your response to the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001.
]
' if you choose to respond, your response will be placed in the NRC Public Document Room (PDR).
Therefore, to the extent possible, the response should not include any personal privacy, proprietary, or safeguards information so that it can be placed in the PDR without redaction.
Dated at King of Prussia, PA this 25th day of May 1999 -
e
f lMAY-25-1999 t 08:03.- USNRC RI/OFC OF REG ADM 6103375241 P.10/10
. 3, .
- - ENCLOSURE 2-i . SYNOPSIS-lThis investigation was-initiated by the U.S. Nuclear Regulatory Commission (NRC), Office of-Investigations (01) Region I-(RI), on May 60 1994, to determine whether-Northeast Nuclear Energy Company (NNECO) wrformed nuclear fuel offloads at Millstone Nuclear Power Station. Unit 1.(M)1), in conformance with its NRC license: prcperly. evaluated employee concerns relative to this
~ activity; and. reported any identified noncompliance to the NRC in a timely.-
complete and accurate manner. This investigation was later expanded-to ascertain'whether officials at NNECO/MP1 have knowingly and intentionally provided the NRC with incdeplete and inaccurate information in a license amendment application and utilized unapproved and.unanalyzed s'ystems' configurations in the cooling of the MP1 spent fuel pool (SFP).
- Based on the' evidence developed during this investigation it is concluded
-that.
1)' In many instances MP1 staff, without the appropriate engineering analyses, willfully performed reactor fuel. offloads in a manner' not consistent with MP1's FSAR. FSAR updates._and License Amendments:
'2) NNECO willfully submitted incomplete 'and inaccurate information to the NRC'
-in its request for License Amendment 40: l
- 3) A former Supervisor, .N; clear Licensing Department, and a Senior Engineer, Nuclear Licensing Department, deliberately caused MP1 management not to report E the REF 92-73 issues in a timely manner. MP1 management willfully failed to
~
' ensure timely reporting of the issues associated with the REF;
. 4) A former MF1 Supervisor of Reactor Engineering, deliberately pre >ared an- a incomplete and inaccurate LER (No. 93 011), which was submitted to t1e NRC on October 18. 1993. NNECO management willfully failed to ensure the submittal.
.of complete and accurate information in the LER: .and
- 5) . An Operations Shift Manager, MP1, deliberately utilized unapproved and unanalyzed systems' configurations,.to augment MP1 SFP cooling during RFOs
.from about 1980 to 1991..without procedures to govern those activities. MP1 management willfully utilized unapproved and unanalyzed systems' configurations to augment SFP cooling during RFOs. .
l JCase No. 1 94 021- 1.
TOT 4! P.10-B