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| 05000280/LER-1984-001-01, :on 840106,overtemp delta-T Signal Tripped Reactor.Caused by Power Surge During Gaitronics Sys Maint. Gaitronics Sys Test Will Be Written & Performed & Results Will Be Used to Develop Procedure |
- on 840106,overtemp delta-T Signal Tripped Reactor.Caused by Power Surge During Gaitronics Sys Maint. Gaitronics Sys Test Will Be Written & Performed & Results Will Be Used to Develop Procedure
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| 05000281/LER-1984-001-02, :on 840113,manual Trip Initiated Upon Closure of Main Steam Trip Valve A.Unwarranted Valve Closure Due to Hairline Crack in Air Line Pipe Nipple of Valve Actuator. Possibly Caused by Mechanical Fatigue.Nipple Replaced |
- on 840113,manual Trip Initiated Upon Closure of Main Steam Trip Valve A.Unwarranted Valve Closure Due to Hairline Crack in Air Line Pipe Nipple of Valve Actuator. Possibly Caused by Mechanical Fatigue.Nipple Replaced
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| 05000280/LER-1984-001, :on 840106,reactor Trip Occurred W/Unit at 100% Power.Caused by Over Temp delta-t Signal.Feedwater to Steam Generator a Isolated & Source Range Channels Manually Reinstated |
- on 840106,reactor Trip Occurred W/Unit at 100% Power.Caused by Over Temp delta-t Signal.Feedwater to Steam Generator a Isolated & Source Range Channels Manually Reinstated
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| 05000281/LER-1984-002-01, :on 840114,at 2% Power Following 840113 Trip, During Replacement of Open Coil in Reactor Trip Relay, Reactor Trip Breaker a Deenergized When First Coil Lead Removed,Resulting in Reactor Trip.Caused by Personnel Error |
- on 840114,at 2% Power Following 840113 Trip, During Replacement of Open Coil in Reactor Trip Relay, Reactor Trip Breaker a Deenergized When First Coil Lead Removed,Resulting in Reactor Trip.Caused by Personnel Error
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| 05000280/LER-1984-002-02, :on 840118,control Room Indications & Annunciators Behaved Erratically Due to Voltage Spike.Caused by Cable Falling Out of Breaker Due to Loose Screw.Cable Reconnected |
- on 840118,control Room Indications & Annunciators Behaved Erratically Due to Voltage Spike.Caused by Cable Falling Out of Breaker Due to Loose Screw.Cable Reconnected
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| 05000280/LER-1984-003-01, :on 840206,reactor Tripped Due to Low Steam Generator Level W/Steam Flow/Feed Flow Mismatch in Steam Generator A.Caused by Tripped Feedwater Breaker Closing. Breaker Replaced |
- on 840206,reactor Tripped Due to Low Steam Generator Level W/Steam Flow/Feed Flow Mismatch in Steam Generator A.Caused by Tripped Feedwater Breaker Closing. Breaker Replaced
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| 05000281/LER-1984-003, :on 840114,while at 23% Power,Feed Flow to Steam Generator a Increased to Full Flow.Valve Opened & Steam Generator a High Level Trip Initiated Turbine Trip, Tripping Reactor.Caused by Air Supply Piping Damage |
- on 840114,while at 23% Power,Feed Flow to Steam Generator a Increased to Full Flow.Valve Opened & Steam Generator a High Level Trip Initiated Turbine Trip, Tripping Reactor.Caused by Air Supply Piping Damage
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| 05000280/LER-1984-004-03, :on 840225,following Shutdown,Specific Activity Sample of Reactor Coolant Showed Peak Dose Equivalent I-131 Level of 1.77 Mci/Cc,Exceeding Tech Spec 3.1.D.2.Caused by Fuel Element Defects in Reactor Core |
- on 840225,following Shutdown,Specific Activity Sample of Reactor Coolant Showed Peak Dose Equivalent I-131 Level of 1.77 Mci/Cc,Exceeding Tech Spec 3.1.D.2.Caused by Fuel Element Defects in Reactor Core
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| 05000281/LER-1984-004, :on 840315,67 of 267 Snubbers Failed to Meet Acceptance Criteria Stipulated in Snubber Administrative Procedures.Snubber Program Being Revised to Provide Better Controls on Maint & Tracking of Snubbers |
- on 840315,67 of 267 Snubbers Failed to Meet Acceptance Criteria Stipulated in Snubber Administrative Procedures.Snubber Program Being Revised to Provide Better Controls on Maint & Tracking of Snubbers
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| 05000280/LER-1984-005, :on 840301,while Performing Mop 26.9,vital Bus Sola Transformer I-I,vital Buses I & III Mistakenly Cross Connected Out of Phase,Causing Spurious Containment High Pressure & High Steam Flow Signals |
- on 840301,while Performing Mop 26.9,vital Bus Sola Transformer I-I,vital Buses I & III Mistakenly Cross Connected Out of Phase,Causing Spurious Containment High Pressure & High Steam Flow Signals
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| 05000281/LER-1984-005-01, :on 840316,reactor Trip Occurred as Result of Reactor Coolant Pump Trip.Caused by Water in Electrical Penetration for Motor Leads.Penetration Replaced W/Spare & Meggered & Type B Tested Satisfactorily |
- on 840316,reactor Trip Occurred as Result of Reactor Coolant Pump Trip.Caused by Water in Electrical Penetration for Motor Leads.Penetration Replaced W/Spare & Meggered & Type B Tested Satisfactorily
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| 05000280/LER-1984-006-01, :on 840301,as Result of Snubber Functional tests,69 of 226 Snubbers Failed to Meet Acceptance Criteria. Cause Not Stated.Snubber Program Revised & Associated Procedures Reviewed |
- on 840301,as Result of Snubber Functional tests,69 of 226 Snubbers Failed to Meet Acceptance Criteria. Cause Not Stated.Snubber Program Revised & Associated Procedures Reviewed
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| 05000281/LER-1984-006, :on 840316,cooldown Rate Exceeded 50 F/Hr. Caused by Control Room Operators Failure to Recognize Increasing Cooldown Rate.Personnel Reinstructed & Operators Required to Read LER |
- on 840316,cooldown Rate Exceeded 50 F/Hr. Caused by Control Room Operators Failure to Recognize Increasing Cooldown Rate.Personnel Reinstructed & Operators Required to Read LER
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| 05000280/LER-1984-007-06, :on 840328,instrument Technicians Determined That Main Feed Regulating Valves Would Not Have Tripped Closed Upon Receipt of Feedwater Isolation Signal.Caused by Unapproved Work Procedure.Procedure Corrected |
- on 840328,instrument Technicians Determined That Main Feed Regulating Valves Would Not Have Tripped Closed Upon Receipt of Feedwater Isolation Signal.Caused by Unapproved Work Procedure.Procedure Corrected
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| 05000281/LER-1984-007, :on 840320,motor Operated Valve Breakers Found Open & Unlocked.Caused by Inadequate Review of Tech Specs. Locks Placed on Valve Breakers |
- on 840320,motor Operated Valve Breakers Found Open & Unlocked.Caused by Inadequate Review of Tech Specs. Locks Placed on Valve Breakers
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| 05000281/LER-1984-008, :on 840323,4160-volt Motor Leads for RHR Pump Motors Improperly Electrically Insulated W/Heat Shrinkable Matl Rated for 1,000 Volts.Caused by Inadequate Maint Procedures.Insulation Replaced |
- on 840323,4160-volt Motor Leads for RHR Pump Motors Improperly Electrically Insulated W/Heat Shrinkable Matl Rated for 1,000 Volts.Caused by Inadequate Maint Procedures.Insulation Replaced
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| 05000280/LER-1984-008-01, :on 840407,following Reactor Trip,Source Range NI-31 Failed high,NI-32 Declared Inoperable Due to Noise.Caused by Faulty preamp.NI-31 Preamp & NI-32 Detector Replaced |
- on 840407,following Reactor Trip,Source Range NI-31 Failed high,NI-32 Declared Inoperable Due to Noise.Caused by Faulty preamp.NI-31 Preamp & NI-32 Detector Replaced
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| 05000280/LER-1984-009, :on 840407,specific Activity Sample of Reactor Coolant Showed Peak Dose Equivalent I-131 Level Exceeding Tech Spec Limit.Caused by Fuel Element Defects in Reactor Core.Level Monitored Every 4 H |
- on 840407,specific Activity Sample of Reactor Coolant Showed Peak Dose Equivalent I-131 Level Exceeding Tech Spec Limit.Caused by Fuel Element Defects in Reactor Core.Level Monitored Every 4 H
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| 05000281/LER-1984-009-01, :on 840415,reactor Trip Occurred as Result of Intermediate Range High Flux Trip.Caused by Spike on Range Detector NI-35.Emergency & Function Restoration Procedures Performed |
- on 840415,reactor Trip Occurred as Result of Intermediate Range High Flux Trip.Caused by Spike on Range Detector NI-35.Emergency & Function Restoration Procedures Performed
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| 05000280/LER-1984-010-03, :on 840517,reanalysis Rept on Compliance to Design Requirements of 10CFR50,App R Received.Insp of Fire Protection Equipment Identified Five Areas of Deficiency. Caused by Changes in NRC Interpretation |
- on 840517,reanalysis Rept on Compliance to Design Requirements of 10CFR50,App R Received.Insp of Fire Protection Equipment Identified Five Areas of Deficiency. Caused by Changes in NRC Interpretation
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| 05000281/LER-1984-010, :on 840418 & 19,reactor Trip Occurred as Result of Turbine Trip from High Level in Feedwater Heater 6A.Caused by Leaking Tube & Flow Blockage in Loop Seal.Tubes Plugged & Matl Removed from Loop Seal |
- on 840418 & 19,reactor Trip Occurred as Result of Turbine Trip from High Level in Feedwater Heater 6A.Caused by Leaking Tube & Flow Blockage in Loop Seal.Tubes Plugged & Matl Removed from Loop Seal
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| 05000280/LER-1984-011-03, :on 840518,operations Personnel Performing Sys Walkdown Following Maint Discovered Intended Heat Sink for Charging Pump Component Cooling Water Sys Isolated.Caused by Inadequate Procedures |
- on 840518,operations Personnel Performing Sys Walkdown Following Maint Discovered Intended Heat Sink for Charging Pump Component Cooling Water Sys Isolated.Caused by Inadequate Procedures
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| 05000280/LER-1984-012-01, :on 840526,specific Activity Sample of Reactor Coolant Showed Peak Dose Equivalent I-131 Level of 1.57 Uci Which Exceeded Tech Spec Limit.Caused by Fuel Element Defects in Reactor Core.Dose Equivalent Monitored Every 4 H |
- on 840526,specific Activity Sample of Reactor Coolant Showed Peak Dose Equivalent I-131 Level of 1.57 Uci Which Exceeded Tech Spec Limit.Caused by Fuel Element Defects in Reactor Core.Dose Equivalent Monitored Every 4 H
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| 05000281/LER-1984-012, :on 840420,reactor Tripped Due to High Flux on Source Range NI-32.Caused by Personnel Error.Personnel Counseled & Replacement Preamp Ordered |
- on 840420,reactor Tripped Due to High Flux on Source Range NI-32.Caused by Personnel Error.Personnel Counseled & Replacement Preamp Ordered
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| 05000281/LER-1984-013-01, :on 840807,reactor Trip Occurred from Completion of Two of Three Logic Matrix on Overpower Delta T Protection.Caused by Blown Control Power Fuse in Instrument Drawer Due to Technician Error |
- on 840807,reactor Trip Occurred from Completion of Two of Three Logic Matrix on Overpower Delta T Protection.Caused by Blown Control Power Fuse in Instrument Drawer Due to Technician Error
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| 05000280/LER-1984-013, :on 840601,w/RCS Solid,At 145 F & 325 Psig,Porv Cycled in Response to Overpressure Condition While Placing Charging Sys in Svc.Caused by Personnel Error |
- on 840601,w/RCS Solid,At 145 F & 325 Psig,Porv Cycled in Response to Overpressure Condition While Placing Charging Sys in Svc.Caused by Personnel Error
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| 05000281/LER-1984-014-01, :on 840821,while Replacing Relay PRB-XB, Auxiliary Feed Pump 2-FW-P-3B Started Upexpectedly.Caused by Incorrectly Positioned Jumper Installed to Prevent Unnecessary Relay Actuation.Jumper Reinstalled |
- on 840821,while Replacing Relay PRB-XB, Auxiliary Feed Pump 2-FW-P-3B Started Upexpectedly.Caused by Incorrectly Positioned Jumper Installed to Prevent Unnecessary Relay Actuation.Jumper Reinstalled
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| 05000280/LER-1984-014, :on 840613,specific Activity Sample of Reactor Coolant Showed Peak Dose Equivalent I-131 Level of 1.99 Uci Which Exceeded Tech Spec Limit.Caused by Fuel Element Defects in Reactor Core.Monitoring Performed Every 4 H |
- on 840613,specific Activity Sample of Reactor Coolant Showed Peak Dose Equivalent I-131 Level of 1.99 Uci Which Exceeded Tech Spec Limit.Caused by Fuel Element Defects in Reactor Core.Monitoring Performed Every 4 H
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| 05000281/LER-1984-015, :on 841029,during Breaker Testing,Load Shedding Initiated & Main Feedpump Tripped Leading to Low Steam Generator Level & Reactor Trip.Caused by Inadequate Procedures.Procedure Revised |
- on 841029,during Breaker Testing,Load Shedding Initiated & Main Feedpump Tripped Leading to Low Steam Generator Level & Reactor Trip.Caused by Inadequate Procedures.Procedure Revised
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| 05000281/LER-1984-015-01, :on 841029,main Feedpump a Tripped as Result of Load Shedding Leading to Low Steam Generator Level & Reactor Trip.Caused by Inadequate Procedures.Operating Procedures Will Be Revised |
- on 841029,main Feedpump a Tripped as Result of Load Shedding Leading to Low Steam Generator Level & Reactor Trip.Caused by Inadequate Procedures.Operating Procedures Will Be Revised
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| 05000280/LER-1984-015, :on 840613,control Room Operator Observed Loss of Main Feed Pump a & Lowering of Steam Generator Water Levels.Caused by Loosening of Bearing Capscrews.Capscrew & Bolt Torque Specified in Maint Procedure |
- on 840613,control Room Operator Observed Loss of Main Feed Pump a & Lowering of Steam Generator Water Levels.Caused by Loosening of Bearing Capscrews.Capscrew & Bolt Torque Specified in Maint Procedure
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| 05000280/LER-1984-016, :on 840619,automatic Reactor Trip Resulted from Exceeding 10% Power on Two of Four Nuclear Power Channels, Ni 44 & Ni 41,w/turbine Unlatched.Caused by Isolation Valve Malfunction Due to Broken Gear Pin |
- on 840619,automatic Reactor Trip Resulted from Exceeding 10% Power on Two of Four Nuclear Power Channels, Ni 44 & Ni 41,w/turbine Unlatched.Caused by Isolation Valve Malfunction Due to Broken Gear Pin
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| 05000281/LER-1984-016-03, :on 841120,reactor Tripped Due to Low Water Level in Steam Generator C.Caused by Main Feedwater Manual Isolation Valves Closing at Startup.Procedures Modified to Include Verification of Position of Valves |
- on 841120,reactor Tripped Due to Low Water Level in Steam Generator C.Caused by Main Feedwater Manual Isolation Valves Closing at Startup.Procedures Modified to Include Verification of Position of Valves
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| 05000281/LER-1984-017-02, :on 841207,drawing Error,Discovered During Tagging Record Review,Indicated That Auxiliary Feedwater Crosstie Capability Unavailable During 840929-1115.Drawing Change Request Initiated |
- on 841207,drawing Error,Discovered During Tagging Record Review,Indicated That Auxiliary Feedwater Crosstie Capability Unavailable During 840929-1115.Drawing Change Request Initiated
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| 05000280/LER-1984-017, :on 840620,control Rod B-6 Became Stuck at 56 Steps Withdrawn,Resulting in Quadrant Power Tilt of Greater than 2% for More than 24 H.Caused by Spring Clamp Separation.Fuel Assembly Removed from Svc |
- on 840620,control Rod B-6 Became Stuck at 56 Steps Withdrawn,Resulting in Quadrant Power Tilt of Greater than 2% for More than 24 H.Caused by Spring Clamp Separation.Fuel Assembly Removed from Svc
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| 05000280/LER-1984-018, :on 840823,operator Discovered Air Hose Blocking Open Fire Door Between Equipment Space 1 & Cable Spreading Room.Caused by Misinterpretation of End of Walkdown Procedures.Hose Removed |
- on 840823,operator Discovered Air Hose Blocking Open Fire Door Between Equipment Space 1 & Cable Spreading Room.Caused by Misinterpretation of End of Walkdown Procedures.Hose Removed
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| 05000281/LER-1984-018-02, :on 841211,spurious Reactor Trip Occurred. Caused by 2 of 3 Logic Matrix for High Pressurizer Level Actuating.Addl Administrative Controls for Work on Energized Components Initiated |
- on 841211,spurious Reactor Trip Occurred. Caused by 2 of 3 Logic Matrix for High Pressurizer Level Actuating.Addl Administrative Controls for Work on Energized Components Initiated
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| 05000281/LER-1984-019-02, :on 841211,reactor Trip Occurred.Caused by Low Condenser Vacuum Due to Leak in Moisture Separator Reheater Crossunder Manway Gasket.Manway Temporarily Sealed,Gasket Replaced & Procedure Revised |
- on 841211,reactor Trip Occurred.Caused by Low Condenser Vacuum Due to Leak in Moisture Separator Reheater Crossunder Manway Gasket.Manway Temporarily Sealed,Gasket Replaced & Procedure Revised
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| 05000280/LER-1984-019, :on 840905,control Room Area Emergency Ventilation Sys Technically Inoperable.Caused by post- Maint Testing Oversight.Flow Test Performed on Both Units Relay Room Emergency Ventilation Fans |
- on 840905,control Room Area Emergency Ventilation Sys Technically Inoperable.Caused by post- Maint Testing Oversight.Flow Test Performed on Both Units Relay Room Emergency Ventilation Fans
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| 05000281/LER-1984-020-02, :on 841231,while Transferring Feed Flow from Bypass Valves to Main Feedwater Regulating Valves,Reactor Trip Occurred Due to Low Level W/Steam Flow/Feed Flow Mismatch in Steam Generator B |
- on 841231,while Transferring Feed Flow from Bypass Valves to Main Feedwater Regulating Valves,Reactor Trip Occurred Due to Low Level W/Steam Flow/Feed Flow Mismatch in Steam Generator B
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| 05000280/LER-1984-020, :on 840926,reactor Trip Occurred Due to Reactor Coolant Pump (RCP) Motor C Trip.Caused by Complete Separation of Phase Main Load Connection Bus Bar A.All Bus Bars in RCP Replaced |
- on 840926,reactor Trip Occurred Due to Reactor Coolant Pump (RCP) Motor C Trip.Caused by Complete Separation of Phase Main Load Connection Bus Bar A.All Bus Bars in RCP Replaced
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| 05000281/LER-1984-021-02, :on 841216,w/unit at Approx 20% Power & Ramping Down for Secondary Sys Repair,Unit Tripped When Breakers for Main Feed Pump B Opened.Caused by Invalid Low Flow Condition.Trip Circuitry Tested |
- on 841216,w/unit at Approx 20% Power & Ramping Down for Secondary Sys Repair,Unit Tripped When Breakers for Main Feed Pump B Opened.Caused by Invalid Low Flow Condition.Trip Circuitry Tested
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| 05000281/LER-1984-021, :on 841216,trip Occurred When Breakers for Main Feed Pump B Opened.Caused by Excessive Drift in Pressure That Input Low Flow Signals to Recirculation Valve/Pump Trip Logic.Procedures Modified |
- on 841216,trip Occurred When Breakers for Main Feed Pump B Opened.Caused by Excessive Drift in Pressure That Input Low Flow Signals to Recirculation Valve/Pump Trip Logic.Procedures Modified
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| 05000280/LER-1984-021, :on 841028,assigned Fire Watch Not Present at Cable Tunnel Area & Carbon Dioxide (CO2) Fire Sys Locked Out.Caused by Personnel error.CO2 Sys Restored & Personnel Counseled on Importance of Proper Fire Watch |
- on 841028,assigned Fire Watch Not Present at Cable Tunnel Area & Carbon Dioxide (CO2) Fire Sys Locked Out.Caused by Personnel error.CO2 Sys Restored & Personnel Counseled on Importance of Proper Fire Watch
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| 05000280/LER-1984-023, :on 841113,spurious Safety Injection Received While Technicians Performing Calibr Procedure CAL-63.Caused by Electrical Transient in Instrument Loops |
- on 841113,spurious Safety Injection Received While Technicians Performing Calibr Procedure CAL-63.Caused by Electrical Transient in Instrument Loops
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| 05000280/LER-1984-024, :on 841116,spurious Safety Injection Occurred When Returning Consequences Limiting Safeguards,High Phase (Equivalent to Containment Depressurization Actuation Sys) to Svc.Impact on Unit Minimal |
- on 841116,spurious Safety Injection Occurred When Returning Consequences Limiting Safeguards,High Phase (Equivalent to Containment Depressurization Actuation Sys) to Svc.Impact on Unit Minimal
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| 05000280/LER-1984-025, :on 841203,during Refueling Outage W/Plant in Cold Shutdown,Source Range & Intermediate Range Trip Signal Occurred.Caused by Voltage Transient Induced Upon Vital Bus 2 During Replacement of Key Switch |
- on 841203,during Refueling Outage W/Plant in Cold Shutdown,Source Range & Intermediate Range Trip Signal Occurred.Caused by Voltage Transient Induced Upon Vital Bus 2 During Replacement of Key Switch
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| 05000280/LER-1984-026-01, :on 841231,reactor Trip Occurred When Reactor Trip Breaker B Opened.Cause Undetermined.Reactor Trip Breaker B Inspected & Shunt Devices Tested.No Discrepancies Found |
- on 841231,reactor Trip Occurred When Reactor Trip Breaker B Opened.Cause Undetermined.Reactor Trip Breaker B Inspected & Shunt Devices Tested.No Discrepancies Found
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| 05000280/LER-1984-027, :on 841218,during Surveillance Testing of Emergency Diesel Generator 3,fire Occurred in Vicinity of Turbocharger.Caused by Leaking Fitting on Fuel Injector Line Which Allowed Fuel Oil to Leak Into Lube Oil |
- on 841218,during Surveillance Testing of Emergency Diesel Generator 3,fire Occurred in Vicinity of Turbocharger.Caused by Leaking Fitting on Fuel Injector Line Which Allowed Fuel Oil to Leak Into Lube Oil
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