Safety Evaluation Concluding Proposed Rev 26 to Rg&E QAP for Station Operation Incorporating Reductions in Stated Commitments Will Continue to Comply with QA Criteria of App B to 10CFR50 & Therefore,AcceptableML17265A618 |
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ML17265A617 |
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Category:SAFETY EVALUATION REPORT--LICENSING & RELATED ISSUES
MONTHYEARML17265A6341999-04-23023 April 1999 Safety Evaluation Supporting Amend 74 to License DPR-18 ML17265A6181999-04-0606 April 1999 Safety Evaluation Concluding Proposed Rev 26 to Rg&E QAP for Station Operation Incorporating Reductions in Stated Commitments Will Continue to Comply with QA Criteria of App B to 10CFR50 & Therefore,Acceptable ML17265A5541999-02-25025 February 1999 Safety Evaluation Approving Request to Apply leak-before- Break Status to Portions of Plant Residual Heat Removal Sys Piping ML17265A5341999-02-0404 February 1999 Safety Evaluation Granting Request Relief 36 from ASME Code Section XI Requirements for Plant Third 10-yr ISI Interval IR 05000244/19912011999-01-29029 January 1999 Safety Evaluation Accepting Licensee 920406 & 981104 Submittals Re Number of Pumps Required for Post LOCA Recirculation Phase Per Action Items Identified in Insp Rept 50-244/91-201 ML17265A3851998-07-30030 July 1998 Safety Evaluation Supporting Amend 72 to License DPR-18 ML17264B1361997-12-0909 December 1997 Safety Evaluation Supporting Amend 70 to License DPR-18 ML20236N4221997-09-15015 September 1997 SER for Operability Assessment of Intermediate Range Neutron Monitoring Instrument for Re Ginna Nuclear Power Plant ML17264A9881997-08-12012 August 1997 SER Accepting Plant Third 10-year Inservice Insp Interval Request for Relief 32 from ASME Code Section XI Requirements ML17264A7901997-01-0909 January 1997 Safety Evaluation Supporting Amend 66 to License DPR-18 ML17264A4991996-05-23023 May 1996 Safety Evaluation Accepting Plant & Related Correspondence Re Rev to RCS Pressure & Temp Limits Rept ML17264A5041996-05-23023 May 1996 Safety Evaluation Supporting Amend 64 to License DPR-18 ML17264A4951996-05-20020 May 1996 Safety Evaluation Supporting Amend 63 to License DPR-18 ML17264A4321996-04-0101 April 1996 Safety Evaluation Supporting Amend 62 to License DPR-18 ML17264A3841996-02-27027 February 1996 Safety Evaluation Accepting Licensee 950619 Submittal of Documentation Discussing Evaluation Model to Be Used for SBLOCA at Plant ML17264A2601995-11-27027 November 1995 Supplemental Safety Evaluation Accepting Licensee 910506, 950203 & 950920 Requests for Deviations from Reg Guide 1.97 Recommendation for Environ Qualified Neutron Flux Monitoring Instrumentation at Plant ML17264A1301995-08-0707 August 1995 Safety Evaluation Authorizing Alternative for Hydrostatic Testing Contained in License Proposal ML17263B1141995-07-0707 July 1995 Safety Evaluation Supporting Relief Request 13,rev 1 ML17263B0991995-06-21021 June 1995 Safety Evaluation Accepting Proposed TS 3.1.1.6 & Associated Action Statements Equivalent to Those Proposed in GL 90-06 ML17263B0341995-04-26026 April 1995 Safety Evaluation Supporting Amend 59 to License DPR-18 ML17263A9441995-02-15015 February 1995 SE Informing That Proposed EAL Changes for Plant Consistent W/Guidance in NUMARC/NESP-007 & Meet Requirements of 10CFR50.47(b)(4) & App E to 10CFR50 ML17263A8221994-10-27027 October 1994 SER Authorizing Proposed Alternatives Contained in Extension to RR 25 to Support Welded Repair or Replacement Activities for Svc Water Sys Components Through 1995 Refueling Outage ML17263A6791994-05-27027 May 1994 Safety Evaluation Accepting Util Concrete Containment Structural Integrity ML17263A5791994-04-11011 April 1994 Safety Evaluation Accepting Alternative Proposed in 10-yr Inservice Insp Program Relief Requests 25 & 26,if Addl Surface Exam Performed on Root Pass of Weld ML17263A4531993-11-0404 November 1993 SER Authorizing Per 10CFR50.55a(a)(3)(ii) Proposed Code Alternative to Code Requirements Based on Determination That Compliance W/Specified Requirements Results in Hardship W/O Compensating Increases in Quality & Safety ML17263A4411993-10-20020 October 1993 Safety Evaluation Supporting Amend 56 to License DPR-18 ML17250B2831993-06-29029 June 1993 Safety Evaluation Granting Relief Requests 23 & 24 to Forgo Hydrostatic Pressure Test Required for Repairs to Svc Water & Auxiliary Feedwater Sys ML17263A2501993-04-20020 April 1993 Safety Evaluation Supporting Amend 52 to License DPR-18 ML17262B0611992-10-20020 October 1992 Safety Evaluation Authorizing Inservice Testing Program Relief Requests ML17262B0151992-09-23023 September 1992 Safety Evaluation Accepting Licensee 920406 Response to Station Blackout rule,10CFR50.63 ML17261B1451990-08-24024 August 1990 Safety Evaluation Supporting Amend 40 to License DPR-18 ML17261B1231990-08-0606 August 1990 Safety Evaluation Accepting Third 10-yr Interval Inservice Insp Program Plan ML17250B0521989-11-0707 November 1989 Safety Evaluation Concluding That Auxiliary Feedwater (AFW) Sys Tech Spec Bases Be Modified as Appropriate When Proper Tech Specs Proposed & Finding Action Statements for Inoperable AFW Pump & Flow Path Unsatisfactory ML17251A5621989-07-0707 July 1989 Safety Evaluation of Flaw Indication in Reactor Vessel Inlet Nozzle N2B.Licensee 1989 Insp Results & Fracture Analysis Demonstrate Structural Integrity of Reactor Pressure Vessel Will Be Maintained During Svc W/Flaw Indication ML17251A5271989-05-30030 May 1989 Safety Evaluation Supporting Amend 37 to License DPR-18 ML17251A4331989-03-30030 March 1989 Partially Deleted Nonproprietary SER Accepting Use of Westinghouse Generic Program Identified in Proprietary WCAP-11799 & Nonproprietary WCAP-11800 as Approach for Implementing Item C.2 of NRC Bulletin 88-002 ML17251A4061989-03-16016 March 1989 SER Re Compliance W/Atws Rule 10CFR50.62, Requirements for Reduction of Risk from ATWS Events for Light Water Cooled Nuclear Power Plants ML17251A2741988-09-23023 September 1988 Safety Evaluation Supporting Amend 30 to License DPR-18 ML17251A1651988-06-23023 June 1988 Safety Evaluation Supporting Amend 29 to License DPR-18 ML17261A4181987-02-10010 February 1987 Safety Evaluation Supporting Amend 22 to License DPR-18. Diagram of Sys Architecture Encl ML17261A3661987-01-0909 January 1987 Sser Re Generic Ltr 83-28,Item 4.3 Concerning Reactor Trip Breaker Automatic Shunt Trip.All Issues Found Acceptable Except for Submission of Proposed Tech Spec Changes for Review ML17309A3931986-12-12012 December 1986 Safety Evaluation Supporting Util Responses to IE Bulletin 80-11 Re Masonry Wall Design ML17251A8701986-11-17017 November 1986 Safety Evaluation Re Projected Values of Matl Properties for Fracture Toughness Requirements for Protection Against PTS Events.Reevaluation of Resistor Temp PTS & Comparison to Pressure Temp Operating Limits Required by 10CFR50,App G ML17251A7341986-08-0808 August 1986 SER Supporting Util 831104 & 850823 Responses to Requirements of Generic Ltr 83-28,Item 2.1 (Part 1) Re Equipment Classification ML17251A6631986-05-0808 May 1986 Safety Evaluation Supporting Amend 14 to License DPR-18 ML17251A6441986-04-10010 April 1986 SER Supporting Responses to Generic Ltr 83-28,Items 3.1.1, 3.1.2,3.2.1,3.2.2 & 4.1 Re post-maint Testing,Verification & Reactor Trip Sys Reliability.Action Required by Item 4.5.1 Will Be Evaluated Per Item 4.5.3 Requirements ML17254A7491986-02-0707 February 1986 Safety Evaluation Re C-E Welded Sleeve Method of Steam Generator Tube Repair.Welded Tube Sleeve Meets Structural Integrity Requirements as Stipulated by NRC Criteria ML17254A6871985-12-16016 December 1985 Safety Evaluation Supporting Amend 12 to License DPR-18 ML17254A6201985-10-25025 October 1985 Safety Evaluation Supporting Licensee 831104 & 850903 Responses to Generic Ltr 83-28 Re post-trip Review Program Description & Procedure.Program & Procedures Acceptable ML17254A5611985-10-0101 October 1985 Safety Evaluation Supporting Util 831104 Response to Generic Ltr 83-28,Items 3.1.3 & 3.2.3 Re post-maint Testing of Reactor Trip Sys.No Testing Requirements Identified in Existing Tech Specs Which Degrade Safety 1999-04-06
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17265A7601999-10-0505 October 1999 Part 21 Rept Re W2 Switch Supplied by W Drawn from Stock, Did Not Operate Properly After Being Installed on 990409. Switch Returned to W on 990514 for Evaluation & Root Cause Analysis ML17265A7621999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Re Ginna Npp.With 991008 Ltr ML17265A7531999-09-23023 September 1999 Part 21 Rept Re Corrective Action & Closeout of 10CFR21 Rept of Noncompliance Re Unacceptable Part for 30-4 Connector. Unacceptable Parts Removed from Stock & Scrapped ML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr 05000244/LER-1999-011, :on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With1999-09-22022 September 1999
- on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With
ML17265A7471999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Re Ginna Npp.With 990909 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed 05000244/LER-1999-004, :on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed1999-08-24024 August 1999
- on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed
ML17265A7341999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Re Ginna Npp.With 990806 Ltr ML17265A7291999-07-29029 July 1999 Interim Part 21 Rept Re safety-related DB-25 Breaker Mechanism Procured from W Did Not Pas Degradatin Checks When Drawn from Stock to Be Installed Into BUS15/03A.Holes Did Not line-up & Tripper Pan Bent 05000244/LER-1999-007, :on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians1999-07-23023 July 1999
- on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians
ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7131999-07-22022 July 1999 Special Rept:On 990407,radiation Monitor RM-14A Was Declared Inoperable.Caused by Failed Communication Link from TSC to Plant Process Computer Sys.Communication Link Was re-established & RM-14A Was Declaed Operable on 990521 05000244/LER-1998-003, :on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored1999-07-22022 July 1999
- on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored
ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7211999-07-19019 July 1999 ISI Rept for Third Interval (1990-1999) Third Period, Second Outage (1999) at Re Ginna Npp. 05000244/LER-1999-010, :on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With1999-07-15015 July 1999
- on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With
ML17265A7011999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Re Ginna Npp.With ML17265A7661999-06-30030 June 1999 1999 Rept of Facility Changes,Tests & Experiments Conducted Without Prior NRC Approval for Jan 1998 Through June 1999, Per 10CFR50.59.With 05000244/LER-1999-001, :on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With1999-06-21021 June 1999
- on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With
ML17265A6761999-06-16016 June 1999 Part 21 Rept Re Defects & noncompliances,10CFR21(d)(3)(ii), Which Requires Written Notification to NRC on Identification of Defect or Failure to Comply. Relays Were Returned to Eaton for Evaluation & Root Cause Analysis 05000244/LER-1999-009, :on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With1999-06-0202 June 1999
- on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With
ML17265A6681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Re Ginna Nuclear Power Plant.With ML17265A6651999-05-27027 May 1999 Interim Rept Re W2 Control Switch,Procured from W,Did Not Operate Satisfactorily When Drawn from Stock to Be Installed in Main Control Board for 1C2 Safety Injection Pump. Estimated That Evaluation Will Be Completed by 991001 05000244/LER-1999-008, :on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With1999-05-27027 May 1999
- on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With
ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr 05000244/LER-1999-006, :on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With1999-05-21021 May 1999
- on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With
ML17265A6591999-05-17017 May 1999 Part 21 Rept Re Relay Deficiency Detected During pre-installation Testing.Caused by Incorrectly Wired Relay Coil.Relays Were Returned to Eaton Corp for Investigation. Relays Were Repaired & Retested ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr 05000244/LER-1999-005, :on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With1999-05-13013 May 1999
- on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With
ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6381999-05-0707 May 1999 Part 21 Rept Re Replacement Turbocharger Exhaust Turbine Side Drain Port Not Functioning as Design Intended.Caused by Manufacturing Deficiency.Turbocharger Was Reaasembled & Reinstalled on B EDG ML17265A6391999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Re Ginna Nuclear Power Plant.With ML17265A6341999-04-23023 April 1999 Safety Evaluation Supporting Amend 74 to License DPR-18 ML17265A6361999-04-23023 April 1999 Part 21 Rept Re Power Supply That Did Not Work Properly When Drawn from Stock & Installed in -25 Vdc Slot.Power Supply Will Be Sent to Vendor to Perform Failure Mode Assessment.Evaluation Will Be Completed by 991001 ML17265A7251999-04-23023 April 1999 Rev 1 to Rept of Development of Rg&E Seismic Safe SD Equipment & Relay Review Lists for USI A-46 ML17265A6301999-04-18018 April 1999 Rev 1 to Cycle 28 COLR for Re Ginna Npp ML17265A6251999-04-15015 April 1999 Special Rept:On 990309,halon Systems Were Removed from Svc & Fire Door F502 Was Blocked Open.Caused by Mods Being Made to CR Emergency Air Treatment Sys.Continuous Fire Watch Was Established with Backup Fire Suppression Equipment ML17265A6551999-04-0909 April 1999 Initial Part 21 Rept Re Mfg Deficiency in Replacement Turbocharger for B EDG Supplied by Coltec Industries. Deficiency Consisted of Missing Drain Port in Intermediate Casing.Required Oil Drain Port Machined Open ML17265A6181999-04-0606 April 1999 Safety Evaluation Concluding Proposed Rev 26 to Rg&E QAP for Station Operation Incorporating Reductions in Stated Commitments Will Continue to Comply with QA Criteria of App B to 10CFR50 & Therefore,Acceptable ML17265A6291999-03-31031 March 1999 Rev 0 to Cycle 28 COLR for Re Ginna Npp ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr 05000244/LER-1999-003, :on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With1999-03-31031 March 1999
- on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With
ML17265A6241999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Ginna Station.With 990409 Ltr 05000244/LER-1999-002, :on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With1999-03-29029 March 1999
- on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With
ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A5581999-03-0101 March 1999 Rev 1 to Gnpp Internal Flooding Probabilistic Safety Assessment Final Rept ML17265A5661999-03-0101 March 1999 Rev 26 to QA Program for Station Operation. 1999-09-30
[Table view] |
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UNITED STATES NUCLEAR REGULATORY COMMISSION WASHINGTON, D.C. 20555-0001 SAFETY EVALUATIONBY THE OFFICE OF NUCLEAR REACTOR REGULATION PROPOSED REVISION 26 TO THE ROCHESTER GAS AND ELECTRIC CORPORATION UALITYASSURANCE PROGRAM FOR STATION OPERATION R. E. GINNA NUCLEAR POWER PLANT DOCKET NO. 50-244
1.0 INTRODUCTION
By letter dated December 21, 1998, (Reference
- 1) as supplemented March 1, 1999, Rochester Gas and Electric Corporation (RG&E) transmitted proposed Revision 26 to the R. E. Ginna Nuclear Power Plant Quality Assurance Program for Station Operation (QAPSO).
Revision 26 to the QAPSO was submitted in accordance with the requirements of 10 CFR 50.54(a)(3) as reflecting changes that reduced commitments in the QAPSO description previously approved by the NRC. However, this submittal also included changes for which RG&E was not seeking NRC approval based on the licensee's conclusion that they had no impact on commitments in the QAPSO.
As a result of a request for additional information (RAI) by the NRC staff (Reference 2), RG&E amended its original submittal via correspondence dated March 1, 1999 (Reference 3). This submittal modified certain changes previously identified in the original submittal and provided the additional information requested by the staff. This evaluation only addresses changes in Revision 26 to the regulatory guides and standards listed in the QAPSO, Table 17.1.7-1, "Conformance of Ginna Station Program to Quality Assurance Standards, Requirements, and Guides," which RG&E has deemed to be reductions iiicommitment pursuant to 10 CFR 50.54(a)(3).
2.0 EVALUATION 2.1 Pro osed Alternative to Re ulato Guide RG 1.58
" uglification of Nuclear Power Plant lns ection Examination andTestin Personnel" Revision1 andits Endorsement of SNT-TC-1A-1975 for the ualification and Certification of Nondestructive Testin Personnel In its December 21, 1998, submittal (Reference 1), RG&E proposed to modify its commitment to RG 1.58 to allow use of the later version of SNT-TC-1A (1980) used in the American Society of Mechanical Engineers (ASME) Code Section XI currently in effect at the R. E. Ginna Nuclear Power Plant. The staff agreed with the basis of RG&E's concerns relative to the presence of this conflict in the QA and Inservice Inspection (ISI) programs.
However, the staff requested an RAI dated February 17, 1999 (Reference 2), that RG8 E clarify its proposed 990409032i 99040b PDR ADQCK 05000244 P
PDR Enclosure alternative to RG 1.58. Accordingly, in its March 1, 1999, response to the staff's RAI (Reference 3), RG&E modified its proposed alternative to RG 1.58 as follows:
"RG&E's ISI Plan endorses ASME Code Section XI. The version of the ASME code endorsed is updated periodically. ASME Code Section XI references standards for the qualification and certification of nondestructive testing personnel.Section XI of the ASME Code contains specific requirements for nondestructive examination and also references the use of other supplementary standards for the qualification and certification of personnel performing nondestructive examinations. The applicable versions of the standards referenced in Section XI of the ASME code, as permitted for use by 10 CFR Part 50.55a, may be used for the qualification and certification of personnel performing nondestructive examinations required by Section III and Section XI of the ASME Code in lieu of the standard identified in Reg. Guide 1.58, Rev. 1, (SNT-TC-IA-1975) provided that other applicable rules contained in Section XI of the ASME Code are met."
The staff finds that RG&E's exception to RG 1.58, above, satisfies the requirements of Appendix B to 10 CFR Part 50, and 10 CFR Part 50.55a and is, therefore, acceptable.
2.2 Pro osedAltemativeto RG1.88 "Collection Stora e andMaintenanceof Nuclear Power Plant ualit Assurance Records" Revision 2 RG&E is committed to RG 1.88 which conditionally endorses ANSI N45.2.9-1974, "Requirements for Collection, Storage, and Maintenance of Quality Assurance Records for Nuclear Power Plants." Section 5.6 of ANSI N45.2.9-1974 specifies the use of a 4-hour fire rated facilityfor non-duplicated records.
However, in its December 21, 1998, submittal (Reference 1) RG&E requested that the requirements in Section 5.6 (Facility) of ANSI N45.2.9-1974 be supplemented by the following alternatives:
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Records may be stored in a 2-hour rated facility meeting the requirements described in QAPSO Section 17.2.15.
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Records may be stored temporarily in 1-hour fire rated cabinets provided that the requirements of QAPSO Section 17.2.15 are met.
As justification for these alternatives, RG&E proposed to revise QAPSO Section 17.2.15, "Records," to incorporate the following provisions:
NFPA 232 2-Hour Rated Protection The requirements contained in QAPSO Section 17.2.15 for alternate records storage facilities are consistent with the guidance provided by the NRC in NUREG-0800, "Standard Review Plan," (SRP) Section 17.1, "QA During the Design and Construction Phases."
Paragraph 17.4 of this section under Quality Assurance Records (Paragraph 17.1.17) describes the use of 2-hour rated records storage facilities meeting NFPA 232 requirements.
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Tem ora Stora eof Records The use of temporary storage is requested to allow the use of 1-hour fire rated cabinets to store records that are awaiting processing for permanent storage (i.e., duplication or transfer to a single facility). The storage of these records in 1-hour rated cabinets willbe controlled by procedures which specify a maximum allowable time limit.
The records processing room in which the 1-hour fire rated containers are stored is protected by sprinklers. The use of sprinklers in this room would limitthe spread of a potential fire, and provide additional protection to the records stored in the cabinets. Therefore, the records stored in these cabinets are effectively providing greater than 1-hour rated protection.
Since the alternatives proposed by RG&E, above, and as described in QAPSO Section 17.2.15, "Records," are explicitly allowed alternatives described in Paragraph 17.4, Section 17.1 of the SRP, the staff finds these alternatives to RG 1.88 acceptable.
2.3 Pro osed Alternative to the 30-Da Corrective Action Com letion Provisions in RG 1.144 "Auditin of ualit Assurance Pro rams for Nuclear Power Plants" Janua 1979 In its December 21, 1998, submittal (Reference 1), RG&E proposed to allow audited organizations to respond to audit findings within the time-frame imposed by their safety-significance (as determined by the licensee's corrective action process) rather than within the
'0-day period imposed by RG 1.144.
RG 1.144 conditionally endorses the provisions in ANSI N45.2.12-1977, "Requirements for Auditing of Quality Assurance Programs for Nuclear Power Plants," as providing an adequate basis for complying with the pertinent requirements of Appendix B to 10 CFR Part 50.
Section 4.5.1 of ANSI N45.2.12-1977 requires that "[i]nthe event that corrective action cannot be completed within thirty days, the audited organization's response shall include a scheduled date for corrective action."
In its RAI dated February 17, 1999 (Reference 2), the NRC requested that RG&E supplement its submittal to clarify the timeliness provisions that would govern corrective actions for significant conditions adverse to quality. While acknowledging that subsection 4.5.1 of ANSI N45.2.12 already allows for delays in corrective actions that cannot be completed within 30 days, the staff was concerned that the licensee's proposal would not sufficiently emphasize the necessity of promptly resolving significant conditions adverse to quality in a manner consistent with the provisions of Criterion XVI, "Corrective Action," of Appendix B to 10 CFR Part 50. Accordingly, RG&E was asked to clarify how its corrective action process would prioritize significant audit findings.
In its March 1, 1999, response to the staff's RAI (Reference 3), RG&E modified its proposed alternative to RG 1.144 specifying that for audit findings that are determined to be significant conditions adverse to quality, the audited organization's response shall be provided within 30 days.
The staff finds that this proposed alternative is consistent with the provisions in Section 17.2, "Quality Assurance During the Operations Phase," of the SRP, and with the requirements of Criterion XVI, "Corrective Action," of Appendix B to 10 CFR Part 50 and is, therefore, acceptable.
4 2.4 Pro osed Alternative to Lead Auditor Certification Provisions in RG 1.146
" uglification of uali Assurance Pro ram Audit Personnel for Nuclear Power Plants" Revision 0 RG&E is currently committed to RG 1.146, Rev. 0, which conditionally endorses ANSI N45.2.23-1978, "Qualification of Quality Assurance Audit Personnel for Nuclear Power Plants."
Section 2.3.4 of ANSI N45.2.23-1978 requires that prospective lead auditors participate in a minimum of five QA audits within a 3-year period prior to qualification.
In lieu of the requirements of Section 2.3.4 of ANSI N45.2.23-1978, RG&E proposed the following alternative in its December 21, 1998, submittal (Reference 1):
"Prospective lead auditors shall demonstrate their ability to effectively implement the audit process and effectively lead an audit team.
RG&E willdescribe this demonstration process in written procedures and shall evaluate and document the results of the demonstration.
Regardless of the methods used for the demonstration, the prospective lead auditor shall have participated in at least one nuclear quality assurance audit within the year preceding the individual's effective date of qualification. Upon successful demonstration of the ability to effectively implement the audit process and effectively lead audits, and having met the other provisions of Section 2.3 of ANSI N45.2.23-1978, the individual may be certified as being qualified to lead audits."
In an October 24, 1996, letter to the Nuclear Energy Institute (Reference 4), the NRC staff provided its position with regards to acceptable industry proposed alternatives on QA processes for qualifying auditors and for conducting annual evaluations of suppliers.
RG8 E's proposed alternative for certifying lead auditors, as described above, is consistent with the staff's position in the cited letter and is, therefore, acceptable.
3.0 CONCLUSION
While the proposed alternatives proposed by RG&E for the RG activities described above constitute a reduction in commitments in the QA program description previously approved by the NRC, such exceptions continue to satisfy the provisions of Section 17.2 of the SRP.
Therefore, the proposed Revision 26 to RG8 E's QAPSO incorporating the reductions in commitments identified above willcontinue to comply with the quality assurance criteria of Appendix B to 10 CFR Part 50 and is, therefore, acceptable.
Principal Contributor: J. Peralta Date:
April 6, 19999
4.0 REFERENCES
RG&E (R.C. Mecredy) letter to USNRC (G.S. Vissing),'"Revised Submittal of Quality Assurance Program for Station Operation - R.E. Ginna Nuclear Power Plant - Docket Number 50-244," dated December 21, 1998.
2.
USNRC (G.S. Vissing) letter to RG&E (R.C. Mecredy), "Revised Submittal of Quality'ssurance Program for Station Operation, Request for Additional Information - R.E.
Ginna Nuclear Power Plant (TAC No. MA4455)," dated February 17, 1999.
3.
RG&E (R.C. Mecredy) letter to USNRC (G.S. Vissing), "Revised Submittal of Quality Assurance Program for Station Operation - R.E. Ginna Nuclear Power Plant - Docket Number 50-244," dated March 1, 1999.
4.
USNRC letter to the Nuclear Energy Institute, "Review of Nuclear Energy Institute (NEI)
Proposed Improvements to Quality Assurance Programs (Reference NEI Letter, dated January 30, 1996)," dated October 24, 1996.