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| 05000280/LER-1975-001, Submittal of Abnormal Occurrence Report No. AO-S2-75-01, the Flooding of the Valve Pit Containing Service Water Valves MOV-SW-203A, B, C, D | Submittal of Abnormal Occurrence Report No. AO-S2-75-01, the Flooding of the Valve Pit Containing Service Water Valves MOV-SW-203A, B, C, D | |
| 05000280/LER-1975-001-03, /03L:on 750218,pump 1-SW-P-6 Supplying Radiation Monitor RM-SW-107 Failed.Caused by Erosion.Sampling Initiated Until Design Mod Installed | /03L:on 750218,pump 1-SW-P-6 Supplying Radiation Monitor RM-SW-107 Failed.Caused by Erosion.Sampling Initiated Until Design Mod Installed | |
| 05000280/LER-1975-002, Submittal of 40 Copies of Report No. AO-S1-75-02, Abnormal Occurrence Report, Station Instrument Air Supply to Containment Instrument Air System | Submittal of 40 Copies of Report No. AO-S1-75-02, Abnormal Occurrence Report, Station Instrument Air Supply to Containment Instrument Air System | |
| 05000280/LER-1975-003, Process Vents Gaseous Waste Release | Process Vents Gaseous Waste Release | |
| 05000281/LER-1975-003-01, /01T:on 750131,steam Generator C Narrow Range Level Channel 2 Indication Found Drifted 65%.Caused by Magnetic Sludge Deposits in Sensing Lines.Channel Placed in Trip Mode & Detector Sensing Lines Blown Down | /01T:on 750131,steam Generator C Narrow Range Level Channel 2 Indication Found Drifted 65%.Caused by Magnetic Sludge Deposits in Sensing Lines.Channel Placed in Trip Mode & Detector Sensing Lines Blown Down | |
| 05000281/LER-1975-004-01, /01T:on 750214,steam Generator C Narrow Range Level Channel 1 Indication Found Drifted High.Caused by Leaking Condensate Pot Isolation Valve Preventing Pot from Maintaining Proper Water Level | /01T:on 750214,steam Generator C Narrow Range Level Channel 1 Indication Found Drifted High.Caused by Leaking Condensate Pot Isolation Valve Preventing Pot from Maintaining Proper Water Level | |
| 05000280/LER-1975-004-01, /01T:on 750131,steam Generator C Narrow Range Level Channel 2 Indication Found Drifted 65%.Caused by Magnetic Sludge Deposits in Sensing Lines.Channel Placed in Trip Mode & Lines Blown Down | /01T:on 750131,steam Generator C Narrow Range Level Channel 2 Indication Found Drifted 65%.Caused by Magnetic Sludge Deposits in Sensing Lines.Channel Placed in Trip Mode & Lines Blown Down | |
| 05000281/LER-1975-005-01, /01T:on 750217,quadrant Tilt of Up to Max of 2.5% Existed for Greater than 2 H W/O Power Reduction.Caused by Card Failure.Actual Tilt Caused by Dropped Rod | /01T:on 750217,quadrant Tilt of Up to Max of 2.5% Existed for Greater than 2 H W/O Power Reduction.Caused by Card Failure.Actual Tilt Caused by Dropped Rod | |
| 05000280/LER-1975-005-01, /01T:on 750214,pressurizer Pressure Comparator Found Out of Calibr.Caused by Component Failure of Hagan Computer Sys Model 118 Signal Comparator A56Y 4111082-001. Comparator Replaced | /01T:on 750214,pressurizer Pressure Comparator Found Out of Calibr.Caused by Component Failure of Hagan Computer Sys Model 118 Signal Comparator A56Y 4111082-001. Comparator Replaced | |
| 05000281/LER-1975-005, Updated LER 75-05/010:on 750225,radial Trip of Max 2.5% Existed.Caused by Prolonged Recovery of Rod F-2.Control Room Alarm Did Not Function Due to Defective Circuit Card. Card Replaced & Staff Cautioned | Updated LER 75-05/010:on 750225,radial Trip of Max 2.5% Existed.Caused by Prolonged Recovery of Rod F-2.Control Room Alarm Did Not Function Due to Defective Circuit Card. Card Replaced & Staff Cautioned | |
| 05000280/LER-1975-006-01, /01T:on 750215 & 19,channel 1 Overpower Setpoint Failed High.Caused Under Investigation.Low Level Amplifier TM-1-412A Replaced & Instrument Calibr Performed | /01T:on 750215 & 19,channel 1 Overpower Setpoint Failed High.Caused Under Investigation.Low Level Amplifier TM-1-412A Replaced & Instrument Calibr Performed | |
| 05000280/LER-1975-006, Supplemental LER 75-06/010:on 750215,module S/N D401 Failed Due to Capacitor C-37 Being Open Circuit.Capacitors Replaced | Supplemental LER 75-06/010:on 750215,module S/N D401 Failed Due to Capacitor C-37 Being Open Circuit.Capacitors Replaced | |
| 05000281/LER-1975-006-01, /01T:on 750427,consequence Limiting Safeguard high-high Train B Would Not Initiate When 3/4 Matrix of Channels 1,2 & 3 Tripped.Cause Unknown.Relay R-LM100C2 Replaced | /01T:on 750427,consequence Limiting Safeguard high-high Train B Would Not Initiate When 3/4 Matrix of Channels 1,2 & 3 Tripped.Cause Unknown.Relay R-LM100C2 Replaced | |
| 05000281/LER-1975-007-01, /01T:on 750427,motor Operator to Valve MOV-CW-206D Failed to Operate.Caused by Mounting Screw of Torque Switch Not Fully Seated.Mounting Screw & Lock Washer Fully Set | /01T:on 750427,motor Operator to Valve MOV-CW-206D Failed to Operate.Caused by Mounting Screw of Torque Switch Not Fully Seated.Mounting Screw & Lock Washer Fully Set | |
| 05000280/LER-1975-007, Submittal of Abnormal Occurrence Report No. AO-S1-75-07, an Uncontrolled and Unplanned Release of Low Level Radioactive Material Was Made to the Discharge Canal | Submittal of Abnormal Occurrence Report No. AO-S1-75-07, an Uncontrolled and Unplanned Release of Low Level Radioactive Material Was Made to the Discharge Canal | |
| 05000280/LER-1975-007-01, /01T:on 750313,uncontrolled & Unplanned Release of Low Level Radioactive Matl Made to Discharge Canal.Caused by Personnel Oversight.Operators Reinstructed on Maintaining Proper Control & Documentation | /01T:on 750313,uncontrolled & Unplanned Release of Low Level Radioactive Matl Made to Discharge Canal.Caused by Personnel Oversight.Operators Reinstructed on Maintaining Proper Control & Documentation | |
| 05000281/LER-1975-008-01, /01T:on 750427,accumulator Discharge Valve MOV-2865C Did Not Receive Signal to Open Upon Safety Injection Initiation.Caused by Disconnected Lead Blocking Signal | /01T:on 750427,accumulator Discharge Valve MOV-2865C Did Not Receive Signal to Open Upon Safety Injection Initiation.Caused by Disconnected Lead Blocking Signal | |
| 05000280/LER-1975-008-01, /01T:on 750402,nuclear Axial Offset Out of Target Band 5% for 1 1/2 H During Startup.Caused by Personnel Error & Inadequate Procedure.Procedure Revised | /01T:on 750402,nuclear Axial Offset Out of Target Band 5% for 1 1/2 H During Startup.Caused by Personnel Error & Inadequate Procedure.Procedure Revised | |
| 05000280/LER-1975-008, Supplementary LER 75-08/01L on 750427.Previously Described Event Caused by Apparent Inadequate Implementation of Administrative Controls During Const & Preoperation. Administrative Control of Electrical Wire Changes Increased | Supplementary LER 75-08/01L on 750427.Previously Described Event Caused by Apparent Inadequate Implementation of Administrative Controls During Const & Preoperation. Administrative Control of Electrical Wire Changes Increased | |
| 05000280/LER-1975-009, Submittal of Abnormal Occurrence Report No. AO-S1-75-09, During Normal Operation the Process Vent Gaseous Radiation Monitor Was Found in the Calibrate Mode | Submittal of Abnormal Occurrence Report No. AO-S1-75-09, During Normal Operation the Process Vent Gaseous Radiation Monitor Was Found in the Calibrate Mode | |
| 05000281/LER-1975-009-01, /01L:on 750613,above Ground Emergency Condensate Storage Tank Discovered W/Less than Required 60,000 Gallons of Water.Caused by Inconsistencies in Operating Procedure 31.2.Tank Filled | /01L:on 750613,above Ground Emergency Condensate Storage Tank Discovered W/Less than Required 60,000 Gallons of Water.Caused by Inconsistencies in Operating Procedure 31.2.Tank Filled | |
| 05000280/LER-1975-009-01, /01T:on 750412,process Vent Gaseous Radiation Monitor Found in Calibr Mode Resulting in Failure to Monitor Process Vent Sys.Caused by Operator Error.Personnel Instructed on Seriousness of Situation | /01T:on 750412,process Vent Gaseous Radiation Monitor Found in Calibr Mode Resulting in Failure to Monitor Process Vent Sys.Caused by Operator Error.Personnel Instructed on Seriousness of Situation | |
| 05000281/LER-1975-010-01, /01T:on 750624,svc Water Pump 2-SW-P-4B Developed Seal Leak.Caused by Electrical Short in Motor Operator.Pump Leak & Motor Operator Repaired | /01T:on 750624,svc Water Pump 2-SW-P-4B Developed Seal Leak.Caused by Electrical Short in Motor Operator.Pump Leak & Motor Operator Repaired | |
| 05000280/LER-1975-010-01, /01T:on 750412,valve FCV-GW-260 Failed to Shut as Required by Tech Specs.Caused by Westinghouse Model MG-6 Relay in Control Circuit for Valve Found Stuck in Operate Position.Relay Cleaned & Adjusted | /01T:on 750412,valve FCV-GW-260 Failed to Shut as Required by Tech Specs.Caused by Westinghouse Model MG-6 Relay in Control Circuit for Valve Found Stuck in Operate Position.Relay Cleaned & Adjusted | |
| 05000280/LER-1975-011, Suppl to LER 75-11/01T:on 750416,pinhole Leak Developed in Recirculation Line on Charging Pump 2-CH-P-1C Causing Ventilation Vent Sampler RMS-VG-109 to Alarm.Leak Found & Isolated | Suppl to LER 75-11/01T:on 750416,pinhole Leak Developed in Recirculation Line on Charging Pump 2-CH-P-1C Causing Ventilation Vent Sampler RMS-VG-109 to Alarm.Leak Found & Isolated | |
| 05000281/LER-1975-011-01, /01T:on 750630,4 Kv Undervoltage Protection Inoperable.Caused by Blown Fuse.Fuses Replaced | /01T:on 750630,4 Kv Undervoltage Protection Inoperable.Caused by Blown Fuse.Fuses Replaced | |
| 05000280/LER-1975-011-01, /01T:on 750416,pinhole Leak Developed in Recirculation Line on Charging Pump 2-CH-P-1C Causing Ventilation Vent Sampler to Alarm.Leak Isolated | /01T:on 750416,pinhole Leak Developed in Recirculation Line on Charging Pump 2-CH-P-1C Causing Ventilation Vent Sampler to Alarm.Leak Isolated | |
| 05000281/LER-1975-012-01, /01T:on 750706:main Steam Line Trip Valve in Steam Line B Closed,Causing Closure of Trip Valves a & C & Reactor Trip.Caused by Faulty Piston O-ring.O-ring Replaced & Air Lines Cleared of Debris | /01T:on 750706:main Steam Line Trip Valve in Steam Line B Closed,Causing Closure of Trip Valves a & C & Reactor Trip.Caused by Faulty Piston O-ring.O-ring Replaced & Air Lines Cleared of Debris | |
| 05000281/LER-1975-012, Suppl to LER 75-12/01T:on 750706,reactor Trip Occurred. Caused by Sudden Closure of Trip Valve in Main Steam Line B Followed by Closure of Main Steam Line Valves a & C | Suppl to LER 75-12/01T:on 750706,reactor Trip Occurred. Caused by Sudden Closure of Trip Valve in Main Steam Line B Followed by Closure of Main Steam Line Valves a & C | |
| 05000280/LER-1975-012-01, /01L:on 750430,emergency Diesel Generator 3 Failed. Caused by Partially Stripped Teeth on Planetary & Spline Shaft Gears.Engine Speed & Loading Verified Sufficient to Disengage Mechanical Drive to turbo-blower | /01L:on 750430,emergency Diesel Generator 3 Failed. Caused by Partially Stripped Teeth on Planetary & Spline Shaft Gears.Engine Speed & Loading Verified Sufficient to Disengage Mechanical Drive to turbo-blower | |
| 05000281/LER-1975-013-01, /01T:on 750720,channel of Change Protection Found Not Conservative.Caused by Failure of Cold Leg Low Level Amplifier.Amplifier Replaced & Channel Calibr | /01T:on 750720,channel of Change Protection Found Not Conservative.Caused by Failure of Cold Leg Low Level Amplifier.Amplifier Replaced & Channel Calibr | |
| 05000280/LER-1975-013-01, /01L:on 750516,chemical Addition Tank Discharge Valve MOV-CS-102B Failed to Function Properly During Periodic Test.Caused by Small Debris in Valve Seat.Valve Reassembled & Tested Satisfactorily | /01L:on 750516,chemical Addition Tank Discharge Valve MOV-CS-102B Failed to Function Properly During Periodic Test.Caused by Small Debris in Valve Seat.Valve Reassembled & Tested Satisfactorily | |
| 05000280/LER-1975-014-01, /01T:on 750801,boron Concentration in Accumulator 1C Approx 1,850 Ppm.Caused by Inleakage Through Loop Check Valve.Primary Sys Pressure Increased to Seat Check Valves. Accumulator Drained | /01T:on 750801,boron Concentration in Accumulator 1C Approx 1,850 Ppm.Caused by Inleakage Through Loop Check Valve.Primary Sys Pressure Increased to Seat Check Valves. Accumulator Drained | |
| 05000280/LER-1975-015, Updated LER 75-15/01T:on 750803,leaking Fitting on Overhead Gas Compressor B Resulted in Unplanned Release of Radioctive Matl from Site.Caused by Loose Fitting.Leaking Fitting Repaired | Updated LER 75-15/01T:on 750803,leaking Fitting on Overhead Gas Compressor B Resulted in Unplanned Release of Radioctive Matl from Site.Caused by Loose Fitting.Leaking Fitting Repaired | |
| 05000280/LER-1975-015-01, /01T:on 750803,leaking Fitting on Overhead Gas Compressor B Resulted in Unplanned Release of Radioactive Matl from Site.Caused by Loose Fitting.Leaking Fitting Repaired | /01T:on 750803,leaking Fitting on Overhead Gas Compressor B Resulted in Unplanned Release of Radioactive Matl from Site.Caused by Loose Fitting.Leaking Fitting Repaired | |
| 05000281/LER-1975-015-01, /01T:on 750807,boron Injection Tank Recirculation Valves TV-2884 A,B & C Found Closed.Caused by Air Supply Valve 2-IA-451 Partially Throttled Due to Vibration | /01T:on 750807,boron Injection Tank Recirculation Valves TV-2884 A,B & C Found Closed.Caused by Air Supply Valve 2-IA-451 Partially Throttled Due to Vibration | |
| 05000280/LER-1975-016-01, /01T:on 750822,Channel II Protection Drifted in Nonconservative Direction.Caused by Incorrect Resistance of Hot Leg Resistance Temp Detector (Rtd).Packing Replaced & RTD Ohmic Characteristic Returned to Normal | /01T:on 750822,Channel II Protection Drifted in Nonconservative Direction.Caused by Incorrect Resistance of Hot Leg Resistance Temp Detector (Rtd).Packing Replaced & RTD Ohmic Characteristic Returned to Normal | |
| 05000281/LER-1975-016-01, /01T:on 750823,low Level Alarm on Boric Acid Tank C Received.Caused by Installation of Carbon Steel Rather than Stainless Steel 304 Flanges & Pipe of Spool Piece.All Improper Installations Will Be Replaced | /01T:on 750823,low Level Alarm on Boric Acid Tank C Received.Caused by Installation of Carbon Steel Rather than Stainless Steel 304 Flanges & Pipe of Spool Piece.All Improper Installations Will Be Replaced | |
| 05000280/LER-1975-016, Updated LER 75-16/010:on 750822 & 23,channel II Protection Drifted in Nonconservative Direction.Caused by Moisture Accumulation Between Senson Insulation & Copper Lead Wire. All RTDs Replaced W/Improved Versions | Updated LER 75-16/010:on 750822 & 23,channel II Protection Drifted in Nonconservative Direction.Caused by Moisture Accumulation Between Senson Insulation & Copper Lead Wire. All RTDs Replaced W/Improved Versions | |
| 05000280/LER-1975-017-01, /01T:on 750915,one Channel of Redundant Heat Tracing Failed.Caused by Breaker Trip on Overload Due to Short Circuit by Svc Water Leak.Leak Secured & Transformer Repaired | /01T:on 750915,one Channel of Redundant Heat Tracing Failed.Caused by Breaker Trip on Overload Due to Short Circuit by Svc Water Leak.Leak Secured & Transformer Repaired | |
| 05000281/LER-1975-017-01, /01T:on 751003,loop C Leg RTD Failed Low,Causing Protection Signals to Fail Low.Caused by Incorrect Ohmic Characteristic of Connected RTD & Spare.Failed Instruments Replaced | /01T:on 751003,loop C Leg RTD Failed Low,Causing Protection Signals to Fail Low.Caused by Incorrect Ohmic Characteristic of Connected RTD & Spare.Failed Instruments Replaced | |
| 05000280/LER-1975-018-01, /01T:on 750924,loop a Instrumentation Drifted Low. Caused by High Moisture Content in Containment Atmosphere. RTD Will Be Repaired or Replaced | /01T:on 750924,loop a Instrumentation Drifted Low. Caused by High Moisture Content in Containment Atmosphere. RTD Will Be Repaired or Replaced | |
| 05000281/LER-1975-018-01, /01T:on 751009,steam Generator Level Transmitter Isolation Valve Body Bonnet Leak Wetted Down RPI Cabling, Causing Grounds & Erratic Indication for 24 Different Rods. Caused by Water Spray | /01T:on 751009,steam Generator Level Transmitter Isolation Valve Body Bonnet Leak Wetted Down RPI Cabling, Causing Grounds & Erratic Indication for 24 Different Rods. Caused by Water Spray | |
| 05000280/LER-1975-019-01, /01T:on 750925,loop B Temperature Change Instrumentation Drifted Low.Caused by Moisture Content of Containment Atmosphere.Spare RTD Placed in Svc & Shutdown Terminated | /01T:on 750925,loop B Temperature Change Instrumentation Drifted Low.Caused by Moisture Content of Containment Atmosphere.Spare RTD Placed in Svc & Shutdown Terminated | |
| 05000281/LER-1975-019-01, /01T:on 751015,boric Acid Transfer Pump D Motor Failed Resulting in Loss of Recircilation of Boron Injection Tank 2.Caused by Boric Acid Present in Stator Windings. Pump B Placed in Svc | /01T:on 751015,boric Acid Transfer Pump D Motor Failed Resulting in Loss of Recircilation of Boron Injection Tank 2.Caused by Boric Acid Present in Stator Windings. Pump B Placed in Svc | |
| 05000281/LER-1975-020-01, /01T:on 751219,steam Generator C Pressure Indication 496 Channel IV Failed High.Caused by Frozen Sensing Line.Louvers Closed & Sealed Allowing Line to Thaw & Transmitter Returned to Normal Svc | /01T:on 751219,steam Generator C Pressure Indication 496 Channel IV Failed High.Caused by Frozen Sensing Line.Louvers Closed & Sealed Allowing Line to Thaw & Transmitter Returned to Normal Svc | |
| 05000281/LER-1975-021-01, /01T:on 751219,channel 3 for Over Temp Indicated 132% While Channels 1 & 2 Indicated 118%.Cause Unknown. Channel Calibr & Returned to Svc | /01T:on 751219,channel 3 for Over Temp Indicated 132% While Channels 1 & 2 Indicated 118%.Cause Unknown. Channel Calibr & Returned to Svc | |
| 05000280/LER-1975-022-01, /01T:on 750927,test of Main Steam Safety Valve Setpoint Indicated Four Valves Not within Plus or Minus 1% of Setpoint.Caused by Setpoint Drift.Valves Adjusted & Retested | /01T:on 750927,test of Main Steam Safety Valve Setpoint Indicated Four Valves Not within Plus or Minus 1% of Setpoint.Caused by Setpoint Drift.Valves Adjusted & Retested | |
| 05000280/LER-1975-023-01, /01T:on 751013,channels P-1-455,P-1-456 & P-1-457 Found Indicating High by 26.4 psi,42.0 Psi & 29.4 Psi, Respectively.Caused by Overranging of Zero Spring in Prior Calibr.Procedure Revised | /01T:on 751013,channels P-1-455,P-1-456 & P-1-457 Found Indicating High by 26.4 psi,42.0 Psi & 29.4 Psi, Respectively.Caused by Overranging of Zero Spring in Prior Calibr.Procedure Revised | |
| 05000280/LER-1975-024-01, /01T:on 750116,containment Leak Rate Test Revealed Overall Integrated Containment Leakage Rate Greater than Acceptable Criterion.Caused by Two Defective Tubes in Steam Generator A.Tubes Plugged | /01T:on 750116,containment Leak Rate Test Revealed Overall Integrated Containment Leakage Rate Greater than Acceptable Criterion.Caused by Two Defective Tubes in Steam Generator A.Tubes Plugged | |