SR-S2-75-02:during Refueling,Fuel Assembly N-20 Incurred Damage to Two of Four Holddown Springs on Top Nozzle Assembly.Fuel Assembly Acceptable for Power Operation in Cycle 2ML20086Q472 |
Person / Time |
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Site: |
Surry ![Dominion icon.png](/w/images/b/b0/Dominion_icon.png) |
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Issue date: |
06/02/1975 |
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From: |
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.) |
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To: |
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Shared Package |
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ML20086Q378 |
List: |
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References |
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SR-S2-75-02, SR-S2-75-2, NUDOCS 8402270562 |
Download: ML20086Q472 (6) |
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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO LER)
MONTHYEARML20132B3291996-12-0606 December 1996 Special Rept:On 961113,operator Discovered Control Switch for Diesel Output Breaker in pull-to-lock Position. Investigation Was Performed to Determine How Long Aac DG Was Inoperable ML20112F6841984-12-11011 December 1984 Special Rept SR-84-4:on 841015,process Vent High Range RM-GW-130-2 & Ventilation Vent High Range RM-VG-131-2 Effluent Monitors Inoperable.Cause Under Investigation. 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Containment Purge Terminated & Compressor Isolated ML20087C1391975-09-15015 September 1975 Ro:On 750802 & 03,condenser Cooling Water Discharge Temp Exceeded 98 F for More than 3 H.Caused by Rising River Water Temp.Util Requested & Was Granted Emergency Relaxation of Tech Spec 4.14.A.1 Effective Until 750806 ML20087C1781975-07-25025 July 1975 SR-S1-75-03:on 750709,I-131 Activity Found to Be 4.6% of Tech Spec Limit.Caused by Containment Purging Operations & Containment Maint Activities.Containment Purge Exhaust Diverted Through Charcoal Filter Sys ML20087C2151975-06-30030 June 1975 SR-S1-75-02:on 750502,rate of Liquid Waste Release Increased to 10% of Tech Spec Limit to Reduce Quantity of Stored Liquid Waste.On 750514,I-131 Activity Found at 6.5% of Tech Spec Limit ML20086Q4721975-06-0202 June 1975 SR-S2-75-02:during Refueling,Fuel Assembly N-20 Incurred Damage to Two of Four Holddown Springs on Top Nozzle Assembly.Fuel Assembly Acceptable for Power Operation in Cycle 2 ML20086Q4151975-06-0202 June 1975 SR-S2-75-01:during Refueling Operation,Cladding Perforation Detected on Fuel Assembly N-10.Fuel Assembly Can Be Safely Operated to end-of-Cycle 2 Design Burnup ML20086R1981975-04-10010 April 1975 USRE-S2-74-01:on 740214,alarm Received Indicating Low Discharge Flow in Containment Vacuum Sys.Caused by Containment Vacuum Pumps Discharging Air.Pumps Removed & Spare Pump Installed ML20086Q7141975-04-0808 April 1975 URSE-S2-74-01:on 740214,alarm Received Indicating Low Discharge Flow in Containment Vacuum Sys.Cause Not Determined.Pumps Disassembled,Inspected,Cleaned & Reassembled ML20086Q8371975-03-0404 March 1975 SR-S1-75-05:on 750929,routine Sampling of Ventilation Vent Gaseous Activity Revealed I-131 Activity in Excess of 4% of Tech Spec Limit.Caused by Containment Purging Operations, Filter Problems & Leakage & Treatment of Radioactive Water ML20086Q9971975-02-24024 February 1975 SR-S1-75-01:on 741120,45 Concrete Blocks Fell Into Reactor Cavity.Reactor Vessel or Associated Sys Not Damaged & All Debris Removed ML20086R1261975-02-0303 February 1975 Ro:On 750128,newly Installed Fish Screens at Intakes Allowed Average of 89% of Fish Impinged During Period to Return to River Alive.Incident Not Considered to Have Caused Significant Mortality.Fish Mortality Data Encl ML20086S3821975-01-24024 January 1975 SR-S1-74-06:damage Discovered on Pipe Restraint Anchors on Safety Injection Accumulator Discharge Lines.Caused by Flashing & Water Hammer Shock Experiences During Early Operation ML20086S4121975-01-10010 January 1975 SR-S1-74-04:on 740904,sampling of Ventilation Vent Activity Revealed I-131 Activity of 5.8% of Tech Spec Limit.Caused by High Activity of Steam Generator a Blowdown Vent.Primary to Secondary Tube Leak Repaired ML20086S3031974-12-13013 December 1974 USRE-S1-74-03:on 741107,small Amount of Low Level Radioactivity Released to James River Via Component Cooling Svc Water.Caused by Inoperability of Pump 1-SW-P-6 Due to Lack of Water Lubrication ML20086S2801974-11-29029 November 1974 SR-S1-74-05:deterioration of Steam Generator Tubes Noted. Caused Not Determined.Sludge Deposits & Deleterious Effect of Sodium Phosphate Chemistry Control Contributed to Magnitude & Rate of Deterioration ML20086S3781974-11-29029 November 1974 SR-S2-74-01:pipe Restraints on Three Safety Injection Accumulator Discharge Lines Experienced Some Degree of Shock & Vibration.Caused by Flashing & Water Hammer Shock Experienced During Early Operation ML20086S5741974-09-19019 September 1974 USRE-S1-74-01:discovered Two Singular Pipe Runs Passing Through Respective Containment Boundary W/Check Valves on Either Side of Containment.Caused by Oversight in Design. Four Check Valves Will Be Installed ML20086S4731974-08-26026 August 1974 Ro:On 740725 & 26,liquid Release Occurred Which Exceeded 4% of Tech Spec Limit.Steam Generator Leakage Being Continuously Monitored & Will Be Repaired During 741015 Refueling Shutdown ML20086S9721974-07-15015 July 1974 SR-S1-74-01:on 740526,reactor Vessel Leakoff High Temp Alarm Received.Caused by Inadequacy of Packing Mfg by J Crane Co. Packing Will Be Replaced W/Grafoil Packing ML20215H5091972-08-16016 August 1972 Ro:On 720727,during Shutdown,Two Employees Injured When Steam Vent Sys Malfunctioned.Caused by Decay Heat Release Piping Disengaging from Piping Support Sys.Workers Treated for Burns.Design Change Investigated.News Release Encl 1996-12-06
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML18152A2811999-10-12012 October 1999 Technical Basis for Elimination of Nozzle Inner Radius Insps (for Nozzles Other than Reactor Vessel),Technical Basis for ASME Section XI Code Case N-619. ML18152B3531999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Surry Power Station,Units 1 & 2.With 991012 Ltr ML18152B6651999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Surry Power Station Units 1 & 2.With 990915 Ltr ML18152B4421999-08-27027 August 1999 LER 99-006-00:on 990802,determined That Plant Was Outside of App R Design Basis Due to Fire Barrier Deficiencies. 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ML18152B3771999-08-13013 August 1999 LER 99-004-00:on 990714,TS Violation Due to non-safety Related Fans Effect on CR Boundary Was Noted.Cause of Event Has Not Yet Been Determined.Cable Spreading Room Doors Were Operned to Reduce Pressure in Rooms ML18152B3791999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Surry Power Station,Units 1 & 2.With 990811 Ltr ML18152B3911999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Surry Power Station,Units 1 & 2.With 990713 Ltr ML18152B4341999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Surry Power Station,Units 1 & 2.With 990614 Ltr ML20195E2401999-05-31031 May 1999 Rev 2 to COLR for SPS Unit 2 Cycle 16 Pattern Ag ML18152B4181999-05-18018 May 1999 LER 99-002-00:on 990425,MSSVs Tested Out of Tolerance for as Found Setpoint.Caused by Minor Setpoint Drift.No Immediate Action Required.Deviation Rept Submitted for Each Valve.With 990518 Ltr ML18152B4161999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Surry Power Station Units 1 & 2.With 990512 Ltr ML18152B4111999-04-28028 April 1999 LER 99-003-00:on 990331,potential Loss of Charging Pumps Was Noted.Caused by Main CR Fire.Station Deviation Was Issued on 990331.With 990428 Ltr ML18152B6511999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Surry Power Station Units 1 & 2 ML18153A2741999-03-29029 March 1999 LER 99-002-00:on 990301,prematurely Released Fire Watches Resulted in Violation of TS 3.21.B.7.Caused by Inadequate Procedure.Procedure for Opening & Sealing Fire Stops Was Revised on 990212 ML18153A2681999-03-19019 March 1999 LER 98-013-01:on 981122,turbine/reactor Tripped on High Due to Short Circuit in Summator for MSL C Loop Channel III Flow Transmitter.Replaced 1-MS-FT1494 Summator & Module Repair Procedure Revised.With 9903190 Ltr ML18152B7331999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Surry Power Station,Units 1 & 2.With 990310 Ltr ML18152B5421999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for Surry Power Station,Units 1 & 2.With 990210 Ltr ML18151A3031999-01-29029 January 1999 ISI Summary Rept for 1998 Refueling Outage,Including Form NIS-1, Owners Rept for ISIs & Form NIS-2, Owners Rept for Repairs & Replacements. 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Deviation Rept Submitted to Document Deviating Condition ML18153A2301998-03-0606 March 1998 LER 98-004-00:on 980206,fire Watch Was Released Prematurely Resulting in Violation of Ts.Caused by Inadequate Planning of Repair Activity.Work Orders Will Include Ref to Applicable Procedures Developed to Assist in Repairs ML18153A2251998-03-0404 March 1998 LER 98-002-00:on 980202,automatic Turbine Trip Resulted in Automatic Reactor Trip.Caused Degraded Generator Voltage Regulator sub-component Failure.Placed Plant in Safe Hot SD & Replaced Intermittent Relay & Relay Socket 1999-09-30
[Table view] |
Text
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rm f, k.s b l SPECIAL REPORT SR-S2-75-02 REPORT ON FUEL ASSDIBLY N-20 DOCKET No. 50-281 LICENSE NO. DPR-37 JUNE 2, 1975 SURRY POWER STATION VIRGINIA ELECTRIC AND POWER COMPANY e
8402270562 750630 PDR ADOCK 05000281 S PDR I
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I. INTRODUCTION During the refueling operations for Cycle 2 of Surry Unit No. 2, fuel assembly N-20 incurred damage to two of the four hold-down springs on the top nozzle assembly.
. l l
II.
SUMMARY
OF OCCURRENCE l l
When fuel assembly L-16 was being removed from core location B-8, l l
two adjacent locking fingers on the fuel handling crane failed to engage the top nozzle, so that the fuel assembly was only supported by the re-maining two fingers. When the assembly was pulled clear of the core, it was free to pivot about the axis formed by the two engaged fingers.
The axis of rotation was perpendicular to the coolant flow maintained through the vessel by the residual heat removal system. This coolant flow caused the lower end of the fuel assembly to drift, and the misalignment of the fuel assembly with the direction of lift cauced it to bind in the crane mast. This binding caused an increase in the nominal load normally required to withdraw a fuel assembly from the core, prompting the crane operator tc cease the fuel assembly withdrawal before an overload condition was reached.
Unaware of the cause of the increased load, the crane operator lowered fuel assembly L-16, the bottom of which had drifted over fuel assembly N-20 which was in core location C-8. The bottom nozzle assembly of L-16 contacted and came partially to rest on the top nozzle assembly of N-20.
Upon contact, the crane operator noted a decrease in the load and then stopped the crane. Two of the bottaa pedestal feet of L-16 were then partially resting on the hold-down springs on faces two and four of fuel assembly N-20.
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both fuel assembly L-16 and N-20 were removed to the spent fuel !
i pit and subjected to a preliminary binocular visual observation and a
[ subsequent visual' examination using remote TV inspection equipment and
- l videotape. The inspections established that the hold-down springs on i faces two and four of assembly N-20 had been plastica 11y deformed such
) that the springs on faces two and four had a permanent set of 1.0 and i
1.1 inches, respectively, relative to their original free height. The hold-l down springs on faces one and three of N-20 showed no evidence of contact.
No additional damage other than the hold-down springs on N-20 was observed i
on either N-20 or L-16 which is not scheduled for operation during Cycle 2.
l Vepco requested Westinghouse, the fuel assembly designer, to evaluate 1
- the extent of the damage and the possibility of adverse consequences of con-i tinued operation of fuel assembly N-20 during Cycle 2 as schedule. An in-dependent consultant was also retained to review the results of the West-l t
inghouse evaluation.
The Westinghouse evaluation consisted of an analysis of the minimum expected hold-down capability of the undamaged springs coupled with the i maximum expected lif t forces during normal cold startup, normal hot operation, and postulated abnormal conditions of reactor coolant pump overspeed. In-l -
I puts to the calculations included uncertainties in coolant'and component temperature, component dimensions and tolerance stack-ups, thermal expansion coefficients, fuel assembly growth during Cycle 1 irradiation, spring material properties, and core pressure drop. As-built information was_used where it l
was available and-pertinent. Quality control / quality assurance records for fuel assembly N-20 were reviewed to ensure that there were no deviations accepted during fabrication which would influence the results of the analysis.
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a __A Upon completion of the Westinghouse analysis, personnel from Vepc6 "
and their consultant met with Westinghouse to review and evaluate tJs results and conclusions. The results of the analyses are discussed below.
The analysis shows that the minimum expected hold-down capability of the springs, when computed at normal power operation and at a.95 per cent x 95 per cent confidence level, exceeds the maximum expected lift forces, (also computed at a 95 per cent x 95 per cent confidence level), thus demonstrating that the remaining hold-down capability is adequate to prevent the assembly from lifting off the lowe. ore plate during normal power operation. The probability of not lifting the assembly is thus gredter than 95 per cent at the 95 per cent confidence level.
The analysis of the heat-up conditions shows to a greater than 95 'peo , ' 's cent x 95 per cent confidence level, that lift forces will not exceed the ~
u hold-down forces with all three reactor coolant pumps operating for reactor coolant temperatures greater than 360 degrees F. In addition, also to greater than 95 per cent x 95 per cent confidence level, a postulated s reactor coolant pump overspeed transient condition of 110 per cdnt or lese during normal power operation will not lift the assembly to the extent that further plastic deformation of the hold-down springs will result. After experiencing a transient in excess of 110 per cent pump overspeed, the two undamaged springs may no longer be capable of providin3 enough hold-down force to keep N-20 on the lower core plate during normal pober operation.
Ill. CONCLUSION
[\
Fuel assembly N-20 is acceptable for power operation in Cycle 2 of -s Surry Unit No. 2 as a result of the following:
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- 1. Ilold-down forces are adequate to prevent lift-off of the fuel assembly during normal power operation provided a pump overspeed in excess of 110 per cent has not occurred.
- 2. Operating procedures will be established to rack out the breaker of a reactor coolant pump in order to prohibit operating with more than two reactor coolant pumps unless the reactor coolant temperature is 360 degrees F or greater.
This will preclude fuel assembly lift-off during startup.
- 3. A design feature of the Surry Power Station prohibits the reactor coolant pumps from running at overspeed conditions.
This feature is an electrical interlock which disconnects the power to the, reactor coolant pumps from its own generator whenever the generator is not connected to the Vepco trans-mission system. (Where it ir synchronized to 60 liz by the
\
e, rid . )
s
,+ .
, -, In order to prove tha.t the interlock operates properly when needed, the speed of the reactor pumps and/or reactor coolant flow in all three loops will be recorded continuously during Cycle 2 operation. If the interlock fails to function properly and an overspeed in excess of 110 per cent of synchronous speqd occurs, the reactor will be shutdown and further evaluation
' "' condbeted before continuing operation, s -
s 1 The above conclusions have been reviewed by both Westinghouse and s, Vepco personrel (including Vepco's independent consultant) and are con-curred with by all parties. The results and recommendations have also been s
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i reviewed and concurred with by the Station and System Nucicar Safety and Operating Cocunittees. The refueling operation is proceeding, and the reactor will be returned to service on or about June 9, 1975, with the conditions described in items I through 3 above imposed.
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