ML19208A102

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LER 79-068/03L-0:on 790812,emergency Feedwater Flow Control Valve 2CV-1025-1 from Pump 2P7B to Steam Generator a Failed to Fully Close from Control Room Demand Signal.Caused by Nonalignment of Limit Stop Switch.Switch Realigned
ML19208A102
Person / Time
Site: Arkansas Nuclear Entergy icon.png
Issue date: 09/05/1979
From: Shively C
ARKANSAS POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19208A101 List:
References
LER-79-068-03L, LER-79-68-3L, NUDOCS 7909120566
Download: ML19208A102 (1)


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NRC F ORM 366 V $ NUCLE AR F'E GUL ATORY COMMISSION (7 77)

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a I 1. from tha electric driven EFW oumo 2P7B. to the "A" steam generator, I o 4 Ifailed to fully close from a Control Room demand signal. The redundant t r s LEFW valves were successfully stroked from the Control Room. This occur  ;

c c Ironce is similar to LER 50-368/79 051.79-043. 79-035, and 78-28. r o 7 IReportable per T.S.6.9.1.9b.  ;

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i ' o LInvestigation revealed that the limit stop switch was out of alignment, ,

i, j i l ! Realianment was made and the valve was successfully stroke tested. The ,

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