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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20029D6631994-05-0303 May 1994 LER 94-003-00:on 940405,loss of Shutdown Cooling Occurred Due to an Inadvertent High Reactor Pressure Isolation Signal.Corrective Action:Operations Department Procedure Used to Restore Shutdown Cooling isolations.W/940503 Ltr ML20029C7501994-04-20020 April 1994 LER 94-001-01:on 940305,ESF Actuation/Isolation & Loss of Shutdown Cooling Occurred.Caused by Personnel Error. Technician counseled.W/940420 Ltr ML20045B4761993-06-14014 June 1993 LER 93-004-00:on 930516,component Failure in EHC Sys Resulted in Generator/Turbine Trip & Reactor Scram.Failed Components Replaced & Addl Monitoring Devices Installed on EHC sys.W/930614 Ltr ML20045B2861993-06-0909 June 1993 LER 93-003-00:on 930513,plant Transient Initiated When 13.8 Kv Pothead Failed,Inducing Voltage Drop & Phase Differential Relay Actuation Due to Loss of Offsite Power on 2 of 4 Vital Buses.Failed Pothead replaced.W/930609 Ltr ML20029C2071991-03-21021 March 1991 LER 91-005-00:on 910219,reactor Scram Relay Malfunction Resulted in Startup Level Control Valve Failing Closed. Caused by Failure of Relay Controlling Position of Rfw 12 Startup Level Control Valve.Relay replaced.W/910321 Ltr ML20029A6441991-02-25025 February 1991 LER 91-003-00:on 910125,channel C Primary Containment Isolation Sys Actuated,Resulting in Trip of Radwaste Area Supply & Exhaust Fans.Caused by Design Deficiency Re Steam Leak Detection Sys Cabinets.Fuse replaced.W/910225 Ltr ML20028H8531991-01-23023 January 1991 LER 90-035-00:on 901227,pipe Section on Svc Water Sys (Ssws) a Loop Developed Minor Through Wall Flaw.Caused by Pipe Corrosion.Pipe Section on Ssws Will Be Replaced Prior to Restart from Current Refueling outage.W/910123 Ltr ML20028H6781991-01-16016 January 1991 LER 90-025-01:on 901104,leak Discovered on Weld on Reactor Recirculation Instrument Line While Investigating Source of Drywell Leakage.Caused by Crack at Welded Joint Due to vibration-induced Fatigue.Line replaced.W/910116 Ltr ML20043F4521990-06-11011 June 1990 LER 90-007-00:on 900517,control Room Received Indication of Half Scram & Isolation of Inboard Reactor Water Cleanup Isolation Valve.Caused by Spurious Trip of Channel a Reactor Protection Sys Epa.Design Change implemented.W/900611 Ltr ML20043F6121990-06-11011 June 1990 LER 90-006-00:on 900512,filtration,recirculation & Ventilation Sys Recirculation Fan E Discovered Running by Nuclear Control Operator.Cause Not Determined.Work Orders Initiated to Inspect Flow switches.W/900611 Ltr ML20043A8691990-05-16016 May 1990 LER 90-004-00:on 900418,ground Fault on Motor Control Ctr Feeder Breaker Occurred & Resulted in de-energization of Reactor B Protection Sys.Cause Not Determined.Feeder Breaker & Trip Device replaced.W/900516 Ltr ML20043A9091990-05-16016 May 1990 LER 90-005-00:on 900419,determined That Inoperability of Liquid Radwaste Discharge Monitor Not Reported in Recent Radioactive Effluent Release Rept.Caused by Procedural Deficiency.Effluent Rept revised.W/900516 Ltr ML20012C5991990-03-15015 March 1990 LER 89-026-01:on 891231,leak from Weld on 1-inch Reactor Recirculation Sys Elbow Tap Flow Transmitter Instrument Line Joint Discovered.Caused by Equipment Failure Due to Installation Deficiency During Plant const.W/900315 Ltr ML20006F8651990-02-19019 February 1990 LER 90-002-00:on 900119,HPCI Outboard Steam Supply Isolation Valve Auto Closed on High Room Differential Temp Signal. Caused by Inoperative Temp Control Loop.Troubleshooting of Loop Initiated to Determine malfunction.W/900219 Ltr ML20011E3931990-02-0505 February 1990 LER 90-001-00:on 900106,turbine Trip on Moisture Separator High Level Resulted in Reactor Scram.Caused by Combination of Equipment Failure & Cognitive Personnel Errors.Moisture Separator Drain Control Instrumentation tuned.W/900205 Ltr ML20006C2571990-01-30030 January 1990 LER 89-026-00:on 891231,leak from Weld on Reactor Recirculation Sys Flow Transmitter Instrument Line Joint Discovered.Cause Not Stated.Instrument Line Cut Out & Replaced W/New Section of piping.W/900130 Ltr ML20011E1301990-01-29029 January 1990 LER 89-025-00:on 891230,turbine Trip Occurred During Performance of Main Turbine Thrust Bearing Wear Detector Surveillance.Caused by Malfunction of Limit Switch.Design Change Implemented for Keylock Bypass switch.W/900129 Ltr ML20005E2401989-12-28028 December 1989 LER 89-024-00:on 891129,determined That Surveillance Frequency for Safety Auxiliaries Cooling Sys Valve EG-HV-2302B Should Have Been Increased.Caused by Data Recording Error.Personnel counseled.W/891228 Ltr ML20005E2421989-12-27027 December 1989 LER 89-021-01:on 891013,concluded That Class 1E Electrical Separation Criteria Not Met in Reactor Protection Sys Panel. Caused by Inadequate Review of 1986 Design Change Package. Nonconforming Power Supplies removed.W/891227 Ltr ML19332E7931989-12-0606 December 1989 LER 89-022-01:on 891016,reactor Protection Sys Electric Protection Assemblies Opened,Resulting in Loss of RHR B Which Had Been Operating in Shutdown Cooling Mode.Caused by Low Voltage Output.Assemblies reset.W/891206 Ltr ML19332E8131989-12-0404 December 1989 LER 89-023-00:on 891104,full Reactor Protection Sys Signal Inadvertently Generated While Pressurizing Drywell,Resulting in Full Scram Signal.Caused by Procedural Deficiency. Integrated Leak Rate Test Procedure revised.W/891204 Ltr ML19327C2561989-11-15015 November 1989 LER 89-022-00:from 891016-27,scrams Experienced on Channel B Reactor Protection Sys Electric Assemblies & Nuclear Steam Supply Shutdown Sys Isolated,Resulting in Loss of Shutdown Cooling.Assemblies & Output Voltages reset.W/891115 Ltr ML19327C2701989-11-13013 November 1989 LER 89-020-00:on 891011,pressure Spike in Reactor Vessel Ref Leg Resulted in ESF Actuation During Filling & Venting of Pressure Transmitter.Caused by Personnel Error.Technicians Counseled & Retrained in Venting procedures.W/891113 Ltr ML19327C2711989-11-13013 November 1989 LER 89-021-00:on 891013,review of GE Transient Analysis Recording Sys Determined That Class 1E Electrical Separation Criteria Not Met in Two Reactor Protection Sys Panels. Nonconforming Power Supplies removed.W/891113 Ltr ML19354D4411989-11-0303 November 1989 LER 89-019-00:on 891004,inadequate Instrumentation Used on Core Spray Pumps for ASME Section XI Testing.Caused by Inadequate Design Change Package.Event Reviewed W/Station Inservice Testing engineer.W/891103 Ltr ML19325E8811989-11-0202 November 1989 LER 89-018-00:on 891003,determined That Two Tech Spec Required Readings Not Taken as Required When Vent Monitoring Sys Inoperable on 890929.Caused by Lack of Adequate Communication.Personnel Involved counseled.W/891102 Ltr 1994-05-03
[Table view] Category:RO)
MONTHYEARML20029D6631994-05-0303 May 1994 LER 94-003-00:on 940405,loss of Shutdown Cooling Occurred Due to an Inadvertent High Reactor Pressure Isolation Signal.Corrective Action:Operations Department Procedure Used to Restore Shutdown Cooling isolations.W/940503 Ltr ML20029C7501994-04-20020 April 1994 LER 94-001-01:on 940305,ESF Actuation/Isolation & Loss of Shutdown Cooling Occurred.Caused by Personnel Error. Technician counseled.W/940420 Ltr ML20045B4761993-06-14014 June 1993 LER 93-004-00:on 930516,component Failure in EHC Sys Resulted in Generator/Turbine Trip & Reactor Scram.Failed Components Replaced & Addl Monitoring Devices Installed on EHC sys.W/930614 Ltr ML20045B2861993-06-0909 June 1993 LER 93-003-00:on 930513,plant Transient Initiated When 13.8 Kv Pothead Failed,Inducing Voltage Drop & Phase Differential Relay Actuation Due to Loss of Offsite Power on 2 of 4 Vital Buses.Failed Pothead replaced.W/930609 Ltr ML20029C2071991-03-21021 March 1991 LER 91-005-00:on 910219,reactor Scram Relay Malfunction Resulted in Startup Level Control Valve Failing Closed. Caused by Failure of Relay Controlling Position of Rfw 12 Startup Level Control Valve.Relay replaced.W/910321 Ltr ML20029A6441991-02-25025 February 1991 LER 91-003-00:on 910125,channel C Primary Containment Isolation Sys Actuated,Resulting in Trip of Radwaste Area Supply & Exhaust Fans.Caused by Design Deficiency Re Steam Leak Detection Sys Cabinets.Fuse replaced.W/910225 Ltr ML20028H8531991-01-23023 January 1991 LER 90-035-00:on 901227,pipe Section on Svc Water Sys (Ssws) a Loop Developed Minor Through Wall Flaw.Caused by Pipe Corrosion.Pipe Section on Ssws Will Be Replaced Prior to Restart from Current Refueling outage.W/910123 Ltr ML20028H6781991-01-16016 January 1991 LER 90-025-01:on 901104,leak Discovered on Weld on Reactor Recirculation Instrument Line While Investigating Source of Drywell Leakage.Caused by Crack at Welded Joint Due to vibration-induced Fatigue.Line replaced.W/910116 Ltr ML20043F4521990-06-11011 June 1990 LER 90-007-00:on 900517,control Room Received Indication of Half Scram & Isolation of Inboard Reactor Water Cleanup Isolation Valve.Caused by Spurious Trip of Channel a Reactor Protection Sys Epa.Design Change implemented.W/900611 Ltr ML20043F6121990-06-11011 June 1990 LER 90-006-00:on 900512,filtration,recirculation & Ventilation Sys Recirculation Fan E Discovered Running by Nuclear Control Operator.Cause Not Determined.Work Orders Initiated to Inspect Flow switches.W/900611 Ltr ML20043A8691990-05-16016 May 1990 LER 90-004-00:on 900418,ground Fault on Motor Control Ctr Feeder Breaker Occurred & Resulted in de-energization of Reactor B Protection Sys.Cause Not Determined.Feeder Breaker & Trip Device replaced.W/900516 Ltr ML20043A9091990-05-16016 May 1990 LER 90-005-00:on 900419,determined That Inoperability of Liquid Radwaste Discharge Monitor Not Reported in Recent Radioactive Effluent Release Rept.Caused by Procedural Deficiency.Effluent Rept revised.W/900516 Ltr ML20012C5991990-03-15015 March 1990 LER 89-026-01:on 891231,leak from Weld on 1-inch Reactor Recirculation Sys Elbow Tap Flow Transmitter Instrument Line Joint Discovered.Caused by Equipment Failure Due to Installation Deficiency During Plant const.W/900315 Ltr ML20006F8651990-02-19019 February 1990 LER 90-002-00:on 900119,HPCI Outboard Steam Supply Isolation Valve Auto Closed on High Room Differential Temp Signal. Caused by Inoperative Temp Control Loop.Troubleshooting of Loop Initiated to Determine malfunction.W/900219 Ltr ML20011E3931990-02-0505 February 1990 LER 90-001-00:on 900106,turbine Trip on Moisture Separator High Level Resulted in Reactor Scram.Caused by Combination of Equipment Failure & Cognitive Personnel Errors.Moisture Separator Drain Control Instrumentation tuned.W/900205 Ltr ML20006C2571990-01-30030 January 1990 LER 89-026-00:on 891231,leak from Weld on Reactor Recirculation Sys Flow Transmitter Instrument Line Joint Discovered.Cause Not Stated.Instrument Line Cut Out & Replaced W/New Section of piping.W/900130 Ltr ML20011E1301990-01-29029 January 1990 LER 89-025-00:on 891230,turbine Trip Occurred During Performance of Main Turbine Thrust Bearing Wear Detector Surveillance.Caused by Malfunction of Limit Switch.Design Change Implemented for Keylock Bypass switch.W/900129 Ltr ML20005E2401989-12-28028 December 1989 LER 89-024-00:on 891129,determined That Surveillance Frequency for Safety Auxiliaries Cooling Sys Valve EG-HV-2302B Should Have Been Increased.Caused by Data Recording Error.Personnel counseled.W/891228 Ltr ML20005E2421989-12-27027 December 1989 LER 89-021-01:on 891013,concluded That Class 1E Electrical Separation Criteria Not Met in Reactor Protection Sys Panel. Caused by Inadequate Review of 1986 Design Change Package. Nonconforming Power Supplies removed.W/891227 Ltr ML19332E7931989-12-0606 December 1989 LER 89-022-01:on 891016,reactor Protection Sys Electric Protection Assemblies Opened,Resulting in Loss of RHR B Which Had Been Operating in Shutdown Cooling Mode.Caused by Low Voltage Output.Assemblies reset.W/891206 Ltr ML19332E8131989-12-0404 December 1989 LER 89-023-00:on 891104,full Reactor Protection Sys Signal Inadvertently Generated While Pressurizing Drywell,Resulting in Full Scram Signal.Caused by Procedural Deficiency. Integrated Leak Rate Test Procedure revised.W/891204 Ltr ML19327C2561989-11-15015 November 1989 LER 89-022-00:from 891016-27,scrams Experienced on Channel B Reactor Protection Sys Electric Assemblies & Nuclear Steam Supply Shutdown Sys Isolated,Resulting in Loss of Shutdown Cooling.Assemblies & Output Voltages reset.W/891115 Ltr ML19327C2701989-11-13013 November 1989 LER 89-020-00:on 891011,pressure Spike in Reactor Vessel Ref Leg Resulted in ESF Actuation During Filling & Venting of Pressure Transmitter.Caused by Personnel Error.Technicians Counseled & Retrained in Venting procedures.W/891113 Ltr ML19327C2711989-11-13013 November 1989 LER 89-021-00:on 891013,review of GE Transient Analysis Recording Sys Determined That Class 1E Electrical Separation Criteria Not Met in Two Reactor Protection Sys Panels. Nonconforming Power Supplies removed.W/891113 Ltr ML19354D4411989-11-0303 November 1989 LER 89-019-00:on 891004,inadequate Instrumentation Used on Core Spray Pumps for ASME Section XI Testing.Caused by Inadequate Design Change Package.Event Reviewed W/Station Inservice Testing engineer.W/891103 Ltr ML19325E8811989-11-0202 November 1989 LER 89-018-00:on 891003,determined That Two Tech Spec Required Readings Not Taken as Required When Vent Monitoring Sys Inoperable on 890929.Caused by Lack of Adequate Communication.Personnel Involved counseled.W/891102 Ltr 1994-05-03
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217F1501999-10-12012 October 1999 Special Rept:On 990929,south Plant Vent (SPV) Range Ng Monitor Was Inoperable.Monitor Was Inoperable for More than 72 H.Caused by Electronic Noise Generated from Noise Suppression Circuit.Replaced Circuit ML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data ML20217N6531999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Hope Creek Generating Station,Unit 1.With ML20217M0211999-09-20020 September 1999 Part 21 Rept Re Possible Deviation of NLI Dc Power Supply Over Voltage Protection Circuit Actuation.Caused by Electrical Circuit Conditions Unique to Remote Engine Panel. Travelled to Hope Creek to Witness Startup Sequence of DG ML20211N5531999-09-0808 September 1999 Safety Evaluation Supporting Amend 121 to License NPF-57 ML20211B3781999-08-13013 August 1999 Special Rept 99-002:on 990730,NPV Radiation Monitoring Sys Was Declared Inoperable.Caused by Voltage Induced in Detector Output by Power Cable to Low Range Sample Pump. Separated Cables & Secured in Place to Prevent Recurrence ML20210U4721999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Hope Creek Generating Station,Unit 1.With ML20216D8331999-07-26026 July 1999 Safety Evaluation Concluding That Licensee IPEEE Complete Re Info Requested by Suppl 4 to GL 88-20 & That IPEEE Results Reasonable Given HCGS Design,Operation & History ML20216D8721999-07-26026 July 1999 Review of Submittal in Response to USNRC GL 88-20,Suppl 4: 'Ipeees,' Fire Submittal Screening Review Technical Evaluation Rept:Hope Creek Rev 1:980518 ML20210F3331999-07-22022 July 1999 Safety Evaluation Granting Relief Requests RR-B1,RR-C1,RR-D1 & RR-B3.Finds That Proposed Alternative for RR-B3 Provides Acceptable Level of Quality & Safety & Authorizes Alternative Pursuant to 10CFR50.55a(a)(3)(i) ML20210C4731999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Hope Creek Generating Station,Unit 1.With ML20216D8901999-06-30030 June 1999 IPEEEs Technical Evaluation Rept High Winds,Floods & Other External Events ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML18107A3441999-06-0101 June 1999 Interim Part 21 Rept Re Premature Over Voltage Protection Actuation in Circuit Specific Application in Dc Power Supply.Testing & Evaluation Activities Will Be Completed on 990716 ML20196A1511999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Hope Creek Generating Station,Unit 1.With ML20206Q4731999-05-14014 May 1999 SER Accepting Response to GL 97-05, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Plant ML20206U1571999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Hope Creek Generating Station,Unit 1.With ML20216D8451999-04-30030 April 1999 Rev 1, Submittal-Only Screening Review of Hope Creek Unit 1 IPEEE (Seismic Portion). Finalized April 1999 ML20206C8481999-04-22022 April 1999 SER Authorizing Pse&G Proposed Relief Requests Associated with Changes Made to Repair Plan for Core Spray Nozzle Weld N5B Pursuant to 10CFR50.55a(a)(3)(i) LR-N990157, Special Rept 99-001:on 990315, C EDG Valid Failure Occurred During Surveillance Testing.Testing Resulted in Unsuccessful Loading Attempt,Due to Failure EDG Output Breaker to Close.Faulty Card Replaced1999-04-12012 April 1999 Special Rept 99-001:on 990315, C EDG Valid Failure Occurred During Surveillance Testing.Testing Resulted in Unsuccessful Loading Attempt,Due to Failure EDG Output Breaker to Close.Faulty Card Replaced ML20205R5901999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Hope Creek Generating Station,Unit 1.With ML20205G6051999-03-19019 March 1999 SER Accepting Relief Request Re Acme Code Case N-567, Alternate Requirements for Class 1,2 & 3 Replacement Components,Section Xi,Div 1 ML20205F8911999-03-18018 March 1999 Safety Evaluation Authorizing Licensee Requests for Second 10-year Interval for Pumps & Valves IST Program ML20204F7951999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Hope Creek Generating Station,Unit 1.With ML18106B0931999-02-25025 February 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Caused by Crack Due to Improper Location of Heated Bar.Only One Part Out of 7396 Pieces in Forging Lot Was Found to Be Cracked.Affected Util,Notified ML18106B0551999-02-0101 February 1999 Part 21 Rept Re Possible Matl Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Defect Is Crack in Center of Forging.Analysis of Part Is Continuing & Further Details Will Be Provided IAW Ncr Timetables.Drawing of Part,Encl ML18106B0441999-01-29029 January 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee Part Number SS-6-T.Caused by Crack in Center of Forging. Continuing Analysis of Part & Will Provide Details in Acoordance with NRC Timetables ML20202F6861999-01-26026 January 1999 Engine Sys,Inc Part 21 (10CFR21-0078) Rept Re Degradation of Synchrostat Model ESSB-4AT Speed Switches Resulting in Heat Related Damage to Power Supply Card Components.Caused by Incorrect Sized Resistor.Notification Sent to Customers ML18107A1871998-12-31031 December 1998 PSEG Annual Rept for 1998. ML20199E7271998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Hope Creek Generating Station,Unit 1.With ML18107A1881998-12-31031 December 1998 PECO 1998 Annual Rept. LR-N980580, Monthly Operating Rept for Nov 1998 for Hope Creek Generating Station,Unit 1.With1998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Hope Creek Generating Station,Unit 1.With ML20198N4161998-11-12012 November 1998 MSIV Alternate Leakage Treatment Pathway Seismic Evaluation LR-N980544, Monthly Operating Rept for Oct 1998 for Hcgs,Unit 1. with1998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Hcgs,Unit 1. with ML20155J9861998-10-31031 October 1998 Non-proprietary TR NEDO-32511, Safety Review for HCGS SRVs Tolerance Analyses LR-N980491, Monthly Operating Rept for Sept 1998 for Hope Creek Generating Station,Unit 1.With1998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Hope Creek Generating Station,Unit 1.With ML17354B0971998-09-0909 September 1998 Part 21 Rept Re Possible Machining Defect in Certain One Inch Stainless Steel Swagelok Front Ferrules,Part Number SS-1613-1.Caused by Tubing Slipping Out of Fitting at Three Times Working Pressure of Tubing.Notified Affected Utils LR-N980439, Monthly Operating Rept for Aug 1998 for Hope Creek Generating Station Unit 1.With1998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Hope Creek Generating Station Unit 1.With LR-N980401, Monthly Operating Rept for July 1998 for Hope Creek Generating Station,Unit 11998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Hope Creek Generating Station,Unit 1 ML20236N6751998-07-0909 July 1998 Part 21 & Deficiency Rept Re Notification of Potential Safety Hazard from Breakage of Cast Iron Suction Heads in Apkd Type Pumps.Caused by Migration of Suction Head Journal Sleeve Along Lower End of Pump Shaft.Will Inspect Pumps LR-N980354, Monthly Operating Rept for June 1998 for Hope Creek Generating Station,Unit 11998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Hope Creek Generating Station,Unit 1 ML20236E9491998-06-30030 June 1998 Rev 0 to non-proprietary Rept 24A5392AB, Lattice Dependent MAPLHGR Rept for Hope Creek Generating Station Reload 7 Cycle 8 ML18106A6821998-06-24024 June 1998 Revised Charting Our Future. ML18106A6681998-06-17017 June 1998 Charting the Future. LR-N980302, Monthly Operating Rept for May 1998 for Hope Creek Generating Station,Unit 11998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Hope Creek Generating Station,Unit 1 ML20248C7381998-05-22022 May 1998 Rev 0 to Safety Evaluation 98-015, Extension of Allowed Out of Service Time for B Emergency Diesel Generator LR-N980247, Monthly Operating Rept for Apr 1998 for Hope Creek Station, Unit 11998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Hope Creek Station, Unit 1 LR-N980196, Monthly Operating Rept for Mar 1998 for Hope Creek Generating Station,Unit 11998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Hope Creek Generating Station,Unit 1 ML20217D5701998-03-20020 March 1998 Part 21 Rept 40 Re Governor Valve Stems Made of Inconel 718 Matl Which Caused Loss of Governor Control.Control Problems Have Been Traced to Valve Stems Mfg by Bw/Ip.Id of Carbon Spacer Should Be Increased to at Least .5005/.5010 ML18106A5851998-03-0303 March 1998 Emergency Response Graded Exercise,S98-03. Nuclear Business Unit Salem,Hope Creek Emergency Preparedness, 980303 1999-09-08
[Table view] |
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, Putac Servico Electric and Gas Company P.O. Box 236 Hancocks B9dge, New Jett.ey 08038 !
' Hope Creek Operations l
! I January 29, 1990 i
- j. U. 8. Nuclear Regulatory Commission I t
Document Control Desk- :
Washington, DC 20555 i
I' Dear Sir l l HOPE CREEK GENERATING STATION DOCKET No. 50-354 '
UNIT NO. 1 LICENSEE EVENT REPORT 89-025-00 l, This Licensee' Event Report is being submitted pursuant to [
the requirements of 10CFR50.73 (a) (2) (iv) .
Since ely, ,
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Hope Creek Operations i RBC/ -t Attachment 80RC Mtg.90-010 C Distribution I
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Amr!RAct (16) l On 12/30/89 at 1947, during the performance of the TBWD section of the M2in Turbine Monthly Functional Test procedure, a turbine trip occurred.
l This trip was followed immediately by a reactor scram via the Reactor Protection System on a turbine control valve fast closure signal. All control rods inserted, and plant systems responded as expected, with minor '
l 0xceptions as noted in the text of this report. Investigation subsequent l to the event determined that a TBWD limit switch had malfunctioned during the test, resulting in the turbine trip circuitry sensing that the turbine l cnd thrust bearing had actually failed. While the initiating cause of
-this event was the TBWD limit switch failure, the root cause of this event l wcs the inadequate prioritization of a design change which had been I p:nding since 1988. This design change would have modified the TBWD -
l' circuitry to prevent a turbine trip signal while testing the TBWD.
Corrective actions included implementing this design change, repairing the TBWD limit switch, reviewing all other " scram reduction" design changes for adequate prioritization, reviewing other turbine trip test procedures for administrative adequacy, and incorporating this event into appropriate training programs.
I
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, LIGNSEE LYDft RDWT (11R) 'I1XT GNTDARTIW IIR IDEER (6)
FACRTIY NAPE (1) DOCIET I M Ht (2) PME (3)
N ** IMEER ** RLY IEE GEIK GNERATING STATIM 05000354 89 -
0 2 5 -
0 0 0 2 G' O 8 PLANT AND SYSTEM IDENTIFICATION General Electric - Boiling Water Reactor (BWR/4)
Main Turbine (EIIS Designation: TA)
Main Steam System (EIIS Designation: SB)
Reactor Protection System (EIIS Designation: JC)
Control Rod Drive System (EIIS Designation: AA)
Rod Position Indication System (EIIS Designation: IG)
IDENTIFICATION OF OCCURRENCE Reactor Scram buring Performance of Main Turbine Thrust Bearing i
Wear Detector (TBWD) Surveillance Due to Malfunction of TBWD Limit Switch and Inadequate Prioritization of a Pending Design Change Event Date: 12/30/89 Event Time: 1947 This LER was initiated by Incident Report No.89-184 CONDITIONS PRIOR TO OCCURRENCE Plant in OPERATIONAL CONDITION 1 (Power Operation), Reactor Power 100%, Unit Load 1118 MWe, Monthly turbine generator surveillance procedure in progress.
pESCRIPT?ON OF OCCURRENCE On 12/30in' it 1947, during the performance of the Main Turbine Monthly F ional Test procedure, a turbine trip occurred.
This trip wt> followed immediately by a reactor scram via the Reactor Protection System (RPS) on a turbine control valve fast closure signal. All control rods inserted, and plant systems responded as expected, with the following exceptions:
Safety Relief Valve (SRV) "11" (lo-lo set) liftod as designed, but SRV "P" (also a lo-lo set) did not.
Additionally, SRV "M" lifted, apparently at a pressure lower than designed.
Control rod 34-27 did not properly indicate rod position.
Additionally, operators did not initially receive a
" full-in" indication on rod 34-11.
Scram Diucharge Volume drain valve IBF-HV-F0ll did not give an open indication after the scram signal was reset.
Operators could not immediately restart Reactor Recirc Pumps "A" and "B".
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, DESCRIPTION OF OCCURRENCE, CONT'D [
During the transient, vessel level decreased to' approximately .
+2 inches, which is 40"'above any Emergency Core Cooling System
-(ECCS)-actuation setpoints. Vessel- level was restored to .
. normal (+35 inches) using the "A" RFP. 'Following stabilization
.of plant parameters, a four hour non-emergency report was made to the NRC Operations Center IAW 10CFR50.72 and station administrative procedures, and an investigation was -initiated ;
to determine the cause of the scram. ;
ANALYSIS OF OCCURRENCE The monthly TBWD test is performed in the control room at the TBWD panel (see Attachment 1). This test temporarily bypasses the thrust bearing wear turbine trip circuit, and exercises-the wear detector mechanism through its limits of travel. . When the
" TEST TURBINE END" pushbutton on the TBWD panel is depressed, the'following actions occur: '
L The " TEST TURBINE END pushbutton backlights i
The " TESTING" lamp is illuminated 3 l -
The " THRUST BEARING WEAR DETECTOR" indicator moves in the negative direction.
At the turbine mid-standard, the actual TBWD mechanism l test drive motor starts to move in the direction of- the L turbine.
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On- the TBWD mechanism, a cam operated limit switch (TWS-11) closes-to maintain the detector in " TEST" while during performance of the test.
When the TBWD reaches the turbine trip setpoint (approximately I ~40 mils), the test motor stops, and the " TEST TURBINE END" pushbutton is released. With TWS-11 still closed, the TBWD drive motor should run back to the "0" (neutral) position, which completes the test.
Contrary to this normal scenario, during the performance of this test on 12/30/89 at about 1947, the drive motor did not drive back to the "0" position when the Nuclear Control Operator (NCO, RO licensed) conducting the test released the
" TEST TURBINE END" pushbutton. With the TBWD still above the turbine trip setpoint, and the pushbutton released, a five second tin.o delay relay was de-energized (the relay maintains the circuit in a " test" condition while the pushbutton is depressed).
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ANALYSIS OF OCCURRENCE, SQFf,R Because of a malfunction of limit switch TWS-ll, the drive motor did'not energize to run the TBWD back below the trip setpoint, and after 5 seconds, a turbine trip occurred, and as previously noted, an RPS-initiated reactor scram occurred.
Investigations conducted subse ent to the scram focused on the conduct _of the test procedure, content of the test procedure, the apparent equipment failure of TBWD limit switch TWS-ll, the NCO's knowledge of the test requirements, and a previously identified design change which had not. been implemented. It should be noted at this point that this scram is very similar to a scram which occurred on 8/26/88 (refer to LER 88-022).
With respect to conduct of the procedure, it was determined that the NCO followed the procedure in a proper manner. The procedure cautions the performer that if the indicator does not move back toward "0" when the " TEST TURBlNE END" pushbutton is released, to depress and hold the pushbutton (to prevent a turbine trip) and to immediately call for assistance. When the NCO realized that the indicator was not moving, he immediately reached for the pushbutton, but the turbine tripped before he could depress the pushbutton.
The TBWD test procedure was reviewed for adequacy. While a previously identified change had not yet been incorporated into the procedure at the time of this incident, the procedure was functional as written, and had no bearing on_this event.
The proper functioning of limit switch TWS-ll was investigated.
When reviewing the equipment history of TWS-11, it was determined that a malfunction of this limit switch (a ' loose limit switch arm) caused an almost identical scram in 1988, as previously noted. Subsequent to the 1988 scram, another switch had been installed. The subject test had been performed two times previous to the scram noted in this report with no apparent precursory results that would indicate the switch was not functioning properly. Immediately following the scram, the Senior Nuclear Shift Supervisor (SNSS, SRO licensed) proceeded to the TBWD mechanism at the main turbine, and discovered that the drive mechanism was stopped at about -40 mila. When he tapped the drive mechanism, it energized and drove to "0".
This troubleshooting by the SNSS produced the only witnessed failure of the limit switch. Subsequent troubleshooting could not reproduce the actual failure, but determined that a less than optimum alignment between the cam and limit switch and a loose terminal screw inside the switch were the primary contributors to the switch failing to properly operate.
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&NALYSIS OF OCCURRENCE. CONT'D In reviewing the NCO's familiarity with the test being performed, it was noted that this was the first time the .NCO '
had performed this test. However, the NCO had received extensive training which covered the aspects of the 1988 TBWD scram, and had practiced performing the procedure in- the i simulator. It was concluded that the NCO was familiar with the procedure and that familiarity (or lack thereof) of the test procedure / methods for the-TBWD did not influence subsequent events.
Lastly, the effect of a. pending design change on the TBWD circuitry was reviewed. Following the 1988 scram, and based on input from the BWR Owners Group Scram Frequency Reduction
~ Committee, in September of 1988, Systems Engineering initiated a design change to- the test circuitry which would entirely bypass'the TBWD trip circuitry during testing. The design change consisted of installing a keylock bypass switch on the TBWD panel-and was scheduled for implementation during the 1991 refueling outage.
APPARENT CAUSE OF OCCURRENCE
~The initiating cause of this event was the failure of the TBWD limit switch, TWS-11. The primary cause of this event, however, was the inadequate prioritization of the previously-described design change.
i PLANT TRANBIENT RESPONSE All plant systems responded as expected with the exception of the system responses noted in the " Description of ' Occurrence".
With respect to these exceptions, the post scram analysis determined the following:
- 1. The "P" SRV io-lo set, 1047 PSIG) did not lift due to a failed pressure transmitter. The transmitter was replaced and retested satisfactorily prior to plant restart.
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- 2. The "M" SRV lifted because the "P" SRV did not. A review of GETARS printouts indicates that reactor pressure increased to approximately 1090 PSIG, which is within the setpoint range of the "M" SRV (with tolerance of the SRV and reactor pressure instrumentation considered). It was determined that the lifting of the "M" SRV was proper.
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PLANT TRANSIENT RESPONSE. CONT'D
- 3. With respect to the improper rod position indication on control rods 34-27 and 34-11, troubleshooting determined that the position indication probes for these two rods required replacement. The probes are currently bypassed, awaiting replacement at the first available opportunity.
- 4. SDV drain valve 1BF-HV-F0ll was tested to determine if a problem existed with the valve or associated position indication. Stroke time testing indicated that the valve was stroking within acceptable time limits, however, closing stroke times indicated a need for increasing the surveillance frequency on the valve from quarterly to monthly. This has been accomplished, and appropriate ASME Section XI Inservice Testing followup will be conducted.
No problems were noted with the associated position indication.
- 5. Troubleshooting on Reactor Recirc Pumps "A" and "B" determined that the inability to immediately restart these pumps stemmed from the timing sequencer controls.
The timing sequencer was cleaned and retested satisfactorily.
PREVIOUS OCCURRENCES As noted elsewhere in this report, a similar scram occurred on August 26, 1988 (refer to LER 88-022-00). However, the failure mode of the TBWD limit switch was different, as such, the corrective actions as described in LER 88-022 (test method changes) would not have prevented this occurrence.
SAFETY S1GNIFICANCE The potential safety impact of this event was minimal, as a plant scram is an analyzed event, and with minor exceptions, all systems responded as expected. None of the abnormal system responses posed a threat to the ability to achieve and maintain safe shutdown conditions. This event posed no threat to the health and safety of the general public.
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- CORRECTIVE ACTIONS
- 1. - The design change to. install a keylock bypass switch on ;,
the. TBWD' panel to entirely . bypass' the turbine. trip circuitry.during TBWD testing was implemented. Use- of-this switch.will preclude any future turbine trips during L
TBWD testing.
- 2. TBWD limit switch TWS-11 was re-aligned and all terminal screwb verified to be properly tightened..
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- 3. A review 'of all previously identified scram' reduction Ll design . changes was accomplished: to ensure proper -
l prioritization of these changes.
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I 4.- A review of all other turbine trip test-procedures will be l' conducted to ensure that adequate procedural cautions exist to prevent a trip and that adequate physical trip l
in lockout protection exists to prevent such a trip.
l S '. Systemu Engineering -will evaluate. the effectiveness and l s irequency of preventive maintenance activities on--the l Recirc Pump-timing.' sequencer.
- 6. The Nuclear Training Department will incorporate a review of'this. event into appropriate lesson plans and training
. courses.
t R Since ely,
. . n General Manager -
Hope' Creek Operations RBC/'
SORC Mtg.90-010
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l-ATTACHMENT 1
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Thrust Bearing Wear Detector Panel L
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MECMANICAL Tair TRIPPED REstTTwo mtst?
MECMANICAL Tate TEST g,, g LOCKED OlL PUSM CUT Talp TO REstT MASTER Trip i SQLENoto TESTl MTORMA.g ELEC !
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