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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO LER)
MONTHYEARML20132B3291996-12-0606 December 1996 Special Rept:On 961113,operator Discovered Control Switch for Diesel Output Breaker in pull-to-lock Position. Investigation Was Performed to Determine How Long Aac DG Was Inoperable BECO-86-173, Partially Withheld Security Event Rept:On 861107,HVAC Duct, Penetrating Vital Area,Removed by Contracted Craft Workers Before Notifying Security.Cause Not Stated.Security Oversight of Subj Contract Work Intensified1986-11-12012 November 1986 Partially Withheld Security Event Rept:On 861107,HVAC Duct, Penetrating Vital Area,Removed by Contracted Craft Workers Before Notifying Security.Cause Not Stated.Security Oversight of Subj Contract Work Intensified BECO-86-171, Partially Withheld Security Event Rept:On 861106,temporary Vital Area Barrier Insp Found Barrier Could Be Breached. Barrier Modified & Compensatory Security Measures Released1986-11-10010 November 1986 Partially Withheld Security Event Rept:On 861106,temporary Vital Area Barrier Insp Found Barrier Could Be Breached. Barrier Modified & Compensatory Security Measures Released ML20211E0731986-09-26026 September 1986 Unplanned Operating Event Rept 85-6, Manual Reactor Trip Following MSIV Closure Due to Inadvertent Emergency Feedwater Actuation,851009 BECO-86-125, Partially Withheld Security Event Rept:On 860826,bomb Threat Received.Search Initiated.No Suspicious Objects Found1986-08-29029 August 1986 Partially Withheld Security Event Rept:On 860826,bomb Threat Received.Search Initiated.No Suspicious Objects Found ML20238E4601986-08-28028 August 1986 Partially Withheld Secrity Event Rept:On 860824,bomb Threat Received for Plants.Bomb Search Initiated.No Suspicious Objects Found ML20211K8211986-06-18018 June 1986 Special Rept:On 860521,valid Failure Occurred on Div 2 Diesel Generator During Performance of Tech Spec Surveillance 4.8.1.1.2.Caused by Failure of Jacket Water Thermostatic Control Valve to Open ML20238E4591986-06-17017 June 1986 Partially Withheld Security Event Rept:On 860612,withheld Discovery Made Re 860604 Moderate Loss of Security Effectiveness.Caused by Inadequate Post Orders & Training for Assignment.Assignments Will Be Specifically Addressed 05000000/LER-1986-009, Ro:On 860312,discovered That LER 2-86-04 & LER 86-009 Not Submitted to Nrc.Caused by Misplaced Repts.Repts Telecopied to Nrc.Procedure for Distribution of Repts Revised1986-04-14014 April 1986 Ro:On 860312,discovered That LER 2-86-04 & LER 86-009 Not Submitted to Nrc.Caused by Misplaced Repts.Repts Telecopied to Nrc.Procedure for Distribution of Repts Revised BECO-86-016, Partially Withheld Security Event Rept:On 860215 Security Officer Appeared to Be Asleep at Post at Vital Area Penetration.Unathorized Entry of Vital Area Did Not Occurr. Security Officer Relieved of Duty & Suspended1986-02-20020 February 1986 Partially Withheld Security Event Rept:On 860215 Security Officer Appeared to Be Asleep at Post at Vital Area Penetration.Unathorized Entry of Vital Area Did Not Occurr. Security Officer Relieved of Duty & Suspended BECO-85-220, Partially Withheld Security Event Rept:On 851204 Vertical Pipe Chase Not Locked.Lock Removed When Surveys Indicated Radiation Level Below Requirement for Locked High Radiation Level.Pipe Chase Will Be Secured1985-12-0909 December 1985 Partially Withheld Security Event Rept:On 851204 Vertical Pipe Chase Not Locked.Lock Removed When Surveys Indicated Radiation Level Below Requirement for Locked High Radiation Level.Pipe Chase Will Be Secured ML20112F6841984-12-11011 December 1984 Special Rept SR-84-4:on 841015,process Vent High Range RM-GW-130-2 & Ventilation Vent High Range RM-VG-131-2 Effluent Monitors Inoperable.Cause Under Investigation. Alternate Methods of Monitoring Gaseous Effluents Confirmed AECM-84-0204, Special Rept 84-017/0:on 840304,Fire Doors 1A401 & OC219 Blocked Open to Support Maint Activities.Fire Watches Established Until Doors Restored1984-04-0606 April 1984 Special Rept 84-017/0:on 840304,Fire Doors 1A401 & OC219 Blocked Open to Support Maint Activities.Fire Watches Established Until Doors Restored ML20081B6171984-02-24024 February 1984 RO SPR-84-003:on 840206,following Trip from 100% Power, Specific Activity Sample of Reactor Coolant Showed Peak Dose Equivalent I-131 Limit of Less than or Equal to 1.0 Uci.Caused by Fuel Element Defects in Reactor Core ML20087B6181984-02-17017 February 1984 RO SPR-84-2:on 840118,specific Activity Sample of Reactor Coolant Showed Peak Dose Equivalent I-131 Level of 1.89 Uci,Exceeding Tech Spec Limit.Caused by Fuel Element Defects in Reactor Core.Dose Level Monitored ML20080N3391984-02-13013 February 1984 RO SPR-84-1:on 840106,specific Activity Sample of Reactor Coolant Showed Peak Dose Equivalent I-131 Level Exceeded Tech Spec Limits.Caused by Known Fuel Element Defects in Core.Tech Spec Requirements Implemented ML20198H3691983-11-14014 November 1983 Ro:On 831003,results of as-found Tests Indicated Crosby Main Steam Relief Valves Had Lift Points Exceeding Tech Spec Limits.Valves Disassembled & Rebuilt by Mfg ML20105D2431983-06-24024 June 1983 Special Rept:Five Individuals Found to Have Received Radiation in Excess of 10CFR20.101 Limits W/O Required Documentation.Caused by computer-based Sys Feature Allowing Use of Outdated Info & Personnel Error.Procedures Revised ML20137G4501981-03-24024 March 1981 Ro:During walk-through of Operator Training Program, O-ring Seal of Filter Holder Found Not Seated Properly Causing Partial Bypass of Filter for Air Sucked Into instrument.Filter-in Lock Adjusted ML20071F0861980-09-25025 September 1980 Ro:On 800912,sample Analysis Taken from Hydrazine Addition Tank Indicated Sodium Chloride in Tank.Anonymous Telcon Indicated Salt May Have Been Added Prior to Labor Strike by Unknown Persons ML20086D5141978-01-0606 January 1978 Telecopy Ro:On 780105,discovered That One of Two Nuclear Engineering Co Model B3-1 Shipping Casks Provided w/1-inch Diameter Lid Bolts Rather than 1-1/4 Inch Size Specified in Certificate of Compliance 6058 05000280/LER-1977-012, RO S1-77-01 Re Failures of Hydraulic Shock Supports (Snubbers).Extent of Failures Reported in LER 77-12.All Snubbers Operable on 771207 Startup1978-01-0505 January 1978 RO S1-77-01 Re Failures of Hydraulic Shock Supports (Snubbers).Extent of Failures Reported in LER 77-12.All Snubbers Operable on 771207 Startup ML20086D5201977-12-14014 December 1977 Telecopy Ro:Heating Steam Coil Leak in Reactor Bldg Ventilation Supply Unit V-AH-4A Resulted in Freezing of Condensate at Inlet to Unit & Subsequent Inoperability of Associated Secondary Containment Isolation Dampers ML20086D5371977-10-14014 October 1977 Telecopy Ro:Insp of Internal Torus Catwalk Support Structure Revealed That Catwalk Mitered Sections Not All Attached to Horizontal Catwalk Support Plates in Some Manner.Attachment Locations Will Be Upgraded ML20086D5501977-10-13013 October 1977 Telecopy Ro:On 771012,local Leak Rate Testing of MSIV AO-2-80A & Nitrogen Instrument Air Sys Isolation Valve CV-7436 Indicated That Leakage Exceeded Tech Spec Acceptance Criteria.Cause Under Investigation ML20086D5541977-10-0505 October 1977 Telecopy Ro:On 771004,local Leak Rate Testing of HPCI Sys Discharge Isolation Check Valve HPCI-9 Indicated That Leakage Exceeded Tech Spec Acceptance Criteria.Cause Under Investigation ML20086S0941977-09-30030 September 1977 RO S2-77-01, Missing Steam Generator Tube Plug-Hot Leg,Generator B,Row 1,Column 42 ML20086D5571977-09-29029 September 1977 Telecopy Ro:On 770929,local Leak Rate Testing of Core Spray Inboard Isolation Check Valve AO-14-13A Indicated That Leakage Exceeded Tech Spec Acceptance Criteria.Cause Under Investigation ML20086D5611977-09-14014 September 1977 Telecopy Ro:On 770913,local Leak Rate Testing of Core Spray Inboard Isolation Check Valve AO 14-13B Indicated That Leakage Exceeded Tech Spec Acceptance Criteria.Related Event on 770914 ML20086D5671977-09-12012 September 1977 Telecopy Ro:Main Steam Drain Isolation Valve MD 2373 & Main Steam Outboard Isolation Valve AO 2-86A Exceeded Tech Spec Acceptance Criteria for Local Leak Rate Tests ML20086D6421977-07-11011 July 1977 Telecopy Ro:On 770709,determined That Recombiner Sys a Offgas Flow Control Valve PCV 7489A Could Be Opened W/ Controlling Solenoid Valve Deenergized.Valve Held from Svc Pending Investigation ML20137G4461977-06-23023 June 1977 Ro:On 770621,radioactive Source Containing 200 Mci Cs-137 Recovered from Brine Well 33.Incident Described in ML20086F0801977-06-0606 June 1977 Ro:On 770506,plant Iodine & Particulate Release Rate Exceeded 4% of Facility Tech Spec Averaged Over Second Calendar Quarter of 1977.Caused by Fuel Perforations Coupled W/End of Cycle Testing & Reactor Coolant & Steam Leaks ML20086D6911977-03-0202 March 1977 Telecopy Ro:On 770301,torus Water Vol Found to Be Slightly Below Min Vol Established by Tech Specs.Water Vol Restored to Normal Operating Level ML20086D7031977-02-24024 February 1977 Telecopy Ro:On 770223,while Withdrawing in-sequence Control Rod to Bring Reactor Critical,Reactor Period of Less than 5 Obtained ML20086F4181976-12-0909 December 1976 RO Re Plant Iodine & Particulate Release Rate Exceeding 4% of Tech Spec 3.8.C.2 Averaged Over Fourth Calendar Quarter 1976.Caused by Leaks in Reactor Water Cleanup Sys.Leaks Repaired & Equipment Modified to Reduce Leakage ML20070J8681976-10-20020 October 1976 RO 76-13:on 760916,normal Boric Acid Makeup to Vol Control Tank Could Not Be Accomplished Due to Plugging of Chemical & Vol Control Sys Line 1-inch-CH-56-152.Cause Unknown.Line Will Be Inspected for Indications of Solidification ML20070J8581976-10-0101 October 1976 RO 76-12:on 760909,low Pressure Alarm Occurred on Safety Injection Accumulator C,Resulting in Pressure Reduction. Caused by Partially Open HCV 1936 & Body to Bonnet Leaks on HCV 1898 & 1549.Valves Repaired & Accumulator Repressurized ML20070J8961976-09-29029 September 1976 RO 76-05:on 760915,pressurizer Level Fell Below 45% Level Setpoint,Resulting in Decreases of Pressurizer Pressure & Vol Control Tank Level.Caused by Leaking Tube in Steam Generator A.Cause of Tube Failure Will Be Evaluated ML20070J8801976-09-24024 September 1976 RO 76-07:on 760913,monthly Average of Gaseous & Airborne Particulate Wastes for Previous 12 Months Found Greater than Tech Spec Limit.Caused by Interpretational Changes in Tech Spec Section 3.11.B.New Limit Approved ML20086D7881976-09-10010 September 1976 Telecopy Ro:On 760909,discovered That Torus Water Vol Several Hundred Cubic Ft Below 68,000 Cubic Ft Min Required by Tech Specs.Caused by Failure to Correct for Vol Vs Level Correlation ML20086S5511976-08-17017 August 1976 SR-S2-76-01 Re Summary of Analysis & Interpretation of Type A,B & C Containment Leak Rate Test Results Obtained During Refueling Outage.No Evidence of Structural Deterioration Found ML20086Q2551976-07-0101 July 1976 Supplemental Rept to SR-S1-75-08 on Containment Leak Rate Testing Including Errors Inherent in Correlating Type a Leakage Test W/Type B & C Tests & Instrument Error Analysis ML20086S7011976-05-0707 May 1976 Suppl 1 to USRE-S1-76-01:751204,no Air Flow Indicated from Local Flow Indicator on Containment Gaseous & Particulate Monitor Cabinet.Caused by Failed Bearing on Vacuum Pump. Bearing Replaced & Pump Tested Satisfactorily ML20086D8231976-05-0505 May 1976 Telecopy Ro:On 760504,during Routine Surveillance Test, Primary Containment Oxygen Concentration Found to Be in Excess of Tech Spec Limit.Caused by Leakage from Drywell Instrument Air Sys Into Containment Nitrogen Supply Line ML20086S5911976-04-0101 April 1976 Ro:On 760322 & 23,temp Difference Across Station Exceeded 15 F.Caused by Rapid Drop in River Water Ambient Temp Making Prediction When Action Necessary to Avoid Temp Increase Difficult ML20086S6981976-02-0404 February 1976 Telecopy Ro:On 760204,main Steam Trip Valve TV-MS-201A Failed to Close When Operated from Control Room.Cause Under Investigation ML20086S7091976-02-0303 February 1976 USRE-S1-76-01:on 751204,no Air Flow Indication Found from Local Flow Indicator on Containment Gaseous & Particulate Monitor Cabinet.Caused by Failed Bearing on Vacuum Pump. Bearing Replaced & Pump Tested Satisfactorily ML20086F4701976-01-27027 January 1976 Ro:On 760117,gaseous Activity Release Rate Exceeded 4% of Tech Spec 3.8.C.1 for More than 48 H.Caused by Increase in Offgas Activity Due to Fuel Cladding Perforations ML20137H3841976-01-12012 January 1976 Ro:On 760106,operator Left Console Key in Switch So That Reactor Not Secured Per Tech Specs.Key Withdrawn from Console.Incident Discussed W/Operators & Large Red Plastic Tag Attached to Key to Make It More Visible 1996-12-06
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML18152A2811999-10-12012 October 1999 Technical Basis for Elimination of Nozzle Inner Radius Insps (for Nozzles Other than Reactor Vessel),Technical Basis for ASME Section XI Code Case N-619. ML18152B3531999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Surry Power Station,Units 1 & 2.With 991012 Ltr ML18152B6651999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Surry Power Station Units 1 & 2.With 990915 Ltr ML18152B4421999-08-27027 August 1999 LER 99-006-00:on 990802,determined That Plant Was Outside of App R Design Basis Due to Fire Barrier Deficiencies. Caused by Original Plant Design Deficiencies.Fire Watches Were Established & Mods Have Been Completed.With 990827 Ltr ML18152B4411999-08-27027 August 1999 LER 99-005-00:on 990731,effluent Radiation Monitors Were Declared Inoperable.Caused by Degraded Heat Trace Circuits for Monitors Sample Suction Line.Degraded Heat Trace Circuit Was Replaced & Addl Heat Trace Is Being Installed ML18151A3981999-08-13013 August 1999 SPS Unit 2 ISI Summary Rept for 1999 Refueling Outage. ML18152B3771999-08-13013 August 1999 LER 99-004-00:on 990714,TS Violation Due to non-safety Related Fans Effect on CR Boundary Was Noted.Cause of Event Has Not Yet Been Determined.Cable Spreading Room Doors Were Operned to Reduce Pressure in Rooms ML18152B3791999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Surry Power Station,Units 1 & 2.With 990811 Ltr ML18152B3911999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Surry Power Station,Units 1 & 2.With 990713 Ltr ML20195E2401999-05-31031 May 1999 Rev 2 to COLR for SPS Unit 2 Cycle 16 Pattern Ag ML18152B4341999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Surry Power Station,Units 1 & 2.With 990614 Ltr ML18152B4181999-05-18018 May 1999 LER 99-002-00:on 990425,MSSVs Tested Out of Tolerance for as Found Setpoint.Caused by Minor Setpoint Drift.No Immediate Action Required.Deviation Rept Submitted for Each Valve.With 990518 Ltr ML18152B4161999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Surry Power Station Units 1 & 2.With 990512 Ltr ML18152B4111999-04-28028 April 1999 LER 99-003-00:on 990331,potential Loss of Charging Pumps Was Noted.Caused by Main CR Fire.Station Deviation Was Issued on 990331.With 990428 Ltr ML18152B6511999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Surry Power Station Units 1 & 2 ML18153A2741999-03-29029 March 1999 LER 99-002-00:on 990301,prematurely Released Fire Watches Resulted in Violation of TS 3.21.B.7.Caused by Inadequate Procedure.Procedure for Opening & Sealing Fire Stops Was Revised on 990212 ML18153A2681999-03-19019 March 1999 LER 98-013-01:on 981122,turbine/reactor Tripped on High Due to Short Circuit in Summator for MSL C Loop Channel III Flow Transmitter.Replaced 1-MS-FT1494 Summator & Module Repair Procedure Revised.With 9903190 Ltr ML18152B7331999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Surry Power Station,Units 1 & 2.With 990310 Ltr ML18152B5421999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for Surry Power Station,Units 1 & 2.With 990210 Ltr ML18151A3031999-01-29029 January 1999 ISI Summary Rept for 1998 Refueling Outage,Including Form NIS-1, Owners Rept for ISIs & Form NIS-2, Owners Rept for Repairs & Replacements. ML18152B7261999-01-21021 January 1999 LER 99-001-00:on 981222,auxiliary Feedwater Pipe Support Missed Surveillance.Caused by Personnel Error.Station Deviation Rept Was Submitted.Two Supports in Question Received Required Code Insp & Were Found Acceptable ML18152B6011998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Surry Power Station,Units 1 & 2.With 990115 Ltr ML18152B5811998-12-16016 December 1998 LER 98-013-00:on 981122,turbine/reactor Trip on High SG Level Occurred.Caused by Instrument Failure.Control Room Operators Placed Unit in Safe,Shutdown Condition ML18152B5781998-12-16016 December 1998 LER 98-014-00:on 981126,manual Reactor Trip in Response to Main Feedwater Regulating Valve Failure Occurred.Caused by Dislocation of Retaining Clip in Positioner.Control Room Operators Placed Unit in Safe,Shutdown Condition ML18152B7121998-12-0404 December 1998 LER 98-S01-00:on 981105,noted Failure to Deactivate Station Access Badge.Caused by Human Error.Licensee Will Now Deactivate Station Badges Before Clearance Is Revoked & Process for Badge Deactivations Have Been Strengthened ML18152B7041998-12-0101 December 1998 LER 98-012-00:on 981102,noted That EDGs Were Concurrently Inoperable.Caused by Required Testing Per TS 3.16.B.1.a.2. Redundant EDG Was Returned to Svc within Two Hour Period, Following Satisfactory Testing.With 981201 Ltr ML18152B5721998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Surry Power Station,Units 1 & 2.With 981214 Ltr ML18152B7081998-11-30030 November 1998 Rev 0 to COLR for Surry 1 Cycle 16,Pattern Un. ML18152B6161998-11-0606 November 1998 LER 98-011-00:on 981008,diesel Driven Fire Pump Failed to Start During Performance of Monthly Operability Test.Caused by Faulty Overspeed Trip Device Failure.Diesel Driven Fire Pump Declared Inoperable ML18152B6241998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Surry Power Station Units 1 & 2.With 981111 Ltr ML18152B6081998-10-23023 October 1998 LER 98-010-01:on 980715,intake Canal Level Probes Were Inoperable Due to Marine Growth.Caused by Design of Canal Level Instrumentation.Canal Level Probes Will Continue to Be Monitored More Closely ML18152B6881998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Surry Power Station Units 1 & 2.With 981012 Ltr ML18153A3271998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Surry Power Station,Units 1 & 2 ML18152B7811998-07-31031 July 1998 LER 98-010-00:on 980715,low Intake Canal Level Instrument Channel I Was Declared Inoperable to Allow Testing of Intake Canal Level Probe 1-CW-LE-102.Subject Probe Was Cleaned by Diver,Tested & Channel I Was Returned to Operable Status ML18153A3161998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Surry Power Station Units 1 & 2.W/980807 Ltr ML18152B7621998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Surry Power Station,Units 1 & 2.W/980707 Ltr ML18153A2581998-06-0303 June 1998 LER 98-009-00:on 980509,nonisolable Leak of Reactor Coolant Pump Seal Injection Line Weld,Was Discovered.Caused by Lack of Fusion or Thermal Fatigue Coupled W/Vibration Stress Due to Loose Rod Hanger.Rcp Seal Injection Line Removed ML18153A3141998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Surry Power Station,Units 1 & 2.W/980610 ML20248F7441998-05-31031 May 1998 Reactor Vessel Working Group,Response to RAI Regarding Reactor Pressure Vessel Integrity ML18152B8241998-05-22022 May 1998 LER 98-008-00:on 980228,auxiliary Ventilation Fans Were Noted in Condition Outside of Design Basis.Caused by Failure to Recognize Potential Impact of Certain Design Basis Accident Scenarios.No Corrective Actions Needed ML18152B8161998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Surry Power Station Units 1 & 2.W/980508 Ltr ML18152B7951998-04-29029 April 1998 LER 98-007-00:on 980330,radiation Monitors Were Declared Inoperable.Caused by Change in Operating Temperature Range. Preplanned Alternate Method of Monitoring Was Initiated IAW TS Table 3.7-6 ML18153A2511998-04-22022 April 1998 LER 98-006-00:on 980324,unisolable Through Wall Leak of RCP Thermowell Was Noted.Cause of Leak Is Unknown.Rtd Will Be Replaced ML18153A2521998-04-22022 April 1998 LER 98-005-01:on 980212,fire Watch Insp Exceeded One Hour. Caused by Lack of Attention to Detail by Individual Involved.Individual Involved Was Coached on Requirement to Perform Fire Watch Patrols within Required Time Frame ML20217P9941998-04-0707 April 1998 Safety Evaluation Granting Licensee Third 10-yr Inservice Insp Program Relief Requests SR-018 - Sr-024 ML18153A2951998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Sps,Units 1 & 2.W/ 980408 Ltr ML18153A2391998-03-13013 March 1998 LER 98-005-00:on 980212,fire Watch Insp Frequency Exceeded One H Occurred.Category 2 Root Cause Evaluation Being Conducted to Determine Cause of Event.Station Deviation Issued ML18153A2341998-03-0909 March 1998 LER 98-003-00:on 980226,no Procedural Guidance for Maintaining EDG Minimum Fuel Supply During Loop,Was Identified.Caused by Absence of Procedural Instructions. Deviation Rept Submitted to Document Deviating Condition ML18153A2301998-03-0606 March 1998 LER 98-004-00:on 980206,fire Watch Was Released Prematurely Resulting in Violation of Ts.Caused by Inadequate Planning of Repair Activity.Work Orders Will Include Ref to Applicable Procedures Developed to Assist in Repairs ML18153A2251998-03-0404 March 1998 LER 98-002-00:on 980202,automatic Turbine Trip Resulted in Automatic Reactor Trip.Caused Degraded Generator Voltage Regulator sub-component Failure.Placed Plant in Safe Hot SD & Replaced Intermittent Relay & Relay Socket 1999-09-30
[Table view] |
Text
VIRGINIA EI.ECTRIC AND Pow .. CO31PANY
. . Ric113t OND .VI Ro r x1 A C3GC1 October 20, 1976 Mr. Norman C. Moseley, Director Serial No. 292 Office of Inspection and Enforcement P0&M/ALH:clw U.S. Nuclear Regulatory Cocsission Region II - Suite 818 Docket Fo. 50-280 230 Peachtree Street, Northwest License No. DPR-32 Atlanta, Georgia 30303
Dear Mr. Moseley:
Pursuant to Surry Power Station Technical Specification 6.6.B.2, the Virginia Electric and Power Company hereby submits a copy of Licensee Event Report USRE-SI-76-13.
The substance of this report has been reviewed by the Station Nuclear Safety and Operating Co=:nittee and will be placed on the agenda for the next meeting of the System Nuclear Safety and Operating Co=mittee.
Very truly yours, C. M. Stallings {
Vice President-Power upply (
and Production Operations Enclosure cc: Mr. Robert W. Reid, Chief Operating Reactors Branch 4 (40 copies USRE-S1-76-13) l l
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/6 8212290075 821130 7 .
" G. ("
PDR FOIA SCHLIsss2-534 PDR l
--....------...t i e t i t f-1 8 (PLEASE PRINT ALL LEQUIRED INF%3
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~ N ME LCENSE NUMBER Q j vl Al SlP lS l t l l0l0l~l0l0l0l0l0l-l0l0l 7 89 14 15 25 l4 26 l1 l1l1l0l l0l3l ,1 30 31 32 CATEGORY pf N E 00CxET NUMBER 01 CGN'T l p l ol 7 8 57 58 M59 60 61 EVENT DATE l 0l 5l 0l-l 0l 2l 8l 0 l l 0l 9l Il 6l 7l 6l [ t l 0REPORT l 1l DAK 5ll 68 69 - 74 75 EVENT DESCRIPTION o2 7 ,8 9 lDuring normal operations, it was discovered that normal boric acid cakeup to the vs 03 7 89 l control tank could not be accomplished due to an apparent plugging of CVCS line 1"c
@ ]56-152. In order to clear the line, recirculation between the boric acid tanks anj 7 8
@9l boron injection tank was secured for five (5) minutes to permit installation of a 7 89 RE l blank flange in the line.
7 89 Since Technical Specification 3.2.C.6 requires con- (cos coy $oE COMPONENT CODE
@ lP l Cl lF l lX lX lX l Xl Xl Xl ]43 VoLAToM 7 89 10 11 12 17 lz l9 l9 l9 l 44 47 W48 CAUSE DESCRIPTION 0
7 89 l Boric acid is transferred through line 1"-CH-56-152 on a regular basis for volume G 09 ltroltankmake-up. This routine usage, coupled with the fact that no malfunctionia 7 89
' 10 l heat tracing was found either in the pipe in question or any upctream pipe (con't) 7 89 FACUTY STATUS % POWEA METHOD OF
7 8 1
9 W 10 l_1_ l 0 l 0 l l N/A l OtSCOVERY
@ l' N/A OtSCoVERY CESCRIPTON 12 13 44 45 48 ACTMTV CCATENT RELEASED AMOUNT OF ACTMTY 12 l,z,jRELEASE l N/A 7 8 9 l_z_,l OF l l N/A LOCATCN OF RELEASE 10 11 44 45 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION Q l0l0l0l Wl 7 89 11 12 13 N/A PERSONNEL INJURIES NUMBER CESCRtPTON
@ l0l0l0l 7 89 l N/A 11 12 OFFSITE CONSEQUENCES DE l N/A -
7 89 LOSS OR DAMAGE TO FAC1UTY '
TYPE
@W 7 89 10 lDESCPSTON N/A PUBUCITY Ql 7 89 N/A ADQtTIONAL FACTORS 18 l Since the capabilities of the safety injection system were not impaired by this eveg 7 89 Q l the health and safety of the general public were not affected.
7 89 NAME: Tyndall L. Baucon PHONE, (804) 337-3184 p %
.* EVENT DESCRI~ ' ION (c::n't) tinuous recirculation, an immediate reactor rampdown was initiated until boron injection tank recirculation was returned to normal. Once the line was cleared of the obstruction, boron recirculation was again secured while the blank flangG was removed. A reactor rampdown was performed during this operation which lastG for approximately three (3) minutes. (USRE-S1-76-13)
CAUSE DESCRIPTION (con't) leaves the cause of the obstruction as an unknown factor. The line was inspectG for potential " cold" spots which could cause isolated solidification of boric acid, but none were found in the area of the obstruction. The line will be in-spected for indications of solidification during the next refueling shutdown.
, During the period of obstruction, the capability to add boric acid to the reactor coolant system was maintained. In addition, the boron injection tank was capable of performing its intended function.
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Distribution Code PDR COORDINATOR ONLY Report sent to HQs and hold copies reproduced Date l 1
Initials j ...._..._____........._..____....____....__................____.......__..____
Incoming Licensee Correspondence
- 1. Licensee Response to Non-Enforcement Report
- 2. Licensee Response to Enforcement Report
- 3. Licensee Response to IE Bulletins 4 General Licensee Correspondence Licensee Event Reports
- a. Licensee / Facility //((M IMa /
- b. Report No. A d d o dM3
- c. Document Date /d M O M d. Date Received /d 'M-7d
- e. Section Chief f. Principal Inspector J 9
- g. Document transferred to Branch l Date Initials j
- h. Licensee Response to Enforcetsnt Report Only l
Acceptable Not-Acceptable Initials 3 , h 2.790 Information YES NO X Initials kib NorE: If Yes, mark necessary documents to delete 2.790 Information and return with this form along with acknowledgement letter F to the PDR Coordinator.
Should the attached and related correspondence be placed in the PDR7 YES Y~ NO Initials I
l', PDR COPRDINATOR ONLY i Incoming Licensee Correspondence and related documents sent to HQs and PDR. /7 Date /!" Initiala d. -
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Vircinia Electric and Pover Co.mpany Eochet No. 50-280 Surry Unit 1 License No. DPR-32 REPORTABLE OCCURRENCE REPORT 30:
Ro-280/76-07 DISTRIBUTION:
Don Lanham, ADM cc With Fnclosures
! Region II Docket Files 280 Rettion II Inspector with enclosures i
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Farue AIC.31e (Erv. 9 53) AsCM 0240
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Form TE-1/76 (6/76) W Inspection / Investigation neports Only Distribution Code PDR COORDINATOR O';LY .
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Report sent to HQs and hold copics reproduced Date_
Initials Incoming Licensee Correspondence
- 1. Licensee Response to Non-Enforcement Report
- 2. Licensee Response to Enforcement Report
- 3. Licensee Response to IE Eulletins
- 4. General Licensee Correspondence h Licensee Event Reports
- a. Licensce/ Facility l Y [ d C Mut./ u /
- b. Report No. OM8 7[-O [
- c. Document Date [t?h M d. Date Received h id7'7 ~7 [
- e. Section Chief M442, f. Principal Inspector M/<
- g. Document transferred to Branch Date Initials
- h. Licensea Response to Enforcement Report Only Accepteble Not-Teceptable Initials 2.790 Information YES NO / ~
Initials kNb NOTE: If Yes, mark necessary documents to delete 2.790 Information and return with this form along with acknowledgement letter to the PDR Coordinator.
h Should the attached and related correspondence be placed in the PDR?
YES NO Initials fh.
PDR COORDINATOR CNLY Incoming Licensee Correspondence and related documents sent to HQs and PDR.
Date [ [' Initials ' //
f
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