05000368/LER-1980-022-03, Steam Driven Emergency Feedwater pump,2P7A,turbine driver,2K3,tripped on Overspeed Upon Receipt of Low Steam Generator Level Signal.Caused by Design Deficiency.Governor Valve Control Modified

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Steam Driven Emergency Feedwater pump,2P7A,turbine driver,2K3,tripped on Overspeed Upon Receipt of Low Steam Generator Level Signal.Caused by Design Deficiency.Governor Valve Control Modified
ML19350E487
Person / Time
Site: Arkansas Nuclear 
Issue date: 06/19/1981
From: Shively C
ARKANSAS POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19350E481 List:
References
LER-80-022-03X, LER-80-22-3X, NUDOCS 8106230160
Download: ML19350E487 (1)


LER-1980-022, Steam Driven Emergency Feedwater pump,2P7A,turbine driver,2K3,tripped on Overspeed Upon Receipt of Low Steam Generator Level Signal.Caused by Design Deficiency.Governor Valve Control Modified
Event date:
Report date:
3681980022R03 - NRC Website

text

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i REVISEDREPORT-PREVIOUSREPORTDATE6f2/80 9

seRC FOnM M4 U.S.'fUCLE AR RECULATORY COMMIS$60N 1.lCENSEE EVENT REPORT EXHIBIT A

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(PLE ASE PRINT OR TYPE ALL REQUIRED.NFORMAf tONI CONTROL 8tOCutl l l l l l g1 11 l

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,oa,o.1, EVENT DE$CR6, VION AND PR0e A8LE CONSEQUE4CES h rim Ilmmediately following a plant trip, the Emergency Feedwater (EFW) Pump, I

f5Trl IPP7A. turbine drivor. 2K3. tripped nn nyerennnd nnnn enenint nf Fra ano 1 g o i.i lto low Steam Generator level.

The Electric Driven EFW PumD. 2P7B. and as-l filT) Isociated valves wre onorablo A connlind (officinnt fi ni., fnr the transientl o.

iresponse.

The overspeed trip was reset & the pump was successfully started s o lii 1 3 times, then declared operable.

Occorronen einilar te tgpe t 50-368/78-1 I o le 1 I 032.79-05E.__7S-072. 74 nR1. 74 1{L4 pennrtable ner T_S 6.9_1.9.b 1

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v C At>tt OESCRIPflON AND CCAnEC flVE AC.aONs 27 g it,ause of the tem Luioine overspeed trips was determined to be desian re-i g i ated. Modifications to the governor valve control optimized governor i

l m ivalve response to speed sianals.

A testina orogram verified EFW turbine I g [ reliability. Refer to LER 50-368/80-050/03X-4 for further informatinn 1

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