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Category:LICENSEE EVENT REPORT (SEE ALSO AO RO)
MONTHYEAR05000324/LER-1992-001, Supplemental LER 92-001-01:on 920202,unit Scrammed During Main Turbine Control Valve Testing.Caused by Excessive Cycling of Turbine Control Valves.Hydraulic Accumulators a & B Disassembled1993-09-0202 September 1993 Supplemental LER 92-001-01:on 920202,unit Scrammed During Main Turbine Control Valve Testing.Caused by Excessive Cycling of Turbine Control Valves.Hydraulic Accumulators a & B Disassembled 05000324/LER-1993-0081993-08-13013 August 1993 LER 93-008-00:on 930714,core Rated Thermal Power Exceeded Allowable Amount Due to Feedwater Flow Inaccuracy.Cause Believed to Be Due to Erosion/Corrosion of FW Flow Elements. FW Instrumentation recalibr.W/930812 Ltr 05000324/LER-1992-0101993-08-12012 August 1993 LER 92-010-01:on 921207,penetration Leakage Exceeded TS Allowable Limit Due to actuator-to-valve Alignment & disk-to-seat Alignment Problems.Line Bored Valve to Achieve concentricity.W/930812 Ltr 05000324/LER-1991-0191993-08-12012 August 1993 LER 91-019-01:on 911112,LLRT Failure of Two MSL Inboard & Outboard Isolation Valves Resulted in Condition Outside Design Basis.Root Cause Analysis in Process.Msls C & D Inboard & Outboard MSIVs Repairs complete.W/930812 Ltr 05000324/LER-1993-0031993-05-10010 May 1993 LER 93-003-00:on 930408,identified That Drywell Spray Outboard Isolation Valve Installed in Reverse Direction. Caused by Design & Installation Error.Appropriate Documents Will Be revised.W/930507 Ltr 05000324/LER-1988-0011990-08-0101 August 1990 LER 88-001-07:on 880102,manual Reactor Scram Occurred Due to Decreasing Main Condenser Vacuum.Reactor Power at 55% & Vacuum Decreased to 22 Inches Mercury.Caused by Leaks on Main Turbine Piping.Piping repaired.W/900801 Ltr 05000324/LER-1983-019, Updated LER 83-019/01T-2:on 830210,instrument Air Tubing to Safety Relief Valve/Automatic Depressurization Sys Valve Accumulator Inadequately Supported.Caused by Rerouted Tubing.Supports Installed1984-07-12012 July 1984 Updated LER 83-019/01T-2:on 830210,instrument Air Tubing to Safety Relief Valve/Automatic Depressurization Sys Valve Accumulator Inadequately Supported.Caused by Rerouted Tubing.Supports Installed 05000325/LER-1982-108, Updated LER 82-108/03L-1:on 821010 & 14,while Performing Automatic Depressurization Sys Valve Operability Test,Valves 1-B21-F013J & 1-B21-F013D & E Failed to Reclose.Caused by Faulty Spring.Valves Replaced1984-05-18018 May 1984 Updated LER 82-108/03L-1:on 821010 & 14,while Performing Automatic Depressurization Sys Valve Operability Test,Valves 1-B21-F013J & 1-B21-F013D & E Failed to Reclose.Caused by Faulty Spring.Valves Replaced 05000325/LER-1982-122, Supplemental LER 82-122/03L-1:on 821030 & 1104,reactor Recirculation Pump 1A Tripped.On 821101 & 04,reactor Recirculation Pump 1B Tripped.Caused by Spurious Action of ATWS Instrument B21-PS-N045C1984-04-0909 April 1984 Supplemental LER 82-122/03L-1:on 821030 & 1104,reactor Recirculation Pump 1A Tripped.On 821101 & 04,reactor Recirculation Pump 1B Tripped.Caused by Spurious Action of ATWS Instrument B21-PS-N045C 05000325/LER-1981-053, Updated LER 81-053/03L-1:on 810922,during Reactor Startup, Reactor Recirculation Pump 1B Tripped.Caused by Spurious Trip Signal from ATWS Low Water Level Instrument B21-LTM- NO24B-2.Instrument replaced.W/840329 Ltr1984-03-29029 March 1984 Updated LER 81-053/03L-1:on 810922,during Reactor Startup, Reactor Recirculation Pump 1B Tripped.Caused by Spurious Trip Signal from ATWS Low Water Level Instrument B21-LTM- NO24B-2.Instrument replaced.W/840329 Ltr 05000325/LER-1981-055, Updated LER 81-055/03L-1:on 820622,drywell Equipment Drain Flow Integrator 1-G16-FQ-K603 Continuously Indicated Dwed Sump Flow W/No Pumps Running.Caused by Water Being Introduced Into Pneumatic calibrator.W/840328 Ltr1984-03-28028 March 1984 Updated LER 81-055/03L-1:on 820622,drywell Equipment Drain Flow Integrator 1-G16-FQ-K603 Continuously Indicated Dwed Sump Flow W/No Pumps Running.Caused by Water Being Introduced Into Pneumatic calibrator.W/840328 Ltr 05000325/LER-1983-063, Updated LER 83-063/03L-1:on 831203,reactor Water Cleanup Sys (Rwcs) Differential Flow Indicator 1-G31-R615 Showed Erroneous Indication.On 831207,spurious Rwcs Alarm Annunciated.Caused by Air in Sensing lines.W/840222 Ltr1984-02-22022 February 1984 Updated LER 83-063/03L-1:on 831203,reactor Water Cleanup Sys (Rwcs) Differential Flow Indicator 1-G31-R615 Showed Erroneous Indication.On 831207,spurious Rwcs Alarm Annunciated.Caused by Air in Sensing lines.W/840222 Ltr 05000325/LER-1983-057, Updated LER 83-057/03L-1:on 831119,during Unit Power Performance,Temp Recorder TR-1258 Printed Erratically.Caused by Dirty Electrical Contacts in Control Board Timing Relay. Contacts Cleaned & Returned to svc.W/840222 Ltr1984-02-22022 February 1984 Updated LER 83-057/03L-1:on 831119,during Unit Power Performance,Temp Recorder TR-1258 Printed Erratically.Caused by Dirty Electrical Contacts in Control Board Timing Relay. Contacts Cleaned & Returned to svc.W/840222 Ltr 05000324/LER-1983-097, Updated LER 83-097/01T-1:on 831212,during Testing,Per IE Bulletin 83-02,crack Indications Discovered in 19 of 131 Welds in Reactor Recirculation & Reactor Water Cleanup Sys. Caused by Stress Corrosion Cracking1984-01-24024 January 1984 Updated LER 83-097/01T-1:on 831212,during Testing,Per IE Bulletin 83-02,crack Indications Discovered in 19 of 131 Welds in Reactor Recirculation & Reactor Water Cleanup Sys. Caused by Stress Corrosion Cracking 05000325/LER-1983-045, Updated LER 83-045/03L-2:on 830919 & 24,inboard PCIV Steam Supply Valve ES1-F007 to RCIC Sys Would Not Completely Reopen.Caused by Loose Limitorque Motor Operator Spring Pack1984-01-24024 January 1984 Updated LER 83-045/03L-2:on 830919 & 24,inboard PCIV Steam Supply Valve ES1-F007 to RCIC Sys Would Not Completely Reopen.Caused by Loose Limitorque Motor Operator Spring Pack 05000324/LER-1982-024, Updated LER 82-024/01T-1:on 820205,determined That Control Bldg Emergency Ventilation Sys Trains Will Not Isolate Upon Receipt of Chlorine Isolation Signal If Control Switch in on Position Due to Design Deficiency1983-11-14014 November 1983 Updated LER 82-024/01T-1:on 820205,determined That Control Bldg Emergency Ventilation Sys Trains Will Not Isolate Upon Receipt of Chlorine Isolation Signal If Control Switch in on Position Due to Design Deficiency 05000324/LER-1983-083, Updated LER 83-083/01T-1:on 830905,supply Valve 2-FP-V39 to Deluge Sys of Both Standby Gas Treatment Sys Discovered Shut.Caused by Operator Error.Valves Tagged for Identification.Auxiliary Operator Disciplined1983-09-23023 September 1983 Updated LER 83-083/01T-1:on 830905,supply Valve 2-FP-V39 to Deluge Sys of Both Standby Gas Treatment Sys Discovered Shut.Caused by Operator Error.Valves Tagged for Identification.Auxiliary Operator Disciplined 05000325/LER-1983-034, Updated LER 83-034/01T-1:on 830811,following Extended Maint & Refueling Outage,Instrument Isolation Valves to 1CAC-PDS-4222 & 4223 Discovered Closed.Caused by Cancelation of Equipment Clearance.Valves Reopened1983-09-12012 September 1983 Updated LER 83-034/01T-1:on 830811,following Extended Maint & Refueling Outage,Instrument Isolation Valves to 1CAC-PDS-4222 & 4223 Discovered Closed.Caused by Cancelation of Equipment Clearance.Valves Reopened 05000325/LER-1983-017, Updated LER 83-017/03L-1:on 830326-28 & 0402,listed Control Rods Had No Indications for Identified Positions.Caused by Loose Prototypic Inlet Piping Connectors Due to Undervessel Work.Connectors Will Be Properly Fastened1983-07-19019 July 1983 Updated LER 83-017/03L-1:on 830326-28 & 0402,listed Control Rods Had No Indications for Identified Positions.Caused by Loose Prototypic Inlet Piping Connectors Due to Undervessel Work.Connectors Will Be Properly Fastened 05000324/LER-1982-131, Supplemental LER 82-131/03L-1:on 821206,one-half Automatic Reactor Scram Signal Received Due to Instrument Downscale Signal from Main Steam Line Radiation Monitor D, 2-D12-RM-K603D.Caused by Disconnection of Instrument Cable1983-03-11011 March 1983 Supplemental LER 82-131/03L-1:on 821206,one-half Automatic Reactor Scram Signal Received Due to Instrument Downscale Signal from Main Steam Line Radiation Monitor D, 2-D12-RM-K603D.Caused by Disconnection of Instrument Cable 05000324/LER-1981-090, Updated LER 81-090/03L-3:on 810817 & 23,suppression Chamber Water Level Indicator 2-CAC-LI-2601-3 Indicated Lower Level & on 810820,indicated Higher Level than Other Indicator.Caused by Changes in Trickle Flow to Wet Ref Leg1983-01-28028 January 1983 Updated LER 81-090/03L-3:on 810817 & 23,suppression Chamber Water Level Indicator 2-CAC-LI-2601-3 Indicated Lower Level & on 810820,indicated Higher Level than Other Indicator.Caused by Changes in Trickle Flow to Wet Ref Leg 05000325/LER-1982-127, Updated LER 82-127/01T-1:on 821103,quick Start Testing of Diesel Generators 2,3 & 4 Not Performed for 12 H Period Per Tech Spec.Caused by Failure to Enter Requirement Into Daily Surveillance Rept on 821102.Testing Performed1982-12-23023 December 1982 Updated LER 82-127/01T-1:on 821103,quick Start Testing of Diesel Generators 2,3 & 4 Not Performed for 12 H Period Per Tech Spec.Caused by Failure to Enter Requirement Into Daily Surveillance Rept on 821102.Testing Performed 05000325/LER-1982-135, Supplemental LER 82-135/03L-1:on 821019,1.5-inch Discrepancy Noted Between Narrow & Wide Range Instruments.Caused by Inoperable RTGB Level Instruments.Plant Mod Package Developed to Increase Accuracy1982-12-23023 December 1982 Supplemental LER 82-135/03L-1:on 821019,1.5-inch Discrepancy Noted Between Narrow & Wide Range Instruments.Caused by Inoperable RTGB Level Instruments.Plant Mod Package Developed to Increase Accuracy 05000325/LER-1982-024, Supplemental LER 82-024/03L-2:on 820214,during Periodic Test,Discovered That Open Position Indication for Drywell to Suppression Vacuum Breaker X18H Could Not Be Achieved.Caused by Failure of Vacuum Breaker to Fully Stroke Open1982-10-13013 October 1982 Supplemental LER 82-024/03L-2:on 820214,during Periodic Test,Discovered That Open Position Indication for Drywell to Suppression Vacuum Breaker X18H Could Not Be Achieved.Caused by Failure of Vacuum Breaker to Fully Stroke Open ML20054L9761982-06-29029 June 1982 LER82-054/03L-0:on 820607,reactor Core Isolation Cooling Sys Turbine Automatically Started on Reactor Low Level,But Tripped Due to Closure of Control Valve 1-E51-V9.Caused by Lack of Turbine Speed Demand Signal Due to Governor Failure 05000325/LER-1982-0531982-06-29029 June 1982 LER 82-053/03L-0:on 820604,during startup,09 Position Found Superimposed on 00 RTGB Position Indication for Fully Inserted Control Rod 10-07.Caused by Defective Rod Position Reed Switch.Investigation Scheduled for 1982 Outage 05000325/LER-1981-092, Updated LER 81-092/01T-2:on 811226,action Statement 3.3.2b Not Entered When B21-LT-N017D-1 Instrument Failed Upscale. Caused by Failure of Operations Personnel to Recognize & Perform Required Action1982-06-21021 June 1982 Updated LER 81-092/01T-2:on 811226,action Statement 3.3.2b Not Entered When B21-LT-N017D-1 Instrument Failed Upscale. Caused by Failure of Operations Personnel to Recognize & Perform Required Action 05000325/LER-1981-093, Updated LER 81-093/01T-2:on 811226,reactor Protection Sys Vessel Low Level Trip instrument,1-B21-LT-NO17D-1,was Indicating Upscale.Caused by Personnel Failure to Recognize & Perform Tech Specs.Personnel Counseled1982-06-18018 June 1982 Updated LER 81-093/01T-2:on 811226,reactor Protection Sys Vessel Low Level Trip instrument,1-B21-LT-NO17D-1,was Indicating Upscale.Caused by Personnel Failure to Recognize & Perform Tech Specs.Personnel Counseled 05000325/LER-1982-038, Updated LER 82-038/03L-1:on 820419.Reactor Scrammed When Electrical Bus 1A-1 Dc de-energized.Caused by Operator Error in Opening 125-volt Dc Battery Charger Output Breaker for Battery 1A-1.Breaker Closed & Power Restored to Bus1982-06-0404 June 1982 Updated LER 82-038/03L-1:on 820419.Reactor Scrammed When Electrical Bus 1A-1 Dc de-energized.Caused by Operator Error in Opening 125-volt Dc Battery Charger Output Breaker for Battery 1A-1.Breaker Closed & Power Restored to Bus ML20062G3081978-12-21021 December 1978 /03L-0 on 781122:HPCI & RCIC Component Tests Were Overlooked Because Rescheduling Technique Provided No Clear Indication of Test Due Dates.Responsible Technician Reinstructed & Admin Operating Instruction AOI-5 Rev ML20064H8961978-12-19019 December 1978 /03L-0 on 781120:Senior Control Operator Did Not Have Completed Hatch Leak Rate Test Before Beginning Reactor Startup Due to Misunderstanding.Test completed.GP-1 Revised to Require Leak Test Verification by Control Operators ML20064H6181978-12-14014 December 1978 /03L-0 on 781114:torus Level of the HPCI Turbine Control Sys Was Slightly Above the Allowed 27 Inches.Proper Torus Level Restored to Normal.Torus Level Indicator Will Be More Clearly Marked ML20064H5971978-12-14014 December 1978 /03L-0 on 781114:Fire Hoses of Radwaste Bldg 3 Elevation Fire Stations Were Found Missing Due to Use by Personnel for Routine Radwaste Washdown.New Firehoses Installed & Mod Re Alternate Water Supply Is in Progress ML20064H5891978-12-14014 December 1978 /03L-0 on 781114:during Periodic Test 9.3.a the HPCI Egr Actuator Failed to Oper Properly Due to Water in Hydraulic Fluid Corroding Egr Actuator.Steam Leaking Past Seat of Valve HPCI E41-F001 Allowed Water Into Fluid ML20062F6781978-12-13013 December 1978 /03L-0 on 781112:reactor Steam Dome High Pressure Switch B32-PS-N018B Did Not Reset & Would Not Allow RHR Valve E11-F008 to Open for Shutdown Cooling at Reactor Pressure of 102psig.Caused by Sticking micro-switch ML20062F6681978-12-13013 December 1978 /03L-0 on 781117:while Reactor Was in Hot Shutdown Torus Level Increased .2 Above Tech Specs.Caused by Demineralized make-up Water Leakage Through Valves from RHR Keep-fill System Causing Torus Level to Rise ML20064G9301978-12-11011 December 1978 /03L-0 on 781109:Reactor Vessel Chemistry Exceeded Tech Spec Limits for Conductivity & Concentration Due to Presence of Organic Compounds in Condensate Sys.Organic Filtration & High Concentration of Ion Resin Cleanup Begun ML20062E4381978-11-30030 November 1978 /03L-0 on 781101:rod Block Monitor(Rbm) Channel a Was Found Out of Calibr During Testing Due to Setpoint Drift.Calibr Frequency Will Be Increased from Once to Twice Per Year ML20064E8001978-11-15015 November 1978 /03L-0 on 781017:reactor Bldg Radiat Exhaust Monitor D12-RM-N010B Failed Safe Causing Reactor Bldg Vent to Isolate,Due to Defective Transistor 2N1711 on 24V Pwr Supply ML20064E4581978-11-14014 November 1978 /01T-0 on 781101:util Was Informed by NRR of Nonconformance w/10CFR50 Append a Gen Design Criteria 54 & 56.Two Reactor bldg-to-torus Vacuum Breaker Lines Have Never Had Design Review by Nrc.Tech Spec Change Effective 781108 ML20064E3371978-11-0909 November 1978 /03L-0 on 781014:RCIC Turbine Was Tripped on Manual Overspeed for Training Purposes & Turbine control- Stop Valve E51-V8 Would Not Reset.Caused by Improperly Worn Adjusted Reset Lever ML20064E2921978-11-0909 November 1978 /03L-0 on 781011:torus Level Dropped Below Tech Spec Minimum While Water from Torus Was Being Pumped,Via Rgr to Radwaste in Efforts to Reduce Torus Water Level. Caused by Operator Being Distracted ML20064E3541978-11-0707 November 1978 /03L-0 on 781006:condensate Storage Tank Level Switch E41-LS-N003 Found Out of Calibration During Periodic Condensate Storage Tank Low Level Channel.Caused by Instru Drift ML20064E3491978-11-0606 November 1978 /03L-0 on 781105:Control Oper Received Control Rod Drift Alarm for Rod 10-31.When Rod Position Display Was Selected,A False 3 Was Superimposed on Actual Rod Position Due to Aground on the Rpls Probe ML20064D8211978-11-0202 November 1978 /03L-0 on 781004:pressure Switch E11-PS-NO16B Failed During Periods Plci Pump Discharges ADS Permissive Test,Due to Corrosion Buildup on Plunger of Switch ML20064C0151978-10-10010 October 1978 /03L-0 on 780911:during Monthly 1 Diesel Generator Load Test,It Was Found That 1 Cylinder Was Not Firing,Due to Faulty Fuel Pump ML20064C0011978-10-0909 October 1978 /03L-0 on 780911:Snubber SW-142SS164 Found Inoperable During Periodic Test.Caused by Seal Degradation & Resulting Loss of Fluid ML20147C9141978-10-0404 October 1978 /03L-0 on 780904:RCIC Isolation Channel a Tripped Momentarily,Causing RCIC Sys to Be Inoper,Due to Defective RX-2 Relay ML20062A0691978-10-0303 October 1978 /03L-0 on 780904:rod Block Monitor B Inoperative Trip Came on & Stayed on for 1/4 of the Control Rod Selection Matrix.Caused by Failed Integrated Circuit in Rod Block Monitor self-test Circuitry ML20064B7231978-10-0303 October 1978 /03L-0 on 780905:during Periodic Test,Radiat Monitor D12-RM-NO10B HI-HI Trip Point Drifted to Higher than Permitted Level.Monitor Recalibrated.Drift Appears to Be Isolated Incident;No Further Action Taken 1993-09-02
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217N3271999-10-21021 October 1999 Part 21 Rept Re non-linear Oxygen Readings with Two (2) Model 225 CMA-X Containment Monitoring Sys at Bsep.Caused by High Gain Produced by 10K Resistor Across Second Stage Amplifier.Engineering Drawings Will Be Revised BSEP-99-0168, Monthly Operating Repts for Sept 1999 for Bsep,Units 1 & 2. with1999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Bsep,Units 1 & 2. with ML20212D0431999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Brunswick Steam Electric Plant,Units 1 & 2 ML20210P9441999-08-10010 August 1999 Safety Evaluation Accepting Licensee Assessment of Impact on Operation of Plant,Unit 1,with Crack Indications of 2.11, 6.36 & 1.74 Inches in Three Separate Jet Pump Risers ML20210P9181999-08-10010 August 1999 Safety Evaluation Authorizing Request for Reliefs CIP-01,02, 06,07,08,09,10 & 11 (with Certain Exceptions) & 12-18,for Second 10-year ISI Interval.Request CIP-04 & 05 Would Result in hardship,CIP-03 Not Required & CIP-11 Denied in Part ML20210N2341999-08-0505 August 1999 SER Accepting Response to NRC GL 87-02, Verification of Seismic Adequacy of Mechanical & Electrical Equipment in Operating Reactors,Unresolved Safety Issues (USI) A-46 ML20210R1191999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Bsep,Units 1 & 2 ML20210R1311999-06-30030 June 1999 Revised Monthly Operating Rept for June 1999 for Bsep,Unit 2 BSEP-99-0118, Monthly Operating Repts for June 1999 for Bsep,Units 1 & 2. with1999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Bsep,Units 1 & 2. with BSEP-99-0095, Monthly Operating Repts for May 1999 for Brunswick Steam Electric Plant,Units 1 & 2.With1999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Brunswick Steam Electric Plant,Units 1 & 2.With ML20210M8581999-05-14014 May 1999 B214R1 RPV Hydrotest Bolted Connection Corrective Action Evaluation, Rev 0 ML20211L3711999-05-10010 May 1999 Rev 0 to ESR 98-00333, Unit 2 Invessel Feedwater Sparger Evaluation ML20206G1871999-05-0404 May 1999 Safety Evaluation Approving Third 10-year ISI Program Requests for Relief (RR) RR-08,RR-15 & RR-17 BSEP-99-0075, Monthly Operating Repts for Apr 1999 for Brunswick Steam Electric Plant,Unit 1 & 2.With1999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Brunswick Steam Electric Plant,Unit 1 & 2.With ML20206N1791999-04-23023 April 1999 Rev 0 to 2B21-0554, Brunswick Unit 2,Cycle 14 Colr BSEP-99-0059, Monthly Operating Repts for Mar 1999 for Brunswick Steam Electric Plant,Units 1 & 2.With1999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Brunswick Steam Electric Plant,Units 1 & 2.With ML20205F9031999-03-30030 March 1999 Safety Evaluation Supporting Proposed Rev to BSEP RERP to Licenses DPR-62 & DPR-71,respectively ML20206N1831999-02-28028 February 1999 Rev 0 to Suppl Reload Licensing Rept for Bsep,Unit 2 Reload 13 Cycle 14 BSEP-99-0043, Monthly Operating Repts for Feb 1999 for Brunswick Steam Electric Plant,Units 1 & 2.With1999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Brunswick Steam Electric Plant,Units 1 & 2.With ML20203D7061999-02-0909 February 1999 SER Accepting Proposed Alternatives Contained in Relief Requests PRR-04,VRR-04,VRR-13,PRR-01,PRR-03,VRR-01.VRR-07, VRR-08 & VRR-09 Denied BSEP-99-0005, Monthly Operating Repts for Dec 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With1998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With BSEP-98-0231, Monthly Operating Repts for Nov 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With1998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With BSEP-98-0218, Monthly Operating Repts for Oct 1998 for Bsep,Units 1 & 2. with1998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Bsep,Units 1 & 2. with BSEP-98-0210, Special Rept:On 980824,temp Element 2-CAC-TE-1258-22 Failed. Cause of Failed Temp Element Cannot Be Conclusively Determined.Temp Element Will Be Replaced & Cable Connections Repaired1998-10-30030 October 1998 Special Rept:On 980824,temp Element 2-CAC-TE-1258-22 Failed. Cause of Failed Temp Element Cannot Be Conclusively Determined.Temp Element Will Be Replaced & Cable Connections Repaired ML20154P8151998-10-16016 October 1998 SER Accepting Revised Safety Analysis of Operational Transient of 920117,for Plant,Unit 1 ML20154P8591998-10-16016 October 1998 SER Accepting Equivalent Margins Analysis for N-16A/B Instrument Nozzles for Plant,Units 1 & 2 BSEP-98-0202, Monthly Operating Repts for Sept 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With1998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With ML20151Y6211998-09-14014 September 1998 BSEP Rept Describing Changes,Tests & Experiments, for Bsep,Units 1 & 2 ML20151Y6371998-09-14014 September 1998 Changes to QA Program, for Bsep,Units 1 & 2 BSEP-98-0185, Monthly Operating Repts for Aug 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With1998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With ML20151T5021998-08-0505 August 1998 Project Implementation Plan, Ngg Yr 2000 Readiness Program, Rev 2 BSEP-98-0164, Monthly Operating Repts for July 1998 for BSEP Units 1 & 21998-07-31031 July 1998 Monthly Operating Repts for July 1998 for BSEP Units 1 & 2 ML20236T1961998-07-0101 July 1998 Rev 1 to 2B21-0088, Brunswick Unit 2,Cycle 13 Colr ML20236T1921998-07-0101 July 1998 Rev 1 to 1B21-0537, Brunswick Unit 1,Cycle 12 Colr BSEP-98-0142, Monthly Operating Repts for June 1998 for BSEP Units 1 & 21998-06-30030 June 1998 Monthly Operating Repts for June 1998 for BSEP Units 1 & 2 ML20236T1971998-06-30030 June 1998 Rev 2 to 24A5412, Supplemental Reload Licensing Rept for Brunswick Steam Electric Plant Unit 2 Reload 12 Cycle 13 ML20249B9691998-06-11011 June 1998 Rev 1 to VC44.F02, Brunswick Steam Electric Plant,Units 1 & 2,ECCS Suction Strainers Replacement Project,Nrc Bulletin 96-003 Final Rept BSEP-98-0129, Monthly Operating Repts for May 1998 for Bsep,Units 1 & 21998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Bsep,Units 1 & 2 ML20151S9041998-05-31031 May 1998 Revised Pages to Monthly Operating Rept for May 1998 for Brunswick Steam Electric Plant,Unit 1 BSEP-98-0104, Monthly Operating Repts for Apr 1998 for Brunswick Steam Electric Plant,Units 1 & 21998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Brunswick Steam Electric Plant,Units 1 & 2 ML20151S8991998-04-30030 April 1998 Revised Pages to Monthly Operating Rept for Apr 1998 for Brunswick Steam Electric Plant,Unit 1 ML20247N7501998-04-30030 April 1998 Rev 0 to BSEP Unit 1,Cycle 12 Colr ML20247N7721998-04-30030 April 1998 Rev 0 to J1103244SRLR, Supplemental Reload Licensing Rept for BSEP Unit 1,Reload 11,Cycle 12 ML20217K8461998-04-24024 April 1998 Safety Evaluation Approving Proposed Use of Code Case N-535 at Brunswick Unit 1 During Second 10-yr Interval,Pursuant to 10CFR50.55a(a)(3)(i).Authorizes Use of Code Case N-535 Until Code Case Included in Future Rev of RG 1.147 ML20217K3941998-04-24024 April 1998 SER Approving Relief Request for Pump Vibration Monitoring, Brunswick Steam Electric Plant,Units 1 & 2 ML20217E6841998-04-23023 April 1998 Safety Evaluation Accepting Code Case N-547, Alternative Exam Requirements for Pressure Retaining Bolting of CRD Housings ML20217E7471998-04-21021 April 1998 Safety Evaluation Accepting Alternative to Insp of Reactor Pressure Vessel Circumferential Welds ML20217B5241998-04-20020 April 1998 SE Accepting Licensee Request for Approval to Use Alternative Exam Requirement for Brunswick,Unit 1,reactor Vessel Stud & Bushing During Second 10-yr ISI Interval Per 10CFR50.55a(a)(3)(ii) BSEP-98-0080, Monthly Operating Repts for Mar 1998 for Bsep,Units 1 & 21998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Bsep,Units 1 & 2 ML20216B1041998-03-0404 March 1998 SER Approving Alternative to Insp of Reactor Pressure Vessel Circumferential Welds for Brunswick Steam Electric Plant, Unit 1 1999-09-30
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V ,
- Carolina Power & Light Company
""emrtmavs4Lva?atsc3 Brunswick Nuclear' Plant !
P. C. Box 10429 Southport, N.C. 28461-0429 August 12, 1993 i
FILE: B09-13510C 10CFR50.73 , ;
SERIAL: BSEP 93-0117 U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D. C. 20555 !
I BRUNSWICK NUCLEAR PLANT UNIT 2 l DOCKET NO. 50-324 .l LICENSE NO. DRP-62 ,
LICENSEE EVENT REPORT 2-93-008 I
i i
Gentlemen: j In accordance with Title 10 of the Code of Federal Regulations, the enclosed j
-Licensee Event Report is submitted. This report fulfills the requirement for a ;
written report within thirty (30) days of a reportable ' occurrence and is submitted in accordance with the format set forth in NUREG-1022,' September 1983.
?
Very truly yours, Nh
. M. Brown, Plant' Manager - Unit 1 'j Brunswick Nuclear Plant t
JFM/jfm ;
1 Enclosure f 1
cc: Mr. S. D. Ebneter Mr. P. D. Milano BSEP NRC Resident Office i
i 170070 9300170089 930813 [c // .)
PDR S
ADOCK 05000324 PDR I ['h R
l- i 1
t NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED OMB NO. 3150-0104 '
(5/92) . EXPIRES: 5/31/95 E STIM ATED BURDEN PER RC SPONSE TO COMPLY WITH TH!S INf ORM ATION cot LE CTION FtE QUEST: 50.0 HRS. FORWARD LICENSEE EVENT RL.,/ ORT (LER) COMMEyTs RtoARo,Na ,URDE N E,T,M,1t yo THE ,NEcRMA1,oN AND RECORDS MANAGEMENT BRANCH (MNBB 771al, U.S. NUCLE AR REGULATORY COMMISSION. WASHINGTON. DC 20H5-DD01. AND TO THE PAPERWDRK REDUCTION PROJECT (3150-0104). OFhCE OF
' MANAGEMENT AND BUDGET. WASH!NGTON, DC 20S03.
FACILIT'Y NAME (1) DOCKET NUMBER {2) PAGE (3)
Brunswick Steam Electric Plant, Unit 2 05000324 1 of 4 i
TITLE 141 CORE RATED THERMAL POWER EXCEEDED THE ALLOWABLE AMOUNT DUE TO FEEDWATER FLOW INACCURACY EVENT DATE (5) LER NUMBER (6) REPORT DATE (7) OTHER FACILITIES INVOLVED (8)
MONTH Day YEAR YEAR t/ONTH CAY YEAR NuMetR NUMBER BSEP 1 05000325 7 14 93 93 - 008 - 0 8 13 93 ' ACurY NAMt OccKtT NuMetR 05000 OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 C"R 8: (Check one or more of the followingM11) 1 MODE $) 20 402ft:) 20.40!.(c) 50 73(aH2Hiv) 73.71(b) 20 405taHini) 50.36(cH1) 50.73laH2Hvi 73.71(c)
PMR (EVEL (10! 100 20 405(aH1Hii) 50 3f4(cH2n 50 73(aH2)M4 OTHER 20 405(aH1Hiul X 50.73taH2Hi) 50.73(eH2)lviiiMA) (Spenfy m Abstract and Text) ;
20 405f aH1Hiv) 50 73iaH2Hiii 50.73(aH2)(voiHE4 20 405(aH1)M 50 73(aH2Heid 50.73(aH2Hul LICENSEE CONTACT FOR THIS LER (12)
AAME TELEPHONE NUVfflR Jeanne F. McGowan, Regulatory Compliance Specialist (919) 457-2136 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
CAUSE Sr$ TIM C OMDONE NT M Af UF ACTURER C A USE SYSTE M COMPONENT MANUF ACTURE R p {
B SJ NZL Y SUPPLEMENTAL REPORT EXPECTED (14) EXPECTED
" U N'" D'* "*" ,
g3 g SUBMISSION of m. cmem Enf cTn susussicN C ATu DATE (15)
ABSTRACT (limit to 1400 spaces, i e. approwmateN fifteen single space typewritten kneal (161 f
On July 14, 1993, Unit 2 was cperating at an indicated power of 100t. A Sodium tracer injection test had been performed on July 2, 1993, to determine the calibration constants for the main steam flow elements and as part of the Brunswick power up-rate project. The >
V preliminary results of the test, received on July 14, 1993, indicated a non-conservative inaccuracy in feedwater flow of 1.094t. This inaccuracy in feedwater flow corresponds to an increase in core tnermal power of approximately 1%. At 1621 hours0.0188 days <br />0.45 hours <br />0.00268 weeks <br />6.167905e-4 months <br /> on July 14, 1993, Unit 2 reduced reactor power to an indicated 2405 MWth Iwhich corresponds to an actual '
reactor power of c100t) Administrative controls were established to ensure core thermal power would not be exceeded. The administrative controls will remain in effect until feedwater instrumentation can be recalibrated.
The cause of the event is believed to be due to erosion / corrosion of the feedwater flow elements.
"Ine safety significance of the event is minimal. Reviews of thermal limit calculations determined that an overpcwer of approximately 11 would have a negligible impact on fuel integrity. No unsafe cperating ccnditions cr transient consequencec would have occurred as a result of the feedwater flow inaccuracy.
The cause classification for thie event per the criteria of NUREG-1022 is Cther.
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NRC FORM,366A U. S. NUCLEAR REcVLATORY COMMISSION APPROVED OMB NO. 3130-0104 j (5/p2) EXPIRES: 5/31/95 ,
, E STIM ATED BURDEN PER RE SPONSE TO COMrY WITH THis INFORMATION COLLECTION REQUEST: 60.0 HRS. FORWARD LICENSEE EVENT REPORT (LER) COMMEu1S u cAnomunotuSmut To rye ,N,oRMuioN AND TEXT CONTINUATION RE CORDS MANAGEMNT MANCH (MNbB 771dl U.S. NUCLE AR REGULATORY COMMISSION. WASHINGTON, DC 205Ek0001, AND TO 5 THE PAPE RWORK REDUCTION PROJECT (3150-0104L OFFfCE OF MANAGFMENT AND BUDGET WASHINGTON DC 205C3.
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FACitJTY NAME 0) DOCKET NUMBER Q) LER NUMBER (6) . PAGE {3) !
SE QUENTIAL REVISION Brunswick Steam Electric Plant "#" "#"
05000324 2 of 4 f Unit 2 93 - 008 - 0 TEKT Uf more space is required. use additionalNRC Form 366A'al(17)
TITLE CORE RATED THERMAL POWER EXCEEDED THE ALLOWABLE AMOUNT DUE TO FEEDWATER FLOW INACCURACY INITIAL CONDITIONS On July 14, 1993, Unit 2 was operating at an indicated power of 100%. A Sodium tracer injection test had been conducted on July 2, 1993 to determine the calibration constants for the main steam flow elements and as part of the Brunswick power up-rate project. The results f rom the Sodium tracer test , received on July 14, 1993, indicated a non-conservative inaccuracy of 1.094%. At 1621 hours0.0188 days <br />0.45 hours <br />0.00268 weeks <br />6.167905e-4 months <br /> on July 14, 1993, Unit 2 reduced reactor power to an indicated 2405 MWth (which corresponds to an actual reactor power of <100%)
EVENT NARRATIVE On October 4, 1989, an Engineering Work Request (EWR) was initiated which identified a mismatch on Brunswick Nuclear Plant (ENP) Unit 1 between the indicated feedwater flow ,
and steam flow. The EWR was initiated to have the calibration data for the Main Steam flow elements reviewed to determine if calibrations needed to be performed. The work l was targeted for March, 1991.
i In March, 1991, the EWR was revised to propose that a Sodium tracer test be performed for Units 1 and 2. The meter differential for the main steam flow elements for both units had not been revised since initial calibration. That value was believed to be inaccurate due to wear on the nozzle plate over the last 15 years. The Sodium tracer ,
test was requested to determine the feedwater flow rate, thereby determining the calibration constants for the main steam flow elements. The main steam flow elements could then be calibrated to ensure the feedwater flow indication and the main steam flow indication are in agreement. The Fodium tracer test was scheduled to be performed in 1992 for Units 1 and 2. Both Units were shutdown in early 1992 and the tests were rescheduled to be performed after each Unit's startup.
Measurement of the flow rate in each of the two feedwater loops on Unit 2 was made by two Sodium tracer tests, on June 30 and July 2, 1993. The data from the test conducted on June 30 was discarded due to weighing errors in the preparation of tracer standards.
The final results of the flow test, released by General Electric (GE) on August 11, l 1993, indicated an actual feedwater flow inaccuracy of 1.094%. An increase of 1.094% ;
in feedwater flow corresponds to an increase in core thermal power of approximately 1% i (based on a manual heat balance calculation). l At 1621 hours0.0188 days <br />0.45 hours <br />0.00268 weeks <br />6.167905e-4 months <br /> on July 14, 1993, Unit 2 reduced reactor power to an indicated 2405 MWth. ,
A Standing Instruction (SI 93-166) was issued to limit core thermal power to less than j or equal to 2405 MWth. Im indicated power of 2409.49 MWth corresponds to 100% power; however, to ensure that core thermal power would not be exceeded, an administrative limit of 2.405 MWth was established until the Process Computer could be changed to reflect the new information. On August 5, 1993, the necessary changes were made to the Procecs Computer and a new Standing Instruction (SI 93-172) was issued to limit core thermal power to less than or equal to 2409.49 MWth indicated. The administrative limit will be in place until the feedwater flow instrumentation can be recalibrated.
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i l NRC FORM 366A U, S. NUCLEAR REGULATORY COMMISSION APPROVED OMB No. 3150-0104 (5/92) EXPlRES: 5/31/95
, ESTIMATED BURDEN PER RE SPONSE TO COMPLY WITH THis
- INFORMATION CDLLE CTION REQUEST 2 $0.0 HRS. FORWARD LICENSEE EVENT REPORT (LER)
COMME NTs REcARomo euRoEN ESTiu ATnO THE imORuATiOuNo ;
TEXT CONTINUATION RE CORDS M ANA GEME NT ORANCH (MNBB 7714), U.S. NUCLE AR j REGULATORY COMMfSSION. WASHINGTON, DC 20565 0001, AND TO THE PAPERWORK REDUCTION PRO.!ECT {3150 0104L OFFICE OF MANAGEMENT AND BUDGET, W ASHINGTON, DC 20503, l FACluTY NAME (1) DOCEET NUMBER (2) LER NUMBER (61 PAGE (3) [
SEQUENTIAL REVISION Brunswick Steam Electric Plant """ """
05000324 3 of 4 i Unit 2 93 - 008 - 0 l
TEKT lit more space is requirect. use additicmst NRC form 36CA 's) (17) 1 l CAUSE OF EVENT The cause of the event is believed to be eresion/ corrosion of the feedwater flow elements. This is based on operating experience at three other plants which have also experienced non-conservative errors in feedwater flow measurement. Visual inspections at two of the plants revealed erosion of the carbon steel piping around the high pressure taps. Flow element wall loss resulted in the non-conservative deviation. The third plant was unclear as to whether this problem existed from construction or was due to nozzle erosion, improper tap location, or fouling.
I CORRECTIVE ACTIONS Corrective actions include the following:
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- 1. Maintain Unit 2 reactor power at less than or equal to 2409.49 MWth )
indicated until the feedwater instrumentation can be recalibrated. l
- 2. Recalibrate the Unit 2 feedwater instrumentation to the calculated flow coefficients based on the tracer test data.
- 3. Perform a _,imilar test on Unit 1 to determine actual feedwater flow.
1 SAFETY ASSESSMENT l An overpower of approximately 1% would non-conservatively affect the calculation of all three monitored thermal limits; Minimum Critical Power Ratio (MCPR) , Maximum Average Planer Linear Heat Generation Rate UMPLHGR), and Peak Linear Heat Generation Rate (PLHGR). The overpower of 1% would result in an increase in all thermal limits of approximately the same magnitude. Typically, Brunswick Nuclear Plant operates with j generous margin to thermal limits (on the order of 5-10%), however, it is possible during powP ascension / maneuvering, that thermal limits may approach to within 1% of l the Technical Specification limits for short periods of time. j The MCPR limit is used to prevent overheating of the fuel rod cladding due to inadequate cooling following postulated events. The derivation of the Safety Limit !
MCPR values for GE fuel designs includes the effects of process monitoring uncertainties. One of the uncertainty inputs is feedwater flow, which is the largest component in reactor power uncertainty. The uncertainty used in feedwater flow is
- 1. 7 f> t , which bounds the detected feedwater flow miscalibration of 1.094t. Therefore, operating with a 1.094% feedwater flow miscalibration does not impact MCPR and the i operating MCPR limits remain valid. Therefore, there is no negative impact on fuel integrity.
The MAPLHGR limits ensure fuel integrity following loss of coolant accidents. The analysis of postulated loss of coolant accidents for Unit 2 assume core thermal power conditions which are approximately 10% greater than the current rated core thermal power of Unit 2. Thus, fuel integrity follcwing a loss of coolant accident would not be affected by an increase in the actual core thermal power of 1%.
The PLHGR limit applies to long term steady state operation and is established to prevent fuel clad cracking due to differential expansion of the fuel pellet. PLHGR is
NRC FCRM 366A U. S. NUCtEAR REGULATORV COMMISSION APPROVED OMB NO. 3150-0104
'(5/921 EXPIRES: 5/31/95
- E STIM ATED BURDEN PER RE SPONSE TO COMPLY WITH THIS INFORMATION CDU.E CTION REQUEST: 60.0 HRS. F ORW ARD !
LICENSEE EVENT REPORT (LER) COMMEuu RtoARo NO BURotN ES1,M,TE TO wE ,N,ORM A1,0N ANo ;
. TEXT CONTINUATION RE CORDS M ANAGfME NT BRANCH (MNBB 77141, U.S. NUCLE AR REGULATORY CDMM6SION WASHINGTON, DC 2055frOOO1. AND TO THE FAPERWORK FIEDUCTION PROJECT (3150-0104). OFFICE OF ;
MANAGEMENT AND BUDGET. WASHINGTON. DC 20503.
FACILfTY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3) i SE QUE NTIAL REVISION Brunswick Steam Electric Plant """" """"'"
Unit 2 05000324 4 of 4 93 - 008 - 0 !
TEKT Uf more spece is reovired. use additional NRC form 36'6A's) (17) i redundant to MAPLHGR and is no longer monitored as a Technical Specification thermal limit. However, a review of the steady state operating histol,/ for Unit 2, Cycle 10 indicates that significant margin has existed due to prolonged reduced power operation. l Therefore, fuel integrity has not been impacted. l In conclusion, no unsafe operating conditicns or transient consequences would have occurred as a result of the f eedwater flow tr.iscalibration. This determination is based upon assessment of conservatisms contained within the supporting basis of the fuel thermal limit calculatiens.
PREVTOUS SIMILAR EVENTS None.
i EIIS COMPONENT IDENTIFICATION !
i System /Cornonent EIIS Code )
l Feedwater System SJ j r
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05000324/LER-1993-003 | LER 93-003-00:on 930408,identified That Drywell Spray Outboard Isolation Valve Installed in Reverse Direction. Caused by Design & Installation Error.Appropriate Documents Will Be revised.W/930507 Ltr | | 05000324/LER-1993-008 | LER 93-008-00:on 930714,core Rated Thermal Power Exceeded Allowable Amount Due to Feedwater Flow Inaccuracy.Cause Believed to Be Due to Erosion/Corrosion of FW Flow Elements. FW Instrumentation recalibr.W/930812 Ltr | |
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