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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20029D6631994-05-0303 May 1994 LER 94-003-00:on 940405,loss of Shutdown Cooling Occurred Due to an Inadvertent High Reactor Pressure Isolation Signal.Corrective Action:Operations Department Procedure Used to Restore Shutdown Cooling isolations.W/940503 Ltr ML20029C7501994-04-20020 April 1994 LER 94-001-01:on 940305,ESF Actuation/Isolation & Loss of Shutdown Cooling Occurred.Caused by Personnel Error. Technician counseled.W/940420 Ltr ML20045B4761993-06-14014 June 1993 LER 93-004-00:on 930516,component Failure in EHC Sys Resulted in Generator/Turbine Trip & Reactor Scram.Failed Components Replaced & Addl Monitoring Devices Installed on EHC sys.W/930614 Ltr ML20045B2861993-06-0909 June 1993 LER 93-003-00:on 930513,plant Transient Initiated When 13.8 Kv Pothead Failed,Inducing Voltage Drop & Phase Differential Relay Actuation Due to Loss of Offsite Power on 2 of 4 Vital Buses.Failed Pothead replaced.W/930609 Ltr ML20029C2071991-03-21021 March 1991 LER 91-005-00:on 910219,reactor Scram Relay Malfunction Resulted in Startup Level Control Valve Failing Closed. Caused by Failure of Relay Controlling Position of Rfw 12 Startup Level Control Valve.Relay replaced.W/910321 Ltr ML20029A6441991-02-25025 February 1991 LER 91-003-00:on 910125,channel C Primary Containment Isolation Sys Actuated,Resulting in Trip of Radwaste Area Supply & Exhaust Fans.Caused by Design Deficiency Re Steam Leak Detection Sys Cabinets.Fuse replaced.W/910225 Ltr ML20028H8531991-01-23023 January 1991 LER 90-035-00:on 901227,pipe Section on Svc Water Sys (Ssws) a Loop Developed Minor Through Wall Flaw.Caused by Pipe Corrosion.Pipe Section on Ssws Will Be Replaced Prior to Restart from Current Refueling outage.W/910123 Ltr ML20028H6781991-01-16016 January 1991 LER 90-025-01:on 901104,leak Discovered on Weld on Reactor Recirculation Instrument Line While Investigating Source of Drywell Leakage.Caused by Crack at Welded Joint Due to vibration-induced Fatigue.Line replaced.W/910116 Ltr ML20043F4521990-06-11011 June 1990 LER 90-007-00:on 900517,control Room Received Indication of Half Scram & Isolation of Inboard Reactor Water Cleanup Isolation Valve.Caused by Spurious Trip of Channel a Reactor Protection Sys Epa.Design Change implemented.W/900611 Ltr ML20043F6121990-06-11011 June 1990 LER 90-006-00:on 900512,filtration,recirculation & Ventilation Sys Recirculation Fan E Discovered Running by Nuclear Control Operator.Cause Not Determined.Work Orders Initiated to Inspect Flow switches.W/900611 Ltr ML20043A8691990-05-16016 May 1990 LER 90-004-00:on 900418,ground Fault on Motor Control Ctr Feeder Breaker Occurred & Resulted in de-energization of Reactor B Protection Sys.Cause Not Determined.Feeder Breaker & Trip Device replaced.W/900516 Ltr ML20043A9091990-05-16016 May 1990 LER 90-005-00:on 900419,determined That Inoperability of Liquid Radwaste Discharge Monitor Not Reported in Recent Radioactive Effluent Release Rept.Caused by Procedural Deficiency.Effluent Rept revised.W/900516 Ltr ML20012C5991990-03-15015 March 1990 LER 89-026-01:on 891231,leak from Weld on 1-inch Reactor Recirculation Sys Elbow Tap Flow Transmitter Instrument Line Joint Discovered.Caused by Equipment Failure Due to Installation Deficiency During Plant const.W/900315 Ltr ML20006F8651990-02-19019 February 1990 LER 90-002-00:on 900119,HPCI Outboard Steam Supply Isolation Valve Auto Closed on High Room Differential Temp Signal. Caused by Inoperative Temp Control Loop.Troubleshooting of Loop Initiated to Determine malfunction.W/900219 Ltr ML20011E3931990-02-0505 February 1990 LER 90-001-00:on 900106,turbine Trip on Moisture Separator High Level Resulted in Reactor Scram.Caused by Combination of Equipment Failure & Cognitive Personnel Errors.Moisture Separator Drain Control Instrumentation tuned.W/900205 Ltr ML20006C2571990-01-30030 January 1990 LER 89-026-00:on 891231,leak from Weld on Reactor Recirculation Sys Flow Transmitter Instrument Line Joint Discovered.Cause Not Stated.Instrument Line Cut Out & Replaced W/New Section of piping.W/900130 Ltr ML20011E1301990-01-29029 January 1990 LER 89-025-00:on 891230,turbine Trip Occurred During Performance of Main Turbine Thrust Bearing Wear Detector Surveillance.Caused by Malfunction of Limit Switch.Design Change Implemented for Keylock Bypass switch.W/900129 Ltr ML20005E2401989-12-28028 December 1989 LER 89-024-00:on 891129,determined That Surveillance Frequency for Safety Auxiliaries Cooling Sys Valve EG-HV-2302B Should Have Been Increased.Caused by Data Recording Error.Personnel counseled.W/891228 Ltr ML20005E2421989-12-27027 December 1989 LER 89-021-01:on 891013,concluded That Class 1E Electrical Separation Criteria Not Met in Reactor Protection Sys Panel. Caused by Inadequate Review of 1986 Design Change Package. Nonconforming Power Supplies removed.W/891227 Ltr ML19332E7931989-12-0606 December 1989 LER 89-022-01:on 891016,reactor Protection Sys Electric Protection Assemblies Opened,Resulting in Loss of RHR B Which Had Been Operating in Shutdown Cooling Mode.Caused by Low Voltage Output.Assemblies reset.W/891206 Ltr ML19332E8131989-12-0404 December 1989 LER 89-023-00:on 891104,full Reactor Protection Sys Signal Inadvertently Generated While Pressurizing Drywell,Resulting in Full Scram Signal.Caused by Procedural Deficiency. Integrated Leak Rate Test Procedure revised.W/891204 Ltr ML19327C2561989-11-15015 November 1989 LER 89-022-00:from 891016-27,scrams Experienced on Channel B Reactor Protection Sys Electric Assemblies & Nuclear Steam Supply Shutdown Sys Isolated,Resulting in Loss of Shutdown Cooling.Assemblies & Output Voltages reset.W/891115 Ltr ML19327C2701989-11-13013 November 1989 LER 89-020-00:on 891011,pressure Spike in Reactor Vessel Ref Leg Resulted in ESF Actuation During Filling & Venting of Pressure Transmitter.Caused by Personnel Error.Technicians Counseled & Retrained in Venting procedures.W/891113 Ltr ML19327C2711989-11-13013 November 1989 LER 89-021-00:on 891013,review of GE Transient Analysis Recording Sys Determined That Class 1E Electrical Separation Criteria Not Met in Two Reactor Protection Sys Panels. Nonconforming Power Supplies removed.W/891113 Ltr ML19354D4411989-11-0303 November 1989 LER 89-019-00:on 891004,inadequate Instrumentation Used on Core Spray Pumps for ASME Section XI Testing.Caused by Inadequate Design Change Package.Event Reviewed W/Station Inservice Testing engineer.W/891103 Ltr ML19325E8811989-11-0202 November 1989 LER 89-018-00:on 891003,determined That Two Tech Spec Required Readings Not Taken as Required When Vent Monitoring Sys Inoperable on 890929.Caused by Lack of Adequate Communication.Personnel Involved counseled.W/891102 Ltr 1994-05-03
[Table view] Category:RO)
MONTHYEARML20029D6631994-05-0303 May 1994 LER 94-003-00:on 940405,loss of Shutdown Cooling Occurred Due to an Inadvertent High Reactor Pressure Isolation Signal.Corrective Action:Operations Department Procedure Used to Restore Shutdown Cooling isolations.W/940503 Ltr ML20029C7501994-04-20020 April 1994 LER 94-001-01:on 940305,ESF Actuation/Isolation & Loss of Shutdown Cooling Occurred.Caused by Personnel Error. Technician counseled.W/940420 Ltr ML20045B4761993-06-14014 June 1993 LER 93-004-00:on 930516,component Failure in EHC Sys Resulted in Generator/Turbine Trip & Reactor Scram.Failed Components Replaced & Addl Monitoring Devices Installed on EHC sys.W/930614 Ltr ML20045B2861993-06-0909 June 1993 LER 93-003-00:on 930513,plant Transient Initiated When 13.8 Kv Pothead Failed,Inducing Voltage Drop & Phase Differential Relay Actuation Due to Loss of Offsite Power on 2 of 4 Vital Buses.Failed Pothead replaced.W/930609 Ltr ML20029C2071991-03-21021 March 1991 LER 91-005-00:on 910219,reactor Scram Relay Malfunction Resulted in Startup Level Control Valve Failing Closed. Caused by Failure of Relay Controlling Position of Rfw 12 Startup Level Control Valve.Relay replaced.W/910321 Ltr ML20029A6441991-02-25025 February 1991 LER 91-003-00:on 910125,channel C Primary Containment Isolation Sys Actuated,Resulting in Trip of Radwaste Area Supply & Exhaust Fans.Caused by Design Deficiency Re Steam Leak Detection Sys Cabinets.Fuse replaced.W/910225 Ltr ML20028H8531991-01-23023 January 1991 LER 90-035-00:on 901227,pipe Section on Svc Water Sys (Ssws) a Loop Developed Minor Through Wall Flaw.Caused by Pipe Corrosion.Pipe Section on Ssws Will Be Replaced Prior to Restart from Current Refueling outage.W/910123 Ltr ML20028H6781991-01-16016 January 1991 LER 90-025-01:on 901104,leak Discovered on Weld on Reactor Recirculation Instrument Line While Investigating Source of Drywell Leakage.Caused by Crack at Welded Joint Due to vibration-induced Fatigue.Line replaced.W/910116 Ltr ML20043F4521990-06-11011 June 1990 LER 90-007-00:on 900517,control Room Received Indication of Half Scram & Isolation of Inboard Reactor Water Cleanup Isolation Valve.Caused by Spurious Trip of Channel a Reactor Protection Sys Epa.Design Change implemented.W/900611 Ltr ML20043F6121990-06-11011 June 1990 LER 90-006-00:on 900512,filtration,recirculation & Ventilation Sys Recirculation Fan E Discovered Running by Nuclear Control Operator.Cause Not Determined.Work Orders Initiated to Inspect Flow switches.W/900611 Ltr ML20043A8691990-05-16016 May 1990 LER 90-004-00:on 900418,ground Fault on Motor Control Ctr Feeder Breaker Occurred & Resulted in de-energization of Reactor B Protection Sys.Cause Not Determined.Feeder Breaker & Trip Device replaced.W/900516 Ltr ML20043A9091990-05-16016 May 1990 LER 90-005-00:on 900419,determined That Inoperability of Liquid Radwaste Discharge Monitor Not Reported in Recent Radioactive Effluent Release Rept.Caused by Procedural Deficiency.Effluent Rept revised.W/900516 Ltr ML20012C5991990-03-15015 March 1990 LER 89-026-01:on 891231,leak from Weld on 1-inch Reactor Recirculation Sys Elbow Tap Flow Transmitter Instrument Line Joint Discovered.Caused by Equipment Failure Due to Installation Deficiency During Plant const.W/900315 Ltr ML20006F8651990-02-19019 February 1990 LER 90-002-00:on 900119,HPCI Outboard Steam Supply Isolation Valve Auto Closed on High Room Differential Temp Signal. Caused by Inoperative Temp Control Loop.Troubleshooting of Loop Initiated to Determine malfunction.W/900219 Ltr ML20011E3931990-02-0505 February 1990 LER 90-001-00:on 900106,turbine Trip on Moisture Separator High Level Resulted in Reactor Scram.Caused by Combination of Equipment Failure & Cognitive Personnel Errors.Moisture Separator Drain Control Instrumentation tuned.W/900205 Ltr ML20006C2571990-01-30030 January 1990 LER 89-026-00:on 891231,leak from Weld on Reactor Recirculation Sys Flow Transmitter Instrument Line Joint Discovered.Cause Not Stated.Instrument Line Cut Out & Replaced W/New Section of piping.W/900130 Ltr ML20011E1301990-01-29029 January 1990 LER 89-025-00:on 891230,turbine Trip Occurred During Performance of Main Turbine Thrust Bearing Wear Detector Surveillance.Caused by Malfunction of Limit Switch.Design Change Implemented for Keylock Bypass switch.W/900129 Ltr ML20005E2401989-12-28028 December 1989 LER 89-024-00:on 891129,determined That Surveillance Frequency for Safety Auxiliaries Cooling Sys Valve EG-HV-2302B Should Have Been Increased.Caused by Data Recording Error.Personnel counseled.W/891228 Ltr ML20005E2421989-12-27027 December 1989 LER 89-021-01:on 891013,concluded That Class 1E Electrical Separation Criteria Not Met in Reactor Protection Sys Panel. Caused by Inadequate Review of 1986 Design Change Package. Nonconforming Power Supplies removed.W/891227 Ltr ML19332E7931989-12-0606 December 1989 LER 89-022-01:on 891016,reactor Protection Sys Electric Protection Assemblies Opened,Resulting in Loss of RHR B Which Had Been Operating in Shutdown Cooling Mode.Caused by Low Voltage Output.Assemblies reset.W/891206 Ltr ML19332E8131989-12-0404 December 1989 LER 89-023-00:on 891104,full Reactor Protection Sys Signal Inadvertently Generated While Pressurizing Drywell,Resulting in Full Scram Signal.Caused by Procedural Deficiency. Integrated Leak Rate Test Procedure revised.W/891204 Ltr ML19327C2561989-11-15015 November 1989 LER 89-022-00:from 891016-27,scrams Experienced on Channel B Reactor Protection Sys Electric Assemblies & Nuclear Steam Supply Shutdown Sys Isolated,Resulting in Loss of Shutdown Cooling.Assemblies & Output Voltages reset.W/891115 Ltr ML19327C2701989-11-13013 November 1989 LER 89-020-00:on 891011,pressure Spike in Reactor Vessel Ref Leg Resulted in ESF Actuation During Filling & Venting of Pressure Transmitter.Caused by Personnel Error.Technicians Counseled & Retrained in Venting procedures.W/891113 Ltr ML19327C2711989-11-13013 November 1989 LER 89-021-00:on 891013,review of GE Transient Analysis Recording Sys Determined That Class 1E Electrical Separation Criteria Not Met in Two Reactor Protection Sys Panels. Nonconforming Power Supplies removed.W/891113 Ltr ML19354D4411989-11-0303 November 1989 LER 89-019-00:on 891004,inadequate Instrumentation Used on Core Spray Pumps for ASME Section XI Testing.Caused by Inadequate Design Change Package.Event Reviewed W/Station Inservice Testing engineer.W/891103 Ltr ML19325E8811989-11-0202 November 1989 LER 89-018-00:on 891003,determined That Two Tech Spec Required Readings Not Taken as Required When Vent Monitoring Sys Inoperable on 890929.Caused by Lack of Adequate Communication.Personnel Involved counseled.W/891102 Ltr 1994-05-03
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217F1501999-10-12012 October 1999 Special Rept:On 990929,south Plant Vent (SPV) Range Ng Monitor Was Inoperable.Monitor Was Inoperable for More than 72 H.Caused by Electronic Noise Generated from Noise Suppression Circuit.Replaced Circuit ML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data ML20217N6531999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Hope Creek Generating Station,Unit 1.With ML20217M0211999-09-20020 September 1999 Part 21 Rept Re Possible Deviation of NLI Dc Power Supply Over Voltage Protection Circuit Actuation.Caused by Electrical Circuit Conditions Unique to Remote Engine Panel. Travelled to Hope Creek to Witness Startup Sequence of DG ML20211N5531999-09-0808 September 1999 Safety Evaluation Supporting Amend 121 to License NPF-57 ML20211B3781999-08-13013 August 1999 Special Rept 99-002:on 990730,NPV Radiation Monitoring Sys Was Declared Inoperable.Caused by Voltage Induced in Detector Output by Power Cable to Low Range Sample Pump. Separated Cables & Secured in Place to Prevent Recurrence ML20210U4721999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Hope Creek Generating Station,Unit 1.With ML20216D8331999-07-26026 July 1999 Safety Evaluation Concluding That Licensee IPEEE Complete Re Info Requested by Suppl 4 to GL 88-20 & That IPEEE Results Reasonable Given HCGS Design,Operation & History ML20216D8721999-07-26026 July 1999 Review of Submittal in Response to USNRC GL 88-20,Suppl 4: 'Ipeees,' Fire Submittal Screening Review Technical Evaluation Rept:Hope Creek Rev 1:980518 ML20210F3331999-07-22022 July 1999 Safety Evaluation Granting Relief Requests RR-B1,RR-C1,RR-D1 & RR-B3.Finds That Proposed Alternative for RR-B3 Provides Acceptable Level of Quality & Safety & Authorizes Alternative Pursuant to 10CFR50.55a(a)(3)(i) ML20210C4731999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Hope Creek Generating Station,Unit 1.With ML20216D8901999-06-30030 June 1999 IPEEEs Technical Evaluation Rept High Winds,Floods & Other External Events ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML18107A3441999-06-0101 June 1999 Interim Part 21 Rept Re Premature Over Voltage Protection Actuation in Circuit Specific Application in Dc Power Supply.Testing & Evaluation Activities Will Be Completed on 990716 ML20196A1511999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Hope Creek Generating Station,Unit 1.With ML20206Q4731999-05-14014 May 1999 SER Accepting Response to GL 97-05, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Plant ML20206U1571999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Hope Creek Generating Station,Unit 1.With ML20216D8451999-04-30030 April 1999 Rev 1, Submittal-Only Screening Review of Hope Creek Unit 1 IPEEE (Seismic Portion). Finalized April 1999 ML20206C8481999-04-22022 April 1999 SER Authorizing Pse&G Proposed Relief Requests Associated with Changes Made to Repair Plan for Core Spray Nozzle Weld N5B Pursuant to 10CFR50.55a(a)(3)(i) LR-N990157, Special Rept 99-001:on 990315, C EDG Valid Failure Occurred During Surveillance Testing.Testing Resulted in Unsuccessful Loading Attempt,Due to Failure EDG Output Breaker to Close.Faulty Card Replaced1999-04-12012 April 1999 Special Rept 99-001:on 990315, C EDG Valid Failure Occurred During Surveillance Testing.Testing Resulted in Unsuccessful Loading Attempt,Due to Failure EDG Output Breaker to Close.Faulty Card Replaced ML20205R5901999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Hope Creek Generating Station,Unit 1.With ML20205G6051999-03-19019 March 1999 SER Accepting Relief Request Re Acme Code Case N-567, Alternate Requirements for Class 1,2 & 3 Replacement Components,Section Xi,Div 1 ML20205F8911999-03-18018 March 1999 Safety Evaluation Authorizing Licensee Requests for Second 10-year Interval for Pumps & Valves IST Program ML20204F7951999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Hope Creek Generating Station,Unit 1.With ML18106B0931999-02-25025 February 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Caused by Crack Due to Improper Location of Heated Bar.Only One Part Out of 7396 Pieces in Forging Lot Was Found to Be Cracked.Affected Util,Notified ML18106B0551999-02-0101 February 1999 Part 21 Rept Re Possible Matl Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Defect Is Crack in Center of Forging.Analysis of Part Is Continuing & Further Details Will Be Provided IAW Ncr Timetables.Drawing of Part,Encl ML18106B0441999-01-29029 January 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee Part Number SS-6-T.Caused by Crack in Center of Forging. Continuing Analysis of Part & Will Provide Details in Acoordance with NRC Timetables ML20202F6861999-01-26026 January 1999 Engine Sys,Inc Part 21 (10CFR21-0078) Rept Re Degradation of Synchrostat Model ESSB-4AT Speed Switches Resulting in Heat Related Damage to Power Supply Card Components.Caused by Incorrect Sized Resistor.Notification Sent to Customers ML18107A1871998-12-31031 December 1998 PSEG Annual Rept for 1998. ML20199E7271998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Hope Creek Generating Station,Unit 1.With ML18107A1881998-12-31031 December 1998 PECO 1998 Annual Rept. LR-N980580, Monthly Operating Rept for Nov 1998 for Hope Creek Generating Station,Unit 1.With1998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Hope Creek Generating Station,Unit 1.With ML20198N4161998-11-12012 November 1998 MSIV Alternate Leakage Treatment Pathway Seismic Evaluation LR-N980544, Monthly Operating Rept for Oct 1998 for Hcgs,Unit 1. with1998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Hcgs,Unit 1. with ML20155J9861998-10-31031 October 1998 Non-proprietary TR NEDO-32511, Safety Review for HCGS SRVs Tolerance Analyses LR-N980491, Monthly Operating Rept for Sept 1998 for Hope Creek Generating Station,Unit 1.With1998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Hope Creek Generating Station,Unit 1.With ML17354B0971998-09-0909 September 1998 Part 21 Rept Re Possible Machining Defect in Certain One Inch Stainless Steel Swagelok Front Ferrules,Part Number SS-1613-1.Caused by Tubing Slipping Out of Fitting at Three Times Working Pressure of Tubing.Notified Affected Utils LR-N980439, Monthly Operating Rept for Aug 1998 for Hope Creek Generating Station Unit 1.With1998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Hope Creek Generating Station Unit 1.With LR-N980401, Monthly Operating Rept for July 1998 for Hope Creek Generating Station,Unit 11998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Hope Creek Generating Station,Unit 1 ML20236N6751998-07-0909 July 1998 Part 21 & Deficiency Rept Re Notification of Potential Safety Hazard from Breakage of Cast Iron Suction Heads in Apkd Type Pumps.Caused by Migration of Suction Head Journal Sleeve Along Lower End of Pump Shaft.Will Inspect Pumps LR-N980354, Monthly Operating Rept for June 1998 for Hope Creek Generating Station,Unit 11998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Hope Creek Generating Station,Unit 1 ML20236E9491998-06-30030 June 1998 Rev 0 to non-proprietary Rept 24A5392AB, Lattice Dependent MAPLHGR Rept for Hope Creek Generating Station Reload 7 Cycle 8 ML18106A6821998-06-24024 June 1998 Revised Charting Our Future. ML18106A6681998-06-17017 June 1998 Charting the Future. LR-N980302, Monthly Operating Rept for May 1998 for Hope Creek Generating Station,Unit 11998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Hope Creek Generating Station,Unit 1 ML20248C7381998-05-22022 May 1998 Rev 0 to Safety Evaluation 98-015, Extension of Allowed Out of Service Time for B Emergency Diesel Generator LR-N980247, Monthly Operating Rept for Apr 1998 for Hope Creek Station, Unit 11998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Hope Creek Station, Unit 1 LR-N980196, Monthly Operating Rept for Mar 1998 for Hope Creek Generating Station,Unit 11998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Hope Creek Generating Station,Unit 1 ML20217D5701998-03-20020 March 1998 Part 21 Rept 40 Re Governor Valve Stems Made of Inconel 718 Matl Which Caused Loss of Governor Control.Control Problems Have Been Traced to Valve Stems Mfg by Bw/Ip.Id of Carbon Spacer Should Be Increased to at Least .5005/.5010 ML18106A5851998-03-0303 March 1998 Emergency Response Graded Exercise,S98-03. Nuclear Business Unit Salem,Hope Creek Emergency Preparedness, 980303 1999-09-08
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, , c i
i O PSEG i i Pubhc Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038 "
Hope Creek Operations December 27, 1989 y
.U. S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555
Dear Sir:
HOPE CREEK GENERATING STATION
[
,.- DOCKET NO. 50-354 UNIT NO. 1 i LICENSEE EVENT-REPORT 89-021-01 i This Revised Licensee Event Report is being submitted pursuant ,
to the requirements of 10CFR50.73 (a) (2) (ii) , and as noted in the original report. Please note that unavailability' of personnel involved in the initial investigation precluded submitting this revision by the date originally expected ,
(12/1/89). ,
Sincer ly,
.J.H :
General Manager - !
Hope Creek Operations ;
RBC/ .
Attachment '
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AB67RACT (16)
On 10/13/89, the Senior Nuclear Shift Supervisor (SNSS, SRO Licensed) was informed by I&C Systems Engineering that an engineering review of a design change affecting the General Electric Transient Analysis Recording System (GETARS) concluded that Class lE electrical separation criteria had not been met in an Reactor Protection System (RPS) panel. Power from an Gxternal Class lE Engineered Safety Features (ESP) Uninterruptable Power Supply (UPS) was connected to a GETARS multiplexer which interfaced with RPS circuitry, and adequate electrical separation was not provided. This configuration was in violation of separation criteria as established by Reg Guide 1.75. The root cause of this occurrence was the inadequate review of a 1986 design change package by construction support personnel.
Actions were immediately taken to rectify the electrical separation deviations - primarily, removing the power supplies which did not conform to separation criteria, and re-powering affected GETARS components from internal RPS panel non-UPS power supplies. Other corrective actions l include submitting an UFSAR change request to reflect the as-built design
! of the current configuration, implementing a design change to return the l GETARS MUXs to original power sources, including this event in continuing
! training for engineering personnel on electrical separation, and l
disseminating this report to all engineering personnel.
l' l
1
y -
N .
h'
- A TIW LIGNSEE LYDf!' RERWT (LIR) TEXT (INIINL' U FACILT!Y )WE (1) IO3LT NLMER (2) la EMER (6) PME (3) ll iTAR ** ENER ** RLY RE GER GMRATING S'IRTIW 05000354 89 -
0 2 1 -
0 1 0 2 7 0 5 I' PLANT AND SYSTEM' IDENTIFICATION General Electric - Boiling Water Reactor (BWR/4)-
. Reactor Protection System (EIIS Designation: JC)
Transient Analysis Monitoring. System (E1IS Designation: IP)
Engineered Safety Features Panels (EIIS Designation: JE)
IDENTIFICATION OF OCCURRENCE Deviation From Electrical Separation Criteria Between Transient Monitoring Circuitry and Reactor Protection System Panel Circuitry Due to inadequate Review of a Design Change Event Date: 3/5/86 Discovery Date: 10/13/89 Discovery Time: 1350 This LER was initiated by Incident Report No.89-137 CONDITIONS PRIOR TO OCCURRENCE Plant in OPERATIONAL CONDITION 5 (Refueling), outage work in progress.
DESCRIPTION OF OCCURRENCE On 10/13/89, the Senior Nuclear Shift Supervisor (SNSS, SRO-Licensed) was informed by I&C Systems Engineering that an engineering review of two design changes affecting General Electric Transient Analysis Recording System (GETARS) concluded that class 1E electrical separation criteria had not
'been met in two Reactor Protection System (RPS) panels. Power !
, from an external Class 1E Engineered Safety Feature (ESP)
L Uninterruptible Power Supply (UPS) was connected to GETARS multiplexers in RPS panel sections with RPS circuits.
I The method utilized to provide this UPS power did not meet the electrical separation criteria of Reg Guide 1.75.
- . APPARENT CAUSE OF OCCURRENCE l
L The root cause of this occurrence was the inadequate review of ;
a design change by construction support personnel in 1986. The j' review failed to discover a design deficiency that did not ensure proper electrical separation between the RPS circuitry and GETARS multiplexers, i
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0 1 0 3 7 0 5 ANAbYSIS OF OCCURRENCE -
General Electric Transient Monitoring System (GETARS) multiplexers number 12 and 14 are used to monitor various RPS signals including scram isolation and Main Steam Isolation ,
Valve (MSIV) positions. During system installation, a Startup Deviation Report (SDR) was generated on 1/30/86 stating that multiplexers (MUX) 12 and 14 were not supplied with !
Uninterruptible power supplies (UPS) as required by the FSAR. ;
(This FSAR requirement existed due to the necessity of utilizing GETARS for acceptance criteria verification during -
the power ascension boss of Power test.) Because MUXs 12 und 14 interface with RPS, the UPS must be Class 1E. The SDR was subsequently dispositioned to provide a Class 1E UPS to these MUXs. A design change request (DCR) was initiated on 3/5/86 to resolve this issue as well as several other GETARS problem areas.
The closest available Class 1E UPS to the subject MUXs is located in the Engineered Safety Features (ESP) side of the RPS/ ESP panels containing the MUXs. However, in accordance with FSAR section 8.1.4.14.1, RPS and ESF must be separated electrically and physically from one another. The method utilized to provide separation involved penetrating the separation wall in the RPS/ESF panel with wires sealed in conduit to connect each MUX to the UPS. This provided physical separation but not electrical separation.
on 10/9/89, the original DCP was reviewed for closure by the Hope Creek I&C group. In this review, the separation issue for ,
these systems was discovered and analyzed. A re-evaluation of the design determined that it did not adequately address electrical separation as required by Reg Guide 1.75. The circuit was routed from the RPS side of the panel to the ESF side of the panel without required separation mechanisms installed in the circuit. It was determined that electrical separation within the MUXs could not be demonstrated in accordance with the requirements of Reg Guide 1.75. <
A Deficiency Report (DR) was generated and a temporary modification was performed to provide conformance with the FSAR separation criteria by removing the Class 1E UPS power from the MUXs. A safety evaluation was prepared to support the temporary modificatior stating in essence that although each class 1E MUX should ee powered from a UPS, the MUXs which ,
monitor the RPS do not provide any useful information in a loss-of-power scenario, since the RPS interrogation power for the RPS will no longer be available. During the second refueling outage, a permanent design change was implemented to reflect this configuration.
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' PREVIOUS OCCURRENCES
,"l A review of past occurrences at Hope Crnet indicates that this l is- the first identified instance of non-conformance with- 1 electrical separation criteria. !
SAFETY SIGNIFICANCE The circumstances described in this report posed minimal safety significance. An' electrical fault could potentially have been -
propagated from the ESF panel to the RPS panel via the as-found electrical arrangement. This scenario -is unlikely, however, because single fuse protection existed between the RPS and ESF
. cabinets, non-safety inputs to GETARS MUXs-were separated via fiber. optic links, and the MUXs are each individually fused at -
.the: power infeeds. Because of the channelized nature of RPS, it is not-possible for such a fault to significantly- degrade the: availability and reliability of RPS.
CORRECTIVE ACTIONS
- 1. An UFSAR change request will be submitted to reflect that MUXs 12 and 14 will not be powered from a UPS.
- 2. A design change was implemented to reconfigure the MUX poue- to its original source, a non-UPS Class 1E power sol 1
- 3. The de61gn change process which was in place in 1986 has been superceded by a new design change procedure. This
_ procedure includes a design input checklist and peer review process. The addition of these enhancements should preclude recurrance of a similar event. Specific
. corrective actions witn respect to the personnel errors :Ln the review of the 1986 design change are not possible, as the design change was prepared by construction support l:
personnel no longer on site.
I 4 '. This incident will be discussed during continuing training L for all E&PB electrical engineers with regard to L electrical separation criteria.
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-CORRECTIVE ACTIONS, CONT'D
.5. This> report -will be . forwarded to the Vice'- President -
'LNuclear , Engineering for dissemination. to all EEPB-a , personnel.
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.J. a n General Manager - y liope Creek Operations ,
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