ML19350E491

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Updated LER 80-036/03X-1:on 800602,steam Driven Emergency Feedwater pump,2P7A,turbine driver,2K3,tripped on Overspeed Following Manual Start.Caused by Design Deficiency.Governor Valve Control Modified
ML19350E491
Person / Time
Site: Arkansas Nuclear Entergy icon.png
Issue date: 06/19/1981
From: Shively C
ARKANSAS POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19350E481 List:
References
LER-80-036-03X, LER-80-36-3X, NUDOCS 8106230167
Download: ML19350E491 (1)


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This occurrence is similar to LER's 50-368/78-032,79-055, 79-072i F6Til 179-081,79-104, .80-022 & 80 030. Reportable per T.S. 6.9.1.9.b. I i

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CAUSE Of SCR4PTION AND CORRECriVE ACTPONS 27 i o [Cause of the EFH turbine overspeed trips was detennined to be design i

[*1:1Irnlatod- Mndi fica t inne te thn nnunenne valun enntrni nntimi7nd nnvernnr j qTil Ivalve response to speed signals. A testing program verified EFW turbine i Refer to I FR Sn-16R/Rn-nc;n/01X-4 for further iaformation. I E lreliabilitv.

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