05000244/LER-1986-001, :on 860118,containment Pressure ESP Actuation Channel Inoperable When Pressure Transmitters Isolated from Containment.Caused by Inadequate Surveillance Procedure. Procedure Revised
| ML20153F246 | |
| Person / Time | |
|---|---|
| Site: | Ginna |
| Issue date: | 02/17/1986 |
| From: | Kober R, Widay J ROCHESTER GAS & ELECTRIC CORP. |
| To: | NRC OFFICE OF ADMINISTRATION (ADM) |
| References | |
| LER-86-001, LER-86-1, NUDOCS 8602250368 | |
| Download: ML20153F246 (4) | |
| Event date: | |
|---|---|
| Report date: | |
| 2441986001R00 - NRC Website | |
text
__
va -== nema,aren, saammes.
pa se aceisovee== me. e o.
UCENSEE EVENT REPORT (LERI seener massa m R.E. Ginna Nuclear Power Plant 0 l5 l0 l0 l el 9l3 l3 1lOFlnl7 Failure to meet miniman degree of redundancy for Engineered Safety Features Actuation System eveerears a 6en namen neeest ears m ofwen eassuvia evo6ves me asDesTN cay Ysaa vaan e hM'n" 3,
esomrw oav vean
'aoutv maeses ooCaeT asvasseam 0181010 log l l 0l 1 1l 8 86 8l6 0!0 l 1 0l0 O!2 1! 7 8!6 ogsgegoici ; i
~
~
rue moont e -- vree evne. ant to rue moeuenameurs or io con > re-.
, ou N
m eses mmm e m isw enen rsries m annuine esamuu m.rewswn rariw g
ga p a,
ne 0 1913 mm**=H'Hsi es.sei.ee es.re w
- a
2, ma===
=e*
=
g m'm*""ad
=F8"**
mrewma*Hu t Q$^.
~c masunn arsw am m,em.w vesasse comract een vue tem um Tel.T._; seveGWh anaase aasa caos J.A. Widay, Technical Section Manaqer 31115 51214 l -l 41414 l 6 cemeters one 6me eos eaos ----e ea: Lune ensemees ne vue amour na "g
M' e
R d
"yyYg[
'7 go
Cause
everehe COnp0sseMT
Cause
eveTees Coe8PO4e97 7%
^1'*',
I I I I I I I l
l l l l l l
/
I I I I I I I I
I l t I i t ausessmewrat me. oat esecreo n.
mour=
o,y vana YeS Ilf res..suisse. fKefCffa susasissicar om ris aso l
g g
4estnace w..er - a.
e, ne.
On January 18, 1986 at approximately 1400 hours0.0162 days <br />0.389 hours <br />0.00231 weeks <br />5.327e-4 months <br /> while the unit was at 93% power a surveillance procedure was performed that caused a violation of the minimum degree of redundancy for the.
containment pressure Engineered Safety Feature Actuation channels.
i This resulted in one of the actuation signals to the Safety Injection, Containment Spray and Main Steam Isolation systems potentially being compromised.
The cause was an inadequacy in a procedure, which should only have been done at Cold or Refueling shutdown, or required the affected channels to be placed in the tripped condition.
<(L L 0602250368 860217
- - I
==>
PDR ADOCK 05000244
.ne,,,, s.
PDR g
e u 8 huCLt!A [41ULI.70AY COMustssoas e mC Pere 3.ea s
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION
- P.aovio ove =o ma#o.
EnPiaf f 3 3t 33 DOCKET NUMelm I2I Lg4 8suuSER ISI
'AGI O
,g
,g,
" m ;;'
2: 1:
R.E. Ginna Nuclear Power Plant 015 j o l0 j o I 21414 816 01Ol1 010 Of 2 0F 0 l3 rm n,
we i m.., on on January 18, 1986 at approximately 1400 hours0.0162 days <br />0.389 hours <br />0.00231 weeks <br />5.327e-4 months <br /> while the unit was at 93% power a surveillance procedure was performed that caused a violation of the minimum degree of redundancy for the containment pressure Engineered Safety Feature Actuation channels.
The pressure channels were rendered inoperable when the pressure transmitters were isolated from containment as part of the test.
The inoperability resulted from cycling of the pressure transmitter manual isolation valves as per the direction of procedure PT-2.10.6
" Containment Pressure Transmitters Manual Isolation Valve Strok-ing".
This procedure is only intended to be used at Cold or Refueling shutdown.
However, the requirement for the plant to be in a Cold / Refueling condition for performance of PT-2.10.6 or proper defeat of the channels being isolated were not identified.
PT-2.10.6 does not state Cold or Refueling Shutdown as an initial condition.
On January 18, 1986 a Results and Test Technician, after notifying the Shift Supervisor and Head Control Operator, proceeded to perform PT-2.10.6.
The test involved stroking closed then immediately opening each of the containment pressure transmitter manual isolation valves, one at a time.
The resulting isolation of the transmitter rendered it inoper-able.
Only one transmitter was done at a time and each was isolated for only a short time (< 10 sec.).
This resulted in not meeting the minimum degree of redundancy as per R.E. Ginna Technical Specification Section 3.5.3.1 and Table 3.5-2.
ESF actuation signals for the Safety Injection, Containment Spray and Main Steam Isolation Systems were potentially compromised during the duration of the test.
On January 18, 1986 during a review of the completed PT-2.10. 6 procedure a Q.C.
Technician identified a possible conflict between the procedure initial conditions and Appendix C of the RG&E QA Manual.
The Q.C. Technician generated a QC Surveillance report to document the conflict.
,.g,,0..
e u 8 muCLEJA REGULa.TOAv ConsnesotaC,se mac 7eean asta LICENSEE EVENT REPORT (LERI TEXT CONTINUATION areaovao ewe to siso-oio.
E mpimES g 3* 1s oocusT muassam 12)
Lem mueseen its PAGE 831 pacnary maasa its
" t m."
- .y
,es=
R.E. Ginna Nuclear Power Plant 015 [0 l0 l0 l2 l 4l 4 8 l6 010l1 0 10 0 13 OF 013 rwa a ~==cr men <m On January 21, 1986 during a review of the completed PT-2.10.6 procedure and a Quality Control Surveillance report generated after the performance of the test, the Results and Test Supervisor reported the error to plant management after reviewing a reference to the RG&E QA Manual Appendix C contained in the procedure.
The QA Manual states that these valves cannot be stroked during normal plant operation to prevent inoperability of the containment pressure transmitters.
Further review determined that this was also a violation of Technical Specifications.
Review of this event has determined that parts of the Containment Spray, Safety Injection and Main Steam Isolation Actuation signals were potentially compromised.
However, due to the short duration of the test the safety significance is minor.
Actuation signal for these systems which do not use containment pressure were not affected.
The following corrective actions have been performed or are planned.
1.
Change PT-2.10.6 to reflect the requirement for the plant to be in Cold or Refueling Shutdown or proper defeat of isolated channels.
2.
Ensure other procedures in the PT-2.10 series contain the correct initial conditicus.
3.
Clarify notes in Append.x C to the QA Manual which state
" Refueling Outages" av make no mention of " Refueling" as it is defined in Technical Specifications.
Also 6dd that this test can be performed at power if the proper precau-tions are taken.
,.g,.o. s -.
t
.... -[?k
,gr, y g R0
- a g
,.;, q
'. ;j &
($
^
{"L j
ROCHESTER GAS AND ELECTRIC CORPORATION e 89 EAST AVENUE, ROCHES'ER, N.Y. 14649-0001
~-g ROGER W. HOBER gg y u man ant a coca t a 546 2700 February 17, 1986 U.S. Nuclear Regulatory Commission y
Document Control Desk Washington, DC 20555
Subject:
LER 86-001, Failure to Meet Minimun Degree of Redun-dancy for Engineered Safety Features Actuation System R.E. Ginna Nuclear Power Plant Docket No. 50-244 In accordance with 10 CFR 50.73, Licensee Event Report System, item (a) (2) (i) which requests a report of, "any operation or condition prohibited by the plant Technical Specifications" the attached Licensee Event Report LER 86-001 is hereby submitted.
V ry truly yours, lY h O
Ro er W. Kober RWK/eeg xc:
U.S. Nuclear Regulatory Commission Region I 631 Park Avenue King of Prussia, PA 19406 i
T/1 i
1