ML18052B228

From kanterella
Jump to navigation Jump to search
LER 87-024-00:on 870714,unusual Event Declared Based on Loss of Offsite Power.Caused by Fault on 1-2 Startup Transformer Due to Contaminants in Deluge Sys Water.Deluge Sys Will Be Flushed quarterly.W/870813 Ltr
ML18052B228
Person / Time
Site: Palisades Entergy icon.png
Issue date: 08/13/1987
From: Bordine T, Kozup C
CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.)
To:
NRC OFFICE OF ADMINISTRATION & RESOURCES MANAGEMENT (ARM)
References
LER-87-024, LER-87-24, NUDOCS 8708180028
Download: ML18052B228 (6)


Text

NllC ......... u.a. NUCLIAll lllQULATOllY ~IC*

. 19-BJ)

LICENSEE EVENT REPORT (LER)

-OVIO ()119 NO. Jll0-41CM IXl'lllll: l/31-

'ACILITY NAMI 111 lDOCKIT ........ IZI I Palisades Nuclear Plant 0 I 6 I 0 I 0 I 0 I 2 15 15 , IOF 015 TITLI l*I Startup Transformer Failure Results in Loss of Offsite Power and Manual Reactor Trip IV NT OATI Ill Liii N~lllll 11) llllll'OllllT DATE 171 OTHlllll 'ACILITIU INYOLVID 181 MONTH DAY YEAR YEAR

<< llQUENTIAL.

NUMel!,_  !'.:::} "E\181Cf< MONTH NUMH" DAY YEAR *ACIL.ITY NAMU DOCKET NUMlllllll N/A 0 1&1010101 I I 011 114 8 7 sh - ol 214 - olo ols 113 sh N/A* 0161010101 I I 11 llllll'OllllT II IU8MITTEO l'UlllllUANT TO THI llllEOUlllllEMENTI OF 10 C,1111 §: I~ OM or.....,.. of IN fol-flf/ 1111 OfllMTINQ MODI Ill N 2CUll2Clll 20.-lcl ID.71C.llZlll*I n.1111111 POWlllll 20. . . C.ICllllJ ID.*lcl111 ID.71c.llZIM ....__ 71.711*1 LIYIL 1101 0 I~ 11 20 . . . C.11111YI ID ** lcll21 ID.71C.llZICril ....__ OTHEllll /!/#City in Aboncr t :*:* .............

?I ((}

{\)

-- 20 .... lollillRll I0.411111111111-rl 20 . . . c.11111*1 I0.731*112111J I0.7JC.1121CUI I0.73C.1121Ulll ID.71c.llZlhrlllllAI ID.7JC.llZIC\'lllllll ID.7JC.llZll*l

..,_.,Id In Te*r. NllC Fomo

.JllAI LICENSEE CONTACT FOii THll LEllll 1121

. NAME TELEl'HONE NUMIER AllllEA CODE CSKozup, Technical Engineer 61116 116141-18191113 COMl'LETE ONE LINE FOl'I EACH COMl'ONENT 'AILUllllE DEIClllllllD .IN THll llllll'OllllT 1111 CAUSE SYSTEM COMPONENT MANUFAC*

TUR ER REPORTABLE TO NPROS t:~;: *::::*.::::::::::.:::*:,:.:*,_i;:**: .: : :.:. CAUSE SYSTEM COMl'ONENT MANUFAC*

TUllEl'I llEl'OlllT Al LI TO Nl'llDS .-.:.-=: : : :~: :~: : : :i: =: !:': ,:i: : :*: =;

-:::.::,:;:,',::::::;:;:::)':}')

x EIA X1 F1M IR G101 810 Yes  ::::: :))\::*:<:::: tt x T1A I F1C 1U M1112 10 No  :::::::::*::::::::::::::::::::::::,::::::::]::*:::

x SIB I IRIV c 161 31 5 No r;:::::::*

,:i:H::::::::t=):'.:-':::*,:::

/:;:=:;:::;: \':\} x S1B I R1L 1Y W111Z I 1 Yes  : 1* :1:1: : : : : : : : *,: :_: 1:1:1: : ~: 1:1:

IUl'l'LIMINTAL llllEl'OllllT EXl'ECTED 11" MONTH DAY "JAR EXl'ECTED fl- ~

IUIMllllON I YES ,,, ...... ~- EJC/IECTED SUllll/$$/ON DA TEI NO DATE 1151 I I I AllTl'IACT 11.im/r ID 14()(/ -

  • 1.1., -ro*l,,,.re1y riflfl*-* rypowr1mn /inn! 1111 On July 14, 1987 at 1322 a loss of off site power occurred while the reactor was critical and operating at 91 percent of rated power. At 1330 the Site Emergency Plan was activated and an Unusual Event was declared based on the loss of off site power.

The loss of off site power occurred due to a fault on the 1-2 startup trans-former [EA;XFMR]. The fault on the 1-2 startup transformer actuated protec-tive relays which tripped the breakers for the 1-1, 1-2, and 1-3 startup transformers resulting in a loss of off-site power. The fault was preceded by the inadvertent actuation of the deluge fire protection system [KP] for the main transformers. A combination of the deluge water contamination and wind currents are attributed with providing the necessary path.to ground for the fault. The deluge system was inadvertently activated during maintenance to correct an alarm problem on the deluge system for the main transformer.

After observing the loss of off site power, the Shift Supervisor ordered a manual reactor trip because of the loss of cooling tower pumps [KE;P] which provide flow for the secondary heat sink. The Plant's two emergency diesel generators [EK;DG] provided power until 2048 on July 14, 1987 when off site power was restored. The Unusual Event was terminated at 2049. After the trip the plant was maintained in hot shutdown using natural circulation flow until forced circulation flow was restored at 2221.

8708180028 870013 PDR s

ADOCK 05000255 PDR 1t1t./1 NllCF_ . .

C~J LER 87-024A-NL02

NRC Form 38GA U.11. NUCLEAR REGULATORY. COMMISSION

,19-831 LICENSEE EVENT REPORT (LER) TEXT CONTINUATION APPROVED OMB NO. 3150--0104 EXPIRES: B/31185 FACILITY NAME 111 DOCKET NUMBER 121 LER NUMBER (61 PAGE 131 Palisades.Nuclear Plant 0 15 IO IO jO 121515 817 - 01214 - 010 012 OF 015 TEXT (If motW - ii f9tluftd. U* ~ NRC Fonn 311&4'iJ 1171 Description On July 14, 1987 at 1322 a loss of offsite power occurred with the reactor critical at 91 percent of rated power. The loss of offsite power resulted in the loss of cooling tower flow to the main condenser. The Shift Supervisor directed the reactor to be manually tripped due to the forthcoming loss of condenser vacuum. The forced circulation ceased after the turbine generator coastdown was completed. The plant's two emergency diesel generators [EK;DG]

provided power until offsite power was restored at 2048. The plant was maintained in hot shutdown using natural circulation flow until forced cir-culation flow was restored at 2221. An Unusual Event was declared at 133Q and was terminated at 2049.

On July 14, 1987 plant I&c*technicians were working to correct an alarm proble~ on the main transformer deluge system [KP]. The system air pressure for the main transformer and the startup transformer deluge systems are cross connected, After calibration of the main transformer pressure switch, PS-1341

[EF;PS] the system air pressure was increased and then decreased to balance the system. The deluge system actuates on differential pressure across a diaphragm [KP;BLL]. One side of the diaphragm has system air pressure, the other side has heat actuated device (HAD) air pressure. Under normal circumstances the air pressure is the same on both sides of the diaphragm with a compensating vent maintaining this equilibrium. However, when the HAD sees a rapid rise in temperature, the air expands increasing the air pressure faster than the compensating vent can release it, thus pushing the diaphragm in and releasing a weight latching mechanism, allowing the deluge valve to open. In this inadvertent actuation, the air supply pressure was reduced quickly which resulted in the air pressure on the HAD side of the diaphragm to be greater and therefore, the diaphragm moved and released the weight latch.

Shortly after the deluge system actuated, a flashover arc jumped from the 'Y' phase insulator bushing cap [EA;INS] to the transformer case of the 1-2 startup transformer [EA;XFMR]. The flashover created a ground fault on the

'Y' phase. The ground fault was sensed by the primary and backup bus differ-ential relay scheme which initiated trips on the 345KV switchyard 'R' bus air blast breakers [EA;BKR] and the startup power breakers to the cooling tower system. The normal fast transfer to the startup power after a reactor trip was blocked due to the faults sensed from the flashover arc. The diesel generators [EK;DG] loaded onto their respective bus via the normal shutdown sequencers as designed.

Reactor trip and loss of forced circulation emergency procedures and initial safety function checks were completed and natural circulation flow was verified by 1339. The major Piant equipment responded as expected during the Plant trip with the exception of the quick open feature for the atmospheric steam dump valves [SB;RV] and the turbine bypass valve [TA;FCV]. These valves did not open until between 18 and 31 seconds after the Plant trip. The Plant remained in hot shutdown on natural circulation flow from the trip until 2221 when a primary coolant pump [AB;P] was started.

NRC FORM 366.A 19*831 LER 87-024A-NL02

I I

NRC Form 3116A U.S. NUCLEAR REGULATORY* COMMISSION I !9-831 LICENSEE EVENT REPORT (LERI TEXT CONTINUATION APPROVED OMB NO. 3150-0104 EXPIRES: B/31/85 FACILITY NAME (1 I DOCKET NUMBER (21 LER NUMBER (II PAGE (31 Palisades Nuclear Plant 0 I 5 I 0 I 0 I 0 I 2 I 5 I 5 81 7 - 0 12 I 4 - 0I0 0 I3 OF 0 I5 TEXT l/f mor9 - io twq-. u* 9dditioM/ NRC Foml 311&4 '*I 1171

[EF;XFMR] were commenced at 1550 and completed at 1950. These activities proceeded in a deliberate manner to allow the balance of *switchyard breakers to be checked, verify status of the main transformer (that is used to backfeed), and to assure all relaying had properly functioned. Plant

  • management's intent at this time was to proceed with the recovery phase cautiously since the Plant was operating very well under natural circulation and no risks for disrupting natural circulation were forseen. At 1950, buses lE, lA and lB were restored to service via backfeeding through the main transformer. However, on the first attempt to backfeed Bus lC, a load shed signal was received and the lC bus was reloaded onto the 1-1 D/G via the normal shutdown sequencer. The subsequent investigation revealed that two startup transformer auxiliary relays were not identified to be reset per the off-normal operating procedure. These relays were reset and buses lC and lD w~re powered from offsite power at 2048. Subsequently, the Off-Normal Operating Procedure for Loss of AC Power was corrected to include restoration of these two relays when backfeeding the lC and lD buses.

Cause Of The Event The root cause of the fault is contaminants in the transformer deluge system water combined with wind currents which allowed the water spray to reach the top of the transformer bushing. These contaminants in the water spray provided a path to ground (ie, transformer case) for an electrical arc. There was no indication the arc traveled along the bushing surface or that the arcing was internal to the bushing or transformer. The contaminants were caused by water not being periodically flushed from the piping.

The proximate cause of the event was the inadvertent actuation of the deluge spray system on. the startup transformer. The I&C technicians.were performing maintenance on the deluge alarm system and had determined that pressure switch PS-1341 required calibration. After calibration, the system air pressure for the main transformer was repressurized for system operation. While raising the system air pressure to pressurize the main transformer deluge system, the regulator was adjusted such that the startup transformer deluge system pressure was too high. These two systems are tied together through a common air supply and pressure regulator. The system air pressure for the startup transformer was lowered by opening an air bleedoff valve. Just as the pressure reached the normal operating.range, the startup transformer deluge system activated. -

The delayed operation' of the turbine bypass valve and the atmospheric steam dumps was determined to be a failure of turbine trip lockout relay 386/AST

[SB;RLY] to make up properly during the event. An inspection of the relay revealed that the spacer between the contacts had broken. As a result of the spacer failure the contacts had shifted so they would not makeup as intended when the cam rotated. This resulted in the disabling of the quick open feature of the turbine bypass valve and the atmospheric steam dumps.

NRC FORM 366A 19-83 1 LER 87-024A-NL02

NRC Form 3UA U.S. NUCLEAR REGULATORY COMMISSION 19-831 LICENSEE EVENT REPORT (LER) TEXT CONTINUATION APPROVEO OMB NO. 3150--0104 EXPIRES: 8/31 /85

,) I~:cii'.iTVN:i:o".i';"i'"-------------------------------r-::::::::~~::::;-:"";::-------.....,~~~~~----------~..,...~~~--~--1 FACILITY NAME (11 DOCKET NUMBER (21 LER NUMllER (91 PAGE (31 Palisades* Nuclear Plant 0 15 IO IO IO 121515 817 - 01214 - 010 014OF015 TEXT IH tnOl9 - ia ,..,,uftd, U* eddmon.I NRC Fonn 3l!S'4 '11 1171 Corrective Actions The contamination in the deluge water lines was caused by corrosion due to the stagnant water in the piping. This contamination will be reduced by quarterly flushes of the deluge system. This flush has been incorporated into the periodic fire system checklists. The deluge spray nozzles were tested to determine if the spray nozzles should be adjusted. The. test showed none of the nozzles sprayed directly up into the bushing and that no adjustments were necessary. In addition, an engineering review of the deluge system is being conducted to determine possible actions which would minimize inadvertent actuations of the deluge system. This review will be completed by September 1987.

The turbine trip lockout relay (386/AST) was replaced prior to Plant startup.

In addition, a review for similar relays in the Plant was conducted. Eleven similar relays were located and inspected. None of these eleven relays exhibited a similar spacer failure or any other anomalies. Because the 386/AST relay also provides logic to the feedwater pump speed ramp down, the closure of turbine generator moisture separator reheater valves and the feedwater regulator valve controls in addition to the turbine bypass and atmospheric steam dump valves, this relay failure is being evaluated to determine if it may have contributed to the anomalies observed on June 20, 1987. Those anomalies are described in Licensee Event Report 87-018, "Improper Valve Operation Results in Reactor Critical At Less Than 525°F".

The evaluation of the failed relay effects on the June 20, 1987 event will be completed by September 1987.

The Palisades offsite power system is being evaluated to determine possible upgrades to the system to improve reliability. The identification of possible options for the upgrade will be completed in September 1987.

Analysis Of The Event The loss of offsite power with a reactor trip is an analyzed transient with no adverse safety consequences. The Plant response to the reactor and turbine trip was consistent with its designed operation with the exception of the atmospheric steam dump valve and the turbine bypass valve which failed to quick open. The review of the primary coolant system parameters indicate that the Plant responded as designed even though the quick open feature did not activate. Natural circulation was established and verified with no problems.

An independent assessment of the Plant trip was conducted by Plant Safety Engineering and they concurredwith the Plant startup after the maintenance repairs.

During the transient, the secondary system was exposed to hydraulic distur-bances. Secondary system equipment inspections revealed no signs of damage other than minor denting of insulation. During startup, Operations and System Engineering walkdowns were performed to look for additional damage which may not have appeared until after startup.

NAC FORM 366A 19.e31 LER 87-024A-NL02

~------

NRC Form 300A U.ll. NUCLEAR REGULATORY COMMISSION

.(9-831 LICENSEE EVENT REPORT (LERI TEXT CONTINUATION APPROVED OMB NO. 3150--0104 EXPIRES: B/31185

> FACILITY NAME (11 DOCKET NUMBER 121 LER NUMBER 1111 PAGE (31 Palisades Nuclear Plant 0 15 I 0 I 0 I 0 1215 I 5 s 11 - 0 1214 - 0 I0 0 15- OF 0 15 TEXT l/f mot9 _.,.ii f9quftt/, u* - N R C Fann .i115"1'*1 (171 As a precaution, the discharge piping of the f eedwater pumps and the conden-sate pumps were non-destructively tested (NDT) for possible damage. The NDT results showed no damage.

Offsite power was lost for over seven hours after the trip. The Plant was ready to backfeed after approximately four hours, but management conser-vatively decided to further investigate the power system for any undetected damage before backfeeding offsite power through the main transformer.

This event is being reported per 10CFR50.73 (a)(2)(iv) as. an event which resulted in the manual actuation of the Reactor Protection System.

NRC FORM 366A 1s.s3 1 LER 87-024A-NL02

-~.

POWERINli MICHlliAN'S PROliRESS General Offices: 1945 West Parnall Road, Jackson, Ml 49201 ~ (517) 788-0550 August 13, 1987 Nuclear Regulatory Commission Document Control Desk Washingt6n, DC 20555 DOCKET 50-255 - LICENSE DPR PALISADES PLANT -

LICENSEE EVENT REPORT 87-024 - STARTUP TRANSFORMER FAILURE RESULTS IN LOSS OF OFFSITE POWER AND MANUAL REACTOR TRIP Licensee Event Report (LER)87-024, (Startup Transformer Failure Results in Loss of Offsite Power and Manual Reactor Trip) is attached. This event is reportable to the NRC per 10CFR50.73(a)(2)(iv).

Thomas C Bordine Staff Licensing Engineer CC Administrator, Region III, NRC NRC Resident Inspector - Palisades OC0887-0128-NL02