Final Deficiency Rept Re Design of Spent Fuel Pool Walls. Caused by Change in Critical Wall Intersection Conditions During Reinforcing.Spent Fuel Pool Reanalyzed & Walls Strut ReinforcedML19326C862 |
Person / Time |
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Arkansas Nuclear |
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Issue date: |
05/05/1975 |
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From: |
Phillips J ARKANSAS POWER & LIGHT CO. |
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To: |
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References |
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NUDOCS 8004280789 |
Download: ML19326C862 (6) |
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Category:DEFICIENCY REPORTS (PER 10CFR50.55E & PART 21)
MONTHYEARML20154E2171998-09-28028 September 1998 Follow-up Part 21 Rept Re Defect with 1200AC & 1200BC Recorders Built Under Westronics 10CFR50 App B Program. Westronics Has Notified Bvps,Ano & RBS & Is Currently Making Arrangements to Implement Design Mods LD-98-024, Part 21 Rept Re Deficiency in CE Current Screening Methodology for Determining Limiting Fuel Assembly for Detailed PWR thermal-hydraulic Sa.Evaluations Were Performed for Affected Plants to Determine Effect of Deficiency1998-08-13013 August 1998 Part 21 Rept Re Deficiency in CE Current Screening Methodology for Determining Limiting Fuel Assembly for Detailed PWR thermal-hydraulic Sa.Evaluations Were Performed for Affected Plants to Determine Effect of Deficiency ML20236X2351998-08-0505 August 1998 Part 21 Rept Re Defect Associated W/Westronics 1200AC & 1200BC Recorders Built Under Westronics 10CFR50,App B Program.Beaver Valley,Arkansas Nuclear One & River Bend Station Notified.Design Mod Is Being Developed ML20249B7791998-06-22022 June 1998 Part 21 Rept Re Findings,Resolutions & Conclusions Re Failure of Safety Related Siemens 4KV,350 MVA,1200 a Circuit Breakers to Latch Closed ML20217C2481998-04-21021 April 1998 Potential Part 21 Rept Re Failure of Siemens Circuit Breaker to Close Latch in Test Position W/Ge Test Flag Installed. Cause Indeterminate.Will Ship Identified Circuit Breakers to Siemens Mfg Facility in Wendell,Nc for Checking Procedure LD-97-033, Part 21 Rept Re Defect in Potter & Brumfield Mdr Relays, Models 170-1 & 7032.Extended Problem to Include All Mdr Relay Models W/Date Codes 93XX-95XX.Root Cause Analysis, Written Rept & Recommended Corrective Actions Due by 9712011997-11-20020 November 1997 Part 21 Rept Re Defect in Potter & Brumfield Mdr Relays, Models 170-1 & 7032.Extended Problem to Include All Mdr Relay Models W/Date Codes 93XX-95XX.Root Cause Analysis, Written Rept & Recommended Corrective Actions Due by 971201 LD-97-028, Part 21 Rept Re Contamination of Lubricant Which Has Led to Hardening of Lubricant in Certain Potter & Brumfield Mdr Relay Models 170-1 & 7032.Will Distribute Copy of Rept to Utils Having ABB-CE Designed Nuclear Steam Supply Sys1997-10-13013 October 1997 Part 21 Rept Re Contamination of Lubricant Which Has Led to Hardening of Lubricant in Certain Potter & Brumfield Mdr Relay Models 170-1 & 7032.Will Distribute Copy of Rept to Utils Having ABB-CE Designed Nuclear Steam Supply Sys ML20211M6491997-10-0808 October 1997 Addenda 1 to Part 21 Rept Re Weldments on Opposed Piston & Coltec-Pielstick Emergency stand-by Diesel gen-set lube-oil & Jacket Water Piping Sys.Revised List of Potentially Affected Utils to Include Asterisked Utils,Submitted ML20211H7911997-09-30030 September 1997 Part 21 Rept Re Failure of Weldment Associated w/lube-oil Piping Sys on 970804 at Millstone,Unit 2.Root Cause Is Not Yet Known.Quality of Weldment Is Being Considered.Listed Util Sites Affected LD-97-024, Part 21 Rept Re Error in Energy Redistribution Factor Used in LOCA Analysis for Listed Plants for Which ABB-CE Performed Analysis.Issued Recommendations Info Bulletin 97-0041997-08-14014 August 1997 Part 21 Rept Re Error in Energy Redistribution Factor Used in LOCA Analysis for Listed Plants for Which ABB-CE Performed Analysis.Issued Recommendations Info Bulletin 97-004 ML20134B2301997-01-24024 January 1997 Final Part 21 Rept Re Potential Safety Concern on Matl Used for Fabrication of Permanent Canal Seal Plate.Correpondence W/Fabricator & Matl Supplier Documents Tig Automated Welding Process Used to Fabricate Angle Pieces LD-96-045, Part 21 Rept Re Application of Certain Aspects of ABB-CE Safety Analysis Methodology1996-10-18018 October 1996 Part 21 Rept Re Application of Certain Aspects of ABB-CE Safety Analysis Methodology LD-96-009, Part 21 Rept Re Potential Instrumentation Decalibr at Low Power.Affected Utils Should Ensure That Log Power Channels Properly Calibr & cross-correlated to Linear Power Channels at 100% Reactor Power1996-04-15015 April 1996 Part 21 Rept Re Potential Instrumentation Decalibr at Low Power.Affected Utils Should Ensure That Log Power Channels Properly Calibr & cross-correlated to Linear Power Channels at 100% Reactor Power ML20101N8441996-04-0505 April 1996 Interim Part 21 Rept Re Potential Safety Concern on Matl for Fabrication of Permanent Canal Seal Plate.Licensee Will Provide Final Rept to NRC in Approx Six Months Upon Completion of Evaluation of Welds ML20082E7421995-04-0404 April 1995 Part 21 Rept Re Nonconformance in Dresser Industries,Inc (Dresser) MSSV Owned by Entergy Operations,Inc ANO Unit 1. Part Used in Safety Valve That Was Not Mfg to Spec Requirements & Not Mfg Nor Provided by Dresser ML20070Q5721994-05-10010 May 1994 Part 21 Rept Re Potential Defect of Samtec,Inc 11-pin Connector Socket in Pro Series Bargraph Instrumentation. All safety-related Bargraphs That May Contain Suspect Connector Have Been Identified & Licensee Notified ML20059H7721994-01-17017 January 1994 Part 21 Rept Re Virginia Power Notifying Fairbands Morse Via Failure Analysis Rept NESML-Q-058 of Defective Air Start Distributor cam,16104412 ML20059F2631994-01-0707 January 1994 Part 21 Rept Re Air Start Distributor Cam Mfg by Fairbanks Morse.Mfg Suggests That Site Referenced in Encl App I Inspect Air Start Distributor Cam as Soon as Practical ML20058G5981993-11-17017 November 1993 Part 21 Rept Re Westronics Recorders,Model 2100C.Signal Input Transition Printed Circuit Board Assembly Redesigned to Improve Recorder Immunity to Electromagnetic Interference.List of Affected Recorders & Locations Encl ML20057G1511993-10-0707 October 1993 Part 21 Rept Re Westronics Model 2100C Series Recorders. Informs That Over Several Tests,Observed That Recorder Would Reset During Peak Acceleration & Door Being Forced Off Recorder.Small Retaining Clips Added to Bottom of Door ML20044G5011993-05-26026 May 1993 Part 21 Rept Re Buffer Amplifier Modules Mfg by Bailey Controls Co Containing Suspect Negative Ref Power Supply Having Safety Implications.Caused by Design Error in Circuitry.Modules Would Not Result in Miscalibration ML20044G5311993-05-26026 May 1993 Suppl to 921207 Part 21 Rept Re Declutch Sys Anomaly in Certain Types of Valve Actuators Supplied by Limitorque Corp.Limitorque Designed New Declutch Lever Which Will Be Available in First Quarter 1993 LD-93-003, Part 21 Rept Re Defect in Potter & Brumfield Model 170-1 Relay.One of Two Rotor Return Springs Broke & Portion of Spring Lodged Between Rotor & Stator.Rotor Springs Supplied by Lewis Spring Co.Info Bulletin Being Prepared1993-01-13013 January 1993 Part 21 Rept Re Defect in Potter & Brumfield Model 170-1 Relay.One of Two Rotor Return Springs Broke & Portion of Spring Lodged Between Rotor & Stator.Rotor Springs Supplied by Lewis Spring Co.Info Bulletin Being Prepared ML20126J5961992-12-31031 December 1992 Part 21 Rept Re Potential Loss of RHR Cooling During Nozzle Dam Removal.Nozzle Dams May Create Trapped Air Column Behind Cold Leg Nozzle Dam.Mod to Nozzle Dams Currently Underway. Ltrs to Affected Utils Encl ML20126F8081992-12-22022 December 1992 Part 21 Rept Re Possible Condition of Gag Plug in Cap of Valves That Cause Valves Not to Lift to Requirement for Providing Full Capacity.Affected Customers Notified.Removal of Caps &/Or Gag Plugs Recommended ML20125C7161992-12-0707 December 1992 Part 21 Rept Re Possibility for Malfunction of Declutching Mechanisms in SMB/SB-000 & SMB/SB/SBD-00 Actuators. Malfunction Only Occurs During Seismic Event.Balanced Levers May Be Purchased from Vendor.List of Affected Utils Encl ML20127P5861992-11-23023 November 1992 Followup to 921005 Part 21 Rept Re Potential Defect in SB/SBD-1 Housing Cover Screws.Procedure Re Replacement of SBD-1 Spring Cover Bolts Encl.All Fasteners Should Be Loosened & Removed.List of Affected Utils Encl 0CAN119206, Part 21 Rept Re Inadequacy of Asea Brown Boveri (ABB) ITE-62L Solid State Relays W/Respect to Electrical Noise Immunity.Subj Relays Installed in Unit 1 RB Cooler Control Circuitry Will Be Replaced During Unit 1 Refueling Outage1992-11-11011 November 1992 Part 21 Rept Re Inadequacy of Asea Brown Boveri (ABB) ITE-62L Solid State Relays W/Respect to Electrical Noise Immunity.Subj Relays Installed in Unit 1 RB Cooler Control Circuitry Will Be Replaced During Unit 1 Refueling Outage ML20115C7151992-10-13013 October 1992 Initial Part 21 Rept Re ABB Pneumatic Timers in Control Circuits for EDG Svc Water Pumps & Reactor Bldg Cooling Fans Exhibiting Early time-out.Significant Disagreement Exists Between Util & Vendor Over Testing Requirements ML20118B2191992-09-23023 September 1992 Suppl to Part 21 Rept Re Potential Deviation in Some Bailey Controls Co 88 Series Modules,Transmitted Via .One Module Found Incapable of Reaching 100% Output at Max Rated Load.Recommends That Circuit Board Assemblies Be Inspected ML20079G5601991-09-16016 September 1991 Part 21 Rept Re Mismatch in Heat Duty Between Air Cooler HX & Jacket Water Hx,Discovered During Review of Generic Ltr 89-13.Initially Reported on 910913.Results of Analysis of Six Different non-design Scenarios Submitted ML20077A4041991-04-29029 April 1991 Deficiency Rept Re Possible Mfg Problems W/Certain Coils Used on Asco Nuclear Qualified Valves.Problems Discussed in NRC Info Notice 86-057.All Purchasers Will Be Notified & Replacement Product Will Be Offered If Item Still in Svc L-91-002, Supplemental Part 21 Rept Re GE Reactor Trip Breakers Used in safety-grade Equipment.Initially Reported on 901228.List of Plants Supplied w/C-E Breakers Encl1991-01-0404 January 1991 Supplemental Part 21 Rept Re GE Reactor Trip Breakers Used in safety-grade Equipment.Initially Reported on 901228.List of Plants Supplied w/C-E Breakers Encl ML20012C1051990-03-0707 March 1990 Part 21 Rept Re Several Failures of Fairbanks Morse Engine Div Piston Pins/Bushings on Upper Pistons.Caused by Incorrect Surface Pattern on Piston Pins.Piston Pins Under Listed Purchase Orders to Be Removed & Replaced NRC-89-3462, Part 21 Rept Re Potential of Ambient Compensated Molded Case Circuit Breakers to Deviate from Published Info. Instantaneous Trip Check Will Be Instituted on All Class 1E Thermal/Magnetic Ambient Breakers Prior to Shipment1989-10-0909 October 1989 Part 21 Rept Re Potential of Ambient Compensated Molded Case Circuit Breakers to Deviate from Published Info. Instantaneous Trip Check Will Be Instituted on All Class 1E Thermal/Magnetic Ambient Breakers Prior to Shipment ML20205F3211988-10-10010 October 1988 Part 21 Rept Re Potential Deviation from Tech Spec Concerning Ry Indicators Due to Operating Temp Effect on Analog Meter Movement.Initially Reported on 881006.Customers Verbally Notified on 881006-07 LD-87-060, Supplemental Part 21 & Deficiency Rept Re Potential Degradation in C-E Pressurizer Heater Sheaths Furnished by Watlow Electric Mfg Co.Initially Reported on 870511.Wetted or Swelled Magnesium Oxide Sleeve Could Cause Fracture1987-10-30030 October 1987 Supplemental Part 21 & Deficiency Rept Re Potential Degradation in C-E Pressurizer Heater Sheaths Furnished by Watlow Electric Mfg Co.Initially Reported on 870511.Wetted or Swelled Magnesium Oxide Sleeve Could Cause Fracture ML20213G8591987-05-11011 May 1987 Part 21 Rept Re Degradation in Pressurizer Heater Sheaths Fabricated from Unannealed Inconel 600.Initially Reported on 870506.Unannealed Watlow Heaters Will Be Replaced Prior to Startup ML20211P7211987-02-23023 February 1987 Part 21 Rept Re Rockbestos Coaxial Cable Used in Sorrento Electronics Digital & Analog high-range Radiation Monitor. Insulation Resistance at High Temp Not High Enough for Ion Chamber & Associated Electronics to Operate Properly 0CAN078605, Part 21 Rept Re Deviation from Purchase Order Specifying Environ Qualification for Limitorque-supplied Buchanan 724 Terminal Strips.Initially Reported on 860712.All Strips Returned.Limitorque Operators Under Continuing Review1986-07-16016 July 1986 Part 21 Rept Re Deviation from Purchase Order Specifying Environ Qualification for Limitorque-supplied Buchanan 724 Terminal Strips.Initially Reported on 860712.All Strips Returned.Limitorque Operators Under Continuing Review ML20206S0841986-06-30030 June 1986 Part 21 Rept Re Possible Cut Wires in Wire Harness of Bbc Brown Boveri K600/K800 Circuit Breakers.Initially Reported on 860509.Safety Implications Listed.Gear Guard Designed to Prevent Cut Wires ML20195D2171986-05-27027 May 1986 Rev 1 to Part 21 Rept Re Dowel Displacement on Connecting Rod Bearings Purchased During Nov 1985 - Apr 1986.Initially Reported on 860421.Rod Bearings Will Be Inspected Dimensionally.Further Info Forthcoming ML20153D8861986-02-17017 February 1986 Part 21 Rept Re Failure of Penetration & Conduit Seal Configurations During Fire Tests.Initially Reported on 860214.Evaluation of Number & Location of Defective Seals in Progress.Nrc Assistance Requested ML20140A5281985-12-19019 December 1985 Part 21 Rept Forwarding Ltr Sent to Customers Re Check Valves Missing Lock Welds on Hinge Supports or Hinge Support Capscrews,Per 851121 Request.List of Customers Receiving Ltr Also Encl ML20134Q1741985-08-29029 August 1985 Part 21 Rept Re Potential Maint Issues Associated w/Anker-Holth Snubbers.Owners of Anker-Holth Snubbers Will Be Informed of Problems & Sent Revs to Technical Instruction Manuals to Include Procedures for Seal & Fluid Maint ML20125B1611985-06-0606 June 1985 Supplemental Part 21 Rept Re Addl Circuit Breakers,Furnished as Spares,W/Overcurrent Trip Devices That May Have Short Time Delay Band Lever.Items Require Insp & Replacement If Link Found Incorrect ML20126C6901985-06-0505 June 1985 Part 21 Rept Re Generator Failure.Concurs W/Encl Louis Allis That Interpolar Connectors Be Removed ML20024D2961983-07-29029 July 1983 Part 21 Rept Re Small Break Operating Guidelines Not Considering Overcooling Transients Caused by Disregarding Extent or Rate of Cooldown.Instructions Sent to Affected Plants Explaining Potential Misuse of Guidelines ML20010F7911981-08-27027 August 1981 Part 21 Rept Re Effects of Spurious Opening of Turbine Bypass Sys Valves on Nuclear Supply Sys.Potential Single Active Failure Could Result in Possibility of Exceeding DNBR Limits ML19330B9911980-07-18018 July 1980 Supplementary Part 21 Rept Re Possibility That Replacement of Buffer Card PN6624610 for Both Power Trains in Bailey Control Co Buffer Module 824 May Result in Loss of 24 Volt Control Power & safety-related Instrumentation 1998-09-28
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217L8931999-10-31031 October 1999 Rev 1 to BAW-10235, Mgt Program for Volumetric Outer Diameter Intergranular Attack in Tubesheets of Once-Through Sgs 05000313/LER-1999-313, :on 990911,AI of EFWS Occurred During Plant Shutdown as Result of Securing Running RCPs Due to Reverse Rotation of Idle Pump.Caused by Failure of Motor anti-rotation Device.Device Was Replaced.With1999-10-11011 October 1999
- on 990911,AI of EFWS Occurred During Plant Shutdown as Result of Securing Running RCPs Due to Reverse Rotation of Idle Pump.Caused by Failure of Motor anti-rotation Device.Device Was Replaced.With
ML20217B6261999-10-0404 October 1999 Safety Evaluation Supporting Amend 202 to License DPR-51 ML20212L1141999-10-0101 October 1999 Safety Evaluation Granting Request for Exemption from Technical Requirements of 10CFR50,App R,Section III.G.2.c 05000368/LER-1999-005-02, :on 990831,two Trip Functions of One Core Protection Calculator Channel Potentially Inoperable Longer than TS Allow Was Discovered.Caused by Resistance Fluctuations.Util Plans to Replace Switch.With1999-09-30030 September 1999
- on 990831,two Trip Functions of One Core Protection Calculator Channel Potentially Inoperable Longer than TS Allow Was Discovered.Caused by Resistance Fluctuations.Util Plans to Replace Switch.With
0CAN109902, Monthly Operating Repts for Sept 1999 for Arkansas Nuclear One,Units 1 & 2.With1999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Arkansas Nuclear One,Units 1 & 2.With ML20216J6271999-09-27027 September 1999 Rev 0 to CALC-98-R-1020-04, ANO-1 Cycle 16 Colr ML20212F5261999-09-22022 September 1999 SER Approving Request Reliefs 1-98-001 & 1-98-200,parts 1,2 & 3 for Second 10-year ISI Interval at Arkansas Nuclear One, Unit 1 ML20212D5611999-09-14014 September 1999 Safety Evaluation Supporting Amend 200 to License DPR-51 ML20212D4091999-09-14014 September 1999 Safety Evaluation Supporting Amend 201 to License DPR-51 ML20211P9551999-09-0909 September 1999 Safety Evaluation Supporting Amend 199 to License DPR-51 0CAN099907, Monthly Operating Repts for Aug 1999 for Ano,Units 1 & 2. with1999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Ano,Units 1 & 2. with ML20211K3311999-08-26026 August 1999 Safety Evaluation Supporting Amends 198 & 209 to Licenses DPR-51 & NPF-06,respectively ML20211F4281999-08-25025 August 1999 Safety Evaluation Concluding That Licensee Provided Acceptable Alternative to Requirements of ASME Code Section XI & That Authorization of Proposed Alternative Would Provide Acceptable Level of Quality & Safety 05000313/LER-1999-002-04, :on 990706,TS Allowable Outage Time for One EDG Was Exceeded Due to Idler Gear Stub Shaft Bracket Bolting Failure.Caused by Loss of Bolt pre-load.Installed New Modified Idler Stub Shaft Assembly.With1999-08-0505 August 1999
- on 990706,TS Allowable Outage Time for One EDG Was Exceeded Due to Idler Gear Stub Shaft Bracket Bolting Failure.Caused by Loss of Bolt pre-load.Installed New Modified Idler Stub Shaft Assembly.With
0CAN089904, Monthly Operating Repts for July 1999 for Ano,Units 1 & 2. with1999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Ano,Units 1 & 2. with ML20210K8831999-07-29029 July 1999 Non-proprietary Addendum B to BAW-2346P,Rev 0 Re ANO-1 Specific MSLB Leak Rates 0CAN079903, Monthly Operating Repts for June 1999 for Ano,Units 1 & 2. with1999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Ano,Units 1 & 2. with ML20196J2771999-06-29029 June 1999 Safety Evaluation Supporting Amend 208 to License NPF-6 05000313/LER-1999-001-04, :on 990521,automatic Actuation of CREVS Occurred Due to Higher than Normal Radiation at Detector When Radioactive Filter Was Moved in Adjacent Area.Training Has Been Provided to Personnel.With1999-06-21021 June 1999
- on 990521,automatic Actuation of CREVS Occurred Due to Higher than Normal Radiation at Detector When Radioactive Filter Was Moved in Adjacent Area.Training Has Been Provided to Personnel.With
ML20195G9531999-06-10010 June 1999 Safety Evaluation Supporting Amend 197 to License DPR-51 ML20207G2901999-06-0707 June 1999 Safety Evaluation Supporting Amend 207 to License NPF-6 ML20207E7231999-06-0202 June 1999 Safety Evaluation Authorizing Proposed Alternative Exam Methods Proposed in Alternative Exam 99-0-002 to Perform General Visual Exam of Accessible Areas & Detailed Visual Exam of Areas Determined to Be Suspect ML20196A6251999-05-31031 May 1999 Non-proprietary Rev 0 to TR BAW-10235, Mgt Program for Volumetric Outer Diameter Intergranular Attack in Tubesheets of Once-Through Sgs ML20196A0191999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Arkansas Nuclear One,Units 1 & 2.With ML20195D1991999-05-28028 May 1999 Probabilistic Operational Assessment of ANO-2 SG Tubing for Cycle 14 ML20207B7071999-05-19019 May 1999 Safety Evaluation Supporting Amends 196 & 206 to Licenses DPR-51 & NPF-6,respectively ML20207A4651999-05-19019 May 1999 Safety Evaluation Supporting Amend 205 to License NPF-6 05000368/LER-1999-004-01, :on 990414,noted That Two Trip Functions of One Core Protection Calculator Channel Were Potentially Inoperable.Caused by Excore Detector Drift.Affected Trip Functions Have Remained Bypassed or Tripped.With1999-05-12012 May 1999
- on 990414,noted That Two Trip Functions of One Core Protection Calculator Channel Were Potentially Inoperable.Caused by Excore Detector Drift.Affected Trip Functions Have Remained Bypassed or Tripped.With
ML20206M7711999-05-11011 May 1999 SER Accepting Relief Request from ASME Code Section XI Requirements for Plant,Units 1 & 2 0CAN059903, Monthly Operating Repts for Apr 1999 for Ano,Units 1 & 2. with1999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Ano,Units 1 & 2. with ML20206F0691999-04-29029 April 1999 Safety Evaluation Accepting Licensee Re ISI Plan for Third 10-year Interval & Associated Requests for Alternatives for Plant,Unit 1 ML20205Q7721999-04-16016 April 1999 Safety Evaluation Supporting Amends 195 & 203 to Licenses DPR-51 & NPF-6,respectively ML20205M6941999-04-12012 April 1999 Safety Evaluation Granting Relief for Second 10-yr Inservice Inspection Interval for Plant,Unit 1 ML20205D6061999-03-31031 March 1999 Safety Evaluation Supporting Licensee Proposed Approach Acceptable to Perform Future Structural Integrity & Operability Assessments of Carbon Steel ML20205R6351999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Ano,Units 1 & 2. with ML20205D4711999-03-26026 March 1999 SER Accepting Util Proposed Alternative to Employ Alternative Welding Matls of Code Cases 2142-1 & 2143-1 for Reactor Coolant System to Facilitate Replacement of Steam Generators at Arkansas Nuclear One,Unit 2 05000368/LER-1999-003, :on 990224,noted That One Excore Nuclear Instrumentation Channel Was Inoperable Longer than Allowed by Ts.Caused by Detector Failure.Proposed Exigent TS Change Was Submitted to Allow Operation.With1999-03-23023 March 1999
- on 990224,noted That One Excore Nuclear Instrumentation Channel Was Inoperable Longer than Allowed by Ts.Caused by Detector Failure.Proposed Exigent TS Change Was Submitted to Allow Operation.With
ML20204H7451999-03-23023 March 1999 Safety Evaluation Supporting Amend 202 to License NPF-6 ML20204B1861999-03-15015 March 1999 Safety Evaluation Authorizing Licensee Request for Alternative to Augmented Exam of Certain Reactor Vessel Shell Welds,Per Provisions of 10CFR50.55a(g)(6)(ii)(A)(5) 05000368/LER-1999-001, :on 990108,TS Requirements for as-lift Settings of MSSV Were Not Met.Caused by Errors in Determination of Effective Seating Area by Vendor During Test Device Qualification.Replaced All Mssvs.With1999-03-0909 March 1999
- on 990108,TS Requirements for as-lift Settings of MSSV Were Not Met.Caused by Errors in Determination of Effective Seating Area by Vendor During Test Device Qualification.Replaced All Mssvs.With
05000368/LER-1999-002-01, :on 990202,noted Failure to Verify Station Battery cell-to-cell & Terminal Tightness.Caused by Inadvertent Omission of Requirements During Procedure Revs. Svc Test Procedures Were Revised.With1999-03-0404 March 1999
- on 990202,noted Failure to Verify Station Battery cell-to-cell & Terminal Tightness.Caused by Inadvertent Omission of Requirements During Procedure Revs. Svc Test Procedures Were Revised.With
0CAN039904, Monthly Operating Repts for Feb 1999 for Ano,Units 1 & 2. with1999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Ano,Units 1 & 2. with ML20212G6381999-02-25025 February 1999 Ano,Unit 2 10CFR50.59 Rept for 980411-990225 ML20203E4891999-02-11011 February 1999 Rev 1 to 97-R-2018-03, ANO-2,COLR for Cycle 14 05000368/LER-1999-001-01, :on 990108,four Main Steam Safety Valves as- Found Lift Values Failed to Meet TS Requirements.Cause of Evaluation in progress.Short-term & long-term Corrective Actions Will Be Described in Suppl to Rept.With1999-01-28028 January 1999
- on 990108,four Main Steam Safety Valves as- Found Lift Values Failed to Meet TS Requirements.Cause of Evaluation in progress.Short-term & long-term Corrective Actions Will Be Described in Suppl to Rept.With
ML20202B4581999-01-26026 January 1999 Safety Evaluation Supporting Amend 200 to License NPF-6 05000313/LER-1998-005-03, :on 981225,two Manual RTs & Manual Actuations of EFWS Due to Reduced Cw Flow to Mc.Caused by Large Intrusions of Fish Exceeding Removal Capability of Traveling Screen.Increased Fish Removal Capability.With1999-01-21021 January 1999
- on 981225,two Manual RTs & Manual Actuations of EFWS Due to Reduced Cw Flow to Mc.Caused by Large Intrusions of Fish Exceeding Removal Capability of Traveling Screen.Increased Fish Removal Capability.With
ML20199F7931999-01-19019 January 1999 Safety Evaluation Supporting Amend 199 to License NPF-6 05000368/LER-1998-008-01, :on 981215,one CR Emergency Chiller,Part of CREVS Discovered to Be Inoperable,While Chiller in Other Train Was Out of Svc for Planned Maint.Caused by Equipment Failure.Operations Personnel Verified.With1999-01-14014 January 1999
- on 981215,one CR Emergency Chiller,Part of CREVS Discovered to Be Inoperable,While Chiller in Other Train Was Out of Svc for Planned Maint.Caused by Equipment Failure.Operations Personnel Verified.With
1999-09-09
[Table view] |
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r A A K A N S A S P O W E A G L I G H T 'C O M P A N Y STH & LOUISIANA STAEETS. LITTLE AOCK. A AK ANS AS 73203.(5013372 4311 May 5, 1975 THIS DOCUMENT CONTAINS.
POOR QUAUTY PAGES Mr. E. Morris Howard, Director Office of Inspection and Enforcement Re'gion IV, Suite 1000 611 Ryan Pla::a Drive Arlington, Texas 76012 Subj ect: Arkansas Power G Light Company Arkansas Nuclear One-Unit 2 Docket No. 50-368 NRC Control No. H00710F4 Significant Deficiency Report Spent Fuel Pool Walls
Dear Mr. Howard:
On February 7,1975, we submitted an interim report for tlk subject deficiency reported on January 9, 1975. Attached is our final report for the subject deficiency.providing a description of the deficiency, analysis of the radiation safety implications and correctiu actions taken.
Very truly yours, i,
fl,l }.3/ ' ;l
,' A ^ f ju !
J. D. Phillips /
Senior Vice Pres 1* nt JDP:lt Attachment cc:
Mr. Donald K. Knuth, Director -
Office of Inspection and Enforcement U. S. Nuclear Regulatory Commission Washington, D. C.
20555 8004280 l
3k, MEMBE A MICOLE SOUTH UTIUTIES SYSTEM T A x P AYING. INVESTC A OWNEC
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4 STATE OF ARKANSAS
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SS COUhTY OF PULASKI
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J. D. Phillips, being duly sworn, states that 'he is a Senior Vice President of Arkansas Power G Light company; that he is authorized on the part of said Company to sign and file with the Nuclear Regulatory Commission this Supplementary Information; that he has read all of the statements made and matters set forth therein are true and correct to the best of his knowledge, information and belief.
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J. D. Phillips' SUBSCRIBED AND SWORN K before me, a Notary Public in and for the County and State above named this d day of. hw
, 197S.
O R n-h. 3 % -
Notary Public My Commission Expires:
March 1, 197s e
C I
FINAL REPORT SPENT FUEL POOL DESIGN This report covers,the design deficiency reported for the Arkansas Nuclear One-Unit 2 Spent Fuel Pool Walls.
The report also covers the safety implications had the deficiency gone undetected as well as a description of the structural analysis and the reinforcement method to be employed.
1)
Description of Deficiency The horizontal reinforcing steel on the inside face of the spent fuel pool and the tilt pit is not properly detailed so as to develop the bars at points of high stress.
This occurs at the junction of cast-west wall with north-south wall.
The horizontal reinforcing steci in these walls is bent to form a 90 degree bend on the inside face of the pool rather.than extending through the wall to the outer face reinforcement to provide proper embedment length to develop the bars.
2)
Analysis of the Radiation Safety Implications In analyzing the safety implications of a postulated failure of the wall separating the spent fuel pool from the fuel tilt pit, the tilt pit was _ assumed to be conpletely dry prior to the failure.
o dd i -i- -
ally, it was conservatively assumed that the spent fuel racks are completely full, with 1/3 core loadings from five subsequent refuel-ings and 1 complete core which had decayed for only 7 days since reactor shutdown.
Following the postulated failure of the wall, the water levels in the tilt pit and the spent fuel pool would equalize, resulting in a decrease 1
of the. total height of water above the top of the active fuel from 26 feet to 19 feet. The resulting increase in the radiation dose rates the operating deck near the edge of the pool would be insignificant.
at Since the normal pool level was selected to ensure that dose rates at the pool surface do not exceed 5 mrem /hr during refueling operations, the doses resulting from the wall failure would be less than the doses encountered when transferring spent fuel from the reactor vessel to the spent fuel racks.
The, decrease in the pool level, however, would result in the loss of suction to the fuel pool cooling pumps and, consequently, the loss of the normal fuel pool cooling system.
The fuci pool pumps would trip on low discharge pressure.
Alarms in the Control Room would alert the Control Room Supervisor of the low pool level and the tripping of the cooling pumps.
A valve line-up to supply makeup water to the pool would be promptly initiated. Makeup to the pool would be provided from the Refueling Water Tank via the fuel pool purification pump at the rate of approximately 150 gpm.
With this makeup rate pool level would be increased at the rate of approximately 1.3 ft/hr.
Approximately 3.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> after loss of normal cooling, the water in. the pool would begin to boil.
The boiloff rate would be approximately 62 gpm.
hhen' this occurs, the rate of level increase in the pool as a result of adding makeup water at 150 gpm would decrease to approximately 0.54 ft/hr.
Since the spent fuci pool racks are designed to provide sufficient thermal circulation to prevent the fuel cladding from being damaged when boiling conditions exist in the pool, no significant release of fission products from the spent fuel to the atmosphere would occur as a result of the postulated wall failure.
D e spent fuel pool would be restored to its normal water level and normal cooling re-established within approximately 8.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> after the wall failure.
In conclusion, it has been determined that the postulated failure of this wall does not represent any hazard to the health and safety of the general public or to any plant operating personnel.
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- 3) Corrective Action Taken hhen the deficiency became known, a check of the structural design calculations was made to verify the design basis.
The original design was based on a fixed condition at the inters'ection of the walls as well as at the base, slab.
Due to the manner in which the reinforcing was detailed, the critical wall intersection conditions changed from the fixed design condition to a hinged condition while the condition at the base slab remained as designed.
lhe spent fuel pool was reanaly:ed using two separate computer programs.
The wall separating the fuel pool and tilt pit was first analyzed with three-dimensional brick elements using CDC computer program 3D/ SAP, general structural analysis program.
Three separate end conditions were used in this analysis. The first considered both vertical edges of the wall hinged with full hydrostatic load. The second considered that just the upper 10 feet of the separation wall was fixed with full hydrostatic load.
The third considered bcth edges hinged and supported by a strut just to the east of the gate opening with full hydrostatic load.
The first two analyses resulted in high transverse shear stresses around the bottom of the fuel pool gate opening and at the intersection with the west wall'of the fuel pool. The third analysis indicated that depending on the stiffness of the strut, the transverse shear stress could be controlled so as to be within the ACI code allowabic Values.
Since the strut will not: interfere with the operating of ' he fuel t
handling equipment and offers the least amount of rework to the exist-ing structure, it was decided that the strut reinforcement was pre-ferable to modifying the intersections to develop full fixity at the wall intersections in order to being the transverse shear within -
allowable values.
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SRI /STARDYNE finite element computer program, which is traceabic to the Control Data Corporation, was then used to model the whole fuel pool to analyze the hydrostatic effect on all other corners as well as to confirm the results of 3D/ SAP..In this case, the plate bending elements were used for the static analysis.
The whole fuel pool was moleled as a three-dimensional struct' ural system,,
with the floor. slabs around the pools modeled as horizontal rigid beam elements.
The thermal aff.cct was calculated by hand and it was determined that the thermal stresses in the walls were not affected significantly by the ' hinged boundary conditions at the wall intersections.
Again, three cases were. considered.
The first was with full hydrostatic load in the spent fuel pool, tilt. pit and cask pit without the strut.
The second was with full hydrostatic load in the spent fuel pool with the strut across the tilt pit supporting the separation wall.
The third run was without any hydrostatic load, but with a precompressed strut.
1 The first run confirmed a hand analysis of the transverse shear stress in the outer corners of the spent fuel pool, tilt pit and cask pit in which these stresses are within the allowable values given in the ACI code for a member without shear reinformement. Consequently, no additional rein-forcement is required in these areas.
The second run con [irmed the results ot 30/ SAP as regards the effect of the strut on the separation wall.
The third run was used to determine the effect of the stiffness of the strut on the separation wall.
From 3D/ SAP it was determined that the stiffness of the strut would have to be large enough so as to keep the shear stresses in the separation wall below the allowable values given by the ACI cod'c for members without shear reinforce-ment for the condition when the spent fuel pool is full and the. tilt pit is empty.
On the other hand, from the results of the third run of the STARDYNE program, it.was determined that the strut should be so designed that it is strong enough to support the separation wall during the opera-tion stage but not so stiff as to impose a significant thermal load into the separation wall. causing excessive transverse shear for the case when the pool and tilt pit have the full hydrostatic load plus the maximum thermal load due to the accident case.
Since it is extremely difficult to _ satisfy these two adverse conditions, if not impossible, a compromise solution has been adopted.
The stiffness of the strut was determined so as to provide a shear stress in the separa-tion wall which would be within the allowable value given by the ACI code for members with shear rcinforcement for.the case of the spent fuel pool
..with hydrostatic load and the tilt pit empty.
The required shear rein -
~forcement will be provided in the existing separation wall by drilling
-holes through the wall and grouting in bolts.
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Althougli-the analysis indicates that a. single strut is. sufficient rein-forcement-an additional strut aligning with the west wall of the spent fuel pool is included.in the reinforcement modifications since it is difficult if not impossible to predict the diagonal crack pattern in
. this areai*
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