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Category:NOTICE OF VIOLATION OF A REGULATION
MONTHYEARML20207F1521999-05-25025 May 1999 Notice of Violation from Investigation Rept 1-94-021 on 940506-960329.Violation Noted:Between 740831-910407,licensee Made Changes to Facility Described in Safety Analysis Rept for Refueling Core Offloads Without Performing Evaluation ML20205M7201999-04-0606 April 1999 Notice of Violation from NRC OI Case 1-96-002 & Conclusions of Millstone Independent Review Team.Violation Noted. E Debarba,Deliberately Discriminated Against Supervisor in Performance Engineering Group at Millstone Station ML20205M7351999-04-0606 April 1999 Notice of Violation from Investigation in Case Numbers 1-96-002 & 1-97-007.Violation Noted:Licensee Discriminated Against Supervisor in Performance Engineering Group at Plant Due to Involvement in Protected Activities ML20207M1131999-03-0909 March 1999 Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $88,000.Violation Noted:Employment of Two Contractor Employees Terminated in Aug 1997,in Part Because Individuals Raised Concerns Re MOV Program Manual ML20199C6381999-01-0707 January 1999 Notice of Violation from Insp on 981006-1123.Violation Noted:On or Before 981120,conduit 9-15,in Fire Area A-24,not Sealed & Tested in Accordance with Astme E-119,fire Endurance Test ML20195H6901998-11-18018 November 1998 Notice of Violation from Insp on 980818-1005.Violation Noted:Engineering Evaluations Not Performed When RCS Heatup Rate Limit Exceeded on 951217 & When RCS Cooldown Rate Limit Exceeded on Three occasions,940424,0728 & 951215 ML20155B1521998-10-23023 October 1998 Notice of Violation from Insp on 980810-0903.Violation Noted:Design Basis,As Described in FSAR Chapter 14,Accident Analyses Had Not Been Correctly Translated Into Plant Procedures & Acceptance Criteria ML20154D1151998-09-11011 September 1998 Notice of Violation from Insp on 980413-24-0511-15,27-29, 0609-11 & 23-25.Violation Noted:Program Implemented TS 6.8.4.a,failed to Include Provisions to Reduce Leakage from RSS Heat Exchangers to SW Sys ML20237B0741998-08-12012 August 1998 Notice of Violation from Insp on 980428-0629.Violation Noted:Licensee Failed to Direct Test Personnel to Close & Lock RHR Outboard Drain Valve ML20237D3041998-08-12012 August 1998 Notice of Violation from Insp on 980413-0508.Violations Noted:Two Examples Identified Where Licensee Not Performing Leakage Testing of safety-related Valves in Sys That Could Contain Highly Radioactive Fluids During Accident ML20249C6931998-06-19019 June 1998 Notice of Violations from Combined Insp on 980301-0427. Violations Noted:Prior to 980424,instrument Min Accuracy of Wind Speed Channels Were Not Measured as Required by Table 3.3-8 of Unit 2 TS 3/4.3.3.4 ML20249B0421998-06-12012 June 1998 Notice of Violations from Insp on 980413-24.Violations Noted:Only 1 RCS Loop Operable W/Plant in Mode 4 on 980407 ML20236L5381998-06-11011 June 1998 Notice of Violation from Insp on 980302-0409.Violation noted:post-mod Test Procedure Did Not Incorporate Requirements Contained in Design Documents ML20249B0811998-06-11011 June 1998 Notice of Violation from Insp on 980209-20.Violation Noted: Between 1992 & 1993,appropriate C/A Not Taken to Prevent Recurring Air Binding Problems for Boric Acid Transfer Pumps ML20249B2171998-05-26026 May 1998 Revised Notice of Violation from Insp on 980101-0228. Violations Noted:As of 980210,21 nonsafety-related SOVs in High Pressure & Low Pressure Safety Injection Sys & Four nonsafety-related SOV in RCS Not Included in EQ Program ML20248E5951998-05-26026 May 1998 Notice of Violation from Insp on 980101-0228.Violation Noted:On 980225,NRC Determined That Written Equipment Control Procedures Were Not Established to Process Revs to Sys Valve Lineups ML20248A7781998-05-22022 May 1998 Notice of Violation from Insp on 980302-31 & 980412. Violation Noted:Structural Steel Support Members Did Not Meet 3-h Fire Barrier Criterion,In That on & Before 980304, Columns D2-54,D2-53 & A4-52 Had Gaps in Fire Rated Coating ML20248F3061998-05-0808 May 1998 Notice of Violation from Insp on 980223-0306.Violation Noted:Listed Examples Were Identified Where Requirements of 10CFR50 App B,Criterion Xvi, Corrective Action, Were Not Met ML20247D8561998-05-0606 May 1998 Notice of Violation from Insp on 980223-26.Violation Noted: Between 1988 & 980226,licensee Failed to Maintain Adequate PASS Program That Ensured Capability to Obtain & Analyze Samples Under Post Accident Conditions ML20217M9091998-04-0808 April 1998 Notice of Violation from Insp on 980209-27.Violation Noted:As of 980227,measures Were Not Established to Assure That Design Basis of safety-related MOVs Was Correctly Translated Into Specifications,Drawings & Instructions ML20216F9841998-04-0303 April 1998 Notice of Violation from Insp on 980105-0206.Violation Noted:Certain Measures for Verifying Adequacy of Plant Design Inadequate ML20216G0921998-04-0101 April 1998 Notice of Violation from Insp on 971027-980128.Violation Noted:Licensee Failed to Perform & Include in Written Records,Safety Evaluations for Approx 250 Changes to FSAR Made Between mid-1996 & mid-1997 ML20196J5911998-03-0909 March 1998 Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $55,000.Violation Noted:As of Sept 1997, Condition Adverse to Quality Existed at Facility Which Had Not Been Promptly Identified & Corrected ML20203H0981998-02-25025 February 1998 Notice of Violation from Insp on 971201-31.Violation Noted: on 971222,equipment Located in safety-related Area,Unit 2 Control Room,Not Restrained in Accordance W/Attachment 3 in Procedure Oa 8 ML20198F0501997-12-30030 December 1997 Notice of Violation from Insp on 970825-29.Violation Noted: as of 970829,adequate Dose Assessment Methods Were Not in Use.Page 23 of Incoming Submittal Was Not Included ML20202J7221997-12-10010 December 1997 Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $2,100,000.Violation Noted:Licensee Did Not Translate Design Features Into Work Instructions & Did Not Verify Adequacy of Designs ML20202J7891997-12-0505 December 1997 Notice of Violation from Insp on 970818-29 & 0908-19. Violations Noted:During NRC Insp That Ended 970919,listed Instances Were Identified Where Requirements of TS 6.8.1a Were Not Met ML20202A7491997-11-21021 November 1997 Notice of Violation Form Insp on 970722-1001.Violation Noted:On 971215 Activities Affecting Quality Were Not Prescribed by Documented Instructions,Procedures or Drawings ML20216C7471997-08-29029 August 1997 Notice of Violation from Insp on 970529-0721.Violation Noted:On Several Occasions in May & June 1997,overcoat Window Was Exceeded by 45 Minutes to 2 Hours & 41 Minutes ML20210S8701997-08-29029 August 1997 Notice of Violation from Insp on 970520-0721.Violations Noted:Overcoat Window Was Exceeded by 45 Minutes to 2 H & 45 Minutes ML20141E3101997-06-24024 June 1997 Notice of Violation from Insp on 970311-0519.Violation Noted:Since Commencement of Operations at Unit 1,applicable Regulatory Requirements & Design Basis Not Correctly Translated Into Drawings & Procedures ML20140F1121997-06-11011 June 1997 Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $55,000.Violation Noted:Licensee Identified Seven Incidents Where Items Containing Safeguards Info Had Not Been Under Control of an Authorized Individual ML20140C5551997-04-11011 April 1997 Notice of Violations from Insp on 970101-0310.Violations Noted:Since Commencement of Operations,Unit 1 Failed to Determine Concentration of Nuclides in Gaseous Effluents Released from Radwaste Storage Bldg Through Exhaust Fan ML20137F3921997-03-24024 March 1997 Notice of Violation from Insp on 961222-970208.Violations Noted:When Repeatedly Depressurizing Unit 2 RHR Sys from 970123-30,operators Did Not Properly Implement Procedures as Required ML20135E6111997-02-24024 February 1997 Notice of Violation from Insp on 961026-1231.Violation Noted:Individual Gained Access to PA W/O Having Authorized or Hand Geometry Confirmed ML20134G3911997-02-0303 February 1997 Notice of Violation from Insp on 961112-22.Violation Noted: Licensee Failed to Establish & Implement Procedure to Verify That Design Basis Relative to Ventilation Air Supply Involving Radwaste Was Maintained as Described by UFSAR IR 07100128/20120021997-01-0606 January 1997 Notice of Violation from Insp on 771128-1202.Violation Noted:Licensee Did Not Test Addl 10 Snubbers for Each Found Inoperable Per Procedure 2733B,hydraulic Snubber Functional Test,Rev 0,770601 ML20135C9951996-12-0303 December 1996 Notice of Violation from Insp on 960827-1025.Violation Noted:All Valves Classified as Containment Isolation Boundaries Did Not Receive Monthly Verification to Insure They Are in Closed Position ML20128M1941996-10-0909 October 1996 Notice of Violation from Insp on 960506-10.Violation Noted; Licensee Failed to Control SGI as Required on 951105 ML20149K7331994-07-13013 July 1994 Notice of Violation & Proposed Imposition of Civil Penalties in Amount of $220,000.Violation Noted:Licensee Failed to Take Action to Address Condition Until 891117,when FWCI Was Inoperable IA-97-223, Notice of Violation & Proposed Imposition of Civil Penalties in Amount of $220,000.Violation Noted:Licensee Failed to Take Action to Address Condition Until 891117,when FWCI Was Inoperable1994-07-13013 July 1994 Notice of Violation & Proposed Imposition of Civil Penalties in Amount of $220,000.Violation Noted:Licensee Failed to Take Action to Address Condition Until 891117,when FWCI Was Inoperable ML20059G0631993-12-23023 December 1993 Notice of Violation from Insp on Stated Date.Violation Noted:Written Licensee Procedures Were Not Established or Implemented Re Testing for Drugs ML20058D3371993-11-22022 November 1993 Notice of Violation from Insp on 930818-0928.Violation Noted:Seismic Brace in Count Rate Module of Radiation Monitor RM-8156 Not Reinstalled During Instrument Calibr ML20058Q0601993-10-15015 October 1993 Notice of Violation from Insp on 920512-14.Violation Noted. Licensee Determined That Records Required to Be Maintained by Commission Regulations or License Conditions Not Complete & Accurate in All Matl Respects ML20057E2971993-09-20020 September 1993 Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $50,000.Noncompliance Noted:During 1991-1992 LORT Program,Facility Failed to Ensure Personnel Licensed Per 10CFR55 Had Completed Requalification Program ML20056H2491993-09-0101 September 1993 Notice of Violation from Insp on 930719-23.Violation Noted: Measures to Assure Conditions Adverse to Quality Not Taken to Promptly Correct Deficiency of Failure to Follow Procedures as Evidenced by Listed Actions ML20056G3681993-08-26026 August 1993 Notice of Violation from Insp on 930614-25.Violation Noted: Dynamic Tests for Seventeen safety-related MOVs Performed in Accordance W/Test Procedures That Did Not Incorporate Requirements & Acceptance Limit for Determining Operability ML20128D6071993-02-0101 February 1993 Notice of Violation from Insp on 921028-1222.Violation Noted:Bypass Jumpers Not Initiated for Scaffolding Installed for Greater than 90 Days as Required by Procedure ACP 2.19 ML20127D8451993-01-11011 January 1993 Notice of Violation from Insp on 920706-24.Violation Noted: on 920706,implementation Plan of Plant Design Change Record 2-123-91 Was Not Translated Correctly Into Work Order M2-92-06984 ML20126K0671992-12-28028 December 1992 Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $62,500.Violation Noted:Between 920711 & 0824, Two Independent Trains of Abfs Not Operable 1999-05-25
[Table view] Category:TEXT-INSPECTION & AUDIT & I&E CIRCULARS
MONTHYEARIR 05000245/19990081999-09-14014 September 1999 Insp Repts 50-245/99-08,50-336/99-08 & 50-423/99-08 on 990615-0809.Four Violations Noted & Being Treated as Ncvs. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000423/19990071999-08-27027 August 1999 Insp Rept 50-423/99-07 on 990614-0715.Violations Noted & Being Treated as Ncvs.Major Areas Inspected:Review of C/A Program Using IP 40500, Effectiveness of Licensee Controls in Identifying,Resolving & Preventing Problems IR 05000336/19990061999-07-19019 July 1999 Insp Repts 50-336/99-06 & 50-423/99-06 on 990420-0614.Ten Violations Occurred & Being Treated as non-cited Violations. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000336/19982191999-06-10010 June 1999 Insp Rept 50-336/98-219 on 981214-18,990126-29,0208-19 & 0301-05.Noncited Violations Identified.Major Areas Inspected:Exam of Licensee Corrective Action Implementation IR 05000245/19990051999-06-0404 June 1999 Errata to Insp Repts 50-245/99-05,50-336/99-05 & 50-423/99-05,consisting of Figure 1 ML20207G1211999-06-0303 June 1999 Insp Repts 50-245/99-05,50-336/99-05 & 50-423/99-05 on 990302-0419.No Violations Noted.Major Areas Inspected: Operations,Maint,Engineering & Plant Support ML20207F1521999-05-25025 May 1999 Notice of Violation from Investigation Rept 1-94-021 on 940506-960329.Violation Noted:Between 740831-910407,licensee Made Changes to Facility Described in Safety Analysis Rept for Refueling Core Offloads Without Performing Evaluation ML20196K2621999-05-24024 May 1999 EN-99-020:on 980525,notice of Violation & Exercise of Enforcement Discretion Will Be Issued to Licensee.Action Based on Severity Level III Problem Consisting of Four Individual Violations Involving Refueling Outage PNO-I-99-022, on 990509,Millstone Unit 2 Established Reactor Criticality.Nrc Staff Providing Augmented Insp Coverage of Restart Activities,Including round-the-clock Observations of Licensee Activities During Key Operational Evolutions1999-05-11011 May 1999 PNO-I-99-022:on 990509,Millstone Unit 2 Established Reactor Criticality.Nrc Staff Providing Augmented Insp Coverage of Restart Activities,Including round-the-clock Observations of Licensee Activities During Key Operational Evolutions IR 05000336/19990031999-05-10010 May 1999 Insp Rept 50-336/99-03 on 990322-26.No Violations Noted. Major Areas Inspected:Review of Actions Taken by Util to Resolve Significant Issues List Item 21,fire Protection ML20206F4601999-04-30030 April 1999 Insp Rept 50-336/99-04 on 990315-31.Violation Noted.Major Areas Inspected:Monitored Licensee Activities During Plant Transition Between Operational Modes,Both During Normal & off-normal Working Hours PNO-I-99-016, on 990406,operators Initiated Plant Cooldown from Normal Operating Pressure & Temp in Mode 3,hot Standby. Cooldown Was Necessary to Minimize Further Degradation of Bonnet Pressure Seal for Valve 2-SI-652 & to Repair Valve1999-04-0707 April 1999 PNO-I-99-016:on 990406,operators Initiated Plant Cooldown from Normal Operating Pressure & Temp in Mode 3,hot Standby. Cooldown Was Necessary to Minimize Further Degradation of Bonnet Pressure Seal for Valve 2-SI-652 & to Repair Valve ML20205M7201999-04-0606 April 1999 Notice of Violation from NRC OI Case 1-96-002 & Conclusions of Millstone Independent Review Team.Violation Noted. E Debarba,Deliberately Discriminated Against Supervisor in Performance Engineering Group at Millstone Station ML20205M7351999-04-0606 April 1999 Notice of Violation from Investigation in Case Numbers 1-96-002 & 1-97-007.Violation Noted:Licensee Discriminated Against Supervisor in Performance Engineering Group at Plant Due to Involvement in Protected Activities IR 05000245/19990021999-04-0202 April 1999 Insp Repts 50-245/99-02,50-336/99-02 & 50-423/99-02 on 990112-0301.Violations Noted.Major Areas Inspected: Operations,Maint,Engineering & Plant Support IR 05000336/19990011999-03-29029 March 1999 Insp Rept 50-336/99-01 on 990117-0217.Violations Noted.Major Areas Inspected:Licensee C/A Program Implementation Using Guidance of NRC IP 40500, Effectiveness of Licensee Controls in Identifying,Resolving & Preventing Problems ML20205J0941999-03-12012 March 1999 Rept of Review of Millstone Units 1,2 & 3:Allegations of Discrimination in NRC Ofc of Investigations Cases 1-96-002, 1-96-007,1-97-007 & Associated Lessons Learned ML20207M1131999-03-0909 March 1999 Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $88,000.Violation Noted:Employment of Two Contractor Employees Terminated in Aug 1997,in Part Because Individuals Raised Concerns Re MOV Program Manual ML20205G6161999-03-0909 March 1999 EN-99-010:on 990309,notice of Proposed Imposition of Civil Penalty in Amount of $88,000 Issued to Licensee.Action Based Upon Severity Level II Problem Involving Discrimination Against Two Contractor Employees at Millstone MOV Dept IR 05000245/19980061999-03-0101 March 1999 Insp Repts 50-245/98-06,50-336/98-06 & 50-423/98-06 on 981123-990111.No Violations Noted.Major Areas Inspected: Operations,Maintenance,Engineering & Plant Support PNO-I-99-006, on 990128,operators Inadvertently Reduced Spent Fuel Pool Water Level by Two Inches When Purification of Spent Fuel Pool Water Initiated.Operators Held Shift Briefing to Discuss Realigning Purification Sys1999-01-29029 January 1999 PNO-I-99-006:on 990128,operators Inadvertently Reduced Spent Fuel Pool Water Level by Two Inches When Purification of Spent Fuel Pool Water Initiated.Operators Held Shift Briefing to Discuss Realigning Purification Sys IR 05000245/19982171999-01-22022 January 1999 Evaluation Repts 50-245/98-217,50-336/98-217 & 50-423/98-217 Conducted on 981026-30.Areas Evaluated:Whether NNECO Has Improved Sufficiently & Has Demonstrated Sustained Performance in Maintaining safety-conscious Work Environ PNO-I-99-004, on 990115,carbon Dioxide Was Inadvertently Discharged Into Unit 3 Cable Spreading Room,Containing Electrical Wiring.Ambulance Reported to Site as Precautionary Measure.Licensee Assembled Event Review1999-01-20020 January 1999 PNO-I-99-004:on 990115,carbon Dioxide Was Inadvertently Discharged Into Unit 3 Cable Spreading Room,Containing Electrical Wiring.Ambulance Reported to Site as Precautionary Measure.Licensee Assembled Event Review IR 05000336/19980051999-01-0707 January 1999 Insp Repts 50-336/98-05 & 50-423/98-05 on 981006-1123. Violations Noted.Major Areas Inspected:Operations, Maintenance,Engineering & Plant Support ML20199C6381999-01-0707 January 1999 Notice of Violation from Insp on 981006-1123.Violation Noted:On or Before 981120,conduit 9-15,in Fire Area A-24,not Sealed & Tested in Accordance with Astme E-119,fire Endurance Test PNO-I-99-001, on 981231,Millstone Unit 2 Began Reloading Fuel Into Reactor After Extended Shutdown.Millstone Unit 3 Went Critical on 981230,after Forced Outage Due to Inadvertent MSIV Closure During Surveillance Testing at Power1999-01-0404 January 1999 PNO-I-99-001:on 981231,Millstone Unit 2 Began Reloading Fuel Into Reactor After Extended Shutdown.Millstone Unit 3 Went Critical on 981230,after Forced Outage Due to Inadvertent MSIV Closure During Surveillance Testing at Power PNO-I-98-062, on 981211,Millstone Unit 3 Tripped from 100% Reactor Power During MSIV Partial Stroke Testing.Solenoid Valve Integral to MSIV Failed to Reopen When Licensed Operator Released Test Switch1998-12-15015 December 1998 PNO-I-98-062:on 981211,Millstone Unit 3 Tripped from 100% Reactor Power During MSIV Partial Stroke Testing.Solenoid Valve Integral to MSIV Failed to Reopen When Licensed Operator Released Test Switch ML20195H6901998-11-18018 November 1998 Notice of Violation from Insp on 980818-1005.Violation Noted:Engineering Evaluations Not Performed When RCS Heatup Rate Limit Exceeded on 951217 & When RCS Cooldown Rate Limit Exceeded on Three occasions,940424,0728 & 951215 IR 05000245/19982161998-11-18018 November 1998 Insp Repts 50-245/98-216,50-336/98-216 & 50-423/98-216 on 980818-1005.Violations Noted.Major Areas Inspected: Operations,Maintenance,Engineering & Plant Support IR 05000336/19982031998-11-0505 November 1998 Insp Rept 50-336/98-203 on 980824-0904.No Violations Noted. Major Areas Inspected:Effectiveness of Configuration Mgt Plan ML20155B1521998-10-23023 October 1998 Notice of Violation from Insp on 980810-0903.Violation Noted:Design Basis,As Described in FSAR Chapter 14,Accident Analyses Had Not Been Correctly Translated Into Plant Procedures & Acceptance Criteria IR 05000336/19982131998-10-23023 October 1998 Insp Rept 50-336/98-213 on 980810-0903.Violations Noted. Major Areas Inspected:Certain Aspects of Accident Mitigation Sys IR 05000245/19982151998-10-14014 October 1998 Evaluation Repts 50-245/98-215,50-336/98-215 & 50-423/98-215 on 980824-28.Major Areas Evaluated:Whether Licensee Has Improved Sufficiently & Has Demonstrated Sustained Performance in Maintaining safety-conscious Work Environ IR 05000336/19980041998-10-0101 October 1998 Insp Rept 50-336/98-04 on 980914-18.No Violations Noted. Major Areas Inspected:Mov Program Associated with GL 89-10 IR 05000245/19982121998-09-25025 September 1998 Insp Repts 50-245/98-212,50-336/98-212 & 50-423/98-212 on 980630-0817.No Violations Noted.Major Areas Inspected: Operations,Maintenance,Engineering & Plant Support IR 05000423/19982111998-09-11011 September 1998 Insp Rept 50-423/98-211 on 980413-24,0511-15,27-29,0609-11 & 23-25.Violation Noted.Major Areas Inspected:Evaluation of Licensee C/As & Other ICAVP Process Activities ML20154D1151998-09-11011 September 1998 Notice of Violation from Insp on 980413-24-0511-15,27-29, 0609-11 & 23-25.Violation Noted:Program Implemented TS 6.8.4.a,failed to Include Provisions to Reduce Leakage from RSS Heat Exchangers to SW Sys IR 05000424/19980061998-09-10010 September 1998 Insp Repts 50-424/98-06 & 50-425/98-06 on 980628-0815.No Violations Noted.Major Areas Inspected:Aspects of Licensee Operations,Engineering,Maint & Plant Support PNO-I-98-039, 980812,Millstone Unit 3 Was Shutdown to Repair Small Leak on Afws Discharge Noted.Current Leakage Does Not Exceed Regulatory Requirements & Shutdown Not Required by Tech Specs.Licensee Issued Press Release on 9808111998-08-12012 August 1998 PNO-I-98-039:980812,Millstone Unit 3 Was Shutdown to Repair Small Leak on Afws Discharge Noted.Current Leakage Does Not Exceed Regulatory Requirements & Shutdown Not Required by Tech Specs.Licensee Issued Press Release on 980811 ML20237D3041998-08-12012 August 1998 Notice of Violation from Insp on 980413-0508.Violations Noted:Two Examples Identified Where Licensee Not Performing Leakage Testing of safety-related Valves in Sys That Could Contain Highly Radioactive Fluids During Accident IR 05000245/19982081998-08-12012 August 1998 Insp Repts 50-245/98-208,50-336/98-208 & 50-423/98-208 on 980428-0629.Violations Noted.Major Areas Inspected: Operations,Maint,Engineering & Plant Support ML20237B0741998-08-12012 August 1998 Notice of Violation from Insp on 980428-0629.Violation Noted:Licensee Failed to Direct Test Personnel to Close & Lock RHR Outboard Drain Valve IR 05000336/19982011998-08-12012 August 1998 Insp Rept 50-336/98-201 on 980413-0508.Violations Noted. Major Areas Inspected:Licensee Ability to Identify & Resolve Deficiencies Focusing,But Not Limited To,Period of CMP Implementation & ICAVP at Parsons Power Group,Inc PNO-I-98-026, on 980701,Millstone Unit 3 Criticality Update Made.Nrc Staff Continues to Provide Augmented Insp of Unit 3 Restart Activities,Including round-the-clock Coverage of Key Operational.Licensee Plans No Press Release1998-07-0101 July 1998 PNO-I-98-026:on 980701,Millstone Unit 3 Criticality Update Made.Nrc Staff Continues to Provide Augmented Insp of Unit 3 Restart Activities,Including round-the-clock Coverage of Key Operational.Licensee Plans No Press Release PNO-I-98-025, on 980630,unit 3 Established Reactor Criticality,However Reactor Was Shut Down When Control Room Operator Noticed Spiking Intermediate Range Monitor.Licensee Troubleshooting1998-06-30030 June 1998 PNO-I-98-025:on 980630,unit 3 Established Reactor Criticality,However Reactor Was Shut Down When Control Room Operator Noticed Spiking Intermediate Range Monitor.Licensee Troubleshooting IR 05000245/19982071998-06-19019 June 1998 Insp Repts 50-245/98-207,50-336/98-207 & 50-423/98-207 on 980301-0427.Violations Noted.Major Areas Inspected:Maint, Operations,Engineering & Plant Support ML20249C6931998-06-19019 June 1998 Notice of Violations from Combined Insp on 980301-0427. Violations Noted:Prior to 980424,instrument Min Accuracy of Wind Speed Channels Were Not Measured as Required by Table 3.3-8 of Unit 2 TS 3/4.3.3.4 IR 05000423/19970831998-06-12012 June 1998 Insp Rept 50-423/97-83 on 980413-24.Violations Noted. Major Areas Inspected:Readiness of Plant Hardware,Staff & Mgt Programs to Support Safe Restart & Continued Operation of Plant Unit 3 ML20249B0421998-06-12012 June 1998 Notice of Violations from Insp on 980413-24.Violations Noted:Only 1 RCS Loop Operable W/Plant in Mode 4 on 980407 IR 05000423/19970821998-06-11011 June 1998 Insp Rept 50-423/97-82 on 980209-20.Violations Noted.Major Areas Inspected:Corrective Actions Processes 1999-09-14
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r APPENDIX A NOTICE OF VIOLATION Northeast Nuclear Energy Company Docket No. 50-245 Millstone Nuclear Power Station, Unit 1 License No. DPR-21 j As a result of the inspection conducted on June 17-28, 1985, and in accordance
.with the NRC Enforcement Policy (10 CFR 2, Appendix C), published in the Fed-eral Register on March 8,1984 (49 FR 8583) the following violations were iden-tified:
1 A. Technical Specification 6.8.1 states in part: " Written procedures shall be established, implemented and maintained covering activities...recom-mended in Appendix "A" of Regulatory Guide 1.33, February,1978.. ." This appendix requires that maintenance that can affect the performance of safety related equipment should be properly performed in accordance with
- written procedures appropriate to the circumstance.
- Contrary to the above requirements, two examples of a violation were identified as follows
- 1. As of June 28, 1985, written calibration procedures were not established for the calibration of safety related pressure switches PS-2-16, PS-2-20, PS-2-54 and PS-2-56 which provide low suction pressure, start prohibit, interlocks for the safety-related Feedwater Coolant Injection (FWCI) pumps A and B.
- 2. On June 18, 1985, it was identified that the self-aligning rod end bushing on a mechanical snubber, pipe support ICHR-8, of the safety-related isolation condenser had slipped partially out of the rod end bushing housing, resulting in an inoperable isolation condenser system until repairs were made. A subsequent review of procedure MP 739.6, " Mechanical Snubber Visual Inspection" revealed that the pro-cedure was incapable of identifying the misaligned rod end bushing.
, The above two examples constitute collectively a Severity Level IV violation. (Supplement I)
- 8. Technical Specification 16.12.2 states that locked doors shall be provided to prevent unauthorized entry into each high radiation area in which the intensity of radiation is greater than 1000 mrem /hr. The licensees admi-nistrative procedure (SHP) 4906, " Posting Radiological Controlled Areas",
, Section 8.4 requires that all high radiation areas with general area dose rates greater than 1000 mrem /hr shall have all entrances locked or shall be continuously quarded,to prevent unauthorized entry into those areas.
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Appendix A 2 Contrary to the above requirement, on June 27, 1985 at approximately 1:00 PM, the door to the Scram Discharge Volume (SDV) high radiation area had been left unlocked and unattended. This area was posted with signs on the door "High Radiation Area, RWP Required for Entry" and " Door Must Be Locked At All Times". A survey of the area disclosed " hot spots" of 2000 mrem /hr. Further, if a reactor scram occurred the general area radiation would be greater than 1000 mrtm/hr.
This is a Severity Level IV violation. (Supplement I)
Pursuant to the provisions of 10 CFR 2.201, Northeast Nuclear Energy Company is hereby required to submit to this office within thirty days of the date of the letter which transmitted this Notice, a written statement or explanation in reply, including: (1) the corrective steps which have been taken and the results achieved; (2) corrective steps which will be taken to avoid further violations; and (3) the date when full compliance will be achieved. Where good cause is shown, consideration will be given to extending this response time.
l 0FFICIAL RECORD COPY CAT MILL 1 85 0001.1.0 10/10/85 l
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- TABLE OF CONTENTS EXECUTIVE
SUMMARY
- DETAILS 1.0 Persons Contacted
- 2.0 Scope of Inspection
' t i 2.1 Objectives 2.2 Inspection Items i 2.3 Conduct of Inspection 3.0 Recovery of Offsite Power 4.0 Safety / Relief Valves and Manual Depressurization ,
4.1 System Description
4.2 Manual Depressurization j 4.3 Availability of Safety / Relief Valves 5.0 Feedwater Coolant Injection (FWCI) System
5.1 System Description
j 5.2 Assessment of FWCI Operation 5.3 Assessment of FWCI Initiation and Availability of i
Relays and Initiating Components 5.4 Availability of FWCI System Pumps
] 5.5 Availability of FWCI Makeup Water l 6.0 Availability of Emergency AC Power System i
! -6.I System Description
- 6.2 Gas turbine Operations j- 6.3 Gas Turbine Availability j 6.4 Availability of Emergency AC Bus Breakers / Relays 7.0 Availability of Isolation Condenser
7.1 System Description
7.2 Equipment Availability 7.3 Visual Inspection 7.4 Operations Simulation 8.0 Administrative Controls l
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Table of Contents 2 9.0 Human Factors Engineering 9.1 Equipment / Facility Identification 9.2 Protective Covers for Relays 9.3 Other Emergency Measures 10.0 Facility Tours 10.1 Areas Toured 10.2 Findings 11.0 Unresolved Items 12.0 Exit Meetings Attachment
EXECUTIVE
SUMMARY
This report documents the results of an announced team inspection performed at the Millstone Point Unit 1 Nuclear Power Plant from June 17, 1985 through June 28, 1985. The inspection examined plant hardware and the operational activities relating to a dominant accident sequence identified in NUREG/CR-3085,
" Interim Reliability Evaluation Program (IREP): Analysis of the Millstone Point Unit 1 Nuclear Power Plant". This probabilistic risk assessment (PRA) study identified the key components and activities which could contribute signift-cantly to the core melt accident sequences or mitigate the consequences of such events. The insights and details of one dominant accident sequence in the IREP study were utilized to develop and conduct the inspection.
f Objectives The inspection objectives were to assess: 1) the availability of selected equipment identified as important contributors to the cause of the accident or important to prevent / mitigate the selected accident sequence in the IREP, and
- 2) the ability of the plant staff to respond to and recover from the accident sequence.
To assess the integral aspects of the plant status and operations, the com-
- plementary station programs, not addressed in the IREP study, were also 1
evaluated. They included administrative controls, implementation of training and QA/QC programs, station initiatives on safety measures, and human factor engineering.
Application of IREP Study Results To increase the effectiveness of the inspection effort and concentrate on risk, the most dominant accident sequence was selected from the Millstone Unit 1 IREP study and the inspection items were identified accordingly.
The selected accident sequence in the IREP study identified the specific plant features and activities important to the accident initiating event, preventive and success features, contributing factors to the consequences, and necessary recovery actions required to mitigate the accident sequence. The items inspected and the conduct of the inspection were derived from details of the selected dominant accident sequence, "A Loss of Normal AC Power".
The initiation of the selected accident sequence was triggered by a loss of normal station power, followed by a failure of a safety / relief valve to reseat after opening. The contributing factors to the core melt consequence were the failures of the Feedwater Coolant Injection (FWCI) into the core and of the operator to manually depressurize the reactor coolant system, which would permit the low pressure coolant system to operate. These failures of the FWCI
Executive Summary 2 system and of manual depressurization will prevent coolant coverage of the core, resulting in core melt down in hour. To mitigate the consequence of the initiating and contributing events, it would be necessary to recover the offsite power within h hour. The sequence frequency was estimated to be 7E-5/ reactor year, according to the IREP study, and it accounted for 23% of the total core melt frequency, thus dominating all other accident sequences. It should be noted that the plant feature and activities selected for inspection have a greater impact on safety than this sequence freqency suggests, as they are common to the majority of all dominant sequences identified in the IREP.
Availability of Equipment The inspection rationale to evaluate the availability of plant equipment was to assure that they would be available to operate in accordance with their intended safety functions should their services be demanded. Accordingly, the plant maintenance program relative to the selected equipment, was inspected to assure that the preventive measures, corrective maintenance, routine work controls (including jumpers, tagging and work orders), and periodic surveillance were 2
addressed and performed effectively. The conduct of inspection, thus, included evaluation of the station maintenance activities to ascertain that it is per-formed adequately and effectively in accordance with the prescribed written procedures, and that generic problems and recurring failures of the equipment were adequately addressed in the station maintenance and surveillance programs.
To assess the implementation of the programs, "AS FOUND" states of the equipment were evaluated by performing "walkthroughs" visual inspection, witnessing of test-in progress and surveillance simulations. The effectiveness of the pre-ventive and corrective maintenance measures were evaluated by reviewing appro-priate work records and the performance trend of the equipment, as well as con-trols and measures for fire prevention and environmental qualification.
Plant Operations and Recovery Actions The Millstone-1 IREP study provided insights related to plant operations, and identified that operator recovery actions or errors made during the course of an accident were very important to the successful recovery from an accident.
Thus, to assure plant safety, a high degree of equipment availability must be complemented by the ability of the plant staff to respond and recover from accidents.
Plant operations were evaluated to ascertain that operators were familiar with the plant equipment and the associated plant procedures during normal, abnormal and emergency situations. The operation of plant systems and equipment identi-fied in the selected accident sequence was demonstrated by the plant staff during "walkthrough" simulations of recovery actions. The operators were evaluated for their ability to utilize the control room indications, to under-i
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Executive Summary 3 l
l l stand automatic features under design-base operations, their knowledge of
- operating procedures and to operate the plant equipment manually. Local or i i alternate train operation was also simulated when normal operation or recovery l action failed due to equiement failures. Control room operations were assessed i s to assure that proper symptom-oriented emergency operating procedures were j available and capable of being effectively used during the accident situation f i and under stress. Also, station operating procedures were verified to be '
j technically correct and clearly identified important operating instructions. ;
1 The foregoing inspection logic is depicted in Figure 1.
- Findings 1
j The inspection findings demonstrated that the plant programs designed to assure i i hardware availability were adequate and the plant staff exhibited an excellent j knowledge of plant operations, equipment and procedures. The plant staff, l during responses to simulated events / activities, readily demonstrated their knowledge of procedures, physical locations of equipment and familiarity with r i overall plant operations. The operator responses were indicat;ve of the j effectiveness of training on procedures and equipment.
I l The high degree of equipment availability and operational readiness is
! indicative of effective management and administrative controls.
l 1 The equipment identified by the IREP accident sequence was found to be included '
) in the Plant " quality" list and controlled under " safety-related" standards, i
The physical plant was well maintained and clean. This indicates that there is I a positive management and staff attitude.
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l The inspection team identified two violations and made observations in j the following areas. l
- Human Factors I
- Equipment Identification i
The plant equipment and their status were identified by color-coded status tags and alpha-numeric identifications, and the areas were i
posted with information, precautions, and signs, related to fire j doors, radiological warnings and security zones. The plant in j general exhibited excellent posting and designations. ,
1 l The following exceptions were observed:
1 The emergency condensate transfer pump did not have any iden-tification.
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4 I Executive Summary 4 '
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Three different equipment identification systems are used, which !'
result in discrepancies in the equipment identification between '
procedure OP337 and electric plugs on CRP 932-F. The three i systems used are station identification numbers, Ebasco's (the -
j architect / engineer), and General Electric drawings. '
i Control Room Indication
! The control room indication for the isolation condenser level is l given in " feet" and the procedure OP 307 is in " inches".
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- Inadvertent Closure of Vital Breaker i
i During battery charger alarm circuit modification in the control room j on April 17, 1985, a production test electrician unknowingly bumped a .
4160 volt tie-breaker in rear panel 908, relay 110-RX, with his leg, closing the breaker. The eleven GE HGA relays, including the 110-RX, are not provided with protective covers to prevent such an event, j The licensee initiated a work order to install the protective covers.
Potential Isolation of Feedwater Coolant Injection Pumps l The Millstone Unit 1 IREP study identified that failure of FWCI pump i pressure permissive switches would prevent feedwater coolant injec-tion and contribute to the core melt accident sequence during the loss of normal AC power accident.
Suction pressure switches PS-2-16 and PS-2-54 provide low suction i pressure, start prohibit interlocks for FWCI pump A; pressure j switches PS-2-20 and PS-2-56 provide the same interlocks for FWCI e I pump B. A single failure of any one of two pressure switches will
! prevent starting of the associated FWCI pump, and therefore, result
! in a loss of FWCI.
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4 These pressure switches are required to be calibrated every refueling ,
! outage, and the calibration data is recorded using " Calibration r j Report" data sheets. This " Calibration Report" is merely data '
3 logging sheet and no written procedure is provided controlling the l calibration activities during which the pressure switches must be j isolated by closing the switch isolation valves. Upon completion of 1 the calibration, the pressure switches must be valved in. If not, !
! the associated FWCI pump would be isolated and would not start even !
- if the FWCI pump actuation was initiated. The lack of procedural
! control over these devices increases the probability of failure to return the systems configurations to operability status and the j potential for error is further enhanced because there is no control
- room nor local indications provided for the status of the pressure
! switch isolation.
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Executive Summary 5 i
This failure to provide a written procedure for safety-related activities is one example of a violation discussed in the report.
Facility and Equipment Surveillance Isolation Condenser Snubber During a visual examination of snubbers on June 18, 1985, the NRC i staff noted that the self-aligning rod end bushing on pipe support ICHR-8 for the isolation condenser, had partially slipped out of the rod end. This bushing connects the snubber to the rigid pipe support via a ball and clevis pin. With the bushing partially disengaged from the snubber, the load carrying capability of the snubber during a seismic event or water hammer is reduced. Subsequent inspection identified two other snubbers, ICSN-4A and 48, that had an excessive-ly large clearance between the bushing and the clevis.
Review of surveillance procedure, MP739.6, " Mechanical Visual Inspec-i tion", indicated that the inspection procedure was incapable of l identifying the problems with the rod end bearings. This inadequacy in the surveillance procedure is another example of a violation discussed in the report.
- Motor Operated Valve (MOV) Surveillance
- On May 15, 1985, a MOV housing on the Low Pressure Coolant Injection i
(LPCI) system fell off. Based on a review of Plant Incident Report
' (PIR) No. 19-75 and discussions with licensee representatives, the staff noted that the station procedure for LPCI operability surveil-lance did not specify sufficient instructions to identify the cracked or loose parts during " walk-down" visual inspections. The licensee has committed to revise the surveillance procedure to clarify the vistal inspection procedures.
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- Radiological Controls During a routine plant tour on June 27, 1985 at approximately 1:00 3
p.m. the NRC staff observed that the door to the Scram Discharge Volume (SDV) high radiation area was unlocked and unattended. In accordance with the station procedure SHP 4906 and Technical Specifi-cation 6.12.2, this area was posted with signs, "High Radiation Area, RWP Required for Entry" and " Door Must Be Locked At All Times".
The failure to follow written procedure and thus to maintain the high radiation area access door with a lock or guard constitutes a violation.
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Executive Summary 6 Conclusion The NRC staff's conclusion was that the plant equipment was in a high state of operational readiness and could be relied upon to respond to accidents.
- The staff concluded that the plant staff was well saalified and, with a high probability, could recover from an accident.
The licensee could improve certain procedures to assure specific equipment availability by taking prompt corrective actions to the staff observations in the findings paragraphs above.
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