|
---|
Category:GENERAL EXTERNAL TECHNICAL REPORTS
MONTHYEARML18152A2811999-10-12012 October 1999 Technical Basis for Elimination of Nozzle Inner Radius Insps (for Nozzles Other than Reactor Vessel),Technical Basis for ASME Section XI Code Case N-619. ML20249C0011997-11-30030 November 1997 Reactor Vessel Fluence Analysis Methodology ML20148E7091997-05-31031 May 1997 Vols 1 & 2 to Verification of Seismic Adequacy of Mechanical & Electrical Equipment in Ors,Usi A-46, Per GL 87-02 ML18151A7101996-09-30030 September 1996 Supplemental Info for VA Power Nomad Code & Model. ML20249C4051996-05-16016 May 1996 Rev 0 to CE-0082, Review of Augmented ISI Frequency for Pressurizer Spray Lines ML20249C4031996-04-23023 April 1996 Rev 0 to CE-0081, Review of Augmented ISI Frequency for Reactor Coolant Bypass Lines ML20092A2611995-08-31031 August 1995 EDG Preventive Maint Insp Outage Probabilistic Safety Assessment for August 1995 ML20078P9261994-09-26026 September 1994 Service Water System Operational Performance Assessment 940711-29 ML18153B4221993-07-31031 July 1993 Rev 11 to Engineering Evaluation 25, Evaluation of Existing Fire Enclosure Around Ventilation Duct,North Anna Power Station. ML18153B4211993-07-31031 July 1993 Rev 11 to Engineering Evaluation 24, Evaluation of Radiant Energy Shields,North Anna Power Station. ML20046D1581993-02-28028 February 1993 Virginia Power Sys Transient Analysis Using Version 1 of North Anna Retran Model. ML18152A0711993-02-0101 February 1993 NFPA Heat & Flame Evaluation of MSA Custom 4500 SCBA Using Enriched O2 Breathing Air for VA Power,Final Rept. ML20116A2901992-09-23023 September 1992 Conceptual Engineering Final Rept NP-2653, RG 1.97 Isolation Devices Type 2,North Anna Power Station. W/One Oversize Encl ML20101B0331992-04-30030 April 1992 Suppl to Update of Settlement Monitoring Points & Graphs NAPS - Supplement to Technical Rept CE-0019,North Anna Settlement Data Oct 1989 - Apr 1992 ML20077A6601991-05-0707 May 1991 Summary Rept on Exam of Steam Generator Tube R11-C14,North Anna Power Station,Unit 1 ML18153C3111990-07-26026 July 1990 Decommisioning Financial Assurance Certification Rept for Surry Power Station & North Anna Power Station. ML20011F6221990-02-26026 February 1990 Analysis of Small Steamline Break Performance W/O Low Pressurizer Pressure Safety Injection North Anna Units 1 & 2. ML20248E8641989-09-19019 September 1989 Rev 0 to Evaluation of Settlement Monitoring Program for Main Plant Structures in Support of Proposed Changes to Tech Spec 3/4.7.12. W/One Oversize Figure ML20246J1391989-08-17017 August 1989 Rev 0 to Safety Sys Outage Mod Insp,Nrc Finding EP-2 ML20246J1581989-08-0909 August 1989 Rev 0 to Safety Sys Outage Mod Insp,Nrc Finding MC-1 ML20246J1261989-07-20020 July 1989 Rev 0 to Coordination of Load Ctr Circuit Breakers,EP-1 ML20246J1191989-07-20020 July 1989 Rev 0 to Response to SSOMI Item IC-8 of NRC ML20246J0991989-07-18018 July 1989 Rev 0 to Response to NRC Ltr of 890626,Serial 89-485,App C, Finding IC-2 ML20246J1071989-07-18018 July 1989 Rev 0 to Response to NRC Ltr of 890626,Serial 89-485,App C, Finding IC-7 ML20246J1481989-06-30030 June 1989 RCS Leakage Detection Sys ML20246K3461989-05-0505 May 1989 Technical Evaluation & Safety Analysis:Solid State Protection Sys Slave Relay Testing REA-88-51 ML20245K7311989-04-26026 April 1989 Rev 0 to 890225 Steam Generator Leak Event Rept ML20056A0341989-04-18018 April 1989 Nonqualified Nuclear Decommissioning Trust Amended & Restated Trust Agreement ML18151A9661989-04-18018 April 1989 Nuclear Decommissioning Trust Agreement. ML20245A5311988-09-13013 September 1988 Simulator Certification Submittal ML20148J6311988-03-16016 March 1988 Generator Tube Fatigue Evaluation & Remedial Actions Rept ML20147F5621988-03-0202 March 1988 Safety Evaluation in Support of Containment Temp Increase for North Anna Power Station ML20196J2901988-02-24024 February 1988 Rev 1 to Civil Engineering Technical Rept 0005, Differential Settlement Between Svc Bldg & Unit 2 Main Steam Valve House ML20148J6401988-02-12012 February 1988 Rev 2 to North Anna Unit 1 870715 Steam Generator Tube Rupture Event Rept ML20091L7041987-10-19019 October 1987 Generator Row 9 Column 51 Tube Failure Analysis ML20235G2441987-09-25025 September 1987 Steam Generator Downcomer Mods Safety Evaluation for North Anna Units 1 & 2 ML20238F6161987-09-15015 September 1987 Rev 1 to North Anna Unit 1 870715 Steam Generator Tube Rupture Event Rept ML18151A1351987-08-28028 August 1987 Rev 1 to SPDS SAR for VEPCO NUREG-0696 Computer Project, North Anna & Surry Nuclear Power Stations. ML20235U6701987-08-0707 August 1987 Loss of Inventory Event 870617-21 ML20235Q0661987-08-0505 August 1987 Metallurgical Svcs Rept FAL-00050 ML20237G9791987-07-29029 July 1987 Rev 0 to North Anna Unit 1 870715 Steam Generator Tube Rupture Event Rept. W/Pages from Facility Updated FSAR ML20235U3431987-07-20020 July 1987 Rev 0 to Chronology Steam Generator Tube Rupture Event North Anna Power Station Unit 1 870715. Related Info Encl ML20238E1611987-07-15015 July 1987 Rept of Emergency Preparedness Events Re Unit 1 Steam Generator Tube Rupture ML20215G5471987-06-17017 June 1987 Safety Evaluation for Change in Methodology & Supporting Analyses ML20235Q0551987-05-21021 May 1987 Investigation Rept FAL-00024, Emergency Diesel Generator Floating Busing Failure ML20206D6721987-03-31031 March 1987 Engineering Analysis Svc & Maint North Anna Power Station Fairbanks-Morse 38 TD8-1/8 Diesel Engines Phase II ML20207B5231986-11-30030 November 1986 Reactor Vessel Fluence & Rt/Pts Evaluations Suppl to WCAP 11016 ML20213D7771986-10-31031 October 1986 RCS Leakage Detection Assessment for Elimination of RCS Main Loop Pipe Break Protective Devices ML20213D7601986-10-31031 October 1986 RCS Loads & Component Support Margins Evaluation for Elimination of Rcs,Main Loop Pipe Break Protective Devices ML20210F6821986-10-17017 October 1986 Reactor Protection Sys Trip Setpoint Drift Characterization 1999-10-12
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217N9281999-10-20020 October 1999 Special Rept:On 991003,PZR PORV Actuation Mitigated RCS low- Temp Overpressure Transient.Caused by a RCP Facilitating Sweeping of Entrained Air Out of RCS Loops.Operating Procedure 2-OP-5.1 Will Be Revised ML20217H3631999-10-14014 October 1999 Rev 0 to COLR for North Anna 2 Cycle 14 Pattern Su ML18152A2811999-10-12012 October 1999 Technical Basis for Elimination of Nozzle Inner Radius Insps (for Nozzles Other than Reactor Vessel),Technical Basis for ASME Section XI Code Case N-619. ML20212J9251999-10-0101 October 1999 Safety Evaluation Accepting Licensee Relief Request IWE-3 for Second 10-year ISI for Plant ML20217D6851999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for North Anna Power Station,Units 1 & 2.With ML20211N2611999-09-0808 September 1999 Safety Evaluation Concluding That Proposed Irradiation of Fuel Rods Beyond Current Lead Rod Burnup Limit & Clarification of Terminology with Respect to Reconstituted Fuel Assemblies Acceptable ML20211J2561999-08-31031 August 1999 Safety Evaluation Accepting Elimination of Augmented ISI Program for Pressurizer Spray Lines at North Anna Unit 2 ML20216E5011999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Naps,Units 1 & 2. with ML20211J2421999-08-31031 August 1999 Safety Evaluation Supporting Removal of Augmented Insp Program on RCS Bypass Lines from Licensing Basis of North Anna,Units 1 & 2 ML20210T0791999-08-13013 August 1999 Safety Evaluation Concluding That Revised Withdrawal Schedules for North Anna Units 1 & 2 Satisfy Requirements of App H to 10CFR50 & Therefore Acceptable ML20210S1411999-07-31031 July 1999 Monthly Operating Repts for July 1999 for North Anna Power Station.With ML20210Q9931999-07-31031 July 1999 Rev 1 to COLR for North Anna Power Station,Unit 2 Cycle 13 Pattern Ud ML20209E5641999-06-30030 June 1999 Monthly Operating Repts for June 1999 for North Anna Power Stations,Units 1 & 2.With ML20195G1901999-05-31031 May 1999 Monthly Operating Rept for May 1999 for NAPS Units 1 & 2. with ML20206L4831999-05-10010 May 1999 SER Accepting Request to Delay Submitting Plant,Unit 1 Class 1 Piping ISI Program for Third Insp Interval Until 010430, to Permit Development of Risk Informed ISI Program for Class 1 Piping ML20206Q6671999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for North Anna Power Station,Units 1 & 2.With ML20205S0391999-04-21021 April 1999 SER Accepting Request for Relief IWE5,per 10CFR50.55a(a)(3) & Proposed Alternatives for IWE2,IWE4,IWE6 & IWL2 Authorized Per 10CFR50.55a(a)(3)(ii) ML20205K3041999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for North Anna Power Station,Units 1 & 2.With ML20207K5921999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for North Anna Power Station,Units 1 & 2.With ML20207E1731999-02-18018 February 1999 Informs Commission of Status of Preparations of IAEA Osart Mission to North Anna Nuclear Power Plant Early Next Year ML20205A0241998-12-31031 December 1998 Summary of Facility Changes,Tests & Experiments,Including Summary of SEs Implemented at Plant During 1998,per 10CFR50.59(b)(2).With ML20199C8781998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for North Anna Power Station,Units 1 & 2.With ML20198H9541998-12-0303 December 1998 Safety Evaluation Authorizing Proposed Alternative for Remainder of Second 10-yr Insp Interval for Plant ML20198J5561998-12-0303 December 1998 ISI Summary Rept for North Anna Power Station,Unit 1 1998 Refueling Outage Owner Rept for Inservice Insps ML20197G8551998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for North Anna Power Station,Units 1 & 2.With ML20196G1381998-11-0303 November 1998 Safety Evaluation Authorizing Rev to Relief Request NDE-32 for Remainder of Second 10-yr Insp Interval for Each Unit ML20195D0571998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for North Anna Power Station,Units 1 & 2.With ML20154L0691998-10-14014 October 1998 COLR for North Anna Power Station Unit 1 Cycle 14 Pattern Xy ML20155J6911998-10-0909 October 1998 Staff Response to Tasking Memorandum & Stakeholder Concerns ML20154H4001998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for North Anna Power Station,Units 1 & 2.With ML20151X8011998-09-10010 September 1998 Special Rept:On 980622,groundwater Level at Piezometer P-22 Was Again Noted to Be Above Max Water Level by 0.71 Feet. Increased Frequency of Piezometer Monitoring & Installed Addl Piezometers at Toe of Slope Along Southwest Section ML20151W4711998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for North Anna Power Station Units 1 & 2.With ML20237A4341998-07-31031 July 1998 Monthly Operating Repts for July 1998 for North Anna Power Station,Units 1 & 2 ML20236V1251998-07-14014 July 1998 ISI Summary Rept for Naps,Unit 2,1998 Refueling Outage Owners Rept of Isis ML20236K5531998-07-0707 July 1998 SER Accepting Request for Change in ISI Commitment on Protection Against Pipe Breaks Outside Containment ML20236M3381998-06-30030 June 1998 Monthly Operating Repts for June 1998 for North Anna Power Station,Units 1 & 2 ML20248M1011998-05-31031 May 1998 Monthly Operating Repts for May 1998 for North Anna Power Station,Units 1 & 2 ML20248C8831998-05-29029 May 1998 SER Accepting Alternatives Proposed by Licensee for Use of Code Case N-535,pursuant to 10CFRa(a)(3)(i) in ASME Section XI Inservice Insp Program ML20247K9281998-05-15015 May 1998 Special Rept:On 980428,letdown PCV Exhibited Slow Response When C RCP Was Started.Cause to Be Determined.Review of Operating Procedure Will Be Performed to Determine If Enhancements Are Necessary ML20216A8971998-05-0606 May 1998 Rev 0 to Cycle 13 Pattern Ud COLR for North Anna Unit 2 ML20247F4441998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for North Anna Power Station,Units 1 & 2 ML20217B5321998-04-20020 April 1998 Safety Evaluation Supporting Proposed Alternative to ASME Code for Surface Exam of Seal Welds on Threaded Caps for Plant Reactor Vessel Head Penetrations for part-length CRDMs ML20217H9611998-04-0707 April 1998 Special Rept:On 980216,groundwater Level at Piezometer P-22, Again Noted to Be Above Max Water Level by 0.41 Feet.Design Package for Installation of Addl Standpipe Piezometers at Toe of Slope Southeast Section,Developed ML20216B1891998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for North Anna Power Station,Units 1 & 2 ML20216E8801998-03-0606 March 1998 Safety Evaluation Authorizing Licensee Request for Relief from ASME Code Requirements,Paragraph IWA-2400(c) (Summer Edition W/Summer 1983 Addenda),For Upcoming Naps,Unit 1 Outage,Per 10CFR50.55a(a)(3)(ii) ML20216E2561998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for North Anna Power Station,Units 1 & 2 ML20199J6431998-02-0202 February 1998 Safety Evaluation Approving Request for Approval to Repair Flaws in Accordance W/Gl 90-05 for ASME Code Class 3 SW Piping for North Anna,Unit 1,as Submitted in ISI Relief Request NDE-46 on 971218 ML20202D5811998-01-31031 January 1998 Monthly Operating Repts for Jan 1998 for North Anna Power Station,Units 1 & 2 ML20198S7571998-01-15015 January 1998 Safety Evaluation Accepting Licensee Request for Approval to Repair Flaws IAW GL-90-05 for ASME Code Class 3 Svc Water Piping ML20198P1351997-12-31031 December 1997 Monthly Operating Repts for Dec 1997 for North Anna Power Station,Units 1 & 2 1999-09-08
[Table view] |
Text
.._, , - . .
e ENCLOSURE 2 NORTH ANNA UNITS 1 & 2 l 582.8'F REACTOR C00 LAM SYSTEM l STONE & WEBSTER / BOP SAFETY EVALUATION
SUMMARY
STONE & WEBSTER ENGINEERING CORPORATION APRIL 1982 4
8206090092 820608 PDR ADOCK 05000338 P PDR
i .
TABLE OF CONTENTS A. Objective B. Conclusions C. Accident Analysis and Environmental Qualification D. Pipe Stress and Supports E. Major Equipment Pipe Rupture Restraints and Equipment Supports F. BOP Systems and NSSS Interfaces G. Review of Technical Specifications 1
A. GLJECTIVE Ta pravide a technical basis for determining that the proposed 2.5'F 1acrease in reactor coolant system Tavg does not involve an unreviewed safety question in accordance with the requirements of 10CFR50.59. This review is limited to systems within Stone & Webster Engineering Corporation's original scope of work. The NSSS and Turbine-Generator review has been performed by Westinghouse and is documented as Enclosure 1.
Our evaluation used the following parameters which bound or are equivalent to the prc. posed uprated conditions:
Main Steam Pressure 100% Power 900 psia Main Steam Temp. No-Load 547'F Main Steam Pressure No-Load 1020 psia RCS Tavg 582.8*F 6 12.12 Steam Flow 10 lb./hr Total 2775.
Reactor Power MW' 2785.
NSSS Power MW t B. CONCLUSION The proposed change in reactor coolant system average temperature has been reviewed and evaluated with respect to the following:
- 1. Accident Analysis and Environmental Qualification '.
- 2. Pipe Stress and Supports
- 3. Major Equipment Pipe Rupture Restraints and Equipment Supports
- 4. B0P System and NSSS Interfaces
- 5. Review of Technical Specifications Based on the results of our review it has been concluded that the proposed 2.5'F increase in Tavg does not represent an unreviewed safety question as defined in 10CFR50.59. The summary of the analyses related to the above l
are attached.
I
- 1. It has been determined that the probability of occurrence or the consequences of an accident or malfunction of equipment important l
to safety and previously evaluated in the Safety Analysis Report has not been increased.
- 2. The possibility for an accident or malfunction of a different type than any evaluated previously in the Safety Analysis Report has not been created.
- 3. The margin of safety as defined in the basis for any Trchnical Specification has not been reduced.
'e I 2
C. ACCIDENT ANALYSIS
- 1. Containment Loss of Coolant Accident The present licensed power level for North Anna 1 & 2 is 2775 MWT (2785 including reactor coolant pump heat). The analyses for con-tainment integrity, containment depressurization, low-head safety injection pump NPSH and recirculation spray pump NPSH for the 2.5*F uprate are bounded by the present analyses which are based on core power of 2900 MWT (2910 MWT including reactor coolant pump heat).
- 2. Containment Main Steam Line Break Analysis The basis of the steam line break analysis is the full guillotine main steam line break at no-load (hot shutdown) condition. The no-load Tasg of 547*F remains unchanged subsequent to the uprate and therefore the Main Steam Line Break conditions remain as previously analyzed.
- 3. Subcompartment Analysis Subcompartment analyses were performed and documented in the FSAR for the reactor cavity, steam generator cubicle and pressurizer cubicle. For the subcooled reactor coolant system, mass and energy releases decrease with increased reactor coolant temperature. The analyses documented in the FSAR are therefore bounding for the uprate.
- 4. Equipment Qualification
- 1. Inside Containment:
Equipment qualification inside the containment is based on the Main Steam Line Break and LOCA post-accident environmental conditions.
The current Steam Line Break and LOCA analyses are bounding for the uprate conditions as discussed in sections 1 & 2.
- 2. Outside Containment:
Post-accidene environments outside containment which are used to generate equipment qualification envelopes are based on the following 1.igh energy line breaks:
- a. Primary System Branch Line Break The Letdown Line Break is part of the basis for the environ-mental qualification in the charging pump cubicle in the auxiliary building. The letdown line temperature increases one degree above the normal operating temperature used in the original analysis. The resulting environmental temperature due to a postulated line break is not significantly affected by this change.
3
~
- 2. Outside Containment-(cont'd.)
- b. Secondary System Break i'
The Main Steam Line Break affects the Main Steam Valve House, the Service Water Valve Pit and the Turbine Building. The Main Steam Valve House environmental envelope is based on no-load power condition which is unaffected by the uprate.
- Equipment qualification temperature and pressure in the Service Water Valve Pit and Turbine Building is limited by the Turbine Building siding pressure retaining capability. Any change to break effluent due to the uprate has no effect on this pressure or temperature and, therefore, on equipment qualification.
- c. Auxiliary Steam Line Break:
1 This affects the Auxiliary Building and the Service Water Valve Pit. The releases are based on the Auxiliary Steam Line relief valve pressure setting which is unchanged by the uprate.
Additionally, the Auxiliary Steam System pressure is controlled by a pressure reduction valve tied into the Main Steam header.
The increased Main Steam operating pressure will not affect the operation of this valve and therefore the Auxiliary Steam System pressure will remain unchanged.
- d. Steam Generator Blowdown Line Break: [
This affects the Pipe Tunnel and the Auxiliary Building. The releases are based on the bounding condition of no-load steam generator pressure which is unchanged by the uprate.
D. PIPE STRESS AND SUPPORTS All piping systems directly affected by the 2.5'F Reactor Coolant System Tavg uprate were reviewed with respect to pipe stress and the adequacy of pipe support designs. The systems most obviously impacted were the Main
' Steam and Feedwater Systems. Pipe stress and support calculations for these systems were reviewed and it was determined that the uprate would have an impact on three Unit 2 Main Steam Mono-Ball supports located on a non-safety related portion of piping. These supports will be modified to accommodate the uprated conditions. All the remaining piping and supports on the Main Steam System and other systems were reviewed at the bounding no-load condition or were evaluated to confirm adequate margins existed within the calculations to accommodate the uprated conditions.
i The piping connected to the reactor coolant loops was reviewed to determine the effect of a possible increase in displacements resulting from increased i Reactor Coolant system temperature. The increase in Reactor Coolant System i temperature is less than one percent and therefore the additional displace-ment is considered to be insignificant. Therefore no reanalysis is necessary and these systems are acceptable.
i
, 4 ,
I
D. PIPE STRESS AND SUPPORTS -(cont'd d
.." reziew of safety related piping for fati3ue effects of thermal transients revealed that only the reactor coolant letdown line required reanalysis.
The 2.5'F increase in Tavg subjected the letdown line to a more severe reinitiation of letdown flow transient than was originally used as a design basis. The results of the analysis showed that the fatigue effects on the piping would remain acceptable subsequent to the proposed uprate. The stress report will be revised to include this information.
It has been determined that previously calculated break points in piping systems, used for the design of rupture restraints, jet shields and large pipe supports will remain unchanged as a result of the uprating. The points of maximum stress within any piping system remain unchanged as the stress increases due to the uprating are uniform. Pipe rupture effects are discussed in Section E.
E. MAJOR EQUIPMENT PIPE RUPTURE RESTRAINTS AND EQUIPMENT SUPPORTS Design calculations for major equipment supports, seismic tanks, vessels, pipe rupture restraints and shields and miscellaneous mechanical equipment have been reviewed with the uprated system parameters for 100% power and no-load conditions.
Of the approximately 450 calculations reviewed, five were found to have used Main Steam or Feedwater System pressures that would not bound values expected subsequent to the 2.5*F Reactor Coolant System Tavg increase. These five calculations were reviewed with respect to the uprated conditions and found acceptable.
Our evaluation concluded that an increase in Reactor Coolant System temperature results in a decrease in LOCA loadings with the frequency content of those loadings being unchanged as a result of the uprating. This conclusion was based on the information contained in the Westinghouse safety evaluation, Enclosure 1.
n" 5
F. BOP SYSTEMS AND NSSS INTERFACES
- 1. Condensate and Feedwater Systems Steam conditions leaving the turbine are unchanged. As a result of increasing Tavg, the Steam Generatar Pressure will not exceed the design pressure and temperature of the Condensate and Feedwater Systems. Equipment such as steam generator feed pumps, condensate pumps, heater drain pumps and feedwater heaters will continue to operate unchanged since design steam flows are greater than those expected subsequent to the uprcting.
A review of the operation of the Main Feedwater Regulating and Bypass Valves has shown that increasing Tavg by 2.5'F will not cause a signi-ficant change in current operating flexibility.
- 2. Main Steam System The Main Steam System piping and components are designed for no-load conditions and are bounded by the proposed 2.5'F Reactor Coolant System Tavg increase.
The operability of the Main Steam Trip Valves (MSTV's) and Non-Return Valves (NRV's) has been reviewed with regard to the uprated conditions.
The review has shown that the MSTV's and NRV's will perform adequately at the uprated conditions. The previous analysec used parameters that bounded the uprated conditions. The structural adequacy of the NRV's and MSTV's was evaluated for impact loadings and was found to be acceptable for the uprated conditions as the analyses used conditions which bounded the uprate.
Because the Main. Steam System transients will remain unchanged as a result of the uprating, the existing Main Steam Safety Valves are adequately sized for the uprated conditions and will not require revised lift settings.
- 3. Component Cooling Water System The increased Reactor Coolant System temperature increases the heat loadings to various Chemical and Volume Control System (CVCS) heat exchangers and therefore the Component Cooling Water System will be required to remove a small amount of additional heat subsequent to the uprate. A review has shown that adequate margin exists in the Component Cooling Water System to remove the additional heat load.
i 2
6
- 4. Steam Generator Blowdown System A review of the entire Steam Generator Blowdown System has indicated that uprating Reactor Coolant System Tavg by 2.5'F will not affect the present safety aspects or operability of the system.
4 The design of the excess flow high energy line break isolation valves was for an inlet pressure of 1100 psig which is higher than the lowest Main Steam Safety Valve setpoint and is therefore acceptable with regard to the uprate.
All remaining portions of the Steam Generator Blowdown System including l
flow control valves, safety valves, tanks and pressure control valves were reviewed for any expected temperature and pressure changes and are unaffected by the uprate.
- 5. Auxiliary Feedwater System The Auxiliary Feedwater System is designed to remove decay and sensible heat from the Reactor Coolant System following a reactor trip. The original Auxiliary Feedwater System requirements were based on an NSSS rating of 2910 MW g and 850 psia steam pressure. The 2.5'F Reactor Coolant System Tavg increase at 2785 MW is bounded by the original analysisthatincludedthe2.5'FTavgibereaseinReactorCoolant System temperature. Therefore, the Auxiliary Feedwater System require-ments are unchanged and the Auxiliary Feedwater Pumps are of adequate capacity and head to supply the required flow at the uprated conditions.
G. REVIEW OF THE TECHNICAL SPECIFICATIONS The Technical Specifications have been reviewed to determine if any sections could be affected by the proposed 2.5'F Tavg increase from 580,3'F to 582.8*F.
With the exception of the Technical Specification revisions recommended by Westinghouse Electric Corporation in their safety evaluation, Enclosure 1, no additional sections are affected.
7
- .-. , - - - - - . _ .