ML20136C405
ML20136C405 | |
Person / Time | |
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Site: | Three Mile Island |
Issue date: | 11/04/1985 |
From: | Conte R NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
To: | |
Shared Package | |
ML20136C327 | List: |
References | |
50-289-85-24, NUDOCS 8511210083 | |
Download: ML20136C405 (30) | |
See also: IR 05000289/1985024
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. U.S. NUCLEAR REGULATORY COMMISSION REGION I Report No. 50-289/85-24 Docket No. 50-289 License No. DPR-50 Priority -- Category C Licensee: GPU Nuclear Corporation Post Office Box 480 Middletown, Pennsylvania 17057 Facility At: Three Mile Island Nuclear Station, Unit 1 Inspection At: Middletown, Pennsylvania Inspection Conducted: October 11-18, 1985 Inspectors: W. Baunack, Project Engineer, Region I N. Blumberg, Lead Reactor Engineer, Region I *J. Cummins, Senior Resident Inspector (Wolf Creek), Region IV N. Dudley, Lead Reactor Engineer (Examiner), Region I *D. Falconer .?r., Lead Reactor Engineer, Region II D. Haverkamp, Technical Assistant for THI-1 Restart, Region I W. Johnson, Senior Resident Inspector (Arkansas), Region IV T. Peebles, Senior Resident Inspector (Turkey Point) Region II R. Urban, Reactor 'gineer, Region I D. Vito, Senior Er srgency Specialist, Region I P. Wen, Reactor Engineer, Reglon I J. White, Senior Radiation Specialist, Region I F. Young, Resident Inspector (TMI-1), Region I Contractor Personnel: B. Gore, Research Scientist, Battelle PNL J. Huenefeld, Research Engineer, Battelle PNL * Participation was limited, generally, to site familiarization training and facility orientation. Approved By: Id R. Conte, TMI-1 Restart Manager //!'/ Date 7 TMI-1 Restart Staff Division of Reactor Projects 8511210083 851107 PDR ADOCK 05000289 G PDR . e -*
. * * . , . ., 2 Inspection Summary: Routine and special (NRC shift coverage) safety inspection (369 hours) of power operations focusing on operator and management performance, related startup testing / operations, decay heat removal system operational verification, licensed operator requalification program, and gaseous radioactive releases. Inspection Results: Operators continued to demonstrate their detailed knowledge of plant design as .well as their ability to safely operate the facility, especially in the manual control mode of integrated control system operation. The level of knowledge of the auxiliary operators was commensurate _with their duties. Maintenance depart- ment personnel, especially instrument and control technicians, worked well with control room operators in keeping them informed of their troubleshooting efforts. Overall, procedures were adequate to support operations and were properly imple- mented. Major safety-related equipment remained in service except when surveillance testing or preventive / corrective maintenance.was conducted. A secondary plant drain line problem impacted the progress of the test program because of recur- reat weld cracking due to fatigue failure. Observations were made of worker actions in building spaces that had the potential to cause unnecessary transients and/or challenges to safety systems and operators. The testing program was interrupted slightly due to the secondary plant drain line problems. Test procedures were properly implemented and, in general, data were in accordance with the test acceptance criteria. Test briefings continued to be used routinely. The operating procedure for the decay heat removal system was adequate for safe
1 operation of the system and it assured that the system was properly lined up
for standby status. The licensee's requalification program is well organized and documented and conforms to regulatory requirements. The licensee is appro- priately quantifying non-routine gaseous releases from the facility during operations. The licensee also provided an interim resolution to our previous inspection finding on the emergency feedwater system safety valves.
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. .. _ _ ._ _ . .- . - . * ., '., 4 DETAILS
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1. Introduction and Overview 1.1 General At the beginning of this inspection period on October 11, 1985, the j > TMI-1 Restart Staff was providing around-the-clock coverage to assess
- restart operating activities. The plant was then at 15% of rated
, power at normal operating conditions. This continuous observation of 1 plant activities was maintained by inspectors from Regions I, II, and IV and by reactor operator examiners from Battelle Pacific Northwest Laboratories, an NRC contractor. Also, Region I inspectors continued ; ' daily coverage of testing activities. Additional Region I personnel were on site during portions of the period to augment the resident inspection staff. 1.2 Facility Restart Operations
, During the period of October 11-18, 1985, the significant TMI-1
> restart operational milestones included (a) completing main turbine generator testing and electric power generation at the 15% and 25% testing-plateaus and (2) initial main turbine generator testing at
j the 40% plateau. The chronological summary of plant operations
during this period is presented below.
, Date Time Operational Highlight or Milestone "
, 10/11/85 7:00 a.m. Reactor at 15% of rated power, reactor coolant average temperature at 567 F and pressure at 2155 psig
10/12/85 2:28 a.m. Conducted overspeed trip test of main turbine generator
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6:00 a.m. Turbine generator on line
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7:30 a.m. Increased power to 28% , ' 10/13/85 5:51 a.m. Commenced power reduct un to repair leak on main steam drain line 6:00 a.m. Turbine generator off line 5:02 p.m. Repairs to main steam drain line completed and turbine generator on line
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- . . _ . - - - -. _ . ' ' ' . . 4 Date Time Operational Highlight or Milestone
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10/14/85 1:00 a.m. Increased power to 29% 1:50 a.m. Commenced power reduction to repair leak on main steam drain line
. 2:02 a.m. Turbine generator off line ,
9:44 p.m. Repairs to main steam drain line completed and turbine generator on line 10:55 p.m. Increased power to 27.8%
' 10/15/85 10:15 a.m. Commenced increasing power to 40% 11:08 a.m. Reactor power at 40%
- 10/16/85 9
- 30 a.m. Commenced power reduction to repair
, leak on main steam drain line [ 10:07 a.m. Turbine generator off line
8:38 p.m. Repairs to main steam drain line completed and turbine generator on line
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- 11 p.m. Increased power to 41.5%
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10/17/85 1:15 a.m. Commenced power reduction to repair
- leak on main steam drain line
1:53 a.m. Turbine generator off line
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10/18/85 7:00 a.m. Reactor at 7% of rated power, steaming , the secondary plant to the main condenser using the turbine bypass
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valves. 1.3 Operational Events Recurring problems with weld failures-in two drain lines from the turbine control valve headers interrupted the startup testing program. Also, early during the period, there was a power escalation delay due to inability of one of the integrated control system (ICS) controllers
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to satisfactorily function in the automatic mode. There were no other events during this period that were considered either operationally significant or matters of special interest to the TMI-1 Restart Staff.
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'. - '. 5 The turbine control valve drain line weld failures did not adversely impact the safe operation of the facility. Nevertheless, the licensee's test program was delayed several days due to the recurring weld failures and these failures resulted in considerable public interest. Therefore, the operating history and sequence of recent operating problems related to these drain lines is described in this section. The piping between the turbine control valves and the high pressure turbine contains moisture drain lines which are one-inch in diameter. Two of these drain lines had been installed with a strainer and an orifice at the time of initial construction of the facility in the early 1970's. The other two drain lines consisted of straight pipe and contained no such strainer or orifice. In 1983 General Electric recommended changing the method of admitting steam to the high pressure end of the turbine. This operational change involved some modifications to the turbine controls and the removal of the strainer and orifice from the two drain lines. The modifications were accomplished prior to the current startup, however, the strainer housings were left in place. On October 9, 1985, a steam leak developed in a weld in one of the drain lines ups ream of its strainer housing. The leak became progressively worse necessitating a turbine shutdown. The leak was repaired on October 12, 1985 by welding a " clam shell" cover over the defective weld. During the remainder of the period, there were three additional weld failures in this line including two field repair welds and a shop weld. In addition, there was one weld failure in the other drain line that contained a strainer housing. Each of these failures necessitated removal of the turbine generator from the grid and a reduction of reactor power to about 5-10% of rated power. The licensee identified the failure mechanism as high cycle fatigue due to vibration with no evidence of corrosion. The licensee, in conjunction with General Electric, developed and implemented, shortly after this inspection period, a design modification to the drain lines. This fix was effective in permitting the licensee to complete testing at the 40% plateau, which will be as de.;ribed in Inspection Report 50-289/85-25. 1.4 Summary This inspection included continued progress of restart testing activities up to the 40% power plateau. Throughout this period there were several power reductions to 5-10% reactor power while repairs were made to the weld failures in two of the drain lines from the four main turbine control valve headers. The TMI-1 Restart
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Staff remained sensitive to an adverse impact on shift supervisor safety duties due to NRC. shift inspector questioning and discussions of matters of a programmatic nature. Accordingly, the shift inspectors referred only implementation matters or status questions to the shift supervisor and referred programmatic (event followup,
i design or procedure adequacy problems) to resident and region-based
NRC personnel. Resident and region-based personnel interfaced with licensee support groups in followup to shift inspector referrals / concerns. The staff's observations and findings regarding plant operation and testing and_ licensee response to operational events is discussed in the report sections that follow. 2. Shift Inspection Activities 2.1 Scope of Review and Observations . During the period of October 11-18, 1985, the TMI-1 Restart Staff ! continued its augmented shift inspection coverage. The NRC shift ) inspectors assessed the adequacy and effectiveness of operating personnel performance based on the inspectors' observations of operating and startup activities to determine that:
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-- operators are attentive and responsive to plant parameters and conditions; -- plant evolutions and testing are planned and properly
- authorized;
! -- procedures are used and followed as required by plant l policy;
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i -- equipment status changes are appropriately documented and
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communicated to appropriate shift personnel; -- the operating conditions of plant equipment are effectively monitored and appropriate corrective action is initiated when required;
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-- backup instrumentation, measurements, and readings are
i used as appropriate when normal instrumentation is found
to be defective or out of tolerance; -- logkeeping is timely, accurate, and adequately reflects plant activities and status;
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-- operators fqllow good operating practices in conducting plant operations; and, -- operator actions are consistent with~ performance-oriented training. , - - , , , , , ----n n --. ,--- -
.. . .. . _ - - . _ _ - _ . _ _ _ _ - . . _ . - _ - _ _ - _ * * * * . . 7 The shift inspectors' observations included, but were not limited to, those reactor plant operation and testing activities, periodic
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surveillance activities, and preventive and corrective maintenance activities listed below. ; Reactor Plant Operation and Testing Activities ' -- routine control room operations including annunciator alarm response -- operating and emergency procedures discussions with shift supervisors, shift foremen, control room operators, and shift technical advisors -- periodic inspection observation tours of areas'outside the control room, including diesel generator rore,, emergency feedwater rooms, control building, turbine building, auxiliary building, intermediate building, electrical switchgear rooms, and outside buildings and yard areas
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-- shift preparation briefings and conduct of turbine overspeed trip testing
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. -- operational preparations for removing train A of extraction steam for weld repair
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: -- power level increase to 25% of rated power -- integrated control system (ICS) tuning -- power level reddctions and increases including turbine generator shutdown /startup for drain line weld repairs -- secondary plant auxiliary operator observation / readings rounds
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-- fire drill ~in vicinity of hot machine shop
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' -- power level increase to 40% of rated power with ICS fully in automatic -- inspector verification of core flood tank valve breakers
j and building spray valve positions
-- operator response to makeup total flow instrument MU-42-FI failure high .
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- - . . . . . - - . . - . - _ . . . . . . * ' * - . . 8 -- shift foreman response to loop A reactor coolant flow nuisance alarm due to plant conditions at low power level -- crew briefings prior to major changes in operating power 1 levels -- operator response to automatic turbir.e trip, while at 10 MWe, due to high moisture separator levels -- operating shift response to rod control shifting to manual
- after experiencing a motor fault
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Periodic Surveillance Activities -- reactor coolant system (RCS) leakage measurements -- RCS heat balance calculations -- reactor building 30 psig analog channel monthly test -- turbine-driven emergency feedwater pump functional test and valve operability test -- reactor protection system channel D monthly test -- control rod movement test -- personnel airlock leak rate measurement 1 -- nuclear service river water pumps and valves inservice inspection testing Preventive and Corrective Maintenance Activities -- auxiliary boiler B repairs -- repairs of weld leaks on secondary system steam line drain piping downstream of turbine control valves -- main feedwater control valves A and B mechanical repairs -- integrated control system oscillation troubleshooting and
j repairs
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' ' - - . . 9 2.2 Assessments of Shift Inspectors 2.2.1 General The shift inspectors assured that any potentially adverse safety concern or regulatory finding was identified promptly to both the licensee's shift supervisor and the TMI-I Restart Manager. Those items requiring additional staff review or followup are described in parag*aph 3 of this report. Also, at the end of their assigned period of shift inspection activities, the inspectors provided their general assessment of facility operational readiness and operating personnel performance. These general assessments included, as applicable, each inspector's overall views related to operations, technical support, maintenance, surveillance, radiological controls, training, emergency planning, physical security, and housekeeping / fire protection. The inspectors' assessments are presented below. 2.2.2 Operator Performance In general, control room operators continued to demonstrate their detailed knowledge of plant design and current status of testing and operational activities. Their operational abilities were rigorously challenged during this period due to the numerous power. level changes and minor transients induced because of integrated control system (ICS) tuning problems. The operators were successful in taking manual control of the ICS and avoiding a significant transient that had the potential to challenge safety-related system. This can be attributed to their alertness and attentiveness to their duties in overall control of the plant. The team concept continued to be evident especially when operators were in manual control of the ICS. These situations demanded continuous and clear communications -between control station operators because of the effect that any one individual could have on the entire plant. At times during these evolutions, communications faultered and emotions got somewhat tense, but shift supervision or licensee management stepped ir and controlled the situation to avoid any major plant transient. During other routine evolutions, control room operator communica- tions became somewhat lax in that valve numbers were referred
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'. . 4 10 to without system designators. In no case did this lapse of communications induce an ineffective exchange of infor- mation resulting in an adverse safety situation. Control room operator communications during routine and transient situations will continue to be routinely followed during shift inspector activities. The shift inspectors continued to assess auxiliary operator knowledge and performance by focusing on how they conducted . their shift tours and discussing related observations and their knowledge of plant equipment operability. In partic- ular, several secondary auxiliary operators were quizzed on how to take manual control of the-emergency feedwater (EFW) flow control valves since that would be an emergency func g tion in accordance with restart condition 1.p. All of the auxiliary operators demonstrated an appropriate knowledge of plant design for their positions including EFW manual control. They demonstrated alertness and attentivess to the numerous observations made on their tours. They kept the control room operators informed of plant status condi- tions as reflected in building spaces. In general, procedures were properly implemented. Shift inspectors noted that the ICS operating procedures did not fit the unique conditions of plant operation for the current mode (see paragraph 3.2.2). Further, certain operators were observed eating in the center console area (see para- graph 3.2.2). The proper use and implementation of facility procedures will continue to be routinely followed during shift inspector activities. Overall, operators were formal and professional in their activities. Minor errors were caught by more experienced operators. Although some signs of inexperience showed through, there were no questions by the TMI-1 Restart Staff on the operators' ability to safely operate TMI-1, 2.2.3 Training The numerous power level changes during this period provided the operators with excellent opportunities to gain opera- tional experience, especially when the ICS needed to be operated in manual. The control room operators' simulator training, in which manual operation of the ICS was quite frequent, appeared to have been effective in preparing the operators for the unique aspects of the test program. Shift supervisor and licensee management continued their emphasis on every event being a learning experience.
m * . . '. , 11 2.2.4 Technical Support Shift technical advisers continued to be effectively used with the the operating shift. There were no recurrent interface problems between operators and test engineers as had been noted in the last inspection report. 2.2.5 Maintenance / Material Condition The shift inspectors provided no significant adverse comments, as noted.in paragraph 3.2.1, regarding the material condition of the plant. Overall, they were satisfied except for certain areas of the turbine
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building. Equipment problems continued to be relatively few and agressively pursued. Instrument and control (I&C) technicians' troubleshooting efforts were coordinated well with the control room operators. There was definite maintenance management involvement and attention to daily problems as evidenced by frequent visits to the control room or to areas of interest in the plant. 2.2.6 Surveillance Testing Surveillance activities were well coordinated with operations department activities. Surveillance procedures were properly implemented. 2.2.7 Radiological Control The miminization of contamination areas was noticeable. Contaminated material was properly secured. Areas were properly posted with useful information. Health physics personnel appeared conscientious in their duties and properly conducted routine surveys. 2.2.8 Emergency Planning No inspector observations were made in this area during this period. 2.2.9 Security Security personnel were observed making special patrols during heavy fog and they were attentive to their duties.
., ., 1 12 - 2.3 Conclusion Control room operators not only continued to demonstrate their detailed knowledge of the facility, but they also demonstrated their ability to safely operate the plant especially in the manual mode of ICS and avoid challenges to safety-related systems. An independent shift organization and team concept continued throughout the inspection period with little evidence of recurrent interface problems between operators and test engineers. Auxiliary operators continued to demonstrate an appropriate knowledge level. Maintenance department personnel worked well with the on-shift organization. Overall, pro- cedures were properly implemented. ' Effective on-the-job training was achieved for operators and technicians. Proper radiological controls were exhibited by all personnel observed. Overall, personnel con-- ducted themselves in a formal and professional manner. 3. Plant Operations
, 4 3.1 Routine Review ! TMI-1 Restart Staff inspectors periodically inspected the facility j to determine the licensee's compliance with general operating
i requirements of Section 6 of the Technical Specifications (TS) in I the following areas: -- review of selected plant parameters for abnormal trends -- plant status from a maintenance / modification viewpoint
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including plant housekeeping and fire protection measures -- control of ongoing and special evolutions, including control room personnel awareness of these evolutions -- control of documents including log-keeping practices -- implementation of radiological controls -- implementation of the security plan including access control, boundary integrity and badging practices The inspectors ,also focused their attention on the areas listed below. -- control' room operations during regular and backshift hours, including frequent observation of activities in progress and periodic reviews of selected sections of the shift foreman's log and control room operator's log and other control room daily logs __ . - ,_ ,
* '. . - 13 l -- followup items identified by shift inspector activities (paragraph 2) -- areas outside the control room -- selected licensee planning meetings As a result of this review, the ir.spectors reviewed specific events in more detail as described in the sections that follow. 3.2 Findings 3.2.1 General In general, housekeeping and fire protection measures remained consistent with previous high standards in safety-related areas. Cigarette butts and a moderate amount of dust were noted on top of safety-related switchgear in the control building. Apparently, this
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material was left over from the shutdown period during which workers provided extensive structural steel fire- proofing in the area. The dust is somewhat expected and
1 the material will be removed during preventive maintenance
on the switchgear. Also, licensee efforts to hold back the boundaries for contaminated areas were notable in permitting free access for management inspection purposes. The turbine building continued to have cleanliness problems with respect to the removal of temporary structures built to support the previous long term outage.
( None of the conditions in the affected areas adversely
affected safe operation of the facility. Overall, the material condition of the plant remained
- quite good. Plant performance continued to be as expected
with only minor safety-related equipment problems. The main steam drain line leak was a persistent secondary plant problem that delayed progress of the power escalation test program. Management involvement and attentiveness to daily activities continued. The maintenance departments' daily planning meetings were conducive to keep management abreast of plant problems and to provide overall direction to proceed deliberately and cautiously during the special test sequences.
. ' ., . . 14 Management continued to insist on briefings, critiques and reviews of plant experiences. The overall direction by operations management appeared to have a calming effect on the results of pre-test activities rather than one of interference with progress. Noise control in the control room continued to be demonstrated. The results of the
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staff's review followup to shift inspector referrals and to those reactive items identified collectively by the TMI-1 Restart Staff as warranting appropriate NRC followup action are summarized below. 3.2.2 Thermocouple Operability During a control room inspection, the inspector determined that four of the fifty-two incore thermocouples were inoperable. Three of the four inoperable thermocouples were located in the same quadrant of the core. The inspector questioned the licensee if these inoperable thermocouples complied with Technical Specifications Table 3.5-2 which requires a minimum of two thermocouples per core quadrant to be operable. The licensee stated that the requirement was met because the backup incore readout , (BIRO) thermocouples has 16 thermocouples with 4 per
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quadrant and this was for the inadequate core cooling instrumentation referred to in the TS. The BIRO thermocouples are checked on a monthly basis in accordance with surveillance procedure 1302-21. As an independent check, the inspector requested a control room operator to obtain a reading for all 16 incore thermocouples. The inspector compared the reading to plant conditions and concluded that the BIRO system was functioning properly. 3.2.3 ICS procedure Adequacy On several occasions shift inspectors noted that operators would place the operating main feedwater pump in manual control (hand control) when starting additional ~ condensate booster pumps or placing a second feedwater pump in opera- tion. These provisions were not dictated in the controlling procedure Operating Procedure 1105-4, " Integrated Control System," dated February 25, 1985. The inspector reviewed this procedure to assuro the procedure was technically adequate and that the procedure could be used as written. The inspector determined the procedure properly addressed . _-_. - - .- ._ _ ._. __
- ~. ., , 15 the operations of the integrated control system (ICS); however, it was silent as to how the operators were currently operating the ICS. The licensee representative stated that taking manual control of the feedwater pump
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was performed so that starting of additional equipment would not cause a small feedwater transient with ICS still in a tuning stage. The inspector reviewed the strip charts of associated parameters and determined that the licensee's statement about the potential for transients was correct. The inspector concluded that although the licensee's approach was correct the procedure should reflect the actual specific steps on how to control the plant. The plant operations manager stated that, because the ICS had not been fully tuned, it was prudent to take manual control to avoid transient conditions. If the ICS could not be tuned so that starting additional equipment would not cause controller cycling, the procedure would be changed. The inspector found this approach acceptable. The inspectors noted at certain times that the licensee was experiencing minor control problems with the ICS in automatic. On one occasion the inspector noted that the licensee required additional operators on the control panels. In one instance the of plant operations manager
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required the additional operators to eat their meals in ' the control room to ensure they were readily available. The inspector noted that Administrative Procedure 1029, step 5.2.g.6 states that meals shall not be eaten at the control console area, however, this restriction does not apply to eating or drinking a single item. The inspector noted that there were extra operators at the console and that' eating did not interfere with operations nor was the eating-done directly over control panels. The inspector discussed the issue with the plant operations manager who stated that'he had given a one time - permission to do this and that eating food was not to interfere with operations. The on-shift NRC inspector independently verified this to be true. The inspector determined that licensee management did not, intentionally, circumvent station procedures as standard
, practice and considered this instance an isolated case.
The inspector concurred with the plant operations manager's concern and action oriented toward safe plant operations by keeping operators close to the panels under these unique conditions. The inspector had no further
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comments in this area.
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. _ . '.. '. . 16 3.2.4 Reactor Protection ~ System Breaker Replacement As noted in NRC Inspection Report 50-289/85-22, (Unresolved Item 289/85-22-05) the licensee shipped the failed breaker CB-10 and breaker CB-11 that indicated some wear to General Electric (GE) in Atlanta, Georgia, for further evaluation. After inspection of breaker CB-11, GE, with GPUN concurrence, replaced the operating mechanism of CB-11 using parts from a spare GPUN breaker. After rebuilding and testing breaker CB-21, it was returned'to the site. On October 16, 1985, the licensee reinstalled breaker CB-11 into the reactor protective system. Preventive Maintenance procedure E-36, "CRD TRIP Breaker Trip Test," was performed. In addition, once the breaker was in ' place, applicable sections of Surveillance Procedure 1303-4.1, " Reactor Protection System," were conducted. The inspector witnessed the installation of the breaker and subsequent testing. The inspector also performed a visual inspection of the breaker. This inspection did not
identify any damage from shipment or any evidence of
, internal misalignment. '
While witnessing SP 1303-4.11, the electrician performing the test inadvertently tripped the breaker by going to shunt-trip instead of undervoltage (UV) trip. Licensee representatives were following the procedure; however, it appeared that the electrician was not familiar with the procedure. This'was compounded by the fact that the licensee was using a page phone instead of a headset to maintain communications with'the control room where the . evolution was being controlled. Immediately the mainten-
. ance supervisor, present at the RPS breaker, recognized the i
situation and took control. He ordered that an I&C technician (individuals who normally perform the test) perform the test and communications be established with a headset at the breaker panel. In addition to witnessing the testing of the breaker, the inspector reviewed the receipt inspection package and job ticket CH-798. No discrepancies were noted. In a related matter, a shift NRC inspector noted that the spare RPS breakers were being stored in the turbine building switchgear room. The inspector brought this to
l the attention of the licensee who immediately placed the !
breakers in a more secure space. The licensee also stated . - , - - - - .- . . .- . . - . .
., ., ' 17 that before an RPS breaker is installed the applicable preventive maintenance procedure will be performed. This procedure requires a visual inspection. The inspector reviewed the licensee's applicable procedures and concluded that they were adequate to determine if the breaker had been physically damaged and that the required testing in place would determine if the breaker was electrically inoperable. Discussions with the licensee indicated that the long-term solution to the breaker storage problem would be resolved once the breakers were properly designated as spare parts and placed in the warehouse inventory. The inspector had no further comments. 3.2.5 Lift of MS-V22A/B During Emergency Feed Pump Operation On several occasions during the operation of emergency feedwater pump (EF-P-1) on main steam pressure, the feedwater pump turbine relief valves (MS-V22A/B) would lift. This was described in detail in NRC Inspection Report 50-289/85-22, (Unresolved Item 189/85-22-03). The licensee committed in a letter dated October 11, 1985, from H. Hukill, GPUN, to T. Murley, NRC, to develop and provide specific guidance to the operators. The licensee issued Operations Department Memo No.85-6, dated October 16, 1985, which addressed lifting of MS-V22A/B during EF-P-1 operation. The inspector reviewed the specific guidance given in the operations department memorandum and concluded that it correctly reflected the commitments in the licensee's letter. 3.2.6 Work in Safety-Related Areas During an inspection of safety-related building spaces on October 16, 1985, the inspector observed that a contractor employee was standing on the "Limitorque" operator for FW-V92A which was about 20 feet off the floor at the intermediate / turbine building interface area. The valve FW-92A is a block valve for the startup feedwater flow control valve; and, since the plant was operating at 40% power, this valve and the associated regulating valve were open supplying feedwater, in part, to the "A" steam generator. The individual was erecting scaffolding in the area. 1 l l
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.. '. . 18 , When the observation was brought to the attention of the operation manager, immediate action was initiated to assure that the individual no longer used any valve operators in that area for standing support in the construction of the scaffolding. Later observations by the inspector confirmed effective results. The inspector expressed concern that workers using valve bodies or operators for construction support work created the. potential for an adverse safety impact in that a transient could result due to inadvertent opening / closing or malfunctioning of an affected valve. The transient could result in.an unnecessary challenge to a safety system and the operators. Licensee management s acknowledged the inspector's concerns and agreed to review this matter with the responsible onsite departments. This area will continue to be routinely followed by the TMI-1 Restart Staff throughout power escalation testing and subsequent power operations. 3.2.7 Nuclear Service River Water ISI Survei11ance On October 17, 1985, the inspectors observed the performance of an inservice inspection (ISI) surveillance on the nuclear service' river water (NSRW) system. Surveillance Procedure (SP) 1300-3I A/8, Revision 23, dated August 20, 1985, was used by two auxiliary operators to perform this surveillance. The inspectors concluded that this ISI was performed in accordance with procedures and no adverse conditions were observed. 3.3 Conclusion No major equipment problems existed that adversely affect safe operation of the facility. Procedures were adequate to support operations and they were properly used and implemented. Licensee management, in general, demonstrated overall control, attentiveness, and s conservative approach to the safe operation of the facility and to the equipment problems. The secondary plant drain line problem presented an obstacle to continued startup testing. The observation of the worker on the valve operator coupled with the latest inspection report findings are indicative of a need for better control of personnel workin'g in safety-related areas. . . . .
.. _. _-. , * ' .. . I 19 4 4. Startup Tssting 4.1 Power Level Plateau Data Review Test results from the test program for the power plateaus of 15% and 25% were reviewed by the inspector to verify that:
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-- test changes were approved and implemented in accordance with administrative procedures;
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changes did not impact the basic objectives of the test;
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-- test deficiencies and exceptions were properly identified,
- resolved, and resolution accepted;
-- the cognizant engineering group had evaluated the test results and signified that testing demonstrated design conditions were met; and,
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~ test results compared with established acceptance criteria , or were properly resolved. The startup tests reviewed for this verification included: -- TP 800/5, " Unit Load Steady State Test," (15% and 25%);
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TP 836/1, "Feedwater System Operation and Tuning," (15%); -- TP 846/1, "Incore Thermocouple Functional Test at Power," (15%);
-- TP 849/1, "ICS Tuning," (15% and 25%); i -- SP 1303-11.19, " Turbine Overspeed Testing;" -- SP 1302-1.1, " Power Range Calibration;" and, -- OP 1105-14, " Loose Parts Vibration Monitoring Data." The details and findings of this review are described below. 4.2 Findings c 4. 2.1 - Unit Load Steady State Test Important plant parameters such as reactor coolant inlet and outlet temperatures, steam generator level, , temperature, outlet pressure, and feedwater flow and' temperature were measured at the 15% and 25% power
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. '.. .. 20 plateaus. The measured data at the 25% power level showed excellent agreement with the predicted values. However, at the 15% power level, some deviations were noted. The licensee and its NSSS vendor (B&W) are evaluating these data. The steady state 15% power level data will be collected again when the unit returns to this power level after the completion of TP 800/8, "RCS Overcooling Test." 4.2.2 Feedwater System Operation and Tuning
r' The feedwater heater drain system was checked at the 15%
power level. No unacceptable conditions were identified. During this test, level indication in the sixth stage ~ drain collecting tank (LI-74) was found out of the acceptable range. This problem was subsequently corrected. Test procedure TP 836/1, step 9.3 calls for checking system response at-the 25% power level when two heater drain pumps are running. Due to the fact that only one heater drain pump was running during the test period, this part of the test was postponed until after the return to 48%'of rated power. 4.2.3 Incore Thermocouple (T/C) Functional Test The incore T/Cs were checked at the 15% power level; 4 out of 52 T/Cs were out of service during this test. The inspector noted the following results: -- The readings from symmetrical T/Cs agreed within +/- 1% of the symmetrical group average readings or corresponding paired T/C reading. --- T/C readings agreed within +/- 2% of the cal- culated values based on expected temperature distribution in the core. -- At 15% power level, the T/C readings were very close to each other. The five highest incore T/C readings ~as selected by the program "TCDSPL" did not necessarily agree with the five highest T/C readings from the Mod Comp computer which were taken at a slightly different time. The licensee designated this as a test deficiency. This matter will be tracked further at a higher power level -by the licensee and TMI-1 Restart Staff.
. -- . - . .-. . - -
_. . ._- - _ * . .. . 21 -- The plant computer uses the program "TCDSPL" to select the five highest incore T/C readings and
. calculate the saturation margin. The accuracy of
this calculation was verified by hand calculation in accordance with the procedure. The result < indicated that the "TCDSPL" program accurately calculated the saturation margin with a 1.3 degrees F deviation from the hand calculation. -- The backup incore readout (BIRO) thermocouple display and the value displayed on the operator's group was onsistent and agreed within the , established acceptance criterion of +/- 16
4
degrees F. ! 4.2.4 Loose Parts Monitor System Test During power escalation testing, the licensee is taking base line data for-the loose parts monitor system (LPMS) at each power level plateau identified on the testing sequence. Operating Procedure (0P) 1150-14, " Loose Parts Monitor System," is being used to operate the system and tape record base line noise levels. The tapes are being
'
sent to B&W for analysis. During the reactor trip at 40% power, base line data will be taken both before and after the trip. - The inspector reviewed OP 1105-14 and noted that it was classified as "not important to safety." This -clarification was confirmed with the licensee's QA representatives. OP 1105-14, paragraph 3.2.a, requires that the LPMS cabinet be inspected once per shift when the reactor coolant pumps are running and that alarm lights be reported. Paragraph 3.2.c requires that each of the LPMS channels be monitored for noise once per shift in the control room or at LpMS cabinet. Neither was being performed. Discussions with an operations engineer indicated that
, failure to check for noise levels was an oversight. The
control room shift and daily logs (non-technical specification required) was immediately revised to check
,
for LPMS noise on the speaker located in the control room.
J I
- _ _ ,, _ _ . , -_ . _ _ . _ _ , , . . _ _ . .
._. . - . - _ . . . _. . '.. '. . 22
The operations engineer stated further that the LPMS now has a common alarm in the control room which had not existed previously. If this alarm is received, the local '
<
alarm panel can be checked. Since this alarm is monitored continuously, the intent of OP 1105-14 LPMS alarm monitoring had been met. He stated that no change to OP ' 1105-14 was required at this time but a change would be considered during procedure OP 1105-14 biennial review. The inspector concurred with the licensee resolution and had no further questions at. this time. 4.2.5 Main Turbine Overspeed Test
I Test C of SP 1303-11.19 specifies that the turbine generator
overspeed trip setting should be between 1980-1998. The actual trip occurred at 1960 RPM. This value was accepted as satisfactory since the procedure states that if the trip setting is below 1980 the turbine can be returned to service. However, the turbine will likely trip on overspeed if full
l load is lost. Trips above the 1998 setting are unacceptable
and must be repaired prior to putting the turbine back on line. All other data in the procedure was satisfactory. This test met TS 4.1.1 and Table 4.1-1 requirements. -4.3 Reactor Coolant System Leak Rate Surveillance
.
The inspector reviewed the reactor coolant system (RCS) leak rate
4
surveillance (SP-1303-1.1) results from October 1-15, 1985. The results indicated that during this period, the RCS leakage was well within the TS limits. The unidentified leak rate as calculated by the licensee was independently analyzed by the inspector (Figure 1). The sampling
data indicated that the average unidentified leak rate was (-)0.21 gpm with a standard deviation of 0.11 gpm. A relatively large variation occurred from October 5-14, 1985. This was expected due to operating conditions and required power maneuvering during this period. The calculated leak rate is highly affected by the Tave
- value, and Tave is very sensitive to power changes when the power
level is below 15%. The inspector also performed an independent calculation using an NRC-developed leak rate computer program (RCSLK 9) for the leak rate determination on 1835-2035 October 15, 1985. The comparison results are shown below:
) i I i 4
- - . . _ - - - - _-__ ' - - ... ~ ...~.~ . . ... . .- 1.0_Ts Limit $ $ 21."-}." 7....~4A7 .n ,. . q . ,.-m - f _p . - f-- .,. p q - ._ ,.__- .. - -- . ._ - ._-,_ - --. _ . . - - .-. -.-.. . _._ .. .._,_. . _-.---- __._..,,- - --- - . - .- ..-- .- - _ , .e- .4.. , _. 1 . j . , u .- % , . . _ .._ _.__. -_ . - -.-..- - ....- -._. . - - _ . . ._- ..__-._ - -.- . _ - { pl }. L 1., _ -.. _-._- . .p __..- . -__-__-_. ...._.-.. . - .. -m- __._ - . . - - - ._-___ j}. . - - ..___ _ _ - . . -- . . . ..- .- - } .-_ _.-.. _ ._ __- m -..-.- . -_ .._- . _ .,_-._ .-..- _ _ . ._._. _ . _ . .. ... . . - _- y7 . , , - . .. -_ . . . 7 7 .-4- -4.{. . -.- - -.._ --.-_-.. -..- - . ._ ... .- . . .. , . .._.- . . - . ,_- .._._ -_.- , l , 7 ,,. , 41 7 --
,
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,'
- . , - - .+ 7- .- 7, g t - t -f +7 p - 7+7 -- - - ,, , + 7i t -- f- t- - " 7" - --- ---" ' ' - - - - -- - '--- --- ---- -- * . . ; . ' r.I nit.la.1C l,tica3 , .- .--j- , y f. t'y.-.; -_-_ . . .. . . . j .__ - ._-._____- - - _--._ - - .._ . ._ _ g . - . .; - - p ..]--- -- -- --_ _ - . - -- _ _ -_-__.. ._._-. a. . .+, J ;, Er -.y-Aig ., . i - . . ., ,,. t " r - - . - - - - - - - - - ---- - .e., . s flot- Shutdo+wnZero* Power ~ Naturalt t - t5 -15%~RTP" - -5 -- 2 B%b28-hRTPERT'R 1 - -g- - ' - -- "--- - - ._. ..__ ' ....,qy4 Thysics Test - Circulation- E -- -- -- -t - -- -- -- --- - - - - - - -- - c , . ..,. ,.-. rey 1. . r e-- t. ,t '-4 - -- - --- - -".------ - "-- p C@- - - - - - - - - - - - . +4 p L. . p.- - + i ~y 'l t y 'r .-- _.-'- p e -.-.--.-- .. . .., . -; L- 7 , i p f 1- 7-} J h.7 _ . pF- J. --. --- - ~.--- --- --p - . -- --- ---. --- - -. --.- --- --- - -- - - .- - - _- . - - .- - -- - q_ . - - --_ _ _.- -p_p-. . . _ - x4 -y 4 .p --f-. .p 4. j-.-- ----- n 7 , . . j t,-y- -- - -- --- - j -4 . . {- - .--- - - - - -, ....-,..-p. y - -e -- -.- . , - - -- -- - - -. --- - -- - .- -- '---- -' --' "- . . , , 7. . q q- , . . . . . t, , ; t- e + Ut, *- 6 +t *t 1 -b - - - - d - t~r - -'- - - - - - ' - - - ~r ' ------ - - a o . , ...; .1+yp . f . ', . f' ? 1 i ,T t -. 3;7- -.7 -.r f t-~-t '-r -- r - - - - -- - -t + t--- ---~ -- --- ~ --'-- - - - - --- ' - " - -- - - - - -- - - --} - -t- --.- ' ------ - * - ' - --"4- m m . . . - 93.4y 7-. 7- . *,}" t, * - t } * t -- - -- - - ------ - . - -- -- '. -- - ---- bt - "- - -"- -h a c .. e 9 . 7+4 .t . - { ---' a t - - -- - - - -. . - _ 7-. - --- -.-- - o .a . .eij 4 -. , . r .. - .4F .a - ,, , , i,f, t ?-r t} tf g t } - t t k-" - - - q'7~ -. - ---"- 4 _.- - -- - -- ~~ ~ ~"- T-b" --- '}' * ~ r ~T ~"T"--"-~ - -. - _. - . ._- - '-"- - } u.2 .y ' - .,4 u . . - , .-j. ? . . p . .. . e 4 p. 37,-.-H. .,. ' ] h ff -hI - - -- y- - -f---- ~-------- ----- M- - - -- - - -- -f - -rf -- - } .- - --h A-- *. 7-]- T - - - - - -- 7- - - * - - - - ., T ~ - . ....._.r.+ , . c ~ p.......1- . , - . y 'k- - , }-.- t . p- J, r+[- .. .c c . . - . . . - . m..e .r,-, . 4 .; 7 }- *, 4 . - . , , . . *3 . _ _ * .e H . .. t rr- - _ ---- _- --- ---- - _ _ - -_-~*- --- - .l _-_ .. a- 1 _. 4,.-g t . . . -.' it*p i ,i - h
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-
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-
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i
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. . . , H, , H- +-+ ,I', ' t. .4, . t4 b 2 9 N, - - . m. ,+tH - . .. . - - .. .E . 3-,... , . . . . , . . .. . . 4 A p,i!. .H. iqi+t..-+.,r- . r. 4 - t y. +-.-H+" + F T ' - C -,t H 11 e A - t- . 4F- F F d +t-- - -t- 1 +*- tH1vE+, i A- +-t ph, t- N --t* t4 e -4-- + r 4- ++ . . . . . . .. -!. ,.7.-,t f j - s- .L4 . . - 4 - - t -t-t-- -"- - - ' I < -- + - -t -+- t't 1." *E .I 4-+ - r- t 4 . . E{ I h l- t f-.- 4 4 y- -' .-t+dfo - d- r-- F gI4t- stand ard.' b'ev2ation L 1 - .1 - -- --- - - - - t , . . -.4 . . .~ + f t- "-t- -'- F- h- ~ I - : . . . ' . .- . t L-.t i i i t t - r!4 - F btt 'j tt 4 k - - - - t --* I-r+ - @ ---+ 3 - .. . ... . . , . . . . . . -. .. ., .3i ,H.1. ..t 3 ,, pp +p, ._,L -te .- 4 7.+ typn . -r~b T- P'~ -di* '- *- - m7T r ir t '-t p--t+ ' . . - . . - _4_-.,...-..........- . . - - . - ~ . _ . . -. 7 7 9, 7,_p .. . ,, , * He t . itrr+ r - tWh3-b- r A tv T~b ' -- ' -+F---{-Fi - - F+ r m'-[ -b'-m*11.I b' M-I4te 1 i 0.1 FIGURE 1
_ __ _ ., __ . _ * .. .. 23
i i
Leak Rate (gpm) Licensee Calculation Inspector Calculation Leakage Plus Losses
'
0.0772 0.07
1
Unidentified Leak Rate -0.2217 -0.06
'
The results from the inspector's calculation agreed closely with the licensee's calculation for the leakage plus losses term. The difference in the unidentified leak rate calculation is due to a correction factor of 0.1644 gpm being included in the licensee's calculation. The applicability of this correction factor is being reviewed by NRR. 4.4 Primary to Secondary Leak Rate Monitoring l The licensee monitors the primary to secondary leakage per surveillance procedure 1301-1, " Shift and Daily Checks," Revision 58. The inspector reviewed the surveillance results from October ; 9-15, 1985. The calculated results indicated that the leak rate was ' ' about 0.2 gph, which is consistent with a previous krypton leak test result. No indication of once through steam generator (OTSG) tube
- degradation was noticed from these data reviews.
! 4.5 Conclusion ! I
Testing for the 15% and 25% power plateaus was accomplished in accordance with procedures, data were acceptable, and test objectives were met. Licensee management was responsive to inspector observations. Problem areas were quickly corrected and actions were taken to preclude their recurrence. Overall licensee
"
l performance in the test area can be considered acceptable and, to
1
date, test results are acceptable. 5. Decay Heat Removal System Procedure Review
] 5.1 Review
,
! The inspector reviewed operating procedure 1104-4, " Decay Heat i Removal System," Revision 54, dated September 5, 1985, to ascertain i
whether it is in accordance with regulatory requirements and whether
t
its technical adequacy is consistent with desired actions and modes of operation. As part of this review, the inspector also examined
, the following documents. 1 i
. - - .- - - __ . . - . '.. - . . 24 -- GAI drawing C-302-640, Revision 37, " Decay Heat Removal;" -- TMI-1 Operations Plant Manual, Section B-6, Revision 1, " Decay Heat Removal System;" and,
- --
ANSI N18.7-1976, " Administrative Controls and Quality Assurance for the Operational Phase of Nuclear Power Plants."
f
In addition to the above, the inspector toured both decay heat vaults. The valve lineup verification was completed during the week of September 30, 1985, just prior to restart. l 5.2 Findings i The inspector determined that the procedure's stepwise instructions . were compatible with checklist information, and provisions for
! signoffs were evident. Appropriate limitations, such as pressure /
l temperature limits, cooldown ratios, and net positive suction head requirements were correctly incorporated into the procedure. Various precautions and notes concerning equipment and
) administrative operability requirements, and appropriate technical
specification requirements were also incorporated into the
i procedure. The startup valve checklist and the P&ID (Piping and j Instrument Diagram) were compatible and agreed with each other. I
During the tour of the "A" & "B" decay heat vaults, the inspector found them to be clean and neat. There was very little extraneous material in the "B" decay heat vault; the "A" decay heat vault was being painted at the time of the tour. Painting equipment that was
left in the "A" decay heat vault during non painting hours was kept . to a minimum, was neatly stored in a' safe corner of the vault and
] did not pose a fire or safety hazard.
The inspector found an out-of-date calibration sticker on pressure transmitter DH7-PT1. The inspector found that the instrument was actually calibrated on August 13, 1982; this instrument is to be ! calibrated every six years. This item was noted to the licensee and the inspector had no further questions. '
'
Before exiting the auxiliary building, the inspector decided to watch the painting crew enter the "A" decay heat vault. Upon rounding a corner of the building wall, the inspector saw a painter ' straddling an RWP boundary. The inspector was unable to determine if the worker was entering the RWP area or if he had previously entered the area and had half exited it to retrieve painting
i equipment. The inspector brought this situation to the attention of
the group radiological controls (Radcon) supervisor.
1 i 1
- <, m. , , .-,m-. m.,- - - . - - . . ,c , . - _ . - ,-._.,.,,,,,m.-.
* * . . 25 The radcon department's review of this matter revealed that the individual was entering the contaminated area. The radcon department was responsive to the inspector's concern on proper contamination control and he had no further comments on this matter. 5.3 Conclusion
s The inspector determined that procedure 1104-4 is adequate to
control safety-related operations within applicable regulatory requirements. If called upon, this procedure can be used for operations to remove decay heat from the core after the plant is shutdown. No adverse conditions were found that would affect plant safety. 6. Licensed Operator Requalification/ Restart Training 6.1 Restart Hearing Issues The licensed operator requalification training program was reviewed to ascertain its conformance to the restart requirements contained in H. Denton's letter to H. Hukill, dated October 2, 1985, and items identified by the Atomic Safety Licensing Board. 6.1.1 Restart Condition 5.a requires that in October of each year the licensee report on the progress towards installation of a TMI-1 exact replica simulator. The licensee letter dated October 3, 1985, from H. Hukill, GPUN, to J. Stolz, NRR provides that report for 1985. The present schedule is for delivery of the simulator on site in June 1986, and training on the simulator to begin in August 1986. The inspector concluded that the licensee complies with Restart Condition 5.a. 6.1.2 Restart Condition 5.b required that until the exact replica simulator is in use the licensee was to provide at least one week of basic principles trainer (BPT) time for licensed operators. The training department has integrated the BPT into the requalification program. Each requalification cycle, which is normally a five day training period, includes at least one 6-hour training session on the BPT. Presently the 1985 requalification program, which contains five cycles, has 38 hours of . training on the BPT spread over eight days. The training department is planning on incorporating an additional nine hours of BPT.use into the present requalification program.
. - - . - - .- . - . - . - _-.. .- .. '..
! 26 i ! i In addition *.o BPT training, one week of training at the
B&W simulator in Lynchburg, Virginia, was provided to each
i
licensed operator. The inspector concluded that the
! licensee complies with restart condition 5.b. . 6.1.3 The certification files of three licensed instructors were < 2
inspected. Each file contained the instructor's certification and completed performance evaluation forms. Each instructor has been evaluated at least eight times in the past year by at least five different evaluators. A t review of the evaluation schedule showed all instructors ! had been evaluated with the periodicity and at the levels
4
required by the Instructor Evaluation Procedure '
6200-ADM-2607.01. The licensee's instructor evaluation program is in place and being properly implemented. The inspector concluded that the licensee complies with their commitments made as a result of the restart hearing.
- 6.1.4 The inspector reviewed ten sets of weekly quizzes, which
had been administered during the 1985 requalification
- , program. Licensee instructors had evaluated all sets of
weekly quizzes for collusion between at least half of the
'
. operators taking the quiz for at least 25'4 of the questions, as required by the licensee's collusion check program. No
- instances of collusion were found by the instructors. The
j inspector determined that the licensee's collusion check j program is in place and being properly implemented. The i inspector concluded that the licensee complies with their , commitments made as a result of the restart hearing.
; 6.1.5 As a result of the reopened hearing on the training
! program and in reference to the ASLB Partial Initial j Decision (PIO) dated May 3, 1985, the licensee has '
developed a procedure, " Trainee Evaluation - Once Back - On-the-Job", 6200-ADM-2682.10, which became effective
! September 13, 1985. However, this procedure is not
expected to be implemented-for licensed operators until
}'
mid 1986. The proper evaluation of trainees to meet ASLB hearing requirements is unresolved pending completion of licensee action and subsequent NRC Region I review :
l i
(50-289/85-24-01).
! 6.2 Requalification Program Review
In addition to the review of the above elements in the requalification program, the inspector reviewed the development
1
process for determining which items were to be included in the 1985
j requalification program. The inspector assured compliance with 10 i l
i
l
! '
. . _ . . - -- . - - - - . . . - , - - - - , . - - - - , , . - . - . , - ,.. . -. - . -..- , . - ,- ,.. -
. . 27 CFR 55, Appendix A. The training department used a formalized system of evaluating training requests from licensed operators and evaluating weaknesses identified by the annual examination. These evaluations were then used to assist in the selected of the requalification program topics. The content of the weekly quizzes and annual requalification examinations was reviewed. 6.3 Requalification Program Finding The questions were well constructed and minimal use was made of true-false, multiple choice questions. A review of the attendance records found that some licensed operators who were not assigned to an operating shift had not attended all requalification lectures. One operator had been specifically exempted by letter and the other operators had not exceeded the allowed limit for missed lectures. All licensed operators had completed the weekly quizzes. A review of the grades on the annual requalification examination showed grades ranging from 75*4 to 95's and averaging about 85%. Three operators failed the examination with overall grades less than 70%. On the retake examination, two of the operators passed with overall grades between 80*4 and 85%, and one operator failed. The operator who failed the retake examination has been removed permanently from licensed duties. The grades on the requalification examination, the grades on the retake examination, and the handling of examination failures is indicative of an effective training program that uses examinations to differentiate between operators who have retained the requalification training and those who have not. 6.4 Conclusion The requalification program is well organized and documented. It conforms to applicable regulations and restart requirements. 7. Gaseous Radioactive Release Assessment The licensee's program for quantifying and controlling gaseous radioactive releases incident to the startup of Unit I was reviewed against the criteria specified in Technical Specification 3.22.2, " Gaseous Effluents," 10 CFR 50, Appendix I, and 10 CFR 20.106, " Radioactivity in Effluents to Unrestricted Areas."
. _ - . . - - . * ..
28 Currently, primary to secondary leakage is occurring at the rate of approximately 0.2 gallons per hour, which results in detectable activity in the main steam system. The measured concentration in the main steam system is ~5.0 E-8 uCi/cc, primarily Xe-135. However, non-condensible gases are concentrated in the condenser and discharged to the environment via the condenser offgas system. The condenser offgas is continuously monitored and recorded by radiation monitor RMA-5. Nominal values for RMA-5 are about 60 counts per minute (cpm) but at the end of the period, the monitor indicated 100 to 150 cpm. Daily grab samples from RMA-5 indicate that the highest activity measured since restart of TMI-I was 5.77 E-7 uC1/cc, Xe-133 and 5.46 E-7 uCi/cc, Xe-135. The 10 CFR 20, Appendix B, Table II, unrestricted limits of 3.0 E-7 uC1/ce, Xe-133 and 1.0 E-7 uCi/cc, Xe-135 are concentration values which may be averaged over a one year period and provide the basis for the applicable Technical Specification 3.22.2.2(b) dose limits. . The Technical Specifications limit the air dose due to noble gases ! released in gaseous effluents during any calendar year to < 10 mrad for gamma radiation and < 20 mrad for beta radiation. Applying the
1 calculation methodology described in the ifcensee's NRC-approved Offsite
- Dose Calculation Manual (ODCM). The following table depicts activity
released via this pathway between October 8 and October 16, 1985.
I
Fraction of Yearly Limit , Total Cumulative Air Dose Technical Specification
l Activity Released at the Site Boundary 3.22.2.2(b) ,
3279 uC1, Xe-133 2.2 E-5 mrad, gamma 0.00022 % of the gamma air dose limit 5624 uC1, Xe-135 3.2.E-5 mrad, beta 0.00016 % of.the beta air dose limit This analysis indicates that the resulting exposure due to these releases to the environment is negligible with respect to regulatory limits.
,
During this inspection the licensee's methods and assumptions used to postulate dose due to the releases to the environment _from the actuation of atmospheric and safety relief valves associated with the main steam system were reviewed. The licensee's " worst case" analysis assumed all
4
valves relieving continuously, i.e., MS-V4 A/B, MS-V21 A/B and MS-V17-20 A/8/C/D, for the duration of a year; and was based on the highest measured concentration at RMA-5, 5.77 E-7 uCi/cc, Xe-133 and 5.46 E-7 uCi/cc, Xe-135. Application of the 00CM indicated the results shown in the table below.
, I J
_ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _
- . - . - . -_ .-. . _ . __- - - . . , , 29
-
Fraction of Yearly Limit
- Technical Specification
l Cumulative Air Dose 3.22.2.2(b)
3.6 E-8 mrad /sec, gamma (3.25 E7 sec/yr) = 11% of gar.na air dose limit
,
1.13 mrad /yr ' 5.7 E-8 mrad /sec, beta (3.15 E7 sec/yr) = 9% of beta air dose limit . 1.8 mrad /yr l , This analysis indicates that any steam relief with the current secondary
^
side source term would result in negligible exposure with respect to regulatory limits. The licensee's calculational techniques and conclusions were
4
independently verified by the inspector, indicating that the assessment methods and assumptions were valid for the control and assessment of gaseous effluents via this pathway.
l-
8. Licensee Action on Previous Inspection Findings
,
8.1 (Closed) Unresolved Item (289/85-22-03): Licensee to issue interim guidance for inadvertent safety valve lift on initiation of turbine
j driven emergency feedwater pump. See Detail paragraph 3.2.4.
8.2 (0 pen) Unresolved Item (289/85-22-05): Licensee to replace unfurbished reactor protection system ac breaker. Licensee
2
evaluation of vendor information remains open. See Details
paragraph 3.2.3. 9. Exit Interview
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The inspectors discussed the inspection scope and findings with licensee management at the exit interview conducted on October 18, 1985. The
- 'following licensee personnel attended the final exit meeting
. ! J. Colitz, Plant Engineer Director ! J. Donnachte Jr., Radiological Engineer
C. Incorvati, Audit Supervisor L. Pitter, Operations Administrative Assistant R. Maag, Licensed Operator Training Supervisor
4 W. Nickel, Superintendent (Catalytic, Inc.)
L. Robinson, Communications Representative
i J. Ross, Manager Plant Operations
D. Shovlin, Manager Plant Maintenance
, C. Smyth, TMI-1 Licensing Manager ,
R. Toole, Operations and Mainte.iance Director G. Troffer, TMI Maintenance and Construction Director (Acting)
'
D. Tuttle, Radiological Contrcls Field Manager S. Williams, Radiological Engineer
i e 4
- _ _ _ m.___ . _ _ _ . _ _ _ _ _ _ _ _ _ _ _ _ _ . _ _ _ _ _ _ _ _ _ . _ _ _ _ _ _ _ . _ _ . _ _ . _ _ _ _ _ _ . _ _ _ _ _ . _ _ . _ _ . _ _ . _ _ _ _ _ _ _ - _ _ _ _ . _ . _ _ _ - . _ _ _ . _ _ _ _ _ . _ _ _ . _ _ . . _ _ - _ _ _ _ _ _ _ _ _ _ . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ . . . _ _ _ _ . _ _ _ _ . . _ _
. *
.. '30 The exit meeting was also attended by S. Maingi, a nuclear engineer I representing the Commonwealth of Pennsylvania. As discussed at the meeting, the inspection results are summarized in the cover page of the inspection report. Licensee representatives indicated that none of the subjects discussed contained proprietary information. Unresolved items are matters about which information is required in order to ascertain whether they are acceptable items, violations or deviations. Unresolved item (s), discussed during the exit meeting, are documented in paragraphs 6.1.5 and 8. . I
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