IR 05000440/2019004

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Integrated Inspection Report 05000440/2019004
ML20030A575
Person / Time
Site: Perry 
(NPF-058)
Issue date: 01/29/2020
From: Billy Dickson
Division Reactor Projects III
To: Payne F
FirstEnergy Nuclear Operating Co
References
EPID L-2019-004-0055 IR 2019004
Preceding documents:
Download: ML20030A575 (29)


Text

January 29, 2020

SUBJECT:

PERRY NUCLEAR POWER PLANT - INTEGRATED INSPECTION REPORT 05000440/2019004

Dear Mr. Payne:

On December 31, 2019, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Perry Nuclear Power Plant. On January 17, 2020, the NRC inspectors discussed the results of this inspection with you and other members of your staff. The results of this inspection are documented in the enclosed report.

No findings or violations of more than minor significance were identified during this inspection.

This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

Billy C. Dickson, Jr, Chief Branch 2 Division of Reactor Projects

Docket No. 05000440 License No. NPF-58

Enclosure:

As stated

Inspection Report

Docket Number:

05000440

License Number:

NPF-58

Report Number:

05000440/2019004

Enterprise Identifier: I-2019-004-0055

Licensee:

FirstEnergy Nuclear Operating Company

Facility:

Perry Nuclear Power Plant

Location:

Perry, OH

Inspection Dates:

October 01, 2019 to December 31, 2019

Inspectors:

L. Alvarado Guilloty, Resident Inspector

S. Bell, Health Physicist

G. Hansen, Sr. Emergency Preparedness Inspector

J. Nance, Resident Inspector

L. Rodriguez, Reactor Inspector

J. Rutkowski, Project Engineer

E. Sanchez Santiago, Senior Reactor Inspector

J. Steffes, Senior Resident Inspector

J. Winslow, Resident Inspector

Approved By:

Billy C. Dickson, Jr, Chief

Branch 2

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Perry Nuclear Power Plant, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

No findings or violations of more than minor significance were identified.

Additional Tracking Items

Type Issue Number Title Report Section Status URI 05000440/2019004-01 Degraded Turbine Overspeed Reset Limit Switch Results in an Extension in USAR Described Test Frequency 71111.18 Open

PLANT STATUS

The plant began the inspection period at rated thermal power. On December 6, 2019, the licensee identified elevated offgas pretreat chemistry results, which was indicative of a fuel defect, from a routine sample. On December 10, 2019, the licensee lowered reactor power to approximately 52 percent to perform power suppression testing and identify potential fuel defects. Following completion of the power suppression testing, Perry began a gradual power ascension on December 12, 2019, and achieved full power on December 14, 2019. The reactor remained at approximately 100 percent power for the remainder of the inspection period.

On April 25, 2018, FirstEnergy Solutions (FES) / FirstEnergy Nuclear Operating Company (FENOC) notified the U.S. Nuclear Regulatory Commission (NRC) that they intend to shut down all four of their operating nuclear power plants (ADAMS Accession Number ML18115A007). On March 21, 2018, FES, FirstEnergy Nuclear Generation (FENGEN), and FENOC filed for bankruptcy. On July 26, 2019, FES/FENOC submitted a letter to the NRC withdrawing the April 25, 2018, certification of permanent cessation of power operations for Davis-Besse Nuclear Power Station and Perry Nuclear Power Plant (ADAMS Accession Number ML19207A097). The NRC continues to maintain focus on public health and safety and the protection of the environment. This will include a continuous evaluation by inspectors to determine whether the licensee's financial condition is impacting safe operation of the plant.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed plant status activities described in IMC 2515, Appendix D, Plant Status, and conducted routine reviews using IP 71152, Problem Identification and Resolution. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

External Flooding Sample (IP Section 03.04) (1 Sample)

(1)

  • Diesel generator rooms; and

71111.04Q - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (5 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1)

"B" train of control room ventilation and emergency recirculation system on October 15 - 17, 2019 (2)

"A" train of emergency service water system on October 23, 2019 (3)

"B" train of residual heat removal (RHR) system on October 30, 2019 (4)

"A" train of standby liquid control system on November 12, 2019 (5)

"A" train of annulus exhaust gas treatment system on November 13, 2019

71111.04S - Equipment Alignment

Complete Walkdown Sample (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated system configurations during a complete walkdown of the reactor core isolation cooling system on November 12-15, 2019

71111.05Q - Fire Protection

Quarterly Inspection (IP Section 03.01) (5 Samples)

The inspectors evaluated fire protection program implementation in the following selected areas:

(1) Emergency service water pump house on October 18, 2019
(2) Diesel generator hallway 620 and 646 foot elevations on October 22, 2019
(3) Auxiliary building 620 foot elevation fire zones 1AB-3A/B on October 24, 2019
(4) Control complex 620 elevation fire zones 1CC-3B/D on October 30, 2019
(5) Intermediate building 654, 665, and 682 foot elevations fire zones 0IB-4/5 on October 31, 2019

71111.06 - Flood Protection Measures

Inspection Activities - Internal Flooding (IP Section 02.02a.) (1 Sample)

The inspectors evaluated internal flooding mitigation protections in the:

(1) Unit 1, Division 1 and 2, and Unit 2, Division 1, motor control center switchgear rooms from a break in a fire protection main line break

71111.07A - Heat Sink Performance

Annual Review (IP Section 02.01) (1 Sample)

The inspectors evaluated readiness and performance of:

(1) Division 3 emergency diesel generator jacket water heat exchanger during the weeks of November 3 and 18, 2019

71111.07T - Heat Sink Performance Triennial Review (IP Section 02.02)

The inspectors evaluated heat exchanger/sink performance on the following:

(1) Residual Heat Removal (RHR) Heat Exchanger "B" (1E12B0001B), cooled by the service water system, Section 02.02.b
(2) Emergency Closed Cooling Water (ECCW) Heat Exchanger "B" (1P42B0001B),cooled by the service water system, Section 02.02.b
(3) Ultimate Heat Sink, Sections 02.02.d.5 and 02.02.d.7

71111.11A - Licensed Operator Requalification Program and Licensed Operator Performance

Requalification Examination Results (IP Section 03.03) (1 Sample)

(1) The inspectors reviewed and evaluated the licensed operator examination failure rates for the requalification biennial written examinations and annual operating tests administered from October 28 - December 9, 2019

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)

(1) The inspectors observed and evaluated licensed operator performance in the Control Room during the downpower and rod pattern adjust associated with power suppression testing on December 10 - 11, 2019

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

(1) The inspectors observed and evaluated an operations crew-evaluated scenario in the plant training simulator on November 19, 2019

71111.12 - Maintenance Effectiveness

Routine Maintenance Effectiveness Inspection (IP Section 02.01) (4 Samples)

The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety significant functions:

(1)

"B" combustible gas mixing compressor failure, CR 2019-09212, during surveillance test on November 1, 2019

(2) Division 3 emergency diesel generator following a diesel generator trip, CR 2019-09378, on reverse power relay actuation on December 5, 2019
(3) Remote shutdown panel switches following, CR 2019-09208, RHR "B" containment spray 1st isolation valve lost all position indication on December 7, 2019
(4) Review of licensee's maintenance rule program periodic review on December 13, 2019

Quality Control (IP Section 02.02) (1 Sample)

The inspectors evaluated maintenance and quality control activities associated with the following equipment performance activities:

(1) Component grade dedication of Bailey BLC2000-721 control unit to replace annulus differential pressure controller following unit failure on November 25 - 27, 2019

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (3 Samples)

The inspectors evaluated the risk assessments for the following planned and emergent work activities:

(1) Plant risk assessment with the "B" train of control room HVAC and emergency recirculation systems out of service for planned work and hot weather in the area with a grid alert on October 2, 2019
(2) Emergent troubleshooting after Division 3 emergency diesel generator tripped on November 5, 2019
(3) Plant risk assessment with the Division 2 RHR systems unavailable for divisional work window and power suppression testing on December 10 - 11, 2019

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 02.02) (2 Samples)

The inspectors evaluated the following operability determinations and functionality assessments:

(1) Past operability evaluation associated with CR 2019-09208, RHR B Containment Spray 1st Isolation Valve Lost All Position Indication on November 1, 2019
(2) Control rod drive system during inability to select control rods on November 1, 2019

71111.18 - Plant Modifications

Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02) (3 Samples)

The inspectors evaluated the following temporary or permanent modifications:

(1) Review of the licensee's extension of USAR described turbine overspeed testing frequency due to degraded test circuitry on November 13 - December 14, 2019
(2) Interim flooding measures in response to a re-evaluation of the local intense precipitation flooding hazard on December 7, 2019
(3) Modification of reactor water cleanup system isolation due to a steam leak on December 16 - 19, 2019

71111.19 - Post-Maintenance Testing

Post-Maintenance Test Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated the following post maintenance tests:

(1) Partial RHR "B" pump and valve operability test after troubleshooting of 1E12-F028B, containment spray "B" first shutoff valve on November 1, 2019
(2) Control rod exercising after troubleshooting and replacement of the malfunctioning beam control card in the Rod Control and Information system on November 2, 2019
(3) Testing following replacement of the channel "C" scram discharge volume high level relay on November 7, 2019
(4) Emergency closed cooling pump "A" test following preventative maintenance window on November 18, 2019

71114.02 - Alert and Notification System Testing

Inspection Review (IP Section 02.01-02.04) (1 Sample)

(1) The inspectors evaluated the following maintenance and testing of the alert and notification system:
  • Annual siren inspection and maintenance records for the period from September 2017 to September 2019
  • Monthly alert notification system (siren) tests for the period from September 2017 to September 2019

71114.03 - Emergency Response Organization Staffing and Augmentation System

Inspection Review (IP Section 02.01-02.02) (1 Sample)

(1) The inspectors evaluated the readiness of the Emergency Preparedness Organization

71114.04 - Emergency Action Level and Emergency Plan Changes

Inspection Review (IP Section 02.01-02.03) (1 Sample)

(1) The inspectors completed an evaluation of submitted Emergency Action Level and Emergency Plan changes on November 21, 2019. This evaluation does not constitute NRC approval

71114.05 - Maintenance of Emergency Preparedness

Inspection Review (IP Section 02.01 - 02.11) (1 Sample)

(1) The inspectors evaluated the maintenance of the emergency preparedness program

RADIATION SAFETY

71124.02 - Occupational ALARA Planning and Controls

Radiological Work Planning (IP Section 02.01) (1 Sample)

The inspectors evaluated the licensees radiological work planning.

(1) The inspectors reviewed the following activities:
  • RWP 190904 and associated ALARA plans; 1R17 Reactor Reassembly
  • RWP 190522 and associated ALARA plans, 1R17 Bioshield In-Service Inspection Activities
  • RWP 190903 and associated ALARA plans; 1R17 In-Vessel Inspection Activities

Verification of Dose Estimates and Exposure Tracking Systems (IP Section 02.02) (1 Sample)

The inspectors evaluated dose estimates and exposure tracking.

(1) The inspectors reviewed the following as low as reasonably achievable planning documents:
  • RWP 190904 and Associated ALARA Plans; 1R17 Reactor Reassembly
  • RWP 190522 and associated ALARA plans; 1R17 Bioshield In-Service Inspection Activities
  • RWP 190903 and associated ALARA plans; 1R17 In-Vessel inspection Activities

Additionally, the inspectors reviewed the following radiological outcome evaluations:

  • RWP 190904; 1R17 Reactor Reassembly post job evaluation
  • RWP 190522; 1R17 Bioshield In-Service Inspection Activities post job evaluation
  • RWP 190903; 1R17 In-Vessel inspection Activities post job evaluation

71124.03 - In-Plant Airborne Radioactivity Control and Mitigation

Self-Contained Breathing Apparatus for Emergency Use (IP Section 02.03) (1 Partial)

The inspectors evaluated self-contained breathing apparatus program implementation.

(1)

(Partial)

This augments the inspection sample documented in NRC Inspection Report

===05000440/2018004

OTHER ACTIVITIES - BASELINE

71151 - Performance Indicator Verification

The inspectors verified licensee performance indicators submittals listed below:

EP01: Drill/Exercise Performance (IP Section 02.12)===

(1)07/01/2018 - 06/30/2019

EP02: ERO Drill Participation (IP Section 02.13) (1 Sample)

(1) 07/01/2018 - 06/30/2019

EP03: Alert & Notification System Reliability (IP Section 02.14) (1 Sample)

(1)07/01/2018 - 06/30/2019

BI01: Reactor Coolant System (RCS) Specific Activity Sample (IP Section 02.10) (1 Sample)

(1)10/01/2018 - 09/30/2019

BI02: RCS Leak Rate Sample (IP Section 02.11) (1 Sample)

(1) 10/01/2018 - 09/30/2019

OR01: Occupational Exposure Control Effectiveness Sample (IP Section 02.15) (1 Sample)

(1) 10/01/2018 - 09/30/2019

71152 - Problem Identification and Resolution

Semiannual Trend Review (IP Section 02.02) (1 Sample)

(1) The inspectors reviewed licensee-identified water fire protection system issues to determine if a trend existed that could, if allowed to continue, compromise the installed spray nozzles' functionality and adversely impact the system ability to suppress fires impacting plant electrical transformers and fires occurring within plant areas with fire protection spray nozzles. The inspectors did not find an adverse trend that would cause the inspectors to question the plant's water fire protection system ability to carry out its design function.

Annual Follow-up of Selected Issues (IP Section 02.03) (2 Samples)

The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:

(1) RCIC Steam supply second drain isolation valve leak caused EOP-3 entry CR2019-10360
(2) Review of plant aggregate risk assessment

INSPECTION RESULTS

Unresolved Item (Open)

Degraded Turbine Overspeed Reset Limit Switch Results in an Extension in USAR Described Test Frequency URI 05000440/2019004-01 71111.18

Description:

On July 27, 2019, a turbine trip and reactor scram occurred during performance of weekly turbine overspeed testing. The turbine trip occurred during performance of step 5.1.2.3 of PTI-N32-P0001, which tests the mechanical overspeed trip, as documented in CR 2019-06321, Turbine Trip during Weekly Turbine Overspeed Test. Troubleshooting efforts identified several discrepant conditions which were addressed during the forced outage, except for one. A ground was discovered associated with the reset limit switch of the turbine overspeed system. The inspectors noted, through review of CR 2019-06587, "Limit Switch Causes - 125 VDC Ground," that the licensee decided not to replace the reset limit switch upon discovery due to personnel safety and the potential for another turbine trip.

Updated Safety Analysis Report (USAR) Section 10.2.2.3 states, in part, that each compartment of the mechanical and electrical overspeed protection systems will be tested at each startup and during normal operations, on a weekly basis, by the following tests:

a. A mechanical overspeed trip test at the the EHC panel to test for operation of the overspeed trip device and mechanical trip valve.

b. A mechanical trip piston test at the EHC panel to test for electrical activation of the trip mechanism.

c. An electrical trip test at the EHC panel to test for operation of the electrical trip valve.

d. A backup overspeed trip test at the EHC panel to test the 2 out of 3 logic circuits.

Updated Safety Analysis Report 10.2.3.6.1.1 states, in part that, turbine assembly inspection interval was selected on the basis of acceptably low probabilities [less than 1.0 E-5] of Perry turbine missile generation. Turbine missile generation probabilities are calculated by using either a methodology by General Electric or a methodology developed by Siemens-Westinghouse.

The methodology for determination of missile probability contains three major components:

-

The probability of the turbine attaining speeds higher than those occurring during normal operation.

-

The estimation of wheel burst probability as a function of speed.

-

The probability of wheel fragment penetrating the turbine casing and thus generating an external missile.

The inspectors reviewed the prompt functionality assessment contained in CR 2019-06321 and determined the licensee contracted with an outside vendor to assess the impacts of changing the turbine overspeed testing on turbine missile probability. The inspectors determined the missile probability analysis, to increase testing frequency from weekly to semi-annually, used a Monte Carlo methodology rather than a methodology by General Electric or Siemens-Westinghouse, as stated in USAR 10.2.3.6.1.1. The inspectors further concluded that the prompt functionality assessment documented that, the use of an alternate analytical method in lieu of the General Electric methodology is judged to be acceptable for this application and consistent with NRC Inspection Manual [Chapter (IMC)] 0326 Appendix C.04 guidance. The NRC inspectors noted that IMC 0326 was revised on October 1, 2019 and changed the Appendix C.04 guidance to Section 08 of IMC 0326.

Following review of the prompt functionality assessment the inspectors developed questions associated with the appropriateness to change USAR described testing frequencies using the prompt functionality assessment process rather than the 10 CFR 50.59 process. The licensee developed a white paper which established the following position.

Guidance for implementation of the requirements of 10 CFR 50.59 is addressed in FENOC procedure NOP-LP-4003 and FENOC Business Practice NOBP-LP-4003A. This procedure

[NOP-LP-4003] includes references to NRC Regulatory Guide (RG) 1.187, "Guidance for Implementation of 10 CFR 50.59, Changes, Tests, and Experiments and NEI 96-07, Revision 1, "Guidelines for 10 CFR 50.59 Implementation. In November 2000, RG 1.187 (Revision 0), endorsed Nuclear Energy Institute (NEI) 96-07, Revision 1, as acceptable for complying with the NRC regulations in 10 CFR 50.59.

The guidance provided in NEI 96-07 regarding applicability of 10 CFR 50.59 to nonconforming and degraded condition is addressed in section 4.4:

Three general courses of action are available to licensees to address non-conforming and degraded conditions. Whether or not 10 CFR 50.59 must be applied, and the focus of a 10 CFR 50.59 evaluation if one is required, depends on the corrective action plan chosen by the licensee, as discussed below:

If the licensee intends to restore the SSC back to its as-designed condition then this corrective action should be performed in accordance with 10 CFR 50, Appendix B (i.e., in a timely manner commensurate with safety). This activity is not subject to 10 CFR 50.59.

If an interim compensatory action is taken to address the condition and involves a temporary procedure or facility change, 10 CFR 50.59 should be applied to the temporary change. The intent is to determine whether the temporary change/compensatory action itself (not the degraded condition) impacts other aspects of the facility or procedures described in the UFSAR. In considering whether a temporary change impacts other aspects of the facility, a licensee should pay particular attention to ancillary aspects of the temporary change that result from actions taken to directly compensate for the degraded condition.

If the licensee corrective action is either to accept the condition as-is resulting in something different than its as-designed condition, or to change the facility or procedures, 10 CFR 50.59 should be applied to the corrective action, unless another regulation applies, e.g., 10 CFR 50.55a. In these cases, the final corrective action becomes the proposed change that would be subject to 10 CFR 50.59.

It is expected the degraded condition of the turbine overspeed protection test circuit ground will be restored to its as designed configuration in a timely manner commensurate with its safety significance. The less frequent test interval that is implemented by the PFA is not viewed to be a compensatory action for the degraded condition, as it does not restore or maintain functionality for the turbine overspeed trip test system. The PFA is not intended to accept the degraded condition as-is, or to change the facility or its procedures. As such, the less frequent turbine trip test interval that is implemented by the PFA was concluded to not require further review under 10 CFR 50.59.

Planned Closure Actions: The inspectors require further evaluation and assessment as to whether the change in overspeed testing frequency, i.e. non-performance on a weekly basis, constitutes a compensatory measure for the degraded equipment and required review in accordance with the 10 CFR 50.59 process. This review is to determine whether a violation exists. Thus, the issue is considered and unresolved item pending completion of inspector review and evaluation and discussion with the Office of Nuclear Reactor Regulation.

Corrective Action References: CR 2019-06321 Turbine Trip During Weekly Turbine Overspeed Test

Minor Violation 71124.03 Minor Violation: The inspectors identified that the licensee failed to perform fit testing, as required by 10 CFR 20.1703(c)(6), for all models and configuration of respirators used at its facility. Specifically, the licensee credited its fit testing of a full face respirator with a rubber strap enclosure for its SCBA type of respirator that is configured with a different harness (Kevlar harness closure system).

Screening: The inspectors determined the performance deficiency was minor. The failure to perform fit testing on each model of respirator was a performance deficiency, in that, the licensee failed to implement a regulatory requirement that was within the licensees ability to foresee and to prevent. The inspectors evaluated the performance deficiency against the criteria contained in IMC 0612. The inspectors determined that the performance deficiency was not a precursor to a significant event; if left uncorrected, did not have the potential to lead to a more significant safety concern; did not impact a performance indicator; and did not adversely affect the cornerstone objective to ensure adequate protection of the worker health and safety from exposure to radiation from radioactive material during routine civilian nuclear reactor operation. Specifically, the inspectors evaluated the potential for the differing configurations to impact the fit of the respirators. In addition, the licensee performed fit testing for individual for both models of respirators, which determined that results were acceptable when individuals were tested with both configurations. Based on the inspectors' review and the licensees testing data, the inspector concluded that differing configurations did not appear to reduce the licensees ability to control and limit the intake of airborne radioactivity and other hazards.

Enforcement:

Title 10 CFR 20.1703(c)(6) requires, in part, that the licensee implement and maintain a Respiratory Protection Program that includes fit testing before the first field use of tight fighting, face-sealing respirators and periodically thereafter at a frequency not to exceed one year. However, the licensees program did not perform fit testing prior to field use on the SCBA full face respirator with the Kevlar harness closure system as required by 10 CFR 20.1703(c)(6). Instead, the licensee performed fit testing on the air purifying style of respirator, with the rubber harness, and took credit for that fit test for the SCBA style of respirator, with the Kevlar harness. The licensee has restored compliance by performing fit testing using respirators with the Kevlar closure system.

The licensee entered this issue into the Corrective Action Program as AR 2018-09900.

This failure to comply with 10 CFR 20.1703(c)(6) constitutes a minor violation that is not subject to enforcement action in accordance with the NRCs Enforcement Policy.

The disposition of this violation closes URI: 05000440/2018004-03.

Observation: Semi-Annual Trend Review - Fire Protection System (Water)71152 The inspectors noted that the licensee had experienced two cases of clogged water spray nozzles during this inspection period. On October 9, 2019, CR 2019-08262 listed 13 clogged water spray nozzles found while performing a surveillance test of the water system protection for interbus transformer LH1A. On November 12, 2019, CR 2019-09579 listed three clogged water spray nozzles found while performing a surveillance test of the water system protection for interbus transformer LH2A. The CRs and/or associated test procedures did state that the nozzles were cleaned, and the surveillance tests successfully completed.

The inspectors knew that the spray systems for these outdoor transformers, after the water flow testing, are drained but usually some moisture remains in the steel lines. Since moisture and air produce an environment conducive to corrosion in carbon steel pipes and that there were two instances of clogged nozzles within an approximately one-month period, the inspectors initiated a search of the licensee's condition report system to determine if an adverse trend existed.

The inspectors originally searched CRs for period extending back eight months and then one year with no more reports of clogged water spray nozzles or internal corrosion of firewater spray lines. Then the inspectors searched back greater than four years since the flow testing of transformer spray nozzles is a once every 24 months test. During this expanded review, the inspectors did not identify any water spray nozzle clogging issues or instances of found clogging or fouling of nozzle spray supply lines.

The inspectors also noted that the number of found clogged spray nozzles would have degraded fire suppression capability but would not have incapacitated fire suppression capability for the interbus transformers. The inspectors did not identify an adverse trend associated with the design function of fire protection water spray nozzles and did not identify any concerns.

Observation: Review of Plant Aggregate Risk Assessment 71152 The inspectors reviewed the aggregated effects of operator burdens, workarounds, control room deficiencies and deficient conditions on plant risk. The inspection included a review of programmatic requirements and processes which resulted in discussions with operations and engineering personnel to determine whether the conditions identified, in aggregate, were manageable and being addressed in a timely manner commensurate with their safety significance. The inspectors reviewed the conditions, monitoring plans and trigger points to assess if the adverse conditions were being appropriately tracked and trended. The inspectors determined, overall, that the licensee was effectively managing adverse conditions and no concerns were identified as part of this review.

Observation: RCIC Steam Supply Second Drain Isolation Valve Leak Caused Secondary Containment Control Emergency Operating Procedure Entry 71152 On December 13, 2019, the control room received the RCIC Pump Room Sump Level High alarm and entered EOP-3, Secondary Containment Control, emergency operating procedure. The inspectors determined that the licensee dispatched an operator to the RCIC pump room and discovered that a previously identified steam leak from the RHR and RCIC Steam Supply Second Drain Isolation valve packing had degraded and that a real emergency did not exist. The inspectors reviewed condition reports, operation narrative logs, operational decision-making issues and the operations aggregate assessment of plant impacts from deficient conditions. The inspectors determined that prior to December 13, 2019, the steam leak on RHR and RCIC Steam Supply Second Drain Isolation valve had been identified three previous times. The inspectors reviewed work orders and notifications written as a direct result of the corrective action documents. In most cases the inspectors were able to determine that the licensee addressed each steam leak identification by adjusting the valve packing and either reducing or eliminating the leak. However, the inspectors noted that during the identification of the steam leak on August 25, 2019, the licensee was not able to eliminate the leak as documented in Notification 601236676, Packing Leak on RHR & RCIC Steam Supply.. The inspectors determined that the licensee put into place a method to monitor the leak using operator rounds and drained the associated sump as needed. During review of narrative logs the inspectors determined that the frequency between sump drains decrease from every two weeks in August to every two and a half days, on average, in December. The licensee documented the emergency procedure entry due to steam leak degradation in CR 2019-10360, Unplanned Entry Into EOP-03 Secondary Containment Control. Corrective actions identified following the EOP-3 procedure entry included continuing to monitor the steam leak using operator rounds but changed the sump drain frequency to shiftly. The steam leak was scheduled to be addressed during the system outage in January 2020. The inspectors did not identify any concerns as part of this review.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On January 17, 2020, the inspectors presented the integrated inspection results to Mr. F. Payne, Site Vice President and other members of the licensee staff.
  • On October 10, 2019, the inspectors presented the Emergency Preparedness Inspection inspection results to Mr. C. Elliott, Operations Manager and other members of the licensee staff.
  • On November 20, 2019, the inspectors presented the radiation protection baseline inspection results to Mr. F. Payne, Site Vice President and other members of the licensee staff.
  • On November 21, 2019, the inspectors presented the Emergency Action Level and Emergency Plan Changes Inspection inspection results to Mr. T. Kledzik, Emergency Response Supervisor and other members of the licensee staff.
  • On December 6, 2019, the inspectors presented the Heat Sink Performance inspection results to Mr. F. Payne, Site Vice President and other members of the licensee staff.
  • On December 17, 2019, the inspectors presented the Licensed Operator Requalification program annual examination results review inspection results to Mr. R. Torres, Fleet Exam Team Lead and other members of the licensee staff.
  • On January 17, 2020, the inspectors presented the integrated inspection results inspection results to Mr. F. Payne, Site Vice President and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.01

Procedures

ONI-ZZZ-1

Tornado or High Winds

Work Orders

200794255

Flood Mitigation Actions - ONI-ZZZ-1

71111.04Q Drawings

2-0641-00000

Residual Heat Removal System

KKK

2-0642-00000

Residual Heat Removal

NN

2-0643-00000

Residual Heat Removal System

CCC

2-0691-00000

Standby Liquid Control System

Z

2-0692-00000

Standby Liquid Control Transfer System

V

2-0791-00000

Emergency Service Water System

BBB

2-0792-00000

Emergency Service Water System

RR

2-0605-00000

Reactor Building Annulus Exhaust Gas Treatment

Y

2-0610-00000

Control Room HVAC and Emergency Recirculation System

CC

Procedures

SVI-E12-T1182B

RHR B LPCI Valve Lineup Verification and System Venting

VLI-C41

Standby Liquid Control System

VLI-E12

Residual Heat Removal System

VLI-M15

Annulus Exhaust Gas Treatment System

VLI-M25/M26

Control Room HVAC and Emergency Recirculation System

VLI-P45

Emergency Service Water System

71111.04S

Corrective Action

Documents

CR 2019-03480

Valve Indicates Open Testable Check Valve

04/12/2019

Drawings

2-0631-00000

Reactor Core Isolation Cooling System

HH

Procedures

VLI-E51

Reactor Core Isolation Cooling System

71111.05Q Fire Plans

FPI-0CC

Control Complex

FPI-0EW

Emergency Service Water Pump House

FPI-0IB

Intermediate Building

FPI-1AB

Auxiliary Building Unit 1

FPI-1DG

Diesel Generator Building Hallway

Procedures

PAP-1910

Fire Protection Program

Work Orders

200717072

Portable Fire Extinguishers Maintenance Inspection

05/09/2019

71111.06

Calculations

IF-8

Flood Zone 21: Critical Volumes, Flood Heights, Flow Rates,

Flood and Alarm Chronology

JL-083

Flooding Analysis of CCB, IB, and FHB - Floor Elevation

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

574'-10"

Drawings

105-0013-00000

Control Complex Floor Plan - El. 620'-6"

K

304-0804-00000

ESW - Control Buillding Plan Above 574'-10"

l

Miscellaneous

PRA-PY1-AL

Internal Flooding Notebook

Procedures

ARI-H13-P970-

0001

Common Long Response Benchboard

ONI-R10

Loss of AC Power

71111.07A

Calculations

E22-042

Division 3 Emergency Diesel Generator Jacket Water Heat

Exchanger Performance Test

Work Orders

200645158

HPCS Diesel Generator Jacket Water Heat Exchanger

Performance Testing

06/04/2019

71111.07T

Calculations

E12-089

Required ESW Flow for the RHR HXs

E12-102

RHR System Heat Exchanger "B" Loop Performance Test

Evaluation

P42-039

Design Basis Heat Load & Required ESW Flow for the ECC

HXs

P42-051

Emergency Closed Cooling Heat Exchanger "B" Loop

Performance Test Evaluation

P45-044

Keepfill Check Valve Leak Rate/Standpipe Draindown Level

Corrective Action

Documents

CR-2011-91278

Results of ESW Related Diver Inspections (March 2011)

03/18/2011

CR-2016-09504

Emergency Service Water (ESW) Loop "C" Flow Rates

Degraded

08/03/2016

CR-2016-12106

High Pressure Core Spray Emergency Service Water Flow

in the Alert Low Range

10/10/2016

CR-2017-07247

Received ESW to RHR HX Flow Low Annunciator Alarm

07/07/2017

CR-2017-09641

Silt Levels in Emergency Service Water (ESW) East and

West Pump Bays

09/19/2017

CR-2018-08003

Small Margin Remaining in RHR Heat Exchanger Loop "B"

09/10/2018

CR-2018-08122

Silt Levels in Emergency Service Water East and West

Pump Bays and Forebay

09/14/2018

Corrective Action

Documents

Resulting from

Inspection

CR-2019-10102

2019 Triennial Heat Sink Inspection: Drawing 21-0016-

00001 Rev. B has Incorrect Work Order Listed

2/03/2019

CR-2019-10124

2019 Triennial Heat Sink Inspection: Housekeeping

Deficiencies Identified in RHR B HX Room 599' and RHR B

2/04/2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Pump Room 574'

CR-2019-10148

2019 Triennial Heat Sink Inspection: Silt Data not Recorded

in Order 200725355 for Intake and Discharge Structures in

the Lake

2/05/2019

CR-2019-10155

2019 Triennial Heat Sink Inspection: CR not Written on Silt

Buildup in Forebay at Time of Diver Inspection for WO 200474126

2/05/2019

CR-2019-10165

2019 Triennial Heat Sink Inspection: Global EMARP-0011

Concerns

2/05/2019

CR-2019-10175

2019 NRC Triennial Heat Sink Inspection, Documentation

for Heat Exchanger Bracing Adequacy can not be Located

2/06/2019

CR-2019-10185

2019 Triennial Heat Sink Inspection: Inadequate Technical

Justification for Deferral of RHR B Eddy Current and Visual

Inspections

2/06/2019

CR-2019-10233

2019 Triennial Heat Sink Inspection: Roll Up CR

2/09/2019

Drawings

015-0002

Emergency Service Water Pump House Plans and

Elevations

F

21-0016-00002

Residual Heat Removal Heat Exchanger 1E12B001B Tube

Sheet Drawing

A

2-0140-00002

Emergency Closed Cooling Heat Exchanger Loop "B"

(1P42B0001B) Tube Sheet Drawing

A

304-0791

Emergency Service Water Piping

T

743-0013

Topography and Storm Drain

G

D-726-210

Offshore Multiport Intake Structure

M

D-726-213

Discharge Structure

E

Engineering

Evaluations

Spec-625

Seismic Qualification Report for Emergency Closed Cooling

Water Heat Exchangers

Miscellaneous

600925874

Revision Notification for First Time Performance -

1E12B0001B/D

04/27/2015

601199944

Revision Notification for Performing PM Less Often -

1E12B0001B

2/31/2018

DI-220

Perry Nuclear Power Plant RHR Heat Exchanger

Performance Program

EMARP-0011

North and West Intake Structures and Discharge Structure

11/13/2017

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Emergency

Service Water

Monitoring

Program Report

Sheet

Inspections

EMARP-0011-

Emergency

Service Water

Monitoring

Program Report

Sheet

Visual Inspection of Emergency Service Water

Pump/Forebay and ESW Normal/Alternate Tunnel

11/27/2017

Procedures

D-726-201

Intake Tunnel Plan and Profile

E

EMARP-0011

Emergency Service Water System Monitoring Program

IOI-0015

Seasonal Variations

ONI-P40

ESW or SW Sunction Path Blockage

ONI-P41

Loss of Service Water

PTI-GEN-P0024

Mussel Treatment

PTI-P45-P0004

Emergency Service Water Manual Valve Operability Test

PTI-P45-P0009A

ESW Forebay Low Level Functional for P45-D004A

SOI-E12

Residual Heat Removal System

SOI-P42

Emergency Closed Cooling System

SOI-P45/P49

Section 7.2

Emergency Service Water and Screen Wash Systems

Work Orders

200208230

Cal Check - ESW Keep Fill Pressure Gauge

05/16/2008

200294673

Calibrate Pressure Gauge Per ICI-B2-0, SEE 302-792, ESW

Keep Fill Line

2/27/2007

200342060

Eddy-Inspect/Clean P42 HX

05/05/2011

200428423

(4Y) RHR Heat Exchangers B and D Performance Testing

11/19/2014

200474126

Inspect ESW Forebay and Normal Intake Tunnel

10/24/2017

200474126

Inspect ESW Forebay and Normal Intake Tunnel

10/24/2017

200518858

Inspect ESW Forebay and Normal Intake Tunnel

09/07/2018

200553883

Inspect East/West Pump Bay and Alternate Intake Tunnel

10/23/2017

200560618

(4Y) Emergency Closed Cooling B Heat Exchanger

Performance Testing

11/09/2015

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

200617665

Inspect East/West Pump Bay and Alternate Intake Tunnel

2/05/2018

200624207

(4Y) RHR Heat Exchangers B and D Performance Testing

09/04/2018

200632868

Emergency Service Water Manual Valve Operability Test

03/03/2017

200656789

Inspect SW/ESW Intake/Discharge Ports

08/09/2016

200656790

Inspect SW/ESW Intake/Discharge Ports

09/13/2017

200661237

ESW System Loop C Flow and Differential Pressure Test

07/08/2019

200690654

Lube/Megger ESW Intake Screen "B" Motor

07/23/2018

200710562

ESW Pump B and Valve Operability Test

04/30/2019

200711981

Inspect SW/ESW Intake/Discharge Ports

09/12/2018

200712729

Emergency Service Water Manual Valve Operability Test

10/06/2018

200714996

ESW Loop A Flow and Differential Pressure Test

04/24/2019

200718770

ESW System Loop and Differential Pressure Test

06/08/2019

200718850

ESW Pump B and Valve Operability Test

08/16/2019

200725357

ESW Forebay Low Level Funtional for P45-D004B

10/14/2018

200728962

(92D) ESW System Loop B Flow and Differential Pressure

Test

08/30/2019

200728965

ESW System Loop A Flow and Differential Pressure Test

07/21/2019

200729052

HPCS ESW Pump and Valve Operability Test

07/08/2019

200764994

Cal Check - Keep Fill Pressure Gauge HPCS ESW

07/09/2019

98-826

RHR B/D HX Inspection

04/06/1999

71111.11A

Miscellaneous

Perry Annual Licensed Operator Requalification Program

Summary Results for 2019

2/16/2019

71111.11Q Miscellaneous

Evolution Specific

Reactivity Plan

December 2019 Power Suppression Test

OT-3070 RP2E

Simulator Scenario Guide

OT-3070-005-

RP1B

Simulator Scenario Guide

71111.12

Corrective Action

Documents

CR 2018-10660

HPCS Agastat TD Relay Outside Times Permitted but

Within Allowable TS Times

2/04/2018

CR 2018-11210

AEGTS Train A Flow Oscillations

2/24/2018

CR 2019-02590

Valve PMT Stroke Issue - Contact Problem on Switch

1C61S0080

03/21/2019

CR 2019-05821

Diesel Procedure Step Performed Out of Order

07/09/2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

CR 2019-09208

RHR B Containment Spray 1st Isolation Valve Lost all

Position Indication

11/01/2019

CR 2019-09212

Combustible Gas Mixing Compressor B Trip on Thermal

Overloads

11/01/2019

CR 2019-09358

10CFR21-2017: EMD Fuel Injector - Seized Plunger and

Bushing

11/05/2019

CR 2019-09378

Div 3 DG Tripped on Reverse Power

11/05/2019

CR 2019-09421

Common Cause Evaluation for Division 3 DG Inoperability

11/06/2019

Corrective Action

Documents

Resulting from

Inspection

CR 2019-10361

Maintenance Rule Evaluation Required on 1E12F0024B and

1C61-S80

2/13/2019

CR 2019-10375

NRC Identified: Infantile Failure of 1C61S0080 - November

2018 to March 2019

2/13/2019

CR 2019-10523

NRC Identified: CR 2019-09212 Maintenance Rule

Evaluation Conclusion was Questioned

2/19/2019

Drawings

208-0039-00004

Remote Shutdown System Division 2 Switch Development

and Locations

L

208-0055-00025

Containment Spray Valve - F028B

Y

208-0055-00036

RHR "B" Test Return MOV F024B

V

208-0206-00037

4.16KV Bus EH13 Diesel Brkr. EH1301

Z

Miscellaneous

A Miniature Instrument & Control Switch for Power Industry

Applications (ElectroSwitch)

11/05/1984

Maintenance Rule

System Basis

Document System

E_C

System Name: Electrical Component Group - Indication

Notification

601219728

BLC2000-721 Control Unit (Blind Controller) Qualification

Report

PY-M51-F-1610

Combustible Gas Control Function Basis Document

Procedures

GEI-0046

Division 3 125Vdc Relays

GEI-0100

Maintenance and Calibration of Power Relay 12ICW52B

NOP-ER-3004

FENOC Maintenance Rule Program

PYBP-PES-0001

Maintenance Rule Reference Guide

SVI-C61-T1202

Remote Shutdown Control Test - Division 2 RHR, ECC, and

ESW

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

SVI-M51-T2003-B

Combustible Gas Mixing System B Operability Test

Work Orders

200341689

Inspect Remote Shutdown Switch 1C61A-S80 as Extent of

Condition for CR 08-46021

11/14/2018

200516341

Relay ICW52B 32B EH13 Bus Reverse Power

2/17/2018

200701831

PY-1E2207038 Cal Check Agastat E7000 TD Relay

05/06/2019

200713648

Perform Static MOV [Motor Operated Valve] Test RHR 'B'

Test VLV [Valve] to Supr [Suppression] Pool

03/21/2019

200730436

Replace PY-1M15R0060B-1 Annulus Differential Pressure

Controller B

200752416

PY-1E2207032 - Calibrate Agastat E7000 DC TD Relay

05/06/2019

200775158

Troubleshoot Cause of AEGTS Train A Flow Oscillations

200775159

Replace Control Unit

200775160

Bailey 721 Controller Non-Safety Stock Code 90895255 to

be Dedicated to Allow Use as Commercial Grade Stock

Code 100027602

200783496

Post Maintenance Testing of Valve 1E12F0024B per Order

200713648 Identified that the Valve would not Stroke Closed

03/21/2019

200804189

While Stroking Open E12F028B for the Div 2 Combustible

Gas Mixing Compressor Run, Valve E12-F028B Lost All

Indication

11/01/2019

200804866

Div 3 DG Tripped on Reverse Power

11/06/2019

WO 200804216

Combustible Gas Mixing System Compressor B Tripped on

Thermal Overloads

11/04/2019

71111.13

Corrective Action

Documents

CR2019-09378

Div 3DG Tripped on Reverse Power

11/05/2019

Procedures

NOP-OP-1007

Risk Management

SVI-E22-T1319

Diesel Generator Start and Load Division 3

Work Orders

200542705

Perform Static MOV Test for RHR C Minimum Flow Valve

200574288

Control Room HVAC

200749548

Perform Static MOV Test for the RHR C Suppression Pool

Suction Valve

200804866

Div 3 DG Tripped on Reverse Power

11/06/2019

71111.15

Corrective Action

Documents

CR-2019-09208

RHR B Containment Spray 1st Isolation Valve Lost All

Position Indication

11/01/2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

CR-2019-09228

Inability to Select Control Rods

11/01/2019

Drawings

208-0055-00025

Residual Heat Removal System, Containment Spray Valve -

F028B

Y

Procedures

NOP-OP-1009

Operability Determinations and Functionality Assessments

SOI-C11(RCIS)

Rod Control and Information System

71111.18

Calculations

H-1G33-112

Design Verification Record of 1G33-Reactor Water Cleanup

System

Corrective Action

Documents

CR 2015-08036

PFA [Prompt Functionality Assessment] Needed for Site

Flooding Issues

07/08/2015

CR 2019-03298

Reactor Water Cleanup Drain Valves (G33F066) Leaking By

04/08/2019

Corrective Action

Documents

Resulting from

Inspection

CR 2019-10368

Discrepancy Between Intermediate Building Roof Drawing

and Calculation Live Load

2/13/2019

Engineering

Changes

19-0178-001

Interim Flooding Protection for Plant Structures - Ground

Level Vulnerabilities

19-0178-002

Temporary Roof Protection for Flood Mitigation

ECP No. 19-0091-

000

Engineering Change Package Design Report to Change the

Safety/Quality Classification of Selected Piping for Test,

Vent, and Drain Connections to ASME Class 1, 2, or 3

Piping to Non-Nuclear Safety (NNS)/quality Group D

Engineering

Evaluations

NORM-LP-7322

Perry Nuclear Power Plant Flooding Focused Evaluation

Report

11/22/2019

Notification

601216082

Evaluate Kill of Downstream Pipe/Cap

04/09/2019

Miscellaneous

TCC-1-G33-LR-

2

Temporary Configuration Change that Installs a Line Kill

Procedures

ONI-ZZZ-1

Tornado or High Winds

PAP-0204

Housekeeping/Cleanliness Control Program

Work Orders

200794255

Flood Mitigation Actions - ONI-ZZZ-1

200799298

Stage Sandbags at Gross Openings (Vents, Louvres,

Penetrations) and Roof Door Openings

09/17/2019

WO 200785169

Penetration P131 Outboard Test Connection Second

04/16/2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Isolation Valve

71111.19

Drawings

208-0055-00025

Residual Heat Removal System, Containment Spray Valve -

F028B

Y

Procedures

SVI-E12-T2002

RHR B Pump and Valve Operability Test

Work Orders

200290508

Replacing the 1C71K051C Relay for Scram Discharge

Volume Level Hi

11/07/2019

200753726

SVI-C11-T1003B Control Rod Exercise Part 2

11/02/2019

200753785

SVI-C11-T1103A Control Rod Exercise Part 1

11/02/2019

200770274

Emergency Closed Cooling Pump "A"

11/18/2019

200804181

Inability to Select Control Rods

11/02/2019

200804189

Containment Spray B First Shutoff

11/01/2019

71114.02

Miscellaneous

FEMA Approval Letter for Perry Nuclear Power Plant Prompt

Alert Siren System (PASS) Design Report Update, Revision

07/17/2015

Perry EPZ Siren Test Data

09/01/2017-

09/30/2019

Perry 2017 EPZ Siren Annual Maintenance Records

09/01/2017 -

2/31/2017

Perry 2018 EPZ Siren Annual Maintenance Records

01/01/2018 -

2/31/2018

Federal Signal Models 2001-130, Equinox, and 508-128

Sirens Installation, Operation, and Service Manual

A5 0017

Tempest T-112/ T-121 Omni-Directional Siren Installation,

Operation, Maintenance and Parts Manual

H

Perry EPZ Siren PI Test Schedules

09/01/2017-

2/31/2019

Procedures

Perry Nuclear Power Plant Prompt Alert Siren System

(PASS) Design Report

NOBP-LP-5018

FENOC Siren Testing and Maintenance

NOP-LP-5005

FENOC Siren Testing and Maintenance

PTI-GEN-P0003

Quarterly Testing of the Emergency Pager System

71114.03

Corrective Action

Documents

CR-2018-07283

ERO Drill - During 8/15/2018 Drill Objective B.1, Notification

of ERO Personnel Not Met

08/16/2018

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

CR-2019-04530

ERO Drill - Objective B.1 Not Met - ERO Not Notified in

Minutes

05/20/2019

Miscellaneous

Technical Support Center Equipment Checklists (Completed

Survey Records)

2/01/2018 -

09/30/2019

Emergency Response Organization Roster

09/20/2019

ERO Augmentation Quarterly Pager Test Records

09/01/2017 -

09/30/2019

Emergency Operations Facility Equipment Checklists

(completed survey records);

2/01/2018 -

09/30/2019

Procedures

NOP-LP-5006

Emergency Response Organization Training Program

PYBP-ERS-0037

Notification of Key Plant Personnel

71114.04

Miscellaneous

Perry Station 10 CFR 50.54(q) Evaluator Qualification and

Training Records Spreadsheet

06/25/2019

PY-2019-013-00

CFR 50.54(q)2

Analysis

Emergency Plan Change - Public Information Response

Team Relocation

05/22/2019

PY-2019-013-00

CFR 50.54(q)3

Screen/Evaluation

Emergency Plan Change - Public Information Team

Relocation

06/03/2019

PY-2019-06-00 10

CFR 50.54(q)2

Analysis

Emergency Plan Change - Elimination of EOF Plant

Operations Assistant Position

04/30/2019

PY-2019-06-00

CFR 50.54(q)3

Screen/Evaluation

Emergency Plan Change - Elimination of EOF Plant

Operations Assistant Position

04/30/2019

PY-2019-09-00 10

CFR 50.54(q)2

Analysis

Emergency Plan Revision 53 - Editorial Changes

05/22/2019

PY-2019-09-00 10

CFR 50.54(q)3

Screen/Evaluation

Emergency Plan Revision 53 - Editorial Changes

05/22/2019

Procedures

EP-0000

Emergency Plan for Perry Nuclear Power Plant

EP-0000

Emergency Plan for Perry Nuclear Power Plant

NOP-LP-5002

Evaluation of Changes to Emergency Plans and Supporting

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Documents 10 CFR 50.54(q)

71114.05

Corrective Action

Documents

CR-2017-11819

Lake County Letter of Agreement was Expired for Two

Months

11/30/2017

CR-2018-05456

ERO Drill 6-6-18: Objective F.6 Not Met - Release Start

Time

06/12/2018

CR-2018-07292

ERO Drill: Objective C1 - Not Met, Failure to Notify Offsite

Agencies within 15 Minutes

08/17/2018

CR-2018-08213

ERO Exercise - Objective U11 and U12 Not Met - Dose

Assessment

09/18/2018

CR-2018-08245

ERO Exercise - Objective C.2 Demonstrate Ability to Notify

NRC within One Hour Not Met

09/19/2018

CR-2018-08276

ERO Exercise - Weaknesses in Dose Assessment

09/19/2018

CR-2018-08293

ERO Exercise - Objective K.7 Not Met - Accuracy of Alert

News Statement

09/20/2018

CR-2018-09836

10/18/18 EOF General Emergency Classification Made

Using Alternate EAL

11/06/2018

CR-2019-00834

Negative Trend Noted in Drill & Exercise Performance for

the Month of January 2019

01/28/2019

CR-2019-04480

ERO Drill - Objective E.6 Was Not Met During 5/15/2019

Integrated Drill

05/17/2019

CR-2019-04730

Protective Action Flow Chart Recommendation

05/18/2019

Corrective Action

Documents

Resulting from

Inspection

CR-2019-08255

NRC EPlan Inspection: NOBP-LP-5018 "FENOC Siren

Testing and Maintenance" Scope of Review Discrepancy

10/09/2019

Miscellaneous

Letters of Agreement with Agencies Supporting Emergency

Preparedness (Sample)

09/01/2017 -

09/30/2019

Emergency Preparedness Drill and Exercise Records

(Sample)

09/01/2017-

09/30/2019

Emergency Response Organization Training and

Qualification Records (Sample)

10/10/2019

KLD TR-1029

Perry Nuclear Power Plant 2018 Population Update Analysis 09/27/2018

KLD TR-481

Perry Nuclear Power Plant Development of Evacuation Time

Estimates

10/01/2012

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

KLD TR-997

Perry Nuclear Power Plant Evacuation Time Estimate

Sensitivity Study Due to the Vrooman Road Closure

05/04/2018

Procedures

Emergency Plan for Perry Nuclear Power Plant

PYBP-ERS-0003

Emergency Plan Facility/ Equipment Inventory Checklists

Self-Assessments MS-C-17-11-24

Fleet Oversight Audit Report of Emergency Preparedness

2/08/2017

MS-C-18-11-24

Fleet Oversight Audit Report of Emergency Preparedness

2/07/2018

71124.02

ALARA Plans

190522

1R17 Bioshield ISI Activities

190903

1R17 In Vessel Inspection Activities

190904

1R17 Reactor Reassembly Activities

0-4

Corrective Action

Documents

CR 2019-02298

Hydraulic Oil Spill into Refueling Cavity

03/13/2019

CR 2019-02512

In Vessel Inspection Outage Project Elevated Dose Levels

03/19/2019

CR 2019-02607

1R17 Bioshield ISI RWP 190522 Estimate Challenged

03/21/2019

CR 2019-03322

1R17 Elevated Reactor Cavity Dose Rates after Second

Draindown

04/08/2019

Miscellaneous

1R17 Outage Alara Report

06/12/2019

190522

1R17 Bioshield ISI Work in Progress Reviews

190522

1R17 Bioshield ISI Activities Alara Post Job Review

08/19/2019

190903

1R17 In Vessel Inspection Activities Work in Progress

Reviews

190903

1R17 In Vessel Inspection Activities Alara Post Job Review

08/20/2019

190904

1R17 Reactor Reassembly Activities Work in Progress

Reviews

0-4

190904

1R17 Alara Post Job Review

07/24/2019

Procedures

NOP-OP-4107

Radiation Work Permits

Radiation Work

Permits (RWPs)

190522

1R17 Bioshield ISI Activities

190903

1R17 In Vessel Inspection Activities

190904

1RF17 Reactor Reassembly Activities

0-4

71151

Miscellaneous

NRC Performance Indicator Data; Emergency Preparedness

- Drill/Exercise Performance (DEP)

07/01/2018 -

06/30/2018

NRC Performance Indicator Data; Emergency Preparedness

- ERO Readiness

07/01/2018 -

06/30/2019

NRC Performance Indicator Data; Emergency Preparedness

- Alert and Notification System Reliability

07/01/2018 -

06/30/2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

NOBP-LP-4012-

Reactor Coolant System Leakage

10/01/2018 -

09/30/2019

Procedures

NOBP-LP-4012

NRC Performance Indicators

71152

Corrective Action

Documents

CR 2018-08732

2018 NRC Fire Protection Inspection - Obstructed Sprinkler

Head on CC-574 Overhead Suppression System

10/04/2018

CR 2018-08805

Motor Fire Pump Pin Hole Leak Downstream of Pump Relief

Valve

10/07/2018

CR 2019-01465

Packing Leak Has Returned on RHR & RCIC Steam Supply

Second Drain Isolation Valve

2/18/2019

CR 2019-05479

Packing Leak on RHR & RCIC Steam Supply Second Drain

Isolation Valve

06/25/2019

CR 2019-07109

Packing Leak on RHR & RCIC Steam Supply

08/25/2019

CR 2019-08262

L -H-1-A Clogged Nozzles Found During Deluge Test PTI-

P54-P0064A

10/09/2019

CR 2019-09579

Three Clogged Nozzles Discovered During Interbus

Transformer LH2A Deluge Testing per PTI-P54-P0065A

11/12/2019

Drawings17-936 Sh37

Interbus Transformer Plan View

05/30/1980

Procedures

NOBP-OP-0012

Operator Work-Arounds, Burdens, Control Room

Deficiencies and Operations Aggregate Assessment

NOP-LP-2001

Corrective Action Program

NOP-OP-1009

Operability Determinations and Functionality Assessments

NOP-OP-1010

Operational Decision-Making

PAP-1910

Fire Protection Program

PTI-P54-P0064A

Water Spray Flow Test for Unit 1 Interbus Transformer A

SOI-P54 (WTR)

Fire Protection System - Water

Work Orders

200694434

PTI-P54P0065A LH-2-A Spray Flow Test

11/11/2019