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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20029D6631994-05-0303 May 1994 LER 94-003-00:on 940405,loss of Shutdown Cooling Occurred Due to an Inadvertent High Reactor Pressure Isolation Signal.Corrective Action:Operations Department Procedure Used to Restore Shutdown Cooling isolations.W/940503 Ltr ML20029C7501994-04-20020 April 1994 LER 94-001-01:on 940305,ESF Actuation/Isolation & Loss of Shutdown Cooling Occurred.Caused by Personnel Error. Technician counseled.W/940420 Ltr ML20045B4761993-06-14014 June 1993 LER 93-004-00:on 930516,component Failure in EHC Sys Resulted in Generator/Turbine Trip & Reactor Scram.Failed Components Replaced & Addl Monitoring Devices Installed on EHC sys.W/930614 Ltr ML20045B2861993-06-0909 June 1993 LER 93-003-00:on 930513,plant Transient Initiated When 13.8 Kv Pothead Failed,Inducing Voltage Drop & Phase Differential Relay Actuation Due to Loss of Offsite Power on 2 of 4 Vital Buses.Failed Pothead replaced.W/930609 Ltr ML20029C2071991-03-21021 March 1991 LER 91-005-00:on 910219,reactor Scram Relay Malfunction Resulted in Startup Level Control Valve Failing Closed. Caused by Failure of Relay Controlling Position of Rfw 12 Startup Level Control Valve.Relay replaced.W/910321 Ltr ML20029A6441991-02-25025 February 1991 LER 91-003-00:on 910125,channel C Primary Containment Isolation Sys Actuated,Resulting in Trip of Radwaste Area Supply & Exhaust Fans.Caused by Design Deficiency Re Steam Leak Detection Sys Cabinets.Fuse replaced.W/910225 Ltr ML20028H8531991-01-23023 January 1991 LER 90-035-00:on 901227,pipe Section on Svc Water Sys (Ssws) a Loop Developed Minor Through Wall Flaw.Caused by Pipe Corrosion.Pipe Section on Ssws Will Be Replaced Prior to Restart from Current Refueling outage.W/910123 Ltr ML20028H6781991-01-16016 January 1991 LER 90-025-01:on 901104,leak Discovered on Weld on Reactor Recirculation Instrument Line While Investigating Source of Drywell Leakage.Caused by Crack at Welded Joint Due to vibration-induced Fatigue.Line replaced.W/910116 Ltr ML20043F4521990-06-11011 June 1990 LER 90-007-00:on 900517,control Room Received Indication of Half Scram & Isolation of Inboard Reactor Water Cleanup Isolation Valve.Caused by Spurious Trip of Channel a Reactor Protection Sys Epa.Design Change implemented.W/900611 Ltr ML20043F6121990-06-11011 June 1990 LER 90-006-00:on 900512,filtration,recirculation & Ventilation Sys Recirculation Fan E Discovered Running by Nuclear Control Operator.Cause Not Determined.Work Orders Initiated to Inspect Flow switches.W/900611 Ltr ML20043A8691990-05-16016 May 1990 LER 90-004-00:on 900418,ground Fault on Motor Control Ctr Feeder Breaker Occurred & Resulted in de-energization of Reactor B Protection Sys.Cause Not Determined.Feeder Breaker & Trip Device replaced.W/900516 Ltr ML20043A9091990-05-16016 May 1990 LER 90-005-00:on 900419,determined That Inoperability of Liquid Radwaste Discharge Monitor Not Reported in Recent Radioactive Effluent Release Rept.Caused by Procedural Deficiency.Effluent Rept revised.W/900516 Ltr ML20012C5991990-03-15015 March 1990 LER 89-026-01:on 891231,leak from Weld on 1-inch Reactor Recirculation Sys Elbow Tap Flow Transmitter Instrument Line Joint Discovered.Caused by Equipment Failure Due to Installation Deficiency During Plant const.W/900315 Ltr ML20006F8651990-02-19019 February 1990 LER 90-002-00:on 900119,HPCI Outboard Steam Supply Isolation Valve Auto Closed on High Room Differential Temp Signal. Caused by Inoperative Temp Control Loop.Troubleshooting of Loop Initiated to Determine malfunction.W/900219 Ltr ML20011E3931990-02-0505 February 1990 LER 90-001-00:on 900106,turbine Trip on Moisture Separator High Level Resulted in Reactor Scram.Caused by Combination of Equipment Failure & Cognitive Personnel Errors.Moisture Separator Drain Control Instrumentation tuned.W/900205 Ltr ML20006C2571990-01-30030 January 1990 LER 89-026-00:on 891231,leak from Weld on Reactor Recirculation Sys Flow Transmitter Instrument Line Joint Discovered.Cause Not Stated.Instrument Line Cut Out & Replaced W/New Section of piping.W/900130 Ltr ML20011E1301990-01-29029 January 1990 LER 89-025-00:on 891230,turbine Trip Occurred During Performance of Main Turbine Thrust Bearing Wear Detector Surveillance.Caused by Malfunction of Limit Switch.Design Change Implemented for Keylock Bypass switch.W/900129 Ltr ML20005E2401989-12-28028 December 1989 LER 89-024-00:on 891129,determined That Surveillance Frequency for Safety Auxiliaries Cooling Sys Valve EG-HV-2302B Should Have Been Increased.Caused by Data Recording Error.Personnel counseled.W/891228 Ltr ML20005E2421989-12-27027 December 1989 LER 89-021-01:on 891013,concluded That Class 1E Electrical Separation Criteria Not Met in Reactor Protection Sys Panel. Caused by Inadequate Review of 1986 Design Change Package. Nonconforming Power Supplies removed.W/891227 Ltr ML19332E7931989-12-0606 December 1989 LER 89-022-01:on 891016,reactor Protection Sys Electric Protection Assemblies Opened,Resulting in Loss of RHR B Which Had Been Operating in Shutdown Cooling Mode.Caused by Low Voltage Output.Assemblies reset.W/891206 Ltr ML19332E8131989-12-0404 December 1989 LER 89-023-00:on 891104,full Reactor Protection Sys Signal Inadvertently Generated While Pressurizing Drywell,Resulting in Full Scram Signal.Caused by Procedural Deficiency. Integrated Leak Rate Test Procedure revised.W/891204 Ltr ML19327C2561989-11-15015 November 1989 LER 89-022-00:from 891016-27,scrams Experienced on Channel B Reactor Protection Sys Electric Assemblies & Nuclear Steam Supply Shutdown Sys Isolated,Resulting in Loss of Shutdown Cooling.Assemblies & Output Voltages reset.W/891115 Ltr ML19327C2701989-11-13013 November 1989 LER 89-020-00:on 891011,pressure Spike in Reactor Vessel Ref Leg Resulted in ESF Actuation During Filling & Venting of Pressure Transmitter.Caused by Personnel Error.Technicians Counseled & Retrained in Venting procedures.W/891113 Ltr ML19327C2711989-11-13013 November 1989 LER 89-021-00:on 891013,review of GE Transient Analysis Recording Sys Determined That Class 1E Electrical Separation Criteria Not Met in Two Reactor Protection Sys Panels. Nonconforming Power Supplies removed.W/891113 Ltr ML19354D4411989-11-0303 November 1989 LER 89-019-00:on 891004,inadequate Instrumentation Used on Core Spray Pumps for ASME Section XI Testing.Caused by Inadequate Design Change Package.Event Reviewed W/Station Inservice Testing engineer.W/891103 Ltr ML19325E8811989-11-0202 November 1989 LER 89-018-00:on 891003,determined That Two Tech Spec Required Readings Not Taken as Required When Vent Monitoring Sys Inoperable on 890929.Caused by Lack of Adequate Communication.Personnel Involved counseled.W/891102 Ltr 1994-05-03
[Table view] Category:RO)
MONTHYEARML20029D6631994-05-0303 May 1994 LER 94-003-00:on 940405,loss of Shutdown Cooling Occurred Due to an Inadvertent High Reactor Pressure Isolation Signal.Corrective Action:Operations Department Procedure Used to Restore Shutdown Cooling isolations.W/940503 Ltr ML20029C7501994-04-20020 April 1994 LER 94-001-01:on 940305,ESF Actuation/Isolation & Loss of Shutdown Cooling Occurred.Caused by Personnel Error. Technician counseled.W/940420 Ltr ML20045B4761993-06-14014 June 1993 LER 93-004-00:on 930516,component Failure in EHC Sys Resulted in Generator/Turbine Trip & Reactor Scram.Failed Components Replaced & Addl Monitoring Devices Installed on EHC sys.W/930614 Ltr ML20045B2861993-06-0909 June 1993 LER 93-003-00:on 930513,plant Transient Initiated When 13.8 Kv Pothead Failed,Inducing Voltage Drop & Phase Differential Relay Actuation Due to Loss of Offsite Power on 2 of 4 Vital Buses.Failed Pothead replaced.W/930609 Ltr ML20029C2071991-03-21021 March 1991 LER 91-005-00:on 910219,reactor Scram Relay Malfunction Resulted in Startup Level Control Valve Failing Closed. Caused by Failure of Relay Controlling Position of Rfw 12 Startup Level Control Valve.Relay replaced.W/910321 Ltr ML20029A6441991-02-25025 February 1991 LER 91-003-00:on 910125,channel C Primary Containment Isolation Sys Actuated,Resulting in Trip of Radwaste Area Supply & Exhaust Fans.Caused by Design Deficiency Re Steam Leak Detection Sys Cabinets.Fuse replaced.W/910225 Ltr ML20028H8531991-01-23023 January 1991 LER 90-035-00:on 901227,pipe Section on Svc Water Sys (Ssws) a Loop Developed Minor Through Wall Flaw.Caused by Pipe Corrosion.Pipe Section on Ssws Will Be Replaced Prior to Restart from Current Refueling outage.W/910123 Ltr ML20028H6781991-01-16016 January 1991 LER 90-025-01:on 901104,leak Discovered on Weld on Reactor Recirculation Instrument Line While Investigating Source of Drywell Leakage.Caused by Crack at Welded Joint Due to vibration-induced Fatigue.Line replaced.W/910116 Ltr ML20043F4521990-06-11011 June 1990 LER 90-007-00:on 900517,control Room Received Indication of Half Scram & Isolation of Inboard Reactor Water Cleanup Isolation Valve.Caused by Spurious Trip of Channel a Reactor Protection Sys Epa.Design Change implemented.W/900611 Ltr ML20043F6121990-06-11011 June 1990 LER 90-006-00:on 900512,filtration,recirculation & Ventilation Sys Recirculation Fan E Discovered Running by Nuclear Control Operator.Cause Not Determined.Work Orders Initiated to Inspect Flow switches.W/900611 Ltr ML20043A8691990-05-16016 May 1990 LER 90-004-00:on 900418,ground Fault on Motor Control Ctr Feeder Breaker Occurred & Resulted in de-energization of Reactor B Protection Sys.Cause Not Determined.Feeder Breaker & Trip Device replaced.W/900516 Ltr ML20043A9091990-05-16016 May 1990 LER 90-005-00:on 900419,determined That Inoperability of Liquid Radwaste Discharge Monitor Not Reported in Recent Radioactive Effluent Release Rept.Caused by Procedural Deficiency.Effluent Rept revised.W/900516 Ltr ML20012C5991990-03-15015 March 1990 LER 89-026-01:on 891231,leak from Weld on 1-inch Reactor Recirculation Sys Elbow Tap Flow Transmitter Instrument Line Joint Discovered.Caused by Equipment Failure Due to Installation Deficiency During Plant const.W/900315 Ltr ML20006F8651990-02-19019 February 1990 LER 90-002-00:on 900119,HPCI Outboard Steam Supply Isolation Valve Auto Closed on High Room Differential Temp Signal. Caused by Inoperative Temp Control Loop.Troubleshooting of Loop Initiated to Determine malfunction.W/900219 Ltr ML20011E3931990-02-0505 February 1990 LER 90-001-00:on 900106,turbine Trip on Moisture Separator High Level Resulted in Reactor Scram.Caused by Combination of Equipment Failure & Cognitive Personnel Errors.Moisture Separator Drain Control Instrumentation tuned.W/900205 Ltr ML20006C2571990-01-30030 January 1990 LER 89-026-00:on 891231,leak from Weld on Reactor Recirculation Sys Flow Transmitter Instrument Line Joint Discovered.Cause Not Stated.Instrument Line Cut Out & Replaced W/New Section of piping.W/900130 Ltr ML20011E1301990-01-29029 January 1990 LER 89-025-00:on 891230,turbine Trip Occurred During Performance of Main Turbine Thrust Bearing Wear Detector Surveillance.Caused by Malfunction of Limit Switch.Design Change Implemented for Keylock Bypass switch.W/900129 Ltr ML20005E2401989-12-28028 December 1989 LER 89-024-00:on 891129,determined That Surveillance Frequency for Safety Auxiliaries Cooling Sys Valve EG-HV-2302B Should Have Been Increased.Caused by Data Recording Error.Personnel counseled.W/891228 Ltr ML20005E2421989-12-27027 December 1989 LER 89-021-01:on 891013,concluded That Class 1E Electrical Separation Criteria Not Met in Reactor Protection Sys Panel. Caused by Inadequate Review of 1986 Design Change Package. Nonconforming Power Supplies removed.W/891227 Ltr ML19332E7931989-12-0606 December 1989 LER 89-022-01:on 891016,reactor Protection Sys Electric Protection Assemblies Opened,Resulting in Loss of RHR B Which Had Been Operating in Shutdown Cooling Mode.Caused by Low Voltage Output.Assemblies reset.W/891206 Ltr ML19332E8131989-12-0404 December 1989 LER 89-023-00:on 891104,full Reactor Protection Sys Signal Inadvertently Generated While Pressurizing Drywell,Resulting in Full Scram Signal.Caused by Procedural Deficiency. Integrated Leak Rate Test Procedure revised.W/891204 Ltr ML19327C2561989-11-15015 November 1989 LER 89-022-00:from 891016-27,scrams Experienced on Channel B Reactor Protection Sys Electric Assemblies & Nuclear Steam Supply Shutdown Sys Isolated,Resulting in Loss of Shutdown Cooling.Assemblies & Output Voltages reset.W/891115 Ltr ML19327C2701989-11-13013 November 1989 LER 89-020-00:on 891011,pressure Spike in Reactor Vessel Ref Leg Resulted in ESF Actuation During Filling & Venting of Pressure Transmitter.Caused by Personnel Error.Technicians Counseled & Retrained in Venting procedures.W/891113 Ltr ML19327C2711989-11-13013 November 1989 LER 89-021-00:on 891013,review of GE Transient Analysis Recording Sys Determined That Class 1E Electrical Separation Criteria Not Met in Two Reactor Protection Sys Panels. Nonconforming Power Supplies removed.W/891113 Ltr ML19354D4411989-11-0303 November 1989 LER 89-019-00:on 891004,inadequate Instrumentation Used on Core Spray Pumps for ASME Section XI Testing.Caused by Inadequate Design Change Package.Event Reviewed W/Station Inservice Testing engineer.W/891103 Ltr ML19325E8811989-11-0202 November 1989 LER 89-018-00:on 891003,determined That Two Tech Spec Required Readings Not Taken as Required When Vent Monitoring Sys Inoperable on 890929.Caused by Lack of Adequate Communication.Personnel Involved counseled.W/891102 Ltr 1994-05-03
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217F1501999-10-12012 October 1999 Special Rept:On 990929,south Plant Vent (SPV) Range Ng Monitor Was Inoperable.Monitor Was Inoperable for More than 72 H.Caused by Electronic Noise Generated from Noise Suppression Circuit.Replaced Circuit ML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data ML20217N6531999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Hope Creek Generating Station,Unit 1.With ML20217M0211999-09-20020 September 1999 Part 21 Rept Re Possible Deviation of NLI Dc Power Supply Over Voltage Protection Circuit Actuation.Caused by Electrical Circuit Conditions Unique to Remote Engine Panel. Travelled to Hope Creek to Witness Startup Sequence of DG ML20211N5531999-09-0808 September 1999 Safety Evaluation Supporting Amend 121 to License NPF-57 ML20211B3781999-08-13013 August 1999 Special Rept 99-002:on 990730,NPV Radiation Monitoring Sys Was Declared Inoperable.Caused by Voltage Induced in Detector Output by Power Cable to Low Range Sample Pump. Separated Cables & Secured in Place to Prevent Recurrence ML20210U4721999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Hope Creek Generating Station,Unit 1.With ML20216D8331999-07-26026 July 1999 Safety Evaluation Concluding That Licensee IPEEE Complete Re Info Requested by Suppl 4 to GL 88-20 & That IPEEE Results Reasonable Given HCGS Design,Operation & History ML20216D8721999-07-26026 July 1999 Review of Submittal in Response to USNRC GL 88-20,Suppl 4: 'Ipeees,' Fire Submittal Screening Review Technical Evaluation Rept:Hope Creek Rev 1:980518 ML20210F3331999-07-22022 July 1999 Safety Evaluation Granting Relief Requests RR-B1,RR-C1,RR-D1 & RR-B3.Finds That Proposed Alternative for RR-B3 Provides Acceptable Level of Quality & Safety & Authorizes Alternative Pursuant to 10CFR50.55a(a)(3)(i) ML20210C4731999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Hope Creek Generating Station,Unit 1.With ML20216D8901999-06-30030 June 1999 IPEEEs Technical Evaluation Rept High Winds,Floods & Other External Events ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML18107A3441999-06-0101 June 1999 Interim Part 21 Rept Re Premature Over Voltage Protection Actuation in Circuit Specific Application in Dc Power Supply.Testing & Evaluation Activities Will Be Completed on 990716 ML20196A1511999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Hope Creek Generating Station,Unit 1.With ML20206Q4731999-05-14014 May 1999 SER Accepting Response to GL 97-05, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Plant ML20206U1571999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Hope Creek Generating Station,Unit 1.With ML20216D8451999-04-30030 April 1999 Rev 1, Submittal-Only Screening Review of Hope Creek Unit 1 IPEEE (Seismic Portion). Finalized April 1999 ML20206C8481999-04-22022 April 1999 SER Authorizing Pse&G Proposed Relief Requests Associated with Changes Made to Repair Plan for Core Spray Nozzle Weld N5B Pursuant to 10CFR50.55a(a)(3)(i) LR-N990157, Special Rept 99-001:on 990315, C EDG Valid Failure Occurred During Surveillance Testing.Testing Resulted in Unsuccessful Loading Attempt,Due to Failure EDG Output Breaker to Close.Faulty Card Replaced1999-04-12012 April 1999 Special Rept 99-001:on 990315, C EDG Valid Failure Occurred During Surveillance Testing.Testing Resulted in Unsuccessful Loading Attempt,Due to Failure EDG Output Breaker to Close.Faulty Card Replaced ML20205R5901999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Hope Creek Generating Station,Unit 1.With ML20205G6051999-03-19019 March 1999 SER Accepting Relief Request Re Acme Code Case N-567, Alternate Requirements for Class 1,2 & 3 Replacement Components,Section Xi,Div 1 ML20205F8911999-03-18018 March 1999 Safety Evaluation Authorizing Licensee Requests for Second 10-year Interval for Pumps & Valves IST Program ML20204F7951999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Hope Creek Generating Station,Unit 1.With ML18106B0931999-02-25025 February 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Caused by Crack Due to Improper Location of Heated Bar.Only One Part Out of 7396 Pieces in Forging Lot Was Found to Be Cracked.Affected Util,Notified ML18106B0551999-02-0101 February 1999 Part 21 Rept Re Possible Matl Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Defect Is Crack in Center of Forging.Analysis of Part Is Continuing & Further Details Will Be Provided IAW Ncr Timetables.Drawing of Part,Encl ML18106B0441999-01-29029 January 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee Part Number SS-6-T.Caused by Crack in Center of Forging. Continuing Analysis of Part & Will Provide Details in Acoordance with NRC Timetables ML20202F6861999-01-26026 January 1999 Engine Sys,Inc Part 21 (10CFR21-0078) Rept Re Degradation of Synchrostat Model ESSB-4AT Speed Switches Resulting in Heat Related Damage to Power Supply Card Components.Caused by Incorrect Sized Resistor.Notification Sent to Customers ML18107A1871998-12-31031 December 1998 PSEG Annual Rept for 1998. ML20199E7271998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Hope Creek Generating Station,Unit 1.With ML18107A1881998-12-31031 December 1998 PECO 1998 Annual Rept. LR-N980580, Monthly Operating Rept for Nov 1998 for Hope Creek Generating Station,Unit 1.With1998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Hope Creek Generating Station,Unit 1.With ML20198N4161998-11-12012 November 1998 MSIV Alternate Leakage Treatment Pathway Seismic Evaluation LR-N980544, Monthly Operating Rept for Oct 1998 for Hcgs,Unit 1. with1998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Hcgs,Unit 1. with ML20155J9861998-10-31031 October 1998 Non-proprietary TR NEDO-32511, Safety Review for HCGS SRVs Tolerance Analyses LR-N980491, Monthly Operating Rept for Sept 1998 for Hope Creek Generating Station,Unit 1.With1998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Hope Creek Generating Station,Unit 1.With ML17354B0971998-09-0909 September 1998 Part 21 Rept Re Possible Machining Defect in Certain One Inch Stainless Steel Swagelok Front Ferrules,Part Number SS-1613-1.Caused by Tubing Slipping Out of Fitting at Three Times Working Pressure of Tubing.Notified Affected Utils LR-N980439, Monthly Operating Rept for Aug 1998 for Hope Creek Generating Station Unit 1.With1998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Hope Creek Generating Station Unit 1.With LR-N980401, Monthly Operating Rept for July 1998 for Hope Creek Generating Station,Unit 11998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Hope Creek Generating Station,Unit 1 ML20236N6751998-07-0909 July 1998 Part 21 & Deficiency Rept Re Notification of Potential Safety Hazard from Breakage of Cast Iron Suction Heads in Apkd Type Pumps.Caused by Migration of Suction Head Journal Sleeve Along Lower End of Pump Shaft.Will Inspect Pumps LR-N980354, Monthly Operating Rept for June 1998 for Hope Creek Generating Station,Unit 11998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Hope Creek Generating Station,Unit 1 ML20236E9491998-06-30030 June 1998 Rev 0 to non-proprietary Rept 24A5392AB, Lattice Dependent MAPLHGR Rept for Hope Creek Generating Station Reload 7 Cycle 8 ML18106A6821998-06-24024 June 1998 Revised Charting Our Future. ML18106A6681998-06-17017 June 1998 Charting the Future. LR-N980302, Monthly Operating Rept for May 1998 for Hope Creek Generating Station,Unit 11998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Hope Creek Generating Station,Unit 1 ML20248C7381998-05-22022 May 1998 Rev 0 to Safety Evaluation 98-015, Extension of Allowed Out of Service Time for B Emergency Diesel Generator LR-N980247, Monthly Operating Rept for Apr 1998 for Hope Creek Station, Unit 11998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Hope Creek Station, Unit 1 LR-N980196, Monthly Operating Rept for Mar 1998 for Hope Creek Generating Station,Unit 11998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Hope Creek Generating Station,Unit 1 ML20217D5701998-03-20020 March 1998 Part 21 Rept 40 Re Governor Valve Stems Made of Inconel 718 Matl Which Caused Loss of Governor Control.Control Problems Have Been Traced to Valve Stems Mfg by Bw/Ip.Id of Carbon Spacer Should Be Increased to at Least .5005/.5010 ML18106A5851998-03-0303 March 1998 Emergency Response Graded Exercise,S98-03. Nuclear Business Unit Salem,Hope Creek Emergency Preparedness, 980303 1999-09-08
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e"4 -O PSEG Pubhc SN ,e Eloctric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038 Hope Creek Operations -
i February 5, 1990 t
U. S. Nuclear Regulatory Commission Document: Control Desk '
Washington, DC 20555 Dear Sir
' HOPE CREEK GENERATING STATION !
DOCKET NO. 50-354 UNIT NO. 1 !
LICENSEE EVENT REPORT 90-001-00 f
This Licensee Event Report is being submitted pursuant to the requirements of 10CFR50.73 (a) (2) (iv) . .
Sincere:gy ,
l l
. . Ha an General- ager -
Hope Creek Operations RBC/'
Attachment ;
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On 1/6/90 at 0120, during performance of a surveillance procedure which tcsts the Main Turbine Combined Intermediate Valves (CIV), the "A" i Moisture Separator experienced a high level condition. In response to ,
this high level condition, the associated dump valve opened, but not in i timo to prevent a turbine trip on moisture separator high level.
ICmediately following the turbine trip, the reactor scrammed on a Turbine Control Valve Closure signal from the Reactor Protection System. All control rods were verified to be inserted, and plant systems responded as expected, with minor exceptions as noted in the text of this report.
Investigation subsequent to the scram determined that multiple causes ;
combined to result in the scram - moisture separator level controllers which were not optimally tuned and the cycling of a CIV prior to atabilization of moisture separator level after cycling a previous CIV. Corrective actions included tuning of the moisture separator drain control instrumentation loops, procedurally increasing the time between cycling of CIV's 6uring the subject surveillance, counselling the Nuclear Control Operator (NCO, R9 licensed) who performed the surveillance, and l i
including a review of the event during the next licensed operator i requalification cycle.
1 1
m In b :
LIGNSEE D1NT REKET (IDO 1 EXT OMIRRTim IX21ElY NAPE (1) ID3Er RMER (2) _, ID EDEER (6)_ PAGE (3) ng ** gggy ** g p 10FE OGK GMRATING ITTATim ' 05000354 0 0 1 -
0 0 0 2 7 0 8 5 i
- PLANT AND SYSTEM IDENTIFICATION General Electric - Boiling Water Reactor (BWR/4)
Main Turbine (EIIS Designation: TA) . :
Reactor Protection System (EIIS Designation: JC)
[ Moisture Separator (EIIS Designation: SN)
Feedwater System (EIIS Designation: SJ) i Condensate System (EIIS Designation: SD) . ;
I IDENTIFICATION OF OCCURRENCE Turbine Trip on Moisture Separator High Level Results in Reactor Scram Due to Equipment Deficiencies and Personnel Error Event Date: 01/06/90 Event Time: 0120 .
This LER was initiated by Incident Report No.90-001 3:
CONDITIONS PRIOR TO OCCURRENCE Plant in OPERATIONAL CONDITION 1 (Power Operation), Reactor ,
Power 97%, Unit Load 1062 MWo. Output limited by feedwater heaters 1C and 2C being out of service. [
t DESCRIPTION OF OCCURRENCE On - 1/6/90 at 0120, during performance of a surveillance- -
procedure which tests the Main Turbine Combined Intermediate !
Valves (CIV), the "A" Moisture Separator experienced a high
- 1evel condition. In response to this high level condition, the associated dump valve opened, but not in time to prevent a turbine trip on moisture separator high level. Immediately following the turbine trip, the reactor scrammed on a Turbine Control Valve (TCV) closure signal from the Reactor Protection System (RPS). All control rods were verified to be inserted,
- and plant systems responded as expected, with the following exceptions:
- 1. The "B" Secondary Condensate Pump (SCP) minimum flow valve -
failed to open, resulting in a trip of the "B" SCP on low flow. ;
- 2. Post-accident monitoring (PAMS) pressure recorders "A" and "B"_did not function properly.
- 3. Redundant Reactivity Control System (RRCS) Division I, channel "B" failed to trip.
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I DESCRIPTION OF OCCURRENCE, CONT'Q !
. t The "H" and "P" Safety _ Relief Valves (SRVs) lifted as designed'
. to control reactor pressure, and vessel level decreased to L approximately 10" (narrow range indication) during-the course ,
of the transient, well above any Emergency Core Cooling System actuation levels. Vessel level was restored using the "A" .
Reactor Feed pump. Plant parameters were stabilized within 30 !
minutes. A.four hour non-emergency report was made to the NRC ;
Operations Center IAW 10CFR50.72, and an investigation -was l initiated to determine the cause of the scram. Due to a scheduling error ~by the LER Coordinator, this report is being f submitted 1 day late, a
ANALYSIS OF OCCURRENCE On.1/6/90 at 0045, the control room Nuclear Control Operator I (NCO, RO licensed) initiated performance of the weekly Turbine Overspeed Protection System Operability Test procedure. The
? purpose of this surveillance is to demonstrate the operability ,.
of the main turbine overspeed protection system by cycling the Turbine.Stop Valves (TSVs) and the Combined. Intermediate Valves 3 h (CIVs) as required by technical specifications.
The first caution in the procedure stated that "At least one L ,
minute between valve operations shall be exercised.to allow the r
' 'EHC System time to stabilize.".. The TSVs were cycled with P satisfactory results, and at 0117:20, the NCO cycled CIV-#1 closed. 31 seconds after completing the cycling of CIV-#1,the .;
! NCO began to cycle CIV-#4. At 0119:36, a " Moisture Separator ;
"A" Emergency Dump Tank High Level" alarm was received, and at 0120:19, the turbine tripped on moisture separator high level i and the reactor scrammed on a TCV closure signal via RPS.
Investigation subsequent to the scram focused on two primary ,
areas; the instrumentation for moisture separator level control l and the NCO's performance of the surveillance test. l l
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~&NALYSIS OF OCCURRENCE. CONT'D
- 1. Moisture Separator Level Control Instrumentation Refer to Attachment 1. Moisture Separator level is normally controlled via the cycling of level control valves LV-1364A, B,
- and C, which route condensate from the Moisture Separator Drain Tank to Feedwater lleaters SA, B and C via individual 8" lines.
In the event of a high Drain Tank level, the Emergency Dump Valve opens and drains directly to the Main Condenser via a single 8" line. The cycling of a CIV induces a significant ,
transient on the-associated Moisture Separator, and a swing in level during the course of cycling a CIV is normal and '
expected, however, not as severe as was experienced in this event.
Following the scram, the response and settings of the Drain Tank level control system (instrumentation and valves) was checked. Investigation determined that a variety of factors '
contributed to a less than adequate response of the level control system for "A" Moisture Separator:
A. Level Controller LIC-1040A was determined to be adjusted
- to a less than optimum setting, which led to a sluggish response of LV-1364A and LV-1364B above the 50% open position. There is no recurring task for preventive maintenance of this controller or tuning of the entire control loop.
B. The air supply to the positioner for LV-1364C was isolated, as such, this valve did not open in response to the Moisture Separator high level transient. LV-1364C was worked several times during the station 2nd refueling outage. Subsequent investigation has determined that the air supply to the positioner was not properly restored by Maintenance Department personnel following one of these maintenance activities.
C. The response for Emergency Dump valve LV-1039A was sluggish above the 50% open position. Again, the tuning ,
of the level control loop for this valve was less than optimum. All instruments in this loop had been individually calibrated during September of 1989, however, a total loop functional test was not required to be performed.
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Lastly, the response of the Moisture Separators during previous testing was reviewed. During the course of interviews with Operations Department control room personnel following the .
i scram, it was determined that the "A" Moisture Separator has experienced level control oscillations in the past during .
CIV cycling. This finding was confirmed by review of plant process computer printouts from past CIV testing. -It was i apparent that the personnel performing the tests waited up to three minutes between CIV cycles to. allow Moisture Separator levels to stabilize. This system response, however, was considered normal and as such, a work request was not initiated
, to troubleshoot the level control system.
Performance of Surveillance Procedure by NCO :
The NCO who performed the testing had done so on many prior ;
occasions. Post scram analysis determined that on this occasion, the NCO deviated from the surveillance procedure during performance of the test. The NCO did not wait 1 minuto '
between cycling CIV's, as required by the procedure for stabilization of EHC system pressures. He did, however, verify EHC system stabilization prior to cycling CIV-#4. As mentioned above, during previous tests, operators had waited up :
to 3 minutes for Moisture Separator levels to stabilize. It-should be noted that the procedure did not specify a waiting period for Moisture Separator stabilization. i APPARENT CAUSE OF OCCURRENCE All of the above factors combined to result in the scram, and
- it is not feasible to reconstruct the event and determine which factor played the primary role in the final result. As such, ,
.the root cause of this event has been classified as a combination of equipment failure and cognitive personnel errors.
PLANT TRANSXENT EMSPONSE
- 1. The "B" Secondary Condensate Pump Minimum Flow Valve did not open due to a failed air line on the valve actuator.
L The severe service of these valves subjects the valve and actuator to significant movement when cycled, making the actuator air lines failure prone. The air line was replaced and the valve retested satisfactorily.
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- 2. PAMS Pressure Recorder "A" was inoperable prior to this !
event due to recorder not advancing properly. .The ,
recorder was repaired and returned to service on 1/11/90.
L l' PAMS Pressure Recorder "B" did not ink properly during this event. The pens were replaced and the recorder was I, returned to service. '
- 3. A review was conducted of the failure of RRCS Division I ,- !
channel B failing to trip. This channel should trip when '
reactor pressure reaches 1071 PSIG. During the course of this event, the highest reactor pressure seen was 1075 i PSIG. Troubleshooting of associated RRCS pressure instrumentation found no problems, and tho' Channel "B" input was tested satisfactorily. It was concluded that Channel "B" did not trip because, with instrumentation ;
tolerances. considered, reactor pressure' did not quite' '
reach the setpoint for Channel "B" RRCS. !
PREVIOUS OCCURRENCES This'isthe first occurrence of a scram (or other type of reportable occurrence) at Hope Creek as a result of level control problems with a Moisture Separator. Additionally, a review of in-house experience indicates no history of significant operational type- problems with the Moisture .
Separators.
SAFETY' SIGNIFICANCE The potential safety impact of this event was minimal, as a- '
plant scram is an analyzed event, and with minor exceptions, all' systems responded as expected. None of the abnormal system -
responses posed a threat to the ability to achieve and maintain -
safe shutdown conditions. This event posed no threat to the i health and safety of the general public.
CORRECTIVE ACTIONS :
- 1. The "A" and "B" Moisture Separator instrumentation loops were tuned while at 25% reactor power following plant "
restart and the subject surveillance was again performed.
Level control of the Moisture Separators was observed during power - ascension from restart to 100%, and no deviations from expected responses were noted. ,
- 2. Planning Department will initiate a recurring task to calibrate Moisture Separator Drain Tank level controller (LIC-1040A).
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- 3. Systems Engineering will develop a loop response functional test for the Moisture Separator level control i instrumentation. !
- 4. The. General Manager and Operations Manager have communicated their expectations to all operators and supervisors regarding deficiencies noted in'this report. . ]
l S. The NCO who performed the subject surveillance test was counselled with regards to his actions in not adhering to the procedure.
- 6. Systems Engineering is pursuing a resolution to the movement of Secondary Condensate Pump Minimum Flow Valves.
~7. This event will be reviewed with all licensed personnel by- I the Nuclear Training Department during the next licensed operator requalification cycle.
- 8. The Maintenance Manager will review control of air I supplies to valve positioners following maintenance on air operated valves with all Maintenance Department personnel.
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ATTACHMENT 1 I MOISTURE SEPARATOR LEVEL CONTROL INSTRUMENTATION ]
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