ML17331A067
ML17331A067 | |
Person / Time | |
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Site: | Cook |
Issue date: | 12/31/1992 |
From: | Fitzpatrick E, Moran W, Svensson B INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG |
To: | |
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ML17331A066 | List: |
References | |
NUDOCS 9303030285 | |
Download: ML17331A067 (24) | |
Text
DONALD C. COOK NUCLEAR PLANT 1992 ANNUAL OPERATING REPORT February 28, 1993 COMPILED BY:
W. R. Moran Senior Engi er REVIEWED BY'. A. Svensson Executive Staff Assistant APPROVED BY' E. E. Fitzpa ick Vice President-Nuc1ear Operations 93030302B5 930226 PDR ADOCK 050003i5 R PDR
TABLE OF CONTENTS PAGE SECTION SECTION TITLE ~NUHBE 1.0 Introduction 1.1 Plant Description 1.2 Report Preparation 2.0 Personnel Radiation Exposure Summary
'.0 Steam Generator In-Service Inspection 3.1 Unit 1 Inspection Summary 3.2 Unit 2 Inspection Summary 4.0 Changes to Procedures 4.1 Maintenance Procedures 4.1.1 Fuse Testing 4.2 Operating Procedures 4.2.1 Operation of Containment Pressure Relief System 4.2.2 Turbine Generator Testing 4.2.3 Transfer to Cold Leg Recirculation 4.3 Environmental Monitoring Procedures 4.3.1 Spill Response Procedure Revisions 5.0 Tests or Experiments Not Described in the FSAR 8 5.1 Tests 5.1.1 Turbine Generator Testing 6.0 Challenges to Pressurizer Power Operated Relief Valves and Safety Valves 7.0 Reactor Coolant Specific Activity 10 8.0 Irradiated Fuel Examinations
- 8. 1 Visual Examinations 11 8.2 Ultrasonic Examinations ll ll 8.3 Fuel Sipping Examination 9.0 Changes to Facility 13 9.1 Design Changes 13
TABLE OF CONTENTS Cont'd.
PAGE SECTION SECTION TITLE NUMBER 9.1.1 Emergency Diesel Generator Control System Modification 13 9.1.2 Abandonment of the Containment Penetration and Weld Channel 13 Pressurization System 9.1.3 Modification of Secondary-side, In-line Chemistry Instrumentation 14 9.1.4 Separation of Auxiliary Feedwater Emergency Leakoff Lines 14 9.1.5 Boron In]ecti.on Tank Modification 14 9.1.6 Removal of Obsolete Westinghouse Radiation Monitors 15 (
9.1.7 Use of Spare Containment Penetration as a Service Penetration 15 9.2 Plant Modifications 15 9.2.1 Installation of Chemical Diffuser Headers in the Forebay 15 9.2.2 Modification of the PA System 16 9.2.3 New Prospect Engineering/Site Design Office Building Construction 16 9.2.4 Radioactive Materials Building Tie-ins to Plant Systems 17 9.3 Minor Modifications 17
'9.3. 1 Relocation of Orifice for Turbine Driven Auxiliary Feedwater Pump 17 9.3.2 Modification of the Ice Machine Glycol Return and Supply Header 17 9.4 Temporary Modifications 18 9.4.1 Close Control Room Ventilation Dampers 1,2-HV-ACRDA 18 9.4.2 Disconnect Inoperable Seismic Accelerometer 18
1.0 INTRODUCTION
~ ~
1.1 PLANT DESCRIPTION The Donald C. Cook Nuclear Plant is owned by Indiana Michigan Power Company and is located five miles north of Bridgman, Michigan. The plant consists of two nuclear power units, each employing a Westinghouse pressurized water reactor nuclear steam supply system.
Each reactor unit employs an ice condenser reactor containment system.
The American Electric Power Service Corporation was the architect-engineer and constructor.
Unit 1 and 2 reactor design power output (and licensed rating) are 3250 MWt and 3411 MWt, respectively. Unit 1 approximate gross and net electrical outputs are 1056 MWe and 1020 MWe, respectively. Unit 2 approximate gross and net electrical outputs are 1100 MWe and 1060 MWe, respectively. The main condenser cooling method is open cycle using Lake Michigan water as the cooling source for each unit.
1.2 E OR EPARATION This report was compiled by W. R. Moran with the following individuals contributing information as follows:
D. L. Noble - Personnel Exposure Summary C. A. Freer - Steam Generator ISI Summary R. G. Vasey - Changes to Procedures B. A. Svensson - Challenges to Pressurizer PORVs and Safety Valves R. G. Vasey - Tests or Experiments Not Described in the FSAR B. A. Svensson - Reactor Coolant Specific Activity T. A. Georgantis - Results of Irradiated Fuel Inspections R. G. Vasey - Changes to Facility - RFCs, MKs, PMs R. G. Vasey - Changes to Facility - Temporary Modifications to Unit 1 & 2
- 2. 0 PERSONNEL RADIATION EXPOSURE
SUMMARY
Table 1 provides'a summary of the number of station, utility, and contractor:
(and others) personnel receiving exposures greater than 100 millirem in 1992.
The total record dose for all personnel was 492.044 rem as measured by thermoluminescent dosimetry (TLD) and reported in accordance with Regulatory Guide 1.16.
TABLE ANNUAL OPERATING REPORT - RG 1.16 FOR 1992 PERSONNEL )100 mR TOTAL MAN-REM STAT. UTIL. CONT. -'STATION UTILITY CONTRACT Reactor Operations & Surveillance Maintenance Personnel 0002 0000 0008 000.477 000.000 001.262 Operations Personnel 0046 0002 0006 010.275 000.580 001.163 Health Physics Personnel 0031 0000 0070 007.956 000.000 024.259 Supervisory Personnel 0001 0000 0000 000.202 000.000 000.000 Engineering Personnel 0000 0000 0002 000.000 000.000 000.325 Routine Maintenance Maintenance Personnel 0083 0001 0298 024.006 000.238 118.059 Operations Personnel 0009 0001 0054 002.483 000.118 029.311 Health Physics Personnel 0009 0000 0032 001.730 000.000 005.886 Supervisory Personnel 0000 0000 0000 .000.000 000.000 000.000 Engineering Personnel 0009 0000 0002 002.054 000.000 000.744 In-Service Inspection Maintenance Personnel 0003 0000 0076 000.377 000.000 027. 172 Operations Personnel 0003 0000 0019 000.632 000.000 006.341 Health Physics Personnel 0001 0000 0016 000.131, 000.000 003.326 Supervisory Personnel 0000 0000 0000 000.000 000.000 000.000 Engineering Personnel 0001 0000 0006 000.117 000.000 001.890
\
Special Maintenance Maintenance Personnel 0013 0000 0166 002.124 000.000 051.826 Operations Personnel 0000 0000 0010 000.000 000.000 002.897 Health Physics Personnel 0002 0000 0018 000.217 000.000 002.691 Supervisory Personnel 0001 0000 0000 000.112 000.000 000.000 Engineering Personnel 0001 0001 0007 000.102 000.367 002.616 Waste Processing Maintenance Personnel 0000 0000 0003 000. 000 000. 000 001.296 Operations Personnel 0000 0000 0004 000.000 000.000 001.162 Health Physics Personnel 0004 0000 0066 000.600 000.000 012.730 Supervisory Personnel 0001 0000 0000 000.206 000.000 000.000 Engineering Personnel 0000 0000 0000 000.000 000.000 000.000 Refueling Maintenance Personnel 0004 0000 0031 000.558 000.000 006.158 Operations Personnel 0006 0000 0038 001.955 000.000 013.789 Health Physics Personnel 0000 0000 0032 000.000 000.000 005.049 Supervisory Personnel 0000 0000 0000 000.000 000.000 000.000 Engineering Personnel 0002 0000 0001 000.495 000.000 000-158 TOTALS Maintenance Personnel Operations Personnel 0089 0001 0461 027.542 000.238 205 '73 0059 0003 0104 015.345 000.698 054.663 Health Physics Personnel 0032 0000 0150 010.634 000.000 053 '41 Supervisory Personnel 0002 0000 0000 000.520 000.000- 000 000 Engineering Personnel 0010 0001 0016 002.768 000.367 005.733 GRAND TOTALS 0192 0005 0731 056.809 001.303 320.110
3.0 STEAM GENERATOR IN-SERVICE INSPECTION 3.1 UNIT 1 INSPECT ON
SUMMARY
SEE ENCLOSURE The Donald C. Cook Unit 1 steam generator inspection/repair program performed during July and August of 1992 was an extensive program. In addition to conducting the basic scope of bobbin coil (BC) and pancake coil (RPC) inspecti.ons of inservice tubes, 364 tubes 'otating potentially defective alloy 600 plugs, susceptible to primary water stress corrosion cracking were removed from their hot leg tubes (see enclosure). A selected number of these tubes were also inspected with a BC probe since they were considered repairable by sleeving. This resulted in 209 of these tubes, among four steam generators, being returned to service with sleeves. The scope of these efforts, combined with removing samples from four different tubes within steam generator 12 to be destructively examined, are listed in Sections I through III of the enclosure to this report.
SUMMARY
Eddy current inspection of Unit 2 generators was performed from March 19 to March 28, 1992. Approximately 6.5S of the total number of tubes in SGs 21 and 24 received an eddy current bobbin coil inspection to the extent as shown in Table 2.
TABLE 2 UNIT 2 STEAM GENERATOR INSPECTION S/G 21 S/G 24 Inspected full length from hot leg 71 69 Inspected to 7C from hot le@ 159 163 Inspected to 6C from hot le@ 4 2 Inspected to 5C from hot leg+ 1 1 No imperfections were found and no plugs were installed. Both of these SGs were returned to service as found.
- 5C, 6C, and 7C indicates that the length of the inspection from the hot leg side was to the fifth, sixth, and seventh support plate on the cold leg side.
4.0 CHANGES TO PROCEDURES This section contains a brief description of the procedure changes implemented under the provisions of 10 CFR50;59 and the associated safety evaluations.
4.1 INTENANCE PROCEDURES Z"
Description of Change:
Plant procedure 12 MHP 5021.082.016, which required periodic sample testing of standard grade fuses installed in circuits fed by battery-backed power buses, was canceled. This procedure is no longer necessary because safety grade fuses are now installed.
Safety Evaluation Summary:
This change was reviewed and it was concluded that it did not represent an unreviewed safety question. This conclusion is based on the fact that the procedure was initially instituted as a test program designed to provide assurance that safety related fuses, purchased as standard grade, would function properly. The fuses have been replaced with safety-grade fuses, providing assurance that the fuses will properly function.
4.2 OPERA IONS ROCEDURE 4.2.1 erat o o Co ta nme t essure Rel ef S ste Description of Change:
Plant Procedure 02-OHP 4021.028.004, "Operation of the Containment Pressure Relief System," was changed to allow the use of the containment purge supply and exhaust system to relieve containment pressure. Because of this change, the exhaust would not pass through charcoal and HEPA filters as described in the FSAR.
Safety Evaluation Summary:
This change was reviewed and it was concluded that represent an unreviewed safety question. This conclusion is it did not based on the fact that the containment isolation valves would remain functional and containment activity levels would be checked prior to making any releases. Releases would only be made if the activity levels were acceptable.
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4.2.2 Turbine Generator Testin Description of Change'.
Two procedures, 02-OHP SP.100 and -101, were written to conduct testing to determine the cause of turbine vibration that occurred in Unit 2. The testing consisted of increasing the turbine speed to 1930 rpm (rated speed is 1800 rpm),
increasing the seal oil supply temperature to 122-131 F and increasing the number 5 and 6 bearing temperature limits to 285 F.
Safety Evaluation Summary This change was reviewed and it was concluded that it did not represent an unreviewed safety question. This conclusion is based on the fact that the testing, had been proposed and approved by the turbine manufacturer personnel who had concluded that it would not adversely impact the turbine integrity or result in an increased risk of turbine missile generation.
4.2.3 ansfe to Co d Le ec rcu at o Description of Change:
Plant procedures 01-,02-0HP 4023.ES-1.3, Revision 2 made changes in the valve manipulation procedure which differ from the description in Section 6.2 of the FSAR. In particular, the SI pump minimum flow valves are closed (Step 4 of the FSAR description) after the RHR and CTS pumps are started (Step 6 of the FSAR description).
Safety Evaluation Summary:
This change was reviewed and it was concluded that it did not represent an unreviewed safety question. This conclusion is based on the fact that these are emergency procedures, and the change in the valve manipulation sequence will not increase the consequences of an accident.
4.3 NVIRONMENTAL MONITORING PROCEDURES 4.3.1 1 Res o se P ocedu e ev s o Description of Change:
Plant procedure PMI-2230, "Spill Response-Oil, Polluting, and Hazardous Materials," was revised to include additional items with regard to establishing an Incident Command System and Emergency Response Plan which meets Michigan Hazardous Waste Operations and Emergency Response requirements, and to address underground storage tank leaks. Four other procedures, PMP 2080 EPP.110, PMP 2081 EPP.103,.203, and .205 also required revisions as a result of these changes.
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Safety Evaluation Summary:
'his change was reviewed and it was concluded that it did not represent an unreviewed safety question. This conclusion is based on the fact that the changes to the procedure would not initiate an accident, would not adversely impact safety related equipment, and do not impact technical specification compliance.
5.0 TEST OR EXPERIMENTS NOT DESCRIBED IN THE FSAR This section describes procedures classified- as a "Test and Experiment" implemented under the provisions of 10 CFR50.59 including the associated safety evaluation.
5.1 5.1.1 Turbine Generator Testin See Section 4.2.2 - Turbine Generator Testing.
6.0 CHALLENGES TO PRESSURIZER POWER OPERATED RELIEF VALVES AND SAFETY VALVES During 1992, there were no challenges on either Unit 1 or Unit 2 to the pressurizer power operated relief valves (PORV's) or the pressurizer safety valves as a result of the valves being called upon to mitigate an actual overpressure condition.
7.0 REACTOR COOLANT SPECIFIC ACTIVITY During 1992, ther'e were no instances on either -Unit 1 or Unit 2 in which the, reactor coolant I-131 specific activity exceeded the limits of Technical Specification 3.4.8.
- 8. 0 IRRADIATED FUEL EXAMINATIONS During 1992 three separate examinations were performed on the irradiated fuel discharged from Unit 2, Cycle 8, and two separate examinations were performed on the irradiated fuel discharged from Unit 1, Cycle 12. These examinations were conducted in parallel with, or shortly after, the core was unloaded.
The intent was to determine fuel rod failures and gross structural defects in the fuel assemblies.
8.1 VISUAL INATIONS The first examination of the irradiated fuel for each unit was by routine binocular inspections of the fuel assemblies per procedure number 12 SHP 4050 QC.002. As each assembly is off-loaded to the spent fuel pool, it is visually examined on all four sides. The examiner is looking specifically for tom or missing grid straps, missing or damaged fuel rods, excessive clad hydriding, or rod bow to gap closure. This inspection is primarily intended to detect fuel damage caused by mechanical interaction between fuel assemblies or baffle )etting, and is done during each refueling. There were no indications of any fuel damage for either unit.
8.2 UL SONIC EXAMINATIONS The second examination of the irradiated fuel for each unit was performed by using ultrasonic testing (UT) methods. The ultrasonic system works by a probe transceiver sending a high frequency sound wave into a fuel rod and measuring the strength of the returning signal, or "ring back." A fuel rod can be determined to have water in it by monitoring the relative strength of this ring back.
presence of water in a fuel rod would indicate that the rod has The a
leak. In this way, not only can an assembly be determined to have leaking rods, but also the numbers and locations of the leaking rods can be identified.
For the Unit 2 UT inspection, the 117 irradiated fuel assemblies that were scheduled for reload 'into Cycle 9 were tested. Of these, two fuel assemblies were determined to each contain one leaking fuel rod.
In order to identify suitable replacement fuel assemblies for the two that contained leaking fuel rods, an additional eight fuel assemblies were tested. The UT methods were employed. None of these additional eight fuel assemblies were found to contain leaking fuel rods.
For the Unit 1 UT inspection, the 113 irradiated fuel assemblies that were scheduled for reload into Cycle 13 were tested. None of the 113 fuel assemblies were found to contain leaking rods.
8.3 EL S P NG EXAMINATION The third examination of the irradiated fuel for Unit 2 was through use of the fuel sipping technique. The technique used for the Unit 2 fuel involved the placement of the fuel assembly to be tested in a leak-tight canister, and a drawing of a partial vacuum in the canister. If the fuel assembly were to contain leaking fuel rods, radioactive gases would accumulate at the top of the canister. The gases at the top of the canister are measured for presence of radioactivity.
The fuel sipping results for the discharged fuel assemblies from Unit 2, Cycle 8 and the two fuel assemblies identified as replacements for the leaking fuel identified during UT confirmed the results of UT.
The Unit 2 fuel was sipped due,to the results of the analysis of the reactor coolant system (RCS) radiochemistry data from Cycle 8. This data indicated the possibility of a "tight" leaking fuel rod, as the
'CS radiochemistry data identified the presence of only gaseous fission products (e.g., xenon) and no indications of solid fission products (e.g., cesium). A concern existed that water may not have entered the "tight" leaking fuel rod and therefore, UT methods may have been inadequate to prevent reloading a leaking fuel rod.
Therefore, it was decided to sip Unit 2 fuel.
9.0 CHANGES TO FACILITY This section contains a brief description of -the design changes implemented under the provisions of 10 CFR50.59 and the associated safety evaluations.
9.1 DESIGN CHANGES 9.1.1 Emer enc Diesel Generator Cont ol S stem Modification Description of Change:
RFC-DC-12-2864 modified the emergency diesel generator control system to allow a controlled, slow start for surveillance testing, taking the diesels up to rated speed in an estimated 25 to 30 seconds. The modification included the installation of a timer to maintain the diesel generator in the slow start mode during the period that it is accelerating from 95-100% of rated speed. This change is intended to reduce the wear on the diesel generators and thereby enhance their overall reliability.
Safety Evaluation Summary:
This change was reviewed and it was concluded that it did not is represent an unreviewed safety question. This conclusion based on the fact that the emergency diesel generators overall reliability will be improved, and the change would not impair the ability of the diesel generator to respond to a fast start demand.
9.1.2 bandonment of the Containment Penetration and Weld Channe ressurization S stem Description of Change:
RFC-DC-12-2895 abandoned- portions of the Containment Penetration and Weld Channel Pressurization System.
Safety Evaluation Summary:
This change was reviewed and it was concluded that it did not conclusion is represent an unreviewed safety question. This based on the fact that no additional equipment that may initiate a design basis accident was installed. Additionally, the limits on the containment leakage were unaffected, ensuring that the leakrates assumed in the accident analysis remained valid.
9.1.3 od c to of Secoda -s de e Chemist nstrumentatio Description of Change:
RFC-DC-12-2915 modified the secondary chemistry instrumention.
The condensate, feedwater, demineralized water, main steam and steam generator blowdown monitors were upgraded in both the turbine building laboratory and the nuclear sampling room.
Safety Evaluation Summary:
This change was reviewed,. and it was concluded that it did not represent an unreviewed safety question. This conclusion is based on the fact that this RFC upgrades existing equipment and does not change the operation of that equipment.
9.1.4 Se aration of Auxilia Feedwater Emer enc Leakoff Lines Description of Change:
RFC-DC-12-3043 modified the auxiliary feedwater pumps emergency leakoff lines. The modification consisted of providing separate flowpaths to a common three inch test line.
The modification was made to preclude deadheading of an auxiliary feedwater pump due to adverse pump-to-pump interaction in response to NRC Bulletin 88-04, "potential safety-related pump loss." The modification also included the addition of orifices to limit the leakoff flow to 75 gallons per minute.
Safety Evaluation Summary:
This change was reviewed and it was concluded that it did not is represent an unreviewed safety question. This conslusion based on the fact that the change makes modifications which improve the performance of equipment important to plant safety in that the change reduces the potential adverse impact of one train on the other.
pron In ect o Tank S stem Modificat o Description of Change:
RFC-DC-12-3050 modified the Boron Injection Tank (BIT) and its associated piping after receiving approval from the NRC for a reduction in the tank's boric acid solution concentration.
The line between the boron injection tank and the boric acid storage tanks was cut and capped, the boron injection tank flush lines were cut and capped, and the boron injection tank vent was modified.
Safety Evaluation Summary:
The changes to the BIT piping systems were reviewed and it was concluded that they did not represent an unreviewed safety question. A previously approved technical specification I
amendment approved the change in the boric acid concentration.
As a result, the boron injection tank no longer performs a safety function during a steam line break transient, the only accident affected by the boron reduction and deactivation of the BIT.
9.1.6 Removal of Obsolete Westin house Radiation Monitors Description of Change:
RFC-DC-12-4078 removed radiation monitors, 1-R1, 2-Rl (control room area monitor) for Unit 1 and Unit 2, respectively, and 12-R3 (radio chemistry lab area monitor), and 1-R4, 2-R4 (charging pump room area monitor). These monitors were replaced with new Eberline monitors installed under RFC-2900 E.02.
Safety Evaluation Summary:
This change was reviewed and it was concluded that it did not conclusion is represent an unreviewed safety question. This based on the fact that the components have been replaced with upgraded equipment.
9.1.7 Use of S are Containment Penetration as a Service Penetratio Description of Change:
RFC-DC-12-4122 removed the end caps on containment penetration number (CPN) 71 and installed flanges with blank covers in their place. This allows hoses and cables to enter the containment through CPN-71 rather than through the lower containment airlock during operational modes where containment integrity is not required, eliminating a personnel hazard.
Safety Evaluation Summary:
This change was reviewed and it was concluded that it did not represent an unieviewed safety question. This conclusion is based on the fact that the penetration will continue to meet its functional requirements, and this change does not adversely impact any safety related equipment.
9.2 PLANT MODIFICATIONS 9.2.1 Instal at o of emical Diffuser cade s the Foreba Description of Change:
Plant Modification (PM)12-837 installed chemical diffuser headers in the forebay, upstream of the trash rack to evenly distribute biocidal chemicals in the forebay for zebra mussel control.
15
Safety Evaluation Summary:
'This change was reviewed and it was concluded that it did not represent an unreviewed safety question. This conclusion is .
based on the fact that implementing the PM will enhance the intake water supply by controlling or eliminating the growth of zebra mussels.
odification of the PA S ste Description of Change:
Plant Modification (PM) 12-1090 modified the plant PA system to help reduce background noise in the control rooms. At the time, paging could be addressed to either Unit 1, Unit 2, the office building, or the entire plant. As a result of the modification, paging can be 'addressed to either the control rooms, the office building, all areas of the plant except the control rooms and office buildings, or the entire plant.
Safety Evaluation Summary:
This change was reviewed and it was concluded that it did not represent an unreviewed safety question'. This conclusion was based on the fact that the implementation of the PM-would still allow the PA system to maintain,its ability to perform its emergency plan functions.
ew P o ect En ineerin S te Desi Office Bu ld n Description of Change:
Plant Modification (PM) 12-1159 constructed a new office building for the Project Engineering and Site Design Groups.
A new building was needed since the proposed site for the new fire protection water storage tanks is where the current offices are for the above mentioned groups. The selected location for this building is outside the protected area, south of the south security gate.
Safety Evaluation Summary:
This change was reviewed and it was concluded that it did not represent an unreviewed safety question. This conclusion was based on the fact that implementing the PM would not impact any safety-related equipment nor Seismic Class I structures that are important to safety and that the only impact to the UFSAR is in the plant layout drawings.
9.2.4 Radioactive Materials Buildin Tie- ns to Plant S stems Description of Change:
Plant Modification (PM) 12-1190 proposed to make various tie-ins from the newly built radioactive materials building to the existing fire protection system, potable water system, sewer system and various plant alarm systems.
Safety Evaluation Summary:
This change was reviewed and it was concluded that it did not represent an unreviewed safety question. This conclusion is based on the fact that implementing the PM would not prevent the above systems from performing their intended safety functions, if any, when called upon.
9.3 OR MODIFICATIONS 9.3.1 Relocation of Orifice for Turbine Drive Auxilia Feedwater Puu Description of Change:
Minor Modification (MM) 12-MM-242 relocated an orifice plate contained in the discharge .piping of the turbine driven auxiliary feedwater pump. The orifice plate was moved further downstream and the associated instrument lines, isolation valves, and transmitters were also relocated.
Safety Evaluation Summary:
This change was reviewed and it was concluded that it did not represent an unreviewed safety question. This conclusion is based on the fact that the change impacts only the location of the orifice plate and associated equipment. It does not impact the function of the auxiliary feedwater system nor does it degrade its structural .integrity.
9.3.2 od cat on o t e Ice ac e G co eturn and Su 1 H~ea de Description of Change:
Minor Modification (MM) 12-MM-267 modified the ice machine glycol supply and return header to accommodate supplemental cooling. The new installation required a tie-in utilizing a tee on a 6" section of pipe using a flange and installing a valve to isolate glycol flow.
Safety Evaluation Summary:
This change was reviewed and it was concluded that it did not represent an unreviewed safety-question. This conclusion was based on the fact that the system is non-safety related and that the modification would not adversely impact systems important to safety.
9.4 TEMPORARY MODIFICATIONS 9.4.1 Close Control Room Ventilation Dam ers 1 2-HV-ACRDA Description of Change:
Temporary Modifications (TMs) 01-92-11 and 02-92-9 administratively maintain closed the control room normal intake damper (HV-ACRDA-1) for both units. This modification is in response to discussions held with the NRC regarding our control room habitability analyses that were submitted in letter AEP:NRC:0389-0 on October ll, 1988. This letter submitted analyses of doses to control room operators following a LOCA. The analyses determined whole body doses that were within the 5 rem limit of General Design Criteria 19 of 10CFR50 Appendix A, and that were within the 50 rem thyroid and skin dose limits that were believed to be acceptable based on the International Commission on Radiological Protection, Publication Number 30. The NRC had informed us that they believe the correct limit for thyroid and skin dose is 30, rather than 50 rem. As a result, several measures were taken to align the control room ventilation system such that the 30 rem limit would not be exceeded during a postulated accident.
These measures included maintaining closed the control room normal intake damper.
Safety Evaluation Summary:
This change was reviewed and it was concluded that it did not represent an unreviewed safety question. This conclusion was based on the fact that the change places the damper in the safe position for the types of events for which the control room ventilation system provides protection. The TM will stay in place until analyses can be completed to bring the control rooms limits for thyroid and skin doses to within the NRC required 30 rem.
I 9.4.2 isconnect Ino erable Seismic Acceleromete Description of Change:
Temporary Modification (TM) 01-92-40 involves disconnecting the power cables to seismic accelerometer No. 12-SMIC=ACL-2 (non-tech. spec) located on the top of the primary shield wall inside containment. This disconnection helps to restore the natural frequency wave form of the remaining three accelerometers (required by technical specifications) until the faulty accelerometer can be replaced.
Safety Evaluation Summary:
This change was reviewed and it was concluded that it did not conclusion is represent an unreviewed safety question. This based on the fact that disconnecting the non-technical specification accelerometer will improve the performance of the other technical specification required accelerometers.
During a design basis earthquake, sufficient information will be available from the accelerometers listed in the technical specification.