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Category:ABNORMAL OCCURRENCE REPORTS (SEE ALSO LER & RO)
MONTHYEARML19343C2181975-12-23023 December 1975 AO 50-219/75-33:on 751212,during 6-month Load Test on Station a batteries,125 Volt Dc Distribution Ctr de-energized.Caused by Personnel Error in Following Procedure.Distribution Ctr re-energized ML20090C9991975-12-12012 December 1975 AO 75-33:on 751212,125-volt Dc Distribution Ctr of Station a Battery Inadvertently de-energized.Caused by Failure to Establish Proper Breaker Lineup Preparation for Conducting Battery Load Test.Procedure changed.W/751219 Memo ML19343C2191975-12-11011 December 1975 AO 50-219/75-32:on 751203,during Testing,Emergency Diesel Generator 1 Failed to Start When Simulated Loss of Power Condition Applied to Fast Start Logic Circuit.Caused by Failure of Relay to Operate Due to Varnish on Armature ML20126E8281975-12-0303 December 1975 AO 50-219/75-31:on 751124,during Operability Test of Torus to Drywell Vacuum Breakers,Alarm Sys 2 Failed to Annunciate in Control Room When V-26-4 Opened.Caused by Failure of Relay Due to Contacts Being Detective.Relay Replaced ML20090D0071975-11-25025 November 1975 AO 75-31:on 751124,drywell Vacuum Breaker Alarm Sys II Failed to Annunciate When Vacuum Breaker V-26-4 Opened. Caused by Component Failure.Corrective Action Under Investigation ML20090D0161975-11-0707 November 1975 AO 75-30:on 751106,low Reactor Pressure Core Spray Valve Permissive Pressure Switches Re 17 a & C Tripped at Pressure Less than Min Required Value.Caused by Switch Repeatability.Pressure Switches Recalibr ML20090D0601975-11-0606 November 1975 AO 75-29:on 751027,torus Drywell Vacuum Breakers Alarm Sys II Failed to Annunciate When Vacuum Breaker V-26-8 Opened. Caused by Sticking Microswitch ML20090D0761975-10-28028 October 1975 AO 75-29:on 751027,torus to Drywell Vacuum Breaker Alarm Sys II Failed to Annunciate When Vacuum Breaker V-26-8 Opened.Caused by Component Failure.Corrective Action Under Investigation ML20090D0941975-10-24024 October 1975 AO 75-28:on 751015,standby Gas Treatment Sys 1 Inoperable. Caused by Air Solenoid Valve Coil Failure.Defective Solenoid Coil Replaced ML20090D1141975-10-17017 October 1975 AO 75-27:on 751008,low Reactor Pressure Core Spray Valve Permissive Pressure Switches RE17B & D Tripped at Pressure Less than Min Required Value.Caused by Switch Repeatability. Pressure Switches Recalibr ML20090D1041975-10-16016 October 1975 AO 75-28:on 751015,standby Gas Treatment Sys 1 Inoperable. Caused by Air Solenoid Valve Coil Failure.Defective Solenoid Coil replaced.W/751016 ML20090D1341975-10-0808 October 1975 AO 75-27:on 751008,low Reactor Pressure Core Spray Valve Permissive Pressure Switches RE17B & D Tripped at Pressures Less than Min Required Value.Caused by Switch Repeatability. Pressure Switches Recalibr ML20090D1501975-09-23023 September 1975 AO 75-26:on 750923,emergency Svc Water Pump 52C Failed to Start Automatically During Routine Surveillance Test of Containment Spray Sys Ii.Caused by Failure of Contact Switch in Time Delay Relay 16 K4B.Relay Replaced ML20090D2071975-09-0808 September 1975 AO 75-24:on 750829,electromatic Relief Valve Pressure Switches 1A83C & 1A83D Tripped at Pressures in Excess of Max Allowable Value.Caused by Instrument Setpoint Repeatability. Switches Reset ML19291C2641975-09-0808 September 1975 AO 73-19:when Closing Signal Was Applied to Breaker S1A,loss of Power Occurred at 4160-volt Ac Bus 1A Causing Trip of Various Pumps.Caused by Incorrect Setting of Current Transformer Ratio Matching Taps.Taps Set Properly ML20090D1941975-09-0808 September 1975 AO 75-25:on 750829,stack Gas Sample Sys Failed to Monitor Stack Releases Continuously While Reactor Was in Unisolated Condition.Caused by Malfunctioning Pump Lubricator.Thermal Overload Protection Reset ML20090D2151975-09-0202 September 1975 AO 75-24:on 750829,electromatic Relief Valve Pressure Switches 1A83C & 1A83D Tripped at Pressures in Excess of Max Allowable Value.Caused by Instrument Setpoint Repeatability. Switches Reset ML20090D2011975-09-0202 September 1975 AO 75-25:on 750829,stack Gas Sample Sys Failed to Monitor Stack Releases Continuously While Reactor Was in Unisolated Condition.Caused by Malfunctioning Pump Lubricator.Thermal Overload Protection Reset ML20090D2241975-08-21021 August 1975 AO 75-23:on 750817-20,stack Effluent for Iodine & Particulates Not Monitored.Caused by Personnel Error.Filter Installed in Operating Stack Gas Sampling Train ML20090D2261975-08-11011 August 1975 Preliminary AO-50-219/75-22:on 750810,stack Gas Sample Line Low Flow Alarm Received.Caused by Stack Gas Sample Pump a Not Running.Thermal Overload Protection Reset ML20090D2471975-08-0404 August 1975 Preliminary AO-50-219/75-21:on 750801,during Routine Surveillance on B Isolation Condensor Sys,Steam Line Valve V-14-32 Failed to Close on Simulation of Steam Line High Flow.Caused by Low Torque Switch Setting.Torque Increased ML20090D2521975-07-17017 July 1975 AO 50-219/75-19:on 750708,during Monthly Surveillance Test on Reactor High Pressure Scram Sensors,Re 03A,B,C & D, A,B & D Tripped Above Normal Trip Points.Caused by Switch Repeatability.Sensors Recalibr ML20090D2561975-07-0909 July 1975 Preliminary AO 50-219/75-19:on 750708,during Monthly Surveillance Test on Reactor High Pressure Scram Sensors,Re 03A,B,C & D,A,B & D Tripped Above Normal Trip Points.Caused by Switch Repeatability.Sensors Recalibr ML20084E1151975-07-0101 July 1975 RO 50-219/75-18:on 750623,two 8-1/2 Inch Handhole Covers in Standby Gas Treatment Filter Train Not in Place.Cause Unknown.Handhole Covers Repositioned & Secured ML20090D2741975-06-27027 June 1975 AO 50-219/75-17:on 750619,during Surveillance Test,Core Spray Sys Parallel Isolation Valve V-20-15 Failed to Demonstrate Operability.Caused by Broken Tab on B Phase of Valve Motor Breaker Stab.Stab Replaced ML20090D2661975-06-24024 June 1975 Preliminary AO 50-219/75-18:on 750623,handhole Covers in Standby Gas Treatment Filter Train 1-1 Not in Place.Cause Under Investigation.Covers Repositioned & Secured ML20090D2781975-06-24024 June 1975 AO 50-219/75-16:on 750614,electromatic Relief Valve Pressure Switches 1A83P & E Tripped at Pressures Exceeding Tech Spec Limit.Caused by Instrument Setpoint Drift.Switches Reset ML20090D2731975-06-19019 June 1975 Preliminary AO 50-219/75-17:on 750619,during Surveillance Test,Core Spray Sys Parallel Isolation Valve V-20-15 Failed to Demonstrate Operability.Caused by Broken Tab on B Phase of Valve Motor Breaker Stab.Stab Replaced ML20090D2901975-06-16016 June 1975 Preliminary AO 50-219/75-16:on 750614,electromatic Relief Valve Pressure Switches 1A83B & E Tripped at Pressure Exceeding Tech Spec Limit.Caused by Instrument Setpoint Drift.Switches Reset ML20090D6561975-06-0606 June 1975 AO-50-219/75-14:on 750529,during Surveillance Test of Containment Spray Pump Operability,Essential Svc Water Pump 1-2 Failed to Develop Sufficient Discharge Pressure.Caused by Dirt in Check Valve V-3-68.Valve Cleaned & Repaired ML20090D2971975-06-0606 June 1975 AO 50-219/75-15:on 750530,calculations of TIP Traces Indicated Total Peaking Factor in One Core Location in Excess of Value of Pf Given in Tech Specs.Caused by Lack of Operating Experience W/New Core Loading ML20090D2981975-06-0202 June 1975 Preliminary AO 50-219/75-15:on 750530,calculations of TIP Traces Indicated Total Peaking Factor in One Core Location in Excess of Value of Pf Given in Tech Specs.Caused by Lack of Operating Experience W/New Core Loading ML20090D6581975-05-30030 May 1975 Preliminary AO-50-219/75-14:on 750529,during Surveillance Test of Containment Spray Pump Operability,Essential Svc Water Pump 1-2 Failed to Develop Sufficient Discharge Pressure.Caused by Dirt in Check Valve V-3-68.Valve Cleaned ML20090D6611975-05-14014 May 1975 AO-50-219/75-13:on 750507,during Surveillance Test,Time Delay Relay 6Kll Failed to de-energize within 15 After Pressure Sensor RE-15C Tripped.Caused by Component Failure.Relay 6Kll Replaced ML20090D6641975-05-0707 May 1975 Preliminary AO-50-219/75-13:on 750507,during Surveillance Test,Time Delay Relay 6Kll Failed to de-energize within 15 After Pressure Sensor RE-15C Tripped.Caused by Component Failure.Relay 6Kll Replaced ML20090D6531975-05-0606 May 1975 AO-50-219/75-12:on 750426,low Reactor Pressure Core Spray Valve Permissive Pressure Switches Re 17B & C Found to Trip at Pressure Less than Tech Spec Value.Caused by Switch Repeatablilty.Switches Recalibr ML20090D6701975-04-28028 April 1975 Preliminary AO-50-219/75-12:on 750426,low Reactor Pressure Core Spray Valve Permissive Pressure Switches Re 178 & C Found to Trip at Pressure Less than Tech Spec Value.Caused by Switch Repeatability.Switches Recalibr ML20090D6751975-04-18018 April 1975 AO-50-219/75-11:on 750410,leakage of Main Line Drain & Bypass Line Exceeded Tech Spec Rate.Caused by Failure of Packing on Valve V-1-110.Valve to Be Repacked ML20090D7001975-04-14014 April 1975 AO-50-219/75-10:on 750404,reactor Bldg to Torus Vacuum Breaker Valves V-26-16 & 18 Leak Rates Exceeded Tech Spec Limits.Caused by Component Failure.Valves Adjusted &/Or Repaired ML20090D6811975-04-11011 April 1975 Preliminary AO-50-219/75-11:on 750410,leakage of Main Line Drain & Bypass Line Exceeded Tech Spec Rate.Caused by Failure of Packing on Valve V-1-110.Valve to Be Repacked ML20090D7131975-04-0808 April 1975 AO-50-219/75-09:on 750329,breaker 1C Tripped Resulting in Fault on Bus 1C.Caused by Fault on Cable 86-25.Cables Replaced ML20090D7061975-04-0707 April 1975 Preliminary AO-50-219/75-10:on 750404,reactor Bldg to Torus Vacuum Breaker Valves V-26-16 & 18 Leak Rates Exceeded Tech Spec Limits.Caused by Component Failure. Valves Adjusted &/Or Repaired ML20090D7271975-04-0303 April 1975 AO-50-219/75-08:on 750325,power Operation Continued W/ Average Linear Heat Generation Rate of Fuel Assemblies in Excess of Max Linear Heat Generation Rate.Caused by Failure to Properly Monitor Reactor Core.Rate Reduced ML20090D7211975-03-31031 March 1975 Preliminary AO-50-219/75-09:on 750329,breaker 1C Tripped Due to Fault on Bus 1C.Caused by Fault on Cable 86-25.Cables Replaced ML20090D7651975-03-27027 March 1975 AO-50-219/75-07:on 750319,during Standby Gas Treatment Sys (SGTS) Test,Dehumidifying Heater EHC-1-5 in SGTS 1 Failed to Energize.Caused by Plugged Orifice in Air Supply to Controller.New Type of Differential Relay Installed ML20090D7361975-03-26026 March 1975 Preliminary AO-50-219/75-08:on 750325,power Operation Continued W/Average Linear Heat Generation Rate of Fuel Assemblies in Excess of Max Linear Heat Generation Rate. Caused by Improper Reactor Core Monitoring.Rate Reduced ML20090D7761975-03-20020 March 1975 Preliminary AO-50-219/75-07:on 750319,during Stanby Gas Treatment Sys (SGTS) Test,Dehumidifying Heater EHC-1-5 in SGTS 1 Failed to Energize.Caused by Plugged Orifice in Air Supply to Controller.New Type of Relay Installed ML20090D7801975-03-19019 March 1975 AO-50-219/75-06:on 750310,stack Gas Sample Sys Failed to Continuously Monitor Stack Releases While Reactor in Unisolated Condition.Caused by Circuit Design.Request to Modify Circuit for Stack Gas Sample Pumps Submitted ML20090D7901975-03-13013 March 1975 AO-50-219/75-05:on 750306,during Monthly Surveillance Test, Containment Spray Pump 51A Failed to Start When Subjected to Simulated Signals.Caused by Breaker Trip Bar Failing to Reset After Previous Breaker Trip.Trip Bar Bushings Cleaned ML20090D7811975-03-11011 March 1975 Preliminary AO-50-219/75-06:on 750310,stack Gas Sample Sys Failed to Monitor Stack Releases While Reactor in Unisolated Condition.Caused by faulty-circuit Design 1975-09-08
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K4451999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Oyster Creek Nuclear Generating Station.With ML20211P6731999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Oyster Creek Nuclear Generating Station.With ML20211A7051999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Oyster Creek Nuclear Station.With ML20209G0631999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Oyster Creek Nuclear Generating Station.With ML20212H5491999-06-18018 June 1999 Non-proprietary Rev 4 to HI-981983, Licensing Rept for Storage Capacity Expansion of Oyster Creek Spent Fuel Pool ML20195E7961999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Oyster Creek Nuclear Generating Station.With ML20206N7431999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Oyster Creek Nuclear Generating Station.With ML20205P5401999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Oyster Creek Nuclear Generating Station.With ML20204C8201999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Oyster Creek Nuclear Generating Station.With ML20199E4671998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Oyster Creek Nuclear Generating Station.With ML20195E8321998-12-31031 December 1998 10CFR50.59(b) Rept of Changes to Oyster Creek Sys & Procedures, for Period of June 1997 to Dec 1998.With ML20198D2091998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Oyster Creek Nuclear Generating Station.With ML20195J8591998-11-12012 November 1998 Rev 11 to 1000-PLN-7200.01, Gpu Nuclear Operational QA Plan ML20195C4271998-11-0606 November 1998 Safety Evaluation Supporting Proposed Ocnpp Mod to Install Core Support Plate Wedges to Structurally Replace Lateral Resistance Provided by Rim Hold Down Bolts for One Operating Cycle ML20155J3021998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Oyster Creek Nuclear Generating Station.With ML20154R4981998-10-20020 October 1998 Core Spray Sys Insp Program - 17R ML20154L3051998-10-14014 October 1998 Safety Evaluation Accepting Licensee Request to Defer Insp of 79 Welds from One Fuel Cycle at 17R Outage ML20154Q3371998-09-30030 September 1998 Rev 8 to Oyster Creek Cycle 17,COLR ML20154L5571998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Oyster Creek Nuclear Generating Station.With ML20151V6311998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Oyster Creek Nuclear Generating Station.With ML20237D5691998-08-31031 August 1998 Rev 0 to MPR-1957, Design Submittal for Oyster Creek Core Plate Wedge Modification ML20237D5711998-08-18018 August 1998 Rev 0 to SE-000222-002, Core Plate Wedge Installation ML20237B0131998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Oyster Creek Nuclear Generating Station ML20236R0511998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Oyster Creek Nuclear Generating Station ML20249B2981998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Oyster Creek Nuclear Station ML20248F3531998-05-21021 May 1998 Part 21 Rept Re Electronic Equipment Repaired or Reworked by Integrated Resources,Inc from Approx 930101-980501.Caused by 1 Capacitor in Each Unit Being Installed W/Reverse Polarity. Policy of Second Checking All Capacitors Is Being Adopted ML20247F1891998-05-0505 May 1998 Risk Evaluation of Post-LOCA Containment Overpressure Request ML20247G0581998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Oyster Creek Nuclear Generating Station ML20216K0341998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Oyster Creek Nuclear Generating Station ML20151Y4651998-03-31031 March 1998 Non-proprietary Version of Rev 1 to GENE-E21-00143, ECCS Suction Strainer Hydraulic Sizing Rept ML20217A4631998-03-23023 March 1998 Safety Evaluation Accepting Use of Three Heats/Lots of Hot Rolled XM-19 Matl in Core Shroud Repair Assemblies Re Licenses DPR-16 & DPR-59,respectively ML20212E2291998-03-0404 March 1998 Rev 11 to 1000-PLN-7200,01, Gpu Nuclear Operational QAP, Consisting of Revised Pages & Pages for Which Pagination Affected ML20216J0841998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Oyster Creek Nuclear Generating Station ML20203B2781998-02-16016 February 1998 10CFR50.59(b) Rept of Changes to Oyster Creek Systems & Procedures ML20203A3801998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Oyster Creek Nuclear Generation Station ML20198P1791997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Oyster Creek Nuclear Station ML20217C7591997-12-31031 December 1997 1997 Annual Environmental Operating Rept for Oyster Creek Nuclear Generating Station ML20197E9131997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Oyster Creek Nuclear Station ML20199E4561997-11-13013 November 1997 Safety Evaluation Accepting Ampacity Derating Analysis in Response to NRC RAI Re GL-92-08, Thermo-Lag 330-1 Fire Barriers, for Plant ML20199D4381997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Oyster Creek Nuclear Station ML20202E8511997-10-21021 October 1997 Rev 0 to Scenario 47, Gpu Nuclear Oyster Creek Nuclear Generating Station Emergency Preparedness (Nrc/Fema Evaluated) 1997 Biennial Exercise. Pages 49 & 59 of Incoming Submittal Were Not Included ML20211M9481997-10-0303 October 1997 Supplemental Part 21 Rept Re Condition Effected Emergency Svc Water Pumps Supplied by Bw/Ip Intl Inc to Gpu Nuclear, Oyster Creek Nuclear Generation Station.No Other Nuclear Generating Stations Effected by Notification ML20198J7361997-09-30030 September 1997 Monthly Operating Rept for Sept 1997 for Oyster Creek Nuclear Generating Station ML20211B7461997-09-24024 September 1997 Part 21 Rept Re Failure of Emergency Service Water Pump Due to Threaded Flange Attaching Column to Top Series Case Failure.Caused by Dissimilar Metals.Pumps in High Ion Svc Will Be Upgraded to 316 Stainless Steel Matl ML20210V0181997-08-31031 August 1997 Monthly Operating Rept for Aug 1997 for Oyster Creek Nuclear Generating Station ML20210L2961997-07-31031 July 1997 Monthly Operating Rept for Jul 1997 for Oyster Creek Nuclear Station ML20149F9961997-07-18018 July 1997 Safety Evaluation Re Gpu Nuclear Operational Quality Assurance Plan,Rev 10 for Three Mile Island Nuclear Generating Station,Unit 1 & Oyster Creek Nuclear Generating Station ML20196H0111997-07-11011 July 1997 Special Rept 97-001:on 970620,removed High Range Radioactive Noble Gas Effluent Monitor (Stack Ragems) from Service to Allow Secondary Calibr IAW Master Surveillance Schedule. Completed Calibr on 970628 & Returned Stack Ragems to Svc ML20210L3081997-06-30030 June 1997 Corrected Page to MOR for June 1997 for Oyster Creek Nuclear Generating Station ML20141H2051997-06-30030 June 1997 Monthly Operating Rept for June 1997 for Oyster Creek Nuclear Station 1999-09-30
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SEVCNTY SCVEN OROVC STRCCT RUTLAND, VI<itM'O NT 0 5'701 REPLY 10:
VYV-3071 p, o, gox ,37 VERNON, VERMONT ol.751 November 14, 1973 Director Directorate of Licensing United States Atomic Energy Commission Washington, D.C. 20545
REFERENCE:
Operating License DPR-28
- Docket No. 50-271 Abnorcal Occurrence N6. A0-73-31 Gentlemen:
As defined in Section 6.7.D.1 of the Technical Specifications for the Vermont Yankee Nuclear Pouer Station, we are rcporting the following Abnormal Occurrence as A0-73-31. .-
On Novenber 7, I973, at 2101, while the plant was in a shut down condition and while the required Control Rod Friction testing uns being perforned on control rod 26-23, a react or scram occurred initiated by a high-high flux signal from the Intermediat e Ranac Neutron "onitoring System.
An inmediate investigation revealed that rod 30-23 cas in the fully withdrm:n position t.hile rod 26-23 was being withdraun for its friction
. test., This situation was a result of inadequate
- y ementation of administrat!ve or procedural controls and constituted a violation of Section 1. A.8 of the Technical Specifications.
Section 14.5.3.2 o,f the Vermont Yankee FSAR deals with cont rol rod withdre,eal errors when the reactor is at pover levels belou the power range. The r,ost severe case occurs when the reactor is just critical at rocu temperature and an out-of-sequence rbd is continuously withdraun.
The resultn of ther.e analyses indicate that no fuel daunge will occur ,
due to the rod withdrawal.
THIS DOCUMENT CONTAINS POOR QUAUTY PAGES i I
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b'ovemb er 14, 1973 Page 2 .
The station had been in a planned shutdoun condition since September 28, 1973, in order to perform core reconstitution and interconnection of the Advanced Off-Gas System. On !!ovenber 7, 1973, work had progressed to the point where final core loading had been completed. At that point, it became desirable to perforu final core verification concurrent with control rod timing and friction tests. In order to accomodate both requirements, it was necessary to install jumpers to the refuel interlock portica of the Reactor Manual Control System in order to allow traversing of the television camera nounted on the fuel grapple chile performing control
, red friction and timing tests. Although the intent of installing the junpers was reasonabic and proper, the ensuing inplementation of this program went beyond the. scope of original intent. 'lhe reasons for this uere the inadequacy of interdepartnental contunications; in addition, certain procedures de:constrated incdequacies, specifically l'urth er, AP 504, Lifted Leads Log, OP 408, Control llod Drive System.
the control rod friction testing uns being performed in accordance uith a Startup Test Proccdure; an approved opcrating procedure did not exist.
The result of the jumper installation was a condition of interlocks thich did not prevent withdrawal of nore than ene control rod at a tire.
The operating personnel cere not adequately inferned of the jumpered interlock status; centrol rod testing was resumed concurrent with core verification. As control rod testing progressed, rod 30-23 uns inadvertantly Icft in the fully withdraun position. After core that verification cor. trol tas completed, and since the reactor operator was not cegnizant rod 30-23 was still uithd::.un, an adjacent lateral control rod 26-23 cas selected cnd its continuous withdrawal begun in preparation for the fricticr.
test. Detteen not ch posit ion O and 26, the operr. tor noticed rnpid source range conitor response. He inmediately initiatcJ control rod insertion.
At th$ t ime a full rod scram 1:ss initiated by the interr;cdiat e ran;;c conit or hi rh-high flus signals . It was later d:monstrated that contr4 rod 30-23 diy, ital position display was functioninl properly. The reactor operat or could not explain his failure to observe the indication of centrol rod 30-23 being fully withdraun.
The iruediate action of the Shif t Supervisor on duty uns to notify birher plant nanancent and to detert. ire i f pe: sonnel were on the re fueling floor during the incident and to request d:wl:4eter reading- of all perronnH at that location en the conservat ive ar.su.:pt ion that a criticality nay heve occurred. 1:ive personnel were on'lhe the refueling floor at the tiec in areas not adiecent t o t he open vennel . i;:xinne dc ;iret er reading of the personkel involved u.. 25 nr; hor.ever thir t ot al uns accunolat ed over a 11 was five hour work period nnd not at t ribut abic t o this incident alone.
also teri fied that the lec.il area nauitors, the contin w a:, ai r uc.:i t or on the refnelin:; floor, as uc11 a- the 1:eactor I:uilding Vent ilation !!.c ..ne t monit on :.hoved m incre.r.ed level of radict ion.
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,t, Page 3 Following the arrival on site of the Assistant Pla'nt Superintendent und the Reactor Engineer, further evaluation determined that the scope of installed jumpers was beyond the original intent. 'the jumpers ucre removed and it was decided to perform a subcriticality test on cach of the two involved control rods which verified their proper effectiveness.
Based upon the above evaluations, it was determined that no fuel failure had occurred and no radiation problem existed. The installed interlock jumpers were removed and a verification test conducted to determine that the rod block interlock was restored.
On Novenber 8,1973, consnitation with off-site higher management and engineering personnel resulted in the renoval of the involved fuel assemblics from the core for sipping and visual inspection. No evidence of Icakage or visual degradation was observed. The following is a listing
'of the assemblics examined and their location:
Assembly Number Core Location VT 164* 27-22
\T 171* - 29-22 VT 167 27-24 Vr 175 '29-24 Vf 049 31-32 In addition, a two rod critien1 test was conducted utilizing control rods 30-23 and 26-23. As a result of this test , it was deternined that with control rod 30-23 in the fully withdrawn position, criticality was achieved when control rod 26-23 was withdr:azn to notch 16.
The filn badr,cs assigned to personnel on the refueling floor at the tire Cf the incident ucre sent out for proc.c:.s ing. 'the recults of the j badge bearing neut ron sensing indicated a t ot aj of 50 or bet a-garena and i zero neutron exposure. This tot al badge eximure was acetoulated over a two day work period. The results of the remaining four bedres indiented that two badr.es neasured 20 nr bet a-r.aum and tuo hadges reasured 0 nr b et a- 9,amma .
Subscrpent calcul ut i ons. by Q2neral Elect ri e Co. veri fied crit ica)) t y Further c:.lculati on at not ch 16 on rod 26-23 with rod 50-23 fully uithdraun.
by Cencral 1:1cetric Co. det ermined that with red 30-23 fully withdr: n and and had rod 20-23 rod 26-23 at not ch 26, the exs cw react ivity was 0.0M t.l.,
been fu))y withdraun, the excess venet ivity would have bt en 0.!)M /J.
- These assenhlies we re visually in'.pect ed.
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. j Directorate of Licensing November 14, 1973 Page 4 General Electric personnel with recognized competency in the arca of core hinctics, and in particular control rod drop accidents, uncontrolled withdrawal incidents, etc. , did a qualitative evaluation of what transr ' red based on the above statistical information. An estimate based upon many previous calculations of a similar nature, was that the bounding results were as follows. The peak fuel center line temperature would have increased no mere than 500*F and the peak clad temperature would have-increased no more than 50 F from the starting conditions. Therefore, the fuel center line temperature was no higher than 585 F an.d the peak clad temperature was no higher than 135*F.
Plant management has discussed at length with all involved personnel
,tl)c signi icance f of this incident and stressed the areas of inadequate personnel performance. Further, a review h:is been uade of the past and present performance of the employees directly invohed in this incident.
- mis assessment has determined that these employees are capable, sincere, and conscientous and that every reasonable assurance exists that they are adequately qualified in all respects to continue in their present assigned job responsibilities.
Upon completion of an indeptl evaluation of the total' incident and the various now apparent inadequacies, it is concluded that no singular outstanding arca was predominant.
The Plant Operations Review Committec (PORC), uct to rev.iew the inci dent and made the following recommendations and/or conclusions:
I 1. The original int ent of the jumpers was reasonabic; however, the f.inal condition obtained was improper and the applied jumper::. should have been renoved imaediately following the complet i on of core veri ficat ion. ,
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- 2. The results obtained from the fuel asse:::blies sipped and inspected on Noven'>er 8,1973, showed no observed indicatj ons which would preclude pl mt startup.
The P1 vnt Operat i ons Revi ew Connit t ee. quest i oned wht the r adt quat e sensitivity to sipping still existed con ,j dering the elapsed shut doun tir.e and recen x aded 't al ing tua ). noun lea!,ers previon t i) reuoved during this shutdpun and sippiny, t o dat ernine if adc qunte sensitivity still existcd. On ::oveuher 11, 1973 tuo fuel I '2 l assemh)ies were sipped in an aticcpt t o prove l I3I and I
) sensitivity. Th( posj t ive J esul t: Obinined veri y the udequacy l of sipping, sensit ivit j os oh ;e rved on l orci,her C, 19 '/3 .
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2 Suberitical testing results of the two involved control rods and the management evaluation of the plant condition on November 7,1973, were deemed sufficient to permit further control rod friction testing following the incident.
- 4. Administrative Procedure AP 504 " Lifted Lead Log" was not adhered to. Jumper installation was not recorded in the general plant log.
- 5. All plant procedures relating to control rod movement shall be modified to reflect interlock requirements imposed by the reactor mode swit ch positi on.
- 6. Specific operating procedures addressing control rod friction and settling test s sha.11. be developed.
- 7. The present AP 501, Lifted Leads Log procedure, is inadequate and a PO!!C sub-committee has been appointed to review and/or revise the current procedure.
S. Until the above appointed PORC sub-committep performs its task, no installation of jumpers or Jifted Icads shall be perforced on the circuitry associated with the Reactor Protection S,vstem, the Primary Contain::.cnt Isolation Systen, any ECC System, the Reactor Manual Control System and any refuel interlock until approved by PORC.
- 9. No further tuo (2) rod critical testing shall be performed on side by side rods.
- 10. The following itens contributed to the incident:
to
- a. A lack of definition on the interfacing of responsjhilities on an int erdepartment al level,
- b. Failure by p1m.1 supervisi on t o exercise ri norous slept icist.,
relati ve to abnornal or inadequat e plant conditions that are encountcred. ,
- c. Operator error. -
- m. ___ _
._- j i
et VCRMONT YANKCC NUCLCAR POWER CORPORA 7i; -
, ]
Directorat'e of Licensing t;oveml>c r 14, 1973 , !
Page 6
. l At the request of the I!: nager of Operations, the I?uclear Salcty Audit and Review Com..ittee ract in a special meetin;; on November 14, J973, to review the incident. The NSAR returned the following conclusiens:
- 1. !!o unrevicwed safety question was involved.
- 2. llic health and safety of the public and plant personnel was not impaired.
- 3. There is no undue rish to the health and safety of the public if the plant is started up and operated in accord with the proposed schedule. .
Sincerely, VEPJ:GNT YANKEli NUCLEAR PO'.iER COPJ'ORATICS
- D kuq, O' .u- ..
. V c~. ' . - :'
B U. Ri J ey
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P] ant Superintendent EFl!!/UFC/' bd .
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1 1
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- Prclinir.ary ,
, ( Abnomal-0ccurronco 1
. Report No. 73-29 ,
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St)MEct: Violation of the Technical' Specifications, paragraph 3.8 A, l i
in that during power operation, by virtue of the fact that an !
I inoperable snubber existed on steam Ilnes to each of the two i,
.lsolat.Lon Condensers, both conden~sers were considorod to bo
. inoperabl e. -
f This event is ccasidered to bo.an abnorcal occurren'cc as defined I in..the Technical Specifications, paragraph 1.15B and D. Notifi/
i;. .
cation of this event,'as required by the Technical Spr cifications, paragraph 6.6.2.n, viti mde to td. Region'i, Dirictorate of Regu-latory Operations,-by telephone on $sturdsy, Nover.her 3,1973, at
./ ; .
,, l 0850, and by telecopior on Honday, Ndvether $,1973, ht 1315. 1 g.
~.l SITUATION: h* nile conducting in 'inipection of the hydraulic shoch'and sway l
!streM. ors (snuhbers) located on varl us systens-in the' Reactor, Building, but. outside of the Drheell, the accteulators on one. ;
i unit'on the steam line to the A IsN otion Condenser bnd one unit ,
on the staan line to the B Isolation Condenser were found to be l
t devoid of fluid, soth units we2+ considered to be inoperabic. l l
To bo detemined upon inspection. .
CAtlSE:
l ItEHRDIAL Af7 TON: -
l As per the requfrements of the Technical Specifications, para-graph 3 d' ,0, an orderly plnnt shutdown was comenced upon noti-4 THIS DOCUMENT CONTAINS !
[/'CfC O[ -
POOR QUAUTY PAGES - !
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Nove5cr2[1h5 s
e fication of the situation at ' 1850. 14canwhile, imedinte. efforts
- were cade. to refill' t.h'c sntthbor accumulator on the A Isolation Condenser atsam line, 'Ihis action was completed by 1845, re- -
turning the sm6ber"to ' service, The load drop which had been started was halted snu autput was.again incrensed to the initial-
' level, Follow-up action ' included replacement of.the acntmaintor on the snubber installed on the Ti Isolation Condensor stecn line, then replacement Of the entire.spubber unit' on the A Isolation condenser steam line. Tnis acti'on was corp 1sted by 1910 Friday cycning. A follow-up check was then made on Saturday evening to insure that'no fluid Io.fs proh' i?. existed, SAFHn' SHNIFICANCE:
[.
Atendrent 67 t'o 'the EDSAR detailr. the,requirepnts .for at losst i, -
one Isolation Condenser to be available as a .hect sink in the i
cycnt of a li)s.iof Coolt.nti-Accident. . In this.sittution, it can he postulated,that this requirement r.ight not have'been r.et, had an earthqtiske . occurred which would require .the snubber to be fully 'openthie, E
S e
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- Prepared by: '
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l c.e t-Ws t. Date: N !6~ 73 l
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